ML13042A373

From kanterella
Jump to navigation Jump to search
IR 05000416-12-005; 09/22/2012 - 12/31/2012; Grand Gulf Nuclear Station, Unit 1, Integrated Resident and Regional Report; Maintenance Effectiveness, Refueling & Other Outage Activities, Occupational ALARA Planning and Controls, and Followup
ML13042A373
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 02/11/2013
From: David Proulx
NRC/RGN-IV/DRP/RPB-C
To: Kevin Mulligan
Entergy Operations
Proulx D
References
Download: ML13042A373 (97)


See also: IR 05000416/2012005

Text

U N IT E D S TA TE S

N U C LE AR R E GU LA TOR Y C OM MI S S I ON

R E G IO N I V

1600 EAST LAMAR BLVD

AR L I NG TO N , TE X AS 7 60 1 1 - 4511

February 11, 2013

Kevin Mulligan

Vice President Operations

Entergy Operations, Inc.

Grand Gulf Nuclear Station

P.O. Box 756

Port Gibson, MS 39150

SUBJECT: GRAND GULF NUCLEAR STATION - NRC INTEGRATED INSPECTION

REPORT NUMBER 05000416/2012005

Dear Mr. Mulligan:

On December 31, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Grand Gulf Nuclear Station, Unit 1. The enclosed inspection report

documents the inspection results which were discussed on January 17, 2013, with you and

other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Four NRC identified and three self-revealing findings of very low safety significance (Green)

were identified during this inspection. Six of these findings were determined to involve

violations of NRC requirements. Further, a licensee-identified violation, which was determined

to be of very low safety significance is listed in this report. The NRC is treating these violations

as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest these non-cited violations, you should provide a response within 30 days of the

date of this inspection report, with the basis for your denial, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the

Regional Administrator, Region IV; the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at

Grand Gulf Nuclear Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV; and the NRC Resident Inspector at

Grand Gulf Nuclear Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

K. Mulligan -2-

NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

David Proulx, Acting Branch Chief

Project Branch C

Division of Reactor Projects

Docket No.: 50-416

License No: NPF-29

Enclosure: Inspection Report 05000416/2012005

w/ Attachments 1: Supplemental Information

2: Request for Information for ALARA Planning & Controls Inspection

cc w/ encl: Electronic Distribution for Grand Gulf Nuclear Station

K. Mulligan -3-

DISTRIBUTION:

Regional Administrator (Elmo.Collins@nrc.gov)

Acting Deputy Regional Administrator (Steven.Reynolds@nrc.gov)

DRP Director (Kriss.Kennedy@nrc.gov)

Acting DRP Deputy Director (Michael.Scott@nrc.gov)

Acting DRS Director (Tom.Blount@nrc.gov)

Acting DRS Deputy Director (Jeff.Clark@nrc.gov)

Senior Resident Inspector (Rich.Smith@nrc.gov)

Resident Inspector (Blake.Rice@nrc.gov)

Acting Branch Chief, DRP/C (David.Proulx@nrc.gov

Senior Project Engineer, DRP/C (Bob.Hagar@nrc.gov)

Project Engineer, DRP/C (Rayomand.Kumana@nrc.gov)

GG Administrative Assistant (Alley.Farrell@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Project Manager (Alan.Wang@nrc.gov)

Branch Chief, DRS/TSB (Ray.Kellar@nrc.gov)

TSB Assistant (Loretta.Williams@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

RIV/ETA: OEDO (John.Cassidy@nrc.gov)

Regional State Liaison Officer (Bill.Maier@nrc.gov)

NSIR/DPR/EP (Eric.Schrader@nrc.gov)

DOCUMENT NAME: R:\_REACTORS\_GG\2012\GG 2012005- RP-RLS 130205.docx

SUNSI Rev Compl. Yes No ADAMS Yes No Reviewer Initials DP

Publicly Avail. Yes No Sensitive Yes No Sens. Type Initials DP

SRI:DRP/C RI:DRP/C SPE:DRP/C C:DRS/EB1 C:DRS/EB2 C:DRS/OB

RLSmith BBRice BHagar TRFarnholtz GMiller VGaddy

/E-Proulx/ E-Proulx/ /RA/ /RA/ /RA/ /RA/

2/11/13 2/11/13 2/6/13 1/31/13 2/4/13 2/4/13

C:DRS/PSB1 C:DRS/PSB2 C:DRS/TSB BC:DRP/C

MHaire GEWerner RKellar DProulx

/RA/ /RA/ /RA/ /RA/

2/4/13 1/31/13 2/5/13 2/11/13

OFFICIAL RECORD COPY

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000416

License: NPF-29

Report: 05000416/2012005

Licensee: Entergy Operations, Inc.

Facility: Grand Gulf Nuclear Station, Unit 1

Location: 7003 Baldhill Road

Port Gibson, MS 39150

Dates: September 22 through December 31, 2012

Inspectors: R. Smith, Senior Resident Inspector

B. Rice, Resident Inspector

S. Achen, Reactor Inspector NSPDP

L. Carson II, Senior Health Physicist

G. George, Senior Reactor Inspector

R. Kumana, Project Engineer

S. Makor, Reactor Inspector

J. Laughlin, Emergency Preparedness Inspector, NSIR

N. Okonkwo, Reactor Inspector

Approved David Proulx, Acting Chief

By: Reactor Projects Branch C

Division of Reactor Projects

-1- Enclosure

SUMMARY OF FINDINGS

IR 05000416/2012005; 09/22/2012 - 12/31/2012; GRAND GULF NUCLEAR STATION, UNIT 1,

Integrated Resident and Regional Report; Maintenance Effectiveness, Refueling and Other

Outage Activities, Occupational ALARA Planning and Controls, and Followup of Events and

Notices of Enforcement Discretion.

The report covered a 3-month period of inspection by resident inspectors and an announced

baseline inspections by region-based inspectors. Six Green non-cited violations and one Green

finding of significance were identified. The significance of most findings is indicated by their

color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance

Determination Process. The cross-cutting aspect is determined using Inspection Manual

Chapter 0310, Components Within the Cross-Cutting Areas. Findings for which the

significance determination process does not apply may be Green or be assigned a severity level

after NRC management review. The NRC's program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4, dated December 2006.

A. NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

Green. The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, involving the licensees

failure to follow procedure EN-LI-118, Root Cause Evaluation Process,

Revision 18, in that they failed to evaluate the risk significances and develop

action plans to address equipment identified during their extent-of-condition

review for a post-scram root cause analysis. The licensee entered this issue into

their corrective action program as Condition Report CR-GGN-2012-11950. The

immediate corrective actions included assigning corrective actions for operations

personnel to properly evaluate the risk significance of the identified components

and perform appropriate corrective actions to correct the degraded conditions.

The licensees failure to properly determine risk significance and associated

action plans to correct degraded equipment that could challenge safe plant

operation is a performance deficiency. The performance deficiency is more than

minor and is therefore a finding because if left uncorrected, it would have the

potential to lead to a more significant safety concern. Specifically, the failure to

take corrective actions to correct degraded equipment has the potential to lead to

initiating events resulting in plant transients. Using NRC Inspection Manual

Chapter 0609, Attachment 4, "Initial Characterization of Findings," the inspectors

determined that the issue affected the Initiating Events Cornerstone. In

accordance with NRC Inspection Manual Chapter 0609, Appendix A, The

Significance Determination Process (SDP) for Findings at Power, the inspectors

determined that the issue has very low safety significance (Green) because the

finding did not cause a reactor trip or the loss of mitigation equipment relied upon

to transition the plant from the onset of the trip to a stable shutdown condition.

-2-

The inspectors determined that the apparent cause of this finding was that when

operations management directed operators to identify the degraded equipment,

they did not encourage those operators to comply with Procedure EN-LI-118.

Therefore, the finding has a cross-cutting aspect in the human performance area,

work practices component because the licensee did not define and effectively

communicate expectations regarding procedural compliance. H.4(b) (Section

4OA3).

Cornerstone: Mitigating Systems

Green. The inspectors reviewed a self-revealing non-cited violation of 10 CFR

50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the

licensees failure to complete preventive maintenance tasks on the high pressure

core spray division III diesel generator output breaker in accordance with the

corresponding preventive maintenance task template. The licensee entered this

issue in their corrective action program as Condition Report CR-GGN-2012-

07992. The immediate corrective actions included replacing the failed control

relay and restoring operability to the division III diesel generator. The long term

corrective actions included revising breaker refurbishment/replacement

procedure with directions to replace the control relay and change the procedure

frequency to every 10 years versus every 12 years.

The inspectors determined that this performance deficiency was more than minor

and is therefore a finding because it is associated with the equipment

performance attribute of the Mitigating Systems Cornerstone and adversely

affected the cornerstone objective of ensuring the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, this failed control relay caused the subject breaker

to fail to close during the division III diesel generator monthly surveillance on

June 5, 2012. The inspectors used NRC Inspection Manual Chapter 0609,

Attachment 4, "Initial Characterization of Findings," to determine that the issue

affected the Mitigating System Cornerstone. Because the finding pertained only

to a degraded condition while the plant was shutdown, the inspectors used

Manual Chapter 0609, Appendix G, Shutdown Operations Significance

Determination Process, Checklist 8, Cold Shutdown or Refueling Operation -

Time to Boil > 2 Hours: RCS Level < 23 Above Top of Flange, to determine that

the finding was of very low safety significance because it did not increase the

likelihood of a loss of reactor coolant system inventory; did not degrade the

licensees ability to terminate a leak path or add RCS inventory when needed; did

not significantly degrade the licensees ability to recover decay heat removal if

lost; and did not affect the safety/relief valves (Green). The inspectors

determined that the cause of this finding was a latent issue that is not reflective

of current performance, therefore no cross-cutting aspect was identified. (Section

1R20.b).

Green. The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,

Criterion III, Design Control, for the licensees failure to establish the gain

-3-

settings used on the power range neutron monitoring system in accordance with

design requirements. The licensee entered this issue into their corrective action

program as Condition Report CR-GGN-2013-00177. The immediate corrective

actions included adjusting gain settings for their average power range monitor

(APRM) instruments to indicate actual core thermal power as determined by the

heat balance. In additioin, the licensee revised their neutron monitoring

procedure to set the initial gains for the average power range monitor to the

maximum value to maintain conservative power indication during future startups.

They also changed their local power range monitor replacement procedure to

use the vendor specified initial gain setting of 3.692 prior to startup.

The finding was more than minor because it affected the design control attribute

of the Mitigating Systems Cornerstone and impacted the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, the incorrect

gain settings caused a violation of technical specification 3.0.4 by rendering the

APRM Neutron Flux High - Setdown scram function and the Neutron Flux -

Upscale, Startup control rod block function inoperable prior to entry into Mode 2.

In accordance with NRC Inspection Manual Chapter 0609, Attachment 4, "Initial

Characterization of Findings," the inspectors determined that the issue affected

the Mitigating Systems Cornerstone. In accordance with NRC Inspection Manual

Chapter 0609, Appendix A, The Significance Determination Process (SDP) for

Findings at Power, the inspectors determined that the issue had very low safety

significance (Green) because although the finding affected a single reactor

protection system trip signal to initiate a reactor scram, it did not affect the

function of other redundant trips or diverse methods of reactor shutdown, did not

involve control manipulations that unintentionally added positive reactivity, and

did not result in a mismanagement of reactivity by operators. Because the

performance deficiency occurred in the past and is not reflective of current

licensee performance, this finding was not assigned a cross-cutting aspect.

(Section 4OA3).

Cornerstone: Barrier Integrity

Green. The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,

Criterion XVI, Corrective Action, involving the failure to correct a condition

adverse to quality in a timely manner. Specifically, the licensee failed to correct

multiple degraded conditions associated with the auxiliary building water intrusion

barrier. The licensee entered this issue into their corrective action program as

Condition Report CR-GGN-2012-10314. Corrective actions included generating

Work Order 318398 and delegating funds to repair the water intrusion barrier at

the next available opportunity.

The finding is more than minor because if left uncorrected, the condition of a

degraded auxiliary building water intrusion barrier could lead to a more significant

safety concern. Specifically, continued degradation of the water intrusion barrier

could lead to the auxiliary building (secondary containment) being degraded such

that the standby gas treatment system would not be able to achieve and maintain

-4-

the design negative pressure of 1/4 inch water column within 120 seconds. Using

Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of

Findings, the inspectors determined that the finding affected the Barrier Integrity

Cornerstone. In accordance with Inspection Manual Chapter 0609, Appendix A,

The Significance Determination Process (SDP) for Findings at Power, the

inspectors determined that the finding had very low safety significance (Green)

because the finding only represents a degradation of the radiological barrier

function provided for the auxiliary building and standby gas treatment system.

The inspectors determined that the apparent cause of this finding was that the

licensee had failed to classify the degraded water intrusion barrier as a condition

adverse to quality that warranted correction in a timely manner. Therefore, the

finding has a cross-cutting aspect in the problem identification and resolution

area, corrective action program component because the licensee failed to

properly classify conditions adverse to quality P.1(c)(Section 1R12).

Green. The inspectors identified a non-cited violation of 10 CFR 50.65(a)(2), for

the failure to monitor the performance of the auxiliary building water intrusion

barrier. The licensee entered this issue into their corrective action program as

Condition Report CR-GGN-2012-11740. Corrective actions included initiating

Condition Report CR-GGN-2012-12286, in which the licensee concluded the

degraded water intrusion barrier had experienced a Maintenance Rule Functional

Failure and required further evaluation to determine if the barrier should be

classified in 10 CFR 50.65 (a)(1).

The finding is more than minor because if left uncorrected, the failure to monitor

the performance of the auxiliary building water intrusion barrier in accordance

with the maintenance rule program could lead to a more significant safety

concern. Specifically, continued unmonitored degradation of the water intrusion

barrier could compromise the integrity of the secondary containment function of

the auxiliary building. Using Inspection Manual Chapter 0609, Attachment 4,

Initial Characterization of Findings, the inspectors determined that the finding

affected the Barrier Integrity Cornerstone. In accordance with Inspection Manual

Chapter 0609, Appendix A, The Significance Determination Process (SDP) for

Findings at Power, the inspectors determined that the finding had a very low

safety significance (Green) because the finding only represents a degradation of

the radiological barrier function provided for the auxiliary building and standby

gas treatment system. The inspectors determined that the apparent cause of this

finding was the licensee failed to recognize that the auxiliary building water

intrusion barrier was scoped into their Maintenance Rule program with the

monitoring criteria of zero occurrences of water intrusion barrier degradation.

Therefore, the finding had a cross-cutting aspect in the human performance area,

work practices component because the licensee failed to follow maintenance rule

program procedures H.4(b)(Section 1R12).

-5-

Cornerstone: Occupational Radiation Safety

Green. The inspector reviewed a self-revealing finding of very low safety

significance because during the refueling outage 18 extended power upgrade,

the licensee did not adequately plan and control work activities for the design and

replacement of the new fuel pool cooling heat exchangers. Specifically, outage

personnel did not perform adequate pre-outage walkdowns, which resulted in

significant unplanned collective exposure. Actual collective dose and hours for

Radiation Work Permit 2012-1086, Fuel Pool Cooling & Cleanup Heat

Exchanger Replacement, was 23.9 person-rem and 12,237 RWP-hours,

respectively. This is compared to the initial planned estimate of 3.74 person-rem

and 1,905 RWP-hours. This finding and procedural concern was entered into the

corrective action program as Condition Reports CR-GGNS-2012-09011 and

CR-GGNS-2012-12398.

The failure to appropriately use ALARA planning and controls procedures to

prevent unplanned and unintended collective doses was a performance

deficiency. This performance deficiency was more than minor because it

affected the Occupational Radiation Safety Cornerstone attribute of Program and

Process in that the failure to adequately implement ALARA procedures caused

the collective radiation dose for the job activity to exceed the planned dose by

more than 50 percent. In addition, this type of issue is addressed in Example 6.j

of IMC 0612, Appendix E, Examples of Minor Issues. Using the Occupational

Radiation Safety Significance Determination Process, the inspector determined

this performance deficiency to be a finding of very low safety significance

because although it involved ALARA planning and controls, the licensees latest

rolling three-year average does not exceed 240 person-rem. This finding has a

cross-cutting aspect in the human performance area, work control component,

because the licensee failed to evaluate the impact of work scope change on

human performance and interdepartmental communication and coordination prior

to commencing work activities. Specifically, there was inappropriate coordination

and communication of work activities between work groups

H.3(b)(Section 2RS02).

Green. The inspectors reviewed a self-revealing non-cited violation of Technical

Specification 5.4.1 for failure to comply with radiological exposure controls

specified in Radiation Work Permit 2012-1402, Refuel Floor High Water

Activities. Specifically, radiation exposure controls in the RWP required the

licensee to verify that fuel pool cleanup (demineralizers) was in-service, and if

dose rates increased by more than 0.2 millirem/hour, change the resins. During

reactor cavity operations, both fuel pool demineralizer trains were inoperable at

least 25 days. In addition, the dryer separator pool and reactor cavity were

isolated from the fuel pool clean up system. Consequently, general area

radiation levels on the reactor cavity floor increased from 0.4 millirem/hour to

6.0 millirem/hour. The actual collective dose and hours for the work activity was

8.24 person-rem and 9,000 RWP-hours, respectively. This is compared to the

planned initial estimate of 4.60 person-rem and 6,987 RWP-hours. This

-6-

Radiation Work Permint and procedure violation was documented in the

licensees corrective action program as Condition Reports CR-GGNS-2012-

04288 and CR-GGNS-2012-12401.

The licensees failure to comply with the RWP to prevent unplanned and

unintended collective doses was a performance deficiency. This performance

deficiency was more than minor because it affected the Occupational Radiation

Safety Cornerstone attribute of Program and Process in that the failure to

adequately implement ALARA procedures caused the collective radiation dose

for the job activity to exceed the planned dose by more than 50 percent. In

addition, this type of issue is addressed in Example 6.i of IMC 0612, Appendix E,

Examples of Minor Issues. Using the Occupational Radiation Safety

Significance Determination Process, the inspector determined this performance

deficiency to be a non-cited violation of very low safety significance because

although it involved ALARA planning and controls, the licensees latest rolling

three-year average does not exceed 240 person-rem. The violation involved a

cross-cutting aspect in the human performance area, work control component,

because the licensee did not appropriately coordinate work activities by

incorporating actions to address the need for work groups to communicate and

coordinate with each other during activities in which interdepartmental

coordination was necessary to assure human performance

H.3(b)(Section 2RS02).

B. Licensee-Identified Violations

One violation of very low safety significance, which was identified by the licensee has

been reviewed by the inspector. Corrective actions taken or planned by the licensee

have been entered into the licensees corrective action program. This violation and

corrective action tracking number is listed in Section 4OA7.

-7-

REPORT DETAILS

Summary of Plant Status

Grand Gulf Nuclear Station (GGNS) began the inspection period at 100 percent rated thermal

power.

On October 21, 2012, the operators reduced power to approximately 87 percent rated

thermal power for a planned control rod testing and returned to 100 percent rated

thermal power the same day.

On November 8, 2012, the operators reduced power to approximately 93 percent rated

thermal power due to a moisture intrusion into the main lube oil and hydrogen seal oil

systems that resulted in a clogging of the hydrogen seal oil filters and a procedurally

required power reduction due to decrease in seal oil pressure. The licensee changed

out the seal oil filters, de-watered the oil systems, and returned to 100 percent rated

thermal power on November 9, 2012.

On November 20, 2012, the operators reduced power to approximately 57 percent rated

thermal power due to an oil leak on the B reactor feedwater pump. The licensee

repaired the leak and returned to 100 percent rated thermal power on November 22,

2012.

On December 8, 2012, the operators began to shutdown and cool down the plant to

perform planned outage 19-01 to fix some long standing balance of plant issues,

including air in leakage to the condenser and a failed open second stage moisture

separator drain valve. The licensee commenced plant startup on December 14, 2012,

and achieved 100 percent rated thermal power after final control rod pattern was

achieved on December 21, 2012.

On December 29, 2012, at 12:18 a.m., the reactor scrammed from 100 percent rated

thermal power due to phase A unit differential signal resulting in a main generator

/turbine trip with a reactor scram. The licensee determined the apparent cause of the

scram and commenced startup activities on December 31, 2012.

The plant continued startup activities through the end of the quarter.

