IR 05000280/1988014

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Insp Repts 50-280/88-14 & 50-281/88-14 on 880403-30.No Violations or Deviations Noted.Major Areas Inspected:Plant Operations,Plant Maint,Plant Surveillance,Ler Review & Followup on Inspector Identified Items
ML18152A917
Person / Time
Site: Surry  Dominion icon.png
Issue date: 05/25/1988
From: Cantrell F, Holland W, Larry Nicholson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A916 List:
References
50-280-88-14, 50-281-88-14, NUDOCS 8806070199
Download: ML18152A917 (11)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA.STREET, ATLANTA, GEORGIA 30323 Report Nos.:

50-280/88-14 and 50-281/88-14 Licensee:

Virginia Electric and Power Company Richmond, Virginia 23261 Docket Nos.:

50-280 and 50-281 Facility Name:

Surry 1 and 2 License Nos.:

DPR-32 and DPR-37 Inspection Conducte~i April 3-30, 1988 Inspectors:

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. 1=</Y W. E. Holl~nd, SenforvR~sident Inspector

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L. E. Ni~holson, Re iijent Inspector Approved by: ~~~.

F.i.%. Cantrell~ ction Chief Division of Reactor Projects SUMMARY Date Sign~d:,{

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Date Signed sj2--5/yY ate Signed Scope:

This routine resident inspection was conducted on site in the areas of plant operations, plant maintenance, plant surveillance, licensee event report review, and followup on inspector identified item Results:

No violations or deviations were identified in this inspection report.

8806070199 880525 PDR ADOCK 05000280 Q

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REPORT DETAIL.

Persons Contacted Licensee Employees *D. L. Benson, Station Manager H. L. Miller, Assistant Station Manager

  • E. S. Grecheck, Assistant Station Manager J. A. Bailey, Superintendent of Operations J. W. Ogren, Superintendent of Maintenance S. P. Sarver, Superintendent of Health Physics R. H. Blount, Superintendent of Technical Servicei R. L. Johnson, Operations Supervisor J. A. Price, Site Quality Assurance Manager
  • G. D. Miller, Licensing Coordinator, Surry
  • Attended exit meeting Other licensee employees contacted included control room operators, shift technical advisors, shift supervisors and other plant personnel.

Exit Interview The inspection scope and findings were summarized on May 2, 1988, with those individuals identified by an asterisk in paragraph No new items were identified by the inspectors during this exi The licensee acknowledged the 1nspection findings with no dissenting comment The licensee did not identify as proprietary any of the materials provided to or reviewed by the inspectors during this inspectio.

Pl ant Status Unit 1 Unit 1 began the reporting period coasting down for the refueling outag On April 8, the unit began a rampdown from approximately 75% power for refueling and was placed in cold shutdown on April 10. At the end of the inspection period the unit was in day 21 of the maintenance/refueling outage which was scheduled to last 55 day Unit 2 Unit 2 began the reporting period at cold shutdown while making repairs to the vital bus III inverter and troubleshooting indicated flow blockage in the auxiliary feedwater (AFW) line. The inspectors monitored the licensee actions regarding the AFW blockage as detailed in paragraph The inverter was repaiTed and the unit achieved criticality at 7:32 pm on April 5, 198 The unit resumed power operation on April 6 and operated at power for the remainder of the inspection perio *

2 Licensee Action on Previous Enforcement Matters (92702)

(Closed) Violation 280; 281/88-01-02, Failure to provide adequate review or approval for replacement parts used in safety-related component The subject violation involved the discovery of hand-made parts of incorrect material and size that contributed to the fail~re of valve 2-CH-MOV-2289 No evaluation or documentation of approval could be produced regarding the defective parts. The licensee stated in their response to this violation, dated March 25, 1988, tha~ significant upgrades in maintenance procedures and philosophies have occurred since the maintenance was performed on this valv In addition, the licensee revised their administrative procedure regarding the subject. The inspector verified that the statement was added to the appropriate administrative procedure to require proper documentation from engineering prior to substitution of safety-related materia This item is close (Open) Unresolved Item 280; 281/88-04-02, Licensee review of steam flow instrumentation accuracy with regards to operation and accident analysis at low power level The item was identified in inspection report 280; 281/88-0 The inspector observed during a startup of the Unit 1 reactor that steam flow indication was not available for operator information until the indicated power level reached approximately 18%.

