ML15147A412

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IR 05000293/2015007; 02/02/2015 - 03/20/2015; Pilgrim Nuclear Power Station (Pnps); Special Inspection to Review the January 27, 2015 Partial Loss of Offsite Power (LOOP) and Reactor Scram Event; Inspection Procedure 93812, Special Inspecti
ML15147A412
Person / Time
Site: Pilgrim
Issue date: 05/27/2015
From: Ho Nieh
Division Reactor Projects I
To: Dent J
Entergy Nuclear Operations
DiPaolo E
References
EA-15-081 IR 2015007
Download: ML15147A412 (68)


See also: IR 05000293/2015007

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BLVD., SUITE 100

KING OF PRUSSIA, PA 19406-2713

May 27, 2015

EA-15-081

Mr. John Dent

Site Vice President

Entergy Nuclear Operations, Inc.

Pilgrim Nuclear Power Station

600 Rocky Hill Road

Plymouth, MA 02360-5508

SUBJECT: PILGRIM NUCLEAR POWER STATION - NRC SPECIAL INSPECTION REPORT

05000293/2015007; AND PRELIMINARY WHITE FINDING

Dear Mr. Dent:

On January 29, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed its initial

assessment of the circumstances surrounding the January 27, 2015 partial loss of offsite power

and reactor trip event at your Pilgrim Nuclear Power Station (PNPS) during a severe winter

storm. Based on this initial assessment, the NRC sent a Special Inspection Team (SIT) to your

site on February 2, 2015. The SIT Charter (Attachment 1 of the enclosed report) provides the

basis and additional details concerning the scope of the inspection. The enclosed report

documents the inspection teams activities and observations conducted in accordance with the

SIT Charter. On March 20, 2015, the SIT discussed the results of the inspection with you and

other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with Commission rules and regulations and with conditions of your license. The

team reviewed selected procedures and records and interviewed personnel. In particular, the

SIT reviewed event evaluations (including technical analyses), causal investigations, relevant

performance history, and extent-of-condition reviews to assess the significance and potential

consequences of several plant equipment, operator performance, and procedural issues that

complicated the loss of offsite power and reactor trip event that occurred during the severe

winter weather event.

The enclosed inspection report discusses a finding that has preliminarily been determined to be

a White finding with low to moderate safety significance that may require additional inspections,

regulatory actions, and oversight. As described in Section 2.5 of the enclosed report, Entergy

Nuclear Operations, Inc. (Entergy) staff failed to identify, evaluate, and correct the condition of

the A safety/relief valve (SRV) failing to open upon manual actuation during a plant cooldown

on February 9, 2013. While the SRVs tested satisfactorily at high pressures at an offsite test

facility, this failure to take actions to preclude repetition resulted in the C SRV failing to open at

reduced pressure during the plant cooldown in response to the partial loss of offsite power event

on January 27, 2015. The self-revealing finding was within Entergys ability to foresee and

J. Dent

2

correct because indications were available to determine that the A SRV valve did not open

upon manual actuation. As a result, the A SRV was inoperable for greater than its Technical

Specification allowed outage time. Entergy staff entered the issue into their corrective action

program (CAP) and conducted a cause evaluation. The finding did not present a current safety

concern because both the A and C SRVs were replaced during the outage following the

January 27, 2015, loss of offsite power and reactor trip event. This finding was assessed based

on the best available information, using the NRCs Significance Determination Process (SDP).

The basis for the NRCs preliminary determination is described in the enclosed report.

The NRC will inform you, in writing, when the final significance has been determined. In

accordance with NRC Inspection Manual Chapter 0609, Significance Determination Process,

we intend to complete and issue our final safety significance determination within 90 days from

the date of this letter. The NRCs significance determination process is designed to encourage

an open dialog between your staff and the NRC; however, the dialogue should not affect the

timeliness of our final determination.

We believe that we have sufficient information to make a final significance determination.

However, before we make a final decision, we are providing you an opportunity to provide your

perspective on the facts and assumptions that the NRC used to arrive at the finding and assess

its significance. Accordingly, you may notify us of your decision within 10 days to: (1) request a

regulatory conference to meet with the NRC and provide your views in person; (2) submit your

position on the finding in writing; or, (3) accept the finding as characterized in the enclosed

inspection report.

If you choose to request a regulatory conference, the meeting should be held in the NRC

Region I office within 30 days of the date of this letter, and will be open for public observation.

The NRC will issue a public meeting notice and a press release to announce the date and time

of the conference. We encourage you to submit supporting documentation at least one week

prior to the conference in an effort to make the conference more efficient and effective. If you

choose to provide a written response, it should be sent to the NRC within 30 days of the date of

this letter. You should clearly mark the response as a Response to Preliminary White Finding

in Inspection Report No. 05000293/2015007; EA-15-081, and send it to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a

copy to the Regional Administrator, Region I, and a copy to the NRC Senior Resident Inspector

at the PNPS.

You may also elect to accept the finding as characterized in this letter and the inspection report,

in which case the NRC will proceed with its regulatory decision. However, if you choose not to

request a regulatory conference or to submit a written response, you will not be allowed to

appeal the NRCs final significance determination.

Please contact Ray McKinley at (610) 337-5150 within 10 days from the issue date of this letter

to notify the NRC of your intentions. If we have not heard from you within 10 days, we will

continue with our significance determination and enforcement decision. Because the NRC

has not made a final determination in this matter, a Notice of Violation is not being issued for

this inspection finding at this time. In addition, please be advised that the number and

characterization of the apparent violation may change based on further NRC review. The

final resolution of this matter will be conveyed in separate correspondence.

J. Dent

3

In addition, this report documents one Severity Level IV non-cited violation (NCV) and six

findings of very low safety significance (Green). Five of the Green findings were determined to

involve violations of NRC requirements. However, because of the very low safety significance

and because they are entered into the CAP, the NRC is treating these violations as NCVs,

consistent with Section 2.3.2.a of the NRC Enforcement Policy. If you contest any NCV in this

report, you should provide a response within 30 days of the date of this inspection report, with

the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control

Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the

Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington,

DC 20555-0001; and the NRC Resident Inspector at PNPS. In addition, if you disagree with the

cross-cutting aspect assigned to any finding, or a finding not associated with a regulatory

requirement in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your disagreement, to the Regional Administrator, Region I,

and the NRC Resident Inspector at PNPS.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390 of the NRC's

"Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be

available electronically for public inspection in the NRC Public Document Room or from the

Publicly Available Records component of the NRCs Agencywide Documents Access and

Management System (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

We appreciate your cooperation. Please contact Eugene DiPaolo of the Division of Reactor

Projects staff at (610) 337-6959 if you have any questions regarding this letter or the enclosed

report.

Sincerely,

/RA/

Ho K. Nieh, Director

Division of Reactor Projects

Docket No.

50-293

License No.

DPR-35

Enclosure:

Inspection Report 05000293/2015007

w/Attachments 1, 2, 3, 4, and 5

cc w/encl:

Distribution via ListServ

ML15147A412

SUNSI Review

Non-Sensitive

Sensitive

Publicly Available

Non-Publicly Available

OFFICE

RI/DRP

RI/DRP

RI/DRP

RI/OE

RI/DRP

NAME

EDiPaolo/EMD

RMcKinley/RRM

DSchroeder/DLS

MMcLauglin/MMM

HNieh/HKN

DATE

5/8/15

5/9/15

5/8/15

5/11/15

5/26/15

1

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No.

50-293

License No.

DPR-35

Report No.

05000293/2015007

Licensee:

Entergy Nuclear Operations, Inc. (Entergy)

Facility:

Pilgrim Nuclear Power Station

Location:

600 Rocky Hill Road

Plymouth, MA 02360

Dates:

February 2, 2015 through March 20, 2015

Inspectors:

E. DiPaolo, Senior Project Engineer, Division of Reactor Projects,

Team Leader

C. Cahill, Senior Reactor Analyst, Division of Reactor Safety (DRS)

S. Pindale, Senior Reactor Inspector, DRS

J. Lilliendahl, Senior Emergency Response Coordinator, DRS

T. Dunn, Operations Engineering, DRS

E. Burket, Emergency Preparedness Inspector, DRS

Approved by:

Daniel L. Schroeder, Branch Chief

Division of Reactor Projects

Team Manager

Ho K. Nieh, Director

Division of Reactor Projects

2

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ........................................................................................................... 3

REPORT DETAILS ..................................................................................................................... 10

1.

Chronology of Events and Event Response Challenges ................................................. 10

2.

Equipment Response to the Event ................................................................................... 12

3.

Event Diagnosis and Crew Performance ......................................................................... 23

4.

Effectiveness of Licensees Response ............................................................................. 30

5.

Implementation of the Emergency Plan ........................................................................... 32

6.

Control of Switchyard Activities, Maintenance Effectiveness, and Assessment of

Operating Experience ...................................................................................................... 36

7.

Risk Significance of the Event .......................................................................................... 39

8.

Exit Meetings .................................................................................................................... 42

ATTACHMENT 1 - SPECIAL INSPECTION TEAM CHARTER .............................................. A1-1

ATTACHMENT 2 - DETAILED SEQUENCE OF EVENTS ..................................................... A2-1

ATTACHMENT 3 - PILGRIM OFFSITE POWER SYSTEM .................................................... A3-1

ATTACHMENT 4 - QUANTITATIVE AND QUALITATIVE EVALUATIONS ............................ A4-1

ATTACHMENT 5 - SUPPLEMENTAL INFORMATION .......................................................... A5-1

KEY POINTS OF CONTACT............................................................................................... A5-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED .................................................. A5-1

LIST OF DOCUMENTS REVIEWED ................................................................................... A5-2

LIST OF ACRONYMS ......................................................................................................... A5-5

3

Enclosure

SUMMARY OF FINDINGS

IR 05000293/2015007; 02/02/2015 - 03/20/2015; Pilgrim Nuclear Power Station (PNPS);

Special Inspection to review the January 27, 2015 partial loss of offsite power (LOOP) and

reactor scram event; Inspection Procedure 93812, Special Inspection.

A six-person U.S. Nuclear Regulatory Commission (NRC) team, comprised of regional

inspectors and a regional senior reactor analyst, conducted this Special Inspection. The team

identified one finding and apparent violation (AV) that has been preliminarily determined to be of

low to moderate safety significance (White), one Severity Level (SL) IV non-cited violation

(NCV), and six findings of very low safety significance (Green), five of which were also NCVs.

The significance of most findings is indicated by their color (i.e., greater than Green, Green,

White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, Significance

Determination Process (SDP), dated June 2, 2011. Cross-cutting aspects are determined

using IMC 0310, Aspects Within the Cross-Cutting Areas, dated December 4, 2014. All

violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement

Policy, dated February 4, 2015. The NRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process,"

Revision 5, dated February 2014.

Cornerstone: Initiating Events

Green. A self-revealing Green finding was identified for Entergys failure to verify that the

diesel-driven air compressor (K-117) was available for service prior to the January 27, 2015

winter storm. Specifically, although K-117 was tested prior to the winter storm, the test

methodology did not reveal that the capacity of the starting battery was inadequate.

The failure to verify that the diesel-driven air compressor (K-117) was available for service

prior to the January 27, 2015 winter storm is a performance deficiency that was within

Entergys ability to foresee and correct. This resulted in a loss of instrument air during the

plant trip which complicated the event response. Entergy entered the issue into the

corrective action program (CAP) as condition report (CR)-PNP-2015-00559 and initiated

actions to supply instrument air with a temporary air compressor. Entergy also revised the

operability test for K-117 air compressor to remove the alternating current (AC) power

source prior to starting the air compressor.

This self-revealing issue was more than minor because it is associated with the procedure

quality and design control attributes of the Initiating Events cornerstone and adversely

impacted the cornerstone objective to limit the likelihood of events that upset plant stability

and challenge critical safety functions during shutdown as well as power operations.

Specifically, failure of K-117 resulted in loss of instrument air, which adversely impacted the

plant response during the January 27, 2015 winter storm. Additionally, this issue is also

associated with the procedure quality and design control attributes of the Mitigating Systems

cornerstone and affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating event to prevent undesirable consequences.

The inspectors screened the issue under the Initiating Events cornerstone using Attachment

4 and Exhibit 1 of Appendix A to IMC 0609, Significance Determination Process, because

that cornerstone was determined to be more impacted by the finding than the Mitigating

Systems cornerstone. The inspectors concluded that a detailed risk evaluation would be

required because the finding involved the complete loss of a support system (instrument air)

that contributes to the likelihood of an initiating event and affects mitigation equipment. A

4

Enclosure

senior reactor analyst performed a detailed risk evaluation of this issue. The NRC model for

PNPS was adjusted to account for a loss of the instrument air compressor on a LOOP. The

change in core damage frequency was very low. A review of the dominant accident

sequences indicated the contribution from a large early release and from external risk

contributors to be very small. Therefore, the issue was determined to be of very low risk

significance (Green).

The finding had a cross-cutting aspect in the area of Human Performance, Design Margins,

because Entergy failed to ensure that the K-117 battery was designed with adequate

margin. This finding is reflective of current performance because the inadequate design

margin of the battery should have been discovered through proper testing [H.6]. (Section

6.1)

Cornerstone: Mitigating Systems

Green. The team identified a Green NCV of Title 10 of the Code of Federal Regulations (10

CFR) 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, when Entergy

staff performed an inadequate past operability determination that assessed performance of

the C safety/relief valve (SRV), which did not open as expected when called upon to

function. Specifically, following the January 27, 2015 reactor scram, operators placed an

open demand for the C SRV twice during post-scram recovery operations, but the valve did

not respond as expected and did not perform its pressure reduction function on both

occasions. Entergys subsequent past operability assessment for the valves operation

incorrectly concluded that the valve was fully capable of performing its required functions

during its installed service. In response to the teams past operability concerns, Entergy

subsequently re-evaluated the past operability of C SRV and concluded that it was

inoperable and placed the issue into the corrective action program (CAP) as CR-PNP-2015-

02051.

The team determined the failure to adequately assess past operability of the C SRV was a

performance deficiency that was reasonably within Entergys ability to foresee and correct.

This NRC-identified performance deficiency is more than minor because it is associated with

the equipment performance attribute of the Mitigating Systems cornerstone and affects the

cornerstone objective of ensuring the availability, reliability, and capability of systems that

respond to initiating events to prevent core damage. The team evaluated the finding using

IMC 0609, Appendix 0609.04, Initial Characterization of Findings, which directed the use of

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power.

Using Exhibit 2, Mitigating Systems Screening Questions, of IMC 0609, Appendix A, the

team determined this finding was not a design or qualification deficiency and was not a

potential or actual loss of system or safety function, and was therefore of very low safety

significance (Green).

The finding had a cross-cutting aspect in Human Performance, Conservative Bias, because

Entergy did not use decision making practices that emphasized prudent choices over those

that are simply allowable. Specifically, Entergy did not appropriately evaluate unexpected

and unsatisfactory performance of the C SRV in consideration of the entire pressure range

that the SRV, including its automatic depressurization system (ADS) function, was required

to be operable [H.14]. (Section 2.4)

5

Enclosure

Apparent Violation. A self-revealing preliminary White finding and AV of 10 CFR 50,

Appendix B, Criterion XVI, Corrective Action, and Technical Specification (TS) 3.5.E,

Automatic Depressurization System, was identified for the failure to identify, evaluate, and

correct a significant condition adverse to quality associated with the A SRV. Specifically,

Entergy failed to identify, evaluate, and correct the A SRVs failure to open upon manual

actuation during a plant cooldown on February 9, 2013. In addition, the failure to take

actions to preclude repetition resulted in the C SRV failing to open due to a similar cause

following the January 27, 2015, LOOP event. Entergy entered this issue in to the CAP as

CR-PNP-2015-01983, CR-PNP-2015-00561, and CR-PNP-2015-01520. Immediate

corrective actions included replacing the A and C SRVs and completing a detailed

operability analysis of the installed SRVs which concluded that a reasonable assurance of

operability existed.

Entergys failure to identify, evaluate, and correct the condition of the A SRVs failure to

open upon manual actuation during a plant cooldown on February 9, 2013, was a

performance deficiency. In addition, the failure to take actions to preclude repetition

resulted in the C SRV failing to open due to a similar cause following the January 27, 2015

LOOP event. The self-revealing finding was within Entergys ability to foresee and correct

because indications were available to determine that the A SRV valve did not open upon

manual actuation. This was discovered as a result of an extent of condition review of the C

SRV failing to open upon manual actuation following the January 27, 2015 LOOP event.

This performance deficiency is more than minor because it could reasonably be viewed as a

precursor to a significant event if two of the four SRVs failed to open when demanded to

depressurize the reactor, following the failure of high pressure injection systems or torus

cooling, to allow low pressure injection systems to maintain reactor coolant system inventory

following certain initiating events. In addition, it is associated with the Mitigating Systems

cornerstone attribute of equipment performance and affected the cornerstone objective of

ensuring the availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences.

The inspectors screened this issue for safety significance in accordance with IMC 0609,

Appendix A, Exhibit 2, Mitigating Systems Screening Questions, issued June 19, 2012.

The screening determined that a detailed risk evaluation was required because it was

assumed that for a year period, two of the four SRVs were in a degraded state such that

they potentially would not have functioned to open at some pressure lower than rated

pressure and would not fulfill their safety function for greater than the TS allowed outage

time. Specifically, the assumptions of failures to open were based on: a failed actual

opening demand at 200 psig reactor pressure on January 27, 2015, for the C SRV;

examination of the valve internals at the testing vendor (National Technical Systems); and a

previous failed actual opening demand at 114 psig reactor pressure on February 9, 2013, for

the A SRV.

The staff determined that there wasnt an existing SDP risk tool that is suitable to assess the

significance of this finding with high confidence, mainly because of the uncertainties

associated with: the degradation mechanism and its rate; the range of reactor pressure at

which the degraded valves could be assumed to fully function; any potential benefit from an

SRV lifting at rated pressure, such that the degradation would be less likely to occur and,

therefore, prevent a subsequent failure at low pressure in the near-term; the time based

nature of plant transient response relative to when high pressure injection sources fail and

the associated impact of reduced decay heat on the SRV depressurization success criteria;

and the ability to credit other high pressure sources of water.

6

Enclosure

Based on the considerations above, the risk evaluation was performed using IMC 0609,

Appendix M, Significance Determination Process Using Qualitative Criteria, issued

April 12, 2012. The NRC made a preliminary determination that the finding was of low to

moderate safety significance (White) based on quantitative and qualitative evaluations.

The detailed risk evaluation is contained in Attachment 4 to this report.

This finding does not present a current safety concern because the A and C SRVs were

replaced during the outage following the January 27, 2015 LOOP and reactor trip event.

Also, Entergy performed a detailed operability analysis of the installed SRVs which

concluded that a reasonable assurance of operability existed.

This finding had a cross-cutting aspect in Problem Identification and Resolution, Evaluation,

because Entergy did not thoroughly evaluate issues to ensure that resolutions address

causes and extent of conditions commensurate with their safety significance. Specifically,

Entergy staff did not thoroughly evaluate the operation of the A SRV during the February 9,

2015 plant cooldown and should have reasonably identified that the A SRV did not open

upon three manual actuation demands [P.2]. (Section 2.5)

Green. A self-revealing Green NCV of TS 5.4.1, Procedures, was identified because

Entergy failed to include appropriate operator actions to both recognize the effects of and

recover systems and components important to safety within Procedure 5.3.8, Loss of

Instrument Air, abnormal operating procedure. Entergy entered this issue into the CAP as

PNP-CR-2015 0888 and issued a revision to Procedure 5.3.8 to provide additional guidance

to operators during a loss of instrument air.

The inspectors determined that the level of detail in Procedure 5.3.8, Loss of Instrument

Air, Revision 39, was inadequate to provide appropriate operator guidance to identify and

mitigate key events of January 27, 2015. This self-revealing performance deficiency was

reasonably within the ability of Entergy personnel to foresee and the issue should have been

prevented. The finding was more than minor because it was associated with the procedure

quality attribute of the Mitigating System cornerstone and adversely affected the cornerstone

objective of ensuring the availability, reliability, and capability of systems that respond to

initiating events to prevent undesired consequences. The lack of adequate instructions in

the procedure adversely affected several operator actions and plant equipment on

January 27, 2015, during the LOOP and loss of instrument air.

The team evaluated the finding using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems

Screening Questions. The team determined this finding was of very low safety significance

(Green) because it was not a design or qualification deficiency, did not result in a loss of

function of a TS required system, and did not represent an actual loss of function of one or

more non-TS trains of equipment designated as a high safety-significant system.

