ML19225B264

From kanterella
Jump to navigation Jump to search
LER 79-017/03L-0 on 790615:while Reactor Subcritical,D Main Steam Line Radiation Monitor Hi-Hi Trip Failed.Caused by Dirty Trip Relay or Dirty Test Switch Contacts. Condition Corrected by Repeated Testing
ML19225B264
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 07/09/1979
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
LER-79-017-031, LER-79-17-31, NUDOCS 7907240386
Download: ML19225B264 (2)


Text

i M [P , l A l P l B l S l 3 l@l0 l0 l- l0 l0 0 l0 l0 l- l0 l0 2bl@l26 4l1LICENSE LICENst NUMBEH l1 l1TYPL l1l@l JO l

S F C A T 58 l@ l 7

Q7 LICENSEE CODE 14 15 CON;)

ITI G I #

% ,3 Q l0 l5 10 l- 10 l2 17 8 @l69ol 611151719 61 DOCKE T NUMBER 68 EVENT DATE

@l 0171 Ol 9l 7 l 980 lh 74 75 REPORT DATE 60 EVENT DESCRIPTION AND PRO 8 ABLE CONSEQUENCES h IO I2I l uirh rhn reactor suberitical and less than 212 F, the "D" main steam l 10131 liinn radiation monitor hi-hi trip failed to function during performance O 4 lof a routine surveillance test. The inoperable channel aas immediately l I O l 5 l lplaced_in a tripped condition. The sa fety sinnificance was minimal since 1 6 lredundant_ channels unre_ operable. 1 10171 1 i O 8 l l

80 7 8 9 ,

SYSTE M CAUSE CAUSE COMP. VALVE CODE CODE SUSCODE COMPONENT CODE SUSCODE SUBCODE 10191 lTIAlh W h (_Zjh I l N l S l T l R l U jh) Wh (Z_j h 7 8 9 10 11 12 13 18 19 20 SE QUE NTI AL OCCUR R E NCE REPORT R F. VISION

_ EVENT YE AR REPORT NO. CODE TYPE N O.

O lLE j[,La'R _RO 7l 9l 22

(-j 23 l 0l 117l 24 26

[/_j 27 l0l3JN 28

[L_j 30 l-31

[0]

32 21 AKEN ACT ON ON PL ANT METH D HOURS S BMIT FOR 9. $UPPL ER MANUFACTU ER lxj@l zl@ Lzj@ l zlh I ol ol of 01 LNJ@ [Y_j@ l43Nl@ lG Ol8l0l@l; 33 34 35 36 3 40 41 42 44 47 }

CAUSE DESCRIPTION AND CORRECTIVE ACTIONS I

i O The radiation monitor was retested and the hi-hL: rip functioned proper l ,

11 11 I l Iv. The orobable cause of the failure was either di rty trip relay or  !

E B l dirty test switch contracts since several operatiens of the relay and l I i I 3 I I switch ;orrected this condition. The surveillance test wa s performed l Il l' I Ldaily for six days to assure proner oneration of the trip circuit. 80 7 8 9 STA S  % POWE R OTHER STATUS ISCOV RY DISCOVERY DESCRIPTION fI- [Hjh lO l 0 l 0 l@! N/A l [B_jh[ Surveillance Test l ACTIVITY CONTENT RE L E asE D oF PE LE ASE AMOUNT OF ACTIVITY LOC ATION OF RE LEASE l i l 6 l {_7J @ [yjgl N/A l [_F/A 45 80 l }

7 8 9 10 11 44 PE RSONNE L E XPOSUR E S NUMBER TYPE D E SCRIPTION l

i 7 l O! Ol Ol@l Zlhl N/A PE RSONNE L INJURIES NuMBtR OtSCRiefiONh )

i a I nl nl nl@l N/A 7/O 71 V A l 7 8 e si i2 sUU L i UJ V LOSS OF OR D AM AGE TO F ACILITY

( 80 TYPE D E SCRIPTION i 9 (_yj@l n/A 80 7 8 9 10 (

' " '

  • NRC USE ONLY

/ ,

2 O ISSUE L3J lyn @oISCRiPTION@ //// j , . , ,

I 68 69 l1ll1I III Il5 80 E 7 8 9 10 g/ 4 f 4'/

NAME OF PREPARER

  • W PHONE-C ,

7 907240 8b

Mr. Boyce H. Grier, Director No. 3 17/03L-0

%4fgce of Inspection & Enforcement, Region 1 3.S. Nuclear Regulatory Conrnission i 631 Park Avenue '

King of Prussia, PA 19406

Dear Mr. Grier:

This LER refers to failure of a main steam line radiation monitor. The governing Technical Specification is Table 3.1.1.

U. S. NUCLE AR REGULATORY COMMISSION i

LICENSEE EVENT REPORT j 368 21 %

.