IR 05000263/2006003

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Inspection Report 05000263-06-003; 05000263-06-010; 04/01/2006 - 06/30/2006; Monticello Nuclear Generating Plant. Fire Protection and Surveillance Testing
ML062000497
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 07/17/2006
From: Burgess B
NRC/RGN-III/DRP/RPB2
To: Conway J
Nuclear Management Co
References
IR-06-003
Download: ML062000497 (33)


Text

uly 17, 2006

SUBJECT:

MONTICELLO NUCLEAR GENERATING PLANT NRC INTEGRATED INSPECTION REPORT 05000263/2006003 (DRP); 05000263/2006010(DRS)

Dear Mr. Conway:

On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Monticello Nuclear Generating Plant. The enclosed integrated inspection report documents the inspection findings which were discussed on July 6, 2006, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, there were two NRC-identified findings of very low safety significance, of which one involved a violation of NRC requirements. However, because this finding was of very low safety significance and because the issue was entered into the licensees corrective action program, the NRC is treating this finding as a non-cited violation in accordance with Section VI.A.1 of the NRCs Enforcement Policy.

If you contest the subject or severity of a non-cited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -

Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Monticello Nuclear Generating Plant. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Bruce L. Burgess, Chief Branch 2 Division of Reactor Projects Docket No. 50-263 License No. DPR-22 Enclosure: Inspection Report 05000263/2006003;05000263/2006010 w/Attachment: Supplemental Information cc w/encl: M. Sellman, Chief Executive Officer and Chief Nuclear Officer Manager, Nuclear Safety Assessment J. Rogoff, Vice President, Counsel, and Secretary Nuclear Asset Manager, Xcel Energy, Inc.

State Liaison Officer, Minnesota Department of Health R. Nelson, President Minnesota Environmental Control Citizens Association (MECCA)

Commissioner, Minnesota Pollution Control Agency D. Gruber, Auditor/Treasurer, Wright County Government Center Commissioner, Minnesota Department of Commerce Manager - Environmental Protection Division Minnesota Attorney Generals Office

SUMMARY OF FINDINGS

Inspection Report 05000263/2006003; 05000263/2006010; 04/01/2006 - 06/30/2006; Monticello

Nuclear Generating Plant. Fire Protection and Surveillance Testing.

This report covers a 3-month period of baseline resident inspection and an announced baseline inspection for emergency preparedness. The inspections were conducted by the resident inspectors and a regional emergency preparedness inspector. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

NRC-Identified

and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

A finding of very low safety significance was identified by the inspectors for failure to control loose materials, located above and adjacent to the Division II low pressure coolant injection (LPCI) inboard isolation valve and associated piping. Once identified, the licensee took action to relocate the material.

The issue was more than minor because the loose items located above and adjacent to the Division II LPCI components impacted the Mitigating Systems objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, it affected the cornerstones attribute for the protection against external factors such as seismic events. The issue was of very low safety significance because the finding did not represent a loss or degradation of equipment specifically designed to mitigate a seismic initiating event, nor did it represent a total loss of any safety function identified by the licensee that contributes to external event initiated core damage accident sequences. This finding had a cross-cutting aspect in the area of Human Performance because licensee personnel failed to determine the potential impact of the unsecured material on the Division II LPCI components during a seismic event as required by station procedures. No violation of NRC requirements was identified. (Section 1R05)

Cornerstone: Barrier Integrity

Green.

A finding of very low safety significance was identified by the inspectors for a violation of 10 CFR 50, Appendix B, Criterion V, when licensee Instrumentation

& Controls (I&C) technicians deviated from existing procedural guidance to perform unauthorized post-maintenance tests during the performance of torus vacuum breaker testing. Specifically, maintenance personnel inappropriately cycled the isolation valves to differential pressure transmitters DPIS-2572 and DPIS-2573 to perform leak checks subsequent to the removal of test equipment. Specific corrective actions taken by the licensee to address this issue included counseling of the responsible technician regarding procedure use and adherence expectations and supervisor discussions with the I&C shop personnel to reinforce standards regarding procedure use and adherence.

This finding was more than minor because if left uncorrected, the performance deficiency could become a more significant safety concern. The inspectors determined that the finding was of very low safety significance because the performance deficiency did not result in an actual open pathway in the physical integrity of the reactor containment, or actual reduction in the defense-in-depth for the atmospheric pressure control or hydrogen control functions of the reactor containment. This finding had a cross-cutting aspect in the area of Human Performance because licensee personnel failed to follow established procedures. (Section 1R22)

Licensee-Identified Violations

None.

