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Category:GENERAL EXTERNAL TECHNICAL REPORTS
MONTHYEARML20199L5891997-12-24024 December 1997 Independent Analysis & Evaluation of AM-241 & Transuranics & Subsequent Dose to Two Male Workers at Connecticut Yankee Atomic Power Plant ML20210P8721997-08-31031 August 1997 Post Decommissioning Activities Rept, for Aug 1997 ML20141A0041997-05-31031 May 1997 Independent Assessment of Radiological Controls Program at Cyap Haddam Neck Plant Final Rept May 1997 ML20137H3031997-03-31031 March 1997 Rev 2 to Nuclear Training Loit/Lout Audit Reviews ML20137C6281997-03-14014 March 1997 Redacted Version of Rev 1 to Nuclear Training Loit/Lout Audit Reviews ML20135E3221997-02-13013 February 1997 Independent Review Team Rept 1996 MP -1 Lout NRC Exam Failures ML20134L2751997-02-0303 February 1997 Draft Rev to GPRI-30, Spent Fuel Storage Facility Licensing Basis/Design Basis ML20134L2911997-01-0808 January 1997 Rev 0 to UFSAR Rev Grpi ML20204B6811996-12-31031 December 1996 Nuclear Lemons Assessment of America Worst Commerical Nuclear Power Plants. 5th Edition ML20237E0751996-12-31031 December 1996 Decommissioning Cost Study for Connecticut Yankee Nuclear Power Plant ML20134L2591996-12-31031 December 1996 Rev 0 to Sys Reclassification ML20134L2721996-12-31031 December 1996 Commitment Mgt Grpi ML20134L2481996-12-30030 December 1996 Rev 0 to Sys Needed for Decommissioning Sys Evaluation Process ML20135E2711996-12-26026 December 1996 Evaluation of Intakes by Two Workers at CT Yankee Atomic Power Co ML20134L2841996-12-23023 December 1996 Rev 0 to Spent Fuel Pool Island Studies ML20134L2871996-12-19019 December 1996 Rev 0 to Grpi for Defueled Condition Fire Protection Technical Requirements ML20134L2381996-12-19019 December 1996 Rev 0 to Accident Analysis ML20058G3481993-10-31031 October 1993 Nonproprietary VIPRE/WRB-1 DNBR Thermal Limit for Westinghouse Fuel Types, for Oct 1993 ML20058G6771993-09-29029 September 1993 Rev 0 to Project Assignment 91-006, Connecticut Yankee Event V Mods ML20058L7411993-07-15015 July 1993 QA Svcs Dept Surveillance Rept SS-169, Assessment of Fitness for Duty Program ML20045F3351993-06-30030 June 1993 IPE for Severe Accident Vulnerabilities RA-93-022, Cy Containment Isolation Failure Probability1993-05-18018 May 1993 Cy Containment Isolation Failure Probability ML20127J5391992-11-30030 November 1992 Connecticut Yankee Structural Reevaluation of Plant Structures to Address SEP Topic III-7.B Load Combinations Code Changes ML20125E5661992-03-31031 March 1992 Nonproprietary PWR SG Tube Repair Limits:Technical Support Document for Expansion Zone PWSCC in Roll Transitions Final Rept A08995, Rev 1 to Auxiliary Initiation Event Analysis1990-09-14014 September 1990 Rev 1 to Auxiliary Initiation Event Analysis ML20062G4951990-07-31031 July 1990 Rev 3 to Northeast Utils USNRC Read & Sign ML20055G4951990-07-31031 July 1990 Decommissioning Financial Assurance Certification Rept ML20044A8481990-07-0202 July 1990 Vol 1 to Connecticut Yankee Simulator Certification Submittal:Connecticut Yankee Simulator Design Info & Certification Program Overview ML20055D8931990-06-30030 June 1990 Fracture Mechanics Evaluation:Haddam Neck Pressurizer ML20043A4831990-04-30030 April 1990 Rev 1 to Technical Rept Supporting Cycle 16 Operation ML20012A2281990-03-0101 March 1990 Vol 6 to Probabilistic Safety Study B13388, Zircaloy Clad Fuel Mechanical Design Rept1989-11-30030 November 1989 Zircaloy Clad Fuel Mechanical Design Rept ML20246N9421989-08-31031 August 1989 Tornado Missile Risk Analysis of Bleed & Feed & Auxiliary Feedwater Safe Shutdown Sys at Connecticut Yankee Atomic Power Station ML20044G5131989-07-31031 July 1989 Rev 1 to Final Rept J5439-89-001R1, Fluidelastic Instability Analysis of U-Bend Region of Westinghouse Model 27 Sg ML20206J9991988-10-31031 October 1988 Crdr Summary Rept, Per Suppl 1 to NUREG-0737 ML20153G4081988-06-0303 June 1988 Rev 0 to Conneticut Yankee Replace Nuclear