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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
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Text
e e 10CFR50.73 Virginia Electric and Power Company Sony Power Station P.O.Bo:x:315 Surry, Virginia 23883 July 13, 1993 U.S. Nuclear Regulatory Commission Serial No.: 93-430.
Document Control Desk SPS:VAS Washington, D. C. 20555 Docket Nos.: 50-280 50-281 License Nos.: DPR-32
Dear Sirs:
DRP-37 Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following updated Licensee Event Report applicable to Surry Power Station Units 1 and 2.
BEPQRTNUMBER 50-280/50-281/93-007-01 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be forwarded to the anagement Safety Review Committee for its review.
Very truly yours, Enclosure cc: Regional Administrator 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 M. W. Branch NRC Senior Resident Inspector Surry Power Station
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NRC FORM366 (6-891 e U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT ILER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON. DC 20503.
FACILITY NAME (1) IDOCKET NUMBER (2) l PAGE (31 Surry Power Station, Units 1 and 2 o 151 o 10 Io 1218 10 I 1 loF 014 TITLE 141 Missed Survei1-.lance Due to Fai1.ure to "Test One Contact or the Auxiliary Feedwater Pump Lo-Lo Steam Generator Level Auto Start Logic EVENT DATE (5) LEA NUMBER (6) REPORT DATE (71 OTHER FACILITIES INVOLVED (Bl MONTH DAY YEAR YEAR :}{ SE~~~~~~AL Jt ~~~~~~ MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERIS) 01s1010101 1 1 oI6 11 6 9 3 9 I 3 - o I o J7 - o J1 o17 1 I3 9 I3 THIS REPORT IS SUBMITTED PURSUANT TO THE RI.QUIREMENTS OF 10 CFR §: (Ch.ck on* or mar* of th* following/ 1111 OPERATING MODE Ill N 20.4051c) II0.73(1l1211iv) 73.71(bl I
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NAME TELEPHONE NUMBER AREA CODE M. R, Kansler, Station Manager COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 MANUFAC- MANUFAC-CAUSE SYSTEM COMPONENT TURER TURER I I I I I I I I I I I I I I I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED 114) MONTH DAY YEAR EXPECTED n ~
SUBMISSION DATE (15)
YES (If Y**. compl*r. EXPECTED SUBMISSION DATE} NO I I I ABSTRACT (Limit to 1400 u>>c*1. i.*.. *pproxim*t*ly fiftHn 1ingl*-11Mc* fyPl!Writt*n /inn} 1161 On April 23, 1993, with Unit 1 operating at 100% power and Unit 2 at Cold Shutdown, the continuing review of Technical Specification (TS) surveillance implementation identified a missed surveillance. TS table 4.1-1, item 26, requires that the Turbine Trip Inputs to Reactor Protection be functionally tested prior to each start up. Periodic Test, 1/2-PT-29.3 is performed to satisfy this requirement, but does not test the circuitry to verify the turbine trip signal is supplied to Reactor Protection. On June 16, 1993, with Unit 1 and Unit 2 at 100% power, an incomplete channel calibration surveillance test was also identified. TS table 4.1-1, item 32a, requires that the steam generator water low low level instrumentation channels for auxiliary feedwater pump auto-start be calibrated during each refueling outage. Contrary to this requirement, PT-15.6 for Unit 2 did not completely test the entire auto-start matrix. Appropriate changes have been made to the procedure.
The health and safety of the public were not affected at any time during these events because subsequent testing determined the affected circuitry was capable of performing the required functions.
This report is being made pursuant to 10CFR50.73(a)(2)(i)(B) as the station was operated in a condition not allowed by the TS 4.1.A.