REPORT DETAILS

Summary of Plant Status

Monticello operated at full power for the entire assessment period except for brief downpower maneuvers to accomplish rod pattern adjustments and to conduct planned surveillance testing activities with the following exceptions:

  • On April 22, 2006, reactor power was reduced to approximately 75 percent full power to facilitate a significant planned control rod pattern adjustment. The evolution was completed successfully and power was restored to 100 percent later the same day.
  • On June 25, 2006, reactor power was reduced to approximately 55 percent full power to facilitate the brush replacement on the 12 recirculation motor-generator set. The maintenance was completed successfully and power was restored to 100 percent power later the same day.

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather

a. Inspection Scope

The inspectors performed a detailed review of the licensees procedures and a walkdown of two systems to observe the licensees preparations for adverse weather, including conditions that could result from high temperatures or high winds. The inspectors focused on plant specific design features for the systems and implementation of the procedures for responding to or mitigating the effects of adverse weather.

Inspection activities included, but were not limited to, a review of the licensees adverse weather procedures, preparations for the summer season, and a review of analysis and requirements identified in the Updated Safety Analysis Report. The inspectors also verified that operator actions specified by plant specific procedures were appropriate.

The inspectors evaluated readiness for seasonal susceptibilities for the following systems for a total of two samples:

  • intake structure pump room ventilation system; and

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial walkdowns of accessible portions of trains of risk-significant mitigating systems equipment. The inspectors reviewed equipment alignment to identify any discrepancies that could impact the function of the system and potentially increase risk. Identified equipment alignment problems were verified by the inspectors to be properly resolved. The inspectors selected redundant or backup systems for inspection during times when equipment was of increased importance due to unavailability of the redundant train or other related equipment. Inspection activities included, but were not limited to, a review of the licensees procedures, verification of equipment alignment, and an observation of material condition, including operating parameters of equipment in-service.

The inspectors selected the following equipment trains to assess operability and proper equipment line-up for a total of three samples:

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors walked down risk-significant fire areas to assess fire protection requirements. The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and had implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems or features. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events, or the potential to impact equipment which could initiate or mitigate a plant transient. The inspection activities included, but were not limited to, the control of transient combustibles and ignition sources, fire detection equipment, manual suppression capabilities, passive suppression capabilities, automatic suppression capabilities, compensatory measures, and barriers to fire propagation.

The inspectors selected the following areas for review for a total of ten samples:

  • Fire Zone 23A, intake structure pump room;
  • Fire Zone 1000, site mitigation;
  • Fire Zone 31A, emergency filtration train building (EFT) 1st floor, Division I;
  • Fire Zone 31B, EFT building 1st floor, Division II;
  • Fire Zone 32A, EFT building 2nd floor, Division I;
  • Fire Zone 32B, EFT building 2nd floor, Division II;
  • Fire Zone 33, EFT building 3rd floor;
  • Fire Zone 5B, reactor building 1001' elevation north;
  • Fire Zone 2D, reactor building railroad shelter.

b. Findings

Introduction:

The inspectors identified a finding of very low safety significance associated with the licensees failure to control loose materials, located above and adjacent to the Division II LPCI inboard isolation valve and associated piping. No violation of NRC requirements was identified.

Description:

On May 25, 2006, the inspectors conducted a fire protection inspection of the west shutdown cooling room. During this inspection, the inspectors identified several pieces of deck grating (approximately 2' x 6' x 2") that were stacked five high and other loose materials being stored on a elevated concrete platform located immediately above the drywell personnel hatch and approximately 12 inches from the edge of the platform that was above and adjacent to the Division II LPCI inboard isolation valve and associated piping. The inspectors concluded that during a seismic event, the material could fall and impact LPCI injection isolation valves, vent valves, and associated piping.

Administrative Work Instruction 4 AWI-04.02.01, Housekeeping, Revision 12, established general housekeeping practices, which are consistent with acceptable industry standards and the criteria set forth for the Monticello Nuclear Generating Plant (MNGP). This procedure specifically states the requirements for storage of items or equipment that are not restrained or secured to prevent or minimize movement during a seismic event during plant operation. In part, Step 4.3.1B states that loose material SHALL be stored at least three

(3) feet from any operable safety related equipment.