-8-

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignment (71111.04)

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

Division I diesel generator during division II allowed outage time

Division I standby service water during division II allowed outage time

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Updated Final Safety Analysis Report, technical specification

requirements, administrative technical specifications, outstanding work orders, condition

reports, and the impact of ongoing work activities on redundant trains of equipment in

order to identify conditions that could have rendered the systems incapable of

performing their intended functions. The inspectors also inspected accessible portions

of the systems to verify system components and support equipment were aligned

correctly and operable. The inspectors examined the material condition of the

components and observed operating parameters of equipment to verify that there were

no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the

corrective action program with the appropriate significance characterization. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of two partial system walkdown samples as

defined in Inspection Procedure 71111.04-05.

b. Findings

No findings were identified.

-9-

.2 Complete Walkdown

a. Inspection Scope

On October 28, 2012, the inspectors performed a complete system alignment inspection

of the residual heat removal system to verify the functional capability of the system. The

inspectors selected this system because it was considered both safety significant and

risk significant in the licensees probabilistic risk assessment. The inspectors inspected

the system to review mechanical and electrical equipment line ups, electrical power

availability, system pressure and temperature indications, as appropriate, component

labeling, component lubrication, component and equipment cooling, hangers and

supports, operability of support systems, and to ensure that ancillary equipment or

debris did not interfere with equipment operation. The inspectors reviewed a sample of

past and outstanding work orders to determine whether any deficiencies significantly

affected the system function. In addition, the inspectors reviewed the corrective action

program database to ensure that system equipment-alignment problems were being

identified and appropriately resolved. Specific documents reviewed during this

inspection are listed in the attachment.

These activities constitute completion of one complete system walkdown sample as

defined in Inspection Procedure 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

Upper control room

Division I diesel generator room

Division I standby service water pump and valve rooms

Reactor core isolation cooling pump room

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

- 10 -

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to affect equipment that could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed; that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four quarterly fire-protection inspection samples

as defined in Inspection Procedure 71111.05-05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures (71111.06)

a. Inspection Scope

The inspectors reviewed the updated safety analysis report, the flooding analysis, and

plant procedures to assess susceptibilities involving internal flooding. Additionally, the

inspectors verified that operator actions for coping with internal flooding can reasonably

achieve the desired outcomes. The inspectors also inspected the areas listed below to

verify the adequacy of equipment seals located below the flood line, floor and wall

penetration seals, watertight door seals, common drain lines and sumps, sump pumps,

level alarms, and control circuits, and temporary or removable flood barriers. Specific

documents reviewed during this inspection are listed in the attachment.

November 14-15, 2012, Turbine Building, elevations 93-0, 111-0; Auxiliary

Building, elevation 103-0; Control Building, elevation 93-0. Inspection of

Unresolved Item 05000416/2012008-07, Potential Internal Flooding Caused by

Circulation Water System Failure.

These activities constitute completion of one flood protection measures inspection

sample as defined in Inspection Procedure 71111.06-05.

b. Findings

No findings were identified.

- 11 -

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11)

.1 Quarterly Review of Licensed Operator Requalification Program

a. Inspection Scope

On October 15, 2012, the inspectors observed a crew of licensed operators in the plants

simulator during a requalification as found evaluation. The inspectors assessed the

following areas:

Licensed operator performance

The ability of the licensee to administer the evaluations

The modeling and performance of the control room simulator

The quality of post-scenario critiques

Follow-up actions taken by the licensee for identified discrepancies

These activities constitute completion of one quarterly licensed operator requalification

program sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Quarterly Observation of Licensed Operator Performance

a. Inspection Scope

On November 20, 2012, the inspectors observed the performance of on-shift licensed

operators in the plants main control room. At the time of the observations, the plant was

in a period of heightened activity due to an unplanned downpower from 100 percent to

57 percent for an emergent repair of an oil leak on the B reactor feedwater pump. The

inspectors observed the operators performance of the following activities:

Pre-job brief

Reactivity management brief

Power reduction via recirculation pump flow reduction

Power reduction via control rod manipulations

- 12 -

In addition, the inspectors assessed the operators adherence to plant procedures,

including EN-OP-115, Revision 12, Conduct of Operations, and other operations

department policies.

As part of this inspection activity, the inspectors also observed the operators use of the

power-to-flow map and the operators awareness of the plants location on the power-to-

flow map to ensure that the plant was operated within the analyzed region. The

inspector also independently verified that the plant was operated within the analyzed

region of the power-to-flow map as the power was being reduced from 100 percent to 57

percent. This inspection activity constitutes the completion of one Operating Experience

Smart Sample (OpESS) FY2007-004, BWR Core Power/ Flow Map - Supplemental

Inspection Guidance for MC 2515D.

These activities constitute completion of one quarterly licensed-operator performance

sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

Auxiliary building (T10)

Residual heat removal system (E12)

Suppression pool makeup system (E30)

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

Implementing appropriate work practices

Identifying and addressing common cause failures

Scoping of systems in accordance with 10 CFR 50.65(b)

Characterizing system reliability issues for performance

Charging unavailability for performance

- 13 -

Trending key parameters for condition monitoring

Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or -(a)(2)

Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of three quarterly maintenance effectiveness

samples as defined in Inspection Procedure 71111.12-05.

b. Findings

(1) Failure to Make Timely Corrective Actions to Repair the Degraded Auxiliary Building

Water Intrusion Barrier

Introduction. The inspectors identified a Green non-cited violation of 10 CFR 50,

Appendix B, Criterion XVI, Corrective Action, involving the failure to promptly correct a

condition adverse to quality. Specifically, the auxiliary building water-intrusion barrier

has been in a degraded condition since April 2004.

Description. The seismic category 1 containment structures incorporated into the design

of Grand Gulf Nuclear Station are the containment building (primary containment),

auxiliary building (secondary containment), and enclosure building. The auxiliary

building completely encircles the containment building from base mat to mid height and

houses normal and safety related equipment. The auxiliary building, in conjunction with

the standby gas treatment system, is designed to limit the thyroid dose and whole body

dose to within the guidelines of 10 CFR Part 100 by reaching and maintaining a negative

pressure of 1/4 inch water column within 120 seconds. The enclosure building is a limited

leakage, steel framed, seismic category 1 structure that completely encloses the

portions of the containment building above the auxiliary building roof levels and is

designed to limit the leakage of radioactive material into the environment during a loss of

coolant accident. To maintain the required leakage limits, a water intrusion barrier, in

the form of a flexible seal, is provided around the entire periphery of the

enclosure/auxiliary building interface. The occurrence of water intrusion into the

auxiliary building is evidence that the water intrusion barrier is degraded. Although the

standby gas treatment system has passed its surveillance requirements of achieving and

- 14 -

maintaining the designed negative pressure, continued degradation of the flexible seal

could challenge the standby gas treatment systems ability to meet its surveillance

requirements.

On October 1, 2012, the inspectors reviewed Condition Report CR-GGN-2012-10314,

which described water leaking into the auxiliary building following a heavy rain storm.

The inspectors performed a detailed historical review of water intrusion into the auxiliary

building and found 18 condition reports had been written between April 2004 and August

2012 identifying occurrences of water leaking into the auxiliary building. The inspectors

also found that the majority of the condition reports written were closed to Work Order

60875, which has been in the Plan status since 2005.

The licensee entered this issue in their corrective action program as Condition Report

CR-GGN-2012-10314. Corrective actions included generating Work Order 318398 and

delegating funds to repair the water intrusion barrier at the next available opportunity.

Analysis. The failure to promptly correct a condition adverse to quality is a performance

deficiency. The inspectors used Inspection Manual Chapter 0612, Appendix B, to

determine that the finding is more than minor because if left uncorrected, the condition of

a degraded auxiliary building water intrusion barrier could lead to a more significant

safety concern. Specifically, continued degradation of the water intrusion barrier could

lead to the auxiliary building (secondary containment) being degraded in that the

standby gas treatment system would not be able to achieve and maintain the design

negative pressure of 1/4 inch water column within 120 seconds. Using Inspection

Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, the inspectors

determined that the finding affected the Barrier Integrity Cornerstone. In accordance

with Inspection Manual Chapter 0609, Appendix A, The Significance Determination

Process (SDP) for Findings at Power, the inspectors determined that the finding had

very low safety significance (Green) because the finding only represents a degradation

of the radiological barrier function provided for the auxiliary building and standby gas

treatment system. The inspectors determined that the apparent cause of this finding

was the licensee had failed to classify the degraded water intrusion barrier as a condition

adverse to quality that warranted prompt correction. Therefore, the finding had a cross-

cutting aspect in the problem identification and resolution area, corrective action

program component because the licensee failed to properly classify conditions adverse

to quality P.1(c).

Enforcement. 10 CFR 50, Appendix B, Criterion 16, Corrective Action, states in part,

measures shall be established to assure that conditions adverse to quality, are promptly

identified and corrected. Contrary to the above, measures establish by the licensee did

not assure that conditions adverse to quality, were promptly identified and corrected.

Specifically, the licensee initiated 18 condition reports from April 2004 through August

2012 identifying auxiliary building water intrusion barrier degradation as evidenced by

water in-leakage and failed to implement corrective actions to address the degraded

barrier. As an immediate corrective action, the licensee generated Work Order 318398

and delegated funds to repair the water-intrusion barrier at the next available

opportunity. This violation is being treated as a non-cited violation (NCV), consistent

- 15 -

with Section 2.3.2 of the Enforcement Policy because it was of very low safety

significance (Green) and it was entered into the licensees corrective action program as

CR-GGN-2012-10314 to address recurrence: NCV 05000416/2012005-01, Failure to

Make Timely Corrective Actions to Repair the Degraded Auxiliary Building Water

Intrusion Barrier.

(2) Failure to Adequately Monitor the Condition of the Auxiliary Building Water Intrusion

Barrier

Introduction. The inspectors identified a Green non-cited violation of 10 CFR

50.65(a)(1), involving the failure to adequately monitor the performance of the auxiliary

building water intrusion barrier.

Description. On October 1, 2012, the inspectors reviewed Condition Report CR-GGN-

2012-10323, which described water leaking into the auxiliary building following a heavy

rain storm. During the review, the inspectors determined the auxiliary building roof

system, which includes a water intrusion barrier, was scoped in the licensees

maintenance rule program with the monitoring criteria of zero occurrences of water

intrusion barrier degradation. The inspectors performed a detailed historical review of

water intrusion into the auxiliary building and found 18 condition reports had been written

between April 2004 and August 2012 identifying the occurrence of auxiliary building

water intrusion barrier degradation as evidenced by water leaking into the auxiliary

building. The inspectors also found that the licensee had not performed any evaluation

of the water-intrusion barrier against the monitoring criteria established in the licensees

maintenance rule program.

When the inspectors brought this concern to the licensees attention, the licensee

entered this issue in their corrective action program as Condition Report CR-GGN-2012-

11740. Corrective actions included initiating Condition Report CR-GGN-2012-12286, in

which the licensee concluded the degraded water-intrusion barrier was a Maintenance

Rule Functional Failure and required further evaluation to determine if the barrier should

be classified a(1).

Analysis. The failure to monitor the performance of the auxiliary building water intrusion

barrier in accordance with the maintenance rule program is a performance deficiency.

The inspectors used Inspection Manual Chapter 0612, Appendix B, to determine that the

finding is more than minor because if left uncorrected, the failure to monitor the

performance of the auxiliary building water intrusion barrier in accordance with the

maintenance rule program could lead to a more significant safety concern. Specifically,

continued unmonitored degradation of the water intrusion barrier could compromise the

integrity of the secondary containment function of the auxiliary building. Using

Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, the

inspectors determined that the finding affected the Barrier Integrity Cornerstone. In

accordance with Inspection Manual Chapter 0609, Appendix A, The Significance

Determination Process (SDP) for Findings at Power, the inspectors determined that the

finding had a very low safety significance (Green) because the finding only represents a

degradation of the radiological barrier function provided for the auxiliary building and

- 16 -

standby gas treatment system. The inspectors determined that the apparent cause of

this finding was the licensee had failed to recognize that the auxiliary building water

intrusion barrier was scoped into their Maintenance Rule program with the monitoring

criteria of zero occurrences of water intrusion barrier degradation. Therefore, the finding

had a cross-cutting aspect in the human performance area, work practices component

because the licensee did not follow maintenance rule program procedures H.4(b).

Enforcement. 10 CFR 50.65 (a)(1), requires, in part, that the holders of an operating

license shall monitor the performance or condition of structures, within the scope of the

rule as defined by 10 CFR 50.65 (b), against licensee-established goals, in a manner

sufficient to provide reasonable assurance that such structures are capable of fulfilling

their intended functions. 10 CFR 50.65 (a)(2) states, in part, that monitoring as specified

in 10 CFR 50.65 (a)(1) is not required where it has been demonstrated that the

performance or condition of an SSC is being effectively controlled through the

performance of appropriate preventive maintenance, such that the SSC remains capable

of performing its intended function.

Contrary to the above, the licensee did not monitor the performance or condition of a

structure within the scope of the rule as defined by 10 CFR 50.65 (b), against licensee-

established goals, in a manner sufficient to provide reasonable assurance that the

structure is capable of fulfilling its intended functions. Specifically, although the auxiliary

building water-intrusion barrier is within the scope of the rule and the licensee had

established a performance goal of zero water leakage for that barrier, between April,

2004, and August, 2012, the licensee documented 18 instances of water leakage

through that barrier, but did not evaluate the barrier in accordance with their

maintenance rule program. This violation is being treated as a non-cited violation

(NCV), consistent with Section 2.3.2 of the Enforcement Policy because it was of very

low safety significance (Green), and it was entered into the licensees corrective action

program as CR-GGN-2012-11740 to address recurrence: NCV 05000416/2012005-02,

Failure to Adequately Monitor the Condition of the Auxiliary Building Water Intrusion

Barrier.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and safety-

related equipment listed below to verify that the appropriate risk assessments were

performed prior to removing equipment for work:

Week of October 28, 2012, during the division II allowed outage time, resulting in

the site being in an increased yellow risk profile during the outage

Week of November 19, 2012, during the unplanned down power to repair an oil

leak on the B reactor feedwater pump, resulting in the site being in a increased

risk profile

- 17 -

Week of December 9, 2012, during the planned outage PO-19-01, resulting in

the licensee entering offline yellow risk for decay heat removal and containment

control

The inspectors selected these activities based on potential risk significance relative to

the reactor safety cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three maintenance risk assessments and

emergent work control inspection samples as defined in Inspection

Procedure 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Evaluations and Functionality Assessments (71111.15)

a. Inspection Scope

The inspectors reviewed the following assessments:

Division II diesel generator time delay relay failure (CR-GGN-2012-12133)

Residual heat removal-fuel pool cooling assist suction valve over thrust (CR-

GGN-2012-11755)

Division II diesel generator jacket water tube wall thinning (CR-GGN-2012-

12060)

Non-conservative Tech Spec allowable values (CR-GGN-2012-09971)

The inspectors selected these operability and functionality assessments based on the

risk significance of the associated components and systems. The inspectors evaluated

the technical adequacy of the evaluations to ensure technical specification operability

was properly justified and to verify the subject component or system remained available

such that no unrecognized increase in risk occurred. The inspectors compared the

- 18 -

operability and design criteria in the appropriate sections of the technical specifications

and Updated Final Safety Analysis Report to the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. Additionally, the

inspectors reviewed a sampling of corrective action documents to verify that the licensee

was identifying and correcting any deficiencies associated with operability evaluations.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four operability evaluations inspection samples

as defined in Inspection Procedure 71111.15-05.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

Standby service water pump B following motor replacement

Division II diesel generator following maintenance activities

Residual heat removal pump B following maintenance activities

Residual heat removal shutdown cooling suction valve E12-F006B and standby

service water blow down valve P41-F016B following maintenance activities

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following (as applicable):

The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the Updated

Final Safety Analysis Report, 10 CFR 50 requirements, licensee procedures, and

various NRC generic communications to ensure that the test results adequately ensured

that the equipment met the licensing basis and design requirements. In addition, the

- 19 -

inspectors reviewed corrective action documents associated with post-maintenance

tests to determine whether the licensee was identifying problems and entering them in

the corrective action program and that the problems were being corrected

commensurate with their importance to safety. Specific documents reviewed during this

inspection are listed in the attachment.

These activities constitute completion of four post-maintenance testing inspection

samples as defined in Inspection Procedure 71111.19-05.

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities (71111.20)

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the planned

outage, started on December 8, 2012, to confirm that licensee personnel had

appropriately considered risk, industry experience, and previous site-specific problems in

developing and implementing a plan that assured maintenance of defense in depth.

During the planned outage, the inspectors observed portions of the shutdown and

cooldown processes and monitored licensee controls over the outage activities listed

below.

Configuration management, including maintenance of defense in depth, is

commensurate with the outage safety plan for key safety functions and

compliance with the applicable technical specifications when taking equipment

out of service.

Status and configuration of electrical systems to ensure that technical

specifications and outage safety-plan requirements were met.

Monitoring of decay heat removal processes, systems, and components.

Verification that outage work was not impacting the ability of the operators to

operate the spent fuel pool cooling system.

Reactor water inventory controls, including flow paths, configurations, and

alternative means for inventory addition, and controls to prevent inventory loss.

Controls over activities that could affect reactivity.

Maintenance of secondary containment as required by the technical

specifications.

Startup and ascension to full power operation.

- 20 -

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one other outage inspection sample as defined

in Inspection Procedure 71111.20-05.

b. Findings

Introduction. The inspectors reviewed a self-revealing non-cited violation of 10 CFR 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees

failure to complete preventive maintenance tasks on the high pressure core spray

division III diesel generator output breaker in accordance with the corresponding

preventive maintenance task template.

Description On June 5, 2012, the high pressure core spray division III diesel generator

output breaker (152-1701) failed to close during a surveillance test. Troubleshooting

revealed that the breaker had failed to close because of intermittent high resistance on

the current relay contacts. Through the subsequent evaluation documented in Condition

Report CR-GGN-2012-07922, the licensee determined that the apparent cause of the

relay failure was age-related and/or cycle-related degradation due to a lack of an

appropriate preventive-maintenance task for the relay. More specifically, although the

licensee had set a recurring preventive-maintenance task to refurbish/replace the

breaker (using preventive maintenance task PMRQ 50018212-02) every 12 +/- 25%

years, and had last completed that task in 1996 such that it was next due on November

2, 2008 (or November 2, 2011 with a 25% extension), the licensee did not complete that

task when it was due. Instead, the licensee deferred that task until September, 2012.

To review the bases for the preventive maintenance tasks performed using PMRQ

50018212-02, the inspectors noted that Preventive Maintenance Basis Template, EN-

Switchgear-Medium Voltage - 1 KV to 7KV, Revision 3, discusses switch and relay

contact failures and states, in part,

High contact resistance may develop over time although a trouble-free period of

10 years should be obtained under mild service conditions. Switch and relay

contact failure may be avoided by measuring the contact resistance at the

detailed inspection.

The inspectors therefore considered that the licensee likely would have prevented the

June 5, 2012, breaker failure if they had performed preventive maintenance task PMRQ

50018212-02 in 2011, and if they had measured the current relay contact resistance at

that time.

The licensee entered this issue in their corrective action program as Condition Report

CR-GGN-2012-07992. Their immediate corrective actions included replacing the failed

control relay and restoring operability to the division III diesel generator. The long-term

corrective actions included revising the breaker refurbishment/replacement procedure to

- 21 -

replace the current relay and changing the procedure frequency to once every 10 years

versus once every 12 years.

Analysis. The licensees failure to complete preventive maintenance tasks on the high

pressure core spray division III diesel generator output breaker in accordance with the

corresponding preventive maintenance task template was a performance deficiency.

Using NRC Inspection Manual Chapter 0612, Appendix B, Issue Screening, the

inspectors determined that this performance deficiency was more than minor and is

therefore a finding because it is associated with the equipment performance attribute of

the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of

ensuring the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, this failed control relay

caused the subject breaker to fail to close during the division III diesel generator monthly

surveillance on June 5, 2012.

