GO2-82-689, Interim Deficiency Rept Re Johnson Controls Design Issue. Initially Reported on 820720.Analysis of Large Bore Piping & Small Bore Design Underway.Next Rept Expected by 821123

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Interim Deficiency Rept Re Johnson Controls Design Issue. Initially Reported on 820720.Analysis of Large Bore Piping & Small Bore Design Underway.Next Rept Expected by 821123
ML20063E030
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 08/18/1982
From: Matlock R
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To: Engelken R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
10CFR-050.55E, 10CFR-50.55E, G2-82-689, GO2-82-689, NUDOCS 8208300112
Download: ML20063E030 (2)


Text

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Washington Public Power Supply System _

P.O. Box 968 3000GeorgeWashingtonWay Richland, Washington 99352b(509)372-5000 40 r. .

Docket No. 50-397 OS

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August 18, 1982 G02-82-689 Mr. R. H. Engelken U.S. Nuclear Regulatory Commission Revion V 1450 Maria Lane, Suite 210 Walnut Creek, California 94596

Subject:

NUCLEAR PROJECT NO. 2 10CFR50.55(e) REPORTABLE CONDITION #201 JOHNSON CONTROLS DESIGN ISSUE

Reference:

Telecon R.T. Johnson (WPPSS) to Tony D'Angelo (USNRC Region V) Same Subject, dated July 20, 1982 In accordance with the provisions of 10CFR50.55(e), your office was notified by telephone of the above subject reportable condition on July 20, 1982.

Attachment A provides the Project's interim report.

We will continue to provide your office with quarterly updates on this subject until all deficiencies are resolved. The next report will be submitted on or before November 23, 1982.

If you have any questions regarding this matter, please contact Roger T. Johnson at (509) 377-2501, extension 2712.

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Program Director, WNP-2 RGM/RTJ/jdb cc: WS Chin, BPC RA Feil, NRC Resident Inspector, WNP-2 A Forrect, Burns and Roe HAPO ND Lewis, NRC J Plunkett, NUS Corporation RE Snaith, Burns and Roe NY V Stello, NRC WNP-2 Files 8208300112 820818 PDR ADOCK 05000397

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e- O WASHINGTON PUBLIC POWER SUPPLY SYSTEM NUCLEAR PROJECT NO. 2 Docket No. 50-397 License No. CPPR-93 Johnson Controls Design Issue INTERIM REPORT Description of Potential Defect or Noncompliance Burns and Roe (BRI), the Architect-Engineer, conducted a Technical Audit of Johnson Controls Incorporated (JCI) to confirm piping instrumentation design adequacy. The JCI organization performs small bore (l" and under) piping design work and installation on the WNP-2 project. JCI requires interface design information from BRI to perform their design work. The audit determined that the large bore piping thermal movement data being utilized by JCI could not be traced by BRI documentation. The information that was being utilized was also found to be discrepant. A reevaluation of the design utilizing the most current thermal movement information provided by BRI resulted in identification of six small bore pipe lines which were overstress by ASME code criteria.

Analysis of Safety Implication Based on the most conservative assumption that the overstressed condition would have led to simultaneous multiple small bore piping failures, there would have been a loss of various instrumentation. The most significant instrumentation loss would have been the automatic main steam line isola-tion and feedwater control on steam line "D". Other control functions would also be affected having varying safety and operational implications.

Therefore, the condition is considered to be reportable.

Corrective Actions Taken BRI has issued current thermal displacement data to JCI and is updating that information to be current with the latest large bore piping analysis.

JCI is now reevaluating their small bore design based on the most current information. JCI has issued corrective action on the six lines which were

! overstressed.

Line 37F - Rerouted Piping 39e - Replaced hanger with snubber type support 42a - Revised support from two-way to three-way i 69a - Revised support from two-way to three-way l 70e - Revised support from two-way to three-way 75e - Rerouted Piping Field revisions are expected to be completed prior to the end of August 1982.

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