Additionally, Step 4.3.3 states that exceptions to the above policies SHALL require prior approval of the Manager System Engineering. In regards to the storage of these materials, the licensee did not meet either requirement. Once informed, the licensee took action to relocate the material to a proper storage location.

Analysis:

The inspectors reviewed this finding using the guidance contained in Appendix B, Issue Disposition Screening, of IMC 0612, Power Reactor Inspection Reports. The inspectors determined that the licensees failure to control loose material near risk-significant equipment and to appropriately implement their housekeeping procedure was a performance deficiency which affected the Mitigating Systems Cornerstone. The inspectors determined that the finding was more than minor because the loose items located above and adjacent to the Division II LPCI components impacted the Mitigating Systems objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, it affected the cornerstones attribute for the protection against external factors such as seismic events.

The inspectors evaluated the finding using IMC 0609, Appendix A, Attachment 1, Significance Determination of Reactor Inspection Findings for At-Power Situations.

Using the Phase 1 SDP worksheet for the Mitigating Systems Cornerstone the inspectors determined that the finding did not represent a loss or degradation of equipment or function specifically designed to mitigate a seismic, flooding, or severe weather initiating event, nor did it represent a total loss of any safety function, identified by the licensee that contributes to external event initiated core damage accident sequences. Therefore, the finding was determined to be of very low safety significance (Green). This finding had a cross-cutting aspect in the area of Human Performance because licensee personnel failed to determine the potential impact of the unsecured material on the Division II LPCI components during a seismic event as required by station procedures.

Enforcement:

The inspectors concluded that no violation of NRC requirements occurred. The licensee entered this finding into their corrective action program (CAP01032480) and took action to relocate the loose material to an appropriate storage location. (FIN 05000263/2006003-01)

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors performed an annual review of flood protection barriers and procedures for coping with external flooding. The inspection focused on determining whether flood mitigation plans and equipment were consistent with design requirements and risk analysis assumptions. The inspection activities included, but were not limited to, a review and/or walkdown to assess design measures, seals, drain systems, contingency equipment condition and availability of temporary equipment and barriers, performance and surveillance tests, procedural adequacy, and compensatory measures.

The inspectors selected the following equipment for a total of one sample:

  • external flood protection measures.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

The inspectors performed a quarterly review of licensed operator requalification training.

The inspection assessed the licensees effectiveness in evaluating the requalification program, ensuring that licensed individuals operate the facility safely and within the conditions of their license, and evaluated licensed operator mastery of high-risk operator actions. The inspection activities included, but were not limited to, a review of high-risk activities, emergency plan performance, clarity and formality of communications, task prioritization, timeliness of actions, alarm response actions, control board operations, procedural implementation, supervisory oversight, group dynamics, simulator fidelity, and licensee critique of performance.

On June 12, 2006, the inspectors observed the following requalification activity for a total of one sample:

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed a system to assess maintenance effectiveness, including maintenance rule activities, work practices, and common cause issues. Inspection activities included, but were not limited to, the licensee's categorization of specific issues including evaluation of performance criteria, appropriate work practices, identification of common cause errors, extent of condition, and trending of key parameters. Additionally, the inspectors reviewed implementation of the Maintenance Rule (10 CFR 50.65)requirements, including a review of scoping, goal-setting, performance monitoring, short-term and long-term corrective actions, functional failure determinations associated with reviewed CAP documents, and current equipment performance status.

The inspectors performed the following maintenance effectiveness review for a total of one sample:

C an issue-oriented review of the 12 reactor protection system (RPS) motor generator (MG) set system because it was designated as risk-significant under the Maintenance Rule and the system experienced abnormal vibrations and higher than normal temperatures following motor replacement.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed maintenance activities to review risk assessments (RAs) and emergent work control. The inspectors verified the performance and adequacy of RAs, management of resultant risk, entry into the appropriate licensee-established risk bands, and the effective planning and control of emergent work activities. The inspection activities included, but were not limited to, a verification that licensee RA procedures were followed and performed appropriately for routine and emergent maintenance, that RAs for the scope of work performed were accurate and complete, that necessary actions were taken to minimize the probability of initiating events, and that activities to ensure that the functionality of mitigating systems and barriers were performed.

Reviews also assessed the licensee's evaluation of plant risk, risk management, scheduling, configuration control, and coordination with other scheduled risk-significant work for these activities. Additionally, the assessment included an evaluation of external factors, the licensee's control of work activities, and appropriate consideration of baseline and cumulative risk.