The inspectors used NRC Inspection Manual Chapter 0609, Attachment 4, "Initial

Characterization of Findings," to determine that the issue affected the Mitigating System

Cornerstone. Because the finding pertained only to a degraded condition while the plant

was shutdown, the inspectors used Manual Chapter 0609, Appendix G, Shutdown

Operations Significance Determination Process, Checklist 8, Cold Shutdown or

Refueling Operation - Time to Boil > 2 Hours: RCS Level < 23 Above Top of Flange, to

determine that the finding was of very low safety significance because it did not increase

the likelihood of a loss of reactor coolant system inventory; did not degrade the

licensees ability to terminate a leak path or add RCS inventory when needed; did not

significantly degrade the licensees ability to recover decay heat removal if lost; and did

not affect the safety/relief valves (Green). The inspectors determined that the cause of

this finding was a latent issue that is not reflective of current performance, therefore no

cross-cutting aspect was identified.

Enforcement. 10 CFR 50, Appendix B, Criterion V, states in part, that activities affecting

quality shall be accomplished in accordance with procedures. Contrary to this

requirement, an activity affecting quality was not accomplished in accordance with

procedures. Specifically, preventive maintenance tasks on the high pressure core spray

division III diesel generator output breaker are prescribed by preventive maintenance

task PMRQ 50018212-02, on November 2, 2011. The licensee did not accomplish

preventive maintenance tasks on the high pressure core spray division III diesel

generator output breaker in accordance with PMRQ 50018212-02, in that PMRQ

50018212-02 required the licensee to refurbish/replace the breaker before November 2,

2011, and the licensee did not do so. As a result, on June 5, 2012, that breaker failed to

close due to high contact resistance on the breakers current relay contacts. As an

immediate corrective action, the licensee replaced the failed relay and restored

operability to the division III diesel generator. This violation is being treated as a non-

cited violation (NCV), consistent with Section 2.3.2 of the Enforcement Policy because it

was of very low safety significance (Green), and it was entered into the licensees

corrective action program as CR-GGN-2012-07992 to address recurrence.

(NCV 05000416/2012005-03, Failure to Perform Preventive Maintenance on

GE Magne-Blast Circuit Breakers in Accordance With the Corresponding Preventive

Maintenance Task Template).

- 22 -

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, procedure

requirements, and technical specifications to ensure that the surveillance activities listed

below demonstrated that the systems, structures, and/or components tested were

capable of performing their intended safety functions. The inspectors either witnessed

or reviewed test data to verify that the significant surveillance test attributes were

adequate to address the following:

Preconditioning

Evaluation of testing impact on the plant

Acceptance criteria

Test equipment

Procedures

Jumper/lifted lead controls

Test data

Testing frequency and method demonstrated technical specification operability

Test equipment removal

Restoration of plant systems

Reference setting data

Annunciators and alarms setpoints

The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing.

November 15, 2012, automatic depressurization system electrical surveillance

November 29, 2012, turbine control valve fast closure functional test for channels

B and D

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of two surveillance testing inspection samples as

defined in Inspection Procedure 71111.22-05.

b. Findings

No findings were identified.

- 23 -

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The NSIR headquarters staff performed an in-office review of the latest revisions of

various Emergency Plan Implementing Procedures (EPIPs) and the Emergency Plan

located under ADAMS accession number ML12265A082 as listed in the Attachment.

The licensee determined that in accordance with 10 CFR 50.54(q), the changes made in

the revisions resulted in no reduction in the effectiveness of the Plan, and that the

revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to

10 CFR 50. The NRC review was not documented in a safety evaluation report and did

not constitute approval of licensee-generated changes; therefore, this revision is subject

to future inspection. The specific documents reviewed during this inspection are listed in

the Attachment.

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.04-05.

b. Findings

No findings were identified.

1EP6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on October

16, 2012, to identify any weaknesses and deficiencies in classification, notification, and

protective action recommendation development activities. The inspectors observed

emergency response operations in the Emergency Operating Facility (EOF) and the

Technical Support Center (TSC), to determine whether the event classification,

notifications, and protective action recommendations were performed in accordance with

procedures. The inspectors also attended the licensee drill critique to compare any

inspector-observed weakness with those identified by the licensee staff in order to

evaluate the critique and to verify whether the licensee staff was properly identifying

weaknesses and entering them into the corrective action program. As part of the

inspection, the inspectors reviewed the drill package and other documents listed in the

attachment.

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.06-05.

- 24 -

b. Findings

No findings were identified.

2. RADIATION SAFETY

Cornerstone: Occupational and Public Radiation Safety

2RS02 Occupational ALARA Planning and Controls (71124.02)

a. Inspection Scope

This area was inspected to assess performance with respect to maintaining occupational

individual and collective radiation exposures as low as is reasonably achievable

(ALARA). The inspector used the requirements in 10 CFR Part 20, the technical

specifications, and the licensees procedures required by technical specifications as

criteria for determining compliance. During the inspection, the inspector interviewed

licensee personnel and reviewed the following items:

Site-specific ALARA procedures and collective exposure history, including the

current 3-year rolling average, site-specific trends in collective exposures, and

source-term measurements

ALARA work activity evaluations/post job reviews, exposure estimates, and

exposure mitigation requirements

The methodology for estimating work activity exposures, the intended dose

outcome, the accuracy of dose rate and man-hour estimates, and intended

versus actual work activity doses and the reasons for any inconsistencies

Records detailing the historical trends and current status of tracked plant source

terms and contingency plans for expected changes in the source term due to

changes in plant fuel performance issues or changes in plant primary chemistry

Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

Audits, self-assessments, and corrective action documents related to ALARA

planning and controls since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in

Inspection Procedure 71124.02-05.

b. Findings

- 25 -

(1) Failure to Adequately Plan and Control Work Activities to Maintain ALARA

Introduction. An inspector reviewed a self-revealing Green finding of very low safety

significance because during Refueling Outage 18, the licensee did not adequately plan

and control work activities for the design and replacement of the new fuel pool cooling

heat exchangers under Radiation Work Permit (RWP) 2012-1086.

Description. While reviewing the post ALARA review package for RWP 2012-1086 from

Refueling Outage 18, Extended Power Upgrade, the inspector identified that the

licensees ALARA planning and control program failed to prevent unplanned and

unintended collective doses related to the design and replacement of the new fuel pool

cooling heat exchangers. Specifically, outage personnel did not perform adequate pre-

outage walkdowns which resulted in significant unplanned collective exposure. The

actual collective dose and hours for the project was 23.9 person-rem and

12,237 RWP-hours, respectively. This is compared to the initial estimate of

3.74 person-rem and 1,905 RWP-hours. Initially, there were approximately 165 work

activities, almost equally split between 2 tasks on RWP 2012-1086, Revision 0.

However, RWP 2012-1086 was revised eight times during the fuel pool cooling heat

exchanger replacement project due to increased work scope. According to the post-job

ALARA review, the project began with only 40 percent of its work activities planned out

and developed on the outage schedule. An additional 60 percent of the project work

activities were added as increased scope after the outage began. The inspector noted

that 63 Engineering Change Notice (ECNs) were added to the fuel pool cooling heat

exchanger replacement project as increased scope. The implementation of the 63

ECNs caused the projected work hours to increase from 975 hours0.0113 days <br />0.271 hours <br />0.00161 weeks <br />3.709875e-4 months <br /> to 7,295 hours0.00341 days <br />0.0819 hours <br />4.877645e-4 weeks <br />1.122475e-4 months <br /> (a

748 percent increase). This increase in work scope was not fully understood nor

justified, and resulted in unintended collective dose. Some causes for the dose

overages were higher dose rates than expected, longer work durations than expected,

and more added work scope than expected. However, there was no documentation in

the ALARA package that justified the dose estimate increases resulting from changes in

the job scope, duration, and work area dose rates. The inspector determined that the

performance deficiency that led to the increased collective dose was not following the

written ALARA Program procedure EN-RP-110, Revision 7, for planning and work

controls and procedure EN-DC-115, Engineering Change Process, Revision 13.

EN-RP-110, Section 4.0.8, states, in part, that Planning and Outage Groups

Responsibilities include: Providing accurate work site person-hours and accurate

work locations for ALARA planning purposes. Provide detailed work plans to

allow for ALARA planning to designate adequate radiological controls.

EN-DC-115, Section 5.3.4(e), states, in part, that Radiation Protection / ALARA

considerations shall be identified early in the engineering change process (by

10 percent design milestone). Radiation Protection / ALARA considerations

should be addressed as an integral part of the design configuration, material

selection, and implementation plan.

Apparent Cause Evaluation (ACE) in CR-GGNS-2012-09011 evaluated why the outage

ALARA goal was exceeded by 114 person-rem. The ACE stated, in part, that the

- 26 -

milestone walkdowns of outage work packages and execution were not completed in a

timely manner and in accordance with procedure EN-FAP-OU-100, Refueling Outage

Preparation and Milestones, Revision 2.

Analysis. The failure to appropriately use the ALARA Planning and Controls procedure

to prevent unplanned and unintended collective doses was a performance deficiency.

This performance deficiency was more than minor because it affected the Occupational

Radiation Safety Cornerstone attribute of Program and Process in that the failure to

adequately implement ALARA procedures caused the collective radiation dose for the

job activity to exceed the planned dose by more than 50 percent. In addition, this type of

issue is addressed in Example 6.j of IMC 0612, Appendix E, Examples of Minor Issues.

Using the Occupational Radiation Safety Significance Determination Process, the

inspector determined this performance deficiency to be a finding of very low safety

significance because although it involved ALARA planning and controls, the licensees

latest rolling three-year average does not exceed 240 person-rem. This finding has a

cross-cutting aspect in the human performance area, work control component, because

the licensee failed to evaluate the impact of work scope change on human performance

and interdepartmental communication and coordination prior to commencing work

activities. Specifically, there was inappropriate coordination and communication of work

activities between work groups H.3(b).

Enforcement. No violation of regulatory requirements occurred. However, this

performance deficiency is directly related to the licensees failure to meet its expectation

to fully implement ALARA outage, planning, and control procedures. This finding and

the procedural concern were entered into the corrective action program as

CR-GGNS-2012-09011 and CR-GGNS-2012-12396: FIN 05000416/2012005-04,

Failure to Adequately Plan and Control Work Activities to Maintain ALARA.

(2) Failure To Follow Radiation Work Permit Requirements During Reactor Cavity High

Water Operations

Introduction. An inspector reviewed a self-revealing Green non-cited violation of

Technical Specification 5.4.1 for failure to comply with radiological exposure controls

specified in Radiation Work Permit (RWP) 2012-1402, Refuel Floor High Water

Activities.

Description. Radiation exposure controls in the RWP required the licensee to verify that

fuel pool cleanup (demineralizers) was inservice, and if dose rates increased by more

than 0.2 millirem/hour, change the resins. During reactor cavity operations, both fuel

pool demineralizer trains were inoperable at least 25 days. In addition, the dryer

separator pool and reactor cavity were isolated from the fuel pool clean up system.

Consequently, general area radiation levels on the reactor cavity floor increased from

0.4 millirem/hour to 6.0 millirem/hour. However, the resins were not changed as

required. The actual collective dose and hours for the work activity was 8.24 person-rem

and 9,000 RWP-hours, respectively. This is compared to the initial estimate of

4.60 person-rem and 6,987 RWP-hours.

- 27 -

Analysis. The licensees failure to implement radiological exposure controls in

accordance with the RWP was the performance deficiency that caused unplanned and

unintended collective doses. This performance deficiency was more than minor

because it affected the Occupational Radiation Safety Cornerstone attribute of Program

and Process in that the failure to adequately implement ALARA procedures caused the

collective radiation dose for the job activity to exceed the planned dose by more than

50 percent. In addition, this type of issue is addressed in Example 6.i of IMC 0612,

Appendix E, Examples of Minor Issues. Using the Occupational Radiation Safety

Significance Determination Process, the inspector determined this performance

deficiency to be a non-cited violation of very low safety significance because although it

involved ALARA planning and controls, the licensees latest rolling three-year average

does not exceed 240 person-rem. This violation involved a cross-cutting aspect in the

human performance area, work control component, because the licensee did not

appropriately coordinate work activities by incorporating actions to address the need for

work groups to communicate and coordinate with each other during activities in which

interdepartmental coordination was necessary to assure human performance H.3(b).

Enforcement. Technical Specification 5.4.1 states that written procedures shall be

established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Section 7.e(1).

Contrary to the above, during Refueling Outage 18, written procedures were not

established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Specifically,

Appendix A of Regulatory Guide 1.33 lists procedures for radiation exposure and

access controls;

licensee procedure EN-RP-100, Revision 7, Radiation Worker Expectations, is

a procedure for radiation exposure and access controls and requires, in part, that

individuals comply with all requirements of the procedure and radiation work

permit (RWP) instructions when performing radiological work;

RWP 2012-1402, Refuel Floor High Water Activities, required the licensee to

verify that fuel pool cleanup system demineralizers were in-service and to

change the resins if dose rates increased by more than 0.2 millirem/hour; and

from March 13 through April 10, 2012, fuel pool cleanup system demineralizers were not

in service. In addition, after dose rates increased by more than 0.2 millirem/hour, the

resins were not changed. Consequently, general area radiation levels on the reactor

cavity floor increased from 0.4 millirem/hour to 6.0 millirem/hour. This violation was

documented in the licensees corrective action program as condition reports CR-GGNS-

2012-04288 and CR-GGNS-2012-12401. This issue is being treated as a non-cited

violation, consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV

05000416/2012005-05, Failure To Follow the Radiation Work Permit Requirements

During Reactor Cavity High Water Operations.

- 28 -

2RS04 Occupational Dose Assessment (71124.04)

a. Inspection Scope

This area was inspected to: (1) determine the accuracy and operability of personal

monitoring equipment; (2) determine the accuracy and effectiveness of the licensees

methods for determining total effective dose equivalent; and (3) ensure occupational

dose is appropriately monitored. The inspector used the requirements in

10 CFR Part 20, the technical specifications, and the licensees procedures required by

technical specifications as criteria for determining compliance. During the inspection,

the inspector interviewed licensee personnel, performed walkdowns of various portions

of the plant, and reviewed the following items:

External dosimetry accreditation, storage, issue, use, and processing of active

and passive dosimeters

The technical competency and adequacy of the licensees internal dosimetry

program

Adequacy of the dosimetry program for special dosimetry situations such as

declared pregnant workers, multiple dosimetry placement, and neutron dose

assessment

Audits, self-assessments, and corrective action documents related to dose

assessment since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in

Inspection Procedure 71124.04-05.

b. Findings

No findings were identified.

- 29 -

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

4OA1 Performance Indicator Verification (71151)

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the performance indicator data submitted by the

licensee for the third Quarter 2012 performance indicators for any obvious

inconsistencies prior to its public release in accordance with Inspection Manual

Chapter 0608, Performance Indicator Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index - Emergency ac Power System (MS06)

a. Inspection Scope

The inspectors sampled licensee submittals for the mitigating systems performance

index - emergency ac power system performance indicator for the period from the fourth

quarter 2011 through third quarter 2012. To determine the accuracy of the performance

indicator data reported during those periods, the inspectors used definitions and

guidance contained in NEI Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator

narrative logs, mitigating systems performance index derivation reports, issue reports,

event reports, and NRC integrated inspection reports for the period of October 2011

through September 2012 to validate the accuracy of the submittals. The inspectors

reviewed the mitigating systems performance index component risk coefficient to

determine if it had changed by more than 25 percent in value since the previous

inspection, and if so, that the change was in accordance with applicable NEI guidance.

The inspectors also reviewed the licensees condition report database to determine if

any problems had been identified with the performance indicator data collected or

transmitted for this indicator and none were identified. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of one mitigating systems performance index -

emergency ac power system sample as defined in Inspection Procedure 71151-05.

- 30 -

b. Findings

No findings were identified.

.3 Mitigating Systems Performance Index - High Pressure Injection Systems (MS07)

a. Inspection Scope

The inspectors sampled licensee submittals for the mitigating systems performance

index - high pressure injection systems performance indicator for the period from the

fourth quarter 2011 through third quarter 2012. To determine the accuracy of the

performance indicator data reported during those periods, the inspectors used definitions

and guidance contained in NEI Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator

narrative logs, issue reports, mitigating systems performance index derivation reports,

event reports, and NRC integrated inspection reports for the period of October 2011

through September 2012 to validate the accuracy of the submittals. The inspectors

reviewed the mitigating systems performance index component risk coefficient to

determine if it had changed by more than 25 percent in value since the previous

inspection, and if so, that the change was in accordance with applicable NEI guidance.

The inspectors also reviewed the licensees condition report database to determine if

any problems had been identified with the performance indicator data collected or

transmitted for this indicator and none were identified. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of one mitigating systems performance index -

high pressure injection system sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.4 Mitigating Systems Performance Index - Heat Removal System (MS08)

a. Inspection Scope

The inspectors sampled licensee submittals for the mitigating systems performance

index - heat removal system performance indicator for the period from the fourth quarter

2011 through third quarter 2012. To determine the accuracy of the performance indicator

data reported during those periods, the inspectors used definitions and guidance

contained in NEI Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6. The inspectors reviewed the licensees operator narrative logs,

issue reports, event reports, mitigating systems performance index derivation reports,

and NRC integrated inspection reports for the period of October 2011 through

September 2012 to validate the accuracy of the submittals. The inspectors reviewed the

mitigating systems performance index component risk coefficient to determine if it had

changed by more than 25 percent in value since the previous inspection, and if so, that

the change was in accordance with applicable NEI guidance. The inspectors also

- 31 -

reviewed the licensees condition report database to determine if any problems had been

identified with the performance indicator data collected or transmitted for this indicator

and none were identified. Specific documents reviewed are described in the attachment

to this report.

These activities constitute completion of one mitigating systems performance index -

heat removal system sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.5 Mitigating Systems Performance Index - Residual Heat Removal System (MS09)

a. Inspection Scope

The inspectors sampled licensee submittals for the mitigating systems performance

index - residual heat removal system performance indicator for the period from the fourth

quarter 2011 through third quarter 2012. To determine the accuracy of the performance

indicator data reported during those periods, the inspectors used definitions and

guidance contained in NEI Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator

narrative logs, issue reports, mitigating systems performance index derivation reports,

event reports, and NRC integrated inspection reports for the period of October 2011

through September 2012 to validate the accuracy of the submittals. The inspectors

reviewed the mitigating systems performance index component risk coefficient to

determine if it had changed by more than 25 percent in value since the previous

inspection, and if so, that the change was in accordance with applicable NEI guidance.

The inspectors also reviewed the licensees condition report database to determine if

any problems had been identified with the performance indicator data collected or

transmitted for this indicator and none were identified. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of one mitigating systems performance index -

residual heat removal system sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.6 Mitigating Systems Performance Index - Cooling Water Systems (MS10)

a. Inspection Scope

The inspectors sampled licensee submittals for the mitigating systems performance

index - cooling water systems performance indicator for the period from the fourth

quarter 2011 through third quarter 2012. To determine the accuracy of the performance

indicator data reported during those periods, the inspectors used definitions and

- 32 -

guidance contained in NEI Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator

narrative logs, issue reports, mitigating systems performance index derivation reports,

event reports, and NRC integrated inspection reports for the period of October 2011

through September 2012 to validate the accuracy of the submittals. The inspectors

reviewed the mitigating systems performance index component risk coefficient to

determine if it had changed by more than 25 percent in value since the previous

inspection, and if so, that the change was in accordance with applicable NEI guidance.

The inspectors also reviewed the licensees condition report database to determine if

any problems had been identified with the performance indicator data collected or

transmitted for this indicator and none were identified. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of one mitigating systems performance index -

cooling water system sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and

addressed. The inspectors reviewed attributes that included the complete and accurate

identification of the problem; the timely correction, commensurate with the safety

significance; the evaluation and disposition of performance issues, generic implications,

common causes, contributing factors, root causes, extent of condition reviews, and

previous occurrences reviews; and the classification, prioritization, focus, and timeliness

of corrective actions. Minor issues entered into the licensees corrective action program

because of the inspectors observations are included in the attached list of documents

reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings were identified.

- 33 -

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. The inspectors

accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status

monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees corrective action program and

associated documents to identify trends that could indicate the existence of a more

significant safety issue. The inspectors focused their review on repetitive equipment

issues, but also considered the results of daily corrective action item screening

discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human

performance results. The inspectors nominally considered the 6-month period of May

20, 2012, through November 20, 2012, although some examples expanded beyond

those dates where the scope of the trend warranted.

