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Category:GENERAL EXTERNAL TECHNICAL REPORTS
MONTHYEARML20199L5891997-12-24024 December 1997 Independent Analysis & Evaluation of AM-241 & Transuranics & Subsequent Dose to Two Male Workers at Connecticut Yankee Atomic Power Plant ML20210P8721997-08-31031 August 1997 Post Decommissioning Activities Rept, for Aug 1997 ML20141A0041997-05-31031 May 1997 Independent Assessment of Radiological Controls Program at Cyap Haddam Neck Plant Final Rept May 1997 ML20137H3031997-03-31031 March 1997 Rev 2 to Nuclear Training Loit/Lout Audit Reviews ML20137C6281997-03-14014 March 1997 Redacted Version of Rev 1 to Nuclear Training Loit/Lout Audit Reviews ML20135E3221997-02-13013 February 1997 Independent Review Team Rept 1996 MP -1 Lout NRC Exam Failures ML20134L2751997-02-0303 February 1997 Draft Rev to GPRI-30, Spent Fuel Storage Facility Licensing Basis/Design Basis ML20134L2911997-01-0808 January 1997 Rev 0 to UFSAR Rev Grpi ML20204B6811996-12-31031 December 1996 Nuclear Lemons Assessment of America Worst Commerical Nuclear Power Plants. 5th Edition ML20237E0751996-12-31031 December 1996 Decommissioning Cost Study for Connecticut Yankee Nuclear Power Plant ML20134L2591996-12-31031 December 1996 Rev 0 to Sys Reclassification ML20134L2721996-12-31031 December 1996 Commitment Mgt Grpi ML20134L2481996-12-30030 December 1996 Rev 0 to Sys Needed for Decommissioning Sys Evaluation Process ML20135E2711996-12-26026 December 1996 Evaluation of Intakes by Two Workers at CT Yankee Atomic Power Co ML20134L2841996-12-23023 December 1996 Rev 0 to Spent Fuel Pool Island Studies ML20134L2871996-12-19019 December 1996 Rev 0 to Grpi for Defueled Condition Fire Protection Technical Requirements ML20134L2381996-12-19019 December 1996 Rev 0 to Accident Analysis ML20058G3481993-10-31031 October 1993 Nonproprietary VIPRE/WRB-1 DNBR Thermal Limit for Westinghouse Fuel Types, for Oct 1993 ML20058G6771993-09-29029 September 1993 Rev 0 to Project Assignment 91-006, Connecticut Yankee Event V Mods ML20058L7411993-07-15015 July 1993 QA Svcs Dept Surveillance Rept SS-169, Assessment of Fitness for Duty Program ML20127J5391992-11-30030 November 1992 Connecticut Yankee Structural Reevaluation of Plant Structures to Address SEP Topic III-7.B Load Combinations Code Changes ML20125E5661992-03-31031 March 1992 Nonproprietary PWR SG Tube Repair Limits:Technical Support Document for Expansion Zone PWSCC in Roll Transitions Final Rept A08995, Rev 1 to Auxiliary Initiation Event Analysis1990-09-14014 September 1990 Rev 1 to Auxiliary Initiation Event Analysis ML20062G4951990-07-31031 July 1990 Rev 3 to Northeast Utils USNRC Read & Sign ML20055G4951990-07-31031 July 1990 Decommissioning Financial Assurance Certification Rept ML20055D8931990-06-30030 June 1990 Fracture Mechanics Evaluation:Haddam Neck Pressurizer ML20246N9421989-08-31031 August 1989 Tornado Missile Risk Analysis of Bleed & Feed & Auxiliary Feedwater Safe Shutdown Sys at Connecticut Yankee Atomic Power Station ML20206J9991988-10-31031 October 1988 Crdr Summary Rept, Per Suppl 1 to NUREG-0737 ML20153G4081988-06-0303 June 1988 Rev 0 to Conneticut Yankee Replace Nuclear Instrumentation Sys, Neo Project Description ML20153G4031988-03-0808 March 1988 Rev 0 to, Connecticut Yankee Modernize Reactor Protection Sys - Phase 2, Conceptual Project Description ML20235B5911987-09-24024 September 1987 Undated Technical Evaluation:Haddam Neck Plant Reanalysis of Non-LOCA DBAs & Tech Spec Change Requests in Support of Reload Cycle 15 B12619, Bimonthly Progress Rept 5:New Switchgear Bldg Const1987-07-31031 July 1987 Bimonthly Progress Rept 5:New Switchgear Bldg Const ML20214R6371987-06-30030 June 1987 Technical Rept Supporting Cycle 15 Operation ML20205Q7011987-04-30030 April 1987 Bimonthly Progress Rept 3:New Switchgear Bldg Const B12480, Const Design Info Submittal:New Switchgear Bldg Const. W/38 Oversize Encl1987-04-30030 April 1987 Const Design Info Submittal:New Switchgear Bldg Const. W/38 Oversize Encl ML20238C3751986-12-31031 