Instrumentation Sys, Neo Project Description ML20153G4031988-03-0808 March 1988 Rev 0 to, Connecticut Yankee Modernize Reactor Protection Sys - Phase 2, Conceptual Project Description ML20235B5911987-09-24024 September 1987 Undated Technical Evaluation:Haddam Neck Plant Reanalysis of Non-LOCA DBAs & Tech Spec Change Requests in Support of Reload Cycle 15 B12619, Bimonthly Progress Rept 5:New Switchgear Bldg Const1987-07-31031 July 1987 Bimonthly Progress Rept 5:New Switchgear Bldg Const ML20214R6371987-06-30030 June 1987 Technical Rept Supporting Cycle 15 Operation ML20205Q7011987-04-30030 April 1987 Bimonthly Progress Rept 3:New Switchgear Bldg Const B12480, Const Design Info Submittal:New Switchgear Bldg Const. W/38 Oversize Encl1987-04-30030 April 1987 Const Design Info Submittal:New Switchgear Bldg Const. W/38 Oversize Encl ML20238C3751986-12-31031 December 1986 Connecticut Yankee 1986 Core XIII - Xiv Refueling Outage ALARA Rept ML20238C3821986-12-31031 December 1986 Connecticut Yankee 1986 Steam Generator Repair Outage ALARA Rept ML20209C7161986-12-31031 December 1986 Vols 1 & 2 to Isap,Haddam Neck Plant,Final Rept ML20206J8871986-06-30030 June 1986 Isap Public Safety Impact Model Project Analyses Summaries ML20202D5071986-06-30030 June 1986 Non-LOCA Transient Analysis ML20205T1201986-05-19019 May 1986 Steam Generator Tube Insp Rept for 1986 Refueling Outage ML20205T1231986-05-0808 May 1986 Steam Generator Tube W/55% Through Wall Defect Safety Evaluation for Structural Integrity CY-86-031, Rev 1 to 4.10.1(D) Inservice Insp of Steam Generator Tubes (Acceptance Criteria)1986-05-0808 May 1986 Rev 1 to 4.10.1(D) Inservice Insp of Steam Generator Tubes (Acceptance Criteria) 1997-08-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K3301999-10-19019 October 1999 Safety Evaluation Supporting Amend 195 to License DPR-61 ML20206C8761999-04-28028 April 1999 Safety Evaluation Supporting Amend 194 to License DPR-61 CY-99-047, Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use1999-03-23023 March 1999 Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use 05000213/LER-1999-001, :on 990105,main Stack RM R-14A Pressure Compensating Signal Was Not Calibrated.Caused by Personnel Error.Revised Calibration Procedure.With1999-02-0101 February 1999
- on 990105,main Stack RM R-14A Pressure Compensating Signal Was Not Calibrated.Caused by Personnel Error.Revised Calibration Procedure.With
05000213/LER-1997-016, :on 970825,discovered That Negative Pressure Was Not Maintained in Sf Bldg,Per Design Basis.Caused by Sf Bldg Ventilation Sys Being Based on Lower Pab Ventilation Flow Rates.Corrected Ventilation Sys Design.With1999-01-25025 January 1999
- on 970825,discovered That Negative Pressure Was Not Maintained in Sf Bldg,Per Design Basis.Caused by Sf Bldg Ventilation Sys Being Based on Lower Pab Ventilation Flow Rates.Corrected Ventilation Sys Design.With
ML20206F1971998-12-31031 December 1998 Annual Rept for 1998 for Cyap. with CY-99-027, Annual Rept for 10CFR50.59, for Jan-Dec 1998.With1998-12-31031 December 1998 Annual Rept for 10CFR50.59, for Jan-Dec 1998.With ML20198G9101998-12-22022 December 1998 Proposed Rev 2 of Cyap QAP for Haddam Neck Plant. Marked Up Rev 1 Included 05000213/LER-1997-018, :on 971003,discovered That Sf Bldg Exhaust Fan Did Not Meet Design Basis.Caused by Higher than Expected Pressure in Pab.Design of Sf Bldg Ventilation Sys Was Corrected.With1998-12-0808 December 1998
- on 971003,discovered That Sf Bldg Exhaust Fan Did Not Meet Design Basis.Caused by Higher than Expected Pressure in Pab.Design of Sf Bldg Ventilation Sys Was Corrected.With
05000213/LER-1998-009, :on 980915,noted Excessive CV,SW-CV-963,seat Leakage in SW Supply Piping to SFP Heat Exchangers.Caused by Subject Cv Disc Being Stuck in Open Position.Valve Was Exercised & Freed from Stuck Open Position.With1998-10-14014 October 1998
- on 980915,noted Excessive CV,SW-CV-963,seat Leakage in SW Supply Piping to SFP Heat Exchangers.Caused by Subject Cv Disc Being Stuck in Open Position.Valve Was Exercised & Freed from Stuck Open Position.With
