IR 05000245/2013002

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IR 05000336-13-002, 05000423-13-002; 01/01/2013 - 03/31/2013: Millstone Power Station Units 2 and 3; Problem Identification and Resolution
ML13102A146
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 04/11/2013
From: Bellamy R R
NRC/RGN-I/DRP/PB5
To: Heacock D
Dominion Nuclear Connecticut
Bellamy R R
References
IR-13-002
Download: ML13102A146 (29)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 2100 RENAISSANCE BOULEVARD, SUITE 100 KING OF PRUSSIA, PENNSYLVANIA 19406-2713 April 11, 2013 Mr. David Heacock President and Chief Nuclear Officer Dominion Resources 5000 Dominion Boulevard Glen Allen, VA 23060-6711

SUBJECT: MILLSTONE POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000336/2013002 AND 05000423/2013002

Dear Mr. Heacock:

On March 31, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Millstone Power Station, Units 2 and 3. The enclosed inspection report documents the inspection results, which were discussed on April 9, 2013 with Stephen E. Scace, Site Vice President, and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

One NRC-identified finding of very low safety significance (Green) was indentified during this inspection.

This finding was determined to involve violations of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV), consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or significance of this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Millstone. If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at Millstone. In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access Management System (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/

Ronald R. Bellamy, PhD, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket Nos.: 50-336, 50-423 License Nos.: DRP-65, NPF-49

Enclosure:

Inspection Report 05000336/2013002 and 05000423/2013002

w/Attachment:

Supplementary Information

cc w/encl: Distribution via ListServ

SUMMARY

IR 05000336/2013002, 05000423/2013002; 01/01/2013-03/31/2013: Millstone Power Station Units 2 and 3; Problem Identification and Resolution.

This report covered a three-month period of inspection by resident inspectors and an in-office review by a specialist from the Office of Nuclear Security and Incident Response (NSIR). The inspectors indentified one finding of very low safety significance (Green) which was a non-cited violation (NCV). The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP), dated June 2, 2011. Cross-cutting aspects are determined using IMC 0310, "Components Within Cross-Cutting Areas," dated October 28, 2011. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy, dated June 7, 2012. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4.

Cornerstone: Mitigating Systems

Green.

The inspectors identified a Green NCV of 10 CFR 50 Appendix B, Criterion XI, "Test Control," for Dominion's failure to perform an adequate post maintenance test (PMT) on 2-RC-404, the Unit 2 'B' power operated relief valve (PORV). Specifically, a stroke test of the valve under hot conditions was not performed prior to entering Mode 3. Since the valve was observed to be leaking, Dominion cooled down the plant to repair the PORV and performed the specified PMTs including the valve stroke under hot conditions. Dominion entered the issue into their corrective action program (CAP), CR506539.

The finding is more than minor because it is associated with the Human Performance attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, Dominion's PMT of the PORV did not adequately demonstrate the valve's capability to stroke under all operating conditions. The finding was of very low safety significance (Green) because the finding did not represent an actual loss of system safety function, did not represent an actual loss of safety function of a single train for greater than its technical specification (TS) allowed outage time, did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with Dominion's maintenance rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and did not involve a loss or degradation of equipment designed to mitigate a seismic, flooding, or severe weather initiating event. The finding had a cross-cutting aspect in Human Performance, Work Control, because Dominion did not adequately incorporate actions to address the impact of work activities on plant operation. Specifically, Dominion incorrectly concluded that the PORV functional test was not required prior to entering Mode 3 H.3(b). (Section 4OA2)

REPORT DETAILS

Summary of Plant Status Millstone Unit 2 and Unit 3 operated at or near 100 percent power for the entire inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

The inspectors reviewed Dominion's preparations for the winter storm on February 8. The inspectors reviewed the implementation of adverse weather preparation procedures before the onset of and during this adverse weather condition. The inspectors verified that operator actions defined in Dominion's adverse weather procedures maintained the readiness of essential systems. The inspectors discussed readiness and staff availability for adverse weather response with operations and work control personnel.

Documents reviewed for each section of this inspection report are listed in the Attachment.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems: Unit 2 'C' charging pump while 'A' was out of service (OOS) for planned maintenance on January 24 'B' Emergency Diesel Generator (EDG) on February 13 while the 'A' EDG was OOS for cylinder liner replacement Facility 2 reactor building closed cooling water (RBCCW) while the Facility 1 RBCCW was OOS for testing on March 13

5 Enclosure Unit 3 'A' motor driven auxiliary feedwater (AFW) pump and train while 'B' MDAFW pump was OOS for testing on March 25. The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the Updated Final Safety Analysis Report (UFSAR), TS, work orders, condition reports (CR), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether Dominion staff had properly identified equipment issues and entered them into the CAP for resolution with the appropriate significance characterization.

b. Findings

No findings were identified.

.2 Full System Walkdown

a. Inspection Scope

On February 1 through 5, the inspectors performed a complete system walkdown of accessible portions of the Unit 2 boric acid system to verify the existing equipment lineup was correct. The inspectors reviewed operating procedures, drawings, equipment line-up check-off lists, and the UFSAR to verify the system was aligned to perform its required safety functions. The inspectors also reviewed electrical power availability, hangar and support functionality, and operability of support systems. The inspectors performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. Additionally, the inspectors reviewed a sample of related CR and work orders to ensure Dominion appropriately evaluated and resolved any deficiencies.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Resident Inspector Quarterly Walkdowns

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that 6 Enclosure Dominion controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression equipment was available for use as specified in the area pre-fire plan, and passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for OOS, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.