This finding had a cross-cutting aspect in the area of Human Performance, Resources,

because Entergy leaders did not ensure that personnel, equipment, procedures, and other

resources were available and adequate to support nuclear safety [H.1]. (Section 3.2)

Green. A self-revealing Green NCV of TS 5.4.1, Procedures, was identified because the

operating crew failed to implement a procedure step to open the reactor core isolation

cooling (RCIC) system cooling water supply valve during a manual startup of the system.

As a result, the RCIC system was operated for over 2 1/2 hours with no cooling water being

supplied to the lubricating oil cooler or to the barometric condenser. Entergy entered the

7

Enclosure

issue into the CAP as CR-PNP-2015-0566, CR-PNP-2015-0570, and CR-PNP-2015-0952

and conducted a human performance review of the Control Room operators involved with

the issue.

The inspectors determined that the failure to implement Procedure 5.3.35.1, Attachment 29,

RCIC Injection - Manual Alignment Checklist, and the Vacuum Tank Pressure Hi Alarm,

C904L-F3, alarm response procedure was a performance deficiency and was reasonably

within the ability of Entergy personnel to foresee and prevent. This self-revealing finding

was more than minor because it was associated with the human performance attribute of

the Mitigating System cornerstone and adversely affected the cornerstone objective of

ensuring the availability, reliability, and capability of systems that respond to initiating events

to prevent undesired consequences. Specifically, on January 27, 2015, reactor operators

failed to open MO-1301-62, cooling water supply valve, during a manual restart of the RCIC

system in accordance with procedure 5.3.35.1, RCIC Injection - Manual Alignment

Checklist. Additionally, the operating crew failed to identify the valve was out of position

even after the Vacuum Tank Pressure Hi Alarm, C904L-F3, was received two minutes after

the system was re-started and the alarm response procedure identified Improper Valve

Lineup as a probable cause.

The team evaluated the finding using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems

Screening Questions. The team determined this finding was not a design or qualification

deficiency and was not a potential or actual loss of system or safety function, and is

therefore of very low safety significance (Green). During the period when the RCIC system

was operated in this condition, no temperature limits were exceeded. The inspectors noted

that in the event of a RCIC system automatic start, the cooling water supply valve would

have opened automatically.

This finding had a cross-cutting aspect in the area of Human Performance, Procedure

Adherence, because Entergy licensed personnel did not implement procedure 5.3.35.1,

RCIC Injection - Manual Alignment Checklist, to open MO-1301-62. Additionally, Entergy

licensed personnel did not implement the Vacuum Tank Pressure Hi Alarm, C904L-F3,

response procedure to check for an improper valve line-up [H.8]. (Section 3.3)

Green. The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, because PNPS staff failed to identify and correct conditions adverse to

quality associated with the partial voiding of the A core spray (CS) discharge header on

January 27, 2015, following the loss of the keepfill system due to a LOOP. PNPS entered

the issue into the CAP as CR-PNP-2015-01406 and planned procedural changes that would

provide guidance to operate the affected pumps in order to prevent pump discharge piping

from voiding if keepfill pressure is lost.

The failure to identify, evaluate, and correct the A CS discharge header partial voiding

following loss of keepfill on January 27, 2015, is a performance deficiency that was within

Entergys ability to foresee and correct. Because the issue was not entered into the CAP,

the condition was neither evaluated nor was corrective action taken or planned. This NRC-

identified issue is more than minor because it is associated with the Mitigating Systems

cornerstone attribute of equipment performance and affected the cornerstone objective of

ensuring the availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences. The inspectors evaluated the finding using IMC

0609, Appendix A, The Significance Determination Process for Findings At-Power, to IMC

0609, Significance Determination Process. This finding was determined to be of very low

8

Enclosure

safety significance (Green) because it was not a deficiency affecting the design or

qualification of a mitigating system and did not represent an actual loss of at least a single

train system or two separate safety systems for greater than the TS allowed outage time.

The finding had a cross-cutting aspect in Problem Identification and Resolution,

Identification, because PNPS personnel did not implement a CAP with a low threshold for

identifying issues. Individuals did not identify the issue completely, accurately, and in a

timely manner in accordance with the program [P.1]. (Section 4.2)

Cornerstone: Emergency Preparedness

Green. The inspectors identified a Green NCV of 10 CFR 50.54(q)(2) for failing to follow

and maintain an emergency plan that meets the requirements of planning standards 10 CFR

50.47(b) and Appendix E. Specifically, on January 27, 2015, following a loss of instrument

air, the indications in the Control Room for Sea Water Bay level were lost, and Entergy did

not implement compensatory measures, as directed by an Emergency Plan Implementing

Procedure, to determine whether a Sea Water Bay level emergency action level (EAL)

threshold had been exceeded. Entergy entered this issue into the CAP as CR-PNP-2015-

00948 and initiated corrective actions to identify alternative means for assessing this EAL in

the event of a loss of Sea Water Bay level instruments.

The inspectors determined that Entergys failure to implement compensatory measures for

out-of-service EAL instrumentation was a performance deficiency that was within Entergys

ability to foresee and correct and should have been prevented. Specifically, Entergy did not

implement the compensatory measure listed in Attachment 9.2 of EP-IP-100.1, Emergency

Action Levels, Revision 10. The inspectors determined that following a loss of instrument

air, the indications for Sea Water Bay level EAL were lost, rendering those EALs ineffective

such that Entergy was not able to determine whether a Sea Water Bay level EAL threshold

had been exceeded and to declare an emergency based on the Sea Water Bay level. This

NRC-identified performance deficiency was more than minor because it was associated with

the emergency response organization performance (program elements not meeting 50.47(b)

planning standards) attribute of the Emergency Preparedness cornerstone and affected the

cornerstone objective of ensuring that the licensee is capable of implementing adequate

measures to protect the health and safety of the public in the event of a radiological

emergency. Specifically, the out-of-service Sea Water Bay level instrumentation could have

led to an emergency not being declared in a timely manner.

The inspectors evaluated the finding using IMC 0609, Attachment 4, Initial Characterization

of Findings, issued June 19, 2012. The attachment instructs the inspectors to utilize IMC

0609, Appendix B, Emergency Preparedness Significance Determination Process, issued

September 23, 2014, when the finding is in the licensees Emergency Preparedness

cornerstone. The inspectors determined the finding was associated with risk significant

planning standard 10 CFR 50.47(b)(4), Emergency Classification System, and

corresponded to the following Green Finding example in Table 5.4-1: an EAL has been

rendered ineffective such that any Alert or Unusual Event would not be declared, or

declared in a degraded manner for a particular off-normal event. Therefore, using Figure

5.4-1, Significance Determination for Ineffective EALs and Overclassification, and the

example in Table 5.4-1, the inspectors determined the finding was of very low safety

significance (Green).

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Enclosure

The finding had a cross-cutting aspect in the area of Human Performance, Documentation,

because Entergy did not maintain complete and accurate documentation. Specifically,

compensatory measures associated with out-of-service EAL instrumentation are not

governed by comprehensive and high-quality programs, processes, and procedures [H.7].

(Section 5.1)

Severity Level IV. An NRC-identified SL IV NCV of 10 CFR Part 50.72(b)(3)(xiii) was

identified when Entergy failed to make a required event notification within eight hours for a

major loss of assessment capability. Specifically, an unplanned loss occurred of all EAL

instrumentation associated with Sea Water Bay level that resulted in an inability to evaluate

all EALs for an abnormal water level condition. Entergy entered the issue into the CAP as

CR-PNP-2015-00949. Compliance was restored on February 5, 2015, when Entergy

reported the major loss of assessment capability under Event Notification50790.

The inspectors determined that Entergys failure to submit an event notification in

accordance with 10 CFR 50.72 within the required time was a performance deficiency that

was reasonably within Entergys ability to foresee and correct, and should have been

prevented. Since the failure to submit a required event report impacts the regulatory

process, the violation was evaluated using Section 2.2.4 of the NRCs Enforcement Policy,

dated July 9, 2013, instead of the SDP. Using the example listed in Section 6.9.d.9, A

licensee fails to make a report required by 10 CFR 50.72 or 10 CFR 50.73, the issue was

evaluated and determined to be a SL IV violation. The inspectors reviewed the condition for

reactor oversight process significance. Because this NRC-identified violation involves the

traditional enforcement process and does not have an underlying technical violation that

would be considered more-than-minor, the inspectors did not assign a cross-cutting aspect

to this violation in accordance with IMC 0612. (Section 5.2)

10

Enclosure

REPORT DETAILS

1.

Chronology of Events and Event Response Challenges

The team conducted a detailed review of the events leading up to, during, and following

the January 27, 2015 LOOP and resulting reactor scram at Entergys PNPS. The team

gathered information from operator narrative logs, the plant process computer, sequence

of events printouts, alarm printouts, and interviews with plant operators and engineering

staff to develop a detailed timeline of the event (Attachment 2). A diagram of the PNPS

switchyard is provided in Attachment 3. The following summary highlights the significant

events and challenges encountered by the PNPS staff:

Date/Time

Event

1/24

PNPS commenced storm preparations.

1/26

High winds and snow impact the site.

1/27 01:33

Control Room receives numerous grid disturbance alarms on 345 kilovolt

(kV) Line 355, operators reported flashing in the switchyard. Control

Room operators commenced power reduction per Procedure 2.1.42,

Operation during Severe Weather, and placed the safety-related Buses

A5 and A6 on the emergency diesel generators (EDGs) A and B,

respectively.

01:33-02:32

Line 355 power interrupted three times.

02:35

Line 355 is lost.

04:02

Reactor trip from 52 percent power due to generator load reject upon loss

of 345 kV Line 342. Per Emergency Operating Procedure (EOP)-1,

Reactor Pressure Vessel Control, operators closed the main steam

isolation valves and placed the RCIC system in level control and the high

pressure coolant injection (HPCI) system in pressure control mode.

04:12

Operators commenced a plant cooldown. Diesel-driven air compressor

K-117 attempted to start and failed to run on low instrument air header

pressure (sustained loss of instrument air).

09:48

Operators secured the HPCI system at approximately 120 psig reactor

vessel pressure, commencing reactor pressure control using SRVs and

the RCIC system. Operators commence periodic operation of the B CS

pump for level control.

09:53

HPCI system declared inoperable following receipt of Gland Seal

Condenser Blower Overload Alarm. Condensate discovered backing-up

through the blower due to the shutdown condensate flow path being

isolated to the Radioactive Waste Building (caused by loss of instrument

air).

10:56

Following challenges in controlling reactor pressure (pressure increased

from approximately 120 psig to 350 psig) and level, operators manually

start the RCIC system in the pressure control mode and begin to open

SRVs for longer periods of time to reestablish cooldown.

16:26

B residual heat removal (RHR) system placed in shutdown cooling.

16:46

EOP-1 exited.

16:57

Reactor temperature <212°F.

1/28 10:47

Instrument air system fully restored using a temporary diesel-driven air

compressor.

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Enclosure

1/30 18:45

Offsite power restored via Lines 355 and 342 following de-icing and

inspection of the switchyard with the assistance of the grid operator,

NSTAR.

1/31 01:30

Safety-related Buses A5 and A6 were restored to their normal offsite

power sources.

PNPS staff began making site preparations on January 24, 2015, in accordance with

plant procedures, for the impact of a forecasted winter storm in the Plymouth,

Massachusetts area. At 01:33 on January 27, during blizzard conditions, Control Room

operators observed numerous grid disturbance alarms associated with one of the two

offsite 345kV distribution lines, Line 355. In addition, operators in the field reported

electrical flash-overs in the switchyard. In accordance with Procedure No. 2.1.42,

Operation during Severe Weather, Revision 21, operators began lowering reactor

power based on the anticipated LOOP. One of the procedures objectives was to lower

reactor power below 130MWe, within the turbine bypass valve capability, to minimize a

potential reactor power transient. Operators transferred safety-related Buses A5 and A6

to their respective EDG sources and placed Reactor Protection System Bus A on its

alternate power supply, per procedure, to improve reliability based on the electrical grid

conditions. Additionally, offsite power remained available to Buses A5 and A6 via the

shutdown transformer (SDT) powered from the stations 23Kv line. At 02:35, Line 355

tripped and the line could not be returned to service.

Challenges

At 04:02, operators observed a generator load reject and automatic reactor scram when

the remaining offsite 345kV distribution line, Line 342, de-energized. Prior to that time,

no grid disturbance alarms originated on Line 342. Grid disturbances originating on Line

355 caused grid disturbance alarms on Line 342. Operators entered EOP-1, Reactor

Pressure Vessel (RPV) Control, due to reactor vessel level <12 inches caused by the

transient. Per EOP-1, Control Room operators closed the main steam isolation valves,

placed the RCIC system in service for RPV level control, and the HPCI system in service

in the RPV pressure control mode. At 04:12, operators commenced a plant cooldown.

All systems responded properly to the LOOP event with the exception of diesel-driven air

compressor K-117, which failed to automatically start and run on low instrument air

pressure. The failure of the K-117 air compressor to start resulted in a sustained loss of

instrument air. Control Room operators ability to cope with and recover from the loss of

instrument air was complicated by the absence of adequate procedural guidance. Refer

to Sections 3, 5, and 6 for detailed team observations and findings associated with the

loss of instrument air.

By 09:48, operators had reduced reactor pressure to approximately 120 psig. Because

of a higher than desired cooldown rate using the HPCI system and due to approaching

the HPCI system low pressure isolation setpoint, operators secured the HPCI system

and transitioned reactor pressure control to manually cycling SRVs and by using the

RCIC system in pressure control mode. RPV level control was achieved by periodically

injecting with the B CS pump.

Shortly after the HPCI system was secured, Control Room operators received the Gland

Seal Condenser Blower Overload Alarm. The cause was promptly determined to be

condensate and cooling water backing up into the blower after the normal discharge flow

path was automatically isolated and the standby flow path to the Radioactive Waste

12

Enclosure

Building was unavailable due to the loss of instrument air. The HPCI system was

declared inoperable per procedural requirements due to the gland seal condenser being

inoperable, however, the HPCI system was still considered available if required to

operate.

The team noted that prior to commencing pressure control by cycling SRVs, operators

raised reactor vessel level to the higher end of the EOP-1 prescribed level band.

Because RPV level was high in the allowable level band, operators opened the SRVs for

only brief periods of time to prevent the consequential RPV level swell from causing a

RCIC system high level isolation at +45 inches. In spite of these precautions, the RCIC

system did isolate at 10:16 on high level. The RCIC system was later restarted in

pressure control mode at 10:56. Complicating operators ability to appropriately control

RPV level was the inability to lower RPV level using the reactor water cleanup (RWCU)

system letdown valve that had failed close on the loss of instrument air. While being

challenged with RPV pressure and level control, reactor pressure increased from 120

psig (09:48) to approximately 330 psig (11:30). At that time, operators prioritized

maintaining an SRV open for longer periods of time to reduce pressure. Following this

change in priorities, the Control Room staff was successful in stabilizing RPV level and

pressure. In addition, a temporary air supply was aligned to the RWCU system letdown

isolation valve and normal RPV level control was restored. The team determined that

the SRVs were manually cycled 105 times (52 for the B SRV and 53 for the D SRV)

while attempting to stabilize pressure and control RPV level with the CS pump.

The team determined that the Control Room operators had planned to operate the B,

C, and D SRVs sequentially to reduce RPV pressure. The A SRV was not used due

to previously identified pilot valve leakage. During the first attempt to open the C SRV

from the Control Room, the expected system response was not observed. With the C

SRV open signal applied approximately 52 seconds, the tailpipe temperature increased

slightly, but the acoustic response was much lower than expected and no reactor

pressure reduction was observed. A second attempt was made to open the C SRV

leaving the open signal applied for 83 seconds, with similar results. Due to the apparent

failure of the C SRV to open on demand at this lower RPV pressure and temperature,

operators continued the RPV depressurization and cooldown using only the B and D

SRVs.

2.

Equipment Response to the Event

a. Inspection Scope

The team reviewed and assessed the initial equipment conditions and equipment

response including consistency with the plants design and regulatory requirements, and

identification of any potential design deficiencies. The team reviewed the adequacy of

associated operability assessments, technical evaluations, corrective and preventive

maintenance, and post-maintenance testing. The team also evaluated the safety

significance of equipment issues identified during the event as well as the impact on the

plants license, TS, regulatory requirements, and aging management programs. The

team reviewed the event timeline, the post trip Scram Report, operator narrative logs,

PNPS CAP CRs, modification packages, drawings, and component maintenance

histories. The team also attended an Operational Safety Review Committee meeting

associated with the operability of the plant SRVs.

13

Enclosure

b.

Findings and Observations

2.1

General Performance

Response to the LOOP and reactor scram event on January 27, 2015, was complicated

by several equipment performance issues. The loss of instrument air because the K-117

diesel-driven air compressor failed to start during the event, along with an inadequate

loss of instrument air abnormal operating procedure, complicated operator recovery

actions. Findings associated with these issues are documented in Sections 3, 5, and 6

of this report. In addition, the HPCI system was declared inoperable, but remained

available, following being secured due to the loss of the gland seal condenser because

of the loss of instrument air and the lack of appropriate procedural guidance.

More significantly, the C SRV did not open upon manual actuation to reduce reactor

pressure. Following disassembly, the valves manufacturer, Curtiss-Wright Flow Control

Company, Target Rock Division, issued 10 CFR Part 21 Interim Report (EN 50900) on

March 17, 2015, due to the potential to induce a defect during the testing of the relief

valve model (three stage Target Rock Model 0867F). On May 1, 2015, Curtiss-Wright

Flow Control Company provided an update to the interim report which stated that the

root cause was not yet determined. As a result of the failure of the C SRV to actuate

during the event, Entergy performed a detailed review of plant parameters associated

with past operations of Model 0867F. During the extent of condition review, Entergy

identified that the A SRV failed to open upon three manual actuations during a LOOP

event that occurred on February 9, 2013. A self-revealing preliminary White finding was

identified and is documented in Section 2.5.

2.2

HPCI System

Shortly after the reactor scram, the HPCI system was operated in the pressure control

mode (i.e., the system was operating in recirculation mode and the HPCI turbine was

removing steam/reducing reactor pressure). Operators shut down the HPCI system

several hours later, at 09:48, when reactor pressure was approaching 100 psig. A few

minutes later, the Gland Seal Condenser Hotwell High Level and Gland Seal Condenser

Blower Overload Alarms were received in the Control Room. Around 10:10, an operator

that was dispatched to the HPCI room reported an acrid smell in the HPCI room, the

gland seal condenser blower motor was hot to the touch, and that he observed water

streaming from the blower housing shaft seal area. There was no significant water

accumulation on the HPCI room floor at that time. Operators declared the HPCI system

inoperable (as of 09:48) in accordance with Procedure 2.2.21.5, HPCI Injection and

Pressure Control, and Procedure 2.2.21, HPCI System. Specifically, the procedure

stated that in the event the HPCI gland seal condenser becomes inoperable, excessive

shaft and valve stem leakage could result in the HPCI area coolers to reach and exceed

their heat load limits, and accordingly, the HPCI system shall be declared inoperable.

An operator again entered the HPCI room several hours later (around 13:00) and

reported approximately one inch of water on the HPCI room floor. The Control Room

Narrative Log indicated that EOP-4, Secondary Containment Control, was entered at

13:07 due to water in the HPCI compartment (greater than one inch). At 13:10, the

Operations Shift Manager determined that no emergency existed as there was no active

leak in the HPCI room and the suspected source of water was from the reactor building

sumps overflowing due to the loss of power. EOP-4 was exited at 13:34.

14

Enclosure

Condensation in the HPCI system from sources such as valve stem and turbine seal

leakage is routed to the HPCI gland seal condenser, which condenses the steam and

uses a condensate pump to return water to the HPCI pump suction (while HPCI is in

service) or to the radioactive waste system (when HPCI is shutdown). Any non-

condensable gases that accumulate in the gland seal condenser are routed via the gland

seal condenser exhauster (blower) to the reactor building ventilation or standby gas

treatment system. In the piping downstream of the condensate pump, there are two

series air-operated valves (AO-2301-64 and -65) that open when the HPCI system is

shut down to route the condensate to the radioactive waste system for processing.

However, during this event, the instrument air system was lost, and as a result, these

two valves failed in the closed position. This configuration resulted in continuing to fill

the HPCI suction piping and the gland seal condenser to the point that water began

leaking from the gland seal blower.

There is a curb that surrounds the gland seal condenser area in the HPCI room.

Therefore, the water that was leaking/spraying from the blower was largely isolated to

this curbed area. However, also at some time after the HPCI system was shut down, the

reactor building sumps, which are located inside the HPCI room (near the entrance)

overflowed into the HPCI room. The four associated sump pumps were not available

due to the loss of power. The majority of the water that comprised the one inch of water

on the HPCI floor was suspected to be from the reactor building floor drain sump.