05000213/LER-1998-008, :on 980721,determined That Main Stack Radiation Monitor RMS-14B Samples Were Not Analyzed to Required Detection Level.Caused by Inadequate Design.Immediately Controlled Temp of Radiation Monitor Room.With1998-09-29029 September 1998
- on 980721,determined That Main Stack Radiation Monitor RMS-14B Samples Were Not Analyzed to Required Detection Level.Caused by Inadequate Design.Immediately Controlled Temp of Radiation Monitor Room.With
05000213/LER-1997-021, :on 971124,found Contaminated Matls Offsite. Caused by Breakdown of Health Physics Program in Effect at Time Contaminated Matl Was Released from Site.Revised Procedures.With1998-09-0101 September 1998
- on 971124,found Contaminated Matls Offsite. Caused by Breakdown of Health Physics Program in Effect at Time Contaminated Matl Was Released from Site.Revised Procedures.With
ML20238F2131998-08-28028 August 1998 SER Accepting Defueled Emergency Plan for Emergency Planning for Connecticut Yankee Atomic Power Co 05000213/LER-1998-007, :on 980714,excessive Check Valve Seat Leakage in SW Supply Piping to SFP Heat Exchangers,Occurred.Caused by SW-CV-963 Disc Sticking in Open Position.Increased Test Frequency from Quarterly to Monthly1998-08-13013 August 1998
- on 980714,excessive Check Valve Seat Leakage in SW Supply Piping to SFP Heat Exchangers,Occurred.Caused by SW-CV-963 Disc Sticking in Open Position.Increased Test Frequency from Quarterly to Monthly
CY-98-136, Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line1998-08-12012 August 1998 Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line ML20237B7461998-07-22022 July 1998 1998 Defueled Emergency Plan Exercise Scenario Manual, Conducted on 980722 ML20202D1621998-06-30030 June 1998 Safety Evaluation Supporting Amend 193 to License DPR-61 05000213/LER-1998-005, :on 980511,determined That Design Deficiency Was Found in Main Stack Flow Rate Monitor.Caused by 1974 Mod Change on Original Installation.Declared F-1101 Channel Out of Svc & Develop Means of Estimating Flow1998-06-0909 June 1998
- on 980511,determined That Design Deficiency Was Found in Main Stack Flow Rate Monitor.Caused by 1974 Mod Change on Original Installation.Declared F-1101 Channel Out of Svc & Develop Means of Estimating Flow
05000213/LER-1998-006, :on 980507,design Deficiency Was Found in Stack RM RMS-14B Sampling Lines.Caused by Design Not Meeting ANSI N13.1-1969 Stds.Corrective Action Plan for RMS-14B Is Being Developed1998-06-0808 June 1998
- on 980507,design Deficiency Was Found in Stack RM RMS-14B Sampling Lines.Caused by Design Not Meeting ANSI N13.1-1969 Stds.Corrective Action Plan for RMS-14B Is Being Developed
05000213/LER-1998-004, :on 980507,discovered Design Deficiency in Stack Radiation Monitor RMS-14B Isokinetic Sampling.Caused by Failure to Account for Spent Fuel Bldg Ventilation Flow. Will Develop CAP for RMS-14B1998-06-0404 June 1998
- on 980507,discovered Design Deficiency in Stack Radiation Monitor RMS-14B Isokinetic Sampling.Caused by Failure to Account for Spent Fuel Bldg Ventilation Flow. Will Develop CAP for RMS-14B
05000213/LER-1998-003, :on 980505,compensatory Sampling Frequency Exceeded Time Limit W/Sw Effluent RM Inoperable.Caused by Personnel Error.Individual Was Counseled & Technicians Were Reminded of Sampling within Required Frequency1998-06-0202 June 1998
- on 980505,compensatory Sampling Frequency Exceeded Time Limit W/Sw Effluent RM Inoperable.Caused by Personnel Error.Individual Was Counseled & Technicians Were Reminded of Sampling within Required Frequency
05000213/LER-1998-002, :on 980421,determined That Visual Insp of Switchgear Cable Shaft Sprinkler Sys Was Not Being Performed Once Per 18 Months.Caused by Inadequate Implementation of License Amend.Fire Watch Patrol Established1998-05-19019 May 1998