Unit 2 Auxiliary Building 480 Volt MCC B61 and B41A, Fire Area A-13 on February 11 Turbine Building Motor Driven Auxiliary Feed Pump Pit, Fire Area T-3 on February 11 6.9 and 4.16KV Switchgear Room, Fire Area T-7 on February 22 West Cable Vault, Fire Area T-8 on February 22 Low Pressure Safety Injection (LPSI) Pump Room, Fire Area A-3 on March 26 Unit 3 Turbine Building Battery Room 6, Fire Area TB-3 on March 22 Engineered Safeguards Features Building Refueling Water Storage Pumps Cubicle, Fire Area ESF-7 on March 21

b. Findings

No findings were identified.

.2 Fire Protection - Drill Observation

a. Inspection Scope

The inspectors evaluated the readiness of the plant fire brigade to fight fires. The inspectors verified that Dominion personnel identified deficiencies, openly discussed them in a self-critical manner and took appropriate corrective actions as required. The inspectors evaluated specific attributes as follows: Proper wearing of turnout gear and self-contained breathing apparatus Proper use and layout of fire hoses Employment of appropriate fire-fighting techniques Sufficient fire-fighting equipment brought to the scene Effectiveness of command and control Search for victims and propagation of the fire into other plant areas Smoke removal operations Utilization of pre-planned strategies Adherence to the pre-planned drill scenario Drill objectives met The inspectors also evaluated the fire brigade's actions to determine whether these actions were in accordance with Dominion's fire-fighting strategies.

7 Enclosure Unit 2 Drill Scenario conducted on March 22 that involved a fire in the motor driven AFW pump cubicle Unit 3 Drill Scenario conducted on March 12 that involved a fire in the 'A' service water (SW) cubicle of the Unit 3 intake structure.

b. Findings

No findings were identified.

1R06 Flood Protection Measures

Internal Flooding Review

a. Inspection Scope

The inspectors reviewed the UFSAR, the site flooding analysis, and plant procedures to assess susceptibilities involving internal flooding. The inspectors also reviewed the CAP to determine if Dominion identified and corrected flooding problems and whether operator actions for coping with flooding were adequate. The inspectors also focused on the Unit 2 DC switchgear rooms (flooding zones A-20 and A-21) to verify the adequacy of equipment seals located below the flood line, floor and water penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, control circuits, and temporary or removable flood barriers.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program

.1 Quarterly Review of Licensed Operator Requalification Testing and Training

a. Inspection Scope

The inspectors observed Unit 3 licensed operator simulator training on January 22, which included an instrument failure (RCS*LT459E), loss of condenser vacuum, and four faulted steam generators (SG). On January 29, the inspectors observed Unit 2 licensed operator simulator training scenario MP2 ES13101A, which included a recirculation pump seal failure and loss of coolant accident. The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classification made by 8 Enclosure the shift manager and the TS action statements entered by the shift technical advisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.

b. Findings

No findings were identified.

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

a. Inspection Scope

The inspectors observed the Unit 2 'B' EDG slow start surveillance and attempted restoration from the cross tying of 480V Bus 22A and 22B following troubleshooting on February 28. The inspectors also observed Unit 2 turbine control valve testing on March 10. The inspectors observed infrequently performed test or evolution briefings, pre-shift briefings, and reactivity control briefings to verify that the briefings met the criteria specified in Dominion's Operations Section Expectations Handbook and Dominion's Administrative Procedure OP-AA-329, "Conduct of Infrequently Performed Tests and Evolutions," Revision 1. Additionally, the inspectors observed test performance to verify that procedure use, crew communications, and coordination of activities among work groups similarly met established expectations and standards.

The inspectors observed routine Unit 3 control room activities on March 27 including radiation monitor and reactor protection system testing, operator response to unplanned control room alarms, and response to a medical emergency onsite. The inspectors observed the operators to verify that the crew appropriately coordinated and prioritized activities, that they used procedures as expected, and ensured the operators performed required turnover briefings.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on structure, system or component (SSC) performance and reliability. The inspectors reviewed system health reports, CAP documents, maintenance work orders, and maintenance rule basis documents to ensure that Dominion was identifying and properly evaluating performance problems within the scope of the maintenance rule. For each sample selected, the inspectors verified that the SSC was properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and verified that the (a) (2) performance criteria established by Dominion staff was reasonable. As applicable, for SSCs classified as (a) (1), the inspectors assessed the adequacy of goals and corrective actions to return these SSCs to (a) (2). Additionally, the inspectors ensured that Dominion staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.

9 Enclosure Unit 2 'B' PORV on January 22 `A` and `B` EDG on February 6 Containment Isolation on February 27 Unit 3 Control Room HVK Chillers on January 30 Maintenance Rule (a)(3) Periodic Self Assessment on March 29

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that Dominion performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that Dominion personnel performed risk assessments as required by 10 CFR 50.65(a) (4) and that the assessments were accurate and complete. When Dominion performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the station's probabilistic risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Unit 2 'C' RBCCW pump during planned surveillance testing on January 10 Yellow risk due to RPS matrix testing with the lower 4160V switchgear room in compensatory cooling on February 14 Emergent work to replace the AC-4 matrix relay in the reactor protection system on March 14 Yellow risk due to the reserve station service transformer and 'C' SW pump OOS for scheduled maintenance on March 21 Unit 3 Emergent Work on 3FWS*CTV41A-D feedwater isolation valve replacement project bypasses SLCRs envelope on February 5 Yellow Risk assessment due to Station Blackout (SBO) and EDG 'B' being unavailable on February 6 Yellow Risk Assessment due to all station Fire Pumps being unavailable on February 22 Emergent Repairs on the main generator output breaker air supply on March 22

