IR 05000321/2019003

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Integrated Inspection Report 05000321/2019003 and 05000366/2019003 and Exercise of Enforcement Discretion
ML19317D284
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 11/12/2019
From: Mark Miller
Division Reactor Projects II
To: Gayheart C
Southern Nuclear Operating Co
Geanette D
References
EA-19-062 IR 2019003
Download: ML19317D284 (17)


Text

November 12, 2019

SUBJECT:

EDWIN I HATCH NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000321/2019003 AND 05000366/2019003 AND EXERCISE OF ENFORCEMENT DISCRETION

Dear Ms. Gayheart:

On September 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Edwin I Hatch Nuclear Plant. On October 17, 2019, the NRC inspectors discussed the results of this inspection with Edwin D. (Sonny) Dean site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report.

Section 71111.11 of the enclosed inspection report discusses NRC review and final determination of an inspection issue, identified by facility staff in January 2019, involving the reactivation of Senior Reactor Operator (SRO) licenses at Plant Hatch. For this issue, the NRC is exercising enforcement discretion in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy and will not issue enforcement action for this violation.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at the Edwin I Hatch Nuclear Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Documents Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/Steven D. Cochrum RA for/

Mark S. Miller, Director Division of Reactor Projects

Docket Nos. 05000321 and 05000366 License Nos. DPR-57 and NPF-5

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000321 and 05000366

License Numbers:

DPR-57 and NPF-5

Report Numbers:

05000321/2019003 and 05000366/2019003

Enterprise Identifier: I-2019-003-0028

Licensee:

Southern Nuclear Operating Co. Inc.

Facility:

Edwin I Hatch Nuclear Plant

Location:

Baxley GA 31513

Inspection Dates:

July 01, 2019 to September 30, 2019

Inspectors:

B. Collins, Reactor Inspector

J. Hickman, Resident Inspector

C. Jones, Senior Resident Inspector

J. Viera, Operations Engineer

Approved By:

Mark S. Miller, Director,

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Edwin I Hatch Nuclear Plant in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

None.

Additional Tracking Items

Type Issue Number Title Report Section Status EDG EA-19-062 Improper SRO License Reactivation 71111.11Q Closed

PLANT STATUS

Unit 1 operated at or near rated thermal power (RTP) for the entire inspection period.

Unit 2 began the inspection period at RTP. On September 12, 2019, the unit was down powered to 50 percent to repair a steam leak on the 'A' reactor feed pump turbine. The unit was returned to RTP on September 17, 2019. On September 20, 2019, the unit was taken offline to repair a steam leak on a feed water check valve and remained offline for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated readiness for impending adverse weather conditions for hurricane Dorian on August 30, 2019.

71111.04Q - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1 C Emergency Diesel Generator (EDG) following the monthly EDG operability surveillance testing on July 17, 2019.
(2) Unit 1 A Core Spray (CS) system alignment following surveillance testing on July 30, 2019.
(3) Unit 1 A Standby Gas Treatment (SBGT) system alignment during dispersed oil particulate (DOP) testing on the B train on August 19, 2019.

71111.05A - Fire Protection (Annual)

Annual Inspection (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated fire brigade performance on August 31, 2019.

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (6 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Unit 1 SBGT system, Fire Zones 1205N and 1205Q on August 27, 2019.
(2) Unit 2 Reactor Core Isolation Cooling (RCIC) Pump and Turbine Room, Fire Zone 2203C on August 27, 2019.
(3) Unit 1 and Unit 2 Refueling Floor, Fire Zones 0201 A/B on September 16, 2019.
(4) Unit 2 High Pressure Coolant Injection (HPCI) Pump Room, Fire Zone 2205Z on September 25, 2019.
(5) Unit 2 Adjustable Speed Drive (ASD) Room, Fire Zones 2210 and 2211 on September 29, 2019.
(6) Unit 2 Chiller Room, Fire Zone 2205N on September 30, 2019.

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Unit 1 northeast and southeast diagonal rooms.

