IR 05000313/2019002

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Integrated Inspection Report No. 05000313/2019002 and 05000368/2019002
ML19214A275
Person / Time
Site: Arkansas Nuclear  
Issue date: 08/01/2019
From: John Dixon
NRC Region 4
To: Richard Anderson
Entergy Operations
References
IR 2019002
Download: ML19214A275 (37)


Text

August 1, 2019

SUBJECT:

ARKANSAS NUCLEAR ONE, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000313/2019002 AND 05000368/2019002

Dear Mr. Anderson:

On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Arkansas Nuclear One, Units 1 and 2. On July 9, 2019, the NRC inspectors discussed the results of this inspection with Mr. B. Patrick, Director, Regulatory Assurance and Performance Improvement, and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. Both findings involved violations of NRC requirements. The inspectors also documented a licensee-identified violation, which was determined to be of very low safety significance, in this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violations or significance of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector at Arkansas Nuclear One.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at Arkansas Nuclear One. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

John L. Dixon, JR, Chief Reactor Projects Branch D

Docket Nos.: 05000313 and 05000368 License Nos.: DPR-51 and NPF-6

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000313 and 05000368

License Numbers:

DPR-51 and NPF-6

Report Numbers:

05000313/2019002 and 05000368/2019002

Enterprise Identifier: I-2019-002-0005

Licensee:

Entergy Operations, Inc.

Facility:

Arkansas Nuclear One, Units 1 and 2

Location:

Russellville, AR

Inspection Dates:

April 1, 2019 to June 30, 2019

Inspectors:

T. DeBey, Resident Inspector

N. Greene, Senior Health Physicist

S. Hedger, Emergency Preparedness Inspector

C. Henderson, Senior Resident Inspector

J. ODonnell, Health Physicist

T. Sullivan, Resident Inspector

Approved By:

John L. Dixon, JR, Chief

Reactor Projects Branch D

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Arkansas Nuclear One, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC and self-revealed findings and violations are summarized in the tables below. A licensee-identified non-cited violation is also documented.

List of Findings and Violations

Failure to Properly Evaluate Operability of the Unit 1 Emergency Diesel Generator 2 Room Ventilation System Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000313/2019002-01 Open/Closed

[P.4] - Trending 71111.15 The inspectors identified a Green finding and associated non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to complete an adequate operability evaluation in accordance with Procedure EN-OP-104, Operability Determination Process, Revision 16. Specifically, the licensee failed to complete an adequate operability evaluation and to identify the temperature switch TS-7904 for emergency diesel generator 2 exhaust fan VEF-24D as a degraded nonconforming condition for multiple failures to maintain its calibration.

Failure to Perform Procedural Steps in Sequence during Surveillance Testing Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000313/2019002-02 Open/Closed

[H.12] - Avoid Complacency 71153 The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One Unit 1, Technical Specification 5.4.1.a, for the licensees failure to implement Procedure OP-1304.206, Unit 1 EFIC Channel B Monthly Test, SG Pressure Greater Than 750 PSIG, Revision 32. Specifically, the licensee failed to perform procedural steps in Procedure OP-1304.206 in sequence, which resulted in the inadvertent actuation of the turbine driven emergency feedwater pump P-7A, which started feeding both steam generators.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period at full power. On May 2, 2019, power was lowered to 85 percent to perform scheduled main turbine throttle and governor valve surveillance testing and was then returned to full power operation.

Unit 2 began the inspection period at full power. On May 6, 2019, power was lowered to 18 percent to facilitate an oil leak repair for reactor coolant pump C. Unit 2 was returned to full power on May 7, 2019. On May 26, 2019, Unit 2 had an automatic reactor trip from 100 percent power after reactor coolant pump B tripped on a ground fault. The unit transitioned to Forced Outage 2F19-01 to troubleshoot and repair reactor coolant pump B ground fault, repair reactor coolant pump C oil leak, and replace all reactor coolant pump control bleed-off lines.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.03) (1 Sample)

Unit 1 and Unit 2 Arkansas River flooding and potential severe weather on May 29, 2019.

Seasonal Extreme Weather Sample (IP Section 03.02) (1 Sample)

The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal hot temperatures for the following systems on April 25, 2019:

  • Unit 2 refueling water storage tank;
  • Unit 1 borated water storage tank;
  • Unit 1 and Unit 2 quality condensate storage tank.

Summer Readiness Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated summer readiness of offsite and onsite alternating current

(ac) power systems on June 18, 2019.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 high pressure safety injection pump C aligned to train A during containment spray pump A maintenance and surveillance testing on April 29, 2019;
(2) Unit 2 train B containment spray system during train A containment spray maintenance on June 3, 2019;
(3) Unit 2 engineering safety feature room A, B, and C safety-related ventilation system on June 11, 2019;
(4) Unit 1 emergency diesel generator 2 exhaust fan D on June 18, 2019;
(5) Unit 2 control element assemblies operating on the lower gripper on June 28, 2019.

71111.04S - Equipment Alignment

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

Unit 2 low pressure safety injection system on May 30, 2019.

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (6 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Unit 1 radwaste processing area, Fire Zone 20-Y, Fire Area C, on April 8, 2019;
(2) Unit 1 upper north piping penetration room, Fire Zone 79-U, Fire Area B-1, on April 11, 2019;
(3) Unit 1 lab and demineralizer access area, Fire Area 67-U, Fire Area B-9, on April 11, 2019;
(4) Unit 2 engineering safety features Room A, Fire Zone 2014-LL, Fire Area B-6, on May 15, 2019;
(5) Unit 2 engineering safety features Room C, Fire Zone 2010-LL, Fire Area B-6, on May 15, 2019;
(6) Unit 2 engineering safety features Room B, Fire Zone 2007-LL, Fire Area AA, on May 16, 2019.

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

Unit 1 breaching of train bay hatch HTC-492 in support of maintenance activities on April 22, 2019.

71111.07A - Heat Sink Performance

Annual Review (IP Section 02.01) (1 Sample)

The inspectors evaluated readiness and performance of:

Unit 2 engineering safety features room A, B, and C room coolers on May 30, 2019.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)

(1) Unit 1 down power to 85 percent thermal rated power for main turbine bypass valve and governor valve surveillance testing on May 2, 2019;
(2) Unit 2 down power to 18 percent thermal rated power for reactor coolant pump C oil leak repair on May 7, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

Unit 1 licensed operator requalification scenario on April 16, 2019.

71111.12 - Maintenance Effectiveness

Quality Control (IP Section 02.02) (2 Samples)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:

(1) Unit 1 and Unit 2 General Electric magne-blast 4160 volt breakers due to bent stop pin identified in Unit 1 high pressure injection pump C breaker preventing it from closing on May 30, 2019;
(2) Unit 1 high pressure injection pump motors on May 30, 2019.

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

Unit 2 low pressure safety injection system on May 17, 2019.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 1 high pressure injection pump B motor replacement and rigging and lifting of motor through hatch HTC-492 on April 11, 2019;
(2) Unit 2 emergent work for train A service water loop supply line to the containment coolers A and B pin hole through wall leak in the lower south piping penetration room on April 24, 2019;
(3) Unit 2 emergent work for control element assemblies 11 and 40 transferring from the upper gripper coil to the lower gripper coil and an unplanned 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> limiting condition for operation entry on April 24, 2019;
(4) Unit 2 high integrated risk for control element assembly 43 ACTM card replacement and transferring five control element assemblies to the lower gripper on April 26, 2019;
(5) Unit 2 Yellow risk for train A containment spray system maintenance outage on April 29, 2019;
(6) Unit 1 emergent work for reactor protection system Channel D nuclear instrument NI-8 causing spurious channel trips on April 30, 2019.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (7 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 2 containment spray pump B inlet check valve excessive clearance operability on April 4, 2019;
(2) Unit 1 high pressure injection pump C and reactor building spray pump B elevated pump vibrations operability on April 9, 2019;
(3) Unit 2 low pressure safety injection pumps A and B recirculation actuation system relays lead termination on April 24, 2019;
(4) Unit 1 train B emergency diesel generator fan coil D temperature limit instrument drift operability on May 2, 2019;
(5) Unit 2 containment spray pumps A and B seal oil coolers re-assembled with the incorrect torqueing requirements operability on May 9, 2019;
(6) Unit 2 train A service water loop supply line to containment coolers A and B pin hole through wall leak in the lower south piping penetration room operability on May 31, 2019;
(7) Unit 2 control element assemblies operating on the lower gripper drop time testing operability on June 28, 2019.