- on 980421,determined That Visual Insp of Switchgear Cable Shaft Sprinkler Sys Was Not Being Performed Once Per 18 Months.Caused by Inadequate Implementation of License Amend.Fire Watch Patrol Established
05000213/LER-1998-001, :on 980409,seismic Monitor Sp Was Not in Compliance W/Ts.Caused by Inadequate Engineering Review. Submitted Proposed License Amend to Correct Issue1998-05-0707 May 1998
- on 980409,seismic Monitor Sp Was Not in Compliance W/Ts.Caused by Inadequate Engineering Review. Submitted Proposed License Amend to Correct Issue
CY-98-068, Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms1998-04-15015 April 1998 Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms CY-98-045, Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing1998-04-13013 April 1998 Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing ML20217A0001998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Haddam Neck Plant ML20217F0611998-03-31031 March 1998 Historical Review Team Rept ML20217K2101998-03-27027 March 1998 Safety Evaluation Supporting Amend 192 to License DPR-61 CY-98-046, Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal1998-03-12012 March 1998 Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal ML20216D6531998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Haddam Neck Plant ML20217D7381998-02-28028 February 1998 Revised MOR for Feb 1998 Haddam Neck Plant CY-98-012, Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant CY-98-010, Annual Rept for 10CFR50.59,Jan-Dec,19971997-12-31031 December 1997 Annual Rept for 10CFR50.59,Jan-Dec,1997 ML20198N6681997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Haddam Neck Plant ML20217P4861997-12-31031 December 1997 1997 Annual Financial Rept, for Cyap ML20199L5891997-12-24024 December 1997 Independent Analysis & Evaluation of AM-241 & Transuranics & Subsequent Dose to Two Male Workers at Connecticut Yankee Atomic Power Plant 05000213/LER-1997-020, :on 971117,determined That Radioactive Effluent Dose Calculations Were Not Performed within Required Frequency.Caused by Procedure Inadequacy.Will Revise Procedures & Will Enhance Tracking Process1997-12-16016 December 1997
- on 971117,determined That Radioactive Effluent Dose Calculations Were Not Performed within Required Frequency.Caused by Procedure Inadequacy.Will Revise Procedures & Will Enhance Tracking Process
ML20203K4271997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Haddam Neck Plant 05000213/LER-1997-017, :on 970924,identified Three Locations of Detectable Plant Related Radioactivity in on-site Landfill Area.Caused by Failure to Conduct Adequate Survey.Access to Area Controlled1997-11-18018 November 1997
- on 970924,identified Three Locations of Detectable Plant Related Radioactivity in on-site Landfill Area.Caused by Failure to Conduct Adequate Survey.Access to Area Controlled
05000213/LER-1997-019, :on 970808,compensatory Sampling Frequency Exceeded W/Rms Determined Inoperable.Caused by Personnel Error Due to Incorrect Interpretation of Ts.Compensatory Sampling to Be Conducted in Time Frame Required1997-11-17017 November 1997
- on 970808,compensatory Sampling Frequency Exceeded W/Rms Determined Inoperable.Caused by Personnel Error Due to Incorrect Interpretation of Ts.Compensatory Sampling to Be Conducted in Time Frame Required
ML20199B1141997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Haddam Neck Plant 05000213/LER-1997-018, :on 971003,Spent Fuel Building Exhaust Fan Flow Was Found Below Design During Testing.Caused by Personnel Error.Evaluated Replacement of Spent Fuel Building Exhaust Fan Capable of Overcoming Higher Pressures1997-10-30030 October 1997
- on 971003,Spent Fuel Building Exhaust Fan Flow Was Found Below Design During Testing.Caused by Personnel Error.Evaluated Replacement of Spent Fuel Building Exhaust Fan Capable of Overcoming Higher Pressures