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or non-conforming conditions: Unit 2 Leak on SW Supply to Vital Switchgear Coolers, X181A/B and X182 on January 2 CR502542 Acoustic Valve Monitoring System failed surveillance on January 15 Unit 3 CR500743/5/7 SW Valves 3SWP*870/873/868 dealloying on January 14 OD000524/525 Main Steam Line Pressure Transmitters Environmental Qualification Covers on February 19 RAS000220 3SWP*TV35B not maintaining SW temperature on 3HVK*CHL1B on January 14 CR503305 Unplanned Entry into TS 3.0.3 for ESF Building Supply and Exhaust fans 3HVQ*FN5A/6A starter replacement with safety injection pump 3SIH*P1A tagged out for maintenance on January 23 OD000529 Leakage and Corrosion identified on SW valves 3SWP*V661, 664, 665, 668 due to dealloying on February 26. The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the operability determinations to assess whether TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to Dominion's evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by Dominion. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.

b. Findings

No findings were identified.

1R18 Plant Modifications

Temporary Modifications 11 Enclosure

a. Inspection Scope

The inspectors reviewed the temporary modifications listed below to determine whether the modifications affected the safety functions of systems that are important to safety. The inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results, and conducted field walkdowns of the modifications to verify that the temporary modifications did not degrade the design bases, licensing bases, and performance capability of the affected systems.

Unit 3 TCC-MP-2013-009, Encapsulation of Dealloying SW Valves 3SWP*V661, 3SWP*V664, 3SWP*V665, and 3SWP*V668, Revision 000 on March 7 TCC-MP-2013-011, Temporary Installation of Main Generator Output Breaker 15G-3U-2 Air Supply on March 23.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test procedure to verify that the procedure adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure was consistent with the information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed test data to verify that the test results adequately demonstrated restoration of the affected safety functions. Unit 2 Turbine Driven AFW Weld Repair on Steam Leak on Trip Throttle Valve 2MS-464 on January 18 'A' EDG cylinder liner replacement and two year preventive maintenance on February 25 AC-4 matrix relay replacement in the reactor protection system on March 14 Unit 3 Chiller 3HVK*CHL1B overhaul and PMT on March 1 Starter replacement on 3SIH*MV8821B, safety injection pump to cold leg injection isolation valve on March 6 Post Maintenance Testing for repairs on main generator output breaker 15G-3U-2 Air Supply on March 22 12 Enclosure

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied TS, the UFSAR, and Dominion procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests: Unit 2 SP2602A, Reactor Coolant System (RCS) Leakage on January 2 'C' RBCCW pump in-service test (IST) on January 10 SP 2604D, LPSI Pump and Min-Recirc Check Valve (IST), Facility 2 on February 4 SP 2612A-005, 'A' SW Pump Comprehensive Pump Test, Revision 001-00 on February 25 (IST) Unit 3 SP 3626.7, 'D' SW pump (IST) on January 15 SP 31005A, MTC and Power Coefficient Measurements on February 15 SP 3622.3, TDAFW Pump Quarterly Operational Test (IST) on February 25 SP3604A.2, "Charging Pump 'B' Operational Readiness Test," Revision 014-02 on March 1 CP 3807F, Operation of the Reactor Plant Sample Sink, Revision 006-03 on March 26 SP3680.1, General RCS Leakage Trending, Revision 005-04 on March 27

b. Findings

No findings were identified. Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

NRC staff from the Office of Nuclear Security and Incident Response (NSIR) performed an in-office review of the latest revisions of various Emergency Plan Implementing 13 Enclosure Procedures and the Emergency Plan located under ADAMS accession number ML12363A067.

Dominion determined that in accordance with 10 CFR 50.54(q), the changes made in the revisions resulted in no reduction in the effectiveness of the Plan, and that the revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The NRC review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, this revision is subject to future inspection.

b. Findings

No findings were identified.

1EP6 Drill Evaluation

Training Observations

a. Inspection Scope

The inspectors observed a simulator training evolution for Unit 2 licensed operators on January 29 which required emergency plan implementation by an operations crew.

Dominion planned for this evolution to be evaluated and included in performance indicator data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors' activities was to note any weaknesses and deficiencies in the crew's performance and ensure that Dominion evaluators noted the same issues and entered them into the corrective action program.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

Reactor Coolant System (RCS) Specific Activity and RCS Leak Rate (4 samples)

a. Inspection Scope

The inspectors reviewed Dominion's submittal for the RCS specific activity and RCS leak rate performance indicators for both Unit 2 and Unit 3 for the period of January 1, 2012 through December 31, 2012. To determine the accuracy of the performance indicator data reported, the inspectors used definitions and guidance contained in NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors also reviewed RCS sample analysis and control room logs of daily measurements of RCS leakage, and compared that information to the data reported by the performance indicator. Additionally, the inspectors observed surveillance activities 14 Enclosure that determined the RCS identified leakage rate, and chemistry personnel taking and analyzing a RCS sample. b. Inspection Findings No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure 71152, "Problem Identification and Resolution," the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that Dominion entered issues into their CAP at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the CAP and periodically attended CR screening meetings.

b. Findings

No findings were identified.