The inspectors also included issues documented outside the normal corrective action

program in major equipment problem lists, repetitive and/or rework maintenance lists,

departmental problem/challenges lists, system health reports, quality assurance

audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.

The inspectors compared and contrasted their results with the results contained in the

licensees corrective action program trending reports. Corrective actions associated with

a sample of the issues identified in the licensees trending reports were reviewed for

adequacy.

These activities constitute completion of one single semi-annual trend inspection sample

as defined in Inspection Procedure 71152-05.

b. Findings and Observations

No findings were identified.

The inspectors identified an increasing trend in condition reports identifying issues within

the work management process. The specific items documented in the condition reports

- 34 -

were reviewed by the inspectors, and it was determined that all were minor in nature.

The inspectors determined that the licensee had properly identified deficiencies in tagout

reviews, emergent work requests, work order impact statements and entered each issue

in the corrective action process. The work management issues have resulted in various

plant impacts, most notably an impact on resources due to repreforming work orders and

tagout reviews. The inspectors determined that although there was an abnormal

increase in work management issues, the licensee did appropriately address the issues

in the corrective action program.

.4 Selected Issue Follow-up Inspection: 4160 Vac Preventative Maintenance Procedures

a. Inspection Scope

The inspectors chose to review Condition Reports CR-GGN-2012-08885,

CR-GGN-2012-9035, and CR-GGN-2012-09111, which addressed programmatic

conditions associated with 4160 Vac breaker testing described as The associated PM,

07-S-12-61, Inspection of GE Magna Blast Circuit Breaker, does not have any specific

steps that would clean or inspect auxiliary contacts though section 7.1.4 requires a

general inspection for any physical damage. The inspectors reviewed the associated

corrective actions for CR-GGN-2011-08885, CR-GGN-2012-9035, and CR-GGN-2012-

09111. The inspectors also reviewed associated procedures and interviewed several

members of the involved licensee staff. Documents reviewed are listed in the

attachment.

These activities constitute completion of one in-depth problem identification and

resolution sample as defined in Inspection Procedure 71152-05.

b. Findings

No findings were identified.

.5 In-depth Review of Operator Workarounds

a. Inspection Scope

The inspectors evaluated the licensees implementation of their process used to identify,

document, track, and resolve operational challenges. Inspection activities included, but

were not limited to, a review of the cumulative effects of the operator workarounds,

operator burdens, control deficiencies, control room alarms and long standing danger

and caution tags on system availability and the potential for improper operation of the

system, for potential impacts on multiple systems, and on the ability of operators to

respond to plant transients or accidents. The inspectors performed a review of the

cumulative effects of operator workarounds, operator burdens, control deficiencies,

control room alarms and long standing danger and caution tags. The documents listed

in the attachment were reviewed to accomplish the objectives of the inspection

procedure. The inspectors reviewed current operational challenge records to determine

whether the licensee was identifying operator challenges at an appropriate threshold,

had entered them into their corrective action program, and had proposed or

- 35 -

implemented appropriate and timely corrective actions, which addressed each issue.

Reviews were conducted to determine if any operator challenge could increase the

possibility of an initiating event, if the challenge was contrary to training, required a

change from long-standing operational practices, or if it created the potential for

inappropriate compensatory actions. Additionally, the inspectors review two licensee

assessments of their process to determine if they were properly assessing the issues

and determining long term corrective actions to reduce the operator challenges. Daily

plant and equipment status logs, degraded instrument logs, and operator aids or tools

being used to compensate for material deficiencies were also assessed to identify any

potential sources of unidentified operator workarounds.

These activities constitute completion of one operator workarounds annual inspection

sample as defined in Inspection Procedure 71152.

b. Findings

No findings were identified.

4OA3 Followup of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) Licensee Event Report 05000416/2012-001-00: Surveillance Test Procedure

Inadequate to Meet the Requirements of Technical Specifications

a. Inspection Scope

On November 19, 2009, the licensee failed to ensure that Technical Specification (TS)

Surveillance Requirement (SR) 3.5.3.1 was met. The 2009 NRC Problem Identification

and Resolution (PI&R) Inspection identified a concern that the surveillance procedure

used to verify the reactor core isolation cooling (RCIC) system piping is filled with water

from the pump discharge valve to the injection valve was inadequate, in that it did not

have a basis (calculation) for the two-minute venting criterion and that there was no

visual means of confirming water flow through the vent line when performing venting of

the RCIC system. The 2009 PI&R inspection team documented the concern as a non-

cited violation in section 4OA2.5a of report 2009008. During the 2011 PI&R inspection,

the team reviewed the non-cited violation identified by the 2009 PI&R inspection and

determined that corrective actions were not taken in a timely enough manner to meet the

requirements of TS (SR) 3.5.3.1, which resulted in the RCIC system being inoperable for

a period of time in excess of TS allowance, which resulted in a condition prohibited by

TS. The licensee confirmed full compliance with TS SR 3.5.3.1 by performing ultrasonic

testing on February 5, 2010, which verified the piping was full of water.

The cause of the occurrence was an inadequate surveillance procedure acceptance

criterion, which resulted in the requirements of SR 3.5.3.1 not being met. The

contributing cause was the lack of technical rigor in evaluation of a potential inadequate

surveillance procedure. Corrective actions included using ultra sonic testing to verify the

RCIC system piping was full of water and revising RCIC surveillance procedures to

incorporate ultra sonic testing to verify the piping is full of water. Documents reviewed

as part of this inspection are listed in the attachment. The enforcement aspects of this

- 36 -

finding were discussed in NRC Inspection Report 05000416/2011006 in Section

4OA2.5a. This LER is closed.

b. Findings

No findings were identified.

.2 (Closed) Licensee Event Report 05000416/2012-002-00: Manual Reactor Scram Due to

a Steam Supply Motor Operated Valve Failure that Resulted in the Inability to Maintain

Reactor Water Level

a. Inspection Scope

On February 19, 2012, at 7:04 p.m., Grand Gulf Nuclear Station (GGNS) was in Mode 1

operating at approximately 22 percent power during a planned plant shutdown with the

reactor feed pump A secured when a manual reactor scram was initiated due to

decreasing reactor pressure vessel (RPV) water level. The cause of the event was a

combination of the isolating steam valve to the reactor feed pump B being out of

position, 90 percent closed, which isolates the main steam header from reactor feed

pump B and a planned power reduction. The power reduction resulted in the turbine

bypass valves (TBPV) opening as designed, then when the TBPVs reached 16 percent

open, reactor feed pump B began to decrease in speed. This resulted in a decreasing

level in the RPV. As level decreased, the control room supervisor directed a manual

scram be inserted prior to reaching the low level scram set point (+11.4 inches narrow

range). After the scram, reactor core isolation cooling (RCIC) was manually started to

inject water into the RPV and reactor feed pump A was restarted to restore and maintain

reactor water level. The appropriate off-normal event procedures were entered to

mitigate the transient with all systems responding as designed. All control rods inserted

to shut down the reactor.

The cause of the event was that equipment deficiencies preventing the high pressure

steam inlet valve to B RFPT from fully opening. Corrective actions included reactor water

level was restored and the plant was placed in a stable condition. The licensee

conducted troubleshooting of the steam supply valve and repaired it during the refueling

outage. Other contributing causes were evaluated and corrective actions were develop

to address these process issues. Documents reviewed as part of this inspection are

listed in the attachment. The enforcement aspects of this finding were discussed in NRC

Inspection Report 05000416/2012002 in Section 4OA3 and documented below. This

LER is closed.

b. Findings

Introduction. The inspectors identified a Green non-cited violation of 10 CFR 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, involving the

licensees failure to follow Procedure EN-LI-118, Root Cause Evaluation Process,

Revision 18, in that they failed to evaluate the risk significances and develop action

plans to address equipment identified during their extent-of-condition review for a post-

scram root-cause analysis.

- 37 -

Description. The inspectors reviewed Licensee Event Report 2012-002-00, Manual

Reactor Scram Due to a Steam Supply Motor Operated Valve Failure that Resulted in

the Inability to Maintain Reactor Water Level. The inspectors identified that the licensee

performed a root-cause analysis under Condition Report CR-GGN-2012-1842. In their

review of the root cause and associated corrective actions, the inspectors noted that

operations were directed by Corrective Actions 34 and 35 to perform an extent-of-

condition review of other systems to identify hidden or longstanding equipment issues

that pose a challenge to the safe operation of the plant. Although the operations

personnel identified numerous components such as valves and pumps in degraded state

that could affect safe plant operations, they did not properly perform Procedure

EN-LI-118, Attachment 9.7, in that they completed step one of evaluating and identifying

the similar components that were a cause of the original scram, but did not perform the

second step of determining the risk significance of these identified components and did

not develop action plans to resolve the degraded conditions.

The inspectors brought this to the attention of the licensee management, and they

reviewed the root cause and corrective actions from the condition report and came to the

same conclusions as the inspectors.

The licensee entered this issue in their corrective action program as Condition Report

CR-GGN-2012-11950. Their immediate corrective actions included assigning corrective

actions for operations personnel to properly evaluate the risk significance of the

identified components and perform appropriate corrective actions to correct the

degraded conditions.

Analysis. The licensees failure to properly determine risk significance and associated

action plans to correct degraded equipment that could challenge safe plant operation is

a performance deficiency. The performance deficiency is more than minor and is

therefore a finding because if left uncorrected, it would have the potential to lead to a

more significant safety concern. Specifically, the failure to take corrective actions to

correct degraded equipment has the potential to lead to initiating events resulting in plant

transients. Using NRC Inspection Manual Chapter 0609, Attachment 4, "Initial

Characterization of Findings," the inspectors determined that the issue affected the

Initiating Events Cornerstone. In accordance with NRC Inspection Manual Chapter

0609, Appendix A, The Significance Determination Process (SDP) for Findings at

Power, the inspectors determined that the issue has very low safety significance

(Green) because the finding did not cause a reactor trip or the loss of mitigation

equipment relied upon to transition the plant from the onset of the trip to a stable

shutdown condition. The inspectors determined that the apparent cause of this finding

was that when operations management directed operators to identify the degraded

equipment, they did not encourage those operators to comply with Procedure EN-LI-118.

Therefore, the finding has a cross-cutting aspect in the human performance area, work

practices component because the licensee did not define and effectively communicate

expectations regarding procedural compliance. H.4(b)

- 38 -

Enforcement. 10 CFR 50, Appendix B, Criterion V, states, in part, that activities affecting

quality shall be prescribed by and accomplished in accordance with documented

instructions, procedures, or drawings, of a type appropriate to the circumstances.

Procedure EN-LI-118, Root Cause Evaluation Process, Revision 18, Attachment 9.7,

requires the licensee to evaluate the previous problem for similar issues and determine

risk significances and associated action plans to resolve the degraded components

identified. Contrary to the above, on or before October 9, 2012, the licensee did not

evaluate a previous problem for similar issues and determine risk significances and

associated action plans. Specifically, although the licensee did properly evaluate and

identify similar components such as valves and pumps in a degraded condition, they did

not determine the risk significance of what they identified or develop action plans to

resolve the degraded components identified. As an immediate corrective action, the

licensee assigned corrective actions to operations personnel to properly evaluate the

risk significance of the identified components and develop action plans to correct the

degraded components. This violation is being treated as a non-cited violation (NCV),

consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety

significance (Green) with no actual safety consequence, and it was entered into the

licensees corrective action program as CR-GGN-2012-11950 to address recurrence:

NCV 05000416/2012005-06, Failure to Evaluate the Risk Significances and Develop

Action Plans to Address Equipment Identified During Extent of Condition Review for a

Post Scram Root Cause Analysis.

.3 (Closed) Licensee Event Report 05000416/2012-003-00: ESF Actuation Due to Division

III Bus Undervoltage following a Lighting Strike

a. Inspection Scope

On April 2, 2012, at 3:11 p.m. central daylight time (CDT) Grand Gulf Nuclear Station

was in mode 5 when a valid engineered safety feature (ESF) actuation for emergency

alternating current power to the division III 4160 volt bus occurred due to degraded

voltage. One of the two offsite 500 kilovolt offsite feeder breakers tripped open causing

a drop in grid voltage that resulted in a trip of normal ESF feeder for division III 4160 volt

bus. The high pressure core spray diesel generator automatically started and energized

the bus. The high pressure core spray system was not running at the time and no

emergency core cooling initiation occurred during this event. The technical specification

required power sources remained operable and in service during this event. The 500

kilovolt feeder was restored by the dispatcher at approximately 3:15 p.m. CDT.

The cause of the event was a lighting strike on the Franklin 500 kilovolt line. Entergy

transmission operation center reported at approximately 3:12 p.m., the Franklin extra

high voltage to Grand Gulf 500 kilovolt line tripped and locked out. The Franklin line in

one of three offsite power sources available to Grand Gulf. The fault was sensed by the

Grand Gulf line realying equipment and the fault was cleared by the dispatcher. Grand

Gulf personnel investigated the event and determined that all onsite equipment

performed as expected. Documents reviewed as part of this inspection are listed in the

attachment. This LER is closed.

- 39 -

b. Findings

No findings were identified.

.4 (Closed) Licensee Event Report 05000416/2012-004-00: Weld Defect Indication Found

in Residual Heat Removal System to Reactor Pressure Vessel Boundary Nozzle

a. Inspection Scope

On April 28, 2012, while the plant was in mode 4, shutdown for refueling outage 18,

ultrasonic testing was being performed on the nozzle weld N6B-KB, residual heat

removal/low pressure coolant injection nozzle to safe end weld. The ultrasonic

examination revealed an indication indicative of intergranular stress corrosion cracking.

The indication was evaluated by personnel and confirmed to be a weld defect. Inservice

Inspection relief request (RR-ISI-17; ML12124A245) to repair the weld was submitted to,

and approved by, the NRC (reference GTC 2012-00011). A full structural weld overlay

repair to the weld in accordance with ASME code requirements was completed on May

14, 2012. A post-weld ultrasonic test was completed satisfactorily on May 16, 2012.

The cause of the weld defect was determined to be the weld and butter were fabricated

with material that is susceptible to IGSCC type cracking. Actions were taken to mitigate

this condition through the stress relieving process of Induction Heating Stress

Improvement (IHSI). A contributing cause for the identification of this condition in 2012

(versus earlier) is the development and use of improved ultrasonic examination

procedures, techniques and training. Documents reviewed as part of this inspection are

listed in the attachment. This LER is closed.

b. Findings

No findings were identified.

.5 (Closed) Licensee Event Report 05000416/2012-005-00: Average Power Range

Monitors Inoperable in Excess of Technical Specification Allowances in Mode 2

a. Inspection Scope

On June 13, 2012, during startup activities for Unit 1 with the reactor in Mode 1

operating at approximately 12 -15 percent (%) power, the Average Power Range Monitor

(APRMs) were indicating a reactor power level lower than expected for the plant

condition. The licensee determined that during Refueling Outage 18 (RF18) the APRMs

were set to indicate flux lower than the actual power level. This resulted in the system

being inoperable during Mode 2 due to the APRM Neutron Flux High - Setdown scram

setpoint being outside of Technical Specification (TS) 3.3.1.1 Reactor Protection System

(RPS) Instrumentation limits. This condition existed when Mode 2 was initially entered

on June 6, 2012 until Mode 1 was entered on June 13, 2012. This condition was limited

to the Power Range Neutron Monitoring (PRNM) system. During startup in Mode 2, the

intermediate range monitors (IRM) and the high reactor pressure trip functions were

operable. Therefore, reactor power transients would have been mitigated by these

- 40 -

functions. The APRM Neutron Flux High - Setdown function is not directly credited in any

safety analyses, and this event did not adversely affect plant safety or the health and

safety of the public.

The apparent cause of this condition was a failure to identify differing operating

characteristics between the old system and the new system during the engineering

change process. The licensee had been entering the minimum gain for the old APRM

instruments, and did not evaluate this practice as part of the engineering change

process. The old instruments indicated much higher than actual power at low power

levels while the new instruments indicated closer to actual levels. As a result, when the

licensee continued to use the minimum gain setting, the new instruments indicated lower

than actual power. The licensee conducted an apparent cause evaluation and identified

other contributing causes and corrective actions. Documents reviewed as part of this

inspection are listed in the attachment. The enforcement aspects of this finding are

documented below. This LER is closed.

b. Findings

Introduction. The inspectors identified a Green non-cited violation of 10 CFR 50,

Appendix B, Criterion III, Design Control, involving the licensees failure to establish the

gain settings used on the power range neutron monitoring (PRNM) system in

accordance with design requirements. Specifically, prior to June 13, 2012, the licensee

used non-conservative gain settings on the average power range monitors (APRMs) and

local power range monitors (LPRMs) causing them to indicate flux lower than the actual

power level, which resulted in violations of Technical Specifications 3.0.4, 3.3.1.1, and

3.3.2.1.

Description. On June 13, 2012, during a reactor startup, the licensee discovered that

reactor power as indicated by the APRM neutron flux was significantly lower than the

apparent power as determined by the heat balance and other indications. The licensee

determined that actual power was approximately 12-15 percent while the APRMs

indicated 6.5 percent. The licensee immediately validated the heat balance inputs and

adjusted APRM and LPRM gains to correct the discrepancy. The licensee reported this

event in License Event Report (LER) 05000416/2012-005-00 as a violation of Technical

Specification 3.3.1.1 Reactor Protection System Instrumentation due to the APRM

Neutron Flux High - Setdown scram function being inoperable. The inspectors reviewed

the LER and concluded that the licensee also violated Technical Specification 3.0.4

because they entered Mode 2 with the required function inoperable and did not meet any

of the allowable exceptions. Furthermore, the inspectors noted that the Neutron Flux -

Upscale, Startup function of Technical Specification 3.3.2.1 Control Rod Block

Instrumentation was also inoperable.

The cause of the technical specification violations was that the licensee had entered

incorrect, non-conservative gains into the APRM and LPRM instruments. During

Refueling Outage 18, the licensee upgraded the PRNM system to a digital General

Electric Hitachi designed Nuclear Measurement and Control System (NUMAC) as part of

the extended power uprate (EPU). This involved replacing all of the APRM instruments

with a new design. The licensee also replaced forty LPRM detectors.

- 41 -

The licensee procedure for initial APRM gain setting directed setting the gain to the

minimum possible before instrument calibration, which is performed between 18 percent

and 21.8 percent reactor power. The apparent reason for this was that the old

instruments did not effectively discriminate gamma flux at low power, and therefore

indicated higher than actual values. The licensee used the minimum gain value to

prevent a rod withdrawal block prior to calibrating the instruments. The new instruments

are more effective at gamma discrimination at low power, and therefore indicate closer

to actual flux. The licensee had never established a basis for determining the initial gain

settings, did not re-evaluate the continued use of these settings during the design

change process, and did not modify the procedures to set a more conservative initial

gain setting. The licensee also discovered during their apparent cause evaluation that

the initial gain setting they used for the replacement LPRM detectors was incorrect. The

licensee had been using 3.000 as the default initial gain setting for uncalibrated LPRMs.

However, the vendor recommended default setting was 3.692. Therefore the forty

replaced LPRMs were providing a non-conservative signal to the APRMs. As a result of

the failure to use conservative gain settings on the LPRMs and APRMs, all APRMs

indicated approximately 40-50 percent of actual thermal power when the error was

discovered.

The APRMs are designed to indicate within tolerances and ensure protective functions

specified in the plant design documents. The inspectors determined that the licensee

had been using initial gain settings for both the LPRMs and APRMs that had not been

evaluated or analyzed to ensure these design requirements were being met. The

licensee carried over this practice when implementing their design change for the new

system instead of evaluating the settings for the new system.

The licensee entered this issue into their corrective action program as Condition Report

CR-GGN-2013-00177. The immediate corrective actions included adjusting gain settings

for their APRM instruments so they indicated actual core thermal power as determined

by the heat balance. The licensee also revised their neutron monitoring procedure to set

the initial gains for the APRMs to the maximum value to maintain conservative power

indication during future startups and changed their LPRM replacement procedure to use

the vendor specified initial gain setting of 3.692 prior to startup.

Analysis. The failure to ensure that the design basis was correctly translated into

specifications, drawings, procedures, and instructions was a performance deficiency.