2.3

SRV Performance

PNPS has four SRVs, manufactured by Target Rock, located on the steam lines inside

the primary containment. They are three-stage dual function valves that operate in a

safety mode or a relief mode. The SRVs comprise the ADS, which is designed to

depressurize the reactor, in the event the HPCI system cannot maintain reactor water

level during certain postulated accidents so that the low pressure emergency core

cooling system (ECCS) can inject water. The SRVs provide: 1) over-pressure relief

operation (self-actuated to limit the pressure rise and prevent spring safety valve

opening); 2) over-pressure safety operation (augment the spring safety valves by

opening in order to prevent RPV over-pressurization); and 3) depressurization operation.

The SRVs are designed with controls to open and close the valves at any steam

pressure above 104 psig, and capable of holding the valves open until the steam

pressure decreases to about 50 psig.

During the January 27, 2015 transient, the operators planned to operate the B, C, and

D SRVs sequentially to reduce reactor pressure in accordance with emergency

procedures. The A SRV was not planned to be used due to previously identified pilot

valve leakage, but was considered by Entergy to be available for use if needed. After

successfully cycling the B SRV, operators applied an open demand to the C SRV for

52 seconds at a reduced plant pressure of approximately 220 psig; however, the

expected system response did not accompany the open demand. Specifically, although

the tailpipe temperature increased (indicative of steam exhausting to the torus), the

acoustic monitor response was less than normal, and reactor pressure continued to

increase. For the next 15 minutes, operators continued to depressurize using other

SRVs, and then attempted to cycle the C SRV again. This time, the open demand

remained for 83 seconds; tailpipe temperature increased and the associated acoustic

monitor indicated a normal response (that the SRV was open), but reactor pressure did

not respond as expected. Due to the abnormal response from the C SRV at reduced

15

Enclosure

plant pressure, operators continued to operate both the B and D SRVs over about a

three hour period, cycling them 52 and 53 times, respectively. The SRVs were cycled

frequently and for short duration (5 - 10 seconds) due to concerns with the associated

reactor vessel water level swell when each SRV opens. The consequence of a high

reactor water level is that the RCIC system would isolate, and in fact, the system did

isolate during the cooldown. The D SRV was subsequently opened and remained open

for about three hours to achieve an effective pressure reduction.

Subsequent to the resulting plant shutdown, Entergy conducted limited as-found

testing of the C SRV while still installed, and removed both the A and C SRVs from

service. The installed as-found test of the C SRV was conducted on January 31, 2015,

and was observed by the NRC resident inspector. This test verified solenoid operation

and movement of the air actuator plunger locally. This was done when the RPV was

depressurized, so there was no operation of the valve internals (no pressure source to

move the main valve). Both the solenoid and associated air operator moved as

designed, with timely solenoid actuation and smooth actuator travel in both directions.

This successful test confirmed only that the solenoid and air operator were free to move

and responded to an actuation signal.

The C SRV was subsequently sent to an offsite testing facility for as-found setpoint

verification, low pressure testing, and an inspection of valve internal components. While

the C SRV satisfactorily stroked during both the setpoint test and additional low

pressure (100 psig) actuation test at the testing facility, the inspection revealed notable

damage to some internal valve main stage parts. Specifically, the main valve piston had

indications of some scoring and the lower piston ring (two rings in total) was seized

within the piston ring. The most noteworthy damage was wear (grooves) in the main

operating cylinder liner where the operating piston rings rest while the valve is in its

closed position. The cylinder liner wear resulted in resistance to valve operation in the

open direction through contact with the operating piston rings. Upon the disassembly,

the technicians noted that the piston was not tightly secured and the locking tab was

slightly rotated out of its grooved position. In its normal/assembled condition, the main

valve stem is threaded into the main piston, torqued, and is secured with a washer and

stem nut with locking tab on the opposite side of the piston (See SRV figure below).

16

Enclosure

The assembly of the valve is such that the main stem is torqued to the piston (100 ft-lbs)

and the stem nut is torqued to the threaded end of the main stem (50 ft-lbs). However,

there has been prior operating experience, including an instance at PNPS in 2013,

where the stem nut was found loose. Based on prior operating experience, there have

been separate issues that may have contributed to torque relaxation or looseness at the

stem/piston or stem nut interface. These included 1) inadequate stem shoulder contact

at the main stem/piston interface, 2) inefficient test gag device that potentially allowed

substantial internal valve impact during full pressure setpoint testing, and 3) a stem nut

torque value that was less than optimal. It was not apparent that a single item alone was

the cause for the identified issues. Further, based on historical operating and internal

inspection data, internal wear problems were not assured even when the old style test

gag device and lower stem nut torque existed (i.e., human performance/installation and

specific in-service vibration levels may also have had negative impacts). The testing

facility currently uses a re-designed test gag device to prevent a large impact force

during the full pressure bench testing, and the vendor recommended an increased stem

nut torque value (100 ft-lbs) in December 2013.

Entergy also sent the A SRV for as-found testing and internals inspection. As stated

earlier, the valve was not selected for cycling during the transient, although it was

considered to be available (the valve was not selected because it previously had a

known pilot valve leak). Both the as-found full pressure lift, including setpoint

Diagram of Target Rock SRV from

NRC Information Notice 2003-01, Failure

of Boiling Water Reactor Target Rock Main

Steam Safety/Relief Valve, dated

January 15, 2003

17

Enclosure

verification, and the 100 psig SRV lift were completed satisfactorily at the testing facility.

However, disassembly and inspection of the valves internal parts yielded similar results

(e.g., operating cylinder liner wear) to that of the C SRV. As a result of the as-found

inspection results of the A and C SRVs, Curtiss-Wright Flow Control Company, Target

Rock Division, issued Interim 10 CFR Part 21 Interim Report (EN 50900) on March 17,

2015, due to the potential to induce a defect during the testing of the relief valve model

(three stage Target Rock Model 0867F).

During the shutdown following the January 27, 2015, reactor scram, Entergy replaced

both the A and C SRVs with refurbished and certified replacement SRVs. Both were

tested with the new test gag design. The A SRV was refurbished prior to the stem nut

torque value change so it was torqued to 50 ft-lbs, and the stem nut for the C SRV,

refurbished later, was torqued in accordance with revised instructions and was torqued

to 100 ft-lbs. With respect to the B and D SRVs, which operated satisfactorily during

the transient, they had both previously been tested prior to their May 2013 installation

and both had a 50 ft-lb torque applied to the stem nut.

2.4

Past Operability Evaluation of C SRV

Introduction. The team identified a Green NCV of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, when Entergy staff performed an inadequate

past operability determination that assessed performance of the C SRV which did not

open as expected when called upon to function. Specifically, following the January 27,

2015, reactor scram, operators placed an open demand for the C SRV twice during

post-scram recovery operations, but the valve did not respond as expected and did not

perform its pressure reduction function on both occasions. Entergys subsequent past

operability assessment for the valves operation incorrectly concluded that the valve was

fully capable of performing its required functions during its installed service.

Description. Following the SRV issues and in particular, the January 27, 2015

unexpected in-service response of the C SRV, Entergy conducted operability

evaluations, both for the prior condition of the C SRV (past operability) and for all four

currently installed SRVs. Entergy examined and assessed SRV data for the B and D

SRVs following the transient and multiple SRV cycles, and concluded that there were no

abnormalities evident from the data. Entergy also reviewed prior test data, including the

as-left full pressure lift test for the B and D SRVs when they were installed in May

2013; both tests were satisfactory. Based on the information reviewed, Entergy judged

both the B and D SRVs to be operable. With respect to the newly installed

replacement A and C SRVs, Entergy confirmed that both SRVs were full pressure lift

setpoint verified using the re-designed test gag device, which minimized the potential for

loss of stem nut preload due to impact forces. In addition, both A and C SRVs were

satisfactorily tested on February 7, 2015, during plant startup activities.

Entergys past operability evaluation (CR-PNP-2015-00561), dated February 5, 2015, for

the C SRV that was removed following the January 27, 2015 reactor scram concluded

that during the first manual operation of the SRV, there was only a partial opening stroke

on the main stage disc; and a full opening (but slower than the open stroke seen on the

B and D SRVs) on the second manual operation. The evaluation also noted that the

subsequent bench tests, conducted at the testing facility, demonstrated acceptable SRV

operation both during the as-found set pressure test (over-pressure lift) and the special

test using the air actuator (at 100 psig). Entergys past operability evaluation concluded

18

Enclosure

that the C SRV was fully capable of performing its required functions during its installed

service, and the ADS was fully operational during the time that the C SRV was

installed, as evidenced by its successful lift during its initial startup test and as-found lift

test after its removal (SRV main seat opening forces are significantly higher at full

reactor pressure). They further concluded that the observed operation at low reactor

pressure (during post-scram operations) would not have prevented its successful

operation to continue with the depressurization of the reactor had the continued use of

C SRV been required.

The team reviewed Entergys operability assessment, which was completed to support

reactor startup following the LOOP event, and found that Entergy demonstrated that

there was reasonable assurance of continued SRV operability for the four installed

SRVs. In particular, the history of similar SRV challenges appears to have been the

result of a combination of several factors. Based on a review of the valve assembly

data, stem shoulder contact, laboratory testing technique/device (test gag), and main

stem to stem nut torque, the team concluded that there was reasonable assurance that

the installed SRVs could perform their intended functions.

However, the team did not agree with Entergys past operability assessment associated

with the C SRV. Although data shows that the valve did in fact open at least partially

and slowly, it did not achieve the design function result intended to reduce reactor

pressure. Updated Final Safety Analysis Report Section 4.4.5 stated that for

depressurization operation, each relief valve is provided with a power actuated device

capable of opening the valve at any steam pressure above 100 psig, and capable of

holding the valve open until the steam pressure decreases to about 50 psig. As this is a

design function of the valve and it was not able to perform this function, the team

considered this valve to be inoperable for this function. Further, TS 3.5.E, Automatic

Depressurization System (ADS), required that the system shall be operable when

reactor pressure is greater than 104 psig. As stated earlier, Control Room operators

discontinued further use of this valve after two attempts because it failed to achieve the

desired pressure reduction result. The team acknowledged that the valve likely would

have performed its over-pressure and ADS function at normal operating pressure due to

the significantly higher opening forces in that condition, but would not (and did not)

perform acceptably at lower reactor pressure. Considering the above, the team

concluded that the past operability assessment for the C SRV was inadequate.

Procedure EN-OP-104, Operability Determination Process, Revision 7, provides a

process to assess operability and functionality when degraded or nonconforming

conditions affecting structures, systems, and components (SSCs) are identified. The

procedure (Definitions - Specified Safety Function) stated that, in addition to providing

the specified safety function, a system is expected to perform as designed, tested, and

maintained. When system capability is degraded to a point where it cannot perform with

reasonable expectation of reliability, the system should be judged inoperable. If the

component or system cannot perform at the level required by TSs, then it should be

considered inoperable. Section 5.11.[12](c) of the procedure stated that when an SSCs

capability or reliability is degraded to the point where there is no longer a reasonable

expectation that it can perform its specified safety function, the SSC should be judged

inoperable. The team concluded that there was not a reasonable expectation of

operability, in particular during low pressure operations, and that Entergy incorrectly

concluded that the C SRV was fully capable of performing its required functions

because Procedure EN-OP-104 was not followed. Also, Procedure EN-LI-102,

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Enclosure

Corrective Action Program, Revision 24, defined significant conditions adverse to

quality as failures, malfunctions, deficiencies, deviations, defective material and

equipment, and nonconformances that adversely affect the safety-related functions of

SSCs deemed significant based on actual or potential consequences to nuclear safety;

and these conditions require the cause of the condition to be determined and corrective

action taken to preclude repetition. In addition, Section 5.5.[2] of the procedure stated

that CRs assigned a Significance Category A (which would be the category for a

significant condition adverse to quality) require a root cause evaluation and corrective

action to preclude repetition. Only an equipment apparent cause analysis was assigned

to evaluate the degraded C SRV performance; and therefore, specific root causes

would not necessarily be identified, and appropriate associated corrective actions to

preclude repetition may not be developed and implemented.

In response to the teams past operability concerns, Entergy subsequently re-evaluated

the past operability of C SRV and concluded that it was inoperable; they initiated CR-

PNP-2015-02051 to document and address this issue.

There has been prior operating experience in the area of similar SRV issues, including

problems at both PNPS and other nuclear utilities. Both the valve vendor and testing

facility have also issued generic communications that included recommendations and

corrective actions. The team found that the parties involved have been appropriately

incorporating these actions (i.e., main stem shoulder engagement, improved test gag

design, stem nut torque values). However, continued generic assessment is warranted

based upon this most recent operational problem. Entergys evaluation (CR-PNP-2015-

00908, Corrective Action 4) is expected to evaluate any additional generic issues

associated with this issue. In addition, Entergy removed all four SRVs during the April

2015 refueling outage to conduct the required full pressure setpoint verification/bench

test as well as conducting a valve disassembly and inspection to confirm the as-found

condition of these valves.

Analysis. The team determined the failure to adequately assess past operability of the

C SRV was a performance deficiency that was reasonably within Entergys ability to

foresee and correct. This NRC-identified performance deficiency is more than minor

because it is associated with the equipment performance attribute of the Mitigating

Systems cornerstone and affects the cornerstone objective of ensuring the availability,

reliability, and capability of systems that respond to initiating events to prevent core

damage. The team evaluated the finding using IMC 0609, Appendix 0609.04, Initial

Characterization of Findings, which directed the use of IMC 0609, Appendix A, The

Significance Determination Process (SDP) for Findings At-Power. Using Exhibit 2,

Mitigating Systems Screening Questions, of IMC 0609, Appendix A, the team

determined this finding was not a design or qualification deficiency and was not a

potential or actual loss of system or safety function, and is therefore of very low safety

significance (Green).

The finding had a cross-cutting aspect in Human Performance, Conservative Bias,

because Entergy did not use decision making practices that emphasized prudent

choices over those that are simply allowable. Specifically, Entergy did not appropriately

evaluate unexpected and unsatisfactory performance of the C SRV in consideration of

the entire pressure range that the SRV, including its ADS function, was required to be

operable [H.14].

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Enclosure

Enforcement. 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, states, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings and shall be accomplished in

accordance with these instructions, procedures, or drawings. Procedure EN-OP-104,

Operability Determination Process, Revision 7, states, in part, that when an SSCs

capability or reliability is degraded to the point where there is no longer a reasonable

expectation that it can perform its specified safety function, the SSC should be

judged inoperable. Contrary to this, on February 5, 2015, Entergy performed a past

operability determination of the C SRV (following the January 27, 2015 reactor scram),

and concluded that the valve was operable during its installed service despite its failure

to perform its pressure reduction function when manually actuated twice by operators.

Because this finding is of very low safety significance and has been entered into

Entergys CAP as CR-PNP-2015-02051, this violation is being treated as an NCV,

consistent with Section 2.3.2.a of the NRC Enforcement Policy. (NCV

05000293/2015007-01, Inadequate Past Operability Assessment of C Safety Relief

Valve)

2.5

Self-Revealing Preliminary White Finding and AV of Criterion 16 and TS 3.5.E

Introduction. A self-revealing preliminary White finding and AV of 10 CFR 50, Appendix

B, Criterion XVI, Corrective Action, and TS 3.5.E, Automatic Depressurization

System, was identified for the failure to identify, evaluate, and correct a significant

condition adverse to quality associated with the A SRV. Specifically, Entergy failed to

identify, evaluate, and correct the A SRVs failure to open upon manual actuation during

a plant cooldown on February 9, 2013. In addition, the failure to take actions to preclude

repetition resulted in the C SRV failing to open due to a similar cause following the

January 27, 2015, LOOP event.

Description. During Entergys investigation of the January 27, 2015 partial LOOP event,

Entergy staff reviewed plant parameter data associated with historical SRV actuations.

During the review, Entergy staff determined that the A SRV similarly did not open

during manual actuations on February 9, 2013, during a plant cooldown following a

LOOP event. This determination was based on Entergys review of the response of

reactor pressure, level, local suppression pool temperature, and SRV tailpipe

temperature.

Entergy identified that, during the February 9, 2013, event, operators attempted to utilize

the A SRV to reduce reactor pressure on three occasions (at 114 psig, 101 psig, and at

98 psig). The operators observed that the A SRV did not yield the appropriate tailpipe

acoustic monitor response, although tailpipe temperature did show an increase.

Following the third opening without observing the appropriate acoustic monitor response,

operators only utilized the C and D SRVs for plant cooldown [note that the operators

considered that the B SRV was less desirable to use due to previously-observed pilot

valve leakage]. Operators wrote CR-PNP-2013-00825 to document the condition and

recommended an action to evaluate performance of the A SRV. Although the CR

discussed the acoustic monitor and SRV tailpipe responses to the opening demand, no

other information of other plant parameters that are normally used to verify an SRV

opening (e.g., reactor level swell, reactor pressure) was documented. The only action

that resulted from CR-PNP-2013-00825 was the replacement of components associated

with the A SRVs acoustic monitor. CR-PNP-2013-00825 documented the conclusion

that no degraded or nonconforming condition existed because the tailpipe thermocouple

21

Enclosure

indicated that the SRV opened based on tailpipe temperature response. The inspectors

noted that although tailpipe temperature did increase following the open demand due to

SRV pilot valve operating, the temperature increase was lower than would be expected

for an open SRV main valve disc.

The inspectors reviewed CR-PNP-2013-00825 and plant parameter data. The team

concluded that information was available, both real-time and post-trip, such that Entergy

could have reasonably identified that the A SRV did not open upon manual actuation

demand on three occasions during the February 9, 2013 plant cooldown. Specifically:

Operators could have reasonably identified that the A SRV did not open based on

lack of reactor pressure response (pressure increased) and that no expected

indicated reactor vessel level swell was observed. Although the valve open demand

was applied for over 1.5 minutes during the first attempt to open the valve at a

reactor pressure of 114 psig, no reactor pressure decrease or reactor vessel level

swell, consistent with the valve opening, occurred. During two subsequent, shorter

opening attempts, similar indications were available.

Review of the work orders that documented the work performed on the A SRV

acoustic monitor following the February 9, 2013 LOOP event did not identify that a

problem existed which impaired the instruments ability to respond to a valve opening

event. No as-found functional testing was performed. Maintenance workers

identified an electrical ground on the system. However, the conditions effect on the

systems ability to respond to the A SRV tailpipe acoustic response was not further

reviewed.

Entergys post-trip event review performed a review of plant equipment performance

during the event. However, although CR-PNP-2013-00825 suggested an evaluation

of the A SRV performance during the February 9, 2013 LOOP event, the post-trip

event review did not identify performance issues with the A SRV. The inspectors

judged that information was available to the post-trip review team to determine that

the A SRV did not open during open demand actuation attempts.

Analysis. Entergys failure to identify, evaluate, and correct the condition of the A

SRVs failure to open upon manual actuation during a plant cooldown on February 9,

2013, was a performance deficiency. In addition, the failure to take actions to preclude

repetition resulted in the C SRV failing to open due to a similar cause following the

January 27, 2015 LOOP event. The self-revealing finding was within Entergys ability to

foresee and correct because indications were available to determine that the A SRV

valve did not open upon manual actuation. This was discovered as a result of an extent

of condition review of the C SRV failing to open upon manual actuation following the

January 27, 2015 LOOP event. This performance deficiency is more than minor

because it could reasonably be viewed as a precursor to a significant event if two of the

four SRVs failed to open when demanded to depressurize the reactor, following the

failure of high pressure injection systems or torus cooling, to allow low pressure injection

systems to maintain reactor coolant system inventory following certain initiating events.

In addition, it is associated with the Mitigating Systems cornerstone attribute of

equipment performance and affected the cornerstone objective of ensuring the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences.

The inspectors screened this issue for safety significance in accordance with IMC 0609,

Appendix A, Exhibit 2, Mitigating Systems Screening Questions, issued June 19, 2012.

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Enclosure

The screening determined that a detailed risk evaluation was required because it was

assumed that for a one year period, two of the four SRVs were in a degraded state such

that they potentially would not have functioned to open at an undetermined pressure

lower than rated pressure and would not fulfill their safety function for greater than the

TS allowed outage time. Specifically, the assumptions of failures to open were based on

a failed actual opening demand at 200 psig reactor pressure on January 27, 2015, for

the C SRV; examination of the valve internals at the testing vendor (National Technical

Systems); and a previous failed actual opening demand at 114 psig reactor pressure on

February 9, 2013, for the A SRV.