December 1986 Connecticut Yankee 1986 Core XIII - Xiv Refueling Outage ALARA Rept ML20238C3821986-12-31031 December 1986 Connecticut Yankee 1986 Steam Generator Repair Outage ALARA Rept ML20209C7161986-12-31031 December 1986 Vols 1 & 2 to Isap,Haddam Neck Plant,Final Rept ML20202D5071986-06-30030 June 1986 Non-LOCA Transient Analysis ML20206J8871986-06-30030 June 1986 Isap Public Safety Impact Model Project Analyses Summaries ML20205T1201986-05-19019 May 1986 Steam Generator Tube Insp Rept for 1986 Refueling Outage ML20205T1231986-05-0808 May 1986 Steam Generator Tube W/55% Through Wall Defect Safety Evaluation for Structural Integrity CY-86-031, Rev 1 to 4.10.1(D) Inservice Insp of Steam Generator Tubes (Acceptance Criteria)1986-05-0808 May 1986 Rev 1 to 4.10.1(D) Inservice Insp of Steam Generator Tubes (Acceptance Criteria) ML20199L0731986-03-31031 March 1986 Probabilistic Safety Study,Northeast Util Svc Company Evaluation of Probabilistic Safety Study Results B12020, Summary of Results of Haddam Neck Probabilistic Safety Study1986-03-31031 March 1986 Summary of Results of Haddam Neck Probabilistic Safety Study ML20138B1561986-03-31031 March 1986 Permanent Exemptions Re Types a & C Leak Testing ML20138B1831986-03-31031 March 1986 Schedular Exemption Requests Re Type C Leak Testing ML20138B2001986-03-31031 March 1986 Status of Containment Integrated Leak Rate Test Program ML20155E7591986-02-28028 February 1986 Best Estimate LOCA Analysis, Vol 5 CY-85-062, Rev 2 to Steam Generator Tube Sleeving & Plugging1986-01-22022 January 1986 Rev 2 to Steam Generator Tube Sleeving & Plugging 1997-08-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K3301999-10-19019 October 1999 Safety Evaluation Supporting Amend 195 to License DPR-61 ML20206C8761999-04-28028 April 1999 Safety Evaluation Supporting Amend 194 to License DPR-61 CY-99-047, Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use1999-03-23023 March 1999 Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use ML20206F1971998-12-31031 December 1998 Annual Rept for 1998 for Cyap. with CY-99-027, Annual Rept for 10CFR50.59, for Jan-Dec 1998.With1998-12-31031 December 1998 Annual Rept for 10CFR50.59, for Jan-Dec 1998.With ML20198G9101998-12-22022 December 1998 Proposed Rev 2 of Cyap QAP for Haddam Neck Plant. Marked Up Rev 1 Included ML20238F2131998-08-28028 August 1998 SER Accepting Defueled Emergency Plan for Emergency Planning for Connecticut Yankee Atomic Power Co CY-98-136, Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line1998-08-12012 August 1998 Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line ML20237B7461998-07-22022 July 1998 1998 Defueled Emergency Plan Exercise Scenario Manual, Conducted on 980722 ML20202D1621998-06-30030 June 1998 Safety Evaluation Supporting Amend 193 to License DPR-61 CY-98-068, Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms1998-04-15015 April 1998 Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms CY-98-045, Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing1998-04-13013 April 1998 Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing ML20217F0611998-03-31031 March 1998 Historical Review Team Rept ML20217A0001998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Haddam Neck Plant ML20217K2101998-03-27027 March 1998 Safety Evaluation Supporting Amend 192 to License DPR-61 CY-98-046, Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal1998-03-12012 March 1998 Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal ML20216D6531998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Haddam Neck Plant ML20217D7381998-02-28028 February 1998 Revised MOR for Feb 1998 Haddam Neck Plant CY-98-012, Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant CY-98-010, Annual Rept for 10CFR50.59,Jan-Dec,19971997-12-31031 December 1997 Annual Rept for 10CFR50.59,Jan-Dec,1997 ML20198N6681997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Haddam Neck Plant ML20217P4861997-12-31031 December 1997 1997 Annual Financial Rept, for Cyap ML20199L5891997-12-24024 