Similar Documents at Ginna |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
" 'ACCELERATED DISTRIBUTION DEMONST$&TION SYSTEM REGULA'I . INFORMATION DISTRIBUTIO SYSTEM (RIDS)
ACCESSION NBR:9204080122 DOC.DATE: 92/03/30 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION BACKUSiW.H. Rochester Gas & Electric Corp.
MECREDY,R.C. Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 92-003-00:on 920229,a reactor trip occured due to Lo .Lo level in "B" Steam Generator. Caused by a plugged instrument tubing for "A" Feedwater Pump Seal Injection Differential Pressure switch. Unplugging of instrument.W/910331 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ( ENCL t TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
SIZE: /5 NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244
, RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PDl-3 LA 1 1 PD1-3 PD 1 1 JOHNSON;A 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DET/EMEB 7E 1 1 NRR/DLPQ/LHFB10 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB8H3 1 1 NRR/DS~T+EBB8D1'EG 1 1 NRR/DST/SRXB 8E 1 1 WLE~=002I 1 1 RES/DSIR/EIB 1 1 RGN FILE 01 1 1 EXTERNAL: EG&G BRYCEEJ.H 3 3 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHYiG A ~ 1 1 NSIC POORE,W. 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS PLEASE HELP US TO REDUCE WAS'ONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 30 ENCL 30
</P(ZSiZ)7E gi/fjl(i(iiirI/
i'!i~Se~,;~/i/lii"l~!it/i,7 ROCHESTER GAS AND ELECTRIC CORPORATION ~ 89 EAST AVENUE, ROCHESTER N. K 14649.0001 ROBERT C. MECREDY TELEPHONE Vice President AREA COOE 7 t 6 546 2700 Oinna Nuclear Production March 30, 1991 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D'C 20555
Subject:
LER 92-003, Feedwater Transient, Due to Loss of "A" Main Feedwater Pump, Causes Lo Lo Steam Generator Level Reactor Trip R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including . the Reactor Protection System (RPS), the attached Event Report LER 92-003 is hereby submitted.
This event has in no way affected the public's health and safety.
Ver truly yours, Robert C. Me edy xco U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector GDO." I:i 9204080122 920330 PDR ADOCK 05000244
~re> r PDR
I
~W
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (64)9) APPROVED 0MB NO. 31504)104 EXPIRES: 4(30(92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT {LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH IP630), V.S. NUCLEAR REGULATOAY COMMISSION. WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3(504)(04), OFFICE OF MANAGEMENTANO BUDGET, WASHINGTON, OC 20M3.
FACILITY NAME (I) DOCKET NUMBER l2) PA E R.E. Ginna Nuclear Power Plant 0 5 0 0 0 2 4 4 1 OF 0 9 Feedwater Transient, Due To Loss of "A" Main Feedwater Pump, Causes Lo Lo Steam-EVENT DATE (5)
Generator Level Reactor LER NUMBER (8) REIIORT DATE (7)
Tri OTHER FACILITIES INVOLVED (6)
MONTH DAY YEAR YEAR ops sEQUENTtAL MONTH OAY YEAR FACILITYNAMES DOCKET NUMBER(SI NUMBER 0 5 0 0 0 0 2 2 9'9 2 9 2 0 0 3 0 0 0 3 3 0 9 2 0 5 0,0 0 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE RtQUIREMENTS OF 10 CFR ()s ICrreck onc or more of tne followinp) (11)
MODE (9) 20A02(b) 20.405(cl 50.73(e) (2)(ivl 73.71(5)
POWE R 20.405( ~ )Ill(0 50.36(el Ill 50.73(el(2)(v) 73.71(c)
LEVEL 0 20.405(e) (1) (9) 50.38(cl(2) 50.73(el(2) (vill OTHER (Specify In Apstrect t>>low enrf In Text, NIIC Form 20.405 (e) (I ) (iii) 50.73( ~ I (2)(i) 50.73(el(2) (xiii)(Al 366AI 20A05(e)(1)(iv) 50.73( ~ l(21(it) 50.73(e) (2)(v(6)(BI 20A05(el(1) (vl ~ 50.73(e I (2 I (III) 60,73( ~ )l2)(x)
LICENSEE CONTACT FOA THIS LER (12)
NAME TELEPHONE NUMBER Wesley'H. Backus AREA CODE Technical Assistant to- the Operations Mana er 3 1 5 5 2 4 - 4 4 4 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBEO IN THIS AEPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC MANUFAC. E'PORTABLE TVREA CAUSE SYSTEM COMPONENT ..w, TVRER TO NPRDS
,. o... QS SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTFD SUBMISSION DATE (15I YES Ilfycs, complere EXPECTED SIJ64IISSIDII DATEI NO ABSTRACT ILlmlt to tc00 sp>>ces, I e., epproxlmetely flfrsen sinpre.specs typswriNsn linNI (18)
On February 29, 1992 at. approximately 1346 EST, with the reactor stable at approximately 974 reactor power, just subsequent to a main feedwater pump trip, a reactor trip occurred due to Lo Lo level (</='74) in the "B" Steam Generator (S/G).