The inspectors observed maintenance or planning for the following activities or risk-significant systems undergoing scheduled or emergent maintenance for a total of seven samples:

  • emergent work on 1AR transformer with the 1R transformer out-of-service;
  • emergent work on the reactor recirculation flow recorder;
  • emergent work due to a body to bonnet leak on MO-2014 (Division I LPCI inboard isolation valve);
  • emergent work due to the discovery of an air leak on the actuator for CV-1729 (B RHR heat exchanger service water outlet control valve);
  • emergent work due to unexpected trip of the Division I control room ventilation train during a routine train swap;
  • emergent work to identify and repair the source of water leakage from the stator cooling water system; and
  • emergent trouble shooting efforts on the automatic reactor pressure control systems to identify the cause of a minor pressure transient.

b. Findings

No findings of significance were identified.

1R14 Operator Performance During Non-Routine Plant Evolutions and Events

a. Inspection Scope

The inspectors reviewed personnel performance for planned non-routine evolutions to review operator performance and the potential for operator contribution to the evolution, transient, or event. The inspectors observed or reviewed records of operator performance during the evolution. Reviews included, but were not limited to, operator logs, pre-job briefings, instrument recorder data, and procedures.

The inspectors observed the following evolutions for a total of three samples:

  • a planned rod pattern adjustment requiring a downpower to approximately 75 percent reactor power and the movement of 21 individual control rods;
  • isolation, testing, and restoration of the RHR shutdown cooling suction piping during a required piping system leakage test; and
  • reduction of reactor power to approximately 55 percent to support the replacement of the 12 recirculation MG set brushes.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed operability evaluations which affected mitigating systems or barrier integrity to ensure that operability was properly justified and that the component or system remained available. The inspection activities included, but were not limited to, a review of the technical adequacy of the operability evaluations to determine the impact on technical specifications (TSs), the significance of the evaluations to ensure that adequate justifications were documented, and that risk was appropriately assessed.

The inspectors reviewed the following operability evaluations for a total of three samples:

  • blown control power fuse on B control room ventilation compressor;
  • body to bonnet leakage on the LPCI inboard isolation valve; and
  • settling of the diesel oil pump house, diesel oil storage tank, and the offgas storage building heating and ventilation exhaust pipe.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors verified that the post-maintenance test procedures and activities were adequate to ensure system operability and functional capability. Activities were selected based upon the structure, system, or component's ability to impact risk. The inspection activities included, but were not limited to, witnessing or reviewing the integration of testing activities, applicability of acceptance criteria, test equipment calibration and control, procedural use and compliance, control of temporary modifications or jumpers required for test performance, documentation of test data, system restoration, and evaluation of test data. Also, the inspectors verified that maintenance and post-maintenance testing activities adequately ensured that the equipment met the licensing basis, TS, and Updated Safety Analysis Report design requirements.

The inspectors selected the following post-maintenance activities for review for a total of five samples:

  • replace sudden pressure relay on 1ARS transformer;
  • repair A control room ventilation damper;
  • repair reactor building exhaust plenum radiation monitor RM-17-452A channel;
  • replace brushes on 12 recirculation MG set; and
  • replace dual coil solenoid valve on B condensate demineralizer.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed surveillance testing activities to assess operational readiness and to ensure that risk-significant structures, systems, and components were capable of performing their intended safety function. Activities were selected based upon risk significance and the potential risk impact from an unidentified deficiency or performance degradation that a system, structure, or component could impose on the unit if the condition was left unresolved. The inspection activities included, but were not limited to, a review for preconditioning, integration of testing activities, applicability of acceptance criteria, test equipment calibration and control, procedural use, control of temporary modifications or jumpers required for test performance, documentation of test data, TS applicability, impact of testing relative to performance indicator (PI) reporting, and evaluation of test data.

The inspectors selected the following surveillance testing activities for review for a total of three samples:

  • reactor building to torus vacuum breaker operability check (inservice testing);
  • anticipated transient without scram (ATWS) recirc trips for reactor pressure and level trip unit test and calibration (routine).

b. Findings

Introduction:

A Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion V, was identified by the inspectors when licensee I&C technicians deviated from existing procedural guidance to perform unauthorized post-maintenance tests during the performance of torus vacuum breaker testing. Specifically, maintenance personnel inappropriately cycled the isolation valves to differential pressure transmitters DPIS-2572 and DPIS-2573 to perform leak checks subsequent to the removal of test equipment.

