05000325/LER-2016-001, Regarding Electrical Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power

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Regarding Electrical Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power
ML16104A391
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 04/06/2016
From: William Gideon
Duke Energy Progress
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
BSEP 16-0021 LER 16-001-00
Download: ML16104A391 (7)


LER-2016-001, Regarding Electrical Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(iv)(B), System Actuation
3252016001R00 - NRC Website

text

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~'ENERGY APR 0 6 2016 Serial: BSEP 16-0021 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001

Subject:

Brunswick Steam Electric Plant, Unit No. 1 Renewed Facility Operating License No. DPR-71 Docket No. 50-325 Licensee Event Report 1-2016-001 William R. Gideon Vice President Brunswick Nuclear Plant P.O. Box 10429 Southport, NC 28461 o: 910.457.3698 10 CFR 50.73 In accordance with the Code of Federal Regulations, Title 10, Part 50.73, Duke Energy Progress, Inc., submits the enclosed Licensee Event Report (LEA). This report fulfills the requirement of 1 O CFR 50.73(a)(1) for a written report within sixty (60) days of a reportable occurrence.

Please refer any questions regarding this submittal to Mr. Lee Grzeck, Manager - Regulatory Affairs, at (910) 457-2487.

William R. Gideon SWR/swr Enclosure: Licensee Event Report 1-2016-001

U.S. Nuclear Regulatory Commission Page 2 of 2 cc (with enclosure):

U.S. Nuclear Regulatory Commission, Region II ATTN: Ms. Catherine Haney, Regional Administrator 245 Peachtree Center Ave, NE, Suite 1200 Atlanta, GA 30303-1257 U.S. Nuclear Regulatory Commission ATTN: Ms. Michelle P. Catts, NRC Senior Resident Inspector 8470 River Road Southport, NC 28461-8869 U.S. Nuclear Regulatory Commission ATTN: Mr. Andrew Hon (Mail Stop OWFN 8G9A) (Electronic Copy Only) 11555 Rockville Pike Rockville, MD 20852-2738 Chair - North Carolina Utilities Commission P.O. Box 29510 Raleigh, NC 27626-0510

NRC FORM 366 U.S. NUCLEAR REGULATORY"COMMISSION APPROVED BY OMB: NO. 3150*0104 EXPIRES: 10/31/2018 (11-2015)

, the NRG may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE Brunswick Steam Electric Plant (BSEP) Unit 1 05000325 1 OF 5
4. TITLE Electrical Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power
5. EVENT DATE
6. LEA NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED YEAR I SEQUENTIAL I REV FACILITY NAME DOCKET NUMBER MONTH DAY YEAR NUMBER NO.

MONTH DAY YEAR 05000 FACILITY NAME DOCKET NUMBER 02 07 2016 2016 - 001

- 00 04 06 2016 05000
9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: {Check all that apply)

D 20.2201 (b)

D 20.22os(a)(s)(i)

D 50.73(a)(2)(ii)(A)

D 50.73(a)(2)(viii)(A) 1 D 20.2201 (d)

D 20.22os(a)(s)(ii)

D 50.73(a)(2)(ii)(B)

D 50.73(a)(2)(viii)(B)

D 20.22os(a)(1)

D 20.22os(a)(4)

D so.1s(a)(2J(iii)

D 50.73(a)(2)(ix)(A)

D 20.22os(a)(2)(i)

D 50.36(c)(1)(i)(A)

~

50.73(a)(2)(iv)(A)

D 50.73(a)(2)(x)

10. POWER LEVEL D 20.22os(a)(2)(ii)

D 50.36(c)(1)(ii)(A)

D 50.73(a)(2)(v)(A)

D 1s.11(a)(4l D 20.22os(a)(2)(iiil D so.ss(c)(2J D 50.73(a)(2)(v)(B)

D 1s.11(a)(s)

D 20.2203(a)(2)(iv)

D so.4s(a)(s)(iil D 50.73(a)(2)(v)(C)

D 1s.11(a)(1J 088 D 20.2203(a)(2)(v)

D 50.73(a)(2)(i)(A)

D 50.73(a)(2)(v)(D)

D 1s.11(a)(2J(i)

D 20.2203(a)(2)(vi)

D 50.73(a)(2)(i)(B)

D 50.73(a)(2)(vii)

D 1s.11(a)(2)(ii)

I.'.

'~"' '*

t;,.*..

D 50.73(a)(2)(i)(C)

D OTHER Specify in Abstract below or in 05000-325 YEAR 2016 -

SEQUENTIAL NUMBER 001 REV NO.

000 opened per design and deenergized the UAT. This interrupted power to emergency busses E1 and E2.

Since the SAT was already locked out, the power source for busses E1 and E2 could not transfer to the SAT. Therefore, a LOOP condition existed on emergency electrical busses E1 and E2. EDG1 and EDG2 were already running and automatically tied to their respective busses, E1 and E2. On Unit 2, EDG3 and EDG4 started per design, but did not connect to their busses because the LOOP condition did not exist on Unit 2.