ML20198M8101997-10-14014 October 1997 SER Accepting Proposed Revs to Util Quality Assurance Program at Facility ML20198J8811997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Haddam Neck Plant 05000213/LER-1997-015, :on 970813,functional Testing of Radiation Monitoring Sys Was Not Performed as Defined in Ts.Caused by Lack of Understanding of Definition of Acot.Revised Appropriate RMS Surveillance Procedure1997-09-12012 September 1997
- on 970813,functional Testing of Radiation Monitoring Sys Was Not Performed as Defined in Ts.Caused by Lack of Understanding of Definition of Acot.Revised Appropriate RMS Surveillance Procedure
05000213/LER-1996-027, :on 961010,boron Injection Flow Path Below Minimum Required Temperature Was Determined.Caused by Inadequate Design of Heat Trace Controls in Rtd.Boric Acid Flow Paths from Bamt Were Declared Inoperable1997-09-12012 September 1997
- on 961010,boron Injection Flow Path Below Minimum Required Temperature Was Determined.Caused by Inadequate Design of Heat Trace Controls in Rtd.Boric Acid Flow Paths from Bamt Were Declared Inoperable
05000213/LER-1996-016, :on 960801,potential for Inadequate RHR Pump NPSH During Sump Recirculation Was Determined.Caused by Failure to Fully Analyze Containment Pressure & Sump Temperature Response.Redesign of Piping Proposed1997-09-12012 September 1997
- on 960801,potential for Inadequate RHR Pump NPSH During Sump Recirculation Was Determined.Caused by Failure to Fully Analyze Containment Pressure & Sump Temperature Response.Redesign of Piping Proposed
05000213/LER-1997-014, :on 970808,ESFA Occurred Due to Deenergization of High Containment Pressure Actuation Circuits.Reemphasized Expectations of Mgt for Performing non-routine Operational Tasks1997-09-0505 September 1997
- on 970808,ESFA Occurred Due to Deenergization of High Containment Pressure Actuation Circuits.Reemphasized Expectations of Mgt for Performing non-routine Operational Tasks
05000213/LER-1996-021, :on 960828,valve Leakage Resulted in Nitrogen Intrusion Into RCS During Cold Shutdown.Caused by Leaking Valve BA-V-355.Training Has Been Been Provided to Operators on Event & Features & Limitations of Sys1997-09-0505 September 1997
- on 960828,valve Leakage Resulted in Nitrogen Intrusion Into RCS During Cold Shutdown.Caused by Leaking Valve BA-V-355.Training Has Been Been Provided to Operators on Event & Features & Limitations of Sys
05000213/LER-1996-005, :on 960301,spent Fuel Cooling Was Shut Down Due to Discovery of Loose Parts.Caused by Inadequate Design. Piping from Both Sent Fuel Pool Cooling Pumps to Plate Exchanger Were Inspected for Loose Parts w/bore-a-scope1997-09-0505 September 1997
- on 960301,spent Fuel Cooling Was Shut Down Due to Discovery of Loose Parts.Caused by Inadequate Design. Piping from Both Sent Fuel Pool Cooling Pumps to Plate Exchanger Were Inspected for Loose Parts w/bore-a-scope
1999-04-28
[Table view] |
Text
r Appendix B INTEGRATED SAFETY EVAL!!ATION NO.:
ISE/CY-85-062 (REV. 2)
PLANT: CONNECTICUT YANKEE PDCR NO.:
798 REV. 1 TITLE:
STEAM GENERATOR TUBE SLEEVING AND PLUGGING REFERENCES 1.
Connecticut Yankee Steam Generator Sleeving 'and Plugging PDCR #798, Rev. O.
2.
J. A. Blaisdell, Integrated Safety Evaluation No. ISE/CY-85-062 (Rev.
- 1) 11/21/85 " Steam Generator Tube Sleeving and Plugging".
3.
Connecticut Yankee Steam Generator Sleeving and Plugging PDCR #798, Rev. 1.
4 M. L. Van Haltern, L. W. Ward, "Small Break LOCA evaluation of Steam Generator Tube Plugging", Safety Evaluation SE/HN-85-085.
5.
M. R. Galler, J. F. Ely " Component Engineering Safety Evaluation",
Dated Januars 13, 1986 6.
L. J. Laskowski, J. 4. Klisiewicz, " Nuclear Materials and Chemistry Safety Evaluation", Dated October 18, 1985 7.
Calc. File C2-517-585-RE, " Connecticut Yankee Plant Parameters vs.
Steam Generator Tube Plugging", Rev. O, Dated April 8,1985 8.
Calc. File C2-517-550-RE " Connecticut Yankee Minimum R. C. Flow Rate with 2000 Steam Generator Tubes Plugged," Rev.1, April 18,1985 9.
" Core Bypass Flow Summary report for Haddam Neck Plant" D. R. Forsyth, September,1985, Westinghouse Electric Corporation.
- 10. Memo, " Impact of tube plugging on Neutronic Safety Parameters", W. M.