.2 Annual Sample: Power Operated Relief Valve (PORV) Post Maintenance Testing

a. Inspection Scope

The inspectors performed an in-depth review of Dominion's corrective actions associated with CR497201, Need to Review Mode 3 Entry on November 15 to Ensure Compliance with TSSR 4.4.3.1.C. Following a rebuild of valve 2-RC-404, 'B' PORV, Dominion entered Mode 3, a mode which required the PORV to be operable, without performing all the required PMTs specified in work order 53102395511. The inspectors reviewed Dominion's assessment of the issue and corrective actions and interviewed licensing and operations personnel in order to determine whether Dominion was appropriately identifying and characterizing the issue and whether the planned or completed corrective actions were appropriate.

b. Findings and Observations

Introduction.

The inspectors identified a Green NCV of 10 CFR 50 Appendix B, Criterion XI, "Test Control," for Dominion's failure to perform an adequate PMT on 2-RC-404, the 'B' PORV. Specifically, a stroke test of the valve under hot conditions was not performed prior to entering Mode 3.

Description.

In October 2012, during the Unit 2 refueling outage, Dominion overhauled the 'B' PORV because of seat leakage during the operating cycle. Work order 53102395511 specified the following PMTs: PORV stroke time IST, normal pressurizer vent path verification and PORV position IST, and PORV functional test. The stroke 15 Enclosure time test was performed on October 21 in Mode 6 and the vent path verification and PORV position test was performed on November 11 in Mode 5, but the functional test was not performed prior to entering Mode 3 on November 15. TS 3.4.3 requires both PORVs to be operable in Mode 3. Dominion entered Mode 4 on November 16 at 08:10 to rework the PORV due to seat leakage. The inspectors questioned why the PORV function test had not been performed prior to entering Mode 3. The primary plant senior reactor operator who determined the post maintenance testing requirements for the PORV repair, put a restraint on the work order indicating that hot functional test had to be performed prior to Mode 2 since the surveillance requirement stated that the PORV had to be stroked at conditions representative of Mode 3 or 4. The shift manager was unaware of the PMT requirement. His concern at the time was low temperature overpressure protection and determined that the stroke time test and vent path verification tests, which were performed under cold plant conditions, were sufficient to demonstrate operability. The inspectors disagreed with the shift manager's determination based on Generic Letter 90-06 which stated that testing of the PORVs in HOT STANDBY (Mode 3) or HOT SHUTDOWN (Mode 4) was required in order to simulate the temperature and pressure environmental effects on the PORV. The inspectors concluded that Dominion's PMT was inadequate because it did not demonstrate the valve's capability to stroke under all operating conditions prior to entering Mode 3.

Analysis.

The inspectors determined that the failure to perform adequate PMT on the PORV in accordance with 10 CFR 50, Appendix B, Criterion XI, was a performance deficiency that was reasonably within Dominion's ability to foresee and correct, and should have been prevented. The finding is more than minor because it is associated with the Human Performance attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, the inspectors concluded that stroking the PORV only under cold conditions following the valve overhaul was insufficient to demonstrate that the valve would be operable under normal operating temperatures and pressures. As a result, the inspectors concluded that there was insufficient basis to justify valve operability when Dominion entered Mode 3. In accordance with IMC 0609.04, Initial Characterization of Findings," and IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power," the inspectors determined that the finding was of very low safety significance (Green) because the finding did not represent an actual loss of system safety function, did not represent an actual loss of safety function of a single train for greater than its TS allowed outage time, did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with Dominion's maintenance rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and did not involve a loss or degradation of equipment designed to mitigate a seismic, flooding, or severe weather initiating event. The inspectors determined that this finding had a cross-cutting aspect in Human Performance, Work Control, because Dominion did not adequately incorporate actions to address the impact of work activities on plant operation. Specifically, Dominion incorrectly concluded that the PORV functional test was not required prior to entering Mode 3 H.3(b).

16 Enclosure

Enforcement.

10 CFR 50, Appendix B, Criterion XI, "Test Control," requires, in part, that a test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures. Test results shall be documented and evaluated to assure that test requirements have been satisfied.

Contrary to the above, from November 15 until November 16, Dominion failed to perform an adequate PMT on the 'B' PORV. Dominion cooled down the plant on November 16 to repair the leaking valve a second time and performed the PORV functional test prior to entering Mode 3. Because this finding was of very low safety significance (Green) and has been entered into Dominion's CAP (CR506539), this violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.

(NCV 5000336/2013002-01: Inadequate Post Maintenance Testing Following PORV Maintenance)

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

(Closed) Licensee Event Report (LER) 05000336/2013-001-00: Historical Acoustic Monitor Channel Check Discovered to Have Not Met Acceptance Criteria On January 15, the required monthly channel check of the 'B' channel pressurizer safety valve acoustic valve monitor system (AVMS) position indication did not meet the acceptance criteria. The 'B' channel of AVMS was declared inoperable and TS 3.3.3.8, Accident Monitoring Instrumentation, Action 3 was entered. Upon review of previous data, Dominion determined that the December 2012 channel check had also failed to meet its acceptance criteria. This had not been recognized on the initial review in December. TS 3.3.3.8 Action 3 requires obtaining quench tank temperature, level, and pressure information and monitoring discharge pipe temperature once per shift when a channel of AVMS position indication is inoperable.

Dominion had not performed the monitoring requirements of TS 3.3.3.8 Action 3 from December 18, 2012 until January 15, 2013. Dominion's failure to perform Action 3 is a minor performance deficiency because the failure to implement the TS requirement had no safety impact and the required indications were always available. Upon discovery in January, Dominion immediately implemented monitoring of the parameters required by TS 3.3.3.8 Action 3. The failure to comply with TS 3.3.3.8 constitutes a minor violation that is not subject to enforcement action in accordance with the NRC's Enforcement Policy. This LER is closed.