The staff determined that there wasnt an existing SDP risk tool that is suitable to assess

the significance of this finding with high confidence, mainly because of the uncertainties

associated with: the degradation mechanism and its rate; the range of reactor pressure

at which the degraded valves could be assumed to fully function; any potential benefit

from an SRV lifting at rated pressure, such that the degradation would be less likely to

occur and, therefore, prevent a subsequent failure at low pressure in the near-term; the

time based nature of plant transient response relative to when high pressure injection

sources fail and the associated impact of reduced decay heat on the SRV

depressurization success criteria; and the ability to credit other high pressure sources of

water.

Based on the considerations above, the risk evaluation was performed using IMC 0609,

Appendix M, Significance Determination Process Using Qualitative Criteria, issued

April 12, 2012. A planning Significance Determination Process Enforcement Review

Panel (SERP) was conducted on April 7, 2015, which concurred with using Appendix M

in this case. The use of Appendix M is appropriate because it is intended to be used

when the probabilistic risk assessment methods and tools, including the existing SDP

appendices, cannot adequately address the findings complexity or provide a reasonable

estimate of the significance due to modeling and other uncertainties within the

established SDP timeliness goal of 90 days or less.

The NRC made a preliminary determination that the finding was of low to moderate

safety significance (White) based on quantitative and qualitative evaluations. The

detailed risk evaluation is contained in Attachment 4 to this report.

This finding had a cross-cutting aspect in Problem Identification and Resolution,

Evaluation, because Entergy did not thoroughly evaluate issues to ensure that

resolutions address causes and extent of conditions commensurate with their safety

significance. Specifically, Entergy staff did not thoroughly evaluate the operation of the

A SRV during the February 9, 2013 plant cooldown and should have reasonably

identified that the A SRV did not open upon three manual actuation demands [P.2].

Enforcement. 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in

part, that measures shall be established to assure that conditions adverse to quality,

such as failures, malfunctions, and deficiencies, are promptly identified and corrected.

In the case of significant conditions adverse to quality, the measures shall assure that

the cause of the condition is determined and corrective action taken to preclude

repetition. TS 3.5.E, Automatic Depressurization System, requires the ADS to be

operable whenever there is irradiated fuel in the reactor vessel and the reactor pressure

is greater than 104 psig and prior to a startup from a Cold Condition. From and after the

date that one valve in the ADS is made or found to be inoperable for any reason,

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Enclosure

continued reactor operation is permissible only during the succeeding 14 days.

Otherwise, an orderly shutdown of the reactor shall be initiated and the reactor shall be

in the Cold Shutdown condition within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Contrary to the above, on February 9, 2013, measures established by Entergy did not

assure that a significant condition adverse to quality was promptly identified, or that the

cause of the condition was determined and corrective actions taken to preclude

repetition. Specifically, indications were available that the A SRV did not open upon

manual actuation during the February 9, 2013 LOOP event. Although this constituted a

significant condition adverse to quality, Entergy failed to identify and correct the

condition, or to take actions to preclude repetition, resulting in a similar occurrence when

the C SRV did not open upon manual actuation during a subsequent LOOP event on

January 27, 2015. As a consequence of this failure, PNPS also violated TS 3.5.E

because the A SRV was rendered inoperable from February 9, 2013, until the valve

was removed from service following the January 27, 2015 LOOP event (greater than the

14 day allowed outage time). Entergy entered this issue in to the CAP as CR-PNP-

2015-01983, CR-PNP-2015-00561, and CR-PNP-2015-01520. This finding does not

present a current safety concern because the A and C SRVs were replaced during the

outage following the January 27, 2015 LOOP and reactor trip event. Also, Entergy

performed a detailed operability analysis of the installed SRVs which concluded that a

reasonable assurance of operability existed. (AV 05000293/2015007-02, Failure to

Identify, Evaluate, and Correct A SRV Failure to Open Upon Manual Actuation)

3.

Event Diagnosis and Crew Performance

a. Inspection Scope

The team reviewed and assessed operator performance during plant preparations for

the storms approach to the PNPS area, during the LOOP and reactor scram event, and

during plant stabilization and plant cooldown to Cold Shutdown. The team reviewed the

event timeline, plant procedures, operating narrative logs, communications (internal and

external), the post trip Scram Report, and PNPS CAP CRs. The team interviewed

Control Room operators who were on shift during the storms approach and during the

LOOP event and the relief operators who performed the plant cooldown to Cold

Shutdown. The team utilized the plant Control Room simulator to verify that the plant

response was consistent with the design and that operator actions during the event were

consistent with plant procedures and operator training.

b. Findings and Observations

3.1

General Performance

The team performed a detailed review of operator performance during the event.

Operator performance was challenged by the LOOP and loss of instrument air. The loss

of instrument air resulted in the HPCI system gland seal condenser overflowing and loss

of RWCU letdown flow, which complicated RPV level control. This resulted in excessive

cycling of the B and D SRVs for pressure control after HPCI was secured. Individual

issues and notable observations are discussed in 3.2 through 3.5 below.

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Enclosure

3.2

Loss of Instrument Air

Introduction. A self-revealing Green NCV of TS 5.4.1, Procedures, was identified

because Entergy failed to include appropriate operator actions to both recognize the

effects of, and recover systems and components important to safety within abnormal

operating procedure 5.3.8, Loss of Instrument Air.

Description. During review of the LOOP and reactor scram event on January 27, 2015,

the team identified that Procedure 5.3.8, Loss of Instrument Air, was inadequate to

provide operator guidance to both identify key adverse effects on the plant and operator

actions to conduct recovery actions to stabilize the plant. During interviews with the

team, on-shift licensed operators stated that the effects of the loss of instrument air were

not immediately recognized or well understood because of the lack of procedural

guidance. The inspectors also noted that a sustained loss of instrument air simulator

scenario had never been performed. The inspectors determined that if the scenario had

been performed, at least some of the inadequate guidance provided by Procedure 5.3.8

would have been identified. Examples of plant systems affected by the loss of

instrument air and not identified in Procedure 5.3.8 as being affected included; HPCI,

RWCU, Control Room Condensate Storage Tank (CST) level indicator LI-3503A, and

Control Room Sea Water Bay level indicators.

The lack of an adequate loss of instrument air abnormal operating procedure adversely

affected the following operator actions and plant equipment on January 27, 2015, during

the loss of instrument air following the LOOP and reactor scram:

The HPCI system was declared inoperable upon discovery of the effects of the gland

seal condenser hotwell pump air operated drain valves to radioactive waste, the

normal shutdown flow path, failing closed due to the loss of instrument air. When the

HPCI system was shut down by Control Room operators, the normal operating flow

path from the turbine gland seal hotwell pump discharge to the HPCI pump suction

became unavailable by design. This caused water to overfill the gland seal

condenser hotwell which caused the Gland Seal Condenser Blower Overload Alarm

to be received. Operators were unaware of the impact that loss of instrument air

would have on the securing of the HPCI system.

RWCU letdown valve CV-1239 failed closed eliminating RWCU letdown which led to

the excessive cycling of SRVs for short durations to keep reactor water level in band

(less than +45 inches) so that RCIC would not isolate when level swelled. RWCU

letdown was recovered approximately ten hours after loss of instrument air following

the implementation of an emergent modification to supply CV-1239 with nitrogen

from portable cylinders.

Sea Water Bay level indicators (LI-3831A and LI-3831B) became inoperable which

eliminated the ability to monitor EAL entry conditions for abnormal Sea Water Bay

level with the lack of an established backup monitoring method. Operators were

unaware of the impact that loss of instrument air would have on intake level EAL

declarations.

The loss of CST level instrumentation (LI-3503A and LI-3503B) directly affected the

operating crews decision to not operate the CS system with preferred suction on the

CST for reactor pressure vessel inventory control. Procedure 5.3.8 did not provide

this procedural guidance.

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Enclosure

Two separate temporary instrument air compressors were required to be installed

with a temporary modification in order to restore instrument air pressure. With the

use of the first temporary air compressor, the attempt to restore air pressure 13

hours into the event resulted in only achieving an instrument air pressure of 80 psig.

A second temporary air compressor was needed to obtain and stabilize air pressure

at 100 psig approximately 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> after the initial loss of instrument air. The loss of

instrument air procedure did not identify any temporary air compressor

contingencies.

Analysis. The inspectors determined that the level of detail in Procedure 5.3.8, Loss of

Instrument Air, Revision 39, was inadequate to provide appropriate operator guidance

to identify and mitigate key events of January 27, 2015. This self-revealing performance

deficiency was reasonably within Entergys ability to foresee and the issue should have

been prevented. The finding was more than minor because it was associated with the

procedure quality attribute of the Mitigating System cornerstone and adversely affected

the cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesired consequences. The lack of

adequate instructions in the procedure adversely affected several operator actions and

plant equipment on January, 27, 2015, during the LOOP and loss of instrument air.

The team evaluated the finding using IMC 0609, Appendix A, Exhibit 2, Mitigating

Systems Screening Questions. The team determined this finding was of very low safety

significance (Green) because it was not a design or qualification deficiency, did not

result in a loss of function of a TS required system, and did not represent an actual loss

of function of one or more non-TS trains of equipment designated as a high safety-

significant system.

This finding had a cross-cutting aspect in the area of Human Performance, Resources,

because Entergy leaders did not ensure that personnel, equipment, procedures, and

other resources were available and adequate to support nuclear safety [H.1].

Enforcement. TS 5.4.1, Procedures, requires that written procedures shall be

established, implemented, and maintained covering the activities recommended in

Regulatory Guide (RG) 1.33, Revision 2, Appendix A, February 1978. RG 1.33,

Appendix A lists loss of instrument air under Procedures for Combating Emergencies

and other significant Events.

Contrary to TS 5.4.1, Entergy failed to establish and maintain a procedure to address the

loss of instrument air with appropriate direction for combating the event. Specifically,

Procedure 5.3.8, Loss of Instrument Air, Revision 39, failed to provide mitigating

operator actions for multiple systems which directly impaired licensed operator actions

and affected the ability to stabilize and cool down the plant during the LOOP and loss of

instrument air events on January 27, 2015. Licensed operator actions were impaired, in

part, due to the procedure not identifying the effects on important plant

systems/components or lack of identification of component restoration or compensatory

actions associated with important plant systems and components. Examples of systems

adversely affected by the loss of instrument air and not identified as being affected in the

abnormal procedure included: the HPCI system, the RWCU system, and Sea Water Bay

level indicators. Entergy entered this issue into the CAP as PNP-CR-2015-0888 and

issued a revision to Procedure 5.3.8 to provide additional guidance to operators during a

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Enclosure

loss of instrument air. However, because the finding was of very low safety significance

(Green) and has been entered into the CAP, this violation is being treated as an NCV,

consistent with section 2.3.2.a of the NRC's Enforcement Policy. (NCV

05000293/2015007-03, Inadequate Loss of Instrument Air Abnormal Operating

Procedure)

3.3

RCIC Manual Restart

Introduction. A self-revealing Green NCV of TS 5.4.1, Procedures, was identified

because the operating crew failed to implement a procedure step to open the RCIC

system cooling water supply valve during a manual startup of the RCIC system. As a

result, the RCIC system was operated for over 2 1/2 hours with no cooling water being

supplied to the lubricating oil cooler or to the barometric condenser.

Description. While the operating crew was conducting a reactor cooldown on

January 27, 2015, with SRVs, reactor level control was being augmented with the use of

RCIC. At 10:16, the RCIC system tripped on high reactor vessel level when an SRV

was opened to control reactor pressure. The RCIC system trip was caused by reactor

vessel level swell rising above the 45 inch trip signal.

When the RCIC system was restarted at 10:56 in accordance with Procedure 5.3.35.1,

Attachment 29, RCIC Injection - Manual Alignment Checklist, the reactor operator

failed to open MO-1301-62, cooling water supply valve, in accordance with procedure

step 2. Step 2 stated: Open/Verify Open MO-1301-62, Cooling Water Supply Valve.

The failure to open MO-1301-62 was an operator human performance error.

Water from the discharge of the RCIC pump supplies the cooling medium for the RCIC

system turbine lubricating oil cooler and the gland seal condenser via valve MO-1301-

62. The pumps suction is normally lined up to the CST. At 10:58, the Control Room

received the Vacuum Tank Pressure Hi Alarm, C904L-F3. The alarm response

procedure identified improper valve lineup under possible causes for the alarm. A

dispatched equipment operator reported at 11:15 that the level in the RCIC vacuum tank

was normal at 1/2 full with no apparent leaks.

Between 12:22 and 12:49, multiple A bus 125 volts direct current (VDC) ground alarms,

C3RC-C7, were received and cleared. At 12:57, the Control Room received the Vacuum

Tank Level High Alarm. This alarm provided another opportunity to investigate the valve

lineup because the alarm response procedure stated to investigate the cause of the

alarm as an operator corrective action. An engineering walk down of the system at

13:10 identified that the barometric condenser vacuum tank sight glass was empty, the

vacuum tank was pressurized to 1.5 psig, and the vacuum tank temperature was 220°F.

Without adequate vacuum in the barometric condenser vacuum tank, the site attributed

that a pump motor (gland seal vacuum pump and/or gland seal condensate pump)

experienced some moisture from out of its pump seal due to the vacuum tank being

pressurized. Both the gland seal vacuum pump and the gland seal condensate pump

motors are powered from A 125 VDC power panel D-7.

Additionally, the pressurized vacuum tank had the potential to cause excessive gland

seal condensate pump leakage. Procedure 2.22.22, Reactor Core Isolation Cooling,

step 5.2, requires RCIC shall be declared inoperative whenever its barometric

condenser condensate pump is inoperative.

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Enclosure

MO-1301-62 was identified as being in the wrong position as the RCIC system was

being secured at 13:32. The control switch for MO-1301-62 remained in the Auto

position. The control switch should have been positioned to the Open position when

RCIC was manually restarted. The team determined that there was no cooling water

supplied to the RCIC lubricating oil cooler or the barometric condenser from the start of

the RCIC system at 10:56 until it was secured at 13:32.

Analysis. The inspectors determined that the failure to implement Procedure 5.3.35.1,

Attachment 29, RCIC Injection - Manual Alignment Checklist, and the Vacuum Tank

Pressure Hi, C904L-F3, alarm response procedure was a performance deficiency and

was reasonably within the ability of Entergy personnel to foresee and prevent. This self-

revealing finding was more than minor because it was associated with the human

performance attribute of the Mitigating System cornerstone and adversely affected the

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesired consequences. Specifically, on

January 27, 2015, reactor operators failed to open MO-1301-62, cooling water supply

valve, during a manual restart of the RCIC system in accordance with Procedure

5.3.35.1, Attachment 29, RCIC Injection - Manual Alignment Checklist. Additionally,

the operating crew failed to identify the valve was out of position even after the Vacuum

Tank Pressure Hi Alarm, C904L-F3, was received two minutes after the system was re-

started and the alarm response procedure identified Improper Valve Lineup as a

probable cause.

The team evaluated the finding using IMC 0609, Appendix A, Exhibit 2, Mitigating

Systems Screening Questions. The team determined this finding was not a design or

qualification deficiency and was not a potential or actual loss of system or safety

function, and is therefore of very low safety significance (Green). During the period

when the RCIC system was operated in this condition, no temperature limits were

exceeded. The inspectors noted that in the event of a RCIC system automatic start, the

cooling water supply valve would have opened automatically.

This finding had a cross-cutting aspect in the area of Human Performance, Procedure

Adherence, because licensed personnel did not implement procedure 5.3.35.1,

Attachment 29, RCIC Injection - Manual Alignment Checklist, to open MO-1301-62.

Additionally, PNPS licensed personnel did not implement the Vacuum Tank Pressure Hi

Alarm, C904L-F3, response procedure to check for an improper valve line-up [H.8].

Enforcement. TS 5.4.1, Procedures, requires that written procedures shall be

established, implemented, and maintained covering the activities recommended in RG

1.33, Revision 2, Appendix A, February 1978. RG 1.33, Appendix A, requires

procedures for operation, abnormal, off-normal, or alarm conditions for the RCIC system.

Step 2 of Procedure 5.3.35.1, Attachment 29, RCIC Injection - Manual Alignment

Checklist, requires that MO-1301-62, cooling water supply valve, be placed in the open

position when manually starting the RCIC system.

Contrary to the above, on January 27, 2015, licensed operators failed to properly

implement Procedure 5.3.35.1, Attachment 29, RCIC Injection - Manual Alignment

Checklist, and open MO-1301-62, cooling water supply valve, during a RCIC system

manual startup following a RCIC system trip. The RCIC system was operated for over 2

1/2 hours with MO-1301-62 closed. Additionally, contrary to Alarm Response Procedure

C904L, Revision 18, operators failed to evaluate the system lineup for an improper valve

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Enclosure

lineup. Entergy entered the issue into the CAP as CR-PNP-2015-0566, CR-PNP-2015-

0570, and CR-PNP-2015-0952 and conducted a human performance review of the

Control Room operators involved with the issue. Because the finding was of very low

safety significance (Green) and has been entered into the CAP, this violation is being

treated as an NCV, consistent with section 2.3.2.a of the NRC's Enforcement Policy.

(NCV 05000293/2015007-04, Failure to Follow RCIC System Manual Restart

Procedure)

3.4

RPV Control during Reactor Cooldown

The team identified a licensed operator training weakness involving the execution of

EOPs during the response to the January 27, 2015 LOOP and reactor scram event.

Specifically, the Control Room operations crew did not effectively implement EOP-1,

RPV Control. While the RCIC system was in level control, the operating crew

maintained a reactor water level band of +40 inches to +20 inches during their cool down

approach to a reactor pressure of 120 psig and the securing of the HPCI system. The

self-imposed narrow reactor water level band resulted in the crew manually starting and

operating the B CS pump when level was lowering to +20 inches. These operator

actions resulted in reactor water level being high in their EOP reactor water level band.

With the planned shutdown of HPCI system and the subsequent use of SRV to control

reactor pressure, reactor water level should have been maintained low in the acceptable

normal band of +45 inches to +12 inches to accommodate reactor water level swells

when the crew opened SRVs.

As a result of not maintaining reactor water level low in the allowable band of +45 inches

to +12 inches, the RCIC system tripped on reactor high water level due to the reactor

level swell upon use of an SRV. Reactor pressure was at 225 psig and rising at the time

of the RCIC trip. In order to limit reactor vessel level increases due to swell, the

operating crew limited the time an SRV was opened. Although EOPs direct alternate

pressure control systems that were available to the crew, the crew elected to just use

SRVs. This crew decision to focus on maintaining reactor vessel level in band resulted

in a reactor pressure rising from 120 psig to 350 psig over an hour and a half, and

opening the B and D SRVs a total of 105 times during the cooldown.

The number of repetitive opening and closing of SRVs was undesirable for the following

reasons:

It exerted significant dynamic loads upon the RPV, the SRV tail pipes, supporting

structures, and the primary containment.

Swell and shrink associated with SRV actuations caused RPV water fluctuations that

complicate level control actions.

The potential for a stuck open SRV was increased.

EOP-1, RPV Pressure leg step P-6 requires when the main condenser is not available

to: Depressurize RPV and maintain cool down rate using Alternate Pressure Control

Systems. Table D, Alternate Pressure Control Systems, provided adequate direction

to stabilize reactor pressure and maintain an appropriate cool down rate.

EOP-1 RPV Level leg states: Restore and maintain RPV water level to +45 inches to

+12 inches using Injection Systems. The EOP users guide addresses this level band

when dealing with SRV actuations, stating that it may be necessary to expand the

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Enclosure

control band (lower than +12 inches) to maintain level below the high level trip set point

(+45 inches).

The inspectors determined that there are several knowledge and training issues that

occurred or became evident during the event. However, these issues did not result in a

failure to comply with the EOP. Operating crew knowledge and training weaknesses

included:

1) EOP reactor water level control strategies on an impending use of SRVs.

2) HPCI system response following a complete loss of instrument air event.

3) Understanding that water level swell above +45 inches is temporary and allowed

during efforts to restore and maintain +45 to +12 inch level band.

CR-PNP-2015-00706 and CR-PNP-2015-00720 were written to address and improve

operator knowledge in these areas.

3.5

Failure to Accurately Model the Simulator for HPCI and RCIC System during a Loss of

Instrument Air

Three minor violations of 10 CFR 55.46(c)(1), "Plant Referenced Simulators," were

identified because the PNPS simulator did not accurately model the actual plant

response, as follows:

1) When the HPCI system was manually secured during the event, the operation of the

condensate pump with no discharge flow path led to the overfilling of the gland seal

exhaust condenser and the receipt of alarms for condenser high level and gland seal

blower overload. For the same event run on the simulator, the gland seal exhaust

condenser tank level never rose or actuated a high level alarm. The high level or

blower overload alarm could not be received because the simulator modeling locks

this function at the condenser level at the time of HPCI shutdown. The simulator did

not model a dynamic gland seal condenser level response unless the HPCI turbine is

in operation.