December 1997 Independent Analysis & Evaluation of AM-241 & Transuranics & Subsequent Dose to Two Male Workers at Connecticut Yankee Atomic Power Plant ML20203K4271997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Haddam Neck Plant ML20199B1141997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Haddam Neck Plant ML20198M8101997-10-14014 October 1997 SER Accepting Proposed Revs to Util Quality Assurance Program at Facility ML20198J8811997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Haddam Neck Plant ML20210P8721997-08-31031 August 1997 Post Decommissioning Activities Rept, for Aug 1997 ML20217Q3171997-08-31031 August 1997 Addl Changes to Proposed Rev 1 to QA Program ML20210U9301997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Haddam Neck Plant CY-97-082, Special Rept:On 970708,routine Surveillance Testing of Seismic Monitoring Sys Instrumentation Revealed,Data Was Not Being Reproduced by Portion of Playback Sys.Station Presently Pursuing Replacement of Seismic Monitoring Sys1997-08-14014 August 1997 Special Rept:On 970708,routine Surveillance Testing of Seismic Monitoring Sys Instrumentation Revealed,Data Was Not Being Reproduced by Portion of Playback Sys.Station Presently Pursuing Replacement of Seismic Monitoring Sys ML20210L0521997-07-31031 July 1997 Monthly Operating Rept for July 1997 for HNP ML20149E4451997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Haddam Neck Plant ML20141A0041997-05-31031 May 1997 Independent Assessment of Radiological Controls Program at Cyap Haddam Neck Plant Final Rept May 1997 ML20140H5241997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Haddam Neck Plant ML20141K4201997-05-22022 May 1997 Safety Evaluation Supporting Amend 191 to License DPR-61 ML20141D4141997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Connecticut Yankee Haddam Neck ML20138G5901997-04-25025 April 1997 Proposed Rev 1 to Cyap QA Program for Haddam Neck Plant ML20137W8051997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Haddam Neck Plant ML20137H3031997-03-31031 March 1997 Rev 2 to Nuclear Training Loit/Lout Audit Reviews ML20137C6281997-03-14014 March 1997 Redacted Version of Rev 1 to Nuclear Training Loit/Lout Audit Reviews ML20137A0801997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Haddam Neck Plant ML20135C5101997-02-26026 February 1997 1996 Refuel Outage ISI Summary Rept for CT Yankee Atomic Power Co B16268, Special Rept:On 970205,declared Main Stack-Wide Range Noble Gas Monitor Inoperable.Caused by Inadequate Calibr Methods. Will Revise Calibr Procedure to Technique to Demonstrate Accuracy & Linearity Over Intended Range of Monitor1997-02-19019 February 1997 Special Rept:On 970205,declared Main Stack-Wide Range Noble Gas Monitor Inoperable.Caused by Inadequate Calibr Methods. Will Revise Calibr Procedure to Technique to Demonstrate Accuracy & Linearity Over Intended Range of Monitor ML20135E3221997-02-13013 February 1997 Independent Review Team Rept 1996 MP -1 Lout NRC Exam Failures ML20134L2751997-02-0303 February 1997 Draft Rev to GPRI-30, Spent Fuel Storage Facility Licensing Basis/Design Basis ML20138K5721997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Haddam Neck Plant.W/ ML20134L2791997-01-10010 January 1997 Rev 0 to QA Program Grpi ML20134L2911997-01-0808 January 1997 Rev 0 to UFSAR Rev Grpi ML20134L2721996-12-31031 December 1996 Commitment Mgt Grpi 1999-04-28
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Page 1 CONN 8CTICUT YANEEE
' STEAM GENERATOR TUBE WITH 554 THRODGE WALL DEFECT SAFETY EVALUATION FOR STRDCTURAL INTEGRITY 1
INTRODUCTION This safety evaluation assessos the structural integrity of Connecticut Yankee's steam generator tube Row 37, Column 73 which contains a 554 through wall defect. It describes the defective tube and evaluates this tube against the plant design bases with respect to maintaining reactor coolant system integrity. 'The criteria of 10CFR50.59a.2 is applied to determineiwhether an unreviewed safety question is created by continued operation of the plant.