The Control Room operators immediately performed the appropriate actions of Emergency Operating Procedures E-0 (Reactor Trip Or Safety Injection) and ES-0.1 (Reactor Trip Response). Both Main Steam Isolation Valves (MSIVs) were subsequently closed to limit a Reactor Coolant System (RCS) cooldown and the plant was stabilized at hot shutdown.
The underlying cause of the event was plugged instrument tubing for the "A" Feedwater Pump Seal Injection Differential Pressure (D/P) switch which tripped the main feedwater pump. (This event is,NUREG-1022 (X) cause code.)
Corrective action taken was the unplugging of the instrument tubing by flushing and the replacement of one section of tubing and connections. Corrective actions to prevent recurrence are discussed in Section V of the text.
NRC Form 366 (64)9)
c NRC FORM 388A US. NUCLEAR REGULATORY COMMISSION
)689) APPROVED 0MB NO. 3)600104 EXPIRES; 4/30/92
~
TIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS
~
LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 600 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH IP.630), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPFRWORK REDUCTION PROJECT 131600104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY kAME 11) DOCKET NUMBER 121 LER NUMBER LS) PAGE IS)
YEAR
"' SEQUENTIAL .~' REVIS10>
NUM ER 'OO NUM ER R.E. Ginna Nuclear Power Plant 0 6 0 0 0 2 4 4 2 0 0 3 0 0 0 2 oF0 9 TEXT ///mo 4Pooo JP~ ooo d/d/ooo/P/RC ronn 38544/)In
-PRE-EVP2FF PLANT CONDITIONS The plant was at approximately 974 steady state reactor power with no major activities in progress.
DESCRIPTION OF EVENT A. DATES AND APPROXIMATE TIMES OF MAZOR OCCURRENCES:
February 29, 1992, 1346 EST: Event Date and Time 0 February 29, 1992, 1346 EST: Discovery Date and Time 0 February 29, 1992, 1346 EST: Control Room operators verify both reactor trip breakers open, and all control and shutdown, rods inserted.
February 29, 1992, 1350 EST: Control Room operators close both Main Steam Isolation Valves (MSIVs) to limit a Reactor Coolant System (RCS) cooldown.
0 February 29, 1992, 1358 EST: Plant stabilized at hot shutdown'ondition.
.B. EVENT:
On February 29, 1992 at approximately 1346 EST, with the reactor stable at approximately 974 reactor power, the Control Room received Annunciator Alarm H-11 (Feed Pump Seal Water Lo Diff Press 15 Psi) followed in approximately five (5) seconds by a trip of the "A" Main Feedwater Pump. The Control Room operators immediately entered Abnormal Procedure, AP-FW.1 (Partial Or Complete Loss Of Main Feedwater) and performed the immediate actions (i.e. starting all three (3) Auxiliary Feedwater (AFW) pumps, and decreasing turbine power= rapidly to less than 50%.)
NRC Form 388A (84)9)
1 f~ h
NRC FORM 366A (689) t LICENSEE EVENT REPORT ILER)
TEXT CONTINUATION UJL NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 31500)05 EXPIRES: E/30/92 TIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 50J) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE IS)
YEAR NUMBER J~
IIa'ECUENTIAL ~Orr REYIBION NUM ER R.E. Ginna Nuclear Power Plant TEXT (Ifrr>>ro BP>>c>> JE ~, lrro JJ(Jor>>J PIC Form 36EA3) (IT) o 5 o o o 24492 0 0 3 0 0 0 3 OF 0 9 During the performance of these immediate actions, a reactor trip occurred due to Lo Lo level (</=174) in the "B" Steam Generator (S/G).