Description:

On April 12, 2006, the inspectors observed the performance of Procedure 0141, Reactor Building to Torus Vacuum Breaker Operability Check, Revision 25. During this procedure, control room operators cycled vacuum relief dampers AO-2379 and AO-2380 and recorded opening and closing times. Additionally, the as-found and as-left trip setting values for the differential pressure indicating switches (DPISs), used to automatically actuate AO-2379 and AO-2380, were also checked.

The inspectors observed the local operation of damper AO-2379 when it was cycled using the control room handswitch, and observed the I&C technicians perform the setpoint checks on the DPIS-2572. This DPIS is used to sense torus vacuum breaker differential pressure and automatically open AO-2379 when a high differential pressure is sensed. To test the DPIS, the I&C technician isolated the pressure source from the torus by shutting Valve I-LE940-P-7, disconnected the high pressure side tubing and connected a pneumatic calibrator to the high pressure side of the DPIS, and artificially induced a high differential pressure to verify the as-found and as-left trip settings. Once the trip settings were verified to be correct, the pneumatic calibrator was removed, high pressure tubing was reinstalled, and Valve I-LE940-P-7 was reopened.

The inspectors noted that the I&C technician deviated from Procedure 0141 when placing DPIS-2572 back in-service. The applicable steps in Procedure 0141 are as follows:

  • STEP 14: Open I-LE940-P-7, Torus/Rx Bldg DP, instrument isolation valve to DPIS-2572.
  • STEP 15: Verify that DPIS-2572 is reading downscale, and verify that the reading is nearly the same as the reading recorded in STEP 1.
  • STEP 16: Seal-wire the instrument isolation valve to DPIS-2572 in the Open position.

Subsequent to STEP 15, the inspectors observed the I&C technicians perform an unauthorized post-maintenance leak test on the tubing connections which were disconnected/reconnected to facilitate test equipment installation. The retest consisted of shutting Valve I-LE940-P-7, monitoring for any upscale trend on DPIS-2572, and, when no trend was observed, re-open I-LE940-P-7. The procedure clearly did not allow for the additional cycling of Valve I-LE-940-P-7, nor did the I&C technicians obtain operations department permission prior to manipulating the valve. The same behavior was observed later in the procedure during an identical sequence of steps used to restore the DPIS associated with AO-2380.

The inspectors immediately communicated their observations to I&C supervision.

Specific corrective actions taken by the licensee included: counseling of responsible technician regarding procedure use and adherence expectations; discussion with the I&C shop personnel to reinforce standards regarding procedure use and adherence, and discussions with the mechanical and electrical maintenance departments which emphasized the proper way to incorporate good practices into existing maintenance procedures. This issue was entered into the licensees corrective action program as CAP01023884.

Analysis:

The inspectors determined that the I&C technicians deviation from existing procedural guidance to perform unauthorized post-maintenance tests during the performance of torus vacuum breaker testing was a performance deficiency warranting a significance evaluation. The inspectors concluded that since the finding could become a more safety significant concern if left uncorrected, it was greater than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued September 30, 2005.

The inspectors evaluated the finding using IMC 0609, Significance Determination Process, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, issued November 22, 2005. The inspectors determined that the finding was of very low safety significance (Green) because the performance deficiency did not result in an actual open pathway in the physical integrity of the reactor containment, or actual reduction in the defense-in-depth for the atmospheric pressure control or hydrogen control functions of the reactor containment. This finding had a cross-cutting aspect in the area of Human Performance because licensee personnel failed to follow established procedures.

Enforcement:

Part 50 of Title 10 of the Code of Federal Regulation, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Contrary to these requirements, during the performance of Procedure 0141, Reactor Building to Torus Vacuum Breaker Operability Check, Revision 25, on two separate occasions, an I&C technician performed unauthorized post-maintenance testing which required additional valve manipulations not prescribed in the procedure. Once notified of the issue, the licensee took action to prevent recurrence of the performance deficiency and entered the issue into their corrective action program (CAP01023884). Because this violation was of very low safety significance and it was entered into the licensees corrective action program, this violation is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy. (NCV 05000263/2006003-02).

1EP2 Alert and Notification System (ANS) Testing

a. Inspection Scope

The inspectors reviewed and discussed with licensee Emergency Preparedness (EP)staff records on the operation, maintenance, and testing of the ANS in the Monticello plants Emergency Planning Zone to determine whether the ANS equipment was adequately maintained and tested during 2004, 2005, and 2006 in accordance with emergency plan commitments and procedures. The inspectors also reviewed a sample of preventative and non-scheduled maintenance records to determine whether ANS equipment malfunctions were given timely attention and whether the corrective action program was adequately used to track these malfunctions. The inspectors reviewed records of scheduled ANS tests conducted from March 2004 through June 2006.