4OA6 Meetings, Including Exit

On April 9, 2013, the inspectors presented the inspection results to Stephen E. Scace, Site Vice President, and other members of the Millstone staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report. At this meeting, NRC Branch Chief Dr. Ronald Bellamy presented the results of the NRC's 2012 annual assessment of Millstone Power Station as detailed in their annual assessment letter (ML13060A342).

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

M. Adams Plant Manager

L. Armstrong Manager, Training R. Acquaro Unit 3 Shift Manager D. Atwood Senior Instructor

G. Auria Nuclear Chemistry Supervisor

K. Bailey Fire Brigade Leader, Unit 3 Plant Equipment Operator
B. Bartron Supervisor, Licensing R. Beal Unit 2 Shift Manager J. Beaudoin Unit 3 Reactor Operator
H. Beeman Supervisor, Nuclear Engineering

T. Berger Unit 3 Shift Manager

E. Brodeur Unit 3 Shift Manager W. Chestnut Supervisor, Nuclear Shift Operations Unit 2
F. Cietek Nuclear Engineer, PRA

T. Cleary Licensing Engineer

G. Closius Licensing Engineer

C. Corey Nuclear Instrument Technician

H. Covin Senior Instructor, Nuclear Operations
L. Crone Supervisor, Nuclear Chemistry
J. Curling Manager, Protection Services

S. Doboe Unit 2 Shift Manager

J. Dorosky Health Physicist III

J. Figueria Fire Brigade Member, Unit 2 Plant Equipment Operator
M. Finnegan Supervisor, Health Physics, ISFSI
J. Foster Fire Brigade Member, Unit 2 Plant Equipment Operator

J. Gauvin Unit 3 Chemistry Technician

A. Gharakhanian Nuclear Engineer III

W. Gorman Supervisor, Instrumentation & Control
J. Grogan Supervisor Nuclear Training K. Grover Manager, Nuclear Operations C. Janus Maintenance Rule Coordinator

C. Karpinski Senior Instructor

D. Koropatkin Fire Brigade Member, Unit 2 Plant Equipment Operator
J. Laine Manager, Radiation Protection/Chemistry
Y. Landry Fire Brigade Member, Unit 2 Plant Equipment Operator S. Loeser Senior Nuclear Instrument Technician
R. MacManus Director, Nuclear Station Safety & Licensing

P. Malzahn Operations Manager On-Call

G. Marshall Manager, Outage and Planning
S. Matthesse Nuclear Chemistry Supervisor, Unit 3
C. Maxson Manager, Nuclear Oversight
S. McArthur Fire Brigade Member, Unit 3 Plant Equipment Operator
R. McDonald Senior Instructor, Nuclear Operations

F. Perkins Unit 3 STA

D. Reed Unit 3 Shift Manager

Attachment

R. Riley Supervisor, Nuclear Shift Operations Unit 3 M. Roche Senior Nuclear Chemistry Technician
L. Salyards Licensing, Nuclear Technology Specialist S. Scace Site Vice President J. Semancik Director of Engineering

A. Smith Asset Management

D. Smith Manager, Emergency Preparedness
S. Smith Manager, Engineering

J. Stoddard Unit 3 Supervisor Nuclear Shift Operations (Acting) T. Stringfellow Unit 3 Unit Supervisor D. Tilton Engineering Supervisor

S. Turowski Supervisor, Health Physics Technical Services
K. Underwood Senior Instructor, Nuclear Operations
C. Vournazos IT Specialist, Meteorological Data
R. Walsh Unit 3 Control Operator B. Wilkens Senior Safety Specialist, Site Fire Marshall

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

Opened/Closed

5000336/2013002-01 NCV Inadequate Post Maintenance Testing Following PORV Maintenance (Section 4OA2)

Closed

05000336/LER-2013-001-00 LER Historical Acoustic Monitor Channel Check Discovered to Have Not Met Acceptance Criteria (Section 4OA3)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

AOP 2560, Storms, High Winds and High Tides, Revision 010-13
AOP 3569, Severe Weather Conditions, Revision 18-00

Section 1R04: Equipment Alignment

Procedures

OP 2304C-002, Boric Acid Valve Lineup, Revision 000-08
OP 2330A-002, RBCCW System Alignment, Facility 2, Revision 000-06
OP 2330A-003, 'A' Pump is Supplying 'A' HX and 'C' Pump is Supplying 'C' HX With 24C Supplying 24E, Revision 000-00
OP 2346B-003, 'B' Diesel Generator (DG) Fuel Oil Valve Alignment, Revision 000-00
OP 2346C-004, 'B' DG SW Valve Alignment, Revision 000-04
Attachment
OP 2346C-005, 'B' DG Starting Air Valve Alignment, Revision 000-00
OP 2346C-006, 'B' DG Jacket Water Valve Alignment, Revision 000-01
OP 2346C-007, 'B' DG Lube Oil Valve Alignment, Revision 000-03
OP 2346C-008, 'B' DG Breaker/Control Switch Alignment, Revision 000
OP 3322, AFW System, Revision 021-16
OP 3322-002, AFW Train A, Revision 006-04
OP 3322-005, Electrical Checklist for AFW System, Revision 006-02

Condition Reports

481384

Miscellaneous

CVCS, Letdown and Boric Acid System Health Reports, 4th Quarter 2011 and 2012
RBCCW System Health Report, 4th Quarter 2012 MRE013477 MRE013481
MRE015355
MRE015699
MRE015797 MRE015922