===71111.07T - Heat Sink Performance

Triennial Review (IP Section 02.02)===

The inspectors evaluated heat exchanger/sink performance on the following from July 22 - 26, 2019:

(1)1A Residual Heat Removal Heat Exchanger (1E11B001A), Section 02.02b

(2) Emergency Diesel Generator 1B Jacket Water/Lube Oil Coolers (1R435004B/5B),

Section 02.02b

(3) High Pressure Coolant Injection Pump Room Cooler 2A (1T41B005A), Section 02.02b
(4) Service Water Intake structure and Altamaha River, Section 02.02d, Specifically Sections 02.02d.4, 02.02d.6 and 02.02d.7 were completed.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Control Room during Unit 2 Rod Pattern Adjustment, Unit 2 power ascension from 90 to 100 percent power, Unit 1 Steam Jet Air Ejector (SJAE) adjustments due to high condensate temperatures, and Unit 2 power ascension from 50 to 100 percent power following steam/feed leak repairs on 2A Reactor Feed Pump on July 2, 2019, August 5, 2019, September 6, 2019, and September 16, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample 1 Partial)

(1) The inspectors observed and evaluated licensed operator requalification scenario in the simulator on September 12, 2019.

(2)

(Partial)

The inspectors evaluated maintenance of operator license conditions in the area of license reactivations performed for refueling activities. Results of this evaluation can be found in Enforcement Action EA-19-062.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Unit 2 HPCI Turbine speed control was lost due to inverter circuit failure on August 22, 2019.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 2 elevated risk when testing the Loss of Coolant Accident/Loss of Site Power (LOCA/LOSP) timer cards after 1B EDG power supply (P/S) replacement, on July 12, 2019.
(2) Unit 1 elevated risk during B residual heat removal (RHR) heat exchanger (HX) tube plugging, on July 24, 2019.
(3) Unit 1 and 2 elevated risk with 1B EDG being declared Operable but Degraded/Nonconforming (OBDN), on July 25, 2019.
(4) Unit 2 elevated risk due to excavation of underground Condensate Storage Tank (CST) piping, on August 2, 2019.
(5) Unit 1 and Unit 2 elevated risk due to high ambient temperatures and elevated Unit 2 condenser bay temperatures on August 14, 2019.
(6) Unit 2 risk during emergent HPCI repairs on August 23, 2019.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (4 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 1 Plant Service Water (PSW) pump A differential pressure ratio and vibration point landed in the alert range on July 11, 2019.
(2) Unit 1 through wall leak of RHR piping during performance of flushing of PSW and RHR Service Water (SW) piping dead-legs on August 9, 2019.
(3) Unit 2 HPCI system inverter failure and the post accident monitoring instrumentation on August 23, 2019.
(4) Unit 2 feedwater check valve steam leak on September 19, 2019.

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Emergent temporary configuration change (TCC) for condenser bay temperature switches on Unit 2.

71111.19 - Post-Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post maintenance tests:

(1)57SV-R43-001-2, Testing the LOCA/LOSP Timer Cards, Ver.7.0 following the replacement of 1B EDG 2B LOCA/LOSP Timer Power Supply on July 15, 2019.

(2) Unit 1 leak test and inspection following RHR Heat Exchanger repairs, Work Order SNC952338, on July 26, 2019.

(3)57SV-C11-002-2, Scram Discharge Volume Level (Thermal Sensors) FT&C, Ver.12.2 following a Unit 2 half scram on August 6, 2019.

(4) Penetrant and leak tests following seal weld of leak off plug on Unit 2 check valve 2B21F007A, work order SNC1049024, on September 30, 2019.

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated Unit 2 forced outage activities due to leak repairs of feedwater check valve 2B21F007A from September 24, 2019, to September 30, 2019.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1)34SV-R43-001-1, Diesel Generator 1A Monthly Test, Version 25.0 on July 2, 2019.

(2)34SV-E51-002-1, RCIC Pump Operability, Version 28.5 on August 8, 2019.