These activities completed one inspection sample.

b. Findings

No findings of significance were identified.

1EP3 Emergency Response Organization (ERO) Augmentation Testing

a. Inspection Scope

The inspectors reviewed and discussed procedures containing details on the primary and alternate methods of initiating an ERO activation to augment the on-shift ERO. The inspectors also discussed the processes and reviewed the procedures for maintaining the Stations ERO roster and the ERO telephone directory. The inspectors reviewed records of quarterly, unannounced, off-hours augmentation tests, which were conducted August 2004 through May 2006 and involved ERO members assigned to the emergency response facilities, to assess the adequacy of the tests and resulting corrective actions.

The inspectors also reviewed records of an additional unannounced, off-hours augmentation drill conducted on June 2, 2004, which involved ERO members actually reporting to their assigned response facilities, to understand how this drills critique resulted in increased consistency between response facilities implementing procedures and the Emergency Plans corresponding minimum staffing commitments.

The inspectors also reviewed the Emergency Call List and the Emergency Preparedness Telephone Directory to verify that good numbers of personnel were assigned to each key and support position. The inspectors reviewed training records of a random sample of 41 ERO members, who were assigned to key and support positions, to verify that they were currently trained for their assigned positions.

These activities completed one inspection sample.

b. Findings

No findings of significance were identified.

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies

a. Inspection Scope

The inspectors reviewed portions of Quality Assurance staffs 2005 and 2006 audits that addressed aspects of the licensees EP program to verify that these independent assessments met the requirements of 10 CFR 50.54(t). The inspectors also assessed the Quality Assurance staffs assessments of the adequacy of the licensees interfaces with State and county emergency management agencies and local support organizations. The inspectors also reviewed records of a sample of EP drills conducted during 2004 and 2005, as well as the May 2005 biennial exercise, to verify that the licensee adequately critiqued these drills and the exercise and to determine if corrective actions on identified concerns were either adequately completed or in progress.

Samples of corrective action program records and completed corrective actions were reviewed to determine whether EP program concerns and issues were adequately addressed.

These activities completed one inspection sample.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors selected emergency preparedness exercises that the licensee had scheduled as providing input to the Drill/Exercise PI. The inspection activities included, but were not limited to, the classification of events, notifications to off-site agencies, protective action recommendation development, and the review of issues identified at the drill critiques. Observations were compared with the licensees observations and corrective action program entries. The inspectors verified that there were no discrepancies between observed performance and PI reported statistics.

The inspectors selected the following emergency preparedness activity for review for a total of one sample:

  • the MNGP Emergency Plant Drill, conducted on May 24, 2006.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

Cornerstones: Mitigating Systems, Barrier Integrity and Emergency Preparedness

.1 Reactor Safety Strategic Area

a. Inspection Scope

The inspectors review of PIs used guidance and definitions contained in Nuclear Energy Institute (NEI) Document 99-02, Revision 4, Regulatory Assessment Performance Indicator Guideline, to assess the accuracy of the PI data. The inspectors review included, but was not limited to, conditions and data from logs, licensee event reports (LERs), CAP documents, and calculations for each PI specified.

The following PIs were reviewed for a total of three samples:

  • Safety System Functional Failures, for the period of July 2004 through March 2006 (Mitigating Systems Cornerstone);

b. Findings

No findings of significance were identified.

.2 Emergency Preparedness Strategic Areas

a. Inspection Scope

The inspectors reviewed the licensees records associated with the three EP performance indicators (PIs) listed below. The inspectors verified that the licensee accurately reported these indicators in accordance with relevant procedures and Nuclear Energy Institute guidance endorsed by the NRC with one minor exception that the licensee planned to correct in its next quarterly PI data submittal. Specifically, the inspectors reviewed licensee records associated with PI data reported to the NRC for the period of April 2005 through March 2006. Reviewed records included: procedural guidance on assessing opportunities for the three PIs; assessments of PI opportunities during pre-designated Control Room Simulator training sessions, the 2005 biennial exercise, and several integrated emergency response facility drills; revisions of the roster of personnel assigned to key ERO positions; and results of ANS operability tests.

The following PIs were reviewed:

  • ERO Drill Participation; and
  • Drill and Exercise Performance.