2) When the RCIC system was operated for 2 1/2 hours with the cooling water supply

valve closed during the event, the Vacuum Tank Level Hi and the Vacuum Tank

Pressure Hi alarms were received. For the same event run on the simulator, no

RCIC system alarms were received.

3) In the actual plant, the HPCI turbine exhaust drain pot drain valve (CV-2301-32) and

HPCI exhaust line drain pot drain valves (CV-9068A and CV-9068B) are operated

directly as solenoid valves. However, these valves are incorrectly modeled on the

simulator as air operated valves that fail closed on loss of air while in the plant they

would not fail closed on loss of air because they are positioned using a direct current

operated solenoid control valve.

Incorrect simulator modeling of the PNPS plant could have resulted in negative operator

training, potentially affecting the ability of operators to take appropriate actions during an

actual event. These performance deficiencies were evaluated against IMC 0612,

Appendix B, Issue Screening. The performance deficiencies were not viewed as a

precursor to a significant event, not related to a performance indicator, and did not

adversely affect a cornerstone objective. If left uncorrected, the performance

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Enclosure

deficiencies did not have the potential to lead to a more significant safety concern. This

performance deficiency has been determined to be a minor violation requiring corrective

actions.

Entergy has taken actions to restore compliance for the three simulator modeling minor

violations by initiating the following corrective action reports: CR-PNP-2015-0563, CR-

PNP-2015-0566, CR-PNP-2015-0706, CR-PNP-2015-0912, and CR-PNP-2015-1075.

4.

Effectiveness of Licensees Response

a. Inspection Scope

The team reviewed and assessed the effectiveness of Entergys overall response to this

event. This included a review of both internal and external communications, directions

of actions from the Control Room and Outage Control Center, and a review of short term

actions taken to address equipment issues. The team interviewed plant personnel

involved in the management and review of the event. The team also reviewed operator

narrative logs, the post trip Scram Report, and PNPS CAP CRs.

b. Findings and Observations

4.1

General Performance

Leading up to the storm, the site was periodically in contact with the grid operator,

NSTAR, ISO-NE, and other plants on the grid. During the approach of the storm,

Control Room operators were in contact with NSTAR at least hourly and, at times,

continuously. Control Room operators were monitoring the storms status by monitoring

the National Weather Service website.

The Emergency Operating Facility was manned to minimum staffing during the storm.

Periodic communications with Massachusetts Emergency Management Agency were

performed to discuss general conditions as a result of the storm.

Following the event, Entergy worked with NSTAR in assessing the PNPS switchyard for

damage and in the recovery effort to assure switchyard reliability prior to re-energization.

The inspectors concluded that Entergys general response to the winter storm was in

accordance with established procedures and incorporated lessons learned from prior

events.

4.2

A CS Discharge Header Pressure Low Alarm

Introduction. The inspectors identified a Green NCV of 10 CFR 50, Appendix B,

Criterion XVI, because PNPS staff failed to identify and correct conditions adverse to

quality associated with the partial voiding of the A CS discharge header on January 27,

2015, following the loss of the keepfill system due to a LOOP.

Description. In order to assure that ECCS discharge headers are filled, vented, and

contain no voiding, a positive pressure is placed on the piping using the keepfill portion

of the Condensate Transfer system. This is performed to assure compliance with TS

Limiting Condition for Operation (LCO) 3.5.H, Core and Containment Cooling Systems,

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Enclosure

which requires that ECCS discharge piping be maintained full of water. At PNPS, the

condensate transfer pumps supply keepfill to the ECCS discharge headers. The CS

discharge piping is normally maintained at approximately 120 psig. With the LOOP, the

condensate transfer pumps were lost. Shortly thereafter at 04:03, the Control Room

started receiving intermittent CS A Discharge Header Pressure Low Alarms

(annunciates at 33.2 psig). The Alarm Response Procedure, ARP-C903L-E7, directs

operators to investigate and correct the cause of the low pressure and to ensure that TS

LCO 3.5.H is satisfied.

During the review of Operations Department Night Order, dated February 6, 2015, which

documented an assessment of operator response during the LOOP, the SIT identified a

condition adverse to quality that had not been documented in the PNPS CAP. The night

order described that the operating crew had not utilized the A CS pump for level control

because the train had a Discharge Header Pressure Low Alarm and the crew had

concern for potential pipe voiding. Pipe voiding could have caused discharge piping

water hammer if the pump was operated. The inspectors noted that no operator

narrative log entry, LCO log entry, or CR documented the condition. In addition, the

issue was not identified in the post trip Scram Report or by Entergys Corporate Event

Response Team that was dispatched to PNPS to independently review the event. The

SIT questioned why the issue had not been entered into the CAP and whether any

ECCS discharge pipe voiding occurred following the LOOP. Entergy entered the issue

into the CAP as CR-PNP-2015-01406.

The evaluation determined that the A CS system was at least partially voided when the

A CS Discharge Header Pressure Low Alarms locked in at 08:26. Similarly, the B CS

system was also at least partially voided when that systems Discharge Header

Pressure Low Alarm locked in later on January 27 at 23:13. However, B CS was not

required to be operable at the time because the unit was in Cold Shutdown. The RHR

system discharge headers were not affected because the RHR pumps were started

shortly after the LOOP event for suppression pool cooling.

Analysis. The failure to identify, evaluate, and correct the A CS discharge header

partial voiding following loss of keepfill on January 27, 2015, is a performance deficiency

that was within Entergys ability to foresee and correct. This NRC-identified issue is

more than minor because it is associated with the Mitigating Systems cornerstone

attribute of equipment performance and affected the cornerstone objective of ensuring

the availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. The inspectors evaluated the finding using IMC

0609, Appendix A, The Significance Determination Process for Findings At-Power, to

IMC 0609, Significance Determination Process. This finding was determined to be of

very low safety significance (Green) because it was not a deficiency affecting the design

or qualification of a mitigating system and did not represent an actual loss of at least a

single train system or two separate safety systems for greater than the TS allowed

outage time.

The finding had a cross-cutting aspect in Problem Identification and Resolution,

Identification, because PNPS personnel did not implement a CAP with a low threshold

for identifying issues. Individuals did not identify the issue completely, accurately, and in

a timely manner in accordance with the program [P.1].

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Enclosure

Enforcement. 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in

part, that measures shall be established to assure that conditions adverse to quality,

such as failures, malfunctions, and deficiencies, are promptly identified and corrected.

Contrary to Criterion XVI, PNPS failed to identify and correct conditions adverse to

quality associated with the partial voiding of the A and B CS discharge headers on

January 27, 2015, following the loss of the keepfill system due to a LOOP. PNPS

entered the issue into the CAP as CR-PNP-2015-01406 and planned procedural

changes that would provide guidance to operate the affected pumps in order to prevent

pump discharge piping from voiding if keepfill pressure is lost. Because this violation is

of very low safety significance and has been entered into Entergys CAP as CR-PNP-

2015-01406, this finding is being treated as an NCV consistent with Section 2.3.2.a of

the NRC Enforcement Policy. (NCV 05000293/2015007-05, Failure to Identify

Condition Adverse to Quality Associated with CS Discharge Header Voiding)

5.

Implementation of the Emergency Plan

a. Inspection Scope

The team reviewed and assessed the adequacy of Entergys implementation of the

PNPS Emergency Plan and EAL classifications. The team interviewed plant personnel

involved in the implementation and maintenance of the Emergency Plan and EALs. The

team reviewed applicable CRs generated as a result of the partial LOOP event to

determine whether the Emergency Plan and equipment required to implement it were

impacted. In addition to reviewing the Emergency Plan and EALs, the team reviewed

the EAL basis document and the procedure which addresses compensatory measures

required for Emergency Plan equipment which is out-of-service.

b. Findings and Observations

The inspectors reviewed Entergys EAL scheme and basis, specifically the LOOP EAL,

to determine whether a threshold had been exceeded. The EAL associated with an

Unusual Event at Pilgrim is SU1.1 and states, loss of all offsite AC power (Table S-3) to

emergency buses A5 and A6 for greater than 15 minutes. Table S-3 lists the following

offsite AC power sources: Startup Transformer, SDT, Unit Auxiliary Transformer, and

Backscuttle via Main Transformer (only if already established). Two 345kV lines (line

342 and line 355) are the preferred power supplies to the offsite sources listed in Table

S-3 with a 23kV line that supplies secondary power. The inspectors determined that

because the 23kV line was available to supply power to the SDT, that offsite power was

still available, and therefore, the entry criteria for the LOOP EAL was not met. The

inspectors determined that Entergy implemented the EALs appropriate at PNPS;

however, the inspectors identified two findings associated with the maintenance and

implementation of the Emergency Plan and 10 CFR 50.72 reporting requirements.

5.1

Failure to Implement Compensatory Measures for Out-of-Service EAL Instrumentation

Introduction. The inspectors identified a Green NCV of 10 CFR 50.54(q)(2) for failing to

follow and maintain an emergency plan that meets the requirements of planning

standards 10 CFR 50.47(b) and Appendix E. Specifically, on January 27, 2015,

following a loss of instrument air, the indications in the Control Room for Sea Water Bay

level were lost, and Entergy did not implement compensatory measures, as directed by

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Enclosure

an Emergency Plan Implementing Procedure, to determine whether a Sea Water Bay

level EAL threshold had been exceeded.

Description. The EAL declaration conditions for low or high Sea Water Bay level are

indicated in the Control Room by instrumentations (LI-3831 A/B) which display water

level in reference to mean sea level (MSL). Operators use these instruments to

determine whether an EAL threshold has been exceeded associated with an abnormal

Sea Water Bay level. The EAL thresholds for an Unusual Event (HU1.5) are Sea Water

Bay water level greater than +13 feet 6 inches MSL or bay water level less than -13 feet

9 inches MSL. The Alert (HA1.6) classification level thresholds are greater than +16 feet

0 inches MSL and -16 feet 0 inches MSL.

Entergy utilized Emergency Plan Implementing Procedures to provide guidance to

operators and emergency response organization members for following and maintaining

the planning standard functions in the approved Emergency Plan. Specifically, Entergy

developed Emergency Plan Implementing Procedure EP-IP-100.1, Emergency Action

Levels, to provide guidance to operators for classifying abnormal plant events and

compensating actions for out-of-service EAL equipment.

On January 27, 2015, PNPS experienced a loss of instrument air which subsequently

led to the loss of indication on LI-3831 A/B in the Control Room. This loss rendered the

associated EALs ineffective since no alternative means existed with which to evaluate

whether EAL thresholds associated with Sea Water Bay level were exceeded. In

response to questions raised by the inspectors, Entergy explained that, although no

compensatory measures had been taken for this event, the compensatory measure for a

loss of instruments LI-3831 A/B indication was to perform a visual inspection of the bay

level as addressed in EP-IP-100.1, Emergency Action Levels. However, the inspectors

determined this was not a viable compensatory measure. Specifically, the

compensatory measure was not addressed in a procedure such that it would provide

guidance to operators the manner in which to perform the visual inspection. Additionally,

Entergy confirmed that Control Room personnel and emergency response organization

personnel had not been trained upon or made aware of the compensatory measure.

The inspectors reviewed tidal data during the event and determined that actual Sea

Water Bay level did not challenge the EAL threshold.

Analysis. The inspectors determined that Entergys failure to implement compensatory

measures for out-of-service EAL instrumentation was a performance deficiency that was

within Entergys ability to foresee and correct and should have been prevented.

Specifically, Entergy did not implement the compensatory measure listed in Attachment

9.2 of EP-IP-100.1, Emergency Action Levels, Revision 10. The inspectors determined

that following a loss of instrument air, the indications for Sea Water Bay level EAL were

lost, rendering those EALs ineffective such that Entergy was not able to determine

whether a Sea Water Bay level EAL threshold had been exceeded and to declare an

emergency based on the Sea Water Bay level. This NRC-identified performance

deficiency was more than minor because it was associated with the emergency

response organization performance (program elements not meeting 50.47(b) planning

standards) attribute of the Emergency Preparedness cornerstone and affected the

cornerstone objective of ensuring that the licensee is capable of implementing adequate

measures to protect the health and safety of the public in the event of a radiological

emergency. Specifically, the out-of-service Sea Water Bay level instrumentation could

have led to an emergency not being declared in a timely manner.

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Enclosure

The inspectors evaluated the finding using IMC 0609, Attachment 4, Initial

Characterization of Findings, issued June 19, 2012. The attachment instructs the

inspectors to utilize IMC 0609, Appendix B, Emergency Preparedness Significance

Determination Process, issued September 23, 2014, when the finding is in the

licensees Emergency Preparedness cornerstone. The inspectors determined the

finding was associated with risk significant planning standard 10 CFR 50.47(b)(4),

Emergency Classification System, and corresponded to the following Green Finding

example in Table 5.4-1: an EAL has been rendered ineffective such that any Alert or

Unusual Event would not be declared, or declared in a degraded manner for a particular

off-normal event. Therefore, using Figure 5.4-1, Significance Determination for

Ineffective EALs and Overclassification, and the example in Table 5.4-1, the inspectors

determined the finding was of very low safety significance (Green).

The finding had a cross-cutting aspect in the area of Human Performance,

Documentation, because Entergy does not maintain complete and accurate

documentation. Specifically, compensatory measures associated with out-of-service

EAL instrumentation are not governed by comprehensive and high-quality programs,

processes, and procedures [H.7].

Enforcement. 10 CFR 50.54(q)(2) requires, in part, that a licensee shall follow and

maintain an emergency plan that meets the planning standards of 10 CFR 50.47(b) and

Appendix E. Emergency Plan Implementing Procedure EP-IP-100.1 directs a

compensatory measure of visual inspection for out-of-service Sea Water Bay EAL

instrumentation. Contrary to the above, on January 27, 2015, Entergy failed to

implement compensatory measures for out-of-service EAL instrumentation. Specifically,

during the partial LOOP event with a subsequent loss of instrument air, the indications

for the Sea Water Bay level (LI-3831A/B) were lost. The loss of these indications

degraded Entergys ability to determine whether an EAL threshold had been exceeded

for low or high Sea Water Bay level and to classify the emergency. Compliance was

restored later on January 27, 2015, when instrument air was returned to service and the

level instruments were functioning properly. Additionally, Entergy initiated corrective

actions to identify alternative means for assessing this EAL in the event of a loss of Sea

Water Bay level instruments. Because this violation is of very low safety significance

and has been entered into Entergys CAP as CR-PNP-2015-00948, this finding is being

treated as an NCV consistent with Section 2.3.2.a of the NRC Enforcement Policy.

(NCV 05000293/2015007-06, Failure to Implement Compensatory Measures for Out-

of-Service EAL Instrumentation)

5.2

Failure to Report a Major Loss of Emergency Assessment Capability

Introduction. An NRC-identified SL IV NCV of 10 CFR Part 50.72(b)(3)(xiii) was

identified when Entergy failed to make a required event notification within eight hours for

a major loss of assessment capability. Specifically, an unplanned loss occurred of all

EAL instrumentation associated with Sea Water Bay level occurred that resulted in an

inability to evaluate all EALs for an abnormal water level condition.

Description. On January 27, 2015, Entergy experienced a partial LOOP at PNPS that

resulted in a subsequent loss of instrument air. The loss of instrument air resulted in a

loss of water level indication in the Sea Water Bays. The affected instruments, LI-3831

A/B, are utilized in assessing conditions for entry into the EALs.

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Enclosure

NUREG-1022, Event Report Guidelines 10 CFR 50.72(b)(3)(xiii), Revision 3,

Supplement 1, endorsed Nuclear Energy Institute (NEI) 13-01, Reportable Action

Levels for Loss of Emergency Preparedness Capabilities, dated July 2014. NEI 13-01

provides specific guidance for reporting under 10 CFR 50.72(b)(3)(xiii) and, as a result,

reduces the need for engineering judgment. Guidance found in NEI 13-01 provides for

an acceptable alternative to guidance found in Section 3.2.13 of NUREG-1022, Revision

3. NUREG-1022, Revision 3, Supplement 1, section 2.1 states that for scenarios in

which an initiating condition (IC) has multiple EALs that assess different conditions (i.e.,

an IC for natural hazards with EALs for high wind speed, seismic event, flooding),

instrumentation failures that result in an inability to evaluate all EALs for one of the

conditions would be considered a major loss of emergency assessment.

The inspectors determined that the January 27, 2015 loss of indication to Sea Water Bay

level instrumentation (LI-3831 A/B) was a major loss of emergency assessment because

of the inability to evaluate all EALs for an abnormal Sea Water Bay level and, therefore,

was reportable under 10 CFR Part 50.72(b)(3)(xiii). The inspectors questioned Entergy

on why they had not reported the event as a major loss of assessment capability.

Entergy believed this unplanned loss was not reportable because they had a

compensatory measure to perform a visual inspection. Entergy has committed to and

implemented NEI 13-01 for determining reportability. NEI 13-01 does not allow for

consideration of compensatory measures when evaluating reportabilty for unplanned

losses of EAL instrumentation. Entergy determined through a subsequent review that

the event was reportable under this criterion.

Analysis. The inspectors determined that Entergys failure to submit an event

notification in accordance with 10 CFR 50.72 within the required time was a performance

deficiency that was reasonably within Entergys ability to foresee and correct, and should

have been prevented. Since the failure to submit a required event report impacts the

regulatory process, the violation was evaluated using Section 2.2.4 of the NRCs

Enforcement Policy, dated July 9, 2013, instead of the SDP. Using the example listed in

Section 6.9.d.9, A licensee fails to make a report required by 10 CFR 50.72 or 10 CFR

50.73, the issue was evaluated and determined to be a SL IV violation. The inspectors

reviewed the condition for reactor oversight process significance. Because this NRC-

identified violation involves the traditional enforcement process and does not have an

underlying technical violation that would be considered more-than-minor, inspectors did

not assign a cross-cutting aspect to this violation in accordance with IMC 0612.

Enforcement. As stated in 10 CFR 50.72(b)(3)(xiii), "Eight Hour Reports," any event that

results in a major loss of emergency assessment capability requires the licensee to

notify the NRC as soon as practical and in all cases within eight-hours of the occurrence.

Contrary to this requirement, on January 27, 2015, Entergy did not notify the NRC within

eight hours of a major loss of emergency assessment capability. Specifically, a partial

LOOP at PNPS resulted in a subsequent loss of instrument air, causing a loss of water

level indication in the Sea Water Bays. The affected instruments are used to determine

if an EAL threshold is exceeded associated with sea water level. Compliance was

restored on February 5, 2015, when Entergy reported the major loss of assessment

capability in EN 50790. Because this SL IV violation was not repetitive or willful, and

was entered into Entergys CAP under CR-PNP-2015-00949, the issue is being treated

as a SL IV NCV, consistent with Section 2.3.2.a of the NRC Enforcement Policy. (NCV 05000293/2015007-07, Failure to Report a Major Loss of Emergency Assessment

Capability)

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Enclosure

6.

Control of Switchyard Activities, Maintenance Effectiveness, and Assessment of

Operating Experience

a. Inspection Scope

The inspectors reviewed the operation and maintenance of the PNPS switchyard to

evaluate the impact of the switchyard on the event. The inspectors interviewed the

switchyard system engineer and reviewed corrective actions from the 2013 winter storm

to evaluate the adequacy of corrective actions for the switchyard. The inspectors

interviewed operators and managers to verify that Entergy was coordinating with the

transmission operator frequently during the January 27, 2015 winter storm. The

inspectors reviewed the documentation of the switchyard inspection which occurred after

the plant shutdown and prior to re-energizing the switchyard to verify that the inspection

was thorough and performed by an experienced switchyard inspector. The inspectors

also walked down the switchyard to verify that the current conditions were as

documented in the inspection results. The inspectors also performed a review of

relevant operating experience to assess Entergys effectiveness at identifying and

correcting issues.

The inspectors reviewed the design, maintenance, and testing of the diesel-driven air

compressor (K-117) to evaluate the failure of K-117 to start during the January 27, 2015

winter storm. The inspectors reviewed the design package for the initial installation of

K-117 to assess the adequacy of the design of the air compressor which was installed in

2004 to replace obsolete air compressors and to improve system reliability. The

inspectors interviewed the cognizant system engineer to evaluate the maintenance

history and historical corrective actions for K-117. The inspectors reviewed the K-117

vendor manual to verify that the air compressor is being operated and maintained in

accordance with the vendor recommendations. The inspectors interviewed the design

and system engineers about the troubleshooting and testing which occurred after the

K-117 failed to start. The inspectors reviewed the apparent cause evaluation that was

conducted for the January 27, 2015 event, as well as apparent cause evaluations for

previous events with K-117 to verify the cause of the January 27, 2015 event was not

previously identified. The inspectors walked down K-117 to evaluate the material

condition of the air compressor.

b. Findings and Observations

The inspectors noted that several procedural improvements were made which

incorporated operating experience from the 2013 winter storm including: continuous

monitoring of the switchyard during the storm, specific guidance to down power the unit

when flashovers were observed in the switchyard, powering the safety-related 4 kV

buses from the sites EDGs, placing one of the reactor protection buses on its alternate

power supply when the LOOP was anticipated, and thorough deicing of the insulators

prior to re-energizing the switchyard. Prior to the event, the switchyard was inspected by

Entergy and by the NRC resident inspectors to verify that no abnormal conditions

existed.