Herwig to A. Gharakhani, NE-85-R-545, Nov.18,1985 l
- 11. W. M. Herwig, M. P. Hills, " Connecticut Yankee Cycle 14 Reload PDCR No.85-795" SE/CY-85-096, Dated December 31, 1985 DESCRIPTION OF CHANGE In the repair of the steam generator tubes, tube sleeves are installed where possible, in lieu of plugs, because they minimize the reduction in primary coolant flow rate.
In regions where it is not practical, steam generator tubes are repaired by plugging the tube at the location of the tubesheet.
Reference 1, Revision 0 of the PDCR, proposed to install sleeves or plugs
,-in steam generator tubes which exhibit defects in excess of technical
. specification limits.
Inconel 690 sleeves 33 inches long, were to be installed in accessible tubes to span defects within six inches of the top
.cf the tube sheet. Defects above this height, or in tubes not accessible h
-to sleeves, were to be plugged.
- 4 o
- L 2
e p@
9 Prior to this repair, 35fr tubes have been plugged. An Integrated Safety Evaluation was performed (Reference 2) which indicated that the existing i
Accident Analyses (LOCA and Non-LOCA) remain valid if no more than 400 effective tubes were plugged.
Reference 3, Revision 1 of this PDCR, increased the number of effective tubes that can be plugged from 400 total to 500 per steam generator.
This Integrated Safety Evaluation is being performed to evaluate the impact of the additional plugged tubes.
DISCUSSION The effect of tube plugging / sleeving was assessed by evaluating the thermal performance of the reactor during hypothetical incidents to ensure that it is not degraded.
Therefore, an evaluation of each transient was performed to determine if it should be reanalyzed.
The consequences of steam generator tube plegging/ sleeving are as follows:
0 Reactor coolant flow is reduced due to increased flow resistance through the steam generator (SG).
O The SG heat transfer area is reduceu.
Thus, to maintain the 100%
steam flow, Tavg must be increased or steam pressure reduced.
O Primary rea: tor coolant mass inventory is reduced.
For the purpose of this evaluation, the following assumptions are appropriate:
- a. The plant will maintain 100% thermal power and design steam flow by lowering the SG pressure by about 34 psi, as indicated by the results of the calculations outlined in Reference 1.
- b. A reduction of 34 psi in SG pressure corresponds to a T reduction and a T increase of approximately 0.5 F (REi1Yence 7).
hot
- c. The Sh secondary inventory (indicated level) is maintained as a function of power level and is not anticipated to change significantly as a result of tube plugging. Also, the density variations are considered to be insignificant.
- d. The reduction in RCS flow rate as a result of 500 effective tubes plugged per SG has been calculated based on the original measured flow rate of 278,000 GPM and the change in the SG resistance due to
~
tube plugging (Reference 8). This results in a new estimated flow of 271,300 GPM.
1
r
- e. There will be no significant change in the key neutronic parameters used in the safety analysis as a result of the tube plugging / sleeving (i.e. moderator and fuel temperature coef ficients, scram worth, ejected rod worth, axial shapes and radial peaking factors.)
(Reference 10)
INTEGRATED SAFETY EVALUATION EFFECT ON DESIGN BASIS ACCIDENTS
. In order to facilitate this evaluation, CY design analyses were grouped into five categories as outlined below:
A - Departure from Nucleate Boiling (DNB) event B - Overcooling events C - Overheating events D - Various reactivity events E - Loss of coolant events A - DNB DESIGN BASIS EVENTS Standard Review Plan (SRP) Section 4.2 specifies the acceptance criteria for various fuel design limits.
One of these states that there will be at least a 95%/95% probability / confidence level that DNB will not occur on the limiting fuel rods during norr 31 operation, operational transients, or any transient conditions arising f rom Condition 1 and 2 events.
In order to meet these bases for CY, the minimum transient DNB ratios were calculated for various transients in the original and/or subsequently revised reference analyses.
Table 1 sunmarizes the current CY design parameters.
The important parameters for analyzing DNB along with their limiting d.irections are also summarized in Table 2.
Tube plugging could affect the DNB design basis events as a result of:
1 - Reduced initial core flow 2 - More rapid primary flow coastdown for the loss of flow event due to increased flow resistance through the steam generator.
'In order to accommodate the first effect, a stu'dy has been performed by Westinghouse to determine the core bypass flow fraction.
The Westinghouse study (Reference 9), confirmed that the bypass flow fraction can be reduced
from 9% to 4.5%.
Therefore, CY Tech. Spec. 3.20 is being revised to reflect this change.
The propgsed Tech. Spec. is as follows:
Original Design Proposed Vessel flow rate, GPM 268,000 257,000 Bypass flow 9%
4.5%
Note:
257,000 GPM was derived at by placing 5% uncertainty on the calculated flow rate of 271,300 GPM.