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Unit 2 temporary modification of reactor coolant pump C access cover on May 9, 2019;
(2) Unit 1 permanent modification of high pressure injection pump B motor replacement on May 28, 2019.

71111.19 - Post-Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (8 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Unit 1 reactor building spray pump A motor balancing maintenance on April 16, 2019;
(2) Unit 2 train B service water piping return header from emergency control room chiller B weld repair on April 22, 2019;
(3) Unit 1 high pressure injection pump B motor replacement on April 25, 2019;
(4) Unit 2 emergent work for control element assembly 40 transferring to the lower gripper on April 25, 2019;
(5) Unit 2 control element assembly 43 ACTM card replacement and transferring five control element assemblies to the lower gripper on April 26, 2019;
(6) Unit 2 containment spray pump A motor preventive maintenance on April 30, 2019;
(7) Unit 2 containment spray pump A seal cooler post maintenance testing on May 1, 2019;
(8) Unit 2 containment spray pump A breaker 2A-304 protective relay preventive maintenance on May 1, 2019.

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Partial)

Unit 2 evaluated Forced Outage 2F19-01 activities from May 26 to June 30, 2019. The inspectors completed inspection procedure Sections 03.01.a and 03.01.c.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Inservice Testing (IP Section 03.01)

Unit 2 low pressure safety injection pump A inservice testing surveillance on April 5, 2019.

Surveillance Tests (other) (IP Section 03.01) (5 Samples)

(1) Unit 2 train A low pressure safety injection and refueling water tank valve stroke surveillance on April 5, 2019;
(2) Unit 2 containment spray pump A surveillance testing on May 8, 2019;
(3) Unit 2 emergency feedwater system to auxiliary feedwater boundary check valve surveillance testing corrective actions on June 4, 2019;
(4) Unit 1 train A and B service water cross-tie valves CV-3640, CV-3642, CV-3644, CV-3644 leakage surveillance testing on June 6, 2019;
(5) Unit 1 emergency diesel generator 2 exhaust fan D temperature instrument calibration surveillance on June 18, 2019.

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

The licensee submitted a summary of emergency plan changes (Revision 43) to the NRC on April 4, 2019. The inspectors conducted an in-office review of the changes from April 22 to May 15, 2019. This evaluation does not constitute NRC approval.

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

Unit 1 loss of coolant accident concurrent with a loss of offsite power with multiple equipment failures on May 15,

RADIATION SAFETY

71124.02 - Occupational ALARA Planning and Controls

Radiological Work Planning (IP Section 02.01) (1 Sample)

The inspectors evaluated the licensees radiological work planning by reviewing the following activities:

  • RWP 2017-2500, 2E-35 A/B Replacement Activities during 2R25;
  • RWP 2018-1404, Maintenance Activities 1R27 (Bulk Work);
  • RWP 2018-2430, 2R26 Reactor Disassembly/Reassembly;
  • RWP 2018-2903, Inspections/Repair of Reactor Vessel Closure Head (RVCH)

Nozzle #49.

Verification of Dose Estimates and Exposure Tracking Systems (IP Section 02.02) (1 Sample)

The inspectors evaluated dose estimates and exposure tracking. The inspectors reviewed the following ALARA planning documents:

  • RWP 2017-2500, 2E-35 A/B Replacement Activities during 2R25;
  • RWP 2018-1404, Maintenance Activities 1R27 (Bulk Work);
  • RWP 2018-2430, 2R26 Reactor Disassembly/Reassembly;
  • RWP 2018-2903, Inspections/Repair of Reactor Vessel Closure Head (RVCH)

Nozzle #49.

Additionally, the inspectors reviewed the following radiological outcome evaluations:

==1R26 ALARA Report, 2016;

  • ==

==2R26 ALARA Report, 2018.

==

71124.04 - Occupational Dose Assessment

External Dosimetry (IP Section 02.02) (1 Sample)

The inspectors evaluated the external dosimetry program implementation.

Internal Dosimetry (IP Section 02.03) (1 Sample)

The inspectors evaluated the internal dosimetry program implementation.

Whole Body Counts

ID Date

1.

===23721 11/14/2018

2. 23089

10/20/2018

3. 20639

3/28/2018

4. 23799

10/19/2018

5. 24295

5/5/2018

In-vitro internal monitoring

ID Date Sample No.

1. 24610

4/5/2018 FIS 2499

2. 24109

4/7/2018 SMI 7572 Dose assessments performed using air sampling and DAC-hr monitoring

  • None were available during this inspection

Source Term Categorization (IP Section 02.01)===

The inspectors evaluated the licensees characterization of the source term and use of scaling factors for the use of hard-to-detect radionuclide activity.

Special Dosimetric Situations (IP Section 02.04) (1 Sample)

The inspectors evaluated special dosimetric situations.

Declared pregnant workers:

ID Date

1.

===21082 10/27/2018

2. 23810

10/27/2018

EDEX exposures:

ID Date

1. 24625

10/13/2019

2. 24628

10/13/2019

Shallow Dose Equivalent:

ID Date Assessment No.

1. 24458

10/19/2018 2018-057

2. 24309

10/25/2018 2018-064

Neutron Dose Assessment:

ID Date

1. 29595

2H18

2. 21914

2H18

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10)

=

(1) Unit 1 (April 1, 2018 - March 31, 2019);
(2) Unit 2 (April 1, 2018 - March 31, 2019).

BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)

(1) Unit 1 (April 1, 2018 - March 31, 2019);
(2) Unit 2 (April 1, 2018 - March 31, 2019).

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (2 Samples)

(1) Unit 1 (April 1, 2018 - March 31, 2019);
(2) Unit 2 (April 1, 2018 - March 31, 2019).

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

Unit 1 and Unit 2 service water pump dissimilar metal connection for pump bowl and column on May 31, 2019.

Semiannual Trend Review (IP Section 02.02) (1 Sample)

Unit 1 and Unit 2 potential adverse trend in human performance events on June 28, 2019.

71153 - Followup of Events and Notices of Enforcement Discretion Event Followup (IP Section 03.01)

(1) Unit 1 automatic actuation of the steam driven emergency feedwater pump during emergency feedwater initiation and control Channel B testing on June 12, 2019;
(2) Unit 2 automatic reactor trip due to a ground fault trip of reactor coolant pump B on May 26,

INSPECTION RESULTS

Licensee-Identified Non-Cited Violation 71124.02 This violation of very low safety significance was identified by the licensee, has been entered into the licensees corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation: Technical Specification 5.4.1(a) requires, in part, that written procedures shall be implemented covering applicable procedures recommended in Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation), Revision 2, Appendix A, February 1978. Section 7(e) of Regulatory Guide 1.33 covers Radiation Protection Procedures.

Contrary to the above, during Refueling Outage 2R20 in October 2009, the licensee failed to implement written procedures for radiation protection when they free released a radioactively contaminated eddy current probe from the radiologically controlled area (RCA), and subsequently shipped it offsite for maintenance, in August 2018, without proper controls.

