IR 05000321/2019001

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Nuclear Regulatory Commission Integrated Inspection Report 05000321/2019001 and 05000366/2019001
ML19130A209
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 05/10/2019
From: Alan Blamey
NRC/RGN-II/DRP/RPB2
To: Vehec T
Southern Nuclear Operating Co
References
IR 2019001
Download: ML19130A209 (40)


Text

May 10, 2019

SUBJECT:

HATCH UNITS 1, 2 - NUCLEAR REGULATORY COMMISSION INTEGRATED INSPECTION REPORT 05000321/2019001 AND 05000366/2019001

Dear Mr. Vehec:

On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Hatch Units 1, 2. On April 23, 2019 the NRC inspectors discussed the results of this inspection with Richard Spring and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

These findings involved violations of NRC requirements.

If you contest the violations, significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC resident inspector at Hatch.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC resident inspector at Hatch. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Alan J. Blamey, Chief

Reactor Projects Branch 2

Division of Reactor Projects

Docket Nos.: 05000321 and 05000366 License Nos.: DPR-57 and NPF-5

Enclosure:

Inspection Report 05000321/2019001 and 05000366/2019001

Inspection Report

Docket Number(s):

05000321 and 05000366

License Number(s):

DPR-57 and NPF-5

Report Number(s):

05000321/2019001 and 05000366/2019001

Enterprise Identifier: I-2019-001-0026

Licensee:

Southern Nuclear Operating Co., Inc.

Facility:

Hatch, Units 1 and 2

Location:

Baxley, GA 31513

Inspection Dates:

January 01, 2019 to March 31, 2019

Inspectors:

B. Collins, Reactor Inspector

C. Dykes, Health Physicist

J. Hickman, Resident Inspector

C. Jones, Senior Resident Inspector

W. Loo, Senior Health Physicist

W. Pursley, Health Physicist

J. Viera, Operations Engineer

M. Greenleaf, Resident Inspector

P. Cooper, Reactor Inspector

Approved By:

Alan J. Blamey, Chief

Reactor Projects Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a Quarterly inspection at Hatch Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and violations being considered in the NRCs assessment are summarized in the table below.

List of Findings and Violations

Failure to Brief Worker of Radiation Dose Rate Levels Prior to Entering a High Radiation Area Cornerstone Significance Cross-cutting Aspect Report Section Occupational Radiation Safety Green NCV 05000321,05000366/2019001-01 Open/Closed

[H.5] - Work Management 71124.01 A self-revealing, Green, Non-Cited Violation (NCV) of Technical Specifications 5.7.1.b was identified when a worker entered a high radiation area (HRA) near the N2NG nozzle piping on the 156 foot elevation of the Unit 2 (U2) drywell without receiving an accurate briefing on radiological conditions and consequently the worker received a dose rate alarm in the drywell.

Failure to apply engineering controls in accordance with plant procedures to minimize potential concentrations of radioactive material in air.

Cornerstone Significance Cross-cutting Aspect Report Section Occupational Radiation Safety Green NCV 05000366,05000321/2019001-02 Open/Closed

[H.5] - Work Management 71124.0

NRC Identified

a Green NCV of 10CFR 20.1701, Use of process or other engineering controls, for the licensees failure to use a High Efficiency Particulate Air Filter (HEPA) unit as prescribed by plant procedures.

Additional Tracking Items

Type Issue number Title Report Section Status URI 05000321,05000366

/2017007-01 Potential Failure to Adequately Justify the Activation Energies by Licensee 71111.21N Closed URI 05000321,05000366

/2017007-02 Potential Failure to Adequately Justify the Activation Energies Determined by 10 CFR 50 Appendix B Vendors 71111.21N Closed

PLANT STATUS

Unit 1 began the inspection period at 100 percent rated thermal power (RTP). On January 13, 2019, the unit was down powered to 80 percent due to an air intrusion event from the condensate system. On January 14, 2019, the unit was returned to 100 percent RTP and operated there for the remainder of the inspection period.

Unit 2 began the inspection period at 95 percent RTP in the end of cycle coast down for the spring 2019 refueling outage. On February 4, 2019, the operators shut the unit down for a scheduled refueling outage. The unit was restarted on March 18, 2019, and reached approximately 97 percent RTP on March 24, 2019, when the operators took manual action to insert a scram due to a loss of condenser vacuum. The unit was restarted on March 27, 2019, and reached 100 percent RTP on March 31,

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.03) (1 Sample)

The inspectors evaluated readiness for impending adverse weather conditions for extended below freezing temperatures on January 29, 2019.

71111.04 - Equipment Alignment

Partial Walkdown (IP Section 02.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Main control room environmental control system on January 31, 2019.
(2) Unit 2 'C' emergency diesel generator (EDG) following Logic System Functional Test on March 4, 2019.
(3) Unit 2 high pressure coolant injection (HPCI) system following return to service testing on March 20, 2019.

71111.04S - Equipment Alignment

Complete Walkdown (IP Section 02.02) (1 Sample)

The inspectors evaluated system configurations during a complete walkdown of the Torus spray system following 42SV-E11-007-2, Air Test On Torus Headers and Nozzles on February 22, 2019.

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (6 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Unit 1 and 2, station battery rooms, fire zones: 1004, 1005, 2004, and 2005, on January 24, 2019.
(2) Unit 2 north and south Torus, fire zones 2203A and 2205A on February 19, 2019.
(3) Unit 2 main steam chase, fire zone 2205H on February 20, 2019.
(4) Unit 2 south east residual heat removal (RHR) & core spray pump room, fire zone 2205B on February 25, 2019.
(5) Unit 2 control rod drive (CRD) pump room, fire zone 2205C on February 26, 2019.
(6) Unit 2 HPCI room, fire zone 2205Z on February 26, 2019.

71111.06 - Flood Protection Measures

Inspection Activities - Underground Cables (IP Section 02.02c.) (1 Sample)

The inspectors evaluated cable submergence protection in:

Safety related cable vaults PB2-AP, PB2-AO, PB2-AN, PB2-AM, and PB2-G.

71111.08G - Inservice Inspection Activities (BWR)

BWR Inservice Inspection Activities Sample - Nondestructive Examination and Welding

Activities (IP Section 03.01)

The inspectors evaluated boiling water reactor non-destructive testing by reviewing the following examinations from February 11 to February 15, 2019:

03.01.a - Nondestructive Examination and Welding Activities.

1. Ultrasonic Examination (UT)

a. 12" feedwater elbow-to-pipe weld (2B21-1FW-12AB-9), ASME Class 2, manual UT (observed).

2. Liquid Penetrant Examination (PT)

a. Work Order (WO) 948451, two 6 plant service water pipe-to-pipe welds (FW-1/ and FW-2/SNC948451-SK1), ASME Class 3 (reviewed; associated with welding package, which was also reviewed).

b. two 6 control rod drive mechanism housing pipe-to-pipe welds (2B11/2-50-19-1, 2B11/2-50-23-1), ASME Class 1 (observed).

3. Magnetic Particle Examination (MT)

a. four pipe lugs near 20 residual heat removal pipe-to-pipe weld (2-E11-2RHR-20-RS-2PL), ASME Class 2 (observed).

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

The inspectors observed and evaluated licensed operator performance in the Control Room during final feedwater temperature reduction, Unit 1 power ascension from 83% to 100%

following an air intrusion event, Unit 2 control rod scram testing, and the restoration of the Unit 2 4160VAC System on January 10 & 14, and March 11 & 13, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

The inspectors observed and evaluated a crew of licensed operators in the plant's simulator during licensed operator requalification training on January 10, 2019.

Inspectors evaluated the facility program for licensed SRO reactivations associated with outage related refueling floor management activities on February 26, 2019. Inspection activities remain in progress with closure planned in a future report.

71111.12 - Maintenance Effectiveness

Quality Control (IP Section 02.02) (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:

Fire Main Rupture Repairs on January 27, 2019.

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (2 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1)2B Station Service Air Compressor spurious trips on January 25, 2019.

(2) Maintenance rule functional failure of the S11-01 power transmission function on the 1C startup transformer (SUT) on February 23, 2019.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 2 risk during final feedwater temperature reduction and several heavy lifts onsite on January 9, 2019.
(2) Unit 1 and Unit 2 elevated risk during a conservative system operation warning while switchyard work was ongoing on March 5, 2019.
(3) Unit 1 and Unit 2 risk during drywell plug installation on March 13, 2019.
(4) Unit 2 risk during reactor startup mode changes while one of two reactor core isolation cooling (RCIC) room coolers were out of service on March 19, 2019.