Inservice Testing (IP Section 03.01) (1 Sample)

(1)34SV-E11-001-1, Residual Heat Removal Pump Operability, Version 28.0 on August 3, 2019.

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated a simulator based emergency scenario on September 12,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS06: Emergency AC Power Systems (IP Section 02.05)===

(1) Unit 1 (July 2018 to June 2019)
(2) Unit 2 (July 2018 to June 2019)

MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)

(1) Unit 1 (July 2018 to June 2019)
(2) Unit 2 (July 2018 to June 2019)

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 (July 2018 to June 2019)
(2) Unit 2 (July 2018 to June 2019)

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends in feedwater flow control that might be indicative of a more significant safety issue.

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Unit 1 B EDG being declared Operable but Degraded/Nonconforming (OBDN) due to minor defect in the outer race of the generators outboard bearing, Condition Report (CR) 10629568.

71153 - Followup of Events and Notices of Enforcement Discretion Event Followup (IP Section 03.01)

(1) The inspectors evaluated the Unit 2 High Pressure Coolant Injection System Inoperability report and licensees response on August 22,

INSPECTION RESULTS

Enforcement Discretion Enforcement Action EA-19-062: Improper SRO License Reactivation 71111.11 Q

Description:

From February 1 through August 8, 2019, NRC inspectors evaluated an inspection issue identified by facility staff on January 31, involving the reactivation of Senior Reactor Operator (SRO) licenses at Plant Hatch. NRC inspection concluded that during refueling outages conducted from 2005 through 2018, there were seventy occurrences of senior operators failing to perform license reactivation in accordance with 10 CFR Part 55.53(f)(2). Specifically, twenty senior operators failed to perform the required minimum number of under instruction reactivation hours prior to assuming duties required of an SRO license.

The failure to achieve the required minimum number of reactivation hours originated from the requirements of NMP-TR-406, License Administration, Section 4.7, Reactivation of a Senior Reactor Operator for Supervising Core Alterations. Section 4.7 permitted licensee staff the option of performing SRO reactivation using a training-only option where training was used as credit in lieu of obtaining the required minimum number of under instruction reactivation hours.

The NRC concluded using a training-only option resulted in violation of 10 CFR Part 55.53(f)(2), which requires that a senior operator licensee must complete a minimum of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of shift functions under the direction of a senior operator in the position to which the individual will be assigned before a resumption of senior operator functions.

Corrective Actions: The following Condition Reports document facility corrective actions to correct the licensed operator reactivation issue identified on January 31, 2019. Final closure corrective actions included an immediate policy change for senior operators reactivating for the Unit 2 Spring 2019 refueling outage and process procedure changes that removed use of a 'training-only' option from NMP-TR-406.

Corrective Action References:

  • 10577066, NMP-TR-406 (Option 1) does not meet NUREG 1021 requirements, 1/31/19
Enforcement:

Significance/Severity: As discussed in Section 6.4.c of the NRC Enforcement Policy, the potential existed for this violation to be characterized at Severity Level III, because multiple licensed SROs were in noncompliance with reactivation requirement conditions.

Violation: Title 10 of the Code of Federal Regulations (10 CFR) Section 55.2, Scope, states that the regulations present in Part 55, Operators Licenses, apply to facility licensees.

Title 10 CFR 55.53 (f), Conditions of Licenses, states, in part, that before the resumption of functions authorized by a senior operator license, an authorized representative of the facility licensee shall ensure completion of Part 55.53(f)(2) requirements.

Title 10 CFR 55.53(f)(2), Conditions of Licenses, states, in part, that a senior operator licensee must complete a minimum of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of shift functions under the direction of a senior operator in the position to which the individual will be assigned before a resumption of senior operator functions if that senior operator licensee has not been active in the performance of senior operator functions.

Contrary to the above, Southern Nuclear Company (SNC) failed to ensure completion of the minimum hours of shift functions under the direction of a senior operator prior to permitting a resumption of functions that required performance by a senior operator licensee. Specifically, for refueling outages conducted from 2005 through 2018, the facility licensee failed to ensure completion of the minimum number of required reactivation hours prior to assigning twenty senior operators, on seventy occasions, the limited duty of supervising Core Alterations, as required by a senior operator licensee.