The Control Room operators performed the immediate actions of Emergency Operating Procedure E-0 (Reactor Trip Or Safety Injection) and transitioned to Emergency Operating Procedure ES-0.1 (Reactor Trip Response) when it was verified that both reactor trip breakers were open, all control and shutdown rods were inserted, and safety injection was not actuated or required.
Both MSIVs were subsequently closed at 1350 EST to limit the RCS cooldown. The closing of the MSIVs mitigated the RCS cooldown and the plant was subsequently stabilized i:n hot shutdown at approximately 1358 EST.
The Intermediate Range Nuclear Instrumentation Channel N-35, after tracking consistent with channel N-36 down to approximately 1E-10 amps, had its indication continue to drop below 1E-11 amps. The N-35 channel returned to normal (i.e. 1E-11 amps) approximately ten (10) hours following the trip.
C INOPERABLE STRUCTURES P COMPONENTS P
'R SYSTEMS THAT CONTRIBUTED TO THE EVENT:
None.
D. OTHER SYSTEMS OR SECONDARY FUNCTIONS APPECTED:
None E. METHOD OP DISCOVERY.
The event was immediately apparent due to alarms and indications in the Control Room.
NRC Form 366A (SJ)9)
t C
E P
NRC FORM 366A (649)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION US. NUCLEAR REGULATORY COMMISSION t APPROVEO OMB NO. 31504(OS EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUESTI 503) HRS. FORWARD COMMENTS REQARDINQ BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F630), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31504104), OFFICE OF MANAGEMENTANO BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER IS) PAGE (3)
YEAR pg SEQUENTIAL NVM Ea ~Q~
REYISION NVMEEa R.E. Ginna Nuclear Power Plant o s o o o 2 4 4 9 2 0 0 3 0 0 0 4 QF 0 TEXT ///IaoIP space /s nqukat, vss ~ /I/oaP/HRC Fcna 356AB/ (12)
F. OPERATOR ACTION:
After the reactor trip, the, Control Room operators performed the actions of Emergency Operating Procedures E-0 (Reactor Trip Or Safety Injection) and ES-0.1 (Reactor Trip Response). The MSIVs were manually actuated closed approximately four (4) minutes after the trip to prevent further plant cooldown. The plant was subsequently stabilized at hot 'hutdown.
Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Commission per 10CFR50.72, Non-Emergency, 4 Hour Notification.
SAFETY-SYSTEM RESPONSES:
None.
III. CAUSE OF EV1PNT A. IMM9)IATE CAUSE:
The reactor trip was due to "B" S/G Lo Lo level
(</=>>~).
INTEFQGPDIATE CAUSE:
The "B" S/G Lo Lo Level (</=174) was due to the imbalance of feedwater flow to steam flow (i.e.
feedwater flow was approximately one half of steam flow) caused by the tripping of the "A" Main Feedwater Pump.
NRC Foaa 366A (6$ 9)
'h I
NRC FORM 366A (SS9)
LICENSEE EVENT REPORT (LER)
(LS. NUCLEAR REGULATORY COMMISSION e APPROVED OMB NO.31600104 6 XP I R ES: O/30/92 ESTIMATED BUADEN PER RESPONSE TO COMPLY WTH 'THIS INFORMATION COLLECTION REQUEST: 608) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS
.TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (315001IM). OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON,DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER IS) PAGE (3)
YEAR SS< BEQUENTIAL
???3 NUMBER
&4 REYISIoN YA NUM 5 R R.E. Ginna Nuclear Power Plant'EXT o s o o o 2 4 4 9 2 003 0005 oF 0 9
///mon <<w>> /o Ioqo(>>d, ooo ~ d/I/ooo/ NRC hmI 366i3/ (17)
The tripping of the "API Main Feedwater Pump was due to the inadvertent operation of the Feedwater Pump Seal Water Differential Pressure (D/P) switch. This D/P switch senses the feedwater pump suction pressure on the low side and the feedwater pump seal injection pressure on the high side. The requirements of differential pressure to protect the. pump seals is that the high side be >/=15 pounds per square inch pressure greater than the low side.
condition is not met, the main feedwater pump will If the above trip in 5 seconds.