The inspector questioned the licensee with regard to whether steam flow instrumentation was providing indication within the design accuracy of the system at low power level. Also the inspector requested that the licensee review the1r accident analysis and operating procedures to evaluate if current low power indication of the instrumentation provides for appropriate automatic and/or operator actions during low power operatio During this period the inspector was provided a copy of an engineering evaluation which concluded that waiting until approxi.mately 25% power to apply channel check tolerance would have no impact on the existing safety analyse The station safety committee reviewed this evaluation and implemented a requirement to verify steam flow indication prior to exceeding 25% power in operations procedure. The inspector reviewed this information and, based on different requirements at other power stations, has requested that further technical review be accomplished by other NRC offices prior to closing this ite This issue will remain open until these reviews are complet.

Unresolved Items Unresolved items are matters about which more information is required to determine weather they are acceptable or may involve violations or deviation No new unresolved items are addressed in this inspection report.

  • 3 Plant Operations Operational Safety Verification (71707)

The inspectors conducted daily inspections in the following areas:

Control room staffing, access, and operator behavior; operator adherence to approved procedures, technical specifications, and limiting conditions for operations; examination of panels containing instrumentation and other reactor protection system elements to determine that required channels are operable; review of control room operator logs, operating orders, plant deviation reports, tagout logs, jumper logs, and tags on components to verify compliance with approved procedure The inspectors conducted weekly inspections in the following areas:

Verification of operability of selected ESF systems by valve alignment, breaker positions, condition of equipment or component(s), and operability of instrumentation and support items essenti a 1 to system actuation or performanc Plant tours which included observation of general plant/equipment conditions, fire protection and preventative measures, control of activities in progress, radiation protection controls, physical security controls, plant housekeeping conditions/cleanliness,. and missile hazards.

The inspectors routinely monitor the temperature of the auxiliary feedwater (AFW)

pump discharge piping to ensure steam binding is prevente Elevated temperatures were noted at the pump discharge headers following the Unit 2 restart during this inspection perio The licensee monitors the local readout from strap-on thermocouple jackets installed on both AFW discharge headers each shift. Temperatures on the headers were observed on April 7 to be 145 and 200 degrees F with the steam-driven pump casing very hot to the touc The 1 i censee implemented a temporary operating procedure (2-TOP-2015, "Unit 2 Auxiliary Feedwater Check Valve Leakage Guideline") that was to determine which of the check valves were leaking by and causing the temperature ris The results of this procedure indicates that although some paths are worse than others, it appears that all the check valves are subject to backleakag The licensee has reviewed Generic Letter 88-03 dated February 17, 198 The licensee has implemented the requirements to monitor fluid conditions within the AFW system and has since developed an abnormal procedure to be invoked when elevated temperatures are presen The inspectors continued an active overview of all actions in this are The inspectors conducted biweekly inspections in the foll owing areas:

Verification review and walkdown of safety-related tagout(s) in effect; review of sampling program (e.g., primary and secondary coolant samples, boric acid tank samples, plant liquid and gaseous samples); observation of control room shift turnover; review of implementation of the plant problem identification system; verification of selected portions of containment isolation lineup(s); and verification that notices to workers are posted as required by 10 CFR 1 *

Certain tours were conducted on backshifts or weekend Backshift or

,,2ekend tours were conducted on April 3, 25, and 2 Inspections included

~reas in the Units 1 and 2 cable vaults, Units 1 and 2 containments, vital battery rooms, steam safeguards areas, emergency switchgear rooms, diesel generator rooms, control room, auxiliary building, cable penetration areas, independent spent fuel storage facility, low level intake structure, and the safeguards va 1 ve pit and pump pit area Reactor coolant system (RCS) leak rates were reviewed to ensure that detected or suspected 1 eakage from the system was recorded, investigated, and evaluated; and that appropriate actions were taken, if require The inspectors routinely independently calculated RCS leak rates using the NRC Independent Measurements Leak Rate Program (RCSLK9).

On a regular basis, radiation work permits (RWPs) were reviewed and specific work activities were monitored to assure they were being conducted per the RWP Selected radiation protection instruments were periodically checked, and equipment operability and calibration frequency were verifie In the course of monthly activities, the inspectors included a review of the licensee's physical security progra The performance of various shifts of the security force was observed in the conduct of daily activities to include: protected and vital areas access controls;

-searching of personnel, packages and vehicles; badge issuance and retrieval; escorting of visitors; and patrols and compensatory posts.