Specifically, the licensee primarily failed to implement the following requirements, in part, in licensee Procedure EN-RP-121, Radioactive Material Control, Revision 4 (effective 11/04/2008), and Revision 15 (effective 12/11/2018):

  • Revision 4, Section 5.7.4 - Unconditional release of materials other than personal items SHALL be released with the following applicable requirements met:
  • Prior to releasing items that have been inside the RCA, ensure the material has been properly surveyed;
  • Item has no detectable loose or fixed contamination greater than the established minimum sensitivity of the combined survey method and instrument.
  • Revision 4, Section 5.7.7 - Conditional release of radioactive material (RAM) is allowed from the RCA if the material is properly labeled.
  • Revision 15, Section 5.5.1 - All radioactive material shall be properly labeled prior to being transported from one location to another.
  • Revision 15, Section 5.6.1 - For Control and Release of Material, items may be considered for free release as long as ALL of the following criteria are met:
  • No detectable fixed activity above background, other than naturally occurring isotopes;
  • No detectable suspected internal contamination;
  • No radioactive labels or markings.

In addition, the licensee's procedure defines RAM, in part, as any item or material which satisfies the following conditions:

  • Has detectable contamination, fixed or loose, greater than the minimum sensitivity of the survey instrument, OR causes a validated alarm on an automated monitor;
  • Has been evaluated to have inaccessible areas that may have become contaminated.

On October 3, 2018, the radioactively contaminated eddy current probe was found to have fixed contamination and alarmed the gamma small articles monitor when surveyed at the request of the nondestructive examination (NDE) group who asked the radiation protection (RP) group to perform surveys on their instrumentation as part of their baseline survey program. The licensee determined that the probe had been stored outside of the RCA since 2009 in the NDE laboratory, untagged as RAM, which violated radiation protection procedures. RP identified the presence of 600 ccpm (corrected counts per minute) of Cs-137 on the eddy current probe. As a result, the probe was tagged as RAM and controlled in a radioactive materials area.

NRC's Inspection Manual Chapter 0609, Appendix D, Public Radiation Safety, states that at a licensee's facility, any equipment or material that came into contact with licensed radioactive material or that had the potential to be contaminated with radioactive material of plant origin and are to be removed from the facility, and must be surveyed for the presence of licensed radioactive material prior to shipment from the facility. In assessing the significance of the performance deficiency, the inspectors determined that the finding was Green, of very low safety significance, because although it involved a failure in radioactive materials control and was transported from the site, surface contamination levels were less than 5 times any limits and there was no radiation exposure above 1 percent of any occupational or public dose limit (less than 0.005 rem).

As immediate corrective actions, the licensee reviewed and updated their procedures to enhance the requirements of surveying equipment, tooling, and components. They also conducted a strategic sweep survey of instrumentation stored in areas of interest outside of the RCA with high sensitivity instruments to avoid future instances of failed controls. No additional radioactive material was identified. These actions were documented in their evaluation via Condition Report CR-ANO-2-2018-02545-01.

Significance: Green

Corrective Action References: Condition Report CR-ANO-2-2018-02545

Observation: Semiannual Trend Review 71152 The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address the identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site.

To verify that the licensee was taking corrective actions to address identified adverse trends that might indicate the existence of a more significant safety issue, the inspectors reviewed the corrective action program documentation associated with a potential adverse trend in human performance events from the time period of December 2018 through June 2019.

Examples of these events included:

  • CR-ANO-2-2019-01359. During performance of Procedure OP-2304.065, maintenance personnel mis-identified the terminal board layout in cabinet 2C99B.

This resulted in the incorrect lead being de-terminated and operations notified maintenance personnel. The leads were re-terminated, and work was stopped. In response, the licensee performed a human performance analysis with Performance Improvement Review Group (PRG) review.

  • CR-ANO-2-2019-01432. During the performance of the cold shutdown test Procedure OP-2102.010, Attachment F, Auxiliary Spray and Charging Bypass Check Valve Test, the charging system flow path was inadvertently isolated resulting in charging pump C supply breaker tripping and charging pump A discharge relief valve opening. The licensee classified this condition report as an adverse condition - Advance Broke Fix to investigate the human performance and process deficiencies.
  • CR-ANO-1-2019-01418. During troubleshooting of temperature switch TSL-5261 Unit 1 emergency diesel generator (EDG) 2 jacket water temperature low switch, maintenance personnel discovered that the temperature switch wiring was incorrect at the switch terminations. Upon further review, it was identified that the lifted lead log was filled out incorrectly while performing Procedure OP-1304.135, EDG 2 Instrument Calibration. This condition resulted in the re-termination being incorrect when maintenance personnel on the next shift re-installed switch TSL-5261 in accordance with the log. This condition report was closed to CR-ANO-2-2019-01359 due to similar human performance issues identified.
  • CR-ANO-1-2019-01515. While preparing to sample SPING 3 (RX-9830, Unit 1 fuel handling area ventilation radiation monitor) via the alternate sampling pump, a chemist closed SS-9830B (sample isolation valve V-13), which was not part of the procedure in use by the chemist. The chemist restored the valve to its original position when discovering that testing was in progress. This disabled the sampling required by the Offsite Dose Calculation Manual. The SPING 3 was in a nonfunctional status at the time of the valve manipulation, and operators secured the spent fuel pool exhaust fan which resulted in a condition where Offsite Dose Calculation Manual requirements no longer apply.
  • CR-ANO-C-2019-02098 and CR-ANO-C-2019-02144. The licensees Nuclear Independent Oversight identified maintenance personnel are not consistently applying human performance tools to mitigate risk.

The licensees immediate corrective actions for the recent potential adverse trend in human performance events included:

  • Multiple work stoppage stand-downs to reinforce the use of human performance tools which occurred on March 4, 2019, May 9, 2019, and June 11, 2019. Specifically:

1. Pre-job brief/job site review - Ensure licensee personnel understand the task,

required roles and responsibilities, plant impact, and human performance traps and tools. Take the time to examine your work area to identify and eliminate or mitigate all hazards.

2. Procedure use and adherence - Follow procedures as written without deviating

from their intent. If the procedure cannot be performed as written or is unclear, stop and correct it or obtain guidance from your supervisor.

3. Verification and validation - Use verification methods to validate assumptions

before, during, and after an action, such as self-check, peer check, concurrent and independent verification.

  • All licensee personnel were required to sign a commitment letter to being an excellent nuclear professional after the May 9, 2019, stand down and prior to re-commencing work activities at the station. This commitment letter reinforced the use of human performance tools, avoiding complacency, taking accountability for performance, maintaining a safety-conscious work environment, and making a commitment to mitigating nuclear, radiological, industrial safety, and environmental risks.

The inspectors noted the following:

1. The licensees immediate actions have not reduced the number of human

performance events that occurred after the stand downs where completed.

2. CR-ANO-C-2019-02144 human performance event trend condition report was

classified as a nonadverse condition, even though multiple human performance errors had consequences associated with them (i.e., lifting relief valves, tripping pump breakers, inadvertent initiation of emergency feedwater to an operating steam generator, and the loss of a safety-related 4160 volt bus until the EDG restored power). The inspectors questioned the classification of Condition Report CR-ANO-C-2019-02144 and whether it was appropriately classified as a nonadverse condition. However, the inspectors noted the licensee was performing a common cause analysis with an organizational programmatic screening as required for an adverse condition.

3. The inspectors questioned the long term sustainability and effectiveness of the

corrective actions implemented by the common cause analysis documented in Condition Report CR-ANO-C-2018-02728. The licensees effectiveness review, completed on January 28, 2019, concluded that the corrective actions where effective. However, the licensees Nuclear Independent Oversight issued a quality assurance finding for corrective action plans that were not being implemented with rigor or having sustainable actions, which included corrective actions associated with common cause analysis documented in CR-ANO-C-2018-02728.