These activities completed three inspection samples.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the routine inspections documented above, the inspectors verified that the licensee entered the problems identified during the inspection into their CAP.

Additionally, the inspectors verified that the licensee was identifying issues at an appropriate threshold and entering them in the CAP, and verified that problems included in the licensee's CAP were properly addressed for resolution. Attributes reviewed included: complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrence reviews were proper and adequate; and that the classification, prioritization and focus were commensurate with safety and sufficient to prevent recurrence of the issue.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished by reviewing daily CAP summary reports and attending corrective action review board meetings.

b. Findings

No findings of significance were identified.

.3 Annual Sample: Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on apparent cause evaluation (ACE) quality, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.2 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the 6 month period of January 2006 through June 2006, although some examples expanded beyond those dates when the scope of the trend warranted.

Inspectors reviewed adverse trend CAP items associated with various events that occurred during the period. The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and maintenance rule assessments.

The specific items reviewed are listed in the Documents Reviewed section attached to this report. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending documents. Corrective actions associated with a sample of the issues identified in the licensees trend report were reviewed for adequacy.

The inspectors also evaluated the licensees CAP documents against the requirements of the licensees corrective action process as specified in 4 AWI-10.01.03, Action Request Process (FP-PA-ARP-01). Additional documents reviewed are listed in the to this report.

Assessment and Observations The inspectors evaluated the licensee trending methodology and observed that the licensee had performed a detailed review. The licensee routinely reviewed cause codes, involved organizations, key words, and system links to identify potential trends in their CAP data. The inspectors compared the licensee process results with the results of the inspectors daily screening and did not identify any discrepancies.

The licensees CAP identified one issue of potential significance. This issue was related to a potential adverse trend in ACE quality. On February 14, 2006, CAP01014715 was written to document problems noted in root cause evaluation and ACE quality and documentation during a nuclear oversight (NOS) assessment. A second CAP was generated, CAP01015572, which identified a potential adverse trend in ACE quality.

The inspectors recognized that both of these CAPs generated corrective actions to remedy the deficiencies identified by both NOS and licensee personnel. At the conclusion of the current inspection period, several of these corrective action items were still open. Because these corrective actions had not been completed, the inspectors were not able to fully evaluate the effectiveness of the corrective actions.

b. Findings

No findings of significance were identified.

.4 Annual Sample: Recirculation Pump Motor-Generator Set Accelerated Brush Wear

a. Inspection Scope

From July of 2005 through April of 2006, the licensee recorded brush wear rates higher than expected on the generator of the 12 recirculation pump MG set. This accelerated wear had also occurred during the previous cycle and, as a result, the licensee reduced power and entered single loop operation to replace the brushes. The licensee had also previously experienced an unplanned plant trip while attempting to change brushes with the MG set on-line. The inspectors chose to perform an in-depth review of the licensees corrective actions for the previous issues and determine if the licensees actions were appropriately focused to correct the problem. Previous CAPs and work orders (WOs) pertaining to brush issues were also reviewed to ensure that the licensees corrective actions were commensurate with the significance of previously identified issues.

b. Issues The inspectors reviewed LER 85-013-00 which reported an event in which a recirculation pump tripped while the licensee was replacing the recirculation MG set exciter brushes. The licensee committed in this document to revise procedures to prevent recurrence.

The inspectors reviewed CAP033440, Abnormal Brush Wear Noted on No. 12 Recirc MG Set Inbd Collector Ring dated May 1, 2004, which discussed accelerated brush wear. This accelerated wear caused the licensee to reduce power and enter single loop operation to replace the brushes. Prior to 2004, a set of brushes was expected to last an entire fuel cycle. A subsequent cause evaluation was indeterminate as to the cause of the excessive brush wear. The licensee reviewed the available evidence and examined potential causes, but could not identify a specific cause.

The inspectors reviewed CAP040083, Actions Taken to Resolve 2004 Brush Wear Problems May Not Be Effective dated July 28, 2005. This condition action documents the recent issue of accelerated brush wear. The corrective action from this CAP is to install an alteration to facilitate on-line brush replacement. This would mitigate the requirement to enter single loop operation while reducing the risk of an unintended plant trip. This alteration is projected to be installed during the next refueling outage.