In accordance with Section 6.4.c of the NRC Enforcement Policy, this violation is characterized at Severity Level III.

Basis for Discretion: In reviewing the circumstances of this issue, the NRC concluded that prior NRC communication from 2005 as well as a lack of clarity in existing guidance, contributed to the facility licensees use of the training-only option in their limited duty SRO reactivation program with subsequent non-compliance. Additionally, the NRC factored in the facility licensees prompt corrective actions which included entering this issue into its Corrective Action Program (CAP) and institution of an immediate policy change for senior operators reactivating for the Unit 2 Spring 2019 refueling outage (February - March 2019).

Lastly on April 29, 2019, process procedure changes to NMP-TR-406 were finalized which removed the training-only option in lieu of reactivation hours as an accepted facility method for performing senior operator reactivation.

Based on these facts, Region 2, in consultation with Office of Enforcement, has refrained from issuing a Notice of Violation and has exercised enforcement discretion in accordance with Section 3.5 of the NRC Enforcement Policy. Enforcement action will not be issued for this violation.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On October 17, 2019, the inspectors presented the integrated inspection results to Edwin D. (Sonny) Dean site Vice President and other members of the licensee staff.
  • On July 25, 2019, the inspectors presented the Triennial Heat Sink Performance Debrief inspection results to Daniel Komm, Plant Manager (Acting Site VP) and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Procedures

