On 9/12/16, an engineering evaluation concluded that a flaw identified on a 1" diameter stainless steel pipe associated with the High Pressure Service Water ( HPSW) System could have failed during a seismic event.
Failure of the pipe would cause flooding of the '2C' Residual Heat Removal (RHR) pump room and impact operation of equipment in the room if needed during a design basis event. The 1" diameter pipe supplies sample water to the '2C' HPSW radiation monitor sample pump. The flaw was identified on 8/16/16 when a 120 drop per minute leak was observed. The leak was the result of a crack located in the pipe at the toe of a fillet weld connecting the pipe to a coupling on an 18" diameter pipe that returns HPSW water to the plant discharge canal.
There were no actual consequences as a result of the leak. The pipe was replaced and the equipment was returned to service. |
|
---|
Category:Letter
MONTHYEARIR 05000277/20240032024-11-0404 November 2024 Integrated Inspection Report 05000277/2024003 and 05000278/2024003 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24284A2842024-10-10010 October 2024 (Wcgs), Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) ML24281A1012024-10-0707 October 2024 Senior Reactor and Reactor Operator Initial License Examinations ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24221A2582024-09-0606 September 2024 Response to Request for Re-Engagement Regarding the Subsequent License Renewal Environmental Review for Peach Bottom Atomic Power Station, Units 2 and 3 ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification 05000277/LER-2024-003, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum IR 05000277/20240052024-08-29029 August 2024 Updated Inspection Plan for Peach Bottom Atomic Power Station, Units 2 and 3 (Report 05000277/2024005 and 05000278/2024005) ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24235A0342024-08-23023 August 2024 U.S. Nuclear Regulatory Commission’S Analysis of Constellation Energy Generation’S Decommissioning Funding Status Report IR 05000277/20240102024-08-23023 August 2024 Fire Protection Team Inspection Report 05000277/2024010 and 05000278/2024010 IR 05000277/20240022024-08-14014 August 2024 Integrated Inspection Report 05000277/2024002 and 05000278/2024002 IR 05000482/20240052024-08-14014 August 2024 Updated Inspection Plan for Wolf Creek Generating Station (Report 05000482/2024005) ML24225A1692024-08-12012 August 2024 10 CFR 50.46 Annual Report ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24214A3232024-08-0101 August 2024 Response to Request for Additional Information - Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24206A1252024-07-24024 July 2024 Revision of Three Procedures and Two Forms That Implement the Radiological Emergency Response Plan (RERP) ML24191A0612024-07-0606 July 2024 Independent Spent Fuel Storage Installation (ISFSI) - Annual Radioactive Effluent Release Report ML24178A4142024-06-26026 June 2024 Revision of One Procedure and One Form That Implement the Radiological Emergency Response Plan (RERP) ML24178A3672024-06-26026 June 2024 Correction to 2023 Annual Radioactive Effluent Release Report – Report 47 ML24177A1512024-06-24024 June 2024 Post Accident Monitoring Instrumentation Report ML24166A1172024-06-20020 June 2024 Regulatory Audit Summary Regarding Proposed Alternative Schedule to Complete Decommissioning Beyond 60 Years RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations IR 05000277/20243012024-06-13013 June 2024 Initial Operator Licensing Examination Report 05000277/2024301 and 05000278/2024301 RS-24-058, Regarding Subsequent License Renewal Environmental Review2024-06-0505 June 2024 Regarding Subsequent License Renewal Environmental Review ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24150A2722024-05-29029 May 2024 Annual Radiological Environmental Operating Report 81, January 1, 2023 Through December 31, 2023 ML24150A0032024-05-28028 May 2024 Request for Exemptions from 10 CFR 50.82(a)(8)(i)(A) and 10 CFR 50.75(h)(1)(iv) and Proposed Amendment to the Decommissioning Trust Agreement ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000277/20240012024-05-13013 