71111.15 - Operability Determinations and Functionality Assessments

Sample Selection (IP Section 02.01) (8 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 2, 2A EDG operability determination following failure of the fuel lines to hold pressure during pressure testing per WO SNC948747 on January 24, 2019.
(2) Unit 1, 1A plant service water (PSW) pump operability determination following discovery of the wrong bolts installed during the visual inspection of seismic supports per WO SNC917621 on January 29, 2019.
(3) Unit 1, 2B standby gas treatment (SBGT) operability determination following indication issues during the logic system functional testing (LSFT) per 34SV-T46-005-2, SBGT LSFT, Ver. 1.0, on January 31, 2019.
(4) Unit 2, 2A Core Spray (CS) pump operability determination following discovery of cut stress cone and exposed wiring after tape removal prior to motor replacement per WO SNC926452 on January 31, 2019.
(5) Unit 1, 1B EDG operability determination following 1B EDG voltage exceeded the acceptance criteria of 4800VAC following a load reject during performance of 34SV-R43--21-2, 1B EDG LOCA/LOSP LSFT on February 18, 2019.
(6) Unit 1, 2B SBGT operability determination following failure to start during periodic performance of 34SV-T46-003-2, Standby Gas Treatment Ventilation and Operability Ver. 11.2, on February 27, 2019.
(7) Unit 2, 2C EDG operability determination following 86G relay lockout exceeding the acceptance criteria during performance of 34SV-R43-022-2, Diesel Generator 2C LOCA/LOSP LSFT Ver. 2.2, on March 1, 2019.
(8) Unit 2, RCIC operability determination following RCIC pump speed response was not as expected and Turbine Cooling Water Supply Valve motor tripped on overload per WO SNC1008315 on March 26, 2019.

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (3 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Design change package (DCP) SNC489864, Degraded Grid modifications to Unit 2.
(2) DCP SNC996054, Power Cell Part Replacement for Adjustable Speed Drive (ASD),

Rev. 1.0, following non-availability of the original parts.

(3) DCP SNC494055, Units 1 & 2 Intermediate Range Monitor Signal Filter Circuit Improvement.

71111.19 - Post Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (8 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Unit 2, Loop A RHR pump operability test following the replacement of 2A RHR pump cabling, 34SV-E11-001-2, Residual Heat Removal Pump Operability, Ver. 20.2 on January 30, 2019.
(2) Diesel Generator 1B Logic System Functional Test, 34SV-R43-024-2, Ver.

3.0, following 2F switchgear degraded grid modification on February 15, 2019.

(3)34SV-R43-022-2, Diesel Generator 2C LOCA/LOSP LSFT, Ver. 2.1 after Degraded Grid modifications performed on Unit 2, February 23, 2019.

(4) Unit 2, drywell return air fan replacement and testing after removing the temporary modification from the 2018 forced outage per WO SNC936300 on February 26, 2019.
(5) Visual Inspection of 2C EDG engine/generator coupling after wrong phase connections of 2C startup transformer (SUT), potential transformers and improper parallel between 2C EDG and 2C SUT, WO SNC1001043 on February 27, 2019.

(6)34SV-E11-010-2, Residual Heat Removal System LPCI LSFT & Auto Actuation, Ver.

3.0 after replacement of the 2D RHR pump motor on March 3, 2019.

(7) Unit 2, 34 SV-E41-005-2, HPCI Operability 165# Test, Ver. 7.13 after repairs made to HPCI auxiliary oil pump breaker connectors, WO SNC1006582, on March 20, 2019.

(8)57SV-S32-002-2, Emergency Buses 2E, 2F, and 2G Undervoltage Relay FT&C, Ver.

14.1 after low voltage on 2G emergency bus alarm received during pump start, WO SNC1000394, February 22, 2019.

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (2 Samples)

(1) The inspectors evaluated the Unit 2 refueling outage H2R26 activities from Feb. 4, 2019 to Mar. 20, 2019.
(2) The inspectors evaluated a Unit 2 forced outage due to a loss of condenser vacuum from March 23, 2019 to March 29, 2019.

===71111.21N - Design Bases Assurance Inspection (Programs)

The inspectors evaluated environmental qualification program information to facilitate closure of the unresolved items (URIs) opened on October 13, 2017, in Design Bases Assurance Inspection (Programs) Report 05000321, 366/2017007 (ADAMS Accession No. ML17286A528).

Select Sample Components to Review - Risk Significant/Low Design (Inside/Outside Containment) (IP Section 02.01) (2 Partials)

(1)

(Partial) 1R24S011 AMC, 600 V motor control center (MCC) 1C.

(2)

(Partial) 1C11D001-0611 solenoid operated valve (SOV), C11-D001EP117, control rod drive (CRD) hydraulic control unit (HCU) SCRAM SOV.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Containment Isolation Valve (ISO) (IP Section 03.01)===

A and C main steam isolation valve (MSIV) local leak rate test (LLRT). 42SV-TET-001-0, LLRT Testing Methodology, Ver. 13.0 and 42SV-TET-001-2, Primary Containment Periodic Type B and Type C Leakage Tests, Ver. 37.1 on February 19, 2019.

In Service Testing (IST) (IP Section 03.01) (1 Sample)

34SV-P41-001-2, Plant Service Water Pump Operability, Ver. 15.0 on January 4, 2019.

Surveillance Testing (IP Section 03.01) (6 Samples)

(1)

(2)34SV-E11-001-1, Residual Heat Removal Pump Operability, Ver. 27.0 on January 16, 2019.

42SP-09-18-17-RM-1-2, Unit 2 Startup Transformer 2E (SUT 2E) Functional Test, Version 1.2 on February 12, 2019.

(3)42SV-E11-007-2, Air Test on Torus Headers and Nozzles, Ver. 1.8 on February 21, 2019.

(4)34SV-R43-003-1, 1C, Diesel Generator 1C Monthly Test, Ver. 20.0 on February 25, 2019.

(5)34SV-C11-010-2, Alternate Rod Insertion LSFT, Ver. 1.0 on March 8, 2019.

(6)52SV-R42-011-2, Unit 2 Station Service Battery Combined Service Performance /

Modified Performance Test, Ver. 5.0 on March 12,

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Contamination and Radioactive Material Control (IP Section 02.03) (1 Sample)

The inspectors evaluated licensee processes for monitoring and controlling contamination and radioactive material. The inspectors verified the following sealed sources are accounted for and are intact:

  • J.L. Shepherd and Associates, Model 6810 Calibrator, Serial No. 79CS-513.
  • J.L. Shepherd and Associates, Model 89-400 Calibrator, Serial No. 0302GY.

High Radiation Area and Very High Radiation Area Controls (IP Section 02.05) (1 Sample)

The inspectors evaluated risk-significant high radiation area and very high radiation area controls.

Instructions to Workers (IP Section 02.02) (1 Sample)

The inspectors evaluated instructions to workers including radiation work permits used to access high radiation areas:

Radiation Work Packages (RWP)

  • RWP No. 19-2013, Reactor Building (RB) - Remove, Replace Torus Proper Hatches, Radiation Protection (RP) Initial Entry, Foreign Material Exclusion (FME)/Access Control Monitor, Coatings/Painting and Support Activities and Diving Activities.
  • RWP No. 19-2209, Refuel Floor Vessel Disassembly/Reassembly, Cavity Work and Support.
  • RWP No. 19-2601, Drywell (DW)/Suppression Chamber (SC) RP and Chemistry Inspection, Surveillance, Sampling, Surveys and Job Coverage.
  • RWP No. 19-2604, DW/SC Operations Inspection, Surveillance, Clearances, LLRT, Valve Line-Ups Includes HCUs/Tip Room and Torus.

Electronic alarming dosimeter alarms

  • 2 electronic dosimeter (ED) alarms, Event Date: 02/04/19
  • ED alarm, event date: 02/06/19

Labeling of containers

  • Unit 2 drywell, units 1 and 2 reactor buildings, waste separation and temporary storage facility

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 02.06) (1 Sample)

The inspectors evaluated radiation worker performance and radiation protection technician proficiency.

Radiological Hazard Assessment (IP Section 02.01) (1 Sample)

The inspectors evaluated radiological hazards assessments and controls. The inspectors reviewed the following:

Radiological surveys

  • Unit 2 Condenser Bay 112 (2TB112), Survey No. 165254
  • Unit 2 Drywell (2DW156), Survey No. 165407
  • Unit 2 Reactor Cavity (2RX228), Survey No. 165263

Risk significant radiological work activities

  • Valve lineup of F45A/120 (drywell ventilation fan)
  • Initial entry for Torus diving

Air sample survey records

  • Air Sample Record No. 19-035-4, Unit 2 Refuel Floor, General Area
  • Air Sample Record No. 19-036-3, Unit 2 Refuel Floor, Disassembly/General Area

Radiological Hazards Control and Work Coverage (IP Section 02.04) (1 Sample)

The inspectors evaluated in-plant radiological conditions during facility walkdowns and observation of radiological work activities.