Failure to Properly Evaluate Operability of the Unit 1 Emergency Diesel Generator 2 Room Ventilation System Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems

Green NCV 05000313/2019002-01 Open/Closed

[P.4] - Trending 71111.15 The inspectors identified a Green finding and associated non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to complete an adequate operability evaluation in accordance with Procedure EN-OP-104, Operability Determination Process, Revision 16. Specifically, the licensee failed to complete an adequate operability evaluation and to identify the temperature switch TS-7904 for emergency diesel generator 2 exhaust fan VEF-24D as a degraded nonconforming condition for multiple failures to maintain its calibration.

Description:

On April 15, 2019, the licensee performed an inspection and calibration of temperature switch TS-7904 for emergency diesel generator (EDG) 2 exhaust fan VEF-24D under Work Order (WO) 52794842. During inspection and calibration, the licensee identified temperature switch TS-7904 was 20 degrees out of the calibration range of 103 to 107 degrees Fahrenheit (F) (as found setpoint was 127 degrees F). This condition was above the required setpoint and above the Safety Analysis Report (SAR) maximum room temperature of 120 degrees F. Exhaust Fan VEF-24D was immediately declared inoperable and was re-calibrated to the required set point range to restore it to operable. The licensee initiated Condition Report CR-ANO-1-2019-00959 to document this issue in the corrective action program and assess operability.

The inspectors reviewed Condition Report CR-ANO-1-2019-00959, the licensing and design basis for the EDG exhaust fan units, the history of the inspection and calibration of temperature switch TS-7904, and the licensees operability evaluation Procedure EN-OP-104, Operability Determination Process, Revision 16. The inspectors noted the following:

  • Procedure EN-OP-104, step 8.10.11, states, in part, a system, structure, or component (SSC) that has been identified as having reduced reliability is considered degraded or nonconforming and evaluated to determine whether a SSC is operable, and reduced reliability is indicated by multiple failures, repetitive failures, or failures that exceed the number of expected failures.
  • Procedure EN-OP-104, step 8.1, states, in part, 1. Determine the impact of the degraded or nonconforming condition on the technical specification SSC or the specified safety function; and 2. Determine if there is an ongoing degradation mechanism that can impact: 1. Future operability based on changing conditions; and

2. SSCs specified safety functions and mission time.

  • EDG 1 and 2 exhaust fans VEF-24A/B/C/D are safety related exhaust fans whose purpose is to support EDG operation by preventing their respective EDG rooms from exceeding 120 degrees F. Each EDG room has two redundant exhaust fans. In the event of a failure of the lead exhaust fan (VEF-24A/C), the backup fan (VEF-24B/D)would be sufficient to cool the respective room.
  • Condition Reports CR-ANO-1-2018-04294 and CR-ANO-1-2018-05007 documented the inability of EDG exhaust fans VEF-24A/B/C/D to achieve the required Unit 1 SAR flow rates to maintain EDG operability when outside ambient temperature was greater than 85 degrees F. This issue was identified by the NRC design basis assurance inspection team and documented as non-citied violation 05000313/2018011-01.
  • Temperature switch TS-7904 inspection and calibration were on a 5-year interval.

Further review of the inspection and calibration history by the inspectors identified temperature switch TS-7904 was out of calibration three of the last five intervals. The inspectors identified this condition as a degrading trend of the temperature switch drift in accordance with Procedure EN-OP-104, and the licensee did not identify this degraded condition. This information was not utilized by the licensee when assessing operability of exhaust fan VEF-24D and operability of EDG 2.

From the information above, the inspectors questioned the operability of exhaust fan VEF-24D to perform its safety function to start within its required temperature band to support operability of EDG 2 when outside ambient air temperature was greater than 85 degrees F and informed the licensee of their issue. In response to the inspectors question, the licensee entered this issue into their corrective action program as Condition Report CR-ANO-1-2019-01032 and immediately re-assessed operability of EDG 2.

The licensee determined temperature switch TS-7904 was subsequently calibrated to within its nominal range of 103 to 107 degrees F, but due to the as-found drift identified, it brought into question the reliability of the component and the undesirable consequences if temperature switch TS-7904 were to drift outside of its allowable temperature range. In response to this information the licensee declared EDG 2 operable-compensatory measure, with the compensatory measure implemented by Standing Order, VEF-24D EDG Exhaust Fan, to manually start exhaust fan VEF-24D any time EDG 2 was started automatically or manually.

Corrective Actions: The licensee implemented Standing Order, VEF-24D EDG Exhaust Fan, as a compensatory measure until temperature switch TS-7904 was replaced on June 6, 2019.

Corrective Action References: Condition Report CR-ANO-1-2019-01032

Performance Assessment:

Performance Deficiency: The licensees failure to identify a reduced-reliability, safety-related component as a degraded nonconforming condition and appropriately assessing operability is a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone. Specifically, temperature switch TS-7904 reduced reliability, degrading instrument drift, and the as-found setpoint above the maximum allowed EDG room temperature of 120 degrees F.

Significance: The inspectors assessed the significance of the finding using Appendix A, Significance Determination of Reactor Inspection Findings for At - Power Situations. The finding was determined to be of very low safety significance (Green) because it:

(1) did not represent a deficiency affecting the design or qualification of a mitigating SSC;
(2) did not represent a loss of system and/or function;
(3) did not represent an actual loss of function of at least a single train for more than its technical specification allowed outage time OR two separate safety systems out-of-service for more than its technical specification allowed outage time; and
(4) did not represent an actual loss of function of one or more nontechnical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Cross-Cutting Aspect: P.4 - Trending: The organization periodically analyzes information from the corrective action program and other assessments in the aggregate to identify programmatic and common cause issues. Specifically, the licensee failed to identify the trend of temperature switch TS-7904 being out of calibration on multiple events.

Enforcement:

Violation: Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances. The instructions, procedures, or drawings shall include appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accomplished. Procedure EN-OP-104, Operability Evaluation, Revision 16, an Appendix B, quality-related procedure, provides instructions for identifying SSC that require operability evaluation and how to assess operability. Procedure EN-OP-104 steps:

  • 8.1, states, in part, 1. Determine the impact of the degraded or nonconforming condition on the technical specification SSC or the specified safety function; and

2. Determine if there is an ongoing degradation mechanism that can impact: 1. Future

operability based on changing conditions; and 2. SSCs specified safety functions and mission time.

  • 8.10.11, states, in part, an SSC that has been identified as having reduced reliability is considered degraded or nonconforming and evaluated to determine whether an SSC is operable, and reduced reliability is indicated by multiple failures, repetitive failures, or failures that exceed the number of expected failures.

Contrary to above, from April 15, 2019, to April 24, 2019, the licensee failed to implement Procedure EN-OP-104, steps 8.1 and 8.10.11. Specifically, the licensee failed to identify temperature switch TS-7904 for EDG 2 exhaust fan VEF-24D as degraded nonconforming condition for multiple failures to maintain its calibration and to complete an adequate operability evaluation. This condition resulted in the licensee declaring EDG 2 as operable-compensatory measure, with compensatory measure being to manually start exhaust fan VEF-24D anytime EDG 2 was started automatically or manually until the associated temperature switch was replaced.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Perform Procedural Steps in Sequence during Surveillance Testing Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems

Green NCV 05000313/2019002-02 Open/Closed

[H.12] - Avoid Complacency 71153 The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One Unit 1, Technical Specification 5.4.1.a, for the licensees failure to implement Procedure OP-1304.206, Unit 1 EFIC Channel B Monthly Test, SG Pressure Greater Than 750 PSIG, Revision 32. Specifically, the licensee failed to perform procedural steps in Procedure OP-1304.206 in sequence, which resulted in the inadvertent actuation of the turbine driven emergency feedwater pump P-7A, which started feeding both steam generators.