May 2024 Integrated Inspection Report 05000277/2024001 and 05000278/2024001 ML24134A1792024-05-13013 May 2024 Supplemental Information in Support of Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations IR 05000277/20245012024-05-0808 May 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000277/2024501 and 05000278/2024501 ML24121A1832024-04-30030 April 2024 Pre-Submittal Meeting Presentation Material Peach Bottom ECCS Compensated Level System Replacement Project RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24118A0032024-04-27027 April 2024 2023 Annual Radioactive Effluent Release Report - Report 47 ML24120A2762024-04-23023 April 2024 Independent Spent Fuel Storage Installation (ISFSI) Facility - Annual Radioactive Effluent Release Report 66 January 1, 2023 Through December 31, 2023 CNL-24-033, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-04-17017 April 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24107A2462024-04-15015 April 2024 Submittal of Changes to Technical Specifications Bases ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24102A0472024-04-11011 April 2024 Operator Licensing Examination Approval 05000277/LER-2024-002, Uncoordinated DC Circuits Cause Unanalyzed Condition2024-04-0808 April 2024 Uncoordinated DC Circuits Cause Unanalyzed Condition RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report RS-24-023, Report on Status of Decommissioning Funding.2024-03-22022 March 2024 Report on Status of Decommissioning Funding. IR 05000277/20244022024-03-12012 March 2024 Cybersecurity Inspection Report 05000277/2024402 and 05000278/2024402 (Cover Letter Only) ML24061A2642024-03-0101 March 2024 Revision of Two Procedures That Implement the Radiological Emergency Response Plan (RERP) for Wolf Creek Generating Station (WCGS) Commissioners ML24060A1192024-02-29029 February 2024 Notification of Conduct of a Fire Protection Team Inspection 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000277/LER-2024-003, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum 05000277/LER-2024-002, Uncoordinated DC Circuits Cause Unanalyzed Condition2024-04-0808 April 2024 Uncoordinated DC Circuits Cause Unanalyzed Condition 05000277/LER-2024-001, Automatic Reactor Scram Due to an Invalid Generator Lockout2024-03-21021 March 2024 Automatic Reactor Scram Due to an Invalid Generator Lockout 05000278/LER-2023-002, Main Steam Isolation Valves Stroke Times Exceed Technical Specification Limit2023-12-14014 December 2023 Main Steam Isolation Valves Stroke Times Exceed Technical Specification Limit 05000278/LER-2023-001, Standby Liquid Control Pump Inoperable for Greater than LCO Window Due to Gas Intrusion2023-11-0707 November 2023 Standby Liquid Control Pump Inoperable for Greater than LCO Window Due to Gas Intrusion 05000277/LER-2022-002, Automatic Depressurization System Safety Relief Valve Actuator Diaphragm Degraded2022-12-15015 December 2022 Automatic Depressurization System Safety Relief Valve Actuator Diaphragm Degraded 05000277/LER-2022-001, Automatic Reactor Scram Due to Loss of Power to Both RPS Buses2022-07-15015 July 2022 Automatic Reactor Scram Due to Loss of Power to Both RPS Buses 05000277/LER-2021-003, Manual Reactor Scram Due to Degrading Condenser Vacuum2022-01-12012 January 2022 Manual Reactor Scram Due to Degrading Condenser Vacuum ML21196A4852021-07-16016 July 2021 LER 2-2021-002-00 for Peach Bottom Atomic Power Station, Unit 2, Safety Relief Valve Inoperability Due to Nitrogen Leakage from Braided Hose Wear 05000278/LER-2017-0012017-12-20020 December 2017 Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line, LER 17-001-00 for Peach Bottom Atomic Power Station (PBAPS), Unit 3 Regarding Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line 05000277/LER-2017-0012017-03-0808 March 2017 Emergency Diesel Generator Exhaust Stacks Nonconforming Design for Tornado Missile Protection, LER 17-001-00 for Peach Bottom Atomic Power Station (PBAPS), Unit 2 Regarding Emergency Diesel Generator Exhaust Stacks Nonconforming Design for Tornado Missile Protection 05000278/LER-2016-0012016-11-22022 November 2016 Leak in