Radiological work package for areas with airborne radioactivity

  • Removal of reactor vessel pressure head

71124.02 - Occupational ALARA Planning and Controls

Implementation of ALARA and Radiological Work Controls (IP Section 02.03) (1 Sample)

The inspectors reviewed as low as reasonably achievable (ALARA) practices and radiological work controls by reviewing the following activities:

  • RWP # 19-2209, 2R24 U2 Reactor Disassembly and Reassembly.
  • RWP # 19-2609, 2R24 In service Inspection (ISI)/Flow Accelerated Corrosion (FAC)

Inspections.

Radiation Worker Performance (IP Section 02.04) (1 Sample)

The inspectors evaluated radiation worker and radiation protection technician performance during reactor head disassembly activities, drywell activities and ISI inspections.

Radiological Work Planning (IP Section 02.01) (1 Sample)

The inspectors evaluated the licensees radiological work planning by reviewing the following activities:

  • ALARA Plan # 19-2209, 2R25 U2 Reactor Disassembly and Reassembly.
  • ALARA Plan # 19-2609, 2R25 ISI/FAC Inspections.
  • ALARA Plan # 19-2615, 2R25 Drywell/CRD Exchange and Support Activities.

Verification of Dose Estimates and Exposure Tracking Systems (IP Section 02.02) (1 Sample)

The inspectors evaluated dose estimates and exposure tracking. The inspectors reviewed the following ALARA planning documents:

  • ALARA Plan # 19-2209, 2R24 U2 Reactor Disassembly and Reassembly.
  • ALARA Plan # 19-2609, 2R24 ISI/FAC Inspection.
  • ALARA Plan # 19-2615, 2R24 Drywell/CRD Exchange and Support Activities.

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Engineering Controls (IP Section 02.01) (1 Sample)

The inspectors evaluated airborne controls and radioactive monitoring. The inspectors reviewed the following.

Installed ventilation systems

  • Plant Hatch refueling floor ventilation.

Temporary ventilation system setups

Portable or installed monitoring systems

  • AMS-4 #1879 on U-1 RX-185, Calibrated 07/70/2018.
  • AMS-4 #1901 on U-2 R/F Floor, Calibrated 04/30/2018.

Self-Contained Breathing Apparatus (SCBA) for Emergency Use (IP Section 02.03) (1 Sample)

The inspectors evaluated SCBA program implementation.

Status and surveillance records for SCBAs

  • Observed inventory of SCBA kits in the control room and reviewed NMP-HP-501-004, Data Sheet 2, monthly "In-Service SCBA Inspection," performed 02/28/2019.

SCBA fit for on-shift operators

  • Reviewed training plan for SCBA qualifications and discussed verified spectacle kits and mask size availability for operators in the control room.

SCBA maintenance check

  • Complete SCBA Test MAS Firehawk 3000 S/N AMZ050191, dated 11/18/2018.
  • Complete SCBA Test MAS Firehawk 3000 S/N AMY165843, dated 09/26/2018.
  • Complete SCBA Test MAS Firehawk 3000 S/N AMZ051237, dated 09/27/2018.

Use of Respiratory Protection Devices (IP Section 02.02) (1 Sample)

The inspectors evaluated respiratory protection. The inspectors reviewed the following:

Evaluations for the use of respiratory protection

  • None were available during this inspection.

Respiratory protection use during work activities

  • Reactor vessel disassembly
  • Condenser bay welding activities

Medical fitness for use of respiratory protection devices

  • 2 operators on shift
  • 2 RP technicians

Observation of donning, doffing and functional test

  • Welders in condenser bay donning/doffing welding hoods
  • Workers entering/exiting drywell
  • Workers on reactor head activities

Respiratory protection device evaluation

  • Powered air purifying respirators staged for issue
  • MSA air purifying respirators for emergency use
  • SCBAs in control room for emergency use

71124.04 - Occupational Dose Assessment

External Dosimetry (IP Section 02.02) (1 Sample)

The inspectors evaluated the external dosimetry program implementation.

Internal Dosimetry (IP Section 02.03) (1 Sample)

The inspectors evaluated the internal dosimetry program implementation.

Whole Body Counts

  • Body count personnel contamination event (PCE) #774, 02/07/19
  • Body counts PCE #780, 2/22/19
  • Body counts PCE #779, 2/22/19

In-vitro internal monitoring

  • None available during the inspection period.

Dose assessments performed using air sampling and derived air concentration (DAC)-hr monitoring

  • PCE #779 DAC-hr evaluated no dose assigned.

Source Term Categorization (IP Section 02.01) (1 Sample)

The inspectors evaluated the licensees characterization of the source term and use of scaling factors for the use of hard-to-detect radionuclide activity.

Special Dosimetric Situations (IP Section 02.04) (1 Sample)

The inspectors evaluated special dosimetric situations.

Declared Pregnant Workers (DWP)

  • DPW #1 declaration end date 3/2019
  • DPW #2 declaration end date 11/2018

EDEX exposures

  • Multibadging was not used during the inspection period.

Shallow Dose Equivalent

  • None available for the inspection period.

Neutron Dose Assessment

  • Unit 1 Drywell Access-November 2018
  • Unit 2 Drywell Access-February 2019
  • Dry Cask Storage-November 2018

71124.05 - Radiation Monitoring Instrumentation

Calibration and Testing Program (IP Section 02.02) (1 Sample)

The inspectors evaluated the calibration and testing program implementation.

Alarm setpoint and calibration method check of personnel contamination monitors, portal monitors and small article monitors:

  • Small Article Monitor (SAM) 12 D21-N2024
  • Gamma exit monitor (GEM) 5 1301-013 D21-N1900
  • Argos 5AB 1301-013 D21-N1903

Failure to meet calibration or source check acceptance criteria

  • HandE Count #554

Walk Downs and Observations (IP Section 02.01) (1 Sample)

The inspectors evaluated radiation monitoring instrumentation during plant walkdowns.

Portable survey instruments

  • Electra #1548, calibration dates 2/3/17, 2/7/18
  • RM25 # 702, calibration dates 6/6/17, 5/4/18
  • Telepole # 0116, calibration dates 9/21/18, 9/5/17
  • Eberline RO-20 #4566, 7/11/18
  • RM25 #689, 5/3/18 Source check demonstration
  • Telepole
  • Microrem
  • RO-20
  • Eberline E-20
  • Electra, RO-2A

Area radiation monitors and continuous air monitors

  • AMS-4 D21-N1754 #1876 (particulate) Cal 04/13/18, #1901 (iodine)
  • AMS-4 D21-N1745, 04/06/17

Personnel contamination monitors, portal monitors and small article monitors

  • Argos 5AB PESB
  • GEM 5 PESB
  • ARGOS 5AB Control Point
  • GEM 5 Control Point
  • SAM 11 Control Point

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) Unit 1 from January 1, 2018 to December 31, 2018.
(2) Unit 2 from January 1, 2018 to December 31, 2018.

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (2 Samples)

(1) Unit 1 from January 1, 2018 to December 31, 2018.
(2) Unit 2 from January 1, 2018 to December 31, 2018.

IE04: Unplanned Scrams with Complications Sample (IP Section 02.03) (2 Samples)

(1) Unit 1 from January 1, 2018 to December 31, 2018.
(2) Unit 2 from January 1, 2018 to December 31, 2018.

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) Unit 1 from March 2018 through December 2018.
(2) Unit 2 from March 2018 through December 2018.

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences

Sample. (IP Section 02.16) (1 Sample)

(1) Unit 1 from March 2018 through December 2018.
(2) Unit 2 from March 2018 through December 2018.

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

Unit 2, potential transformer wiring at 2C startup transformer (SUT) did not match drawing SNC489862E101, Condition Report (CR)

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

===71003 - Post-Approval Site Inspection for License Renewal

The inspectors reviewed a sample of license renewal activities to verify that the licensee completed the necessary actions to comply with the conditions listed in the renewed facility operating license.

Post-Approval Site Inspection for License Renewal===

1. Treated Water Systems Piping Inspection Program (UFSAR Section 18.4.2)

a. Ultrasonic Testing (UT), 2E21F002B, Group A-1, 14 Carbon Steel b. UT, 2N22F367, Group A-2, 2.5 Carbon Steel c. UT, 2E21F020A, Group A-3, 2 Carbon Steel d. UT, 2E41F3029B, Group B-1, 1 Stainless Steel e. UT, CRD HCU46-43, Group B-1, 3/4 Stainless Steel f.

