ML073241325

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Email from K. Cotton, NRR to S. Shaeffer, Rii on Final Farley Aitnrc Slides.Ppt
ML073241325
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 09/18/2007
From: Cotton K
Office of Nuclear Reactor Regulation
To: Scott Shaeffer
Office of Nuclear Reactor Regulation
References
FOIA/PA-2008-0016
Download: ML073241325 (8)


Text

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From:

To:

Date:

Subject:

Karen Cotton Scott Shaeffer 09/18/2007 5:47:28 PM Final Farley AITNRC slides.ppt f5 sw I

af en Cotton - Farl-ey Ai TUR-C" -slid'e-sppt PaQe 1 }1 LLre Cotn-FalvAT R lds DtPo

/ U.S.NRC UNITED STATES NUCLEAR REGULATOAY COMMISSION Protecting People and the Environment Senate Committee on Environment and Public Works Briefing September 19, 2.007 1

NRC Staff Headquarters David Decker - Congressional Affairs Timothy McGinty - Nuclear Reactor Regulation (NRR), Deputy Director of Division of Operating Reactor Licensing (DORL)

Steven Alexander - NRR, PRA Operations Support;

& Maintenance Branch, Augmented Inspection Team Member Karen Cotton -

NRR, DORL, Joseph M. Farley Nuclear Plant -

Project Manager Region II Scott Shaeffer - Chief, Reactor Projects Branch 2 Michael Ernstes - Chief, Training and Development Branch 2

I Karen" Cotton - Farley AITNRC sliqe-s-kpý,K~n ottol-Fa~eyATNRC~ide~pptPage3 Sf),U.S.NRC Joseph M. Farley Nuclear Plant Operator - Southern Nuclear Operating Company

  • Units-Two
  • Unit 1 - 830 MWt Unit2-839 MWt 3

Kareýn Cotton - Fa~riey AITNRC siqoeS.Pt Page4

  • U.S.NRC History of events On May 3, 2007 The U.S. Nuclear Regulatory Commission completed a supplemental inspection regarding the Cooling Water Systems.

several significant weaknesses were identified regarding:

  • evaluations for repeat safety-related breaker failures

- the thoroughness of design modification reviews for the installation of new breakers 4

tton - Farley AiTNRC slides.ppt I-'age 5 I Karen Cotton - Farley AITNRC slides.ppt Page b 1 History of events On September 4, 2007

  • After a planned maintenance on the 1 B component cooling water (CCW) pump, the licensee encountered a problem when testing the functional relationships between the Unit 1 1 B CCW pump and the 1C CCW pump.
  • The Cutler-Hammer breaker failed to close when the licensee attempted to manually start the 1C CCW pump from the control room.

On September 5, 2007

  • The 1A CCW pump Allis-Chalmers breaker failed to close when manually started from the control room when the licensee tested the functionality of the 1B CCW pump and the 1A CCW pump.

5

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-FrHy AITNRC~sie e"

Augmented Inspection Team

  • The previous events precipitated the formation of an Augmented Inspection Team
  • The team was chartered on September 10, 2007 6

Karen Cotton -

sldes Pa&77

(-,,ý.".S.]NIEC Next Steps

  • Public Exit Meeting; September 20, 2007 at the site NRC will continue to:

Confirm root cause analysis and extent of condition

- Evaluate potential findings or violations Monitor interim and long-term corrective action for the identified breaker problems Develop AIT Inspection Report 7