Section 1R05: Fire Protection

Procedures

U2-24-FPP-FHA, Millstone Unit 2 Fire Hazards Analysis, Revision 12 U2-24-FFS, MP2 Firefighting Strategies, Revision 0 MNPS Fire Protection Evaluation Report, Analysis 84, Battery Room No. 6, Fire Area
TB-3, Revision 17.3 MNPS Fire Protection Evaluation Report, Analysis 51, Fire Area
ESF-7, Refueling Water Recirculation Pumps Cubicle, Revision 17.3
CM-AA-FPA-100, Fire Protection/ Appendix R (Fire Safe Shutdown) Program, Revision 6
EOP 3509, Fire Emergency, Revision 024-03
EOP 3509.13, Train 'B' SW Cubicle Fire, Revision 2
EOP 3509.10, Battery Room Fire, Revision 000-01

Condition Reports

509493
509781

Miscellaneous

Millstone 3 Fire Fighting Strategy, Fire Area
TB-3, Turbine Building Battery Room 6, Revision 0 Millstone 3 Fire Fighting Strategy, Fire Area
ESF-7, Refueling Water Recirculation Pumps Cubicle, Revision 0 41829-13-FP, Fire Protection Permit for the Turbine Building 38.6 ft level

Section 1R06: Flood Protection Measures

Condition Reports

454282
447663
408322
508967
Attachment Miscellaneous CA22083
CA216046 CA190063 CA195246
CA188353
CA176411
MPS2 Probabilistic Risk Assessment Model Notebook, Revision 1
NUREG 0800, Standard Review Plan 3.4.1, Internal Flood Protection for Onsite Equipment
Failures, Revision 3 NUREG 0800, Standard Review Plan 3.6.1, Plant Design for Protection against Postulated
Piping Failures in Fluid Systems outside Containment, Revision 3
98-ENG-02411-C2, MP2 Evaluation of Flooding Outside Containment, Revision 1
MP-REA-847, Request for Engineering Assistance, DC Switchgear

Section 1R11: Licensed Operator Requalification Program

Procedures

OP 2344A, 480Volt Load Centers, Revision 023-03
SP 2613L, Diesel Generator Slow Start Operability Test, Facility 2, Revision 005-04
SP 2651L, Main Stop Valve Operability Test, Revision 004
SP 2651M, Combined Intermediate Valves Operability Test, Revision 004
SP 2651N, Main Control Valve Operability Test, Revision 005

Miscellaneous

AOP 3571, Instrument Failure Response, Revision 09-007
AOP 3559, Loss of Vacuum, Revision 09-04
AOP Rapid Downpower, Revision 17-06
EOP35-E0, Reactor trip or Safety Injection, Revision 26-01
EOP35-E2, Faulted SG Isolation, Revision 11-00 EOP35-ECA2.1, Uncontrolled Depressurization of all SGs, Revision 15-02
OP 2301C, Reactor Coolant Pump Operation, Revision 019-06
AOP 2568, Reactor Coolant System Leak, Revision 007-06
AOP 2575, Rapid Downpower, Revision 004-04
EOP 2525, Standard Post Trip Actions, Revision 024
EOP 2532, Loss of Coolant Accident, Revision 029-01
AOP 3570, Earthquake, Revision 013-01

Section 1R12: Maintenance Effectiveness

Condition Reports

505154
503431
496278
492544
497644
499792
499802

Miscellaneous

ACE19239, MP2 'B' EDG Output Breaker Trip While Performing a Fast Start Surveillance Test Containment Isolation System Health Report 4th Quarter 2011 and 2012 EDG and Fuel Oil System Health Report 4th Quarter 2011 and 2012 EDG Unavailability January 2011 to December 2012
ER-AA-MRL-100, Implementing Maintenance Rule, Revision 5
DM3-00-146-09, Revised Throttle Position of HVK heat Exchanger Throttle Valve 3SWP*V13, dated 10/7/2009
Attachment ACE019111, 'B' Chiller Did Not Start during Control Building Chiller Swap, dated April 19, 2012 MRule Monthly Review Report for December 2012
Maintenance Rule Program Health Report Q4-2012 MRE013459
MRE015918
MRE015917 MRE015432
MRE015131
MRE015097
MRE015074
MRE015073
MRE014984
MRE014980
MRE014729
MRE013479
MRE013482
MRE013496
MRE013499
MRE013650
MRE013651
MRE013652 MRE013885
MRE013935
MRE014166 MRE014299
MRE014706
MRE014811
MRE015025
MRE015192
MRE015194
MRE015257
MRE015319
MRE015447
MRE015457
MRE013639
MRE015641 MRE015674
MRE015737
MRE015748 8002055-FA, Failure Analysis for
EGB-13P Governor/Actuator, Revision 1
ACE 018846
ODM000280, Revision 0
ODM000222, Revision 1 MRE015966 ACE019355
Maintenance Rule functions for reactor pressurizer Pressurizer System Health Report 4th Quarter 2011 and 2012 Pressurizer Unavailability January 2011 to December 2012
Maintenance Rule (a)(3) Periodic Self Assessment dated February 23, 2013

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

PT 21412J, MP2 RSST OLTC Meter INCON Model 1250B Setup Procedure, Revision 000-00
WM-AA-100, Work Management Process, Revision 20
NF-AA-PRA-370, Probabilistic Risk Assessment Procedures and Methods: PRA Guidelines for
MRule (a)(4) for the Dominion Sites, Revision 15
DNES-AA-NAF-MRL-1001, Maintenance Rule (a)(4) Basis Document, Revision 2
WM-AA-20, Risk Assessment of Maintenance Activities, Revision 1
NF-AA-PRA-101-3050, Probabilistic Risk Assessment Procedures and Methods: Maintenance
Rule (a)(4) PRA Support Guidelines, Revision 3 Scheduler's Evaluation for Millstone 3 On-line Schedule dated February 6, 2013
EOOS on line Risk Monitor Printout from February 6, 2013