NRC Farm 366 (6-891 i_
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 0-0l04 (6-89) 315
-IMATEO BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE E* T REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO l'HE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (61 PAGE (3)
Surry Power Station, Units 1 & 2 0 1s I O I O I O 12 I 81 0 91 3 - 0 IO I 7 - 01 1 0 I2 OF OI 4 TEXT (ff mom -ctJ i& n,quirwl, U/IIJ 11dditia1111/ NRC Form .-:A '11) (17) 1.O DESCRIPTION OF THE EVENT On April 23, 1993, with Unit 1 operating at 100% power and Unit 2 at Cold Shutdown for a scheduled refueling outage, the continuing review of Technical Specification (TS) surveillance implementation by Engineering identified a missed surveillance. TS table 4.1-1, item 28, requires that the Turbine Trip Inputs to Reactor Protection [EIIS-JC] be functionally tested prior to each start up if not done within the previous week. A turbine trip is sensed by two out of three signals from auto stop oil pressure or four out of four stop valve closure signals. A turbine trip causes a direct reactor trip above 10% power.
Periodic Test procedure, 1/2-PT-29.3, "Turbine Trip Setpoint" is performed to satisfy this requirement, but does not verify that the turbine trip signal (two out of three Auto Stop Oil Channels [EIIS-JJ] and four out of four Turbine Stop Valves [EIIS-JJ-V]) is supplied to Reactor Protection. This procedure verifies the turbine trip, but does not test the reactor protection circuitry as required by TS table 4.1-1, item 28. The surveillance requirement of item 28 is not met until a reactor protection logic test (either 1/2-PT-8.1, "Reactor Protection System Logic for Normal Operations" or 1/2-PT-8.2, "Reactor Protection Logic") and also 1/2-PT-29.3 are both performed. During some previous start ups, reactor protection logic testing was not performed until after the unit was on line. There have been short periods of missed surveillances following these start ups before the monthly logic testing (1/2-PT-8.1) was performed.
On June 16, 1993, with Unit 1 and Unit 2 at 100% power, the continuing review of TS surveillance implementation by Engineering identified that a complete channel calibration surveillance test was not performed during certain refueling outages due to a procedural deficiency. TS table 4.1-1, item 32a, requires that the steam generator water low low level instrumentation channels [EIIS-SG-LI] for auxiliary feedwater pump [EIIS-BA-P] auto-start be calibrated during each refueling outage. Contrary to this requirement, PT-15.8 for Unit 2, "Steam Generator Low Low Level Test", did not completely test one contact in the 2 out of 3 logic circuitry of the auto-start matrix of the turbine driven auxiliary feedwater pump. Therefore, TS 4.1.A requirements have not been fully met during certain refueling outages. Unit 1 procedures had been changed to incorporate complete testing of the entire auto-start matrix for the turbine driven auxiliary feedwater pump.
This report is being made pursuant to 10CFR50.73(a)(2)(i)(B) as the station was operated in a condition not allowed by TS 4.1.A.
- 2. O SIGNIFICANT SAFETY CONSEQUENCES AND IMPLICATIONS No significant safety consequences resulted from these conditions because subsequent testing determined the affected circuitry was capable of performing the required functions. Monthly Periodic Logic Testing was satisfactorily performed shortly after each start up for each unit and the turbine trip reactor protection circuitry proved to be operable. Subsequent testing verified the steam generator low low level 2 out of 3 logic auto-start matrix for the turbine driven auxiliary feedwater pump to be operable.
Therefore, the health and safety of the public were not affected at any time during these previous events.
NRC Form 366A (6-89)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-89) , APPROVED 0MB NO. 3150-0104
-ATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE E V . REPORT (LERI INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1"HE PAPERWORK REDUCTION PROJECT' (3150-01041. OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON. DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3)
LER NUMBER (6)
YEAR SEQUENTIAL ::::::::::: REVISION Surry Power Station, Units 1 & 2 -:-:-:-:-:* NUMBER :::::::::: NUMBER o Is 1o ] o 1o ] 2] 8 Io 9 J3 - o I 01 7 - o11 o] 3 OF o I4 TEXT (ff man, S{J(Jctl is mquintd, use odditional NRC Form 366A 's/ 117)
- 3. O CAUSE PE THE EVENT These events were caused by personnel error resulting in a procedural deficiency for not fully testing turbine trip to reactor trip components and steam generator low low level logic I
circuitry for turbine driven auxiliary feedwater pump auto-start.