The performance deficiency was more than minor because it affected the design control

attribute of the Mitigating Systems Cornerstone and impacted the cornerstone objective

to ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, the incorrect gain settings led

to a violation of technical specification 3.0.4 by rendering the APRM Neutron Flux High -

Setdown scram function and the Neutron Flux - Upscale, Startup control rod block

function inoperable prior to entry into Mode 2. In accordance with NRC Inspection

Manual Chapter 0609, Attachment 4, "Initial Characterization of Findings," the issue was

determined to affect the Mitigating Systems Cornerstone. In accordance with NRC

Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process

(SDP) for Findings at Power, the issue was determined to have very low safety

significance (Green) because although the finding affected a single reactor protection

- 42 -

system (RPS) trip signal to initiate a reactor scram, it did not affect the function of other

redundant trips or diverse methods of reactor shutdown, did not involve control

manipulations that unintentionally added positive reactivity, and did not result in a

mismanagement of reactivity by operators. This finding was not assigned a cross-cutting

aspect because the performance deficiency occurred in the past and is not reflective of

current licensee performance.

Enforcement. 10 CFR 50, Appendix B, Criterion III, requires, in part, that measures

shall be established to assure that the design basis is correctly translated into

procedures. Contrary to the above, prior to June 13, 2012, measures established by

the licensee did not assure that the design basis was correctly translated into

procedures. Specifically, those measure did not assure that the bases for the APRM

and LPRM gain settings were correctly translated into the licensees maintenance and

operating procedures. The licensees immediate actions were to set appropriate gain

settings for their APRM instruments and submit an LER for the violation of technical

specifications. This violation is being treated as an NCV, consistent with Section 2.3.2 of

the Enforcement Policy, because it was of very low safety significance (Green) and was

entered into the licensees corrective action program as CR-GGN-2013-00177 to

address recurrence NCV 05000416/2012005-07, Failure to Establish Gain Settings on

APRM and LPRM Instruments in Accordance with Design Requirements.

.6 (Closed) Licensee Event Report 05000416/2012-006-00: Special Nuclear Material

Inventory Discrepancy

a. Inspection Scope

On July 25, 2012, at 3:34 p.m. the licensee determined that a source range monitor

detector was not in its expected storage location. This met the reporting criteria in 10

CFR 72.74 and 10 CFR 74.11 as a loss of special nuclear material. The Source Range

Monitor (SRM) detector contained an estimated maximum activity of 0.187 microcuries,

which is equivalent to 0.00292 grams of all Special Nuclear Material (SNM) isotopes,

including U-235. This also met the reporting criteria in 10 CFR 20.2201 (a) (1) (ii) as a

loss of licensed material of a quantity greater than ten times that specified in Appendix C

to 10 CFR Part 20. According to special nuclear material (SNM) inventory sheets, the

SRM detector was expected to be stored in an SNM Item Control Area (ICA) on the 208

foot elevation of the Auxiliary building. However, during performance of the annual

physical inventory of SNM, the SRM detector could not be located. Subsequent

investigations concluded that the SRM was removed from the 208 foot elevation of the

Auxiliary building SNM ICA during clean up at the end of Refueling Outage 18, along

with other material that was stored in the area, and discarded as radioactive waste.

The inspector reviewed the licensee event report, NRC Event Notification 48133, and

the licensees corrective action reports, which documented this event and its causes.

The inspectors verified that the cause of the event was identified, radiological

consequences were assessed, and that corrective actions were reasonable. The

enforcement aspects of this violation are discussed in Section 4OA7 of this report. This

licensee event report is closed.

- 43 -

.7 (Closed) Licensee Event Report 05000416/2012-007-00: Standby Service Water

System Administratively Inoperable For A Period Longer Than Allowed By Technical

Specifications

a. Inspection Scope

On August 18, 1987, a 10 CFR 50.59 safety evaluation was performed for a change to

the Final Safety Analysis Report (FSAR) to relax methodology for single passive failures

of standby service water components. On July 19, 2012, with the plant in mode 1 at

approximately 100 percent power, during the inspectors reviewed FSAR change

NPEFSAR 87/0067 and determined prior NRC approval of the change was required.

This resulted in SSW being administratively inoperable for a period longer than allowed

by technical specifications due to relaxation of the passive failure methodology without

prior NRC approval. The licensee determined that the event posed no threat to public

health and safety as there had been no passive failures that had challenged operability.

The licensee implemented compensatory measures and they have submitted a request

to revise the SSW passive failure methodology to the NRC. Procedures are in place to

prevent recurrence.

The apparent cause for this issue is misapplication of industry documents that were

used for justification in the 10 CFR 50.59 safety evaluation due to lack of understanding

their applicability. The NUREG-0138 document did not specifically address single

passive failures for systems such as the standby service water system. These

documents were based on single passive failures of emergency core cooling systems.

Therefore, the licensee should have responded with a "YES" answer to questions 1 and

2 in the safety evaluation, which would have required prior NRC approval before these

changes were made to the GGNS FSAR. As stated above the licensee has submitted a

request to the NRC seeking approval of changes to the standby passive failure

methodology and has implement compensatory measures as an interim actions.

Documents reviewed as part of this inspection are listed in the attachment. The

enforcement aspects of this finding were discussed in NRC Inspection Report

05000416/2012008 in Section 1R21.2.3. This LER is closed.

b. Findings

No findings were identified.

.8 Reactor Scram Following a Phase A Unit Differential Relay Trip

a. Inspection Scope

On December 29, 2012 at approximately 12:18 a.m, the plant scrammed from 100

percent power. Upon responding to the site at 2:30 a.m., the inspectors learned that the

initial cause of the scram appeared to be the phase A unit differential relay tripping,

causing a generator lockout relay to trip, which resulted in a turbine trip and reactor

scram due to power being greater than 40 percent. The inspectors verified that all the

control rods were inserted and settled at position 00, and that reactor water level

- 44 -

lowered to approximately +7 inches narrow range (approximately 174 inches above top

of active fuel) and being maintained with reactor feedwater pump turbine A at

approximately +36 inches using startup level control. Reactor vessel pressure increased

on the trip from its nominal value of approximately 1035 psig to approximately 1116 psig,

and this caused the low-low level set to initiate as expected.

Additionally, the valve B21-F047A (automatic depressurization system safety relief

valve) lifted (normal mechanical lift pressure is 1113 psig), but the valve did not close

when it should have, and lowered reactor pressure vessel pressure to approximately 675

psig. The licensee entered their procedures to shut the valve, and when they took the

control switch to close, the valve closed. They also removed the fuses for this valve.

The licensee determined that the mechanical relief function for the valve was inoperable

but the safety relief function and automatic depressurization function were still operable.

The licensees maintained the plant in a hot shutdown condition until restart. The

inspectors reviewed the force outage list with plant staff and monitored troubleshooting

of plant issues. The licensee could not duplicate the condition with the phase A unit

differential relay through testing but elected to replace this relay prior to restart.

Additionally the licensee placed recording equipment on the various relays to monitor

response during startup.

Specific documents reviewed during this event follow-up are listed in the attachment.

These activities constitute completion of one event follow-up as defined in Inspection

Procedure 71153-05.

b. Findings

No findings were identified.

4OA5 Other Activities

.1 Power Uprate Related Inspection Activities: Licensee Actions for New or More Likely

Initiating Events (IP 71004)

a. Inspection Scope

During the inspection period, the inspectors verified that the licensee has taken all

required actions to address the effects of new or more probable initiating events as

stated in the license amendment, licensee commitments, or in the safety evaluation

report. The inspectors verified that the applicable Off-Normal Event Procedures,

Emergency Procedures, and Severe Accident Procedures had been revised to

incorporate the operational changes made due to the extended power uprate.

These activities constitute the completion of one inspection sample as defined in

Inspection Procedure 71004, Section 2.01.

- 45 -

b. Findings

No findings were identified.

.2 Power Uprate Related Inspection Activities: Completion of the Grand Gulf Nuclear

Station Extended Power Uprate Inspection Plan (IP 71004)

a. Inspection Scope

Inspection Procedure 71004, Power Uprate, requires that several samples be selected

for inspection. The samples selected were risk-informed and focused on items

concerning new integrated plant response characteristics, new operator procedures, and

plant safety during any required tests. The inspection effort is summarized below in

which each sample, applicable inspection procedure used and report number in which

the results were documented are provided.

Report No.: 05000416/2012002

Sample Description Procedure

Standby service water siphon line 71111.18

extension modification

Standby liquid control system (Boron-10 71111.18

enrichment change) modification

Steam dryer assembly welding processes 71111.08

and examinations

Review of Anticipated Transient Without a 71111.17

Scram Safety Evaluation

Flow Accelerated Corrosion monitoring and 71004

maintenance program

Report No.: 05000416/2012003

Sample Description Procedure

Power Range Neutron Monitoring 71111.18

modification

Replacement steam dryer 10CFR50.59 71111.18

Evaluation for current operating power limit

(3898 MWth)

Post modification test for ultimate heat sink 71111.19

siphon piping replacement and extension

Power Range Neutron Monitoring system 71111.19

post maintenance test after installation

- 46 -

Operator training and requalification 71111.11

program

Power Range Neutron Monitoring system 71111.22

functional test prior to startup

Report No.: 05000416/2012004

Sample Description Procedure

Power ascension testing as described in 71004

Appendix 9 of the EPU license amendment

Power Range Neutron Monitoring system 71111.22

calibration at EPU power (4408 MWth)

Operator actions during integrated plant 71004

evolutions

Operator training at EPU power (4408 71111.11

MWth)

Report No.: 05000416/2012005

Sample Description Procedure

Verify licensee has taken all necessary 71004

actions to address the effects of new or

more likely initiating events as stated in the

license amendment, licensee

commitments, or the safety evaluation

.3 Licensee Strike Contingency Plans (92709)

a. Inspection Scope

On October 1, 2012, Grand Gulf Nuclear Station initiated a lockout of bargaining unit

security officers due to their vote against the ratification of the contract that expired

September 30, 2012. In accordance with Inspection Procedure 92709, Licensee Strike

Contingency Plans, the resident inspectors monitored the need for compensatory

measures on a daily basis and reported adverse conditions to regional management and

security specialists for assessment. The residents also verified support from the local

authorities were adequate to ensure that personnel had unimpeded access to the plant,

delivery of support goods and offsite shipment of radioactive materials were

unencumbered, unimpeded access to medical care and ambulance services, and

unimpeded access to the local fire department to supplement the site fire fighting unit.

Security inspectors from the regional office provided oversight for the turn-over of the

bargaining security force to the contingency security force. The bargaining unit security

force voted to ratify a new contract on November 16, 2012. The resident inspectors

- 47 -

interviewed security management and along with regional security inspectors reviewed

the sites reintegration plan to ensure adequate security coverage would be maintained

during the reintegration process. Documents reviewed are listed in the attachments.

b. Findings

No findings were identified.

.4 (Closed) URI 05000416/2012008-07, Potential Internal Flooding Caused by Circulation

Water System Failure

a. Inspection Scope

On October 9, 2012, the NRC issued NRC Inspection Report 05000416/2012008, which

documented the results of an component design bases inspection conducted from

June 25, 2012, to September 10, 2012. In this inspection report, the NRC issued

Unresolved Item 05000416/2012008-07, Potential Internal Flooding Caused by

Circulation Water System Failure. This unresolved item was related to the licensees

evaluation of internal flooding events resulting from the postulated failure of circulating

water system components in the turbine building Calculation M6.3.051, Circulating

Water System-Calculate Revised Plant Flooding Elevations Due to Aux Cooling Tower,

Revision B. Specifically, the licensees design basis flooding analysis was based on a

steady state comparison of the volume of the circulating water system to the available

volume in the unit 1 turbine building, the canceled unit 2 turbine building, the radwaste

building, and control building. The inspectors determined this analysis failed to consider

the effects of large sliding doors, which are not watertight when closed, between the

unit 1 turbine building and the unit 2 turbine building and between the unit 1 turbine

building and radwaste building. It also failed to consider closed nonwatertight doors

between unit 1 turbine building and the control building. Additionally, it failed to include

the contribution of makeup flow from plant service water. With the assumption that the

doors are closed and wont fail, the inspectors questioned whether the flood level in the

unit 1 turbine building could increase to levels that would affect adjacent auxiliary

building and control building rooms that contain safety-related equipment.

During the component design bases inspection, the licensee performed

Calculation M6.3.051-001, Circulating Water Systems - Calculate Revised

Unit 1 Turbine Building and Unit 1 Control Building Flooding Elevations,

Revision 0, to correct deficiencies with the original internal flood analysis

(Condition Report CR-GGN-2012-09424). This analysis concluded that, with closed

doors and contribution of plant service water, the water level in the unit 1 turbine building

would increase, but the increase would not affect safety-related equipment in the

adjacent auxiliary and control building rooms. Although the analysis concluded that

plant protection from internal floods would not be adversely affected, the inspectors

disagreed with the assumption for flowrate from a postulated expansion joint failure in

the circulating water system. The calculation used the methodology of NRC Branch

Technical Position MEB 3-1 to predict the maximum flow from a failed circulating water

system expansion joint. Applying the MEB 3-1 methodology to the 10-foot diameter

expansion joint resulted in a postulated crack of 5-feet long and 1-inch wide. This crack

- 48 -

resulted in a calculated leak rate of approximately 15,500 gallons per minute. The

inspectors questioned the applicability of NRC Branch Technical Position MEB 3-1 to

nonsafety-related expansion joints and whether the crack leak rate should be

significantly higher if a gross failure was assumed in the updated final safety analysis

report. The inspectors discussed this design and licensing basis issue with NRC staff in

the Office of Nuclear Reactor Regulation. Due to complexity of establishing the

appropriate design and licensing bases for this issue, this item was considered

unresolved pending further NRC review to determine if a finding existed.

On November 15, 2012, the inspectors completed an internal flooding inspection, as

documented in Section 1R06 of this report. During the inspection, the inspectors toured

the circulating water system, including the circulating water pumps, from the cooling

tower to the unit 1 condenser. The inspection included a visual inspection of the doors

connecting the unit 1 turbine building to adjacent buildings, including complete

inspection of the flood barriers connecting the unit 1 turbine building to the auxiliary

building.

Additionally, during this inspection, the inspector requested the licensee perform an

internal flood analysis assuming the expansion joint failure leak rate was

290,000 gallons per minute. This represented a complete failure of the expansion joint

and runout flow of the circulating water system pumps. This analysis concluded that the

water level in the unit 1 turbine building would increase, but the increase would not affect

safety-related equipment in the adjacent auxiliary and control building rooms.

From the review, the inspectors determined that the auxiliary building flood barriers

would mitigate affects of an internal flood. Additionally, the inspectors determined that it

is very unlikely that a failure of the expansion joint would discharge the entire volume of

water of the circulating water system assumed in the internal flood analysis based on the

configuration and operation of the circulating water system. That is, the circulating water

system is an open system; when the system loses vacuum, the deep draft pumps would

shut down leaving a large water volume in the circulating water system basin and only

contents in the circulating water system pipe would drain through the failed expansion

joint.

Since the inspectors confirmed that safety-related equipment would not be affected,

assuming the maximum expansion joint failure leak rate and flood barriers would protect

the auxiliary building, the inspectors did not identify a finding. Therefore, Unresolved

Item 05000416/2012008-07, Potential Internal Flooding Caused by Circulation Water

System Failure, is closed.

b. Findings

No findings were identified.

.5 Temporary Instruction 2515/187 - Inspection Near Term Task Force Recommendation

2.3 Flooding Walkdowns

- 49 -

a. Inspection Scope

Inspectors verified that the licensees walkdown packages, WP1, WP2, WP6, and WP7

contained the elements as specified in NEI 12-07 Walkdown Guidance document. The

inspectors accompanied the licensee on their walkdown of the plant yard topography

inside the protected area and the safety related switchgear room on the 111 ft. elevation

in the control building and verified that the licensee confirmed the following flood

protection features:

Visual inspection of the flood protection feature was performed if the flood

protection feature was relevant. External visual inspection for indications of

degradation that would prevent its credited function from being performed was

performed

Critical SSC dimensions

Available physical margin, where applicable, was determined

Flood protection feature functionality was determined using either visual

observation or by review of other documents

The inspectors independently performed their walkdown and verified that the following

flood protection features were in place:

Plant yard grade at the 133 ft. elevation of the control building was such that

water would be shed away from the building

Staged sandbags were properly stored and in good material condition

Reasonable simulation building sandbag flood barrier

The inspectors verified that noncompliances with current licensing requirements and

issues identified in accordance with the 10 CFR 50.54(f) letter, Item 2.g of Enclosure 4,

were entered into the licensees corrective action program. In addition, issues identified

in response to Item 2.g that could challenge risk significant equipment and the licensees

ability to mitigate the consequences will be subject to additional NRC evaluation.

b. Findings

No NRC-identified or self-revealing findings were identified.

.6 Temporary Instruction 2515/188 - Inspection of Near-Term Task Force

Recommendation 2.3 Seismic Walkdowns

The inspectors accompanied the licensee on their seismic walkdowns of the following

areas and equipment:

- 50 -

Date Building Elevation Area Equipment

09/18/2012 Diesel Generator 136 ft 1D308 Control Panel H13P401

Building

10/05/2012 Auxiliary Building 93 ft 1A106 E12B002B

10/09/2012 Control Building 189 ft OC703 Control Panel H13P669

10/09/2012 Control Building 189 ft OC703 E51N602A

The inspectors verified that the licensee confirmed that the following seismic features

associated with listed equipment were free of potential adverse seismic conditions such

as:

Anchorage was free of bent, broken, missing, or loose hardware

Anchorage was free of corrosion that is more than mild surface oxidation

Anchorage was free of visible cracks in the concrete near the anchors

Anchorage configuration was consistent with plant documentation

SSCs will not be damaged from impact by nearby equipment of structures

Overhead equipment, distribution systems, ceiling tiles and lighting, and masonry

block walls are secure and not likely to collapse onto the equipment

Attached lines have adequate flexibility to avoid damage

The area appears to be free of potentially adverse seismic interactions that could

cause a fire in the area

The area appears to be free of potentially adverse seismic interactions

associated with housekeeping practices, storage of portable equipment, and

temporary installations (e.g. scaffolding, lead shielding)

The inspectors independently performed their walkdown and verified that the equipment

and areas listed in Table 2 were free of potential adverse seismic conditions as

described above.

- 51 -

Date Building Elevation Area Equipment

10/18/2012 SSW Pump Building 133 ft 2M110 Y47N005B

11/28/2012 Auxiliary Building 93 ft 1A104 E51F046

Observations made during the walkdown that could not be determined to be acceptable

were entered into the licensees corrective action program for evaluation.

Additionally, inspectors verified that items that could allow the spent fuel pool to drain

down rapidly were added to the SWEL and these items were walked down by the

licensee.

b. Findings

No NRC-identified findings or self-revealing findings were identified.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On January 17, 2013, the inspectors presented the inspection results to Mr. Kevin Mulligan, Site

Vice President of Operations, and other members of the licensee staff. The licensee

acknowledged the issues presented. The inspector asked the licensee whether any materials

examined during the inspection should be considered proprietary. No proprietary information

was identified.

On December 3, 2012, the inspector presented the results of the radiation safety inspection to

Ms. C. Perino, Director of Nuclear Safety Assurance, and other members of the licensee staff.

The licensee acknowledged the issues presented. The inspector asked the licensee whether

any materials examined during the inspection should be considered proprietary. No proprietary

information was identified.

4OA7 Licensee-Identified Violations

The following violation of very low security significance (Green) was identified by the licensee

and is a violation of NRC requirements which met the criteria of NRC Enforcement Policy for

being dispositioned as a non-cited violation.

10 CFR 74.19 requires, in part, that each licensee keep records of inventory including location,

transfer, and disposal of all special nuclear material and conduct an annual physical inventory of

all special nuclear material in its possession. Contrary to the above, before July 25, 2012, the

licensee did not keep records of inventory including location, transfer, and disposal of all special

nuclear material, in that on that date and after completing an inventory and records review of

SNM pursuant to the material control and accounting program, licensee reactor engineers

declared a source range monitor (SRM) detector lost. Specifically, SRM with serial number

1OF007J5 was not in its expected storage location. Using Manual Chapter 0609, Appendix D,

- 52 -

Public Radiation Safety Significance Determination Process, the inspectors determined that

this finding had very low safety significance (Green) because it resulted in no dose to a member

of the public in the restricted area, controlled area or the unrestricted area.