Following the winter storm, Entergy worked with the local grid operator, NSTAR, to

perform switchyard deicing and to perform thorough inspections of switchyard

components prior to restoring Lines 342 and 355 to service. Normal switchyard

alignment was restored on January 30 at 18:45, approximately 3 days and 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> after

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Enclosure

it was lost. Safety-related Buses A5 and A6 were restored to their normal offsite power

sources on January 31 at 01:30. Prior to the partial LOOP and until normal offsite power

was restored, the sites safety-related EDGs supplied power to Buses A5 and A6.

Based on the performance of the electrical switchyard during the winter storm on

January 27, 2015, Entergy made additional procedural changes to their operating

strategy. The inspectors reviewed Procedure No. 2.1.42, Operation during Severe

Weather, Revision 22, which incorporated the learned operating experience. Entergy

refined the existing procedural guidance to require placing the unit in Hot Shutdown 12

hours prior to the prediction of blizzard weather conditions on site. The inspectors

concluded that the guidance was an appropriate interim action until either more specific

weather conditions could be established or modifications were implemented to the

improve switchyard performance during similar weather conditions.

6.1

Diesel-Driven Air Compressor (K-117) Failure to Start

Introduction. A self-revealing Green finding was identified for Entergys failure to

adequately test the diesel-driven air compressor (K-117) prior to the January 27, 2015

winter storm. Specifically, although K-117 was tested prior to the winter storm, the test

methodology did not reveal that the capacity of the starting battery was inadequate.

Description. PNPS normally supplies instrument air from two electric motor-driven air

compressors which are supplied by non-vital power. K-117 provides a backup source of

instrument air when the motor-driven air compressors are not available, such as during a

LOOP or during maintenance. To start without AC power, K-117 is equipped with a 24

VDC battery which starts the diesel engine and powers the air compressors

programmable logic controller (PLC).

Procedure 2.1.42, Operation during Severe Weather, provides guidance for preparing

PNPS for severe weather events. Procedure 2.1.42, Section 7.2, Site Preparations

Prior to the Severe Weather, states in part, Perform or verify performed (within the past

7 days) PNPS 8.C.35, Diesel Powered Air Compressor Operability Test, for operability

and availability in case of loss of motor-driven air compressors. Procedure 2.1.42,

Section 7.7 (High Winds) and Section 7.10 (Snowstorms) have similar requirements for

verifying the availability of K-117.

The operational surveillance for K-117, Procedure 8.C.35, starts and loads the air

compressor, but it performs the start with AC power connected and without regard for

the outside temperature. K-117 is located outside and its associated 24 VDC battery is

in an unheated compartment. A batterys capacity is reduced as its temperature is

lowered. Therefore, the operational surveillance demonstrates the ability for the diesel

engine to run and the compressor to discharge high pressure air, but the test does not

demonstrate the ability for K-117 to start at low temperatures and without AC power.

On January 22, 2015, K-117 was tested in accordance with Procedure 8.C.35 as

directed by Procedure 2.1.42 and functioned normally. The inspectors noted that the

outside air temperature was approximately 32 degrees on January 22 at the time of the

test, but was approximately 29 degrees on January 27 at the time of the LOOP. When

offsite power was lost on January 27, 2015, K-117 attempted to start. Because of the

lower outside temperature and AC power being unavailable, the K-117 battery did not

have sufficient capacity to start the air compressor and provide adequate power to the

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Enclosure

PLC. As the diesel engine started, it drew current from the battery which lowered the

battery voltage below the minimum for the PLC to operate. When the PLC voltage

dropped below its minimum, it stopped sending a start signal to the diesel and generated

a fault signal which prevented further starting attempts. This resulted in a loss of

instrument air during the plant trip which complicated the event response.

Entergy entered this issue into their CAP as CR-PNP-2015-00559 and performed an

apparent cause evaluation. As part of Entergys apparent cause evaluation, the K-117

battery was replaced and the original battery was tested. The original battery was found

to be aged, as expected, but still adequate based on the vendor recommendation.

Entergy therefore determined that the design of the 24 VDC circuit was marginal to

supply both the starter and the PLC during a cold weather event. Entergy initiated

actions to supply instrument air with a temporary air compressor and planned a

modification to provide a separate power supply to the PLC.

Analysis. The failure to verify that the diesel-driven air compressor (K-117) was

available for service prior to the January 27, 2015 winter storm is a performance

deficiency that was within Entergys ability to foresee and correct. This resulted in a loss

of instrument air during the plant trip which complicated the event response. This

self-revealing issue was more than minor because it is associated with the procedure

quality and design control attributes of the Initiating Events cornerstone and adversely

impacted the cornerstone objective to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. Specifically, failure of K-117 resulted in loss of instrument air which

adversely impacted the plant response during the January 27, 2015 winter storm.

Additionally, this issue is also associated with the procedure quality and design control

attributes of the Mitigating Systems cornerstone and affected the cornerstone objective

to ensure the availability, reliability, and capability of systems that respond to initiating

event to prevent undesirable consequences.

The inspectors screened the issue under the Initiating Events cornerstone using

Attachment 4 and Exhibit 1 of Appendix A to IMC 0609, Significance Determination

Process, because that cornerstone was determined to be more impacted by the finding

than the Mitigating Systems cornerstone. The inspectors concluded that a detailed risk

evaluation would be required because the finding involved the complete loss of a

support system (instrument air) that contributes to the likelihood of an initiating event and

affects mitigation equipment. A senior reactor analyst performed a detailed risk

evaluation of this issue. The NRC model for PNPS was adjusted to account for a loss of

the instrument air compressor on a LOOP. The change in core damage frequency was

very low. A review of the dominant accident sequences indicated the contribution from a

large early release and from external risk contributors to be very small. Therefore, the

issue was determined to be of very low risk significance (Green).

The finding had a cross-cutting aspect in the area of Human Performance, Design

Margins, because Entergy failed to ensure that the K-117 battery was designed with

adequate margin. This finding is reflective of current performance because the

inadequate design margin of the battery should have been discovered through proper

testing. [H.6]

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Enclosure

Enforcement. This finding does not involve enforcement action because the

performance deficiency was associated with the non-safety-related diesel-driven air

compressor and no violation of a regulatory requirement was identified. Entergy entered

the issue into the CAP as CR-PNP-2015-00559 and initiated actions to supply

instrument air with a temporary air compressor. Entergy also revised the operability test

for K-117 air compressor to remove the AC power source prior to starting the air

compressor. Because this finding does not involve a violation and is of very low safety

significance, it is identified as a finding (FIN 05000293/2015007-08, Inadequate Testing

of the Diesel-Driven Air Compressor)

7.

Risk Significance of the Event

a. Initial Assessment

The initial risk assessment for this event is documented in the enclosed SIT charter

(Attachment 1).

Final Assessment

In accordance with the SIT charter, a Region I senior reactor analyst used the

information developed by the team and the PNPS Standardized Plant Analysis Risk

(SPAR) Model Revision 8.24, created in May 2014, to perform an event analysis. Based

on the specifics of the event, a limited test model was developed by Idaho National

Laboratory. This included 24-hour credit for recovery of EDG power given fire water

injection. Version (c) incorporates 3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> operator recovery, single high pressure

injection fault tree, containment vent in SBO-CHRIS-2 event tree logic. This event was

modeled as a switchyard-related LOOP initiating event.

Key Modeling Assumptions. The following modeling assumptions were determined to

be significant to the modeling of this event analysis:

This analysis models the January 27, 2015 reactor trip at PNPS as a switchyard-

related LOOP initiating event.

o The probability of switchyard-related LOOP (IE-LOOPSC) was set to 1.0; all

other initiating event probabilities were set to zero.

SDT Availability. The 23kV power source via the SDT was available throughout the

event. Given a postulated failure of a diesel generator, the SDT will automatically

align to power safety buses A5 and/or A6.

o To allow credit for the SDT availability, the house events HE-LOOP (House

Event - Loss of Offsite Power IE Has Occurred) and HE-LOOPSC (House Event

- Switchyard-Related Loss of Offsite Power IE Has Occurred) must be removed

from the ACP-23KV (Shutdown Transformer Offsite Power Supply) fault tree.

Offsite Power Recovery. The key offsite power recovery times for PNPS that are

modeled within the plant SPAR model are:

o 30 Minutes - LOOP and subsequent Station Blackout (SBO) combined with

failures/unavailabilities to RCIC, HPCI, and reactor depressurization.

40

Enclosure

o 1 Hour - LOOP and subsequent SBO with two or more stuck open SRVs (given

successful RCIC or HPCI operation).

o 3 Hours - LOOP and subsequent SBO with operators failing to recover offsite

power prior to the depletion of the switchyard batteries.

Offsite power was restored via Line 342 at 1635 on January 29 (approximately 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br />

after the LOOP initiated). Based on the event information (switchyard inspections and

insulator cleaning), it was determined that offsite power could not have been restored

prior to depletion of the switchyard batteries (3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />).

o Therefore, basic events OEP-XHE-XL-NR30MSC (Operators Fail to Recover

Offsite Power in 30 Minutes), OEP-XHE-XL-NR01HSC (Operators Fail to

Recover Offsite Power in 1 Hour), and OEP-XHE-XL-NR03HSC (Operators Fail

to Recover Offsite Power in 3 Hours) were set to TRUE.

Initiation of Firewater Injection. The current SPAR model has a generic screening

valve of 0.3 for the human error probability for basic event FWS-XHE-XM-ERRLT

(Operators Fail to Align Firewater Injection). As identified in the

PNPS Final Accident Sequence Precursor Analysis for Licensee Event Report 293-

13-009, the screening value was determined to be conservative; therefore, the

human failure event was reevaluated using SPAR-Hand and basic event FWS-XHE-

XM-ERRLT was set to 4E-2 from its screening value of 0.3. This was determined to

adequately represent the human error probability for this event.

Electrical Power Alignment to Buses A5 and A6. The plant had aligned the safety-

related buses, A5 and A6, to the EDGs and divorced from offsite power as part of

their storm preparations. The following modifications were made to account for this

planned configuration:

o ACP-CRB-CC-504 (4.16KV Startup Transformer Feeder Circuit BKR 152-504

Fails to Open Results in Loss of Power to Bus A5), ACP-CRB-CC-505 (4.16KV

Unit Auxiliary Transformer Feeder Circuit BKR 152-505 Fails To Open Results in

Loss of Power to Bus A5), ACP-CRB-CC-604 (4.16KV Startup Transformer

Feeder Circuit BKR 152-604 Fails to Open Results in Loss of Power to Bus A6),

and ACP-CRB-CC-605, (4.16KV Unit Auxiliary Transformer Feeder Circuit BKR

152-605 Fails to Open Results in Loss of Power to Bus A6) were set to FALSE.

o EPS-DGN-FS-DGA (EDG-A X107A Engine Fails to Start) and EPS-DGN-FS-

DGB (EDG-B X107B Engine Fails to Start) were set to FALSE.

SRV Operations. When pressure control could no longer be obtained satisfactorily

with RCIC or HPCI, SRVs were opened multiple times to control reactor pressure.

Operators attempted to open SRV C two times. During both attempts, operators did

not observe the expected reactor pressure and level response and declared the

valve inoperable. Operators continued with the depressurization cycling SRV B and

SRV D 52 and 53 times respectively. The following model modifications were made

to account for these conditions:

41

Enclosure

o ADS-SRV-CC-203-3A (SRV RV-203-3A Fail to Open) was set to TRUE

o B SRV was cycled 52 times and D SRV was cycled 53 times. To account for

the increased failure of these valves to open on demand and successfully

reclose, the failure probability was modified by the binominal expansion method

per the guidance in RASP Vol. 1, section 10.4. ADS-SRV-CC-203-3B (SRV RV-

203-3B Fails to Open) was set to 1.25E-1, ADS-SRV-CC-203-3D (SRV RV-203-

3D Fail to Open) was set to 1.27E-1, ADS-SRV-OO-203-3B (SRV RV-203-3B

Fails to Reclose) was set to 4.26E-2, ADS-SRV-OO-203-3D (SRV RV-203-3D

Fails to Reclose) was set to 4.34E-2 and PPR-SRV-OO-2VLVS (Two or More

SRVs Fail to Close) was set to 1.85E-3.

Depressurization Success Criteria. Successful depressurization usually assumes

that two of four SRVs operate successfully to ensure depressurization. The analyst

assumed that successful depressurization could be completed with a single SRV

because decay heat would be lower since the failures occur sometime after the

initiating event. As a result the following modifications were made:

o Basic Event ADS-SRV-CF-203-3ABCD (SRVs RV-203-3A, 3B, 3C & 3D Fail

from Common Cause) and depressurization logic gate DEP1 was changed from

3 of 4 to fail the function to 4 of 4 to fail the function. This translates to success

of the function with only one SRV.

Alternate High Pressure Injection. Given the lower reactor decay heat loading,

control rod drive (CRD) flow was determined to be adequate given a failure of high

pressure injection (HPCI and RCIC) and ability to depressurize to the low pressure

injection sources. The CRD fault tree was modified to show successful injection on

loss of instrument air. This was considered adequate since the CRD pumps would

deliver adequate flow when a reactor scram was inserted. The switch yard centered

LOOP event tree was modified to have this alternate injection top event after

depressurization was challenged.

No credit was assumed for successful operation of the A or C SRV on a reactor

repressurization.

Due to voiding in the CS system, Loop A, and the potential for failure due to water

hammer, LCS-MDP-FS-215A (CS Train P-215A Pump Fails to Start) was

conservatively set to TRUE. This had a minimal impact on the assessment.

Analysis Results.

The final point estimate conditional core damage probability (CCDP) for this event is

4.93x10-5. The dominant accident sequence is LOOP sequence (CCDP= 3.3x10-5)

which contributes approximately 14 percent of the total internal events CCDP. The

events logic and important component failures in LOOP sequence 14 are:

A non-recoverable switchyard-related LOOP occurs,

Reactor scram succeeds,

Emergency power succeeds,

SRVs reclose (if opened),

42

Enclosure

RCIC/HPCI initially succeed,

Suppression Pool Cooling fails,

Failure to depressurize due to the common cause failure of the SRVs,

CRD is successful,

Containment Spray fails,

Containment Venting succeeds, and

Long Term Injection fails.

8.

Exit Meetings

On March 20, 2015, the team presented their overall assessment and observations to

members of PNPS management led by Mr. John Dent, Site Vice President, and other

members of his staff. The inspectors confirmed that any proprietary information

reviewed during the inspection was returned to Entergy.

ATTACHMENT 1 - SPECIAL INSPECTION TEAM CHARTER

ATTACHMENT 2 - DETAILED SEQUENCE OF EVENTS

ATTACHMENT 3 - PILGRIM OFFSITE POWER SYSTEM

ATTACHMENT 4 - QUANTITATIVE AND QUALITATIVE EVALUATIONS

ATTACHMENT 5 - SUPPLEMENTAL INFORMATION

A1-1

Attachment 1

Special Inspection Team Charter

Pilgrim Nuclear Power Plant

Reactor Trip due to the loss of both 345kV offsite power lines

January 27, 2015

Background:

On January 27, 2015, during a winter storm, Pilgrim was reducing power from 80% due to a loss

of one 345 kilovolt (kV) offsite line. At 4:02 AM, the reactor received an automatic scram signal

from a main turbine load reject signal while at 52% power. The main turbine load reject signal

was due to the loss of the second 345kV offsite line. Both high pressure coolant injection

(HPCI) and reactor core isolation cooling pumps started as expected. The station had already

placed the safety buses on their respective emergency diesels due to the degrading switchyard

conditions so the emergency diesel generators (EDGs) were running and loaded at the time of

the automatic scram. The NRC dispatched inspectors to monitor licensee activities on-site and

in the Control Room throughout the duration of the event, and the Region I Incident Response

Center entered the monitoring mode at 12:43 PM due to multiple issues with equipment used to

bring the unit to cold shutdown and the potential for further challenges due to the ongoing winter

storm. The NRC exited the monitoring mode at 7:01 PM, because the plant had maintained

shutdown cooling for approximately two hours and was stable. The station did maintain access

to offsite power through the 23kV line. The station response was complicated by a number of

equipment issues such as:

1) Diesel-driven air compressor failed to start, resulting in a loss of station and instrument

air. Initiation of reactor coolant letdown was delayed based on the initial loss of

instrument air.

2) The A safety relief valve (SRV) had existing pilot valve leakage so plant operators did

not use it to assist in depressurization of the reactor. The C SRV was operated

manually from the Control Room and the indication showed the valve was open, but the

operators did not see the expected plant response. Plant operators reduced pressure

using the B and D SRVs.

3) HPCI became inoperable during the event after a gland seal motor thermal overload

opened. The failure caused the gland seal system to leak which caused approximately

1 of water to accumulate on the floor of the HPCI room because the sump pumps were

de- energized due to the loss of non-vital power.

4) The 23kV line remained operable and vital buses were powered by the EDGs, but there

were intermittent alarms associated with the 23kV line.

Pilgrim had a similar event during a severe winter storm in February 2013, which resulted in a

partial loss of offsite power. Therefore, this event tripped the deterministic criterion for repetitive

failures in the switchyard, which impacted safety-related systems.

Basis for the Formation of the Special Inspection Team:

The Inspection Manual Chapter (IMC) 0309 review concluded that one of the deterministic

criteria in Enclosure 1 of IMC 0309 was met due to the repetitive nature of the switchyard

failures and the multiple equipment challenges the licensee experienced. The calculated risk

was in the mid E-5 range.

A1-2

Attachment 1

To assess the risk significance of the plant transient, the Region I Senior Reactor Analyst (SRA)

used the Pilgrim standardized plant analysis risk (SPAR) model to conduct an event

assessment. Specific entries were made into the SPAR model based upon the trip with loss of

condenser heat sink, loss of the 345kV offsite power, failure of the diesel-driven air compressor,

and failure of the C SRV to open on demand.

Although HPCI was declared inoperable during the event, it was considered to be available for

injection. Additionally, at the time of failure, decay heat was sufficiently low such that control rod

drive (CRD) could provide adequate high pressure make-up. CRD is not normally credited in

the SPAR model as a high pressure injection source. Although the large early release

frequency (LERF) screening multiplier is 1.0, given the conservatism, the initial power at the

time of the event (52%), insights from State-of-the-Art Reactor Consequence Analyses and

credit for CRD, the SRA qualitatively assessed the LERF to not be greater than the Special

Inspection Team (SIT)/Augmented Inspection Team (AIT) overlap.

The resulting conditional core damage probability was 6.61E-5, which is in the AIT/SIT overlap

range.

Objectives of the Special Inspection:

The SIT will review Entergys organizational and operator response to the event, equipment and

design deficiencies, and the causes for the event and subsequent issues. The team will collect

data, as necessary, to refine the existing risk analysis. Additionally, the team leader will review

lessons learned identified during this special inspection and, if appropriate, prepare a feedback

form on recommendations for revising the Reactor Oversight Process baseline inspection

procedures.

To accomplish these objectives, the team will:

1) Develop a complete sequence of events, including follow-up actions taken by Entergy.

This review should consider any licensee-developed timelines, strip chart recordings,

computer points and trends, sequence of events printouts, or other data used by Entergy

to analyze and/or reconstruct the event.

2) Review and assess the equipment response to the event and evaluate whether it was

consistent with plant design and licensing basis. In addition, review and assess the

adequacy of associated operability assessments, technical or engineering evaluations,

corrective and preventive maintenance, and post-maintenance testing. Evaluate the

safety significance of any equipment issues identified as well as their impact on the

plants license, technical specifications, regulatory requirements, or aging management

programs.

3) Review and assess operator performance including procedures, operator narrative logs,

communications (internal and external), and appropriateness of NRC reporting during

the event. Consider use of the plant specific simulator to verify that the plant response

was consistent with the design, including any operator actions taken.

4) Review and assess the effectiveness of Entergys response to this event. This should

include internal and external communications, directions of actions from the outage

control center, and short term actions taken to address the identified equipment issues.

A1-3

Attachment 1

5) Assess Entergys implementation of their Emergency Plan and Emergency Action Level

(EAL) classifications and evaluate Entergys EAL scheme for potential generic issues.