Condition Reports

501911
504625
504739
508844

Miscellaneous

High Risk Contingency Plan and Troubleshooting Plan for the Replacement of the
AC-4 Relay

Section 1R15: Operability Evaluations

Procedures

OP3314D, ESF Building Ventilation and Air Conditioning, Revision 12-04
OP-AA-102, Operability Determination, Revision 9
SP 2410A, Acoustic Valve Monitoring System Channel Check, Revision 009-9
Attachment Condition Reports
500743
500745
500747
503305
501793
501879
506519
506524
502542
502839
328821
409893
428785

Miscellaneous

IOD000181, SW Leak on the Supply Piping to Switchgear Room Coolers, X181A/B and X182
RAS 000220, HVK SW Valve Throttled Requiring Analysis to Restore Functionality
ETE-CCE-2013-1001, No Title, dated January 17, 2013 Drawing 25212-26933 Service Water Revision 75
OD000529, SW Valves 3SWP*V661, 664, 665 and 668 Dealloying, Revision 1
OD000524, Evaluate 3MSS*PTs given Condition of Associated Insulation Boxes/Straps
OD000525, OD to Support Comp. Actions Taken to reinforce 3MSS*PT Insulation Boxes
IOD 0000173, An Evaluation of Degraded and Non-Conforming Conditions as Identified in ACR01750
EQR 134-4, Millstone Equipment Qualification Record Rosemount Steam Pressure Transmitters, Revision 7 Calc US(B)-330, Thermal Analysis of Pressure Transducers Exposed to HELB Environment (MSVB), Revision 6 ACE019377, AVMS Ch
RC-201 determined to have not met TS Acceptance Criteria in December 2012 ACE017059, 3SWP*V696 has a through-wall weep (LTCA) March 30, 2009
IOD 0000173, An Evaluation of Degraded and Non-Conforming Conditions as Identified in ACR01750 on March 26, 2011 IOD000184, SW Valves 3SWP*V870 and V873 have through wall weepage on January 30, 2013 MRE016100, SW Valves 3SWP*V870 and V873 have through wall weepage on February 5, 2013
Condition Reports:
505671
505983
505990
500743
500745
500747
504101

Section 1R18: Plant Modifications

Miscellaneous

OD 000529, Unit 3 'B' Train SW valves are Dealloying, Revision 1
ARP 3353.MGB, Main Generator Breaker Panel Annunciator Response, Revision 000-06
NUC
WC 12, 345kV Transmission Facilities Testing and Maintenance, Revision 005
212-39659 SH. 5, Pressure Scale and Pneumatic Regulation of Three Pole Circuit Breaker Type PKG with Own Compressor Plant [3GML-BKR], Revision D
OP 3324F, Main Generator Breaker, Revision 008-05
TCC-MP-2013-011, Temporary Installation of Main Generator Output Breaker 15G-3U-2 Air Supply
SO-13-005, Standing Order, dated February 15, 2013
AWO 53102611778, Install Temp Mod
TCC-MP-2013-011

Condition Reports

505581
508886
Attachment

Section 1R19: Post-Maintenance Testing

Procedures

SP 2401D, RPS Matrix Logic and Trip Path Relay Test, Revision 014-01
SP 2613A-001, Periodic DG Operability Test, Facility 1 (Fast Start, Loaded Run), Revision 021
SP 2613K, Periodic DG Slow start Operability Test, Facility 1, Loaded Run), Revision 004-01
SP 2613O-001, 'A' EDG Hot Restart, Revision 000-06
ER-AA-102, Preventive Maintenance Program, Revision 7
ARP 3353.MGB, Main Generator Breaker Panel Annunciator Response, Revision 000-06 NUC
WC 12, 345kV Transmission Facilities Testing and Maintenance, Revision 005
OP 3324F, Main Generator Breaker, Revision 008-05

Condition Reports

406423
414547
502912
505434
505435
505522
505524
505543
505629
505710
505723
505763
505799
505881
505884
505886
505992
506010
506031
506064
506078
506198
506282
506297
506317
506341
506368
506468
505581
508886
Maintenance Orders/Work Orders 53102413594
53102415854
53102506964
53102509879
53102548840
53102579404
53102589664
53M20204645 53M20215188
53M20507486
53M20807844
53M30416532 53102380085
53102393497
53102587417

Miscellaneous

MP3-12-01087, MCC Starter Replacement Project - Twenty Three QA Starters (Group 7), Revision 1 25212-39659 SH. 5, Pressure Scale and Pneumatic Regulation of Three Pole Circuit Breaker Type PKG with Own Compressor Plant [3GML-BKR], Revision D
TCC-MP-2013-011, Temporary Installation of Main Generator Output Breaker 15G-3U-2 Air Supply
SO-13-005, Standing Order, dated February 15, 2013