- 53 -

Attachment 1: SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Dorsey, Security Manager

H. Farris, Assistant Operations Manager

J. Gerard, Interim Operations Manager

J. Giles, Manager, Training

M. Krupa, Director, Major Projects

C. Justiss, Licensing

C. Lewis, Manager, Emergency Preparedness

E. Mason, Auditor, Quality Assurance

J. Miller, General Plant Manager

R. Miller, Manager, Radiation Protection

K. Mulligan, Site Vice President Operations

L. Patterson, Manager, Program Engineering

C. Perino, Director, Nuclear Safety Assurance

J. Richardson, Director, Power Upgrade Project

R. Scarbrough, Specialist and Lead Offsite Liaison, Licensing

J. Seiter, Acting Manager, Licensing

J. Shaw, Manager, System Engineering

T. Thurmon, Supervisor, Design Engineering-Mechanical

T. Trichell, Manager, Radiation Protection

D. Wiles, Engineering Director

E. Wright, Supervisor, ALARA

NRC Personnel

None

A1-1 Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000416/2012005-01 NCV Failure to Make Timely Corrective Actions to Repair the Degraded

Auxiliary Building Water Intrusion Barrier (Section 1R12.b.1)05000416/2012005-02 NCV Failure to Adequately Monitor the Condition of the Auxiliary

Building Water Intrusion Barrier (Section (1R12.b.2)05000416/2012005-03 NCV Failure to Implement Adequate Procedure Instructions to Perform

Preventive Maintenance Requiring the Periodic Replacement of

the Control Relays in GE Magne Blast Circuit Breakers (Section

1R20.b)05000416/2012005-04 FIN Failure to Adequately Plan and Control Work Activities to Maintain

ALARA (Section 2RS02.b.1)05000416/2012005-05 NCV Failure To Follow the Radiation Work Permit Requirements During

Reactor Cavity High Water Operations (Section 2RS02.b.2)05000416/2012005-06 NCV Failure to Evaluate the Risk Significances and Develop Action

Plans to Address Equipment Identified During Extent of Condition

Review for a Post Scram Root Cause Analysis (Section 4A03.2.b)05000416/2012005-07 NCV Failure to Establish Gain Settings on APRM and LPRM

Instruments in Accordance with Design Requirements (Section

4A03.5.b)

TI 2515/187 Inspection Near Term Task Force Recommendation 2.3 Flooding

Walkdowns (Section 4OA5.5)

TI 2515/188 Inspection of Near-Term Task Force Recommendation 2.3

Seismic Walkdowns (Section 4OA5.6)

Closed

05000416/2012008-07 URI Potential Internal Flooding Caused by Circulation Water System

Failure (Section 4OA5.4)

05000416/2012-001-00 LER Surveillance Test Procedure Inadequate to Meet the

Requirements of Technical Specifications (Section 4OA3.1)

05000416/2012-002-00 LER Manual Reactor Scram Due to a Steam Supply Motor Operated

Valve Failure that Resulted in the Inability to Maintain Reactor

Water Level (Section 4OA3.2)

05000416/2012-003-00 LER ESF Actuation Due to Division III Bus Undervoltage following a

Lighting Strike (Section 4OA3.3)

05000416/2012-004-00 LER Weld Defect Indication Found in Residual Heat Removal System

to Reactor Pressure Vessel Boundary Nozzle (Section 4OA3.4)

A1-2

Closed

05000416/2012-005-00 LER Average Power Range Monitors Inoperable in Excess of

Technical Specification Allowances in Mode 2 (Section 4OA3.5)

05000416/2012-006-00 LER Special Nuclear Material Inventory Discrepancy (Section

4OA3.6)

05000416/2012-007-00 LER Standby Service Water System Administratively Inoperable For A

Period Longer Than Allowed By Technical Specifications

(Section 4OA3.7)

A1-3

LIST OF DOCUMENTS REVIEWED

Section 1R04: Equipment Alignment

PROCEDURE

NUMBER TITLE REVISION

04-1-01-P75-1 Standby Diesel Generator System 96

04-1-01-P41-1 Standby Service Water System 136

04-1-01-E12-1 System Operating Instruction, Residual Heat Removal 142

System

DRAWINGS

NUMBER TITLE REVISION

M-1085D Residual Heat Removal System 4

OTHER DOCUMENTS

NUMBER TITLE DATE

System Health Report E12 Residual Heat Removal November

16, 2012

CONDITION REPORTS

CR-GGN-2005-03708 CR-GGN-2005-03838 CR-GGN-2005-05026

CR-GGN-2005-05042 CR-GGN-2012-05501 CR-GGN-2012-10989

CR-GGN-2012-06866 CR-GGN-2012-09577 CR-GGN-2012-11077

CR-GGN-2012-07028 CR-GGN-2012-09842 CR-GGN-2012-11081

CR-GGN-2012-07030 CR-GGN-2012-10054 CR-GGN-2012-11126

CR-GGN-2012-07342 CR-GGN-2012-10055 CR-GGN-2012-11265

CR-GGN-2012-07602 CR-GGN-2012-10365 CR-GGN-2012-11441

CR-GGN-2012-07633 CR-GGN-2012-10372 CR-GGN-2012-11511

CR-GGN-2012-07738 CR-GGN-2012-10377 CR-GGN-2012-11513

CR-GGN-2012-07739 CR-GGN-2012-10404 CR-GGN-2012-11514

CR-GGN-2012-07792 CR-GGN-2012-10406 CR-GGN-2012-11516

CR-GGN-2012-08733 CR-GGN-2012-10447 CR-GGN-2012-11537

CR-GGN-2012-08896 CR-GGN-2012-10461 CR-GGN-2012-11581

A1-4

CONDITION REPORTS

CR-GGN-2012-08906 CR-GGN-2012-10556 CR-GGN-2012-11784

CR-GGN-2012-09028 CR-GGN-2012-10584 CR-GGN-2012-11785

CR-GGN-2012-09257 CR-GGN-2012-10603 CR-GGN-2012-11968

CR-GGN-2012-09309 CR-GGN-2012-10617 CR-GGN-2012-11987

CR-GGN-2012-09493 CR-GGN-2012-10675 CR-GGN-2012-11991

CR-GGN-2012-09513 CR-GGN-2012-10944 CR-GGN-2012-11993

CR-GGN-2012-09535 CR-GGN-2012-09380 CR-GGN-2012-11362

CR-GGN-2012-06676 CR-GGN-2012-09494 CR-GGN-2012-11365

CR-GGN-2012-06981 CR-GGN-2012-09699 CR-GGN-2012-11445

CR-GGN-2012-07273 CR-GGN-2012-09825 CR-GGN-2012-11487

CR-GGN-2012-07400 CR-GGN-2012-09840 CR-GGN-2012-11644

CR-GGN-2012-07891 CR-GGN-2012-09855 CR-GGN-2012-11820

CR-GGN-2012-07961 CR-GGN-2012-09889 CR-GGN-2012-11931

CR-GGN-2012-08019 CR-GGN-2012-09989 CR-GGN-2012-11936

CR-GGN-2012-08599 CR-GGN-2012-10000 CR-GGN-2012-11941

CR-GGN-2012-08621 CR-GGN-2012-10097 CR-GGN-2012-11947

CR-GGN-2012-08649 CR-GGN-2012-10548 CR-GGN-2012-11949

CR-GGN-2012-08651 CR-GGN-2012-10558 CR-GGN-2012-11951

CR-GGN-2012-08833 CR-GGN-2012-10574 CR-GGN-2012-11952

CR-GGN-2012-08899 CR-GGN-2012-10797 CR-GGN-2012-11953

CR-GGN-2012-09022 CR-GGN-2012-10882 CR-GGN-2012-11955

CR-GGN-2012-09033 CR-GGN-2012-11184 CR-GGN-2012-11977

CR-GGN-2012-09034 CR-GGN-2012-11272 CR-GGN-2012-11981

CR-GGN-2012-09107 CR-GGN-2012-11337 CR-GGN-2012-11982

Section 1R05: Fire Protection

PROCEDURES

NUMBER TITLE REVISION

Fire Pre Plan C- Upper Relay Room - Unit 1 Area 25A

17

A1-5

Section 1R05: Fire Protection

PROCEDURES

NUMBER TITLE REVISION

04-1-01-P64-3 Fire Protection Cardox System 26

GGNS MS-55 GGNS Mechanical Standard GGNS TRM Required Fire 0

Rated Floor, Walls & Ceilings

Fire Pre-Plan SSW Pump House and Valve Room, Room 1M110-SSW A 1

SSW-01 Pump House Room 1M112-SSW A Valve Room

Fire Pre-Plan DIV I Diesel Generator Room 1D302, Area 12, Elevation 133 5

DG-02

Fire Pre-Plan A- RCIC Pump Room - 1A104 1

03

OTHER DOCUMENTS

NUMBER TITLE DATE

2012-08 Transient Combustible Evaluation

9A.5.64 GG UFSAR Fire Area 64

9A.5.60.1 GG UFSAR Fire Area 60

Chemetron Fire Systems Manual January 8,

1979

9A.5.2.4 Fire Zone 1A104: RCIC Room, Elev. 93 0

DRAWINGS

NUMBER TITLE REVISION

A-629 Unit I and Common Buildings Fire Protection Misc. Notes and 0

Details

E-0965 Raceway Plan Water Treatment Building El. 1330 and 7

STDBY Water Pump HS Basin A & B Fire and Smoke

Detection System Units I & II

CALCULATION

NUMBER TITLE DATE

MC-QSP64- Fire Zone Yard/Fire Area 59 June 13,

86058 2001

A1-6

CONDITION REPORTS

CR-GGN-2012-11435 CR-GGN-2009-05026

Section 1R06: Flood Protection Measures

PROCEDURES

NUMBER TITLE REVISION

05-1-02-VI-1 Off-Normal Event Procedure Flooding 109

04-1-02-1H13-P680- Alarm Response Instruction, Turbine Building E 100

8A1-C1 Floor Drain Sump Level Hi-Hi

04-1-02-1H13-P680- Alarm Response Instruction, Turbine Building W 100

8A1-B1 Equipment Drain Sump Level Hi-Hi

04-1-02-1H13-P680- Alarm Response Instruction, Turbine Building E 100

8A1-A1 Equipment Drain Sump Level Hi-Hi

04-1-02-1H13-P680- Alarm Response Instruction, Turbine Building W 100

8A1-D1 Floor Drain Sump Level Hi-Hi

04-1-02-1H13-P870- Alarm Response Instruction, Circulating Water 113

6A-G1 Expansion Joint Seal Level Hi

CALCULATIONS

NUMBER TITLE REVISION

M6.3.051 Circulating Water System - Calculate Revised Plant Flooding B

Elevations Due to the Aux Cooling Tower

M6.3.043 Circulating Water System - Calculate Water Volume of C

Circulating Water System

A1-7

CALCULATIONS

NUMBER TITLE REVISION

M6.3.051-001 Circulating Water Systems - Calculate Revised Unit 1 0

Turbine Building and Unit 1 Control Building Flooding

Elevations

DRAWINGS

NUMBER TITLE REVISION

C-1706C Unit 1 & 2 Circulating Water System Circulating Water 11

Piping Sections and Details

M154.0- Garlock Style 204 & 204HP Expansion Joints 1

N1N71G521A-

1.2-006

M-1059A P&I Diagram, Circulation Water System 41

M-1059B P&I Diagram, Circulating Water System, Unit 1 18

SFD-1059 System Flow Diagram, Circulating Water System, Unit 1 2

A-0010 Units 1 & 2 General Floor Plan, Fl. Plan at El. 93-0 & 10

103-0

A-0011 Units 1 & 2 Gen. Fl. Plan. - Fl. Plan at El. 111-0, 113- 8

0, 118-0, & 119-0

E-1152-033 Schematic Diagram, Circulating Water System, Main 14

Control Room Annunciation, Unit 1

ENGINEERING CHANGES

NUMBER TITLE REVISION

A1-8

ENGINEERING CHANGES

NUMBER TITLE REVISION

EC 38959 Calculate Revised Unit 1 Turbine Building and Unit 1 0

Control Building Flooding Elevations

VENDOR DOCUMENTS

NUMBER TITLE REVISION

9645-A-021.0 Bechtel Material Requisition - Watertight Doors 8

WORK ORDERS

WO 52306120 01 WO 52323476 01 WO 52323703 01

CONDITION REPORTS

CR-GGN-2012-09424 CR-GGN-2012-12448 CR-GGN-2012-12449

Section 1R11: Licensed Operator Requalification Program

PROCEDURES

NUMBER TITLE REVISION

03-1-01-2 Integrated Operating Instruction Power Operations 152

EN-RE-215 Reactivity Maneuver Plan (BWR) 1

EN-RE-215 Reactivity Maneuver Plan 1

OTHER DOCUMENTS

NUMBER TITLE REVISION /

DATE

2012 Cycle 6 Licensed Operator Requal Simulator Training

Plan Simulator Differences

GSMS-LOR- LOR Training APRM Downscale/Loss of Condenser 18

WEX17 Vacuum/LOCA/Degraded ECCS (EP-2, EP-3)