6) Assess whether maintenance-related activities could have contributed to the event, or

impacted the response and recovery. In addition, evaluate Entergys control of

switchyard activities (including coordination with the transmission operator) that may

have affected offsite power reliability and its effect on plant safety.

7) Review relevant operating experience to assess Entergys effectiveness at identifying

and correcting any similar equipment issues.

8) Collect any data necessary to refine the existing risk analysis and document the final

independent risk analysis in the SIT report.

Guidance:

Inspection Procedure 93812, Special Inspection, provides additional guidance to be used by

the SIT. Team duties will be as described in Inspection Procedure 93812. The inspection

should emphasize fact-finding in its review of the circumstances surrounding the event. It is not

the responsibility of the team to examine the regulatory process. Safety concerns identified that

are not directly related to the event should be reported to the Region I office for appropriate

action.

The Team will conduct an entrance meeting and begin the inspection on Monday, February 2,

2015. While on site, the Team Leader will provide daily briefings to Region I management, who

will coordinate with the Office of Nuclear Reactor Regulation, to ensure that all other parties are

kept informed. A report documenting the results of the inspection will be issued within 45 days

following the final exit meeting for the inspection.

This Charter may be modified should the team develop significant new information that warrants

review.

A2-1

Attachment 2

DETAILED SEQUENCE OF EVENTS

The sequence of events was constructed by the team from review of the Control Room Narrative Log, corrective

action program condition reports, post transient review reports, process plant computer (PPC) data (alarm message

file and plant parameter graphs) and plant personnel interviews.

1/24/15 13:11

Site initiated Procedure 2.1.37, Storm Preparations.

1/27/15 01:33

(Time Approximate) Non-licensed operator observed an electrical flash over in switchyard from

the System Engineering conference room and reported it to the Control Room. Operator stated

that 3-4 flashovers were observed between 01:33 and 04:02.

1/27/15 01:33

Received numerous grid disturbance alarms. Line 355 experienced a phase A phase to ground

fault. ACB-102 and ACB-105 tripped open and ACB-102 reclosed automatically.

1/27/15 01:34

Operator lower core flow to 43 mlb/hr in accordance with Procedure 2.1.42, Operation During

Severe Weather. Reactor power lowered to 77%.

1/27/15 02:00

(Time Approximate ) ACB-105 manually reclosed (no auto closure by design).

1/27/15 02:06

(Time Approximate) Non-licensed Operator observed flash in switchyard from System

Engineering conference room and reported it to the Control Room.

1/27/15 02:06

Received numerous grid disturbance alarms including Line 342 and Line 355 undervoltage.

ACB-102 and ACB-105 tripped open. ACB-102 auto reclosed.

1/27/15 02:08

Placed Bus A6 on EDG B in accordance with Procedure 2.1.42.

1/27/15 02:12

Placed Bus A5 on EDG A in accordance with Procedure 2.1.42.

1/27/15 02:15

(Time Approximate) ACB-105 manually reclosed.

1/27/15 02:27

Placed Reactor Protection System Bus (RPS) 'A' on its backup power supply in accordance

with Procedure 2.1.42.

1/27/15 02:28

Received numerous grid disturbance alarms including Line 342 and Line 355 undervoltage.

ACB-102 and ACB-105 tripped open. ACB-102 automatically recloses.

1/27/15 02:31

(Time Approximate) ACB-105 manually reclosed.

1/27/15 02:32

Received numerous grid disturbance alarms including Line 342 and line 355 undervoltage.

ACB-102 and ACB-105 tripped open. ACB-102 automatically recloses.

1/27/15 02:35

Received numerous grid disturbance alarms including Line 342 and line 355 undervoltage.

ACB-102 tripped open (Switchyard disconnected from Line 355).

1/27/15 03:00

Wind speed approximately 54 mph (220' Tower).

1/27/15 03:24

Commenced insertion of control rods to reduce reactor power.

1/27/15 04:00

Wind Speed approximately 61 mph (220' Tower).

1/27/15 04:02

(Time Approximate) Non-licensed operator and Operations Manager observed flash in

switchyard from System Engineering conference room.

1/27/15 04:02

Line 342 faulted. Automatic reactor scram on load reject at 52% reactor thermal power.

A2-2

Attachment 2

1/27/15 04:03

Entered EOP-1, Reactor Pressure Vessel Control, for reactor vessel level < 12 inches.

Operators place the HPCI system in operation for pressure control and the RCIC system in

operation for reactor vessel level control. Main steam isolation valves are closed. Emergency

action levels were reviewed, however, no entry conditions were met.

1/27/15 04:08

All control rods verified inserted.

1/27/15 04:08 Operations entered Procedure 5.3.8, Loss of Instrument Air. Electric-driven air compressor

K-111 was out-of-service for motor replacement, electric-driven air compressor K-110 lost its

power source due to the loss the 345 kV power lines, and diesel-driven air compressor K-117

attempted to start but failed to run.

1/27/15 04:12

Operators commenced cooldown with the HPCI system for pressure control.

1/27/15 06:01

Entered EOP-3, Primary Containment Control, due to Torus Bulk temperature >80°F.

1/27/15 06:40

10 CFR50.72 non-emergency Notification was made due to actuation of the reactor protection

system (EN 50769).

1/27/15 08:30

Operator and engineering walk down of the switchyard revealed ice buildup throughout the

switchyard.

1/27/15 09:36

Operators commenced transitioning reactor water makeup for level control from the RCIC by

periodically operating CS pump 'B'. CS pump B was operated 8 times during the cooldown for

RPV level control. Several of these starts exceeded the vendor recommendations for

consecutive large motor starts. This condition was successfully evaluated (CR-PNP-2015-

00810).

1/27/15 09:48

With reactor pressure at approximately 120 psig, operators shutdown the HPCI system which

was operating in pressure control mode due a higher than desired cooldown rate and due to

approaching the HPCI system low pressure isolation setpoint for the system. Operators

commenced reactor pressure control by periodically manually opening safety/relief valves

(SRVs) from the Control Room. Operators commence operating the RCIC system in the

pressure control mode.

1/27/15 09:50

The HPCI Gland Seal Condenser Hotwell Hi Level Alarm received in the Control Room.

1/27/15 09:53

HPCI Gland Seal Condenser Blower Overload Alarm received in Control Room. This was

caused by condensate and cooling water backing up into the blower after the normal operating

flow path was secured and the normal shutdown flow path to radioactive waste through air

operated valves not opening due to the loss of instrument air. The HPCI system was declared

inoperable per procedural requirements due to the gland seal condenser being considered

inoperable. The HPCI system was still considered available if required to operate.

1/27/15 09:58

Operators commenced using SRV D for reactor pressure control. SRV D was manually

opened 53 times between 09:58 and 13:16.

1/27/15 10:15 Operators attempted to open SRV C for pressure control but plant parameters indicate that the

main valve failed to open. No reactor pressure decrease occurred.

1/27/15 10:15

Operators applied open demand to SRV C for 52 seconds. Although tailpipe temperature

increased, tailpipe acoustic response was not consistent with valve opening. No reactor

pressure decrease occurred.

A2-3

Attachment 2

1/27/15 10:16

RCIC system isolated due to reactor high level of +45" caused by level being high in the

operating band (12-45) and level swell due to opening SRV D.

1/27/15 10:16

Operators commenced using SRV B for reactor pressure control. SRV B was manually

opened 52 times between 10:16 and 13:24.

1/27/15 10:32

SRV C open demand applied for 83 seconds. Tailpipe and acoustic response responded to

the open signal, however, reactor pressure response was not consistent with the valve opening.

Reactor pressure increased from 262 psig to 266 psig. Operators declare SRV C inoperable.

1/27/15 10:56

RCIC system started in pressure control mode. Operator failed to open MO-1301-62 (cooling

water supply valve) as required by procedure.

1/27/15 12:57

RCIC Vacuum Tank High Level Alarm is received.

1/27/15 13:07

Entered EOP-4, Secondary Containment Control, due to water level in HPCI compartment

>1".

1/27/15 13:10

The Shift Manager has determined that no emergency exists as there is no active leak in the

HPCI system room. Suspect source of leakage is from reactor building sumps overflowing as

there is no power to the sump pumps and there are no active leaks.

1/27/15 13:24

EOP-4 was exited.

1/27/15 13:26

SRV-3D open demand was applied continuously until 17:04.

1/27/15 13:32

RCIC system secured. Reactor water level being maintained by periodically operating Core

Spray Pump B.

1/27/15 14:11

Reactor water cleanup letdown flow restored for RPV level control.

1/27/15 13:59

FLEX diesel air compressor installed to supply station compressed air. Instrument air pressure

increased, however, the capacity of the compressor was not sufficient to increase system

pressure to normal.

1/27/15 16:26 Shutdown cooling on RHR loop B is commenced.

1/27/15 16:56

Shift Manager completed 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> NRC Notification IAW 10CFR50.72(b)(3)(v)(D) for the HPCI

system being declared inoperable due to loss of the gland seal condenser. (EN#50771)

1/27/15 16:57

Moderator temperature < 212°F. PNPS entered Cold Shutdown.

1/27/15 19:46

EOP-1 is exited.

1/27/15 21:05 RCIC cooling water valve, MO-1301-62, found out of position. (CR-PNP-2015-570) (Note: Time

based upon condition report)

1/28/15 10:47

Temporary offsite air compressor is placed into service. Loss of Instrument Air Procedure is

exited.

1/29/15 16:07

Line 342 is energized by NSTAR.

1/29/15 16:35

Closed ACB-103 to energize SUT from Line 342 and exited LOOP condition.

1/29/15 17:05

Non-safety related 4160VAC Buses A1, A2, A3, and A4 are re-energized from the SUT.

A2-4

Attachment 2

1/29/15 19:00

Safety-related 4160VAC Bus A5 power is transferred from EDG A to the SUT.

1/29/15 19:44

EDG A is secured.

1/30/15 18:45

Line 355 is re-energized. Normal switchyard breaker alignment is established.

1/31/15 01:30

Safety-related 4160VAC Bus A6 power supply is transferred from EDG B to the SUT.

1/31/15 01:51

EDG B is secured.

A3-1

Attachment 3

A4-1

Attachment 4

QUANTITATIVE AND QUALITATIVE EVALUATIONS

The inspectors screened this issue for safety significance in accordance with Inspection Manual

Chapter (IMC) 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions. The

screening determined that a detailed risk evaluation was required because it was assumed that

for a one year period, two of the four safety relief valves (SRVs) were in a degraded state such

that they potentially would not have functioned to open at some pressure lower than rated

pressure and would not fulfill their safety function for greater than the Technical Specification

allowed outage time. Specifically, the assumptions of failures to open were based on: a failed

actual opening demand at 200 psig reactor pressure on January 27, 2015, for the C, serial

number (SN)9 SRV; examination of the valve internals at the testing vendor (National Technical

Systems (NTS)); and a previous failed actual opening demand at 114 psig reactor pressure on

February 9, 2013, for the A, SN4 SRV.

The staff determined that there isnt an existing significance determination process (SDP) risk

tool that is suitable to assess the significance of this finding with high confidence, mainly

because of the uncertainties associated with: the degradation mechanism and its rate; the

range of reactor pressure at which the degraded valves could be assumed to fully function; any

potential benefit from an SRV lifting at rated pressure, such that the degradation would be less

likely to occur and, therefore, prevent a subsequent failure at low pressure in the near-term; the

time based nature of plant transient response relative to when high pressure injection sources

fail and the associated impact of reduced decay heat on the SRV depressurization success

criteria; and the ability to credit other high pressure sources of water.

The following degraded conditions were identified with the valves and influence the assumptions

made in developing the risk assessment:

Fretting between the piston rings and the main body guide (cylinder):

This condition resulted in grooves being worn into the main body guide contributing to

binding of the main piston. Specifically, both the A (SN4) and C (SN9) SRVs exhibited

failure to open when demanded in lower pressure applications. In both cases, based on

resistance temperature detector indications, the second stage pilot opened but the main

piston failed to open. Significant internal wear on the main body guide was identified in both

valves. A (SN4) SRV was not selected to function during the winter 2015 snow event,

however based on subsequent reviews it was found not to have opened, at low reactor

pressure, when demanded on during the winter 2013 plant response.

Loose Main Piston and Retention Nut:

Loose pistons and retention nuts (hand tight), along with thread damage were observed

during the as-found inspection of the A (SN4) and C (SN9) SRVs at NTS.

New and overhauled valves, from Hope Creek and Hatch respectively, that had completed

acceptance testing were disassembled and inspected at NTS. Additionally, in February

2015, a spare, rebuilt SRV (SN6) from Pilgrim was being certification tested at NTS and

after the 6th test, the valves main stage spring-height had shortened enough to where it

could no longer re-seat the main disc. Upon disassembly, it was discovered that the main

stage stem nut had lost its thread preload (loose) and the staked portion of the lock tab

washer had partially disengaged from the piston slot. The piston had loosened on the stem.

As discussed in Information Notice 2003-01 Failure of a Boiling Water Reactor Target Rock

Main Steam Safety/Relief Valve, valves with loose pistons and piston retaining nuts have

A4-2

Attachment 4

challenged the operation of SRVs at rated pressures. With this condition, the number of

cycles and plant specific environmental condition influence the progression of the initial

degradation and, therefore, an increase in failure likelihood is expected (although it cannot

be predicted). Since multiple events can place numerous challenges on the SRVs early in

an event and at high pressure, valves with this deficiency can see higher failure to open and

failure to close rates.

Shortened/Relaxed Main Springs:

The A (SN4) and C (SN9) SRVs also exhibited shortened/relaxed main spring. GE SIL

196, Supplement 17, acknowledges that To date no SRV operational problems have been

associated with spring relaxation. However, it is hypothetically possible that spring

relaxation, if great enough, could cause the spring to fall out of position and cause

anomalous valve behavior. Other valves examined after acceptance overhaul testing also

exhibited unsatisfactory short springs.

The tables below capture a summary of history and performance of the Pilgrim SRVs:

Valves with Fretting Damage

These serial numbers were in-service during the following periods of time at the

following positions:

Serial

Number

SRV

Position

Installed

Mon/Yr

Removed

Mon/Yr

Removed

Reason for

Removal

3

RV-203-3B

05/2011

04/2013

23 months

1st Stage

Pilot Leakage

4

RV-203-3A

05/2011

02/2015

45 months

2nd Stage

Pilot Leakage

9

RV-203-3C

10/2013

02/2015

15 months

Main stage

issue

Notes: SN3, SN4, and SN9 exhibited most if not all of the following degraded

conditions: Main spring too short. Bulge in main disc/stem. Lock tab washer out of stake

recess. Piston not torqued. Stem nut not torqued. Main stem/piston stack-up dimension

out-of-spec. Guide fretting. Piston and ring fretting. Piston cocked on stem.

A4-3

Attachment 4

Valves with No Fretting Damage

Serial numbers SN2, SN5, and SN6 were unaffected by fretting from normal in-service

vibration based on disassembly and inspection of the main stage internals.

Serial

Number

SRV

Position

Installed

Mon-Yr

Removed

Mon-Yr

Length

In-Service

Reason for Removal

2

RV-203-3D

05/2011

04/2013

23 months

1st Stage Pilot Leakage

(Note 1)

5

RV-203-3C

05/2011

12/2011

7 months

2nd Stage Pilot Leakage

(Note 2)

6

RV-203-3C

12/2011

10/2013

22 months

2nd Stage Pilot Leakage

(Note 3)

1

SN2: Main spring short and replaced. Main disc/stem replaced due to bulge in

stem. Lock tab washer out of recess. Piston not torqued. Stem nut was still

torqued. Main stem/piston stack-up dimension out-of-spec. No guide fretting.

2

SN5: Main spring short and replaced. Main disc/stem bulged and tested so it

could be reused.

3

SN6: Main spring short and replaced. Piston not torqued. Stem nut not torqued.

Lock tab washer in recess. Main stem/piston stack-up dimension out-of-spec.

Main disc/stem, main piston, and guide reused.

Justification for Use of IMC 0609, Appendix M:

Based on the considerations above, the risk evaluation was performed using IMC 0609,

Appendix M, Significance Determination Process Using Qualitative Criteria, issued April 12,

2012. A planning Significance Determination Process Enforcement Review Panel (SERP) was

conducted on April 7, 2015, which concurred with using Appendix M in this case. The use of

Appendix M is appropriate because it is intended to be used when the probabilistic risk

assessment (PRA) methods and tools, including the existing SDP appendices, cannot

adequately address the findings complexity or provide a reasonable estimate of the significance

due to modeling and other uncertainties within the established SDP timeliness goal of 90 days

or less.

Detailed Risk Evaluation:

The detailed risk evaluation (DRE) was conducted by the Special Inspection Team (SIT)

inspectors and a Region I senior reactor analyst. Assistance with thermo-hydraulic analysis

reviews was provided by the Office of Nuclear Regulatory Research (RES). Information used in

this DRE included detailed observation and inspection of the SRVs at NTS Huntsville, Alabama,

review of design basis information, operating and emergency procedures, and additional

analysis conducted by Entergy.

The worst case bounding analysis would include the failure of the A and C SRV to open for all

events over a one year exposure period. The resulting increase in core damage frequency

(CDF) is heavily driven by the increase in the common cause failure (CCF) probability from its

baseline of 7E-5 to approximately 0.3. This resulted in an increase in CDF of mid E-4. This

appears to be overly conservative since both the A and C SRV passed as-found high

pressure American Society of Mechanical Engineers code required testing and a subsequent

A4-4

Attachment 4

lower pressure special test at 100 psig at NTS. This, and the fact that the A SRV successfully

functioned at high pressure in the plant after the failed low pressure attempt, partially supports

the theory that the valves would function at high pressure and subsequently operate again at

low pressure. However, it cannot be ruled out that other testing factors, such as the testing gag

which imparts a higher opening force, or the cooldown, shipment, and reheating of the valve,

may have resulted in a preconditioning of the valve influencing their success.

The range of degradation impacts the accident sequences and success criteria. Absent other

failure contributors, initial SRV success at high pressure or repressurization during the event

might aid in overcoming this condition. Since the Standardized Plant Analysis Risk (SPAR)

models are relatively static they cannot readily accommodate these time/scenario dependent

variations.

Based on the available information, evaluation tools, and judgment, the condition was bounded

by considering the failure of the A and C SRV for medium loss of coolant accident (MLOCA)

events and by increasing the SRV fail to open (FTO) and fail to close (FTC) by a factor of 10 to

account for the degradation of the valves in non MLOCA cases.

Due to the high number of identified loose pistons and nuts and spring shortening identified at

Pilgrim and through other facilities it was assumed for modeling all events, other than MLOCA,

that the SRV FTO and FTC was 10x higher.

MLOCA

The MLOCA event can be most closely modeled since modeling does not assume SRVs are

challenged at high pressure early in the event and the event is usually mitigated in a mid-

pressure range.

The following assumptions and changes were made to the model:

The CCF alpha factors were updated based on inputs from Idaho National

Laboratory. Basic events ZA-ADS-SRV-CC-04A01 - ZA-ADS-SRV-CC-04A04 were

modified as follows:

o 1=9.46

a=63.8

b=3.64

o 2=3.89E-2

a=2.62

b=64.8

o 3=1.09E-2

a=73.3

b=66.7

o 4=4.26E-3

a=28.7

b=67.1

The probability of failure of the A and C SRV to open was set to TRUE.

Given that the break size would provide for some degree of depressurization, a

success criterion of 1 of 4 SRVs was assumed. The application of 1/4 SRV criterion

is to all MLOCA sequences, meaning that it is being applied to high pressure coolant

injection (HPCI) fail to start situations for which the licensee Modular Accident

Analysis Program (MAAP) calculations did not provide a basis. For this case this

could be non-conservative.

No recovery credit was assigned.

No credit was assigned for successful operation of the valves if the plant

repressurized. The operators would have had no knowledge of this as a possible

remedy to free a stuck valve. Given that the emergency operating procedures

(EOPs) direct the operators to stabilize and reduce pressure, actions by the operator

could place the plant in an intermediate pressure below any assumed pressure

success point.

SRV lifts that occur at full pressure, as a means of conditioning the valve for later

successful operation at intermediate pressure (and what break size would be a

A4-5

Attachment 4

transition point where no such early lift would take place) was not considered. The

SPAR model does not assume a high pressure SRV challenge for MLOCA. It should

be noted that MAAP developers do not recommend using quantitative results during

the first 3 minutes of a transient because of limitations in the code models [EPRI TR-

1020236, pg. 8-2]. The MAAP results should be viewed qualitatively in this regard,

and corroborated by other sources (e.g., operating experience, simulator,

knowledge).