With a vessel flow rate of 257,000 GPM and a 4.5% bypass flow, the net core flow is 245,400 GPM which exceeds the original design value of 244,600 GPM.
Since the net core flow rate, which is the key input in the safety analyses, remains above the design value, it can be concluded that the initial starting point for*the DNB design basis events remains valid.
The slightly nonconservative effect of more rapid primary flow coastdown caused by increased flow resistance for the loss of flow event is more than compensated for by the proposed change in the Hot Full Power (HFP) moderatur coefficient of the plant. The proposed change imposes a more restrictive limit on the HFP moderator coefficient (CY Tech. Spec. 3.16),
as outlined below:
HFP Moderator Coefficient Original Design Proposed Tech. Spec 10.
PCM/F 0.0 PCM/F Based on the above discussion, it has been concluded that plugging 500 effective tubes per SG at CY will not impact the DNB design bases of the plant.
f B - OVERC00 LING DESIGN BASIS t
j Overcooling t/ansients are performed to address the following:
To assure that worst containment pressure and temperature remain below the containment design conditions and also to provide the most adverse containment response to be used for Equipment Qualification.
O To demonstrate that the limits of 10CFR20 are met for Condition 2 events.
To demonstrate that radiological doses do not exceed 10CFR100 limits for Condition 4 events..
l 1
L
The worst overcooling transient is the double ended rupture of the main steam line.
Even though this transient is a Condition 4 event, it has been analyzed using more limiting acceptance criteria of "no return to criticality".
Table 3 summarizes the key safety parameters along with their limiting directions for this class of transient.
Tube plugging / sleeving could affect the c'onsequence of this class of transients as follows:
1.
Reduced heat transfer surface area would lower the rate and extent of the primary cooldown.
2.
Increased SG resistance would lower the RCS flow rate, and therefore degrade the heat transfer between the primary and secondary coolant.
As indicated in Table 3, both of these effects are in the conservative direction.
Therefore, tube plugging / sleeving will reduce the consequences of the overcooling events.
C - OVERHEATING DESIGN BASES The purpose of analyzing the overheating transients are as follows:
To demonstrate that the RCS pressure will not exceed 110% of design pressure during Condition 1 and 2 events.
(This criteria is assured by applying the more stringent requirement that the pressurizer "must not be filled with water.)
To detennine the design bases of the auxiliary feedwater system.
The most limiting transients analyzed in this category are the loss of load and loss of nonnal feedwater events.
Table 4 sumarizes the key safety parameters along with their limiting directions for this class of events.
The effects of tube plugging / sleeving on these events are as follows:
- 1. Reduced RCS flow rate
- 2. Reduced SG heat transfer area
- 3. Decreased RCS mass inventory However, the most important parameter for this class of events is the moderatortemperaturecoefficient(MTC). As indicated in Section A, CY Tech. Spec. 3.16 is being revised to impose a more restrictive limit on the
. hot full power MTC. The reduction in the maximum allowable MTC more than compensates for the effects of SG tube repair.
D - VARIOUS REACTIVITY EVENTS The following transients can be grouped under this category:
0 Rod withdrawal Boron dilution 0
Dropped rod Control rod ejection This class of transients is affected by changes in core kinetics characteristics, control rod worths, and core power distributions.
As indicated previously, SG tube repair will not cause a significant change in any of the key neutronic parameters of the plant.
E - LOSS OF COOLANT ACCIDENT (LOCA)
References 4 and 11 address the impact of plugging / sleeving 500 tubes per steam generator on the small and large break LOCA analysis for Connecticut Yankee.
These evaluations concluded that the current LOCA design basis analyses will not be affected.
MECHANICAL ASPECTS OF TUBE PLUGGING / SLEEVING Repairing steam generator tubes by sleeving, although not formerly done at Connecticut Yankee, has been done at several other PWRs.
As stated in Reference 5, sleeving is a repair process that requires sleeves to be inserted inside the defective tube in a manner to completely span the defective tube region.
Plastic expansion of the sleeve against the tube, at the top and bottom of the sleeve, provides a leak limiting joint which exhibits sufficient mechanical strength to withstand normal operating, test and postulated accident loading conditions.
The tube repair program will be conducted in accordance with the requirements 6f the project design specifications.
These specifications (SP-ME-516, SP-ME-518 and SP-ME-538) require that the sleeve and plug design, materials of construction, and installation method are qualified by testing and analyses to establish that:
1.