Section 1R22: Surveillance Testing

Procedures

OP 2330A22, 'C' RBCCW Pump Maintenance, Revision 000-08
SP 2612A-003, 'A' SW Pump and Facility 1 Discharge Check Valve IST, Revision 004-00 SP3626.7, SW Pump 3SWP*P1D Operational Readiness Test, Revision 016-05
SP3626.7-011, SW Pump 3SWP*P1D Comprehensive Test, Revision 000-02
SP 3622.3, Auxiliary Feedwater Pump 3FWA*P2 Operational Readiness Test, Revision 017-12
SP 3622.3-001, TDAFW Pump Operational Readiness and Quarterly IST Group 'B' Pump Tests, Revision 014-05
SP 3646A.9-021, Auxiliary Feedwater Pump Start S941 - Relay K641, Slave Actuation, Revision 002-02 SP3604A.2, Charging Pump 'B' Operational Readiness Test, Revision 014-02
SP3604A.2-001, 3CHS*P3B Quarterly IST Pump Test (Two Charging Pumps Aligned for Service), Revision 16
Attachment SP3604A.5-014, Quarterly CVCS Stroke Testing - 'B' Train, Revision 000-03 SP3630D.2-001, 3CCE*P1B Quarterly IST Pump Test, Revision 009-02
SP3630D.3-004, 3CCE*TV37B Failure Test, Revision 000-04
SP3630D.3-005, Train 'B' CCE Valve Stroke Time Test, Revision 000-01
SP 31005A, Moderator Temperature Coefficient and Power Coefficient Measurements, Power Exchange Method, Revision 003-01
CP 3807F Operation of the Reactor Plant Sample Sink, Revision 006-03
SP 3680.1, General Trending Procedure,
SP 3680.1-003, Containment Leakage Trending, Revision 002-01 RCS Leakage Report, Millstone Unit 3 for March 26, 2013

Condition Reports

501911
502838
502071
505964
505973
506375
506379
506499
506503
505581
508886
509244

Miscellaneous

ETE-MP-2013-1009, Motor vendor discovered several discrepancies during the performance testing of a motor overhaul on Unit 3 'D' SW Pump, Revision 0
ETE-MP-2012-1234, Flow Loop Uncertainties in Support of the MP2 SW System IST, Revision 1 PA90-070-1240EE, Calculate Orifice Plate Bore, Beta Ratio and Flowrate versus Differential Pressure for Millstone Unit 2 SW System, Revision 0 92-120, MP2 SWS Design Basis Alignments - Summer & Winter, Revision 5
98-ENG-02697M2, MP2 SW Pumps Acceptance Curves, Revision 1
Estimating Temperature Reactivity Coefficients by Experimental Procedures Combined with Isothermal Temperature Coefficient Measurements and Dynamic Identification, Tsuji (etal), Journal of Nuclear Science and Technology, Vol 43, No. 5, Pages 576-586 (2006) AWO 53102457292

Section 1EP4: Emergency Action Level and Emergency Plan Changes

Emergency Plan, Revision 45

Section 1EP6: Drill Evaluation

Procedures

OP 2301C, Reactor Coolant Pump Operation, Revision 019-06
AOP 2568, Reactor Coolant System Leak, Revision 007-06
AOP 2575, Rapid Downpower, Revision 004-04
EOP 2525, Standard Post Trip Actions, Revision 024
EOP 2532, Loss of Coolant Accident, Revision 029-01

Section 4OA1: Performance Indicator Verification

Procedures

CP 2802N, Primary Systems Sampling and Analysis, Revision 001-04
SP 2832-001, Reactor Coolant Analysis for
DEI-131, Revision 007-00
NF-AA-NSA-101-5009, Reactor Coolant System Leak Monitoring, Revision 1
NF-AA-FPA-3001, Reactor Coolant System Radiochemistry Analysis, Revision 2
NF-AA-FPA-3002, Monthly Fuel Reliability Indicator, Revision 1
SP 3601F.6, Reactor Coolant System Water Inventory Measurement, Revision 006-06
CP 3802E-001, Reactor Coolant Gas Sample Calculations, Revision 000-01
Attachment
CP-3807F, Operation of the Reactor Plant Sample Sink, revision 006-03 Unit 3 Dose Equivalent Xe 1333 Report for March 27, 2013
Unit 3 RCS Degas Gamma Spectrum Analysis for March 27, 2013 Unit 3 RCS Gas Gamma Spectrum Analysis for March 27, 2013

Miscellaneous

Barrier Integrity PI data, reported from January 1, 2012 to December 31, 2012
NRC Information Notice 94-46, Nonconservative Reactor Coolant System Leakage Calculation
NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6

Section 4OA2: Problem Identification and Resolution

Procedures

MP-20-WP-GDL40, Pre and Post Maintenance Testing, Revision 013-03

Condition Reports

497453
506539
Maintenance/Work Orders 53102395511
53102577809
Attachment

LIST OF ACRONYMS

ADAMS Agencywide Documents Access and Management System
AFW auxiliary feedwater system
AV [[]]

MS acoustic valve monitor system

CAP Corrective Action Program

CFR Code of Federal Regulations
CR condition reports

DG diesel generator DRP Division of Reactor Projects

DRS Division of Reactor Safety

EDG emergency diesel generator
EP emergency preparedness

IMC Inspection Manual Chapter IST in-service test

LER licensee event report

NCV non-cited violation
NEI Nuclear Energy Institute
NRC Nuclear Regulatory Commission
NS [[]]

IR Office of Nuclear Security and Incident Response

OOS out of service
PA [[]]

RS Publicly Available Records

PI performance indicator
PMT post maintenance testing
PORV power operated relief valve
RBC [[]]

CW reactor building closed cooling water

RCS reactor coolant system

SBO station blackout
SDP Significance Determination Process

SG steam generator SSC structure, system, or component

SW service water

TS technical specifications
UFS [[]]
AR Updated Final Safety Analysis Report