During a routine review of operational data, the inspector witnessed a temperature transient in the component cooling system (CC) that appeared to be a result of degraded station vacuum priming to the CC heat exchanger The CC heat exchangers at this station consist of four shell and tube units, mounted horizontally, with one pass on each side of the heat exchange Component cooling water enters and exits the shell side through two 18-i nch openings while the service water enters through a 30-inch opening and travels through copper-nickel tubes. The 11A 11 and 118

heat exchangers are located at an elevation of ~pproximately 25 feet above sea level with the 11 C

and 11 0

heat exchangers located directly underneat Although all four heat exchangers are located in the Unit 1 turbine building basement, they may be aligned to support either uni Technical Specifications require two heat exchangers to be operable for one unit operation and three exchangers operable for two unit operatio The service water that flows through the tube-side is gravity fed from the intake canal that is required by Technical Specification to be maintained at a level 18 feet above sea leve Each service water side of the CC heat exchangers has a connection to the station vacuum priming system to aid in establishing service water flo This vacuum system consists of one vacuum priming tank, three vacuum primih~ pumps and the associated valves and piping that are primarily used to support main condenser operatio No mention is made of the vacuum priming system in either the Final Safety Analysis Report (FSAR) or the Technical Specifications.

..

The inspector questioned the reliance of this non-safety related system to maintain adequate service water flow through the component cooling water heat exchanger A rise in CC temperatures was corrected by blowing down the vacuum priming lines to the upper heat exchange Discussions with plant personnel and station management indicated that service water flow may degrade through the upper heat exchangers during certain a 11 owab 1 e operating conditions (i.e., low canal level with warm service water).

This situation is of particular concern during the current refueling outage when the canal level had been planned to be maintained low and the entire CC load carried by the two upper heat exchanger These concerns were identified by both the resident inspector and regional management to station management on May 4 and May 6, 1988, respectivel The licensee performed a design basis review that verified that the CC heat exchangers w~re designed to be fully operable without the aid of the vacuum priming system; however, it was also determined that the vacuum priming system is not seismically qualified upstream of the isolation va 1 ves 1 ocated directly above the heat exchanger A 11 four CC heat exchangers were declared inoperable on May 20 and actions performed to close the vacuum priming isolation valves and return the seismic supports for the vacuum piping from the heat exchangers to the va 1 ve These supports had been removed and missing for an unspecified period of tim The licensee also established an administrative low level limit of 27 feet in the intake cana The licensee also provided a letter from Virginia Power to the NRC dated April 26, 1988, that stated that the component cooling water system can be operated at any intake canal level consistent with the Technical Specifications and that vacuum priming is not required for continued system operation following flow initiatio The inspector held further discussions with the licensee on this issue and it was agreed that the licensee would conduct a test of the system after completion of all work scheduled during the present Unit 1 outage on the portion of the service water system which provides for flow to the component cooling water heat exchanger The test wi 11 verify that service water fl ow to the A and 8 component cooling water heat exchangers (upper) does not degrade at low canal levels with vacuum priming isolate The resident inspectors are continuing to monitor the performance of the CC heat exchangers and will review the licensee's test result The inspectors monitored the licensee actions with regards to the failure of the primary system power operated relief valves (PORV) that occurred on April 15, 198 While performing evolutions to take Unit 1 to cold shutdown for refueling in accordance with Operation Procedure 3.3, the reactor operator attempted to open the pressurizer PORV 1-PCV-145 No indication of valve movement was noted with the main control board switch held in the open position for approximately 15 second The switch was returned to the 11 auto 11 position and a similar attempt was made to open the other PORV, 1-PCV-1455C, with identical result The operator tried a second time to open each valve and the valves responded correctl The licensee identified this problem on station deviation Sl-88-295, and made a 4-hour report to the NR The inspectors will monitor licensee evaluation and repair of the PORV 1 s during the Unit 1 outag '

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Engineered Safety Feature System Walkdown (71710)

The inspector performed a walkdown of the components that are identified as important in the risk-based inspection guide developed for Surry. This PRA-based guide (EGG-REQ-7746, 11 PRA Applications Program For Inspection At The Surry Nuclear Power Station 11, dated July 1987) was developed to enable the inspector to quickly focus on only those components that perform vital functions during accident sequence The inspector used this modified checklist to perform walkdowns on both units. This verification also included the following:

confirmation that the licensee 1 s system lineup procedure matches plant drawings and actual plant configuration; hanger~

and supports are operable; housekeeping is adequate; valves and/or breakers in the system are installed correctly and appear to be operable; fire protection/prevention is adequate; major system components are properly labeled and appear to be operable; instrumentation is properly installed, calibrated, and functioning; and valves and/or breakers are in correct position as required by plant procedure and unit statu Within the areas inspected, no violations or deviations were identifie.