UT, 2B21F015, Group B-3, 3/4 Stainless Steel

2. Gas System Components Inspection (UFSAR Section 18.4.3)

a. UT, 2Y52A001C, Group A, Carbon Steel Tank b. UT, 2G11F019, Group A, 3 Carbon Steel Pipe c. UT, 2E41F3029A, Group B, 1 Stainless Steel Pipe d. Visual Exam (VE), 2T41B002A/B, Group C, Room Coolers e. VE, 2R43R003A, Group D, Internal

INSPECTION RESULTS

Minor Violation 71111.21N Minor Violation: The licensees failure to maintain an auditable qualification record in accordance with 10 CFR 50.49(j) was a performance deficiency. Specifically, the qualification test report for the scram solenoid pilot valves did not document the basis for the activation energy value used for its diaphragm elastomer (Viton) subcomponent.

The scram solenoid pilot valves (SSPV) safety function was to change position to allow the control rods to be inserted during a reactor trip. The licensee's qualification test report for these valves did not document the basis for the activation energy value used for its diaphragm elastomer subcomponent. The licensees EQ specification stated, in part, that the contractor clearly identifies and documents the aging characteristics (e.g. activation energy) of all age sensitive components and provides detailed description, auditable analysis, and justification of how the accelerated aging characteristics were established. After the inspection had concluded, the licensee was able to contact the SSPV vendor and retrieve the missing information.

10 CFR 50.49(j) requires, in part, that an auditable record be maintained to permit verification that equipment important to safety subject to 10 CFR 50.49 are qualified to perform their safety function during and following a design bases accident. Contrary to the above, the licensee failed to maintain an auditable record when they were unable to produce the necessary documentation to permit verification that the SSPVs were qualified as required.

Screening: The inspectors determined the performance deficiency was minor. This performance deficiency was screened in accordance with Inspection Manual Chapter (IMC)0612 Appendix B, "Issue Screening," dated January 1, 2018, and was determined to be of minor significance because the failure to maintain the record in an auditable manner could not be reasonably viewed as a precursor to a significant event, would not have the potential to lead to a more significant safety concern if left uncorrected, did not relate to a performance indicator that would have caused the performance indicator to exceed a threshold, and did not adversely affect a cornerstone objective. Specifically, the licensee was ultimately able to retrieve the missing information in the qualification test report.

Enforcement:

This failure to comply with 10 CFR 50.49(j) constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy. The licensee has taken actions to restore compliance.

Minor Violation 71111.21N Minor Violation: The licensee's failure to maintain an auditable qualification record in accordance with 10 CFR 50.49(j) was a performance deficiency. Specifically, the licensee misidentified the material of construction (and therefore activation energy) of the SSPV needle obturator.

The scram solenoid pilot valves (SSPVs) safety function was to change position to allow the control rods to be inserted during a reactor trip. Inspectors determined that the licensees calculation, BH1-CS-0035, Rev. 2, attributed an activation energy for their SSPV needle obturator to that of a Nylon/glass fiber composite material. The actual material used in the obturator, Zytel 103, was a Nylon 6/6 material that lacked any glass fiber reinforcement. Due to this discrepancy, an incorrect activation energy was assigned by the licensee for this needle.

10 CFR 50.49(j) requires, in part, that a record of qualification must be maintained in an auditable form to permit verification that each item of electric equipment important to safety covered by 10 CFR 50.49 is qualified for its application and meets its performance requirements when subjected to the conditions predicted to be present when it must perform its safety function up to the end of its qualified life. Contrary to the above, the failure to maintain accurate calculations limiting the qualified life of the SSPVs failed to permit verification that the SSPVs were qualified for their application and that they meet their performance requirements when subjected to the conditions predicted to be present when they must perform their safety function.

Screening: The inspectors determined the performance deficiency was minor. This performance deficiency was screened in accordance with Inspection Manual Chapter (IMC)0612 Appendix B, "Issue Screening," dated January 1, 2018, and was determined to be of minor significance because the failure to use the proper material in the analysis could not be reasonably be viewed as a precursor to a significant event, would not have the potential to lead to a more significant safety concern if left uncorrected, did not relate to a performance indicator that would have caused the performance indicator to exceed a threshold, and did not adversely affect a cornerstone objective. Specifically, the failure to have a technical justification for the needle obturators activation energy did not adversely affect the designated qualified lives of the SSPVs.

Enforcement:

This failure to comply with 10 CFR 50.49(j) constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy. The licensee has taken actions to restore compliance.

Minor Violation 71111.21N Minor Violation: The licensees failure to justify the basis by which the activation energy was established for Bussman/Gould fuses installed in motor control center 1R24S011 was a performance deficiency. Specifically, the licensee used activation energies taken from an Appendix B vendors database without justifying that the activation energies selected were applicable to the materials or failure mechanisms present in the fuses.

Bussman/Gould fuses are used in 600 V motor control centers which connect to safety-related equipment used in the mitigation of design basis events. The inspectors noted that on August 21, 2001, the licensee updated qualified life calculation SMNH-89-035 for the Bussman/Gould fuses by mixing qualification testing performed by two separate Appendix B vendors, Nutherm International and Wyle Laboratories. Nutherm qualified the fuses using a high temperature/long time aging regime, coupled with a low activation energy to obtain a qualified life of approximately 15 years. Wyle qualified the fuses using a low temperature/short time aging regime, coupled with a high activation energy to obtain a qualified life of approximately 15 years. In calculation SMNH-89-035, the licensee replaced the activation energies established by Nutherm with the values established by Wyle. This combined data from the two vendors resulted in a qualified life of over 100 years for the fuses.

The inspectors determined that licensee calculation SMNH-89-035 did not establish that the updated activation energies selected were suitable and/or applicable to replace the existing values. Specifically, the calculation did not demonstrate that the values were based on the same material, failure parameters or degradation mechanisms as the activation energies originally chosen.

10 CFR 50.49(j) requires, in part, that a record of qualification must be maintained in an auditable form to permit verification that each item of electric equipment important to safety is qualified for its application and meets its specified performance requirements. Contrary to the above, the licensee failed to maintain a record of qualification that demonstrated that the fuses were qualified for their application and that they met their specified performance requirements when the licensee's calculation failed to ensure that the activation energies selected from the Wyle Aging Library were appropriate for their fuses' materials of construction.

Screening: The inspectors determined the performance deficiency was minor. This performance deficiency was screened in accordance with Inspection Manual Chapter (IMC)0612 Appendix B, "Issue Screening," dated January 1, 2018, and was determined to be of minor significance because in this case the failure to ensure the updated activation energies were suitable could not be reasonably be viewed as a precursor to a significant event, would not have the potential to lead to a more significant safety concern if left uncorrected, did not relate to a performance indicator that would have caused the performance indicator to exceed a threshold, and did not adversely affect a cornerstone objective. Specifically, the licensee was able to use test data and activation energies provided by the original Appendix B vendor, along with actual plant temperatures, to establish a qualified life longer than the licensees current license period.

Enforcement:

This failure to comply with 10 CFR 50.49(j) constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy. The licensee has taken actions to restore compliance.

Unresolved Item (Closed)

Potential Failure to Adequately Justify the Activation Energies by Licensee 05000321,05000366/2017007-01 71111.21N

Description:

unresolved item (URI) 05000321, 366/2017007-01 was opened in inspection report 05000321, 366/2017007 (Agency wide Documents Access and Management System (ADAMS) Accession No. ML17286A528) to determine if a performance deficiency existed and if that performance deficiency was more than minor for the licensee's potential failure to justify the activation energies of their scram solenoid pilot valve (SSPV) Zytel needle obturator and their 600 V motor control center (MCC) (1R24S011) fuses.

The inspectors performed additional inspection and review of licensee-supplied additional documentation, as well as consulted with NRC staff via environment qualification panel discussions. Based upon information provided to the inspectors as well as the industry (see Agency wide Documents Access and Management System (ADAMS) Accession No.

ML18338A088 and ML19036A556), and based upon the results of the panel discussions, the inspectors determined that two minor violations of 10 CFR 50.49(j) existed.

Specifically, a minor violation was identified by the inspectors with regard to the basis of the activation energy of the SSPV needle obturator. The licensee mis-identified the material of construction (and therefore the activation energy) of the SSPV needle obturator. An additional minor violation was identified by the inspectors for the licensee's failure to ensure that the activation energies that were used for their MCC fuses was applicable to the materials of fuse construction when they revised them to higher (less conservative) values.