Description:

On May 9, 2019, the licensee was performing emergency feedwater initiation and control (EFIC) Channel B surveillance testing in accordance with Procedure OP-1304.206. During the performance of this surveillance test the licensee inadvertently actuated the turbine driven emergency feedwater (EFW) pump P-7A and commenced feeding both once through steam generators. The licensees immediate actions were to secure EFW pump P-7A, to close both EFW steam admission valves, and to lower reactor power to 99 percent. The closure of the steam admission valves caused the licensee to declare them inoperable.

The licensee performed a prompt investigation to determine the preliminary cause of the inadvertent initiation of EFW pump P-7A and identified that a human performance error occurred during the performance of Procedure OP-1304.206, Section 8.8, ESAS Trip Test.

Licensee personnel failed to perform the following Procedure OP-1304.206 steps:

  • 8.8.7 press and release train B EFW (EFW pump P-7A) reset pushbutton on the remote switch matrix;
  • 8.8.8 verify the tripped 1 indicator on the EFW trip module in EFIC Channel B goes on solid after testing train B EFW bus 1.

These steps were not performed prior to performing step 8.8.9 press and release manual at the manual/auto pushbutton for the EFIC system train B EFW bus 2 trip. This resulted in both the EFIC system train B EFW bus 1 and bus 2 to trip at the same time, causing the actuation of the EFW pump P-7A and the unplanned feeding of both steam generators by the EFW system. The licensee entered this issue into their corrective action program as Condition Report CR-ANO-1-2019-01181, and performed an adverse condition analysis which identified the causal factors (CFs) of the event to be:

  • CF 1: Clear Performance Standards - Clear performance standards were not consistently set and reinforced. Personnel responsible for oversight of the maintenance did not identify and correct degrading standards of performance in procedure use and adherence.
  • CF 2: Inadequate Procedure Use and Adherence - Personnel were transitioning between reader-doer and performer-verifier modes during performance of the task without recognizing the inherent risk in this activity, leading to gaps in human performance tool use, unclear communications, and subsequent failure to perform the procedure as written.
  • CF 3: Verbal Communication - Personnel did not utilize three-way communication to verify that the intended action was taken in the proper sequence.

Corrective Actions: The licensee halted the transient by securing EFW pump P-7A, closing both EFW steam admission valves, and lowering power to 99 percent. The licensee initiated an instrumentation and control work stoppage to allow management to assess the impacts of the error and to formulate a recovery plan to prevent future occurrences.

Corrective Action References: Condition Report CR-ANO-1-2019-01181

Performance Assessment:

Performance Deficiency: The licensees failure to perform procedural steps in sequence during EFIC Channel B monthly surveillance testing was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Human Performance attribute of the Mitigating Systems cornerstone. Specifically, the licensee failed to perform procedural steps in sequence during EFIC Channel B monthly testing, resulting in the inadvertent actuation of the EFW pump P-7A, the unplanned feeding of both steam generators by the EFW system, and both EFW steam admission valves to be inoperable.

Significance: The inspectors assessed the significance of the finding using Appendix A, Significance Determination of Reactor Inspection Findings for At - Power Situations. The inspectors determined that the finding had very low safety significance (Green) because it:

(1) was not a design deficiency;
(2) did not represent a loss of system and/or function;
(3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and
(4) did not result in the loss of a high safety-significant, nontechnical specification train.

Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. Specifically, the licensee failed to use their human performance tools to ensure procedural steps were performed in sequence (i.e., failure to use three-way communications; not all personnel involved attended the pre-job brief; and the use of reader-doer instead of performer-verifier mode).

Enforcement:

Violation: Unit 1 Technical Specification 5.4.1.a requires, in part, that written procedures be established, implemented, and maintained covering the applicable procedures recommended in Appendix A to Regulatory Guide 1.33, Quality Assurance Program Requirements, Revision 2, February 1978. Regulatory Guide 1.33, Appendix A, Section 9, states that maintenance that can affect the performance of safety related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. The licensee established Procedure OP-1304.206, Unit 1 EFIC Channel B Monthly Test, SG Pressure Greater Than 750 PSIG, Revision 32, to perform surveillance testing of the EFIC Channel B during power operations with steam generator pressures greater than 750 PSIG. Procedure OP-1304.206 provides the following steps:

  • 8.8.7 press and release train B EFW (EFW pump P-7A) reset pushbutton, on the remote switch matrix prior to performing, and;
  • 8.8.8 verify the tripped 1 indicator on the EFW trip module in EFIC Channel B goes on solid.

Contrary to the above, on May 9, 2019, the licensee failed to implement Procedure OP-1304.206, steps 8.8.7 and 8.8.8. This resulted in the inadvertent actuation of the EFW pump P-7A and the unplanned feeding of both steam generators by the EFW system.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On May 9, 2019, the inspectors presented the radiation safety inspection results to Mr. B. Davis, Acting Site Vice President and Director of Engineering, and other members of the licensee staff.
  • On May 15, 2019, the inspectors presented the emergency plan revision in-office review inspection results to Mr. A Sherrill, Manager, Emergency Preparedness, and other members of the licensee staff.
  • On July 9, 2019, the inspectors presented the integrated inspection results to Mr. B. Patrick, Director, Regulatory Assurance and Performance Improvement, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Calculations