34AB-Y22-002-0

Naturally Occurring Phenomena

Version 19.0

NMP-OS-017

Severe Weather

Version 1.1

NMP-OS-020

Station Response to Southern Company Alert Conditions

Version 1.2

71111.04Q Drawings

H-13414

Elementary Diagram Diesel Generator 1C

Version 54.0

H-16020

Unit 1 Standby Gas Treatment System P & I D Sheet 1

Version 30.0

H-16331

Unit 1 Core Spray System P & I D

Version 37.0

Procedures

34SO-E21-001-1

Core Spray System

Version 24.6

34SO-R43-001-1

Diesel Generator Standby AC System

Version 29.1

34SO-T46-001-1

Standby Gas Treatment System

Version 21.5

71111.05A

Procedures

NMP-TR-425

Fire Drill Program

Version 9.0

NMP-TR-425-F01 Fire Drill Scenario Development and Approval Sheet

08/15/2019

NMP-TR-425-F08 Pre-Drill Checklist

Version 4.0

NMP-TR-425-F14 Fire Drill Package

Version 1.1

71111.05Q Drawings

A-43865, Sh. 074

Refueling Floor, Fire Zones 0201 A/B

Version 3.0

A-43956, Sh. 100

Unit 2 RCIC Pump and Turbine Room, Fire Zone 2203C

Version 2.0

A-43965, Sh. 065 Standby Gas and HVAC, Fire Zone 1205N

Revision 2

A-43965, Sh. 103

Unit 2 HPCI Pump Room, Fire Zone 2205Z

Version 2.0

A-43965, Sh. 112

U2 Chiller Room, Fire Zone 2205N

Version 4.0

A-43965, Sh. 113

Unit 2 ASD, Fire Zone 2210

Version 5.0

Miscellaneous

Fire Protection Fire Hazards Analysis

Version 36.0

71111.06

Engineering

Evaluations

E. I. Hatch Individual Plant Examination

December

1992

Miscellaneous

Updated Final Safety Analysis Report

71111.07T

Corrective Action

Documents

Resulting from

Inspection

10632323

GL 89-13 Heat Exchanger As-Found Condition Inspections

7/26/2019

Miscellaneous

2IT-TET-014-1

Safeguard Equipment Area Cooler Data: HPCI Pump Room

Cooler 2A

1/4/08

2IT-TET-014-1

Safeguard Equipment Area Cooler Data: HPCI Pump Room

Cooler 2A

1/27/11

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2IT-TET-014-1

Safeguard Equipment Area Cooler Data: HPCI Pump Room

Cooler 2A

3/25/14

NDE Reports

Inspection Summary Hatch Unit 1B Emergency Diesel

Generator Jacket Water Cooler - 1R43B005B

May 2018

Inspection Summary Hatch Unit 1 High Pressure Coolant

Injection Pump Room Cooler - 1T41B005A

May 2017

Inspection Summary Hatch Unit 1B Emergency Diesel

Generator Lube Oil Cooler - 1R43B004B

May 2018

2IT-TET-012-1S

Piping/Component Inspection Report: 1A RHR Heat

Exchanger

2-8-08

2IT-TET-012-1S

Piping/Component Inspection Report: 1A RHR Heat

Exchanger

2-14-08

2IT-TET-012-1S

Piping/Component Inspection Report: 1A RHR Heat

Exchanger

2-15-14

RER SNC843238

Hatch Unit 2 Structural Monitoring Inspection Report: Intake

Structure

2017

RER SNC921613

Hatch Unit 1 Structural Monitoring Inspection Report: Intake

Structure

2018

SNC425433

(excerpt)

Piping/Component Visual Inspection Report: 1B EDG Heat

Exchangers

4-29-14

SNC785938

(excerpt)

Piping/Component Visual Inspection Report: 1B EDG Heat

Exchangers

5/30/2018

Procedures

NMP-CH-005

E.I. Hatch Nuclear Plant Chemistry Program

Ver. 4.1

71111.11Q Corrective Action

Documents

10186462

Fuel Assembly Damaged During Fuel Movement

2/22/16

10577066

NMP-TR-406 (Option 1) does not meet NUREG 1021

requirements

01/31/19

10577173

CFAM: SRO License activation for Core Alterations

01/31/19

2172

Fuel movement error during execution of Fuel Shuffle Step

  1. 69

04/14/2011

2206

Step 103 of Fuel movement

04/14/2011

777912

Fuel Assembly Hits Core Light

2/24/2014

Miscellaneous

H-LT-AF-112

RFPT Oil Temp Cont/ASD Cell bypass/SDV Fail/ATWS

Version 1.0

H2C26-081319-

014

Recovery from Power Reduction Due to Elevated Conbay

Temperatures

08/15/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Procedures

34SO-N61-001-1

Main Condenser Vacuum System and Closeout

Version 27.0

2CC-ERP-018-0

Target Rod Pattern Development

Version 16.0

2CC-ERP-018-0

Target Rod Pattern Development,

Version 16.0

2TR-TRN-002-0

License Continuing Training Program

Version 13.0

DI-TRN-55-601

Operations Personnel Qualification Instructions

Version 4.0

NMP-TR-406

License Administration

Version 7.2

NMP-TR-406

License Administration

Version 8

NMP-TR-406-F02 SRO Reactivation for Core Alterations

Version 3.2

71111.12

Corrective Action

Documents

CR10640117

HPCI System inverter circuit failure

08/22/2019

CR10648029

Maintenance Rule Functional Failure on 2E41K065

09/20/2019

Procedures

NEI 99-02

Regulatory Assessment Performance Indicator Guigeline

Revision 7

NMP-AD-006

Infrequently Performed Tests and Evolutions

Version 12.8

NMP-ES-027

Maintenance Rule Program

Version 10.0

NUMARC 93-01

Industry Guideline for Monitoring the Effectiveness of

Maintenance at Nuclear

Power Plants

Revision 4A

71111.13

Corrective Action

Documents

CR 10629568

Generator outboard bearing issues on the 1B EDG

07/17/2019

CR10627205

Diesel Generator B Loading Timer Failure

07/09/2019

Drawings

H-21084

Edwin I. Hatch Nuclear Plant Unit No.2 Condensate Make-

Up and Storage at Tank Outside Building

Version 18.0

Engineering

Evaluations

ODMI 2-19-001

Unit 2 Conbay Elevated Temperatures

08/14/2019

Miscellaneous

Equipment Out of Service Calculations

07/12/2019

Equipment Out of Service Calculations

07/25/2019

Equipment Out of Service Calculations

07/24/2019

Procedures

34SO-N71-001-2

Main Condenser Vacuum Parameters and Limitations

Version 36.4

57SV-R43-001-2

Testing the LOCA/LOSP Timer Cards

Version 7.0

NMP-DP-001

Operational Risk Awareness

Version 15.0

NMP-OS-010-002 Hatch Protected Equipment Logs

Version 11.0

Work Orders

SNC1028120

Install new 3 inch piping down stream of 2P11F051 valve to

newly installed test flange.