- DBSCRIPTION OF DEFBCTIVE TUBE on May 6, 1986, during preparation of the Maddam Neck Steam Genera-tor Tube Inservice Inspection Final Report, it was discovered that a tube at Row 37, Column 73 (Tube 37-73) of the 42 Steam Generator should have been plugged during the recently completed refueling outage. A. transcription error during the evaluation of the eddy-current test data for this tube resulted in the tube at Row 37, Column 33 (Tube 37-33) being plugged by mistake. Tube 37-73 has a small diameter pit that is 55% of the nominal tube wall thickness.
The plugging limit, as defined in Specification 4.10.1.D.1.f is greater than or equal to 50% of the nominal tube wall thickness.
Further data verification has shown this to be a unique error.
DESIGN BASES The original design bases for Connecticut Yankee steam genera-tors include the ASME Boiler and Pressure Vessel Code,Section VIII, 1962 Edition; the Safety Technical Specification, Facil-l ity Description and safety Analysis, Vestinghouse Electric Corp. Technical Manual 1440-C78 for Model 27 Steam Generator, l n December 1966; Westinghouse Report WNEP-8521: Connecticut l .oEE Yankee Steam Generators Stress Report, 4-1-85 and ASME Code 380- Cases No. 1270N and 1273N.
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Basically, the tube design considers pressure retention capabi-g lity af ter accounting for anticipated numbers of normal, acci-no dont and test loading cycles. Also, tubes are designed for 88 vibrational stability in -the fluid environment.
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5 The safety Technical Specification (Section 4.10.1.D.1.f)
S$ requires that defective tubes containing flaws 2 through m a.e wall be plugged. This specification, however, does, 504not provide definitive engineering basis that a 50% throughwall flaw thres-hold constitutes the required margin .of safety beyond which 1
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" " * " * * ' " ~ , Page 2 CONNECTICUT YANKEE STEAM GENERATOR TUBE WITE 55% THROUCE WALL D8FBCT SAFETY EVALUATION FOR STRUCTURAL INTEGRITY corrective action is re qu ired'. Regulatory Guide 1.121, " Bases for Plugging Degraded PWR Steam Generator Tubes", does provide the criteria to judge acceptability of degraded or defective tubes.
PROPOSED CHANCES The requirements of the Safety Technical Specification must be changed to allow the defective tube, Row 37, Column 73 of No. 2 steam generator to remain in service until the end of operation of cycle fourteen.
In support o'f this change to the technical specifications is NUSCO Calculation No. 85-053-685GP, " Evaluation of a 554 through wall Defect in a Steam Generator Tube". This calculation demonstrates the following:
- 1. The allowable end-of-cycle pit depth for Connecticut Yankee steam generator tubes is 894 through wall for a single large (.187" diameter) pit.
- 2. The projected maximum end-of-cycle pit depth for the subject pit is 834.
7 l 3. This allowable pit depth satisfies Regulatory Guide 1.121
. and provides margins of safety which exceed the requ ire--
ments of the ASME Code Section III.
POSTULATED FAILURES The existence of an unplugged defective tube in the No. 2 steam generator has negligible effect on the probability of tube rupture.
This failure is reviewed with respect to effect, and preventative safeguards are noted.
The safety hazard arising from a potential rupture of the defective tube is that primary cooling water could leak into the secondary side with resultant dispersion of radioactivity. Such failure could encompass a pin-hole leak to a completely severed tube. The latter situation is a worst case scenario in which the severed tube is able to whip around damaging adjacent tubes. Past failures of steam generator tubes demonstrate that it is very unlikely that tubes containing pit type defects will sever. Instead, tubes will rupture in a ductile manner, leaking before exhibiting a complete break.