The upper and lower mechanical joints have been qualified by design, analysis and design verification testing to ensure:
- leak tightness
- pressure retaining / load carrying capability for nonnal and faulted design loading conditions
, j
- adequate resistance to potential stress-corrosion cracking and general corrosion concerns, and
- the hard rolling of the bottom tube sleeve joint will not degrade the tube-to-tubesheet weld.
2.
The tube design minimizes the increase to primary flow resistance.
3.
The tube sleeves are purchased according to appropriate specifications.
4.
The tube sleeves are inspected and tested prior to installation to ensure that they are manufactured according to specifications and have the required structural integrity.
5.
The installation process is monitored to ensure proper installation.
The purchase specifications further require that the tube sleeves and plugs be inspected and tested prior to installation to ensure that they are manufactured according to specifications and have the required structural integrity.
Proper installation is assured by process control monitors and by inspection.
Since all installed tube sleeves will be subject to the qualification program requirements, purchase specification and installation / inspection procedures repairing defective steam generator tubes by sleeving will not increase the probability of any previously analyzed accident (e.g. steam generator tube rupture.)
NUCLEAR MATERIALS AND CHEMISTRY ASPECTS OF TUBt PLUGGING / SLEEVING l.
As indicated in Reference 6, the sleeve repair leads to an upgrade in corrosion resistance as compared to the original tubing.
No unacceptable accelerated corrosion effects as a result of crevices, or tensile stresses associated with the sleeve have been identified based upon available data.
Thus, the probability of occurrence of a steam generator tube rupture event l
is not increased by the sleeving repair process.
Because of the above assessments, this PDCR will not increase the probability of occurrence or the consequences of an accident or malfunction of equipnent important to safety previously evaluated in the safety l
analysis report.
POTENTIAL FOR CREATION OF AN UNANALYZED ACCIDENT Reference 5 considered the possibility of a number of failure modes associated with repairing steam generator tubes by sleeving or plugging.
l
. These include:
1.
failures caused by inadequate design or improper installation, and 2.
failures caused by installation of a defective sleeve.
Because of the extensive qualification process, sleeve specification, inspection and testing, and controls on sleeve installation, these f ailure modes are considered to be improbable.
As a result, this PDCR does not create the possibility of an accident or malfunction of a different type than any evaluated previously in the safety analysis report.
EFFECT ON THE MARGIN OF SAFETY The design specification for the sleeves / plugs, the sleeve / plug inspection, sleeve / plug testing and installation procedures will result in a repaired steam generator tube which is structurally sound. The repaired tube will provide a pressure boundary barrier which meets all necessary requirements.
Therefore, repairing sesam generator tubes by sleeving and/or plugging does not reduce the margin of safety as specified in the basis of any technical specification.
SUMMARY
AND CONCLUSION Because of the above assessments, the changes implemented by this PDCR are considered to be safe and do not constitute an unreviewed safety question, as defined in 10CFR50.59, since it does not:
1.
increase the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the safety analysis report, 2.
create the possibility for an accident or malfunction of a different type than previously analyzed in the safety analysis report, or 3.
reduce the margin of safety as defined in the basis of any techpicals cification, k9h7 I OMA fl//2/fh
'S. Rai, Supervisor
/
A'. Gharikhani, Engineer
/M.
. Transient Analysis Section Transient Analysis Section
$YWErb
/J'A.Blaisdell, Manager C
L5afety Analysis Branch
_9_
TABLE 1 CY DESIGN PARAMETERS Core power 1825 Mwth.
System pressure 2000.0 psig.
Inlet temperature 540.6 F Initial total flow rate 268,000 GPM.
Core bypass fraction 9%
Enthalpy rise hot channel factor 1.78 Heat flux hot channel factor 3.09 TABLE 2 IMPORTANT PARAMETERS FOR ANALYZING DNB EVENTS PARAMETER LIMITING. DIRECTION Core power Maximum System pressure Minimum Inlet temperature Maximum Inlet core flow rate and pump coastdown characteristics Miniraum Core bypass flow Maximum Radial and axial power distribution Maximum o
10-1 TABLE 3 IMPORTANT PARAMETERS FOR ANALYZING OVERC00 LING EVENTS PARAMETER LIMITING DIRECTION Shutdown margin Minimum Moderator feedback Maximum 4
Power peaking factors Maximum RCS flow rate Maximum SG. heat transfer area and inventory Maximum TABLE 4 IMPORTANT PARAMETERS FOR ANALYZING OVERHEATING EVENTS PARAMETER LIMITING DIRECTION Doppler coefficient Maximum Moderator coefficient Maximum Trip reactivity Minimum Decay heat Maximum SG. heat transfer area and inventory Minimum RCS flow rate and inventory Minimum 1
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