During an inspection to measure for the new brush holders, a small oil leak was identified from the outboard end bearing, which is directly adjacent to the brushes that are experiencing the accelerated wear. The licensee initiated CAP01010042, Small Oil Leak From 12 REC MG Outboard Bearing, which noted that the leak could potentially contribute to the accelerated brush wear. The licensee initiated a WO to repair the oil leak. This work is projected to be completed during the next refueling outage.

The inspectors concluded that the licensees actions to date appear to be appropriately focused to correct the problem and were commensurate with the risk-significance of the issues. These corrective actions have not been completed yet as they are scheduled to be completed during the next refueling outage.

No findings of significance were identified.

4OA3 Event Follow-up

.1 (Closed) LER 50-263/2006-001-00: Unplanned LCO [Limiting Condition of Operation]

due to Emergency Filter Flexible Connector Failure On February 2, 2006, the licensee declared both control room EFTs inoperable (see Section 4OA3.1 of Inspection Report 05000263/2006002). The condition was identified subsequent to the automatic tripping of the A EFT, which was caused by the failure of a rubber boot located at the suction of the fan that services the A EFT train. The licensee declared both A and B EFT trains inoperable due to the unevaluated impact that the failure had on the B EFT train and the as-found condition of a similar boot for the B EFT fan. The licensee evaluated these instances to be of very low safety significance because the risk of requiring control room ventilation to be isolated is negligible and degradation of EFT ventilation system reliability (loss of both trains, for example) poses a negligible risk impact. The licensee attributed the cause to a failure by the station to consider the effects of increased operation time on the preventive maintenance frequency for both EFTs. Corrective actions included replacing the rubber boots on the A and B EFT trains and revising the station procedures to increase the replacement frequency for the rubber boots. The LER was reviewed by the inspectors and no findings of significance were identified. The licensee entered this issue into their corrective action program as CAP01013115.

.2 Division I and II 4160 Volt Electrical Busses Inoperable Due to Loss of Ventilation

On May 27, 2006, at 1:10 a.m., the licensee made a 10 CFR 50.72 8-hour non-emergency report which discussed the status of the Division I and II 4160 volt busses. The Division II 4160 volt electrical busses were declared inoperable due to a loss of ventilation which led to room temperature exceeding the 104° F limit. The operators entered the abnormal procedure for loss of ventilation and took compensatory actions to open turbine building doors to provide additional cooling. Upon opening the required doors, operators declared the Division I 4160 volt electrical busses inoperable.

At 5:45 p.m., ventilation was readjusted, all doors were closed, and the Division I and II 4160 volt busses were declared operable.

The inspectors evaluated the licensees initial response to this event, which included actions taken to restore ventilation to the 4160 volt electrical bus rooms. No significant issues were identified during the initial evaluation.

.3 Partial Group 2 Isolation Due to the A Reactor Building Exhaust Plenum Radiation

Monitor Spiking High On June 18, 2006, at 3:07 a.m., the licensee made a 10 CFR 50.72 8-hour non-emergency report which discussed a partial Group 2 isolation due to a spike on the A reactor building exhaust plenum radiation monitor. The radiation monitor signal resulted in a closure of the drywell containment atmosphere monitor and the oxygen analyzer primary containment isolation valves, as well as a reactor building ventilation isolation, start of the A standby gas treatment system, and transfer of the control room ventilation to the high radiation mode.

The inspectors evaluated the licensees initial response to this event, which included actions taken to declare the A reactor building plenum radiation monitor inoperable and place it in a downscale trip condition. No significant issues were identified during the initial evaluation.

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to Mr. Conway and other members of licensee management on July 6, 2006. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

.2 Interim Exit Meetings

Interim exits were conducted for:

4OA7 Licensee-Identified Violations

None.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

J. Conway, Site Vice President
R. Jacobs, Site Director for Operations
B. Sawatzke, Plant Manager
R. Baumer, Licensing
B. Guldemond, Nuclear Safety Assurance Manager
K. Jepsen, Radiation Protection Manager

Nuclear Regulatory Commission

B. Burgess, Chief, Reactor Projects Branch 2

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000263/2006003-01 FIN Improper Loose Material Storage Adjacent to LPCI Components (Section 1R05)
05000263/2006003-02 NCV I&C Technicians Performed Unauthorized Post Maintenance Tests During a Torus to Reactor Building Vacuum Breaker Operability Check (Section 1R22)

Closed

50-263/2006-001-00 LER Unplanned LCO Due to Emergency Filter Flexible Connector Failure (Section 4OA3)

Discussed

None.

Attachment

LIST OF DOCUMENTS REVIEWED