The design basis for the plant adequately addresses such an event by r- __. _ __.__ _ _ A
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p.g 3 CONNBCTICDT YANQE STEAM GENERATOR TUBE WITH 55% THRODCE IIALL DEFECT SAFETY EVALUATION FOR STRUCTURAL INTEGRITY requiring in-service radiation monitoring and primary to secondary leakage monitoring.
In summary, the worst credible postulated failure resulting from this defect is a ductile rupture preceded by leakage. This leakage would be readily detected and the plant shut down before additional tubes would rupture. Since the single rupture is a design basis for the plant, postulated failures are not significant with respect to public health and safety.
UNREVIEWED SAFETY QUESTION DETERMINATION
- 1. Effect of Proposed Change on the Probability of Occurence or The Consequences of an Accident or Malfunction of Equipment Important to Safety Previously Evaluated in the Safety Analysis Report.
o A single defective steam generator tube has a negligible effect on the probability of occurence of previously analyzed acci-dents (e.g., tube rupture). Furthermore, this defective steam generator tube meets the original and current structural design requirements for normal and faulted loading conditions. Thus, the probability of occurence of an accident or malfunction of equipment important to safety is not increased.
o A single defective steam generator tube has no effect on the
,' consequences of previously analyzed accidents as a tube rupture has been considered in the design basis of the plant. Thus, the consequences of an accident or malfunction of equipment impor-tant to safety is not increased.
- 2. Etf act of Proposed Change with Respect to Creating Accident or Malfunction Possibilities of a Different type than Previously Evaluated in the Safety Analysis Report.
o The possibility that a defective tube might create an accident not previously analyzed was investigated. Tube rupture is an analysed accident, and no other credible failure can be postu-lated from this degradation. Thus, the original component design criteria are met and no new accidents would be created.
- 3. The Effect of the Proposed Change on the Margin of safety as Defined in the Basis for Any Technical specification The Connecticut Yankee Technical specification Basis' section
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Page 4 CONNECTICUT YANKEE STEAM GENERATOR TUBE WITE 554 THRODGE WALL DEFECT SAFETY EVALUATION FOR STRUCTURAL INTEGRITY 4.10.1.D.1.f requires that steam generator tubes with imperfec-tions with depths 50% of the nominal wall thickness and larger be plugged. The technical basis for the 50% plugging limit and the associated safety margin is not defined in the Safety Technical Specification. In the absence of a specific technical basis supporting the 50% plugging limit, a technical evaluation was made in accordance with Regulatory Guide 1.121, " Bases for Plugging Degraded PWR Steam Genertor Tubes"' to assess the impact of the specific flaw in steam generator tube 37-73 on the reactor coolant pressure boundary integrity / safety margins.
The indication has been characterized as a pit with a diameter of .080 inches and 554 throughwall. Using the worst case pro- l grossion rate and inspection error the projected end-of-cycle depth will be 834. Based on NUSCO Calculation 85-053-685GP, it is . concluded that the limiting defect depth for the pit type indication which will assure the necessary margin against burst
, for the normal and/or f aulted design conditions is a pit-type 1
defect of 894 throughwall. Therefore, it is concluded that the safety margin against burst required by Regulatory Guide 1.121 would not be compro=ised by operating with the 55% deep pit-type indication during the upcoming cycle and the required reactor coolant pressure boundary integrity would be main-tained.
Previous burst testing on steam generator tubes (Reference 1 from Calculation 85-053-685GP, Revision 0), clearly illustrates
. that single large pits up to 92% through wall have a greater l margin to burst than 50% through wall uniformly thinned tubes.
Based on the above evaluation, it is concluded that the margin of safety is not reduced.
In conclusion, continued operation through the end of cycle 14 as proposed by this safety evaluation, does not constitute an unreviewed safety question as defined in 10CrR50.59.
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CONNECTICUT YANKEE STRAM GENERATOR TUBE WITH 55% THRODGE WALL DEFECT SAFETY EVALUATION FOR STRUCTURAL INTEGRITY Prepared by:
N. R. CALLER' 7/P/((
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M. KUPIR$KI V Reviewed by:
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