The inadvertent operation of the Seal Water D/P switch was due to the plugging of the high pressure side tubing to the D/P switch, followed by gradual decrease of pressure in the isolated high pressure side tubing to the D/P switch.
C ROOT CAUSE The plugging of the high pressure side tubing to the D/P switch was due to an accumulation of corrosion
-products that built up over several years in an area of no flow through this tubing (i.e. a dead leg).
The pressure decrease in the high. pressure side tubing was most probably due to a combination of plugging of the high side tubing and a slight amount of seepage of fluid from a tubing connection on the high pressure side.
NAC FomI 366A (649)
NRC FORM366A (649)
LICENSEE EVENT REPORT (LER)
UA. NUCLEAR REGULATORY COMMISSION e APPROVED OMB NO. 31500104' XP I 1 ES: O/30 f92 ESTIMATFO BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (315001(M), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL gg.'EvrsloN
@4 NUMEER :::oS NUMBER R.E. Ginna Nuclear Power Plant o s o o o 2 4 4 9 2 0 0 3 0 0 0 6oF TEXT Il/more eaeoe Je rFFJred, rree aA(rooaor NRC %%drm 35EAB) (IT)
ANALYSXS OP EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF). including the Reactor Protection System
, (RPS)". The "B" S/G Lo Lo level reactor trip was an automatic actuation of the RPS.
An assessment was performed considering both the safety consequences and . implications of this event with the following results and conclusions:
There were no safety consequences or implications attributed to. the reactor trip because:
o The two reactor trip -breakers opened as required.
o All control and shutdown rods inserted as designed.
o The plant was stabilized at hot shutdown.
The Ginna updated Final Safety Analysis Report (UFSAR)
Chapter 15.2.6, "Loss Of Normal Feedwater", was reviewed and compared to the plant response for this event. The UFSAR .transient is a complete loss of Main Feedwater (MFW) at full power, with only one AFW pump available one (1) minute after the loss of MFW, and secondary steam relief (i.e. decay heat removal) through the safety valves only.
The protection against a loss of MFW includes the reactor trip on Lo Lo S/G water .features level and the start of the AFW pumps. These protection operated as designed.
The UFSAR transient resulted in a reactor trip on Lo Lo-S/G water level with S/G levels continuing to decrease and pressurizer (PZR) level and RCS average temperature (TAVG) increasing until the flow from one (1) AFW pump could remove decay heat at approximately 30 minutes into the event. All parameters then trended towards normal.
NRC Form 366A (689)
I t
NRC FORM 368A US. NUCLEAR REGULATORY COMMISSION (669) APPROVEO OMB NO. 31500'108 EXPIRES: 8/30/92 ESTIMATED BURDEN PEA AESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 600 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND AEPOATS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, ANO TO 1HE PAPERWORK REDUCTION PROJECT (316001(M), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) I.ER NUMBER (8) PAGE (3) 5(@ 6 8QVCNTIAL REVOION YEAR a.i NVM884 NUM684 RE E. Ginna Nuclear Power Plant o 6 o o o 2 4 4 9 2 0 0 3 0 0 0 7 OF 0 9 TEXT ///more e/>>ce/en//I/rer/ Iree //I/or>>/HRC Form 38843/ (IT)
The plant transient for this event resulted in a PZR level increase to 56.4% and a TAVG increase to 577 F. -
S/G levels remained in the narrow range throughout the transient. This was due to operator's actions to reduce power, steam dump action and the additional AFW flow.
Based on the above evaluation, the plant transient of February 29, 1992 is bounded by the UFSAR Safety Analysis assumptions.
Following the reactor trip, pressurizer level decreased to 0% but began to increase above 0% within approximately five (5) minutes. This is an expected observed transient.
The moderate RCS cooldown did not result in any core voiding. This was confirmed by the Reactor Vessel Level Indicating System (RVLIS), which always indicated a level of 100%.
A slow cooldown occurred during the post trip recovery period. This cooldown was bounded by the plant accident analysis and did not exceed the technical specification limit of 100 F per hour. Additional protection was provided by closure of the MSIVs.