Revision 0

SNC952338

Unit 1 RHR Heat Exchanger Tube Leak Testing

07/25/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.15

Drawings

6511-20

Electrical Equipment Separation for Safeguard Sys.

Revision 1

H-24100

Edwin I. Hatch Nuclear Plant Unit No.2 HPCI System 2E41

Elementary Diagram Sheet 10 of 11

Version 20.0

H-24435

Edwin I. Hatch Nuclear Plant Unit No.2 Elementary Diagram

ATTS, System 2A70, Sheet 35 of 35

Revision 3

H-27664

Edwin I. Hatch Nuclear Plant Unit No.2 HPCI System 2E41

Elementary Diagram Sheet 1 of 11

Version 42.0

H-27666

Edwin I. Hatch Nuclear Plant Unit No.2 High Pressure

Coolant Injection Sys 2E41 Elementary Diagram Sheet 3

Version 28.0

Miscellaneous

Unit 1 Technical Specifications

Ammendment

294

Unit 2 Technical Specifications

Ammendment

239

Operability

Evaluations

2-2019-003

Prompt Determination of Operability for 2B21F077A -

Feedwater Check Valve

09/16/2019

CR10626823

Unit 1 PSW pump 1A differential pressure ratio and vibration

point landed in the alert range

07/08/2019

CR10634238

Through wall leak on Unit 2 RHR Piping

08/02/2019

CR10640117

HPCI system inverter circuit failure

08/22/2019

ODMI 2-19-001

Unit 2 Condenser Bay Elevated Temperatures

08/14/2019

71111.18

Engineering

Changes

SNC1041769

Emergent TCC for condenser bay temperature switches

Revision 1.0

71111.19

Procedures

57SV-C11-002-2

Scram Discharge Volume Level (Thermal Sensors) FT&C

Version 12.2

NMP-MA-014

Post Maintenance Testing/Post Modification Testing

Version 2.1

NMP-MA-014-

001

Post Maintenance Testing Guidance

Version 5.2

Work Orders

SNC1039991

Received a half scram on Unit 2 during performance of

57SV-C11-002-2

08/05/2019

SNC1049024

Seal weld leak off plug on check valve 2B21F007A

09/29/2019

SNC952338

Unit 1 RHR HX Repairs

07/25/2019

71111.20

Procedures

34GO-OPS-001-2 Plant Startup

Version 51.4

34GO-OPS-013-2 Normal Plant Shutdown

Version 33.2

NMP-RE-008-F02 Simplified Reactivity Management Plan

09/23/2019

NMP-RE-008-F02 Recovery from Power Reduction Due to Elevated Conbay

08/13/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Temperatures

71114.06

Miscellaneous

H-LT-AF-112

RFPT oil temp controller fails, ASD cell bypass, scram

discharge volume drain valves fail, ATWS

Version 1.0

71152

Corrective Action

Documents

CR 10629568

1B EDG being declared Operable but

Degraded/Nonconforming (OBDN) due to minor defect in

the outer race of the generators outboard bearing

07/17/2019

CAR 276475

Feedwater Transient on Unit 2

08/21/2019

TE 1049457

Yokogawa Controller Failure Analysis Report

08/19/2019

Procedures

NMP-GM-002

Corrective Action Program

Version 15.1

NMP-GM-002-

2

Effectiveness Review Instructions

Version 5.2

71153

Corrective Action

Documents

10640117

Shift received "HPCI System inverter circuit failure" (P601-

20)

08/22/2019