CALC-92-E-0078-

LPSI Pump NPSH Calculation

Corrective Action

Documents

CR-ANO-

1-2018-04294, 1-2019-00959, 1-2019-01061, 1-2019-01032,

1-2019-01033, C-2019-01992, C-2019-01993

Corrective Action

Documents

Resulting from

Inspection

CR-ANO-

1-2019-01036, C-2019-01552

Engineering

Changes

EC-51913

Start-up Transformer #2 Non-Segregated Bus Duct Flood

Modification

Procedures

OP-1015.033

ANO Switchyard and Transformer Yard Controls

OP-1106.006

Emergency Feedwater Pump Operation

109

OP-1107.001

Electric System Operations

23

OP-1202.007

Degraded Power

OP-1203.007

Abnormal ES Bus Voltage and Degraded Offsite Power

OP-1203.025

Natural Emergencies

OP-1203.12H

Annunciator K09 Corrective Action

OP-2017.001

Electrical System Operations

29

OP-2104.005

Containment Spray

OP-2106.006

Emergency Feedwater System Operations

100

OP-2203.008

Natural Emergencies

OP-2203.012F

Annunciator 2K06 Corrective Action

OP-2203.054

Abnormal Grid

Work Orders

WO 25596, 516790-15, 523470-01

71111.04

Calculations

CALC-88-E-0032-

LOCA Containment Analysis for ANO-2 SGR and Power

Uprate

CALC-91-E-0116-

NPSH Calculation for HPSI and RB Spray

CALC-94-0094-

Room 2010 Heat Load Evaluation

CALC-94-E-0095-

Room 2007/2009 Heat Load Evaluation

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CALC-94-E-0095-

Room 2013/2014 Heat Load Evaluation

Corrective Action

Documents

CR-ANO-

1-2019-00959, 1-2019-01061, 2-2019-00944, 2-2019-01084,

2-2019-01096

Corrective Action

Documents

Resulting from

Inspection

CR-ANO-

1-2019-01228, 1-2019-01032, 1-2019-01033, 2-2019-01264,

2-2019-01269

Drawings

M-2210 Sheet 2

P&ID Service Water System

M-2232 Sheet 1

P&ID Safety Injection System

2

M-2236 Sheet 1

P&ID Containment Spray System

Miscellaneous

ULD-2-SYS-05

Containment Spray System

ULD-SYS-30

ANO Unit 2 Auxiliary Building HVAC System

Procedures

OP-1104.036

Emergency Diesel Generator Operation

OP-2104.005

Containment Spray

OP-2104.039

HPSI System Operation

86, 87

OP-2104.040

LPSI System Operations

OP-2203.003

CEA Malfunction

OP-2203.012E

Annunciator 2K05 Corrective Action

OP-2203.012F

Annunciator 2K06 Corrective Action

Work Orders

WO 2820434

71111.04S

Calculations

CALC-92-E-0078-

LPSI Pump NPSH Calculation

Corrective Action

Documents

CR-ANO-

2-2004-00065, 2-2012-03023, 2-2015-00070, 2-2016-02461,

2-2017-01180, 2-2017-02118, 2-2017-04416, 2-2018-00653,

2-2019-01003, 2-2019-01921, C-2018-01693,

Drawings

M-2232, Sheet 1

P&ID Safety Injection

2

Engineering

Changes

EC-72499

Replace 2P-60B LPSI Allis-Chambers Motor with New

Siemens Motor WO-477487 Task 30

EC-74087

Recommended Standby Oil Level Band for 2P-35B and 2P-

60B

Miscellaneous

ULD-2-SYS-04

Low Pressure Safety Injection and Shutdown Cooling

System

Procedures

OP-2104.040

LPSI System Operations

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OP-2107.001

Electrical System Operations

2

OP-2203.012E

Annunciator 2K05 Corrective Action

OP-2203.012F

Annunciator 2K06 Corrective Action

OP-2403.011

2P-60 A and B Low Pressure Safety Injection Motor

Maintenance

Work Orders

WO 383683, 402313, 450476, 472947, 52680297,

71111.05Q Corrective Action

Documents

CR-ANO-

2-2013-02426, 2-2015-00906, 2-2016-03077, 2-2019-00785

Corrective Action

Documents

Resulting from

Inspection

CR-ANO-

2-2019-01275, 2-2019-01282

Fire Plans

PFP-U1

ANO Prefire Plan (Unit 1)

PFP-U2

ANO Prefire Plan (Unit 2)