A1-9

OTHER DOCUMENTS

NUMBER TITLE REVISION /

DATE

Grand Gulf Cycle Periodic Log November

19 20, 2012

Section 1R12: Maintenance Effectiveness

PROCEDURES

NUMBER TITLE REVISION /

DATE

GGNS-C-399.0 Maintenance Rule Inspection of Structures, Tanks, and 9

Transformers Inspections

EN-DC-204 Maintenance Rule Scope and Basis 2

EN-DC-150 Condition Monitoring of Maintenance Rule Structures 2

EN-DC-203 Maintenance Rule Program 1

EN-DC-205 Maintenance Rule Monitoring 4

EN-DC-206 Maintenance Rule (a)(1) Process 1

OTHER DOCUMENTS

NUMBER TITLE REVISION /

DATE

EQ04.10 9kV Power Cable 1

ER-GG-2005- Evaluate Water Inleakage into the Enclosure Bldg. 0

0144-000

GGNS-96-0075 Assessment of Grand Gulf Compliance with the Guidelines of 2

NEI 96-03, Rev. D and the Maintenance Rule for Monitoring

the Condition of Structures

EN-DC-205, Maintenance Rule Functional Failure Evaluation, CR-GGN- October 5,

Attachment 9.1 2012-08921 CA 00051 2012

CONDITION REPORTS

CR-GGN-2004-01732 CR-GGN-2005-01165 CR-GGN-2005-02254

CR-GGN-2007-05125 CR-GGN-2007-05143 CR-GGN-2008-00828

CR-GGN-2010-07623 CR-GGN-2010-08332 CR-GGN-2012-11767

A1-10

CONDITION REPORTS

CR-GGN-2012-11740 CR-GGN-1997-00841 CR-GGN-2005-01294

CR-GGN-2009-01302 CR-GGN-2009-01630 CR-GGN-2010-00863

CR-GGN-2011-00360 CR-GGN-2011-01595 CR-GGN-2012-10323

CR-GGN-2011-00403 CR-GGN-2012-00525 CR-GGN-2012-07736

CR-GGN-2011-00749 CR-GGN-2012-00827 CR-GGN-2012-07829

CR-GGN-2011-00789 CR-GGN-2012-01486 CR-GGN-2012-07832

CR-GGN-2011-00791 CR-GGN-2012-03280 CR-GGN-2012-08225

CR-GGN-2011-00819 CR-GGN-2012-03839 CR-GGN-2012-08584

CR-GGN-2011-00820 CR-GGN-2012-04274 CR-GGN-2012-08625

CR-GGN-2011-00850 CR-GGN-2012-04292 CR-GGN-2012-08742

CR-GGN-2011-00985 CR-GGN-2012-04419 CR-GGN-2012-08897

CR-GGN-2011-01306 CR-GGN-2012-04437 CR-GGN-2012-09087

CR-GGN-2011-01710 CR-GGN-2012-04478 CR-GGN-2012-09273

CR-GGN-2011-01942 CR-GGN-2012-04584 CR-GGN-2012-09291

CR-GGN-2011-02393 CR-GGN-2012-04668 CR-GGN-2012-09510

CR-GGN-2011-03391 CR-GGN-2012-04773 CR-GGN-2012-09671

CR-GGN-2011-04582 CR-GGN-2012-04900 CR-GGN-2012-09785

CR-GGN-2011-05213 CR-GGN-2012-05083 CR-GGN-2012-10305

CR-GGN-2011-05446 CR-GGN-2012-05304 CR-GGN-2012-11309

CR-GGN-2011-05808 CR-GGN-2012-05501 CR-GGN-2012-11311

CR-GGN-2011-06528 CR-GGN-2012-05550 CR-GGN-2012-11312

CR-GGN-2011-06563 CR-GGN-2012-05557 CR-GGN-2012-11313

CR-GGN-2011-06972 CR-GGN-2012-05654 CR-GGN-2012-11315

CR-GGN-2011-07724 CR-GGN-2012-05820 CR-GGN-2012-11328

CR-GGN-2011-08175 CR-GGN-2012-05839 CR-GGN-2012-11415

CR-GGN-2011-08187 CR-GGN-2012-05846 CR-GGN-2012-11611

A1-11

CONDITION REPORTS

CR-GGN-2011-08198 CR-GGN-2012-05949 CR-GGN-2012-11755

CR-GGN-2011-09249 CR-GGN-2012-05973 CR-GGN-2012-12098

CR-GGN-2012-00038 CR-GGN-2012-06021 CR-GGN-2012-12391

CR-GGN-2012-00148 CR-GGN-2012-06132 CR-GGN-2012-06265

CR-GGN-2011-03391 CR-GGN-2012-00303 CR-GGN-2011-00070

CR-GGN-2010-00501 CR-GGN-2011-02621 CR-GGN-2012-01222

CR-GGN-2010-00690 CR-GGN-2011-02781 CR-GGN-2012-01541

CR-GGN-2010-00869 CR-GGN-2011-03103 CR-GGN-2012-03080

CR-GGN-2010-00895 CR-GGN-2011-03370 CR-GGN-2012-03278

CR-GGN-2010-01039 CR-GGN-2011-03394 CR-GGN-2012-03289

CR-GGN-2010-01381 CR-GGN-2011-03437 CR-GGN-2012-03290

CR-GGN-2010-01608 CR-GGN-2011-03804 CR-GGN-2012-03988

CR-GGN-2010-01646 CR-GGN-2011-04596 CR-GGN-2012-04241

CR-GGN-2010-01935 CR-GGN-2011-05352 CR-GGN-2012-04808

CR-GGN-2010-01964 CR-GGN-2011-06275 CR-GGN-2012-05074

CR-GGN-2010-02111 CR-GGN-2011-06290 CR-GGN-2012-05381

CR-GGN-2010-02304 CR-GGN-2011-08150 CR-GGN-2012-05659

CR-GGN-2010-02320 CR-GGN-2011-08617 CR-GGN-2012-05958

CR-GGN-2010-02587 CR-GGN-2011-08683 CR-GGN-2012-08069

CR-GGN-2010-02679 CR-GGN-2011-08806 CR-GGN-2012-09008

CR-GGN-2010-03097 CR-GGN-2011-08860 CR-GGN-2012-10348

CR-GGN-2010-04544 CR-GGN-2011-08986 CR-GGN-2012-10937

CR-GGN-2010-04920 CR-GGN-2011-08987 CR-GGN-2012-11224

CR-GGN-2010-06589 CR-GGN-2011-09170 CR-GGN-2012-11262

CR-GGN-2010-07439 CR-GGN-2011-09335 CR-GGN-2012-11333

CR-GGN-2010-08449 CR-GGN-2012-00498 CR-GGN-2012-11390

A1-12

CONDITION REPORTS

CR-GGN-2010-08534 CR-GGN-2012-00538 CR-GGN-2012-12323

CR-GGN-2010-08654 CR-GGN-2012-00623 CR-GGN-2012-12324

CR-GGN-2011-00226 CR-GGN-2012-00653 CR-GGN-2012-01176

CR-GGN-2011-00710 CR-GGN-2012-00708 CR-GGN-2011-02441

CR-GGN-2011-00795 CR-GGN-2012-00791 CR-GGN-2011-02254

CR-GGN-2011-01077 CR-GGN-2012-01071 CR-GGN-2012-01142

CR-GGN-2011-01534 CR-GGN-2012-01126 CR-GGN-2012-01160

CR-GGN-2012-01176 CR-GGN-2012-01222 CR-GGN-2012-12323

CR-GGN-2012-12324 CR-GGN-2012-00303 CR-GGN-2012-11408

CR-GGN-2012-12286

WORK ORDERS

WO 68420 WO 52266186

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

PROCEDURES

NUMBER TITLE REVISION /

DATE

02-S-01-17 Control of Limiting Conditions for Operation 123

EN-WM-101 Online Emergent Work Add/Delete Approval Form November 1,

2012

07-S-02-300 Fuel and Core Component Movement Control 125

07-S-05-300 Control and Use of Cranes and Hoists 113

EN-MA-119 Material Handling Program 13

05-1-02-V-12 Off-Normal Event Procedure, Condensate/Reactor Water 25

High Conductivity

EN-WM-101 Attachment 9.1 Online Emergent Work Add/Delete Approval 9

Form, WO 52313215

01-S-18-6, Risk Assessment of Maintenance Activities 119

Attachment VI

02-S-01-41 On Line Risk Assessment 7

A1-13

OTHER DOCUMENTS

NUMBER TITLE DATE

LCOTR No.:1-TS-12-0290

LCOTR No.:1-TS-12-0228

LCOTR No.:1-TS-12-0261

Shutdown Condition 1, Mode: 4, State: Cold S/D, Fuel December 9,

Status: Fueled 2012

9:34 pm

Shutdown Condition 1, Mode: 4, State: Cold S/D, Fuel December

Status: Fueled 10, 2012

7 am

Shutdown Condition 1, Mode: 4, State: Cold S/D, Fuel December

Status: Fueled 10, 2012

10:56 am

Shutdown Condition 1, Mode: 4, State: Cold S/D, Fuel December

Status: Fueled 10, 2012

3:45 pm

Shutdown Condition 1, Mode: 4, State: Cold S/D, Fuel December

Status: Fueled 10, 2012

7:50 pm

Shutdown Condition 1, Mode: 4, State: Cold S/D, Fuel December

Status: Fueled 11, 2012

7:20 pm

Shutdown Condition 1, Mode: 4, State: Cold S/D, Fuel December

Status: Fueled 12, 2012

8:07 pm

Shutdown Condition 1, Mode: 4, State: Cold S/D, Fuel December

Status: Fueled 12, 2012

10 pm

Shutdown Condition 1, Mode: 4, State: Cold S/D, Fuel December

Status: Fueled 13, 2012

1:02 am

Shutdown Condition 1, Mode: 4, State: Cold S/D, Fuel December

Status: Fueled 13, 2012

1:35 am

CONDITION REPORTS

CR-GGN-2012-11938

A1-14

WORK ORDERS

WO 282280 WO 00134296 WO 278119

WO 324956 WO 52342882 WO 52353819

WO 0322617

ENGINEERING CHANGES

EC No. 39577 EC No. 41383

Section 1R15: Operability Evaluations

PROCEDURE

NUMBER TITLE REVISION

EN-OP-104 Operability Determination Process: CR-GGN-2012-12133 6

OTHER DOCUMENTS

NUMBER TITLE DATE

460000286 Limitorque Valve Controls July 16, 2007

ASM Handbook, Volume 13A - Corrosion: Fundamentals, 2003

Testing, and Protection

Structural Analysis and design of Process Equipment, 2nd 1989

Edition

Eddie Current Test Data for Div II Emergency Diesel November 1,

Generator Jacket Water Heat Exchanger 2012

NRC Regulatory Guide 1.9 March 2007

NRC Regulatory Guide 1.32 February

1977

DRAWINGS

NUMBER TITLE REVISION

E-1111-013 P75 Stand-by Diesel Generator SYS DIV II Train B Start 16

Circuit

E-1111-012 P75 Stand-by Diesel Generator SYS DIV II Train A Start and 13

Stop Circuit

A1-15

DRAWINGS

NUMBER TITLE REVISION

Figure 1 Boundary and Support Systems of Emergency Diesel 4

Generator Systems

CALCULATIONS

NUMBER TITLE REVISION /

DATE

MC-Q1P75- Standby Diesel Jacket Water Operating Parameters 1

98030

CONDITION REPORTS

CR-GGN-2012-12060 CR-GGN-2012-12133 CR-GGN-2012-11755

ENGINEERING CHANGES

EC No. 40834 EC No. 40821 EC No. 40897

Section 1R19: Post-Maintenance Testing

PROCEDURES

NUMBER TITLE REVISION

07-S-23-P75-2 Diesel Generator DIV I and DIV II Functional Check 2

Overspeed Trip Switch and Emergency Stop Switch

06-OP-1P41-Q- Standby Service Water Loop B Valve and Pump Operability 122

005 Test

06-OP-1E12-Q- LPCI/RHR Subsystem B MOV Functional Test 111

0006

06-OP-1E12-M- LPCI/RHR Subsystem B Monthly Functional Test 113

0002

06-OP-1E12-Q- LPCI/RHR Subsystem B Quarterly Functional Test 118

0024

06-0P-1P41-M- SSW Loop B Operability Check 112

0005

06-OP-1P75-M- Standby Diesel Generator 12 Functional Test 131

0002, Attachment

A1-16

Section 1R19: Post-Maintenance Testing

PROCEDURES

NUMBER TITLE REVISION

II

06-OP-1P75-M- Standby Diesel Generator 12 Functional Test 131

0002, Attachment

I

04-1-03-P75-1 Div 2 Diesel Generator Unexcited Run 7

OTHER DOCUMENTS

NUMBER TITLE DATE

Open Documents on LCOs for Diesel Generator 12 November 5,

2012

Analysis for Static Test of Gate and Globe Valves, Valve

1P41F016B

MOV Torque Switch Setpoint Methodology Set Point

Calculations, Valve No. 1P41F016B

MOV Torque Switch Setpoint Methodology Set Point

Calculations, Valve No. 1E12F006B

Preliminary Vibration Data on SSW B

41329 Stator Winding Test Report, Grand Gulf SSW Pump

GNRO-2012- Reply to Notice of Violation EA-2012-015 February 13,

00007 2012

TR-110392 Eddy Current Testing of Service Water Heat Exchangers for February

Engineers Guideline 1999

ASM Handbook, Vol. 13A-Corrosion: Fundamentals, Testing, 2003

Protection

WORK ORDERS

WO 00121405 01 WO 00282241 01 WO 00314300 01

WO 00319437 01 WO 00318398 01 WO 00320182 02

WO 52421359 01 WO 00272998 01 WO 00272998 04

WO 00082560 04 WO 00082560 01 WO 00082560 03

WO 00082560 08 WO 00332736 01

A1-17

CONDITION REPORTS

CR-GGN-2012-11949 CR-GGN-2012-

Section 1R20: Refueling and Other Outage Activities

PROCEDURES

NUMBER TITLE REVISION

PO 19-01 Shutdown Operations Protection Plan: December 17, 2012 13

07-S-12-150 General Electric AM 4.16 KV Breaker Overhaul Instruction 0

07-S-12-61 Inspection of GE Magne Blast Circuit Breakers 3

07-S-12-61 Inspection of GE Magne Blast Circuit Breakers 4

07-S-12-150 General Electric AM 4.16 KV Breaker Overhaul Instruction 1

DRAWINGS

NUMBER TITLE REVISION

E-1188-018 Schematic Diagram, HPCS Power supply System Breaker 11

No.1

E-1009 One Line Meter & Relay Diagram 4.16KV E.S.F. System Bus 9

17AC

OTHER DOCUMENTS

NUMBER TITLE REVISION /

DATE

GG19-013 December Startup Power Profile

GG19-014 December Startup Power Profile

PO-19-01 Critical Path December 9,

2012

PO-19-01 Critical Path December

10, 2012

A1-18

OTHER DOCUMENTS

NUMBER TITLE REVISION /

DATE

PO-19-01 Critical Path December

11, 2012

PO-19-01 Critical Path December

12, 2012

GGNS PO-19-01 Planned Outage Daily Update December

10, 2012

GGNS PO-19-01 Planned Outage Daily Update December

11, 2012

GGNS PO-19-01 Planned Outage Daily Update December

12, 2012

GGNS PO-19-01 Planned Outage Daily Update December

13, 2012

LT-Apparent Cause Evaluation Report: Failure of the Division June 27,

III Diesel Generators Output Breaker to Close 2012

GEK-7320F Instruction, Magne Blast Circuit Breaker Types AM-4.16-350- F

2C, AM-4.16-350-2H

PM Basis EN-Switchgear-Medium Voltage-1KV to 7KV 3

Template

ACE Report CR-GGN-2012-07922 dated 06-27-2012

1000011 Guidance on Overhaul of Magne-Blast Circuit Breakers December

2000

CONDITION REPORTS

CR-GGN-2012-07922 CR-GGN-2012-07935

Section 1R22: Surveillance Testing

PROCEDURE

NUMBER TITLE REVISION

06-EL-1B21-Q- ADS Timers Functional Test and Calibration 102

0001

A1-19

Section 1R22: Surveillance Testing

PROCEDURE

NUMBER TITLE REVISION

06-IC-1C71-Q- Turbine Control Valve Fast Closure (RPS/EOC RPT) 104

2003 Functional Test

WORK ORDERS

WO 52439342 01 WO 52439341 01 WO 52439340 01

Section 1EP6: Drill Evaluation

PROCEDURES

NUMBER TITLE REVISION

10-S-01-1 Activation of the Emergency Plan 121

OTHER DOCUMENTS

NUMBER TITLE DATE

Emergency Notification Form, Message Number 1 October 16,

2012

GGNS-EP Group Drill, Emergency Facility Log October 16,

2012

Attachment 2 Objectives/Evaluation Criteria, Performance Indicators

Attachment 3 PCRS Items, Lessons Learned

Repair and Corrective Actions-Admin Status Board October 16,

2012

GGNS 2012 EP Drill (Blue Team) October 16,

2012

CONDITION REPORTS

CR-GGN-2012-11584 CR-GGN-2012-11599 CR-GGN-2012-11601

CR-GGN-2012-11602 CR-GGN-2012-11623 CR-GGN-2012-11625

CR-GGN-2012-11626 CR-GGN-2012-11627 CR-GGN-2012-11630

CR-GGN-2012-11631 CR-GGN-2012-11632 CR-GGN-2012-11657

CR-GGN-2012-11658 CR-GGN-2012-11661 CR-GGN-2012-11683

A1-20

Section 2RS02: Occupational ALARA Planning and Controls

PROCEDURES

NUMBER TITLE REVISION

EN-CY-112 BWR Shutdown and Startup Chemistry 0

EN-FAP-OU-100 Refueling Outage Preparation & Milestones 2

EN-MA-101 Conduct of Maintenance 3

EN-DC-115 Engineering Change Process 13

EN-RP-100 Radiation Worker Expectations 7

EN-RP-101 Access Control for Radiologically Controlled Areas 6

EN-RP-102 Radiological Control 3

EN-RP-108 Radiological Posting 11

EN-RP-110 ALARA Program 7

EN-RP-143 Source Control 9

EN-RP-151 Radiological Diving 2

EN-RP-201 Dosimetry Administration 3

EN-RP-202 Personnel Monitoring 8

EN-RP-204 Special Monitoring Requirements 6

EN-RP-503 Selection, Issue and Use of Respiratory Protection 5

AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES

NUMBER TITLE DATE

QA 14/15-2011 GGNS 2011 RP-RW Audit Report Final November 30,

2011

CONDITION REPORTS

CR-GGN-2012-00109 CR-GGN-2012-00640 CR-GGN-2012-00971

CR-GGN-2012-01210 CR-GGN-2012-01212 CR-GGN-2012-01215

CR-GGN-2012-01656 CR-GGN-2012-01750 CR-GGN-2012-01977

A1-21

CR-GGN-2012-04288 CR-GGN-2012-04504 CR-GGN-2012-04762

CR-GGN-2012-04944 CR-GGN-2012-05211 CR-GGN-2012-05239

CR-GGN-2012-05746 CR-GGN-2012-05807 CR-GGN-2012-06716

CR-GGN-2012-09064 CR-GGN-2012-12396 CR-GGN-2012-12400

CR-GGN-2012-01303 CR-GGN-2012-01514 CR-GGN-2012-09011

CR-GGN-2012-04830 CR-GGN-2012-04903 CR-GGN-2012-12401

CR-GGN-2012-00977 CR-GGN-2012-01133 CR-GGN-2012-09061

CR-GGN-2012-05320 CR-GGN-2012-05523 CR-GGN-2012-12405

RADIATION EXPOSURE PERMITS-ALARA POST-JOB REVIEWS

NUMBER TITLE REVISION

RWP-1086 Fuel Pool Cooling & Cleanup Modification 8

RWP-1402 Refuel Floor High Water 2

RWP-1403 Reactor Assembly/Disassembly 5

RWP-1406 Dryer/Separator Replacement 16

RWP-1505 Scaffold 2

RWP-1508 Under Vessel Activities 4

RWP-1511 General Drywell Maintenance 3

RWP-1516 In-Service Inspection 4

OTHER DOCUMENTS

NUMBER TITLE DATE

5-Year Exposure Reduction Plan 2012-2016

Grand Gulf Refuel Outage18 Report

Temporary Shielding Request 08-2

Temporary Shielding Request 12-47

Temporary Shielding Request 12-50

Refuel Outage18 Detailed Water Plan

A1-22

OTHER DOCUMENTS

NUMBER TITLE DATE

Survey GG-1203- 185 Auxiliary South Side Elevation March 27, 2012

3444

Survey GG-1202- 208 Containment Auxiliary Platform February 28,

1383 2012

Survey GG-1202- 208 Containment Refuel Bridge February 27,

1329 2012

Section 2RS04: Occupational Dose Assessment (71124.04)