High Pressure Coolant Injection Drain Pipe Results in a Loss of Safety Function, LER 16-001-00 for Peach Bottom, Unit 3, Regarding Leak in High Pressure Coolant Injection Drain Pipe Results in a Loss of Safety Function 05000277/LER-2016-0012016-11-11011 November 2016 Leak in High Pressure Service Water Pipe Results in Condition Prohibited by Technical Specifications, LER 16-001-00 for Peach Bottom, Unit 2, Regarding Leak in High Pressure Service Water Pipe Results in Condition Prohibited by Technical Specifications 05000278/LER-2015-0012016-02-26026 February 2016 Loss of High Pressure Coolant Injection System Function as a Result of Failed Flow Controller Signal Converter, LER 15-001-00 for Peach Bottom, Unit 3, Regarding Loss of High Pressure Coolant Injection System Function as a Result of Failed Flow Controller Signal Converter ML13058A0432013-02-22022 February 2013 Submittal of Independent Spent Fuel Storage Installation (ISFSI) Cask Event Report ML1007702362010-03-12012 March 2010 60-Day Security Event Report 2-10-S01 ML0927401622009-09-30030 September 2009 LER 09-S01-00 for Peach Bottom, Units 2 & 3 Regarding Unescorted Access Granted to Contract Worker Who Did Not Provide Complete Work History Information ML1015505682009-07-10010 July 2009 Event Notification for Peach Bottom on Elevated Tritium Levels Found in On-Site Well ML0434503772004-12-10010 December 2004 LER-04-S01-00 for Peach Bottom Atomic Power Station (PBAPS) Unit 2 and Unit 3, 60 Day Security Event Report 2-04-S01 ML19095A7391976-12-0505 December 1976 Reporting Abnormal Occurrence No. 50-278-74-33 at Peach Bottom Atomic Power Station for Failure of Main Steam Line High Flow Switch dPIS-3-2-116C to Trip During Surveillance Test 2024-09-05
[Table view] |
comments regarding burden estimate to the FOIA, Pnvacy and Information Col ections Branch
- T 5 F53), U.S Nuclear Regulatory Commission, Washington, DC 20555-0001 or by e ma to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
05000-277
3. LER NUMBER
001 0 2016 Unit Conditions Prior to the Event Unit 2 and Unit 3 were both operating in Mode 1 at approximately 100% rated thermal power. There were no structures, systems or components out of service that contributed to this event.
Description of Event
The High Pressure Service Water (HPSW) system (EIIS: BI) is a safety-related system that provides cooling water to four heat exchangers in the Residual Heat Removal (RHR) system (EIIS: BO) during post-accident conditions. The HPSW system consists of four 4,500 gpm pumps that normally draw water from the Conowingo Pond. The system can also be lined up to draw water from the Emergency Cooling Tower (ECT) (EIIS: BS) in the event that suction from the pond becomes unavailable. Water is pumped to the RHR heat exchangers, each of which is located in a watertight room. Water exits the heat exchangers through 14" diameter pipes. Those pipes from the 'A' and 'C' heat exchangers combine into an 18" diameter line, which later combines with an 18" diameter line from the 'B' and 'D' heat exchanger into a 24" diameter line that goes to the plant discharge canal. On the 18" diameter return line from the 'A' and 'C' heat exchangers, there is a pipe connection for a line to the HPSW radiation monitor sample pump.
The line is a 1" diameter Schedule 40S (0.133" wall thickness) Type 304 stainless steel pipe that was installed as part of a 1994 modification. The line is connected to the 18" diameter HPSW line with a socket weld connection to a half-coupling. The 1" pipe has a short span from the half-coupling to a rigid support on the wall, with two small valves in the span.
On 8/16/16, at approximately 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br />, in PBAPS Unit 2, a 120 drop per minute leak was identified on the 1" pipe to the '2C' HPSW radiation monitor sample pump. Inspection determined that the leak was from a crack in the pipe located at the toe of the weld to the half-coupling on the 18" diameter HPSW return line from the 'A' and 'C' RHR heat exchangers. The crack was approximately 1" long and located between the 11:00 o'clock and 2:00 o'clock positions on the pipe.
