ML19263C340

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LER 79-008/03L-0 on 790126: LPCI Min Flow Value MO-2-1501-13A Failed to Close Completely During LPCI Pump Operability Surveillance.Cause of Failure Unknown
ML19263C340
Person / Time
Site: Dresden Constellation icon.png
Issue date: 02/09/1979
From: Achterberg J
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17173A614 List:
References
LER-79-008-03L, LER-79-8-3L, NUDOCS 7902220013
Download: ML19263C340 (1)


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o ,Il cally closes when sufficient flow is sensed in the LPCI pump discharge header. l o c  ! Safety si",nificante was minimal since remaining 3 LPCI pumps were available to m?et i No previous similar occurrences. l oI7 l the required systen flow.

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@ REPORT l 7l 9l _l l0 l 0l 8l l/ l 0l 3l lL 3J l-l 31 0l 32 21 22 23 24 26 27 23 D ATT A CH*/ E N T P pn D-4 PR I'/ E CO '.*P. CC'/PO N E N T AC TI O '4 rUTUnE EFFECT EFurOC4 = " A%F ACTU RER TAAE. ACTlDN ONPLANT ^ ' E I'r S D POUPS " Su e '.1 TT E D FCPMdLi SU P P LI E R lJJx l@l zl@ L_zJ@ l zl@ l01010101 LNJ@ l 'il@ l zi@ l zi 91 91 91@ ,47 J, J3 36 31, 4J 41 42 43 44 CAUSE CESCRIPTION AND CCRRECTIVE ACTIO?

3 io l The cause of the failure is unknown. The valve operator motor and the thermal over- l

, , l load contacts were checked with no anomalies found. The breaker was reset and the (

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, , j valve was successfully cycl-i three times from the control room. [

,;3 electrical maintenance checked the amperage of the motor and found it sa t is f ac tcrry. l l

No further corrective action is planned. l l

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