Miscellaneous

Fire Impairment

3167 and 8054

Procedures

COPD-024

Risk Assessment Guidelines

EN-DC-161

Control of Combustibles

EN-DC-330

Fire Protection Program

OP-1000.120

ANO Fire Impairment Program

OP-1003.014

ANO Fire Protection Program

OP-2405.016

Unit 2 Penetration Fire Barrier Visual Inspection

Work Orders

WO 456698, 516652, 52600436

71111.06

Calculations

CALC-95-R-0024-

Basic Requirements for the Component Database on Station

Doors and Hatches

Corrective Action

Documents

CR-ANO-

1-2019-00256, 1-2019-00911, C-2015-01888, C-2015-

01929, C-2019-00241, C-2019-00252, C-2019-01773, C-

2019-01976

Corrective Action

Documents

Resulting from

Inspection

CR-ANO-

C-2019-00621

Engineering

Changes

EC-368727

EC-58301

Review of Opening Hatch HTC-492 During Normal

Operation for HELB and Flooding Concerns Identified in CR-

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

ANO-C-2015-01888

EC-63132

Evaluate Internal Flooding Effects Due to CW Pipe Break or

Rupture on the Unit 1 and Unit 2 Turbine Buildings CR-ANO-

C-2016-00873

EC-74710

HELB Doors and Hatches Documents Clean-Up

Procedures

OP-1015.052

Passive Barrier Breach Permitting Process

1, 2

OP-1104.018

Spent Resin Transfer Operations

Work Orders

WO 368727, 512890

71111.07A

Calculations

CALC-91-R-2013-

Service Water Performance Testing Methodology

CALC-94-0094-

Room 2010 Heat Load Evaluation

CALC-94-E-0095-

Room 2007/2009 Heat Load Evaluation

CALC-94-E-0095-

Room 2013/2014 Heat Load Evaluation

Corrective Action

Documents

CR-ANO

2-2012-01037, 2-2012-03023, 2-2017-01566

Corrective Action

Documents

Resulting from

Inspection

CR-ANO

2-2019-01265, 2-2019-01266

Engineering

Changes

EC-72776

Document the Results of the 2R25 As-Left Service Water

Flow Test

EC-73958

Excess Airflow Effects on AB Room Cooler Thermal

Performance and Other Impacts Including Changes to SW

Methodology Report

EC-80295

Document the Results of the 2R26 As-Left Service Water

Flow Test WO 503112

Miscellaneous

ULD-2-SYS-30

ANO Unit 2 Auxiliary Building HVAC System

Procedures

OP-2104.005

Containment Spray

OP-2104.039

HPSI System Operation

OP-2104.040

LPSI System Operations

OP-2203.012E

Annunciator 2K05 Corrective Action

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OP-2305.062

Service Water System Flow Testing

Work Orders

WO 2439, 503112, 52541048, 52736254

71111.12

Calculations

CALC-91-EQ-

1001-01

Large Motors Program Resolution Project Plan

Corrective Action

Documents

CR-ANO-

1-2018-05167, 1-2019-00484, 1-2019-00531, 1-2019-00860,

2-2017-03691, 2-2018-02583, 2-2018-03739, 2-2018-04196,

2-2018-04446, 2-2018-04450, 2-2019-00328, 2-2019-00887,

2-2019-00889, 2-2019-00890, 2-2019-03337, 2-2019-03561,

C-2019-01219,

Corrective Action

Documents

Resulting from

Inspection

CR-ANO-

2-2019-00975

Drawings

M-2236, Sheet 1

P&ID Containment Spray System

Miscellaneous

ULD-2-SYS-04

Low Pressure Safety Injection and Shutdown Cooling

System

Procedures

EM-WM-107

Post Maintenance Testing

OP-2104.004

Shutdown Cooling System

OP-2104.040

LPSI System Operations

OP-2305.003

ESF Response Time Test

Work Orders

WO 477487, 478089, 479504, 510351, 512119, 519804,

2770826,

71111.13

Corrective Action

Documents

CR-ANO-

1-2019-00860, 1-2019-01056, 1-2019-01070, 1-2019-01073,

2-2019-00944, 2-2019-01073, 2-2019-01084, 2-2019-01096,

Engineering

Changes

EC-80852

Temporary Support over HTC-483 for P-36B Motor

Replacement

Procedures

COPD-024

Risk Assessment Guidelines

EN-FAP-WM-002

Critical Evolutions

EN-OP-119

Protected Equipment Postings

EN-WM-104

On Line Risk Assessment

OP-1015.021

ANO-2 EOP/AOP User Guide

OP-1015.052

Passive Barrier Breach Permitting Process

1, 2

OP-2203.003

CEA Malfunction

Work Orders

WO 2780, 523624, 52271362, 52790576, 52820434

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.15

Calculations

CALC-88-E-0200-

P-T Calculation for Unit 2 Service Water System

Corrective Action

Documents

CR-ANO-

1-1993-00577, 1-1994-00168, 1-2002-00202, 1-2009-01061,

1-2016-02577, 1-2017-01323, 1-2018-00467, 1-2018-04294,

1-2019-00959, 2-2010-02863, 2-2010-02865, 2-2016-04277,

2-2018-03527, 2-2018-03532, 2-2018-03579, 2-2019-00675,

2-2019-00780, 2-2019-00856, 2-2019-00863, 2-2019-00935,

2-2019-00936, 2-2019-00937, 2-2019-00938, 2-2019-00948,

2-2019-00949, 2-2019-00951, 2-2019-00952, 2-2019-

00953, 2-2019-00954, 2-2019-00955, 2-2019-00956, 2-

2019-00957, 2-2019-00958, 2-2019-00959, 2-2019-01073,

2-2019-01084, 2-2019-01096, 2-2019-01171, 2-2019-01172,

C-2014-01256

CR-WF3-

2011-03190

Corrective Action

Documents

Resulting from

Inspection

CR-ANO-

1-2019-01032, 1-2019-01055, 2-2019-00975

Drawings

ISO 2HBC-76-2

ISO 2HCC-313-1

Engineering

Changes

EC-73910

Baseline Reference Values for the ANO-1 IST Components

Engineering

Evaluations

ER-ANO-2002-

00795-000

Evaluation of Fabricated Replacement Shells for 2E-47A and

2E-48B

ER-ANO-2002-

00795-001

Use of 3/8 SA515 Gr 70 Plate on 2E-47E

ER-ANO-2004-

0899-000

Miscellaneous

Tagout SW-082

Repair Leak

Procedures

CEP-WP-004

Weld Map

7.4

EN-DC-117

PMT and Special Instructions

EN-OP-104

Operability Determination Process

EN-WM-105

Planning

EN-WM-107

Post Maintenance Testing

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OP-1104.005

Reactor Building Spray System Operation

OP-1104.036

Emergency Diesel Generator Operation

OP-1203.012A

Annunciator K01 Corrective Actions

OP-2104.004

SDC System

OP-2104.005

Containment Spray

OP-2104.036

Emergency Diesel Generator Operations

Work Orders

WO 261219, 395275, 461547, 511635, 521657, 522220, 524108,

24122, 52774476, 52796462, 52798635, 52805005,

2809497, 52810242, 52825505

71111.18

Calculations

CALC-10-E-0010-

ANO-1 HPI Rooms GOTHIC Heat-up Calculations

CALC-87-D-1016-

Thermal and Hydraulic Calculation for Lube Oil Cooler E-

39A, E-39B, and E-39C

CALC-87-E-0011-

Post LOCA HPI Temperature with No Room Cooling with

Two Trains of ECCS Available

CALC-92-R-2010-

Non-Permanent Plant Equipment to Remain Inside the ANO-

Containment Building

Corrective Action

Documents

CR-ANO-

1-2019-00879, 2-2018-04242, 2-2019-00701, 2-2019-00718,

2-2019-01219, 2-2019-01240, C-2019-01678

Drawings

M-231 Sheet 1

P&ID Makeup and Purification System

116

M-232 Sheet 1

P&ID Decay Heat Removal System

108

Engineering

Changes

EC-80852

High Pressure Injection Pump B Motor Replacement

EC-82335

2P-32C Access Cover Temporary Enclosure

Procedures

EN-QV-102

Quality Control Inspection Program

OP-1015.036

Containment Building Closeout

OP-1104.002

Makeup and Purification System Operation

OP-1104.004

Decay Heat Removal Operating Procedure

130

OP-1202.012

Repetitive Tasks

OP-1203.041

Small Break LOCA Cooldown

OP-1305.040

Service Water Flow Testing

Work Orders

WO 21614, 52271362

71111.19

Corrective Action

CR-ANO-

1-2019-00910, 2-2010-02863, 2-2010-02865, 2-2016-04277,

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

2-2017-02269, 2-2019-00780, 2-2019-00856, 2-2019-00863,

2-2019-00935, 2-2019-00936, 2-2019-00937, 2-2019-00938,

2-2019-00944, 2-2019-00948, 2-2019-00949, 2-2019-00951,

2-2019-00952, 2-2019-00953, 2-2019-00954, 2-2019-00955,

2-2019-00956, 2-2019-00957, 2-2019-00958, 2-2019-00959,

2-2019-01084, 2-2019-01130

Corrective Action

Documents

Resulting from

Inspection

CR-ANO-

1-2019-00879, 2-2019-00863, 2-2019-01132, 2-2019-01171,

2-2019-01172

Miscellaneous

CEP-WP-004

Weld Map

7.4

ER 991782N201

ISO 2HBC-76-2

ISO 2HCC-313-1

MAI-21068

NDE 2-BOP-UT-

10-017

Tagout SW-082

Repair Leak

TD W180.0050

Instructions for Installing and Operation Seal Injection Water

Coolers

Procedures

EN-WM-107

Post Maintenance Testing

OP-1104.002

Makeup and Purification System Operation

OP-1305.040

Service Water Flow Test

OP-1416.052

Unit 1 and 2 IAC66K Relay Test Instructions

OP-1416.064

Unit 1 and 2 HFC11B and HFC21B Relay Test Instructions

OP-2104.005

Containment Spray

OP-2104.036

EDG Ops

Work Orders

WO 261219, 461547, 521657, 522220, 522780, 5280434,

271362, 52790576, 52798126, 52810242

71111.20

Corrective Action

Documents

Resulting from

Inspection

CR-ANO-

2-2019-01461, 2-2019-01462, 2-2019-01463, 2-2019-01464

Engineering

EC-83134

Engineering Evaluation 01: Acceptability of Rigging 2P-32B

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Changes

in Mode 5 and Deviations from EC53308 Requirements

EC-83154

Procedures

EN-OU-108

Shutdown Safety Management Program

OP-1015.016

RCS/PZR Temperature vs Time

OP-2102.010

Plant Cooldown

OP-2104.004

Shutdown Cooling System

71111.22

Calculations

CALC-91-R-2013-

Service Water Performance Testing Methodology

CALC-92-E-0078-

Unit 2 CSS Pump Performance Requirements

CALC-97-E-0020-

Instrument Error Analysis for Containment Spray Pump

Local Indicators to Support Containment Spray Pump

Inservice Testing

CALC-97-E-0020-

Loop Error Analysis for 2FT-5610 and 2FT-5616 to Support

Containment Spray Pump IST

Corrective Action

Documents

CR-ANO-

1-2013-01728, 1-2014-01535, 1-2016-01004, 1-2019-00959,

1-2019-01125, 2-2011-01925, 2-2017-02189, 2-2017-03337,

2-2018-04357, 2-2019-00944, 2-2019-01264, C-2017-

01651, C-2017-01780

Corrective Action

Documents

Resulting from

Inspection

CR-ANO-

1-2019-01032, 1-2019-01035, 1-2019-01055, 2-2019-01478

Drawings

M-209, Sheet 1

P&ID Circulating Water, Service Water, and Fire Water

Intake Structure

115

Engineering

Changes

EC-44915

CV-3640/3644 Valve Rotation 18 Degrees

EC-75425

Documentation of Baseline for ANO-2 Reference Values for

IST

EC-77690

Document Analysis of 1R27 As-Found and As-Left Service

Water Flow Test per CALC-91-R-2013-01

EC-81619

Calculation Change Evaluation

Engineering

Evaluations

ER-ANO-2005-

0072-000

Inservice Testing Acceptance Criteria for Unit 2 Containment

Spray Pumps

Miscellaneous

PIF 2-19-0049

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

SEP-ANO-2-IST-

ANO Unit 2 Inservice Testing Bases Document

SEP-ANO-IST-2

ANO Unit 2 Inservice Testing Plan

SEP-ANO-IST-3

ANO Unit 2 Inservice Testing Cross Reference Document

STM-2-05

Emergency Core Cooling System

ULD-1-SYS-10

ANO Unit 1 Service Water System

Procedures

OP-1015.001

Conduct of Operations

118

OP-1104.029

Service Water and Auxiliary Cooling System

119

OP-1104.036

Emergency Diesel Generator Operation

OP-2104.005

Containment Spray

OP-2104.040

LPSI System Operations

OP-2106.006

Emergency Feedwater System Operations

100

Work Orders

WO 23470-01, 52704842-01, 52788661, 52794379, 52807284,

2820434, 52794842

71114.04

Miscellaneous

0CAN041901

Emergency Plan Revision 43, Arkansas Nuclear One - Units

and 2, Docket Nos. 50-313, 50-368, and 72-13; Renewed

Facility Operating License Nos. DPR-51 and NPF-6

04/04/2019

9.1,

Process

Applicability

Determination

Form

EC 71778, Super Particulate Iodine Noble Gas (SPING)