Maintenance Inspections (62703)

The in spec tor continued to fo 11 ow the effort to locate an apparent blockage in the auxiliary feedwater (AFW) line to the 11A 11 steam generator that was observed following the Unit 2 reactor trip on March 27, 198 This issue was also discussed in Inspection Report 280; 281/88-0 Fibroscopic examination of the entire length of pipe from the AFW headers up to the point that AFW ties into the 11A11 main feed line revealed no obstructio The licensee then disassembled and inspected all the motor-operated valves downstream of the AFW headers and found no contributor to blockage. However, the tack welds that secure the discs to the stem nuts were found to be cracked in three of the six valves. This item was reviewed by a region-based specialist and discussed in Inspection Report 280;281/88-1 The AFW system was subsequently reassembled and retested using all possible flowpaths with each of the three pump Results of this testing indicated all parameters functioning normally with no indications of blockage note The results of the inspections and testing were closely monitored by the resident inspector and were the subject of several conference calls between station and NRC managemen The licensee concluded that the apparent blockage was no longer present and the unit returned to power operations on April 5, 198 Outage related maintenance items (Unit 1)

During this inspection period, the residents selected several maintenance items for monitoring during the Unit 1 maintenance/refueling outage. They were:

  • Auxiliary Feedwater System Repairs This area includes overhaul/repair of auxiliary feedwater motor operated valves and other work associated with the syste The area also includes overhaul of the Terry turbine which is the prime mover for the steam driven auxiliary feedwater pum When the inspection period ended, the turbine had been disassembled and repairs were in progress on the roto Design Change 85-32, Vital Bus Upgrade (UPS)

This area includes replacement of the Unit 1 DC vital power supply for the 11A 11 bus including new batteries and solid state battery charger/inverter packag When the inspection period ended, the new power supply inverter/battery chargers and batteries were being installe Recirculation Spray Heat Exchanger Replacement This area includes replacement of the four recirculation spray heat exchangers which are located in containment with new heat exchanger The replacements were required due to degradation of the heat exchanger tubes (90/10 copper/nickel).

The new heat exchangers have tubes made of titanium which is a more corrosion resistant material and should provide for a 1 anger service 1 if At the end of the inspection period, the four old heat exchangers had been removed from containment and the new heat exchangers were being moved into position in containmen Overhaul of the Pressurizer Power Operated Relief Valves (l-PCV-1455C and l-PCV-1456).

The subject PORVs were scheduled for overhaul due to seat leakage during unit operation at powe The inspection period ended prior to troubleshooting of the PORV stroke problem identified in paragraph The review of the above items was ongoing when the.inspection period ende This review will be addressed in more detail in next month's inspection repor Within the areas inspected, no violations or deviations were identifie.

Surveillance Inspections (61726)

During the reporting period, the inspectors reviewed various surveillance activities to assure compliance with the appropriate procedures as follows:

Test prerequisites were me Tests were performed in accordance with approved procedure L

Test procedures appeared to perform their intended functio Adequate coordination existed among personnel involved in the tes Test data was properly collected and recorde Inspection areas included the following:

On April 3, the inspector witnessed portions of Periodic Test l-PT-17.1, Containment Spray System, that verified operability of the containment spray pumps 1-CS-P-lA & Bas required by Technical Specification No discrepancies were note On April 6, 1988, the inspector witnessed portions of the monthly operability test of the emergency diesel generator #3 per Periodic Test l-PT-22.3 The diesel started and carried the required load with no abnormalitie No discrepancies were note On April 22, 1988, the inspector witnessed portions of testing to verify that the uncollected leakage from the safety injection system recirculation loop is within the requirements of Technical Specification Table 4.11-1. "This test is performed each refueling in accordance with procedure l-PT-16.100, System Leakage Test -For Safety Injection System -