These violations were determined to be minor because even though the licensee had not documented all necessary information to justify qualification, the incomplete or undocumented information was determined to not adversely impact the licensee's determination of qualification for the SSPVs and the MCC fuses.

The licensee generated two condition reports and intends to revise the necessary qualification documentation to include the missing information and correct the incorrect information.

Corrective Action Reference(s): 10593732 10593733

Unresolved Item (Closed)

Potential Failure to Adequately Justify the Activation Energies Determined by 10 CFR 50 Appendix B Vendors 05000321,05000366/2017007-02 71111.21N

Description:

unresolved item (URI) 05000321, 366/2017007-02 was opened in inspection report 05000321, 366/2017007 (Agency wide Documents Access and Management System (ADAMS) Accession No. ML17286A528) to determine if a performance deficiency existed for the licensee's potential failure to have an adequate justification for the activation energies of their ASCO scram solenoid pilot valve (SSPV) diaphragms and their 600 V motor control center (MCC) subcomponents, when that qualification work was performed by their Appendix B vendors. Specifically, inspectors were concerned that the basis was incomplete with respect to the requirements of 10 CFR 50.49.

Inspectors reviewed additional information provided by the licensee, performed further inspection, and held discussions with an NRC environmental qualification panel to resolve this URI. Additionally, the inspectors reviewed the updated guidance in ADAMS Accession Number ML18338A088 and Inspection Manual Chapter Inspection Procedure 71111.21N (Accession No. ML19036A556), which stated that:

"Beyond ensuring that vendor programs satisfy the 10 CFR Part 50, Appendix B, requirements and confirming that EQ equipment is received as procured, licensees are not required to validate information (e.g., activation energy) contained in the EQ reports provided by Appendix B vendors."

Based on the additional review and the above mentioned guidance, the inspectors identified one minor violation of 10 CFR 50.49(j) for the missing references to the basis for the activation energy of the Viton material in the SSPVs. With regard to the qualification work presented by NLI for the various MCC components, the inspectors did not identify a performance deficiency.

The licensee generated a condition report to address this minor violation and condition adverse to quality and plans to update their qualification documentation to include the missing information.

Corrective Action Reference(s): 10593734 Failure to Brief Worker of Radiation Dose Rate Levels Prior to Entering a High Radiation Area Cornerstone Significance Cross-cutting Aspect Report Section Occupational Radiation Safety

Green NCV 05000321,05000366/2019001-01 Open/Closed

[H.5] - Work Management 71124.01 A self-revealing, Green, Non-Cited Violation (NCV) of Technical Specifications 5.7.1.b was identified when a worker entered a high radiation area (HRA) near the N2NG nozzle piping on the 156 foot elevation of the Unit 2 (U2) drywell without receiving an accurate briefing on radiological conditions and consequently the worker received a dose rate alarm in the drywell.

Description:

On February 6, 2019, a worker received a 265 milli-roentgen per hour (mrem/hr)electronic dosimeter (ED) dose rate alarm while performing ultrasound (ISI) on the N2NG piping nozzle on the 156 foot elevation of the U2 drywell. The U2 Drywell was a posted HRA. Prior to entering, the worker was briefed on dose rates in the area based on a radiation survey performed on February 5, 2019, with the N2NG shield doors closed. Maximum dose rates in the area did not exceed 60 mrem/hr. Based on the licensee work order, the ISI is required to be performed with the N2NG shield doors open. On February 6, 2019, prior to the worker's entry, the shield doors were opened and RP performed a survey. However, RP did not use this survey to brief the worker and RP did not reevaluate his ED setpoints based on this information. The worker received an ED alarm upon entering the N2NG piping area and immediately exited the area and reported to RP. A follow-up radiation survey found general area dose rate levels in the area up to 385 mrem/hr.

Corrective Action(s): The licensee took immediate corrective action including restricting RCA access for the individuals involved and performing confirmatory surveys of the area. In addition, the licensee established an event investigation team to perform a causal analysis and determine if additional actions are necessary.

Corrective Action Reference(s): Condition Report 10579232

Performance Assessment:

Performance Deficiency: The worker's entry to perform work on the N2NG piping inside the U2 Drywell which was a posted HRA without being made aware of the dose rates in the area, as required by Technical Specification 5.7.1.b.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Human Performance attribute of the Occupational Radiation Safety cornerstone.

Significance: The inspectors assessed the significance of the finding using Appendix C, Occupational Radiation Safety SDP. This finding was determined to be more than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of Human Performance and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. Specifically, workers who enter HRAs without knowledge of the radiological conditions in the area could receive unintended occupational exposures.

Cross-cutting Aspect: H.5 - Work Management: The organization implements a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. The work process includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. During the inspection, the NRC observed weaknesses in RP processes for planning, controlling, communicating and executing high risk radiological activities assuring radiological safety is the overriding priority.

Enforcement:

Violation: Technical Specification 5.7.1.b requires, in part, that entry into a HRA with a radiation monitoring device may be made after dose rate levels in the area have been established and personnel are made aware of them. Contrary to this, on February 6, 2019, a worker entered a HRA area near the N2NG nozzle piping on the 158 foot elevation of the U2 drywell, without being made aware of the dose rates in the area.

Enforcement Action: This violation is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the Enforcement Policy.

Failure to apply engineering controls in accordance with plant procedures to minimize potential concentrations of radioactive material in air.

Cornerstone Significance Cross-cutting Aspect Report Section Occupational Radiation Safety

Green NCV 05000366,05000321/2019001-02 Open/Closed`

[H.5] - Work Management 71124.03 NRC Identified a Green NCV of 10CFR 20.1701, Use of process or other engineering controls, for the licensees failure to use a High Efficiency Particulate Air Filter (HEPA) unit as prescribed by plant procedures.

Description:

On February 5, 2019, The licensee failed to adequately use engineering controls during removal of U2 reactor pressure vessel (RPV) head vent piping. The inspectors observed workers being exposed to primary reactor coolant system (RCS) steam when disconnecting the piping flanges because the HEPA inlet was too far away. Licensee procedure NMP-HP-509, Selection and Control of Portable Ventilation Units, Figure 2, Effective Capture Velocity Based on Distance From End of Hose, list a capture velocity for a 2000 CFM HEPA unit at 15 inches from the source of the contaminant as 123 feet per minute (FPM) for an open ended 10 inch hose. Figure 1, Range of Capture Velocities for Various Work Activities, recommends 200-500 FPM for active dispersion of contaminants. Based on the presence of steam in the workers breathing zone the engineering control was not adequately applied under the circumstances.

The workers were on a high risk radiation work permit (RWP) due to potential for airborne and high dose rates. The area was posted as a High Radiation Area and a Highly Contaminated Area. Dose rates in the work area were as high as 100 millirem per hour (mr/hr) and loose surface contamination levels were as high as 32 mr/hr per 100 square centimeters in the work area. The U2 reactor head internal components are considered an Alpha Level II area until results are evaluated. The ALARA plan, Reactor Cavity Disassembly and Reassembly 2R25, directed a 2000 CFM HEPA unit be used..

There was an RP technician (RPT) and a Lead RPT observing from the hand rails on the refuel floor. The workers on the RPV head were performing the work in accordance with licensee procedure 52GM-MME-105-2, Reactor Vessel Disassembly. The HEPA hose was positioned at the main flange into the RPV and the 2000 CFM HEPA unit was turned on. The workers began loosening the bolts on two flanges simultaneously. The second flange appeared to be a few feet away from the HEPA inlet. Some steam from the first flange and all steam from the second flange was out of the effective range of the HEPA and was observed in the workers breathing zone. At no time did the RPT or the lead RPT stop the work to remedy the HEPA controls. There were no measurable intakes of radioactive material as a result of RPs failure to implement the required radiological work controls.

Corrective Action(s):

Licensee performed an RP organizational stand down on February 6, 2019, to reinforce RP fundamentals and plans additional corrective actions following processing of the event through the corrective action program (CAP).

Corrective Action Reference(s): 10579200

Performance Assessment:

Performance Deficiency: Failure to employ engineering controls as required by licensee procedure NMP-HP-509.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Human Performance attribute of the Occupational Radiation Safety cornerstone. The failure to provide clear instructions for the application of engineering controls in work plans coupled with the failure of workers to use these devices within their evaluated limits, if left uncorrected, could result in unplanned uptakes of airborne radioactive material by workers when breaching primary systems.