Based on the above and a review of post trip data and past plant transients, it can be concluded that the plant operated as designed and that there was no unreviewed safety questions and that the public's health and safety was assured at all times.
V. CORRECTIVE ACTION
.A. ACTION TAKEN TO RLITURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
o The S/G levels were returned to their normal operating levels by addition of AFW, subsequent to the Reactor Trip.
N/IC Form 366A (669)
NRC FORM 3SSA US. NUCLEAR REGULATORY COMMISSION ISJ)9) APPROVEO OMB NO. 3)504)104 J EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT ILER) INFORMATION COLLECTION REQUEST: 50J) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON, DC 20555, AND TO THE PAPERWO)IK REDUCTION PROJECT (3)504)104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME 11) DOCKET NUMBER 12) LER NUMBER 15) PAGE IS)
YEAR SEQUENTiAL PPi('REVSION NUM ER 'W% NUM ER R.K.'inna Nuclear Power Plant 0 5 0 0 0 4 9 2 0 0 3 0 0 0 80FO 9 Jpoco /4 nqaked, u44 ~ //I/ono/HRC %%d SSSA'4/ 117) o As the Intermediate Range NIS Channel N-35 ~
tracked NIS Channel N-36 for its normal operating range and returned to normal approximately ten (10) hours after the trip, no immediate action was deemed necessary. This abnormality has been observed and researched extensively in the past in cooperation with the NSS vendor, Westinghouse.
No technical basis has been identified as to why the 1E-11 idle current does not maintain indication at 1E-11 amps. Rochester Gas and Electric Corporation (RG&E) and Westinghouse
'concurred that the channel was operable and capable of performing all intended functions.
Further evaluations of, the response characteristics of NIS Channel N-35 will be performed during the,1992 Annual Refueling and Maintenance Outage.
0 The "A" Feedwater pump seal water D/P switch tubing was unplugged and flushed completely. This included both the high side and low side tubing.
In addition, similar tubing 'for the "B" Feedwater pump was also flushed completely.
0 The "A" Feedwater, pump seal water D/P switch high side and low side tubing connections were checked for evidence of seepage and serviceability, and one section of tubing and connections was replaced.
0 EWR 4960 was designed and scheduled for installation during the upcoming 1992 outage.
The installation schedule was revised, and this modification was installed as a result of this transient. The feedwater pump seal water D/P switch time delay relays for both pumps were replaced, and the time delay setting was changed from five (5) seconds to a new setting of sixty (60) seconds. This modification provides a better opportunity for the operators to prepare for and mitigate a transient resulting from an impending trip of a MFW pump. In addition, the increased time delay does not compromise reliable operation of the MFW pumps on loss of seal water D/P, and also eliminates inadvertent MFW pump trips due to pressure surges and other short-term transients affecting the seal water D/P switch.
NRC Fono 3SSA )54)9)
NRC FORM388A (669)
US. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION t ~ APPROVED OM 8 NO. 31500104 E XP I R ES: 8/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F430), U.S. NUCLEAR
'EGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO SHE PAPERWORK REDUCTION PROJECT (3150d)04l. OFFICE OF MANAGEMFNTAND BUDGET,WASHINGTON, DC 20503.
FACILITY NAME (I) DOCKET NUMBER (2) LER NUMBER (8) PAGE (3)
YEAR IK SEQVENTIAL NVMSER i~s~R'EYOtON S. / NVMSER R.E. Ginna Nuclear Power Plant TEXT ///Ivory tpooo /o Toqoked. voo ~ NRC hvm 35683/ (17) o 6 o o o2 4 92 003 00 p 9 oF p 9 B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
As the underlying cause of the event was determined to be the plugging of the instrument tubing to the D/P switch because of a no flow condition, the following actions are being planned:
0 Flushing will be performed on selected secondary system instrument tubing during the 1992 outage.
0 Based on the results of flushing during the 1992 outage, a frequency of periodic flushing of selected instrument tubing will be established.
The areas determined, on a maintenance schedule.
if any, will then be put VI ADDITIONAL INFORMATION A. FAILED COMPONENTS.
None B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same underlying cause at Ginna Station could be identified.
C. SPECIAL COMMENTS~
None.
NRC Form 388A (669)
~ ~