PROCEDURES

NUMBER TITLE REVISION

EN-RP-201 Dosimetry Administration 3

EN-RP-202 Personnel Monitoring 8

EN-RP-204 Special Monitoring Requirements 6

EN-RP-206 Dosimeter of Legal Record 7

EN-RP-503 Selection, Issue and Use of Respiratory Protection 5

AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES

NUMBER TITLE DATE

QA 14/15-2011 GGNS 2011 RP-RW Audit Report Final November 30,

2011

OTHER DOCUMENTS

NUMBER TITLE DATE

11-02 ANI Information Bulletin: Neutron Monitoring July 2012

Dosimeter of Legal Record November 26,

2012

CONDITION REPORT

CR-GGN-2012-01949 CR-GGN-2012-01960 CR-GGN-2012-02250

CR-GGN-2012-03738 CR-GGN-2012-4404 CR-GGN-2012-04524

A1-23

CR-GGN-2012-06766 CR-GGN-2012-6700 CR-GGN-2012-4844

CR-GGN-2012-02727 CR-GGN-2012-03475

Section 4OA1: Performance Indicator Verification

PROCEDURE

NUMBER TITLE REVISION

EN-LI-114 Performance Indicator Process 6

OTHER DOCUMENTS

NUMBER TITLE DATE

NRC Performance Indicator Technique/Data Sheet, Heat 4th Quarter

Removal (RCIC/EFW/AFW) 2011

NRC Performance Indicator Technique/Data Sheet 1st Quarter

2012

NRC Performance Indicator Technique/Data Sheet 2nd Quarter

2012

NRC Performance Indicator Technique/Data Sheet 3rd Quarter

2012

NRC Resident Questions about E51-RCIC MSPI Data 4th Quarter

2011-3rd

Quarter 2012

Surveillance Tests for RCIC/E51 System

NRC Performance Indicator Technique/Data Sheet, Residual 4th Quarter

Heat Removal (RHR) 2011

NRC Performance Indicator Technique/Data Sheet 1st Quarter

2012

NRC Performance Indicator Technique/Data Sheet 2nd Quarter

2012

NRC Performance Indicator Technique/Data Sheet 3rd Quarter

2012

NRC Resident Questions about E12- Residual Heat Removal 4th Quarter

2011-3rd

Quarter 2012

Residual Heat Removal 4th Quarter

2011

A1-24

OTHER DOCUMENTS

NUMBER TITLE DATE

NRC Performance Indicator Technique/Data Sheet, High 4th Quarter

Pressure Injection (HPCS/HPCI/HPI/HPSI/FCI/HPI) 2011

NRC Performance Indicator Technique/Data Sheet, High 1st Quarter

Pressure Injection (HPCS/HPCI/HPI/HPSI/FCI/HPI) 2012

NRC Performance Indicator Technique/Data Sheet, High 2nd Quarter

Pressure Injection (HPCS/HPCI/HPI/HPSI/FCI/HPI) 2012

NRC Performance Indicator Technique/Data Sheet, High 3rd Quarter

Pressure Injection (HPCS/HPCI/HPI/HPSI/FCI/HPI) 2012

NRC Performance Indicator Technique/Data Sheet, 4th Quarter

Emergency AC Power (EDG) 2011

NRC Performance Indicator Technique/Data Sheet, 1st Quarter

Emergency AC Power (EDG) 2012

NRC Performance Indicator Technique/Data Sheet, 2nd Quarter

Emergency AC Power (EDG) 2012

NRC Performance Indicator Technique/Data Sheet, 3rd Quarter

Emergency AC Power (EDG) 2012

NRC Resident Questions about Division I and II Standby 4th Quarter

Diesel Generators 2011-3rd

Quarter 2012

NRC Resident Questions about E22 High Pressure Core 4th Quarter

Spray 2011-3rd

Quarter 2012

NRC Performance Indicator Technique/Data Sheet, Cooling 4th Quarter

Water Support 2011

NRC Performance Indicator Technique/Data Sheet, Cooling 1st Quarter

Water Support 2012

NRC Performance Indicator Technique/Data Sheet, Cooling 2nd Quarter

Water Support 2012

NRC Performance Indicator Technique/Data Sheet, Cooling 3rd Quarter

Water Support 2012

Operations Surveillances for Stand-by Service Water P41

System

A1-25

Section 4OA2: Identification and Resolution of Problems

PROCEDURES

NUMBER TITLE REVISION/

DATE

04-1-01-P44-1 Plant Service Water/Radial Well System 99

05-1-02-III-12 Off-Normal Event Procedure 0

EN-WM-100 Work Request Generation, Screening, and Classification 8

EN-FAP-OP-009 Tagging Performance Indicator Program 2

EN-LI-121 Entergy Trending Process 12

EN-WM-101 On-Line Work Management Process 9

EN-OP-117, Operator Aggregate Assessment of Plant Deficiencies April 2012

Attachment 9.5

EN-OP-117 Operations Assessments 4

EN-FAP-OP-006 Operator Aggregate Impact Index Performance Indicator 0

EN-OP-117, Operator Aggregate Assessment of Plant Deficiencies November

Attachment 9.5 2012

07-S-12-61 Inspection of GE MagnaBlast Circuit Breakers 110

OTHER DOCUMENTS

NUMBER TITLE DATE

Standing Orders October 14,

2012

Operator Compensatory Actions October 2012

ODMIs In Effect November 14,

2012

List of Inputs to Operation Aggregate Index October 2012

Tagouts Older than 90 days Report August 19,

2012

Caution Tagouts Older than 90 days Report August 19,

2012

Items Affecting Operations Aggregate Index March 1,

2012

Remaining Open Actions For Open GGN Crs with Operability April 17, 2012

Code: OPERABLE DNC

A1-26

OTHER DOCUMENTS

NUMBER TITLE DATE

GGNS Quarterly Trend Report 1st and 2nd Quarter 2012 October 3,

2012

Open ODMI Actions March 2012

Remaining Open Actions For Open GGN Crs with Operability April 17, 2012

Code: OPERABLE-COMP MEAS

Grand Gulf Operator Aggregate Impact Index November

2011

Grand Gulf Operator Aggregate Impact Index December

2011

Grand Gulf Operator Aggregate Impact Index January 2012

Grand Gulf Operator Aggregate Impact Index February

2012

Grand Gulf Operator Aggregate Impact Index March 2012

Grand Gulf Operator Aggregate Impact Index April 2012

Grand Gulf Operator Aggregate Impact Index May 2012

Grand Gulf Operator Aggregate Impact Index June 2012

Grand Gulf Operator Aggregate Impact Index July 2012

Grand Gulf Operator Aggregate Impact Index August 2012

Grand Gulf Operator Aggregate Impact Index September

2012

Grand Gulf Operator Aggregate Impact Index October 2012

Grand Gulf Operator Aggregate Impact Index November

2012

Grand Gulf Operator Burdens (OB) November

2011

Grand Gulf Operator Burdens (OB) December

2011

Grand Gulf Operator Burdens (OB) January 2012

Grand Gulf Operator Burdens (OB) February

2012

A1-27

OTHER DOCUMENTS

NUMBER TITLE DATE

Grand Gulf Operator Burdens (OB) March 2012

Grand Gulf Operator Burdens (OB) April 2012

Grand Gulf Operator Burdens (OB) May 2012

Grand Gulf Operator Burdens (OB) June 2012

Grand Gulf Operator Burdens (OB) July 2012

Grand Gulf Operator Burdens (OB) August 2012

Grand Gulf Operator Burdens (OB) September

2012

Grand Gulf Operator Burdens (OB) October 2012

Grand Gulf Operator Burdens (OB) November

2012

Grand Gulf Operator Workarounds (OWA) November

2011

Grand Gulf Operator Workarounds (OWA) December

2011

Grand Gulf Operator Workarounds (OWA) January 2012

Grand Gulf Operator Workarounds (OWA) February

2012

Grand Gulf Operator Workarounds (OWA) March 2012

Grand Gulf Operator Workarounds (OWA) April 2012

Grand Gulf Operator Workarounds (OWA) May 2012

Grand Gulf Operator Workarounds (OWA) June 2012

Grand Gulf Operator Workarounds (OWA) July 2012

A1-28

OTHER DOCUMENTS

NUMBER TITLE DATE

Grand Gulf Operator Workarounds (OWA) August 2012

Grand Gulf Operator Workarounds (OWA) September

2012

Grand Gulf Operator Workarounds (OWA) October 2012

Grand Gulf Operator Workarounds (OWA) November

2012

Grand Gulf Control Room Deficiencies November

2011

Grand Gulf Control Room Deficiencies December

2011

Grand Gulf Control Room Deficiencies January 2012

Grand Gulf Control Room Deficiencies February

2012

Grand Gulf Control Room Deficiencies March 2012

Grand Gulf Control Room Deficiencies April 2012

Grand Gulf Control Room Deficiencies May 2012

Grand Gulf Control Room Deficiencies June 2012

Grand Gulf Control Room Deficiencies July 2012

Grand Gulf Control Room Deficiencies August 2012

Grand Gulf Control Room Deficiencies September

2012

Grand Gulf Control Room Deficiencies October 2012

Grand Gulf Control Room Deficiencies November

2012

A1-29

OTHER DOCUMENTS

NUMBER TITLE DATE

Grand Gulf Control Room Alarm (CRA) November

2011

Grand Gulf Control Room Alarm (CRA) December

2011

Grand Gulf Control Room Alarm (CRA) January 2012

Grand Gulf Control Room Alarm (CRA) February

2012

Grand Gulf Control Room Alarm (CRA) March 2012

Grand Gulf Control Room Alarm (CRA) April 2012

Grand Gulf Control Room Alarm (CRA) May 2012

Grand Gulf Control Room Alarm (CRA) June 2012

Grand Gulf Control Room Alarm (CRA) July 2012

Grand Gulf Control Room Alarm (CRA) August 2012

Grand Gulf Control Room Alarm (CRA) September

2012

Grand Gulf Control Room Alarm (CRA) October 2012

Grand Gulf Control Room Alarm (CRA) November

2012

Grand Gulf Caution Tags > 90 days November

2011-

November

2012

Grand Gulf Tagouts > 90 days November

2011-

November

2012

A1-30

CONDITION REPORTS

CR-GGN-2012-08881 CR-GGN-2012-10487 CR-GGN-2012-10890

CR-GGN-2012-09914 CR-GGN-2012-10502 CR-GGN-2012-10910

CR-GGN-2012-09941 CR-GGN-2012-10503 CR-GGN-2012-10911

CR-GGN-2012-09942 CR-GGN-2012-10504 CR-GGN-2012-10919

CR-GGN-2012-10032 CR-GGN-2012-10505 CR-GGN-2012-10920

CR-GGN-2012-10033 CR-GGN-2012-10506 CR-GGN-2012-11071

CR-GGN-2012-10037 CR-GGN-2012-10508 CR-GGN-2012-11114

CR-GGN-2012-10071 CR-GGN-2012-10509 CR-GGN-2012-11115

CR-GGN-2012-10102 CR-GGN-2012-10510 CR-GGN-2012-11151

CR-GGN-2012-10108 CR-GGN-2012-10511 CR-GGN-2012-11504

CR-GGN-2012-10143 CR-GGN-2012-10512 CR-GGN-2012-11506

CR-GGN-2012-10217 CR-GGN-2012-10513 CR-GGN-2012-11564

CR-GGN-2012-10224 CR-GGN-2012-10514 CR-GGN-2012-11568

CR-GGN-2012-10228 CR-GGN-2012-10515 CR-GGN-2012-11615

CR-GGN-2012-10237 CR-GGN-2012-10530 CR-GGN-2012-11665

CR-GGN-2012-10247 CR-GGN-2012-10531 CR-GGN-2012-11668

CR-GGN-2012-10253 CR-GGN-2012-10532 CR-GGN-2012-11669

CR-GGN-2012-10287 CR-GGN-2012-10533 CR-GGN-2012-11673

CR-GGN-2012-10306 CR-GGN-2012-10578 CR-GGN-2012-11674

CR-GGN-2012-10311 CR-GGN-2012-10598 CR-GGN-2012-11675

CR-GGN-2012-10313 CR-GGN-2012-10599 CR-GGN-2012-11676

CR-GGN-2012-10412 CR-GGN-2012-10610 CR-GGN-2012-11794

CR-GGN-2012-10431 CR-GGN-2012-10611 CR-GGN-2012-11819

CR-GGN-2012-10436 CR-GGN-2012-10612 CR-GGN-2012-11830

CR-GGN-2012-10438 CR-GGN-2012-10615 CR-GGN-2012-11832

CR-GGN-2012-10443 CR-GGN-2012-10622 CR-GGN-2012-11874

CR-GGN-2012-10450 CR-GGN-2012-10635 CR-GGN-2012-11943

CR-GGN-2012-10451 CR-GGN-2012-10636 CR-GGN-2012-11944

CR-GGN-2012-10463 CR-GGN-2012-10666 CR-GGN-2012-11961

A1-31

CONDITION REPORTS

CR-GGN-2012-10464 CR-GGN-2012-10735 CR-GGN-2012-11979

CR-GGN-2012-10467 CR-GGN-2012-10816 CR-GGN-2012-12165

CR-GGN-2012-10468 CR-GGN-2012-10819 CR-GGN-2012-12166

CR-GGN-2012-10469 CR-GGN-2012-10820 CR-GGN-2012-12215

CR-GGN-2012-10471 CR-GGN-2012-10828 CR-GGN-2012-12218

CR-GGN-2012-10472 CR-GGN-2012-10829 CR-GGN-2012-12236

CR-GGN-2012-10476 CR-GGN-2012-10859 CR-GGN-2012-12332

CR-GGN-2012-10478 CR-GGN-2012-10860 CR-GGN-2012-12336

CR-GGN-2012-10479 CR-GGN-2012-10861 CR-GGN-2012-12344

CR-GGN-2012-10481 CR-GGN-2012-10862 CR-GGN-2012-12345

CR-GGN-2012-10482 CR-GGN-2012-10863 CR-GGN-2012-12380

CR-GGN-2012-10484 CR-GGN-2012-10886 CR-GGN-2012-12381

CR-GGN-2012-10485 CR-GGN-2012-12472 CR-GGN-2012-12457

CR-GGN-2012-10486 CR-GGN-2012-12458 CR-GGN-2012-09693

CR-GGN-2012-09889 CR-GGN-2012-12187 CR-GGN-2012-01486

CR-GGN-2012-08885 CR-GGN-2012-09035 CR-GGN-2012-09111

Section 4OA3: Event Follow-Up

PROCEDURES

NUMBER TITLE REVISION

EN-LI-118 Root Cause Evaluation Process 18

05-S-01-EP-1 Emergency/Severe Accident Procedure Support Documents 27

06-RE-1C51-O- Local Power Range Monitor Calibration 112

0001

17-S-02-40 Bypassing and Unbypassing LRPMs 116

04-1-01-C51-1 Neutron Monitoring 28

04-1-02-1H13- LPRM DNSC 206

P680-5A-C9

A1-32

Section 4OA3: Event Follow-Up

PROCEDURES

NUMBER TITLE REVISION

07-S-33-C51-2 LPRM Detector Removal/Installation 112

07-S-33-C51-2 LPRM Detector Removal/Installation 113

03-1-01-1 Cold Shutdown to Generator Carrying Minimum Load 154

06-RE-1C51-O- Local Power Range Monitor Calibration 112

0001

06-RE-1C51-W- APRM Gain Adjustment 106

0001

01-S-06-26 Post-Trip Analysis, Scram # 126, December 31, 2012 20

02-S-01-27 Operations Philosophy 49

01-S-06-5 Event Notification Worksheet EN #48637 110

OTHER DOCUMENTS

NUMBER TITLE REVISION /

DATE

00160640 Action Request Identification October 22,

2012

CA 34 for CR-GGN-2012-1842

CA 35 for CR-GGN-2012-1842

CA 43 for CR-GGN-2012-1842

GNRO-2012- GGNS LER 2012-001-00 Surveillance Test Procedure March 13,

00013 Inadequate to meet the Requirements of Technical 2012

Specifications

GNRO-2012- GGNS LER 2012-002-00 Manual Reactor Scram Due to a April 19, 2012

00028 Steam Supply Motor Operated Valve Failure that Resulted in

the Inability to Maintain Reactor Water Level

A1-33

OTHER DOCUMENTS

NUMBER TITLE REVISION /

DATE

GNRO-2012- GGNS LER 2012-003-00 Actuation Due to Division III Bus May 29, 2012

00048 Undervoltage following a Lightening Strike

GNRO-2012- GGNS LER 2012-004-00 Weld Defect Indication Found in June 27,

00069 Residual Heat Removal System to Reactor Pressure Vessel 2012

Boundary Nozzle

GNRO-2012- GGNS LER 2012-005-00 Average Power Range Monitors August 13,

00084 Inoperable in Excess of Technical Specifications Allowances 2012

in Mode 2

GNRO-2012- Special Report 2012-006-00 Special Nuclear Inventory August 23,

00090 Discrepancy 2012

Root Cause Evaluation Report, Inability to Maintain Reactor July 11, 2012

Water Lever, CR-GGN-2012-1842

Apparent Cause Evaluation Report PRNM Issues During 1

RF18 Power Ascension, CR-GGN-2012-8224

GNRO- GGNS LER 2012-007-00 Standby Service Water System September

2012/00108 Administratively Inoperable For A Period Longer Than 14, 2012

Allowed By Technical Specifications

Core Operating Limits Report LBDCR

12034

22A3739AE Neutron Monitoring System 6

SDC-C71 Reactor Protection System 0

SDC-C51 Neutron Monitoring System 0

Chapter 7 GG UFSAR Chapter 7

GG Technical Specifications and Bases

SCN No: Standard/Specific Change Notice December

96/0001 30, 2003

DRN No: 04- SDC-C51 Neutron Monitoring System 0

1210

A1-34

OTHER DOCUMENTS

NUMBER TITLE REVISION /

DATE

DRN No: 05- SDC-C71 0

1185

Forced Outage Worklist December

18, 2012

CONDITION REPORTS

CR-GGN-2012-07669 CR-GGN-2012-11950 CR-GGN-2007-03818

CR-GGN-2011-00099 CR-GGN-2009-06249 CR-GGN-2012-04887

CR-GGN-2012-06386 CR-GGN-2012-08224 CR-GGN-2012-11950

CR-GGN-2012-08258 CR-GGN-2012-08224 CR-GGN-2012-08349

CR-GGN-2012-08351 CR-GGN-2013-00177 CR-GGN-2013-00178

ENGINEERING CHANGES

EC No. 19461 EC No. 21999

Section 4OA7: Licensee-Identified Violations

CONDITION REPORTS

CR-GGNS-2012-09405

TI 187/188

PROCEDURES

NUMBER TITLE REVISION /

DATE

07-S-14-310 Inspection of Mechanical Seals on Doors 10

EN-DC-170 Fukushima Near Term Task Force Recommendation 2.3 0

Flooding Walkdown Procedure

GGNS-CS-12- Flooding Walkdown Submittal Report for Resolution of 0

0002 Fukushima Near-Term Task Force Recommendation 2.3:

Flooding

A1-35

EN-DC-168 Fukushima Near-Term Task Force Recommendation 2.3 0

Seismic Walk-down Procedure

05-1-02-VI-2 Hurricanes, Tornados, and Severe Weather 119

05-1-02-VI-1 Off-Normal Event Procedure Flooding 109

EN-EP-302 Severe Weather Response 0

DRAWINGS

NUMBER TITLE REVISION /

DATE

07-S-14-310 Inspection of Mechanical Seals on Doors 10

J-0133G Installation detail-Seismic and Non Seismic Tubing Run- 3

STDBY. Diesel Generator

J-0157T Area Temp. Element 6

J-135B-002 Standby Service Water Pump House A and B Temperature 5

J-1512 Standby Service Water Pump House Basin A 8

J-1512- U2-C Standby Service Water Pump House Basin A A

J-KA1512 Standby Service Water Pump House Basin A A

M-1026 Diesel Generator Building, Unit 1 15

M-1106A D. Gen., ECCS., ESF. ELEC. SWGR., SSW. & CIRC. WTR. 12

PP. HSE. VENT. SYS. - Unit 1

9645-J-561.0- Thermo Electric Drawing 27620

Q1C61N403A-

1.1-0010

OTHER

NUMBER TITLE REVISION /

DATE

Endorsement of Nuclear Energy Institute 12-07, Guidelines May 31, 2012

for Performing Verification Walkdowns of Plant Flood

Protection Features

WP1 Yard Inside PA (North) 0

WP2 Yard Inside PA (South) 0

WP 3 Yard Outside PA (North) 0

WP4 Yard Outside PA (South) 0

A1-36

OTHER

NUMBER TITLE REVISION /

DATE

AWC-041 DG, El. 133, Room 1D308,DSL

AWC-050 SSW, El. 133, Room 2M112, SSW

SWEL1-084 H22P401, STBY DG Engine Control Panel

SWEL1-068 Y47N005B, Temperature Element (SSW Pump House B

Space)

SWEL SWEL Excel Sheet September

17, 2012

US Army Corp of Engineers: Sandbagging Techniques 2004

ER-GG-2004- Acceptance of corrosion of conduit and electric boxes (CR- July 1, 2004

0272-000 GGN-2004-02612)

PMP Site Drainage Modifications 1

GGNS-CS-12- GGNS Flooding Walkdown Submittal Report for Resolution of 0

00003 Fukushima Near-Term Task Force Recommendation 2.3:

Flooding

GGNS-CS-12- GGNS Flooding Walkdown Submittal Report for Resolution of 0

00002 Fukushima Near-Term Task Force Recommendation 2.3:

Seismic

GGNS-CS-12- GGNS Flooding Walkdown Submittal Report for Resolution of 0

00004 Fukushima Near-Term Task Force Recommendation 2.3:

Flooding

CONDITION REPORTS

CR-GGN-2012-10896 CR-GGN-2012-10894 CR-GGN-2012-10895

CR-GGN-2012-10907 CR-GGN-2012-10897 CR-GGN-2012-11034

CR-GGN-2012-10870 CR-GGN-2012-10872 CR-GGN-2012-10894

CR-GGN-2012-10876 CR-GGN-2012-11007 CR-GGN-2012-11010

CR-GGN-2012-11009 CR-GGN-2012-11008 CR-GGN-2012-10869

CR-GGN-2012-10868 CR-GGN-2012-11126 CR-GGN-2012-11128

CR-GGN-2012-11129 CR-GGN-2012-11130 CR-GGN-2012-11078

CR-GGN-2012-11081 CR-GGN-2012-11084 CR-GGN-2012-11328

CR-GGN-2012-11334 CR-GGN-2012-11335 CR-GGN-2012-11337

A1-37

CR-GGN-2012-11306 CR-GGN-2012-11307 CR-GGN-2012-11308

CR-GGN-2012-11309 CR-GGN-2012-11455 CR-GGN-2012-11456

CR-GGN-2012-11457 CR-GGN-2012-11458 CR-GGN-2012-11459

CR-GGN-2012-11460 CR-GGN-2012-11461 CR-GGN-2012-11462

CR-GGN-2012-11463 CR-GGN-2012-11464 CR-GGN-2012-11465

CR-GGN-2012-11466 CR-GGN-2012-11467 CR-GGN-2012-11468

CR-GGN02004-02612 CR-GGN-2008-01269 CR-GGN-2008-05146

CR-GGN-2012-10894 CR-GGN-2012-10895 CR-GGN-2012-10896

CR-GGN-2012-10897 CR-GGN-2012-10907 CR-GGN-2012-11034

CR-GGN-2012-10325 CR-GGN-2012-12338 CR-GGN-2012-12331

CR-GGN-2012-12329 CR-GGN-2012-12338

A1-38

Attachment 2: Request for Information for ALARA Planning & Controls Inspection

1. Items needed to support the ALARA Planning & Controls (71124.02) inspection to be

conducted by Louis C. Carson II are as follows:

Date of Last Inspection: February 18, 2011

A. List of contacts and telephone numbers for ALARA program personnel

B. Applicable organization charts

C. Copies of audits, self-assessments, and LERs, written since date of last inspection,

focusing on ALARA

D. Procedure index for ALARA Program

E. Please provide specific procedures related to the following areas noted below.

Additional Specific Procedures may be requested by number after the inspector

reviews the procedure indexes.

1. ALARA Program

2. ALARA Committee

3. Radiation Work Permit Preparation

F. A summary list of corrective action documents (including corporate and subtiered

systems) written since date of last inspection, related to the ALARA program. In

addition to ALARA, the summary should also address Radiation Work Permit

violations, Electronic Dosimeter Alarms, and RWP Dose Estimates

NOTE: The lists should indicate the significance level of each issue and the search

criteria used. Please provide documents which are searchable.

G. List of work activities greater than 1 rem, since date of last inspection.

Include original dose estimate and actual dose.

H. Site dose totals and 3-year rolling averages for the past 3 years (based on dose of

record)

I. Outline of source term reduction strategy

J. A major focus of this inspection will be the results of the power upgrade outage,

please provide the following:

Annual GGNS ALARA Report for 2011

Last post Refueling-Power- Outage Report

List of ALARA Package that Exceeded the Original Dose Projections

A2-1 Attachment

Provide Written Justifications if Dose were Exceeded by 50% & 5 Person-Rem

2. Occupational Dose Assessment (Inspection Procedure 71124.04) to be reviewed:

Date of Last Inspection: August 18, 2010

A List of contacts and telephone numbers for the following areas:

1 Radiological effluent control

2 Engineered safety feature air cleaning systems

B Applicable organization charts

C Audits, self assessments, surveillances, vendor or NUPIC audits of contractor

support, and LERs written since September 2010 related to Occupational Dose

Assessment

D Procedure indexes for Occupational Dose Assessment

E Please provide specific procedures related to the following areas. Additional

Specific Procedures may be requested after the inspector reviews the procedure

indexes.

1. Radiation Protection Program

2. Radiation Protection Conduct of Operations

3. Personnel Dosimetry Program

4. Radiological Posting and Warning Devices

5. Air Sample Analysis

6. Performance of High Exposure Work

7. Declared Pregnant Worker

8. Bioassay Program

F List of corrective action documents (including corporate and subtiered systems)

written since September 2010 associated with:

1. NVLAP accreditation

2. Dosimetry (TLD/OSL, etc.) problems

3. Electronic alarming dosimeters

4. Bioassays or internally deposited radionuclides or internal dose

A2-2

5. Neutron dose

NOTE; The lists should indicate the significance level of each issue and the

search criteria used.

G List of positive whole body counts since, September 2010 names redacted if

desired

H Part 61 analyses/scaling factors

I The most recent National Voluntary Laboratory Accreditation Program (NVLAP)

accreditation report on the licensee or dosimetry vendor, as appropriate

Please provide this information to me by November 1, 2012; thank you in advance. If you have

any questions pertaining to the requested information or the upcoming inspection, my office

number is (817) 200-1221, or you can reach me by email at Louis.Carson@nrc.gov.

A2-3