Due to the length of the crack, the structural integrity of the pipe was questionable. If the pipe were to shear at the crack location, it was estimated that 77 gpm would flow through the opening into the 'C' RHR room. As a result of the identified condition, the following equipment was declared inoperable at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on 8/16/16:
- One low pressure ECCS injection subsystem per TS 3.5.1.A due to flooding potential in the 'C' RHR room
- One RHR suppression pool cooling subsystem per TS 3.6.2.3.A due to flooding potential in the 'C' RHR room
- One RHR suppression pool spray subsystem per TS 3.6.2.4.A due to flooding potential in the 'C' RHR room
- One RHR drywell spray subsystem per TS 3.6.2.5.A due to flooding potential in the 'C' RHR room
- One HPSW subsystem per TS 3.7.1.A due to through-wall leak in ASME Class 3 piping comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch 'T 5 F53), U.S Nuclear Regulatory Commission, Washington, DC 20555-0001 or by e-ma to Infocollects Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104) Office of Management and Budget. Washington X 20503. If a means used to impose an 'nformation co lection does not display a currently valid OMB control number, the NRC may nut conduct or sponsor, and a person is not requ'red to respond to, the information collection.
05000-277
3. LER NUMBER
2016 0 001
- The emergency heat sink per TS 3.7.3.6 due to potential for loss of inventory (applies to both Units 2 and 3) The pipe was replaced and the affected equipment was restored to an operable status on 8/18/16 at 0610 hours0.00706 days <br />0.169 hours <br />0.00101 weeks <br />2.32105e-4 months <br />. The elapsed time from the discovery of the failure to when the equipment was returned to service was approximately 45 hours5.208333e-4 days <br />0.0125 hours <br />7.440476e-5 weeks <br />1.71225e-5 months <br /> and 40 minutes.
Analysis of the Event
Initial evaluation of the flaw could not determine if the pipe would have failed during a seismic event.
More detailed modeling of the pipe from its connection on the 18" diameter HPSW line to the first anchor point on the wall determined that seismic stresses could have caused the crack to propagate and result in a complete fracture of the pipe. This conclusion was reached on 9/12/16 and is considered to be the time at which a reportable event was identified. It is unknown at what time the crack developed into the as- found condition, however it is likely that it existed for a period of time greater than the TS required completion time for the systems to be restored to an operable status (7 days for each condition). Since the condition existed for a period of time longer than the TS required completion time, the condition resulted in a condition prohibited by TS and is being reported pursuant to 10CFR 50.73(a)(2)(i)(B).
Cause of the Event
To determine the cause of the crack, the section of the pipe and the socket weld were sent to an off-site lab for failure analysis. The cracking initiated at the toe of the weld on the outer diameter of the pipe and propagated in one general direction through the pipe wall. The fracture surface was examined by scanning electron microscopy and had transgranular features which are typical of fatigue. There were no material anomalies at the fracture origins and the weld appeared to be of generally good quality. The analysis concluded that the leak was caused by fatigue cracking caused by cyclic loading conditions, such as vibration.
The pipe was anchored to the wall a short distance from its connection to the 18" diameter HPSW line.
This design did not adequately account for vibration in the HPSW line, which resulted in bending stresses in the 1" pipe at the toe of the fillet weld connection to the half coupling. In addition, a 2:1 weld was not used with the socket weld. The current standard for fillet welds on small bore piping subject to vibration is to use a weld with a length to depth ratio of 2:1 in order to mitigate stress from vibration. A contributing cause is that the pipe appeared to have been slightly distorted in the downward direction.
Corrective Actions
The pipe was replaced between the 18" HPSW pipe and the first valve. A 2:1 weld was utilized at the socket to mitigate vibration impacts. The configuration of the 1" pipe is used at a total of 16 locations at the plant for the supply and return lines for radiation monitors for the HPSW system. All were visually inspected to determine if similar flaws existed on the other lines. No flaws were identified. Non- comments regarding burden estimate to the FOIA, Pnvacy and Information Collecfions Branch (T-5 F53), U S Nuc'ear Regulatory Commission Washington. DC 20555-0001, or by e-mail to Infocollects Resource@nrc gov and to the Desk Officer, Office of Information and Regulatory Affairs, used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
05000-277
3. LER NUMBER
001 0 2016 destructive examinations have been scheduled to obtain additional information on the condition of the piping.
Previous Similar Occurrences Since the modification in 1994 that installed the radiation monitors and associated piping, there have been no other documented cases of leakage from this piping.