External Recirculation Loo No discrepancies were note The inspectors routinely monitored the licensee performance with regards to local leak rate testing of containment isolation valves to establish an as-found total containment leak rate. _ This testing is performed per procedure l-PT-16.4, Containment Isolation Valve Leakag During testing of penetration #70, it was discovered that containment isolation valve l-RS-11 was being held in the open position. This valve is a 10-inch, 150 lb. weighted swing check valve manufactured by Schutte and Koerteri n The weighted arm that is designed to hold the valve closed was found to be approximately eight degrees beyond top dead center, resulting in the valve being held in the full open positio The licensee examined the three other identical valves in Unit 1 (l-RS-17, l-CS-13 and 24) and found that although they were being held in the full closed position, they had the potential to remain open once opened (once the weights had swung over top dead center).

The licensee considered this situation to constitute a violation of containment integrity and reported it pursuant to the requirements of 10 CFR 50.72.b. An entry was made to Unit 2 containment that verified the corresponding valves in that unit are in the closed position. A final engineering evaluation and additional corrective action was being developed as the inspection period ende The inspectors will continue to review this area during the next inspection perio Within the areas inspected, no violations or deviations were identifie *

9 Licensee Event Report (LER) Review (927001 The inspector reviewed the LERs listed below to ascertain whether NRC reporting requirements were being met and to determine appropriateness of the corrective action(s).

The inspector's review also included followup on implementation of corrective action and review of licensee documentation that all required corrective action(s) were complet LERs that identify violation(s) of regulation(s) and that meet the criteria of 10 CFR, Part 2, Appendix C,Section V shall be identified as Licensee Identified Violations (LIV) in the following closeout paragraph LIVs are considered first-time occurrence violations which meet the NRC enforcement policy criteria for exemption from issuance of a Notice of Violatio These items are identified to allow for proper evaluation of corrective actions in the event that similar events occur in the futur (Closed)

LER 280/87-24, Reactor Trip on Low Flow Due to Reactor Coolant Pump Trip. This report discussed the September 20, 1987, reactor trip on Unit 1 from 100 percent power due to low reactor coolant system flo Approximately 35 seconds after the reactor trip, a high steam flow with low RCS Tavg safety injection occurre The SI signal was only present for approximately 2 seconds and determined to be spuriou A low flow signal from the rector coolant pump trip was determined to be from the 18 1 reactor coolant pump breaker tripping on an instantaneous ground faul An engineering evaluation determined that the bus bar failure was caused by vibration of the unsupported length of feeder cable lead The bus bars on A and C RCPs were visually inspected and meggered to verify their integrity prior to unit restart. The licensee has subsequently issued an engineering work request (EWR) to add cable restraints to the feeder cables of each motor during the present refueling outage. Similar work is scheduled on Unit 2 during its upcoming refueling outag The inspector reviewed the EWRs and monitored progress during the Unit 1 refueling outag Thii LER is close (Closed) LER 280/87-33, Charging Pump Component Cooling Water System Inoperable Due to Inadequate Test Procedur The issue involved improper venting of the subject system after testing of a system componen This condition resulted in both charging pump component cooling pumps becoming air bound and inoperabl Immediate corrective action included venting of the system and restarting a charging pump component cooling pump to restore flo Additional corrective action to prevent recurrence was in the form of a revision to Periodic Test (PT)-53.18, "ASME Hydrostatic/

Pneumatic Pressure Tests" to include detailed instructions for depressuri zing and venting of systems at completion of testin The inspector reviewed the revised procedure, revision dated April 21, 198 This item is identified as a LIV (280/88-14-01) for failure to provide adequate procedure for restoration of a system after testing. This LER is closed.

1 Followup on Inspector Identified Items (92701)

(Closed)

Inspector Followup Item (IFI)

280; 281/87-28-01, Review Corrective Actions For Grinnel Valve This item was opened following the failure of the primary drain header isolation valve, 1-DG-14, during the failed loop stop valve packing event described in LER 87-1 This valve type utilizes a rubber diaphragm that tend to deteriorate with age and is used extensively throughout the statio The inspector reviewed the licensee program to periodically replace the diaphragms as well as the specific corrective actions for 1-DG-14, which involved changing it to a ball-type valv This item is closed.