Results:

Base Case CDF = 1.19E-7

Conditional Case = 1.46E-6

CDF = 1.34E-6

The dominant sequence is a MLOCA with a CCF of the SRV and the failure of HPCI to run

given that it started.

Non-MLOCA:

The following assumptions and changes were made to the model:

The CCF alpha factors were updated based on inputs from Idaho National

Laboratory. Basic events ZA-ADS-SRV-CC-04A01 - ZA-ADS-SRV-CC-04A04 were

modified as follows:

o 1=9.46

a=6.38E1

b=3.64

o 2=3.89E-2

a=2.62

b=6.48E1

o 3=1.09E-2

a=7.33E-1

6.67E1

o 4=4.26E-3

a=2.87E-1

6.71E1

ADS-SRV-CC-203-3A through ADS-SRV-CC-203-3D was increased from 2.77E-3 to

2.77E-2, to account for the potential increase in FTO probabilities.

ADS-SRV-OO-203-3A through ADS-SRV-OO-203-3D was increased from 8.55E-4 to

8.55E-3 to account for the potential increase in FTC probabilities.

The base case SRV success criteria of 2 of 4 SRVs was not modified.

No recovery credit was assigned.

No credit was assigned for successful operation of the valves if the plant

repressurized. The operators would have had no knowledge of this as a possible

remedy to free a stuck valve. Given that the EOPs direct the operators to stabilize

and reduce pressure, actions by the operator could place the plant in an intermediate

pressure below any assumed pressure success point.

SRV lift that occur at full pressure, as a means of conditioning the valve for later

successful operation at intermediate pressure (and what break size would be a

transition point where no such early lift would take place) was not considered.

Results:

Base Case CDF = 2.08E-5

Conditional Case = 2.30E-5

CDF = 2.2E-6

The dominant sequence impacted by this change is a loss of salt service water, resulting in

a loss of suppression pool cooling, with a failure of late injection due to the failure of SRVs

to allow depressurization. All of the dominant sequences (LOSSW, LOCHS LOMFW,

TRANS, and LOSGV) have the potential to lift SRVs at the onset of the event. In these

A4-6

Attachment 4

events multiple lifts are expected to occur therefore with the observed degradations it is

appropriate to assume an increased failure probability.

External Events

The performance deficiency also would have implications for external events risk. Given the

nature of the condition, a detailed evaluation is not practical. SRVs are front line systems

credited in many external event scenarios. Therefore it would be reasonable to assume that

the contribution from external events would be equal to those from internal events.

Large Early Release Frequency

The large early release frequency (LERF) assessment was informed by NUREG-1675,

Basis Document for Large Early Release Frequency (LERF) SDP. The failure of the SRVs

would be considered a Type A finding. Most of the dominant sequences involve a failure of

high pressure injection and a failure to depressurize. NUREG-1765, Table 2, assumes 1.0

for high-pressure sequences with a dry drywell, and 0.6 for high-pressure sequences with a

flooded drywell. The former value is bounding, but not necessarily conservative, in that liner

melt-through is expected to occur shortly after vessel failure if the drywell is dry. The latter

value is affected by the mode of reactor coolant system rupture, operator actions following

the onset of core damage, and phenomenological issues related to direct containment

heating and fuel-coolant interactions.

Recent evaluations (e.g., SOARCA Peach Bottom) have indicated that the likelihood of

severe accident-induced main steam line creep rupture or a stuck-open relief valve prior to

vessel breach is potentially higher than typically estimated in PRAs. This same case was

made in a 2003 report prepared for NRC/RES by Energy Research, Inc.1 These failure

modes would lead to a more benign containment response at the time of vessel breach, in

terms of direct containment heating and fuel-coolant interaction-induced containment failure.

Therefore, some credit below a LERF multiplier of 1.0 should be assigned.

Total Estimated Change in CDF

Given the above assumptions it is likely that the combined CDF could be in the mid E-6 range.

Licensees Risk Evaluation:

The licensees assessment was influenced by the following assumptions:

1. Pilgrims SRVs have consistently opened at high reactor pressure vessel (RPV) pressure.

2. Once an SRV cycles at high RPV pressure, it is conditioned to open at low RPV pressure.

3. There have been no FTCs to date for Pilgrims model of SRVs.

4. SRVs 3B and 3D exhibited full functionality as compared with SRVs 3A and 3C therefore,

they should not be considered as candidates for common cause failure.

Entergy staff conducted numerous MAAP thermo-hydraulic runs in an attempt to model the

condition. Their analysis focused mainly on the MLOCA. Their PRA analysis calculated a CDF

of low E-8 for the MLOCA case. The large difference between their results and the SPAR was

1 Esmaili et al., The Probability of High-Pressure Melt Ejection-Induced Direct Containment Heating

Failure in Boiling Water Reactors with Mark I Design, ERI/NRC-03-204, November 2003.

A4-7

Attachment 4

their application of CCF which was two orders of magnitude less. Requests were made for

comparison of the increased SRV FTO and FTC frequencies.

Although some insights were gained from the modeling, the outcomes are largely influenced by

the assumptions. Specifically, 500 psig was assumed to be the pressure above which the force

would be sufficient to open a stuck shut SRV. No consideration was given for the operator

response to stabilize and reduce pressure in accordance with the EOPs. Additionally, Entergys

MAAP run executed emergency depressurization at -125 inches, which represents the top of

active fuel (TAF); however, Entergys EOPs allow for this down to -150 inches, which is the

minimum for steam cooling. Although depressurization could occur higher, the failure to

evaluate at the lower level was non-conservative. Finally, failures of the valves due to the

performance deficiency did not consider the increased failure potentials at high pressure.

Given the above, concerns for cases other than MLOCA, the licensee considered the

following:

1. To account for the degraded opening characteristics observed at low pressure in SRV 3A

and 3C, the FTO frequency was increased by 10X to account for uncertainties with these

two valves.

2. Fault exposure was 1 year.

3. Assuming the above the CDF for internal events was 1.0E-7.

Most of the observed high pressure successes of the SRVs has been on the test stand. As

stated in the May 1, 2015 Curtis-Wright Interim 10 CFR Part 21 Report, Event Notification 50900, the test rig is believed to impart excessive impact loads which are much greater than

those under normal in-plant full flow conditions. This may not adequately model in plant

response.

Entergy is also crediting high pressure lifts to condition the valves at low pressure. As stated

above, much of the evidence to support this is obtained from test stand observations, in which

excessive impact loads are applied. This may not adequately model in plant response.

Entergys application of CCF is inconsistent with the RASP guidance. The valves should be

treated as a single CCF grouping since it has not been shown that they should be uncoupled. It

is important to note that the increased failure probability was only applied to the 3A and 3C SRV

although the performance history of these valves indicate that it is probable that they will exhibit

most if not all of the following:

Main spring too short

Bulge in main disc/stem

Lock tab washer out of stake recess

Piston not torqued

Hex jam nut not torqued

Main stem/piston stack-up dimension out-of-spec

Guide fretting

Piston and ring fretting

Piston cocked on stem

As stated above, Entergy does not believe that there is any impact on the valves ability to

reclose. This is not supported by the May 1, 2015 Curtis-Wright Interim 10 CFR Part 21 Report,

EN 50900. Specifically, Target Rock believes the most likely root cause is excessive impact

A4-8

Attachment 4

loads during limited flow testing that relieves the torque applied to the piston/stem interface (de-

torqueing) that may subsequently lead to creation of a significant clearance between the piston

and the main disc (de-shouldering). If the excessive impact load also damages the locking tab,

plant vibratory loads can allow the piston to rotate creating/increasing the clearance between it

and the stem. If the clearance becomes significant, the piston tilts in its guide bore which can

inhibit valve reclosing under certain conditions.

IMC 0609 APPENDIX M, TABLE 4.1

Qualitative Decision-Making Attributes for NRC Management Review

The NRC made a preliminary determination that the finding was of low to moderate safety

significance (White) based on the quantitative and qualitative evaluations. Additional

considerations are listed below:

Decision

Attribute

Applicable

to Decision?

Basis for Input to Decision - Provide qualitative and/or

quantitative information for management review and decision

making.

1. Finding can

be bounded

using qualitative

and/or

quantitative

information?

Yes

The SRAs performed a bounding quantitative assessment

using Pilgrim SPAR Model. The bounding risk, assuming

failure of the A and C SRVs to open for all events; is mid

E-4. Details are discussed in Section 2. Based on

uncertainty associated with the SRV performance, this

bounding risk was considered to be conservative. This

uncertainty can strongly influence the specific initiating

events, success criteria and CCF. Factors contributing to the

NRCs preliminary White finding are further described below

and in this Attachment.

2. Defense-in-

Depth affected?

Yes

SRVs and low pressure injection provide redundancy and

backup to the high pressure injection sources. They are

required to perform both an over-pressure protection function

and means to rapidly reduce pressure to allow for low

pressure sources to inject into the reactor vessel. Emergency

depressurizations are directed in the EOPs when the

suppression pool reaches its heat capacity limit, when there is

a reactor coolant leak into secondary containment, and when

level reaches the minimum steam cooling water level. The

as-found condition of the A and C SRV impacts these

functions.

3. Performance

Deficiency effect

on the Safety

Margin

maintained?

Yes

Reduced depressurization reliability increases the likelihood

that peak cladding temperature limits and core damage can

occur.

A4-9

Attachment 4

4. The extent

the performance

deficiency

affects other

equipment.

Yes

The failure of the licensee to identify and correct the condition

of the A SRV following the 2013 winter storm event resulted

in the failure to identify a likely common cause failure

mechanism prior to the demand failure of the C SRV during

the January 2015 plant transient.

5. Degree of

degradation of

failed or

unavailable

component(s)

Yes

Two valves are known to fail on demand at low pressure. In

addition, the loose piston and nut and relaxed spring have the

potential to impact valve operation over the entire range. This

could result in valves failing to open, close or stick in an

intermediate condition. Due to preliminary Part 21 reports, it

is likely that all four SRVs will exhibit loose piston and nut as a

result of the post maintenance testing at NTS. The degree of

further degradation due to plant specific conditions cannot be

determined.

6. Period of

time effect on

the performance

deficiency.

Yes

Greater than 1 year. Due to preliminary Part 21 reports, it is

likely that all four SRVs will exhibit loose piston and nut as a

result of the post maintenance testing. Therefore it is likely

that the valves were nonconforming with respect to piston and

nut torque upon installation. The fretting that was determined

to cause binding at low pressure is time dependent based on

the looseness of the piston and plant vibrations.

7. The

likelihood that

the licensees

recovery actions

would

successfully

mitigate the

performance

deficiency.

Yes

There are no recovery actions identified. No credit was

assigned for successful operation of the valves if the plant

repressurized. The operators would have had no knowledge

of this as a possible remedy to free a stuck valve. Given that

the EOPs direct the operators to stabilize and reduce

pressure, actions by the operator could place the plant in an

intermediate pressure below any assumed pressure success

point. Additionally, if the valve sticks due piston misalignment

there is no recovery.

8. Additional

qualitative

circumstances

associated with

the finding that

regional

management

should consider

in the evaluation

process

Yes

Entergy had the ability to readily identify the failure of the A

SRV. Additionally, Entergy was slow to identify that the C

SRV was inoperable when failing to open on demand in its

required band, doing so only after NRC identification.

Entergys claim that the C SRV was slow to open, or that it

partially opened was not consistent with the plant response

which clearly showed that the expected level and pressure

response was not obtained.

A5-1

Attachment 5

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel Contacted

J. Dent, Site Vice President

S. Verrochi, General Manager Plant Operations

D. Berkland, Senior Lead Engineer

R. Byrne, Licensing

D. Calabrese, Manager, Emergency Preparedness

W. Carroll, Senior Project Engineer

F. Clifford, Assistant Operations Manager, Support

J. Cotter, Superintendent, Operations Training

P. Doody, Senior Lead Engineer

P. Harizi, Design Engineer

S. Hudson, Senior Lead Engineer

J. Macdonald, Senior Manager, Operations

P. Miner, LicensingD. Noyes, Director, Regulatory & Performance Improvement

J. ODonnell, RCIC and HPCI System Engineer

J. Parmenter, Emergency Preparedness Analyst

C. Perkins, Manager, Regulatory Affairs

B. Rancourt, Senior Lead Engineer

M. Williams, Root Cause Evaluator

\\

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened 05000352/2015007-02

AV

Failure to Identify, Evaluate, and Correct A SRV

Failure to Open Upon Manual Actuation (Section

2.5)

Opened/Closed 05000293/2015007-01

NCV

Inadequate Past Operability Assessment of C

Safety Relief Valve (Section 2.4)05000293/2015007-03

NCV

Inadequate Loss of Instrument Air Abnormal

Operating Procedure (Section 3.2)05000293/2015007-04

NCV

Failure to Follow RCIC System Manual Restart

Procedure (Section 3.3)05000293/2015007-05

NCV

Failure to Identify Condition Adverse to Quality

Associated with CS Discharge Header Voiding

(Section 4.2)

A5-2

Attachment 5 05000293/2015007-06

NCV

Failure to Implement Compensatory Measures for

Out-of-Service EAL Instrumentation (Section 5.1)05000293/2015007-07

NCV (SL-IV) Failure to Report a Major Loss of Emergency

Assessment Capability (Section 5.2)05000293/2015007-08

FIN

Inadequate Testing of the Diesel-Driven Air

Compressor (Section 6.1)

LIST OF DOCUMENTS REVIEWED

In addition to the documents identified in the body of this report, the inspectors reviewed the

following documents and records.

Procedures

2.1.42, Operation during Severe Weather, Revision 21 and Revision 22

2.2.21.5, HPCI Injection and Pressure Control, Revision 17

2.2.23, Automatic Depressurization System, Revision 36

3.M.4-17.4, Lubrication Sampling and Change Procedure, Revision 43

ARP-C903C, Alarm Response Procedure, Revision 17

ARP-C904L, Alarm Response Procedure, Revision 18

EN-LI-102, Corrective Action Program, Revision 24

EN-OP-104, Operability Determination Process, Revision 7

Master/LCC Procedure No. 2, Abnormal Conditions Alert, Revision 17.1

2.2.21, High Pressure Coolant Injection System, Revision 84

8.M.1-20, High Water Level Scram Discharge Tank Instrumentation Calibration/Functional Test

without Half-Scrams - Critical Maintenance, Revision 72

EN-FAP-EP-010, Severe Weather Response, Revision 1

5.3.8, Loss of Instrument Air, Revision 39

EP-AD-601, Emergency Action Level Technical Design Bases Document, Revision 4

0-RQ-06-02-06(07), Hurricane with Intake Structure Fouling, Revision 1

0-0-RQ-04-04-87, Coastal Storm JITT - Table Top, Revision 0

0-0-RQ-04-04-87, Coastal Storm JITT - Table Top, Revision 1

5.3.37 Loss of Spent Fuel Pool Cooling Event, Revision 2

0-RQ-06-02-134, Hurricane with Loss of Instrument Air System, Revision 0

0-RQ-06-02-122, Seismic Event- Loss of Instrument Air-LOCA, Revision 0

SDBD-23, High Pressure Coolant Injection (HPCI) System, Revision 1

EP-IP-100.1, Emergency Action Levels (EALs), Revision 10

EP-AD-601, Emergency Action Level Technical Bases Document, Revision 4

3.M.4-17.4, Lubricating, Sampling and Change Procedure, Revision 43

8.C.35, Diesel Powered Air Compressor Operability Test, Revision 29

A5-3

Attachment 5

2.4.16, Distribution Alignment Electrical System Malfunctions, Revision 43

2.4.A.23, Loss/Degradation of 23kV Line, Revision 22

2.2.36, Instrument Air Systems, Revision 79

Condition Reports

CR-PNP-2015-00888

CR-PNP-2015-00626

CR-PNP-2015-00730

CR-PNP-2015-00720

CR-PNP-2015-00715

CR-PNP-2015-00697

CR-PNP-2015-00693

CR-PNP-2015-00563

CR-PNP-2015-00770

CR-PNP-2015-00949*

CR-PNP-2015-00948*

CR-PNP-2015-00730

CR-PNP-2015-00561

CR-PNP-2015-00563

CR-PNP-2015-00906*

CR-PNP-2015-00870*

CR-PNP-2013-05651

CR-PNP-2015-00720

CR-PNP-2013-00011

CR-PNP-2015-00908

CR-PNP-2013-00798

CR-PNP-2013-00856

CR-PNP-2013-00863

CR-PNP-2013-00863

CR-PNP-2013-03727

CR-PNP-2013-07652

CR-PNP-2015-00559

CR-PNP-2015-00715

CR-PNP-2015-00886

CR-PNP-2015-00892*

  • designates CRs generated based on NRC identified issues

Work Orders

00403652-01

00403652-02

00403895-01

00403895-02

00350555-01

52372898-07

52372899-07

52368095-01

52370370-01

403590-11

Completed Tests

3.M.4-6, Removal, Installation, Test, Disassembly, Inspection, and Reassembly of Main Steam

Safety/Relief Valves - Critical Maintenance, performed 5/23/13

8.5.6.4, ADS Operability for Alternate Shutdown Panel, performed 5/11/13

8.5.6.2, Special Test for ADS System, Manual Opening of Relief Valves, performed 5/29/13

Data/Parameter Graph for Installed SRV Test (SRV 3B), performed 5/29/13

Data/Parameter Graph for Installed SRV Test (SRV 3D), performed 5/29/13

Data/Parameter Graph for Installed SRV Test (SRV 3C), performed 10/21/13

Miscellaneous

Pilgrim Station Scram Report Number 15-01 for reactor scram occurring on January 27, 2015

Pilgrim Nuclear Power Station Probabilistic Safety Assessment System Notebook, High

Pressure Coolant Injection, Appendix E16, PNPS-NE-07-006, Revision 1

Pilgrim Nuclear Power Station Emergency Plan, Revision 44

Event Notification 50790, Loss of Sea Water Intake Bay Level

Instrumentation Due to Loss of Instrument Air, dated 2/5/2015

High Pressure Coolant Injection System, Reference Text, Revision 15

Automatic Depressurization System, Reference Text, Revision 6

O-RO-03-04-06, EOP-04 Secondary Containment Control, Revision 9

O-RO-03-04-09, EOP-17/27, Emergency RPV Depressurization, Revision 8

Operability Evaluation for CR-PNP-2015-00908 (SRVs), 2/5/15

Past Operability Evaluation for CR-PNP-2015-00561 (SRV C), 2/5/15

V-2072, Vendor Manual for K-117 Backup Diesel Air Compressor, Revision 0

PDC 02-05, Replacement of Diesel-Driven Backup Air Compressor, Revision 0

A5-4

Attachment 5

Design Basis Documents

SDBD-01, Automatic Depressurization System/Main Steam System, Revision E1

SDBD-23, High Pressure Coolant Injection System, Revision 1

Drawings

M244, Sh. 1, HPCI System, Revision 31

M15, Equipment Location, Reactor Building Plan Basement, Revision E22

M252, Sh. 1, Nuclear Boiler, Revision 69

M18C-13, Air Compressor Control Power Electrical Wiring Diagram, Revision 0

A5-5

Attachment 5

LIST OF ACRONYMS

10 CFR

Title 10 of the Code of Federal Regulations

AC

Alternating Current

ADS

Automatic Depressurization System

AV

Apparent Violation

CAP

Corrective Action Program

CCDP

Conditional Core Damage Probability

CCF

Common Cause Failure

CR

Condition Report

CS

Core Spray

CST

Condensate Storage Tank

DRS

Division of Reactor Safety

EAL

Emergency Action Level

ECCS

Emergency Core Cooling System

EDG

Emergency Diesel Generator

EN

Event Notification

Entergy

Entergy Nuclear Operations, Inc.

EOP

Emergency Operating Procedure

HPCI

High Pressure Coolant Injection

IC

Initiating Condition

kV

Kilovolt

LCO

Limiting Condition for Operation

LOOP

Loss of Offsite Power

MSL

Mean Sea Level

NCV

Non-cited Violation

NEI

Nuclear Energy Institute

NRC

Nuclear Regulatory Commission

NTS

National Technical Systems

PNPS

Pilgrim Nuclear Power Station

PLC

Programmable Logic Controller

RCIC

Reactor Core Isolation Cooling

RG

Regulatory Guide

RHR

Residual Heat Removal

RPV

Reactor Pressure Vessel

RWCU

Reactor Water Cleanup

SBO

Station Blackout

SERP

Significance Determination Process Enforcement Review Panel

SDP

Significance Determination Process

SDT

Shutdown Transformer

SIT

Special Inspection Team

SL

Severity Level

SPAR

Standardized Plant Analysis Risk

SRV

Safety/Relief Valve

SSC

Structure, System, and Component

TS

Technical Specification

VDC

Volts Direct Current