Procedure 1/2-PT-29.3 does test the turbine trip but does not test the reactor protection circuitry. Procedure 1/2-PT-8.1 or 1/2-PT-8.2 overlap to check the reactor protection circuitry. Procedure 1/2-PT-29.3 and 1/2-PT-8.1 or 1/2-PT-8.2 must both be performed to satisfy TS table 4.1-1, item 28.
Procedure PT-15.8 did not completely test the entire auto-start matrix for the turbine driven auxiliary feedwater pump for Unit 2. During certain refueling outages, it has been determined that the Unit 2 procedure failed to verify one set of contacts operable in the 2 out of 3 auto-start logic. A request to revise the procedure had been written to specify testing for each of the logic combinations in the 2 out of 3 auto-start matrix. However, a permanent change was never submitted for the Unit 2 procedure due to personnel error.
Unit 1 procedures had been changed to incorporate complete testing of the entire auto-start matrix for the turbine driven auxiliary feedwater pump.
4.0 IMMEDIATE CORRECTIVE ACJIONCS)
The immediate corrective action was to verify that Unit 1 had been fully tested (1-PT-29.3 and 1-PT-8.1 have been satisfactorily performed). It was also verified that Unit 2 was fully tested prior to start up following refueling for cycle 12 operation (2-PT-29.3 and 2-PT-8.2 have been performed).
At 1737 on June 16, 1993, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> clock was entered in accordance with TS 4.0.3 due to missed surveillance. The untested steam generator water low low level instrumentation channel was placed in trip by lifting the affected leads, and the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> clock was exited on 6/17/93 at 1328 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.05304e-4 months <br />. After satisfactory testing of the affected contacts, the auto-start matrix for the turbine driven auxiliary feedwater pump was proven operable and the pump was returned to service.
- 5. o ADDITIONAL CORRECTIVE ACTION CS)
Appropriate changes will be made to the surveillance procedures to ensure TS table 4.1-1, item 28 requirements are met. Appropriate changes have been made to the surveillance procedure for Unit 2 to ensure TS table 4.1-1, item 32a requirements are met.
- 6. o ACTIONS JO PREVENT RECURRENCE The revision to the Unit 1 and 2 surveillance procedures to ensure TS table 4.1-1, item 28 and 32a requirements are met will be sufficient to preclude recurrence. In addition, a I structured review of TS required surveillance's, including engineering reviews, procedure upgrades and Quality Assurance activities is being undertaken to identify other NRC Form 366A (6-89)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-89) APPROVED 0MB NO. 3150-0104
- EXPIRES: 4/30/92
~ATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE E A REPORT ILER) INeORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P-530). U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE
.I OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NA!V)E (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
Surry Power Station, ~nits 1 & 2 0 15 IO IO IO I 218 IO 9I 3 - 0 I Ol 7 - 0 11 0 I 4 OF O 14 TEXT (ff mom &paCtJ is n,quintd, USl1 additional NRC Form 366A's) (171 surveillance deficiencies. This program will continue until the TS required surveillance's and associated procedures have been reviewed. Any additional discrepancies will be appropriately dispositioned, categorized and reported in accordance with the Station's deviation reporting and corrective action programs.
The process in which procedures are permanently revised will be changed to ensure that both units are evaluated whenever a change request is submitted for a single unit.
7.0 SIMILAR EVENTS Missed surveillances concerning failure to test entire component circuitry include:
LEA S1-92-003-00/1/2: Incomplete Engineering Safety Features Testing Due to Procedure Deficiency LEA S2-91-007-00: Failure to Full Flow Test 2-RH-47 Due to Procedure Deficiency 8.0 ADDITIONAL INFORMATION None.
NRC Form 366A (6-89)