Significance: The inspectors assessed the significance of the finding using Appendix C, Occupational Radiation Safety SDP, dated August 12, 2008, and IMC 0609, Attachment 4, Initial Characterization of Findings, dated October 7, 2016. Because the inspection finding is not related to ALARA, the finding does not involve an overexposure or substantial potential for overexposure and it did not affect the licensees ability to assess dose the inspectors determined it to be of very low safety significance (GREEN).

Cross-cutting Aspect: H.5 - Work Management: The organization implements a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. The work process includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. During the inspection, the NRC observed weaknesses in RP processes for planning, controlling, communicating and executing high risk radiological activities assuring radiological safety is the overriding priority.

Enforcement:

Violation: 10CFR 20.1701, requires that, The licensee shall use, to the extent practical, process or other engineering controls (e.g. containment, decontamination, or ventilation) to control the concentration of radioactive material in air. Licensee procedure NMP HP-509, Selection and Control of Portable Ventilation Units, defines the limits for the application of open ended HEPA hoses as an engineering control. Specifically, procedure NMP-HP-509, Version 1.3, Figure 2, Effective Capture Velocity Based on Distance From End of Hose, list capture velocities for a 2000 CFM HEPA when used with an open ended 10 inch hose. Capture velocities are not evaluated for distances greater than 15 inches from the source of the contaminant. Contrary to the above, on February 5, 2019, while disassembling the reactor vessel head piping the licensee failed to implement adequate engineering controls to control the concentration of radioactive material in air in that the licensee failed to follow procedure NMP-HP-509, Figure 2, and position the HEPA hose inlet within 15 inches from the source of the contaminant.

Enforcement Action: This violation is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 23, 2019, the inspector presented the quarterly resident inspector inspection results to Richard Spring and other members of the licensee staff.
  • On March 21, 2019, the inspector presented the Design Bases Assurance Inspection (programs) URI Closure Exit Meeting to James Collins and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71003

Work Orders

SNC656530

SNC656545

SNC656533

SNC605730

SNC656538

SNC724547

SNC401628

SNC656490

SNC656503

SNC640464

SNC655758

71111.01

Engineering

Evaluations

SCNH-13-020

Hatch Probable Maximum Flood Hydraulics - Severe

Accident Management (SAM) for Fukushima Near-Term

Task Force (NTTF) Recommendation 2.1 Flooding Re-

evaluation

Version 1.0

SCNH-13-021

Evaluation of Plant Hatch Local Intense Precipitation -

Severe Accident Management (SAM) for Fukushima Near-

Term Task Force (NTTF) Recommendation 2.1 Flooding Re-

evaluation

Version 1.0

Procedures

34AB-Y22-002-0

Naturally Occurring Phenomena

Version 19.0

DI-OPS-36-0989

Cold Weather Checks

Version 23.4

NMP-OS-017

Severe Weather

Version 1.1

71111.04

Drawings

H-16042

Control BLDG & Cable Spreading Rooms Air Conditioning

Control Diagram

Version 37.0

H-26014, Sheet 1

Unit 2 RHR System P&ID

Version 65.0

H-26015, Sheet 2

Unit 2 RHR System P&ID

Version 60.0

H-26020, Sheet 1

Unit 2 HPCI System P&ID

Version 52.0

Procedures

34SO-E41-001-2

High Pressure Coolant Injection (HPCI) System

Version 30.4

34SO-R43-001-2,

Attachments 3

and 4

Diesel Generator Standby AC System

Version 30.1

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

34SO-Z41-001-1

Control Room Ventilation System

Version 23.1

2SV-E11-007-2

Air Test on Torus Headers and Nozzles

Version 1.8

71111.05Q Drawings

A-43965, Sheet

101B

Unit 2 SE RHR & Core Spray Pump Room, Fire Zone

205B.

Ver. 1.0

A-43965, Sheet

2B

Unit 2 CRD Pump Room, Fire Zone 2205C.

Ver. 1.0

A-43965, Sheet

103B

Unit 2 HPCI Room, Fire Zone 2205Z.

Ver. 1.0

A-43965, Sheet

108B

Unit 2 Main Steam Chase, Fire Zone 2205H.

Ver. 3.0

A-43965, Sheets

011, 012, 017,

and 018

Station Battery Rooms, Fire zones: 1004, 1005, 2004, and

2005.

Ver. 2.0

A-43965, Sheets

104B and 105B

Unit 2 North and South Torus, Fire Zones 2203A and 2205A. Ver. 2.0

Miscellaneous

Fire Protection Fire Hazards Analysis (FHA)

36.0

71111.06

Calculations

BH2-M-387

Mechanical Calculations

July 14,

1983

Miscellaneous

Updated Final Safety Analysis Report

E.I. Hatch Individual Plant Examination

December

1992

Procedures

2PM-Y46-001-0

Inground Pullbox Debris Removal/Inspection

Version 10.0

71111.08G Calibration

Records

IR Thermometer

Exelon PowerLabs, LLC, Certificate of Calibration

08/08/2018

10# MT Test

Weight

Georgia Power Company Equipment Calibration Information

Sheet

2/18/95

Engineering

Evaluations

DOEJ-

HRSNC947680-

S001

Flaw Evaluation of 6 HBC Service Water Piping (Hatch Unit

2) to 2C Diesel Generator

Miscellaneous

508

Procedure Qualification Record

1-26-84

2

Procedure Qualification Record

8-22-84

563

Procedure Qualification Record

9-6-84

Arnaud

Sonic Systems International, Inc. Certificate of Qualification

(MT)

1/3/19

Arnaud

Sonic Systems International, Inc. Vision Acuity Record

01/03/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Chabotte, Jr.

International Quality Consultants, Inc. Nondestructive/Visual

Examination Certification Record (PT)

2/02/2018

Chabotte, Jr.

International Quality Consultants, Inc. Vision Examination

Record

01/28/19

FW-

1/SNC948451-

SK1

Weld Process Control Sheet for WO SNC948451

2-21-19

FW-

2/SNC948451-

SK1

Weld Process Control Sheet for WO SNC948451

2-21-19

HNP-34

Welder Performance Qualification Test (Baxley)

03/02/2011

Jennings

Sonic Systems International, Inc. Certificate of Qualification

(UT LII-PDI)

1/7/19

Nash

Sonic Systems International, Inc. Certificate of Qualification

(PT)

1/23/2019

Nash

Sonic Systems International, Inc. Vision Acuity Record

01/17/2019

Shipping

  1. N1285476

Lincoln Electric Company Certified Material Test Report for

SNC46023-0068

27AUG2018

Sir-Chem Dry

Powder 63

Circle Systems, Inc. Certificate of Compliance

October 17,

2017

Spotcheck

Cleaner, SKC-S

Magnaflux Certification

04/20/2015

Spotcheck

Developer, SKD-

S2

Magnaflux Certification

03/30/2015

Spotcheck

Penetrant, SKL-

SP2

Magnaflux Certification

10/24/2013

TS11OA-13

Welding Procedure Specification

Ultragel II UT

Couplant

Magnaflux Certification

03/03/2017

UT Calibration

Block Number

165-H

Certification Report

January 19,

2006

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NDE Reports

2B11/2-50-19-1

Southern Nuclear Liquid Penetrant Examination Record

2/13/2019

2B11/2-50-23-1

Southern Nuclear Liquid Penetrant Examination Record

2/13/2019

2B21-1FW-12AB-

Southern Nuclear UT Calibration/Examination Record

2/12/2019

2E11-2RHR-20-

RS-2PL-1,-2,-3,-4

Southern Nuclear Magnetic Particle Examination Report

2/13/2019

FW-1,-

2/SNC948451-

SK1

Southern Nuclear Liquid Penetration Examination Record

2-21-2019

Jennings

Sonic Systems International, Inc. Vision Acuity Record

2-11-2018

Operability

Evaluations

2-18-004/0

Prompt Determination of Operability: Pinhole Leak in PSW

Piping to 2C Diesel Generator

05/29/18

Procedures

NMP-ES-024-301

Southern Nuclear Liquid Penetrant Examination Color

Contrast and Fluorescent

13.0

NMP-ES-024-501

Southern Nuclear PDI Generic Procedure for the Ultrasonic

Examination of Austenitic Pipe Welds (Appendix VIII)