Radiation Monitoring System Replacement Project,

Associated Child ECs 71779, 74229, 76289 and Field

Change Request (FCR) Tracked by AR 28349128349103/14/2018

9.2,

CFR

50.54(q)(3)

Screening

Procedure/Document Number: EC74229, Revision: 0

09/20/2018

9.3,

CFR

50.54(q)(3)

Evaluation

Procedure/Document Number: EC74229, Revision: 0

09/20/2018

9.3,

CFR

50.54(q)(3)

Procedure/Document Number: EC 717778 and 71779,

Revision: 0

10/03/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Evaluation

9.3,

CFR

50.54(q)(3)

Evaluation

Procedure/Document Number: ANO Emergency Plan,

Revision: 43

03/21/2019

Procedures

EN-EP-305

Emergency Planning 10CFR50.54(q) Review Program

71114.06

Corrective Action

Documents

Resulting from

Inspection

CR-ANO-

1-2019-01245, 2-2019-01478

Procedures

OP-1202.002

Loss of Subcooling Margin

OP-1202.010

ESAS

OP-1203.039

Excess RCS Leakage

OP-1203.041

Small Break LOCA Cooldown

OP-1903.011

Emergency Response/Notifications

71124.02

Corrective Action

Documents

CR-ANO-

1-2018-00306, 1-2018-01063, 2018-01273, 1-2018-01359,

1-2018-01840, 1-2018-02388, 1-2018-02484, 1-2018-03229,

1-2018-03492, 1-2018-03544, 1-2019-01039, 2-2017-06115,

2-2018-00740, 2-2018-00862, 2-2018-02545, 2-2018-03171,

2-2019-01128, C-2018-01264, C-2018-01465, C-2018-

01622, C-2018-02513, C-2018-02799, C-2018-04302, C-

2018-04354, C-2019-00313

Miscellaneous

1R26 ALARA Report

2016

1R27 ALARA Report

2018

2R25 ALARA Report

2017

2R26 ALARA Report

2018

ANO Alpha Hazard Evaluation

10/15/2018

ANO Full 5-Year Exposure Reduction Plan 2019-2023

2/11/2018

ANO-2018-0083

2018 Radiation Energy Distribution Evaluation

2/12/2018

Procedures

EN-RP-100

Radiation Worker Expectations

EN-RP-102

Radiological Control

EN-RP-105

Radiological Work Permits

EN-RP-106

Radiological Survey Documentation

EN-RP-110

ALARA Program

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

EN-RP-110-01

ALARA Initiative Deferrals

EN-RP-110-03

Collective Radiation Exposure (CRE) Reduction Guidelines

EN-RP-110-04

Radiation Protection Risk Assessment Process

EN-RP-110-06

Outage Dose Estimating and Tracking

EN-RP-121

Radioactive Material Control

EN-RP-121

Radioactive Material Control

Radiation Work

Permits (RWPs)

2016-1404

Routine Maintenance Activities During 1R26 (Bulk Work)

2017-2500

2E-35 A/B Replacement Activities During 2R25

2018-1401

Radiation Protection Activities 1R27

2018-1404

Maintenance Activities 1R27 (Bulk Work)

2018-1501

Replace Service Water Piping VCC-2 A/B to include both

locations

2018-2430

2R26 Reactor Disassembly/Re-Assembly

2018-2903

Inspections/Repair of Reactor Vessel Closure Head (RVCH)

Nozzle #49

2019-2057

U2 Reactor Building Power Entries for Surveys and Repairs

Related to 2P-32C ("C" Reactor Coolant Pump) Oil Leak

Self-Assessments ANO-2018-0010

ANO 2017 Annual Radiation Protection Report

01/30/2018

ANO-2019-0011

ANO 2018 Annual Radiation Protection Report

2/28/2019

LO-ALO-2018-

00062-02

Self-Assessment: Radiation Safety - ALARA & Dose

Assessment

11/01/2018

71124.04

Corrective Action

Documents

CR-ANO-

1-2018-02983, 2-2018-02350, 2-2018-03530, 2-2018-03816,

C-2017-04510, C-2017-04582, C-2018-00617, C-2018-

00633, C-2018-01033, C-2018-01248, C-2018-02585, C-

2018-02587, C-2018-03632, C-2018-03925, C-2018-03926,

C-2018-04312, C-2018-04599, C-2019-00220, C-2019-

221, C-2019-00458, C-2019-00616, C-2019-00725, HQN-

2018-01384

Miscellaneous

Aggregate DLR DDE / SRD Comparison Report

3/21/2019

2018

NVLAP Accreditation Certificate

1/1/2018

2019

NVLAP Accreditation Certificate

2/17/2018

ANO-2018-0015

2018 Neutron Dose Assignment Protocol

2/19/2018

ANO-2018-0079

2017-2018 ANO Evaluation of Internal Dose Monitoring

2/4/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

C-2017-04510

Dosimetry Investigation Report ID 22453

11/28/2017

C-2017-04582

Dosimetry Investigation Report ID 20029

2/5/2017

C-2018-01248

Dosimetry Investigation Report ID 21535

3/14/2018

C-2018-01248

Dosimetry Investigation Report ID 21329

3/14/2018

EN-RPT-18-001-

RO

Standardization of a Bias between DLR and SRDs in the

Entergy Fleet

9/25/2018

Procedures

1000.031

Radiation Protection Manual

EN-RP-104

Personnel Contamination Events

EN-RP-201

Dosimetry Administration

EN-RP-202

Personnel Monitoring

EN-RP-203

Dose Assessment

EN-RP-204

Special Monitoring Requirements

EN-RP-204-01

Effective Dose Equivalent (EDEX) Monitoring

EN-RP-205

Prenatal Monitoring

EN-RP-206

Dosimeter of Legal Record Quality Assurance

EN-RP-208

Whole Body Counting / In-Vitro Bioassay

EN-RP-210

Area Monitoring Program

EN-RP-311

Electronic Alarming Dosimeters

Radiation Work

Permits (RWPs)

2018-1902

Diving Activities in Support of Fuel Transfer System Repair

2018-2056

U2 Containment Power Entries for Inspection & Minor

Maintenance

2018-2903

Inspections/Repair of Rx Vessel Closure Head (RVCH)

Nozzle #49

Self-Assessments ANO-2019-0011

Arkansas Nuclear One 2018 Annual Radiation Protection

Report

2/28/2019

LO-ALO-2018-

00062-02

Self-Assessment: Radiation Safety - ALARA & Dose

Assessment

11/1/2018

71152

Corrective Action

Documents

CR-ANO-

1-2019-00529, 1-2019-01181, 2-2019-01429, 2-2019-01430,

2-2019-01431, C-2019-00970, C-2019-01147, 2-2019-

01359, 2-2019-01432, 1-2019-01418, C-2019-02098, C-

2019-02144, 1-2018-05311, 2-2018-03018, C-2019-00649,

1-2019-01181

71153

CR-ANO-

1-2019-01181

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Miscellaneous

STM 1-66

Emergency Feedwater Initiation and Control

Procedures

OP-1203.012K

Annunciator K12 Corrective Action

OP-1304.206

Unit 1 EFIC Channel B Monthly Test, SG Pressure Greater

Than 750 psig

2