7.0

NMP-MA-05-002

General Welding Standard for Pressure Boundary

Applications

5.4

Work Orders

WO SNC948451

Work Order: CR10496677 - PSW Leak Permanent Repair

71111.11Q Corrective Action

Documents

10570690

Derate due to degraded condensate demin system

January 13,

2019

Miscellaneous

H-LT-SG-50322

LORP Scenario, Shutdown Cooling Operations/Loss of SD

cooling

January 10,

2019

Procedures

34GO-OPS-005-1

Power Changes

Version 30.2

34GO-OPS-042-2

MSR Extraction Steam and Heater Shell Drain System

Version 23.1

34SO-R22-001-2

4160 V A/C System

Version 22.1

2SV-C11-003-0

Control Rod Scram Testing

Version 11.0

71111.12

Corrective Action

Documents

10559746

2P51C001B 2B SSAC Tripped/Shutdown alarm received

December 4,

2018

10567790

Maintenance Rule Functional Failure

January 3,

2019

10576716

UL/FM Documentation

January 30,

2019

10593128

CR to declare a Maintenance Rule FF for the S11-01 Power

March 19,

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Transmission Function on SAT 1C

2019

Engineering

Evaluations

TE1038008

Perform MRule Evaluation for CR10585184 - PT Wiring

found incorrect at SAT 2C

March 19,

2019

Procedures

50AC-MNT-001-0

Maintenance Program

Version 35.0

NEI 99-02

Regulatory Assessment Performance Indicator Guideline

NMP-ES-027

Maintenance Rule Program

Version 9.0

NMP-ES-074-006

Fleet Lubrication Instruction

Version 3.1

NUMARC 93-01

Industry Guideline for Monitoring the Effectiveness of

Maintenance at Nuclear Power Plants

4A

Work Orders

SNC984094

2B SSAC Tripped/Shutdown Alarm received

March 4,

2019

SNC985001

2B SSAC Running Loaded for a Long Period of Time

March 27,

2019

SNC994098

Fire Main Rupture Between 1Y43F300D and 1Y43F308H

January 26,

2019

71111.13

Calculations

Equipment Out of Service Calculations

January 10,

2019

Equipment Out of Service Calculations

March 5,

2019

Equipment Out of Service Calculations

March 13,

2019

Corrective Action

Documents

10591933

2T41B004B (RCIC Pump Room Cooler) Low Flow

March 15,

2019

Procedures

NMP-DP-001

Operational Risk Awareness

Ver. 16.0

NMP-OS-010-002

Hatch Protected Equipment Logs

Ver. 11.0

NMP-RE-008-F01

Detailed Reactivity Management Plan for Final Feedwater

Temperature Reduction

Ver. 2.1

Work Orders

SNC1005958

2T41B004B Low Flow

March 21,

2019

SNC1006487

2T41B004B Low Flow (RCIC Pump Room Cooler)

March 20,

2019

71111.15

Corrective Action

Documents

10165289

1B PSW pump lower restraint broken bolt

January 7,

2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

10569967

Bolts not installed per drawing

January 10,

2019

10574672

Results of the 2A EDG Fuel Line(s) Pressure Testing

January 24,

2019

10576814

Failure of Relay 2T46-CR6B to Energize

January 30,

2019

10577193

2A CS Pump Phase 2 stress cone cut, exposing wires

January 31,

2019

10582811

Engineering to evaluate B EDG maximum generator voltage

following load reject testing

February 16,

2019

10587089

G Relay lockout outside acceptance criteria

March 1,

2019

10587094

Investigate and resolve why acceptance criteria was

exceeded during 2C EDG LOCA/LOSP LSFT

March 1,

2019

10593459

Breaker for alternate 600V supply would not close on first

attempt

March 20,

2019

10594609

RCIC speed response not as expected

March 24,

2019

10594968

RCIC steam line cond drain valve tripped on overload when

operated

March 25,

2019

Procedures

34SV-R43-21-2

1B EDG LOCA/LOSP LSFT

Ver. 2.2

NMP-AD-012

Operability Determinations and Functional Assessments

Ver. 13.3

Work Orders

SNC1008315

2E51-F046 Tripped on Overload

March 27,

2019

71111.18

Corrective Action

Documents

CAR 269621

Unit 1 auto scram due to 'A' and 'B' IRMs spiking upscale

June 27,

2017

Engineering

Changes

DCP SNC489864

Degraded Grid - U2 SAT C & E Replacement

Ver. 8.0

Design Change

Package (DCP)

SNC494055

Units 1 & 2 IRM Signal Filter Circuit Improvement

December

20, 2018

Procedures

NMP-AD-008

Applicability Determinations

Ver. 21.0

NMP-AD-009

Licensing Document Change Requests

Ver. 15.0

NMP-AD-010

CFR 50.59 Screenings and Evaluations

Ver. 16.0

NMP-MA-014

Post Maintenance Testing/Post Modification Testing

Ver. 2.1

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.19

Corrective Action

Documents

10585018

Update findings on 4160V bus 2G UV alarm during 2B CS

start

February 22,

2019

10592769

HPCI aux oil pump failed to start

March 19,

2019

Procedures

34SV-024-2

Diesel Generator 1B LSFT

Ver. 3.0

34SV-E11-001-2

Residual Heat Removal Pump Operability

Ver. 20.2

34SV-E11-010-2

Residual Heat Removal System LPCI LSFT & Auto

Actuation

Ver. 3.0

34SV-E11-012-2

Residual Heat Removal System SDC LSFT

Ver. 3.0

34SV-E41-005-2

HPCI Operability 165# Test

Ver. 7.13

2SP-03-04-19-

SB-1-2

RHR 2B Loop Auto-Start LSFT

Ver. 1.0

2SP-03-04-19-

SB-2-2

RHR Bus Power Monitoring LSFT

Ver. 1.0

2PM-T47-001-0

Primary Containment Cooling System Maintenance

Ver. 10.4

57SV-S32-002-2

Emergency Buses 2E, 2F and 2G Undervoltage Relay FT&C Ver. 14.1

NMP-MA-014

Post Maintenance Testing/Post Modification Testing

Ver. 2.1

NMP-MA-014-001 Post Maintenance Testing Guidance

Ver. 5.2

Work Orders

SNC1000394

Received Alarm 2G 4160V Low Voltage Alarm on Pump

Start

February 22,

2019

SNC1000862

2C Auto Voltage Regulator Repairs

February 26,

2019

SNC1001043

Visual Inspection of 2C EDG Engine/Generator Coupling

February 24,

2019

SNC1006582

HPCI Aux Oil Pump Failed to Start

March 19,

2019

SNC936300

Replace Fan Motor per 51GM-MEL-001-0

March 19,

2019

SNC946205

Replace Fan Motor per 51GM-MEL-001-0

March 29,

2019

71111.20

Procedures

31GO-OPS-024-0

Outage Safety Assessment

Ver. 5.0

34GO-G41-003-2

Fuel Pool Cooling and Cleanup System

Ver. 28.0

34GO-OPS-001-2

Plant Startup

Ver. 51.2

34GO-OPS-013-2

Normal Plant Shutdown

Ver. 33.2

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

34GO-OPS-015-2

Maintaining Cold Shutdown or Refueling Condition

Ver. 16.0

34GO-OPS-028-2

Drywell Closeout

Ver. 7.21

34GO-OPS-029-0

Torus and Torus Area Closeout

Ver. 3.2

34GO-OPS-065-0

Control Rod Movement

Ver. 15.4

34SV-SUV-019-2

Mode 4 Surveillance Checks

Ver. 41.18

2FH-ERP-001-0

Control Blade Unlatching, Installation, Removal and

Exchange

Ver. 9.0

2IT-TET-006-2

ISI Pressure Test of the Class 1 System and Recirculation

Pumps(s) Runback Test

Ver. 18.10

2GM-C11-001-0

CRD Removal and Installation

Ver. 7.0

2GM-MME-004-

Reactor Vessel Reassembly

Ver. 20.2

71111.21N Corrective Action

Documents

Resulting from

Inspection

10593732

10593732

10593733

71111.22

Corrective Action

Documents

10589354

2R42-S001A Recharge PCV Readings

March 8,

2019

Procedures

34SV-C11-010-2

Alternate Rod Insertion LSFT

Ver. 1.0

34SV-E11-001-1

Residual Heat Removal Pump Operability

Ver. 27.0

34SV-E11-002-1

RHR Valve Operability

Ver. 21.6

34SV-P41-001-2

Plant Service Water Pump Operability

Ver. 15.0

34SV-R43-003-1

Diesel Generator 1C Monthly Test

Ver. 20.0

2SP-09-18-17-

RM-1-2

Unit 2 Station Auxiliary Transformer 2E Functional Test

Ver. 1.2

2SV-E11-007-2

Air Test on Torus Headers and Nozzles

Ver. 1.8

2SV-TET-001-0

LLRT Testing Methodology

Ver. 13.0

2SV-TET-001-2

Primary Containment Periodic Type B and Type C Leakage

Tests

Ver. 37.1

2IT-CAL-017-2

Transformer Fault Pressure Relay

Ver. 5.0

2IT-MEL-021-2

Trip Test of Start Up Transformer 2E Protective Relays

Ver. 2.0

2SV-R42-011-2

Unit 2 Station Service Battery Combined Service

Performance/Modified Performance Test

Ver. 5.0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Work Orders

SNC660508

2SV-R42-006-0 & 52SV-R42-011-2 Battery Service Test

March 11,

2019

SNC971671

New 2E SAT Transformer Testing

March 1,

2019

71124.01

Corrective Action

Documents

CR 10514273

CR 10578680

CR 10578754

CR 10580308

Procedures

2RP-RAD-016-0

Control of High Radiation Areas

Version 35.4

NMP-HP-001

Radiation Protection Standard Practices

Version 6.2

NMP-HP-206

Issuance, Use, and Control of Radiation Work Permits

Version 5.0

NMP-HP-300

Radiation and Contamination Surveys

Version 5.2

NMP-HP-302

Restricted Area Classification, Postings, and Access Control

Version 10.6

NMP-HP-302-001

Radiological Key Control

Version 3.2

NMP-HP-303

Personnel Decontamination

Version 4.0

NMP-HP-403

Control and Monitoring of Materials in Radiation Controlled

Areas

Version 3.8

NMP-HP-404

Release of Materials from the RCA and Protected Areas

Version 4.2

Radiation

Surveys

Air Sample Record Nos. 19-036-1 and 19-036-2, Unit 2

Refuel Floor, General Area

Unit 2 Condenser Bay (2TB112), Survey Nos. 165241 and

165272

Unit 2 Drywell (2DW156), Survey Nos. 165320 and 165392

Radiation Work

Permits (RWPs)

RWP No. 19-

2605

DW/SC ISI and Supporting Activities

71124.02

Procedures

NMP-AD-035

ALARA Program

Version 1.9

NMP-HP-204

ALARA Planning and Job Review

Version 6.4

NMP-HP-204-001

ALARA Planning

Version 1.0

71124.03

ALARA Plans

NMP-HP-204-001

- ALARA PLAN

Reactor Cavity Disassembly and Reassembly 2R25

2/04/2019

Calibration

Records

Supplied

Breathing Air

Compressors,

Grade D Air Sample Results for 2nd and 3rd Quarters of

2018

05/17/2018

and

9/14/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Atlas Copco, U1

TB 130 and Eagle

Air Compressed

Gas System

Compressors

Procedures

2GM-MME-015-

Reactor Vessel Disassembly

Version 1.0

2HI-OCB-002-0

Portable HEPA Air Filtration Units and Vacuum Maintenance

and Operation

Version 10.3

NMP-HP-301

Airborne Radioactivity Sampling and Evaluation

Version 4.1

NMP-HP-501

Radiological Respiratory Protection Program

Version 1.2

NMP-HP-509

Selection and Control of Portable Ventilation Units

Version 1.3

Radiation

Surveys

MNP-HP-305

2018 Alpha

Program

2018 Alpha Characterization Study

10/17/2018

RIS #165339

U2 Cavity (2RX226)

2/05/2019

RIS #165417

U2 Reactor Cavity (2RX228)

2/05/2019

Radiation Work

Permits (RWPs)

RWP 19-2209

Refuel Floor Vessel Disassembly/Reassembly, Cavity Work

and Support

Revision 0.0

71124.04

Corrective Action

Documents

10586796

Miscellaneous

Gamma Spec

06Feb19-005

Nasal Swabs Left

2/06/2019

Gamma Spec

06Feb19-006

Nasal Swabs Right

2/06/2019

NMP-HP-104

Environmental Background reads, authenticated

2/21/2018

NMP-HP-105,

Data Sheet 1

DDE Discrepancy Investigation Form, ID # ***28 ; ID# **43,

03/05/2018;

03/05/2018

PCE Analysis

PCE, Analysis report ID ***63, multiple analysis reports;

PCE, Analysis report ID ***14, multiple analysis reports;

PCE, Analysis report ID ***78,

2/22/19;

2/22/19;

2/07/19

Procedures

NMP-HP-104-003

Performing Whole Body Counts

Version 1.2

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NMP-HP-104-008

Resolving Unidentified Peaks and Assignments of Dose

Version 1.0

NMP-HP-104-011

Performing Whole Body Counts Using Apex-In Vivo

Version 1.0

NMP-HP-108

Issuance, Use and Collection of Personnel Dosimetry

Version 2.7

NMP-HP-303

Personnel Decontamination

Version 4.0

Radiation

Surveys

Survey #166368

PCE #779

2/17/19

Survey #166372

PCE #780

2/17/19

71124.05

Calibration

Records

2HI-OCB-100:

HPX-1052

Electra 1B/AP5BD Calibration Data Sheet #D21-N1631,

2/03/17,

2/07/18

2HI-OCB-107:

HPX-1115

RM-25 Calibration Data Sheet Dn21-N 1539,

06/13/2017,

05/04/2018

64CL-OCB-011-0

Post-LOCA Monitors, MPL # 2D11-K621A,

03-05-15

Apex-In Vivo

Calibration

Apex-In Vivo Calibration Check Count

01/2019 -

2/2019

HPX-0977,

AMS-4 High Voltage and Flow Calibration

  1. D21-N1754 Radial Head;
  1. D21-N1754 InLine Head

04/17/2018

HPX-0978 AMS-4

Calibration

  1. D21-N1745 Radial Head;
  1. D21-N1745 InLine Head

04/09/2017

NMP-HP-104

Mirion Technologies, Calibration of the Canberra People

Mover WBC System at the SN Plant Hatch Dosimetry

Department; Mirion Technologies, Calibration of the

Canberra People Mover WBC System at the SN Plant Hatch

In-Processing Facility; Efficiency Calibration Verification

Counts, In-Processing People Mover,

06/08/2017;

06/08/2017;

06/17/2017

NMP-HP-711

Operation and Calibration of HandECount Sample Counter,

10/2018-

2/2018

NMP-HP-78, Data

Sheet 1

Telepole Gamma Calibration, #0116,

09/21/2018,

09-15-2017

NP-HP-703

RO-2, RO-2A, RO-20 Operation and Calibration, #4566,

07/11/18

Corrective Action

Documents

10503223

10518282

10453715

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Miscellaneous

64CL-OCB-042-0, Inter laboratory Cross-Check

10/31/2018

NMP-HP-701

Daily Instruments Source Check Log

01/2019-

2/2019

Procedures

64CL-OCB-011-0

Post-LOCA Monitors

Version 7.2

NMP-HP-718

Operation and Calibration of the Canberra GEM-5 Gamma

Exit Monitor

Version 2.4

Self-Assessments NMP-GM-003-

F18

Check-in Self-Assessment Report

08/2018

71151

Corrective Action

Documents

CAR 272541

Cause Determination Report Summary for 3 Incidents

Involving RP Procedural and Regulatory Non-Compliance,

04/11/2018.

Miscellaneous

Hatch Key Performance Indicators

January

2018 through

December

2018

CR#10461882

Dose and Dose Rate Alarm Report from 02/14/2018 to

07/11/2019

07/11/2018

G-20181225-211-

C

Radioactive Gas Release Permit

2/26/2018

HIS-20 Report

Plant Hatch Access Control Alarms Report From 07/25/2018

to 01/02/2019

01/10/2019

L-2018113-367-B

Radioactive Liquid Release Permit

11/13/2018

NEI 99-02

Regulatory Assessment Performance Indicator Guideline

Rev. 7

Procedures

NMP-AD-029

Preparation and Reporting of Regulatory Assessment

Performance Indicator

Data and the Monthly Operating Report

Ver. 1.1

71152

Corrective Action

Documents

10585184

PT Wiring found incorrect at SAT 2C

February 23,

2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

10585783

Unexpected loss of 1C Startup Transformer

February 26,

2019

10586844

Ground associated with wire D8 never installed

March 1,

2019

10587094

Investigate and resolve why acceptance criteria was

exceeded on the 2C EDG LOCA/LOSP LSFT

March 1,

2019

10587312

Wires found reversed (2H11P652)

March 2,

2019

10587356

Relay did not energize as it should during LSFT

March 3,

2019

Procedures

NMP-AD-029

Preparation and Reporting of Regulatory Assessment

Performance Indicator Data and the Monthly Operating

Report

Ver. 1.0

NMP-GM-002

Corrective Action Program

Version 15.1

NMP-GM-002-

2

Effectiveness Review Instructions

Ver. 5.2

Work Orders

SNC489862

Degraded Grid - U2 Splice Box & Cable Bus DCP

March 29,

2017