Following shutdown of the main turbine, reactor pressure was initially controlled by opening safety/relief valves [SB]. When pressure was stable, licensed personnel manually started the HPCI system and maintained control of reactor pressure, and they started the RCIC system for the purpose of maintaining reactor water level. After the manual scram, reactor water level decreased below Low Level 1 per the normal, expected water level shrinkage that follows a reactor scram. The low water level resulted in additional, redundant RPS actuation signals being received, and Group 2 and Group 6 PCIVs received an auto closure signal. The momentary loss of power that occurred between the LOOP and energizing the busses via the EDGs also resulted in Group 1, Group 3, and Group 1 O PCIVs receiving a closure signal.

All affected PCIVs closed per design.

Standby Gas Treatment System (SBGT) [BH] fans started due to the LOOP condition. However, associated Secondary Containment dampers [VA] did not reposition because the relays in the damper control logic are not designed to seal in, and the duration of the transient when the bus was depowered was too brief for the dampers to physically complete their movement before the EDGs repowered the busses and the signal cleared.

Operations personnel promptly performed a walkdown of plant equipment and noted evidence that an arc flash had occurred in a balance of plant 4160-volt circuit breaker cubicle which supplies the 18 Reactor Recirculation Pump Variable Frequency Drive (VFD) unit. The breaker cubicle showed evidence of an electrical* explosion; that is, the cubicle door was deformed. Per Emergency Action Level HA2.1, evidence of an explosion in an area affecting safe shutdown equipment requires entry into an Alert. Thus, the Alert was declared at 1326 EST.

At 1628 EST on February 7, 2016, offsite power was restored to electrical busses E1 and E2 by connecting the UAT to the grid and supplying power to the busses from the UAT, which is their normal source. At 1751 EST, the emergency classification was downgraded to an Unusual Event (UE) because the plant no longer met the criteria for an Alert, since the source of the explosion was determined not to have affected safe shutdown equipment. The UE emergency declaration was terminated at 1814 EST.

Event Causes The initiating event was two arc flashes that occurred in a non-segregated bus (i.e., a bus in which all three phases lie within a single housing) and in a circuit breaker cubicle which powers the 18 VFD for a Reactor Recirculation system pump. The first arc flash occurred in an area of the bus housing outdoors where water had accumulated. The fault created a voltage imbalance which led to the second arc flash which occurred in the breaker cubicle where cable insulation was found to be degraded.

05000-325 YEAR 2016 -

SEQUENTIAL NUMBER 001 REV NO.

000 Water entered the non-segregated bus housing through a degraded seal and an area that had previously been repaired. The water created the conditions conducive to an arc flash.

In the breaker cubicle for the 1 B VFD, it was found that during installation in 201 O of electrical stress-relieving insulation (i.e., "stress cones"), the dielectric insulation on a cable jacket had been damaged when a piece of semiconducting material was being removed. The arc flash occurred at the point where the cable insulation had been damaged.

The root cause of the moisture intrusion into the non-segregated bus was inspection procedures did not contain sufficient specific detail based on highest risk locations (i.e., specifically, horizontal surfaces through which bars penetrate) to ensure that deficiencies that can lead to water intrusion are identified and corrected during its implementation. A contributing cause was that the design of the bus housing is not optimum for the application because it is susceptible to corrosion leading to water intrusion.

The root cause of the damaged cable insulation was failure to specify and use a depth-limiting cutting tool for removing semiconducting material from cable insulation. When workers removed semiconducting material from the cable during initial installation of the cable termination stress cone, the underlying cable dielectric insulation was scored, reducing its insulating effectiveness. This contributed to conditions which led to an arc fault in the affected 4160-volt cable. A contributing cause was lack of a post-installation test method which would be adequate to detect insulation deficiencies.

Safety Assessment

In this event, a LOOP occurred on Unit 1 emergency busses E1 and E2 due to lockout of the SAT and interruption of power to the UAT. The reactor was immediately and safely shut down by manual scram in accordance with station operating procedures. The RCIC system and HPCI system operated as designed and controlled reactor water level and pressure, respectively. All four station EDGs started as expected, and EDGs 1 and 2 supplied power to affected emergency busses E1 and E2. Unit 2 busses E3 and E4 were not affected by the event, and they remained powered by their normal, offsite sources. In addition, the site's supplemental diesel generator was available and could have been used if necessary to mitigate the event. The SAT was not damaged by the event. The UAT remained available for backfeed, and backfeed was implemented per procedure during the event. All safety systems operated per design in response to the event.

Based on the foregoing analysis, it's concluded that this event had no adverse impact on the health and safety of the public.

Corrective Actions

05000-325 YEAR 2016 -

SEQUENTIAL NUMBER 001 Any changes to the corrective actions and schedules noted below will be made in accordance with the site's corrective action program.

REV NO.

000

  • Affected equipment related to the event has been repaired, including the affected non-segregated bus housing, conductors and stress cones, and circuit breaker. These actions are completed.
  • The procedure for splicing and terminating wires and cables will be revised to include lessons learned from this event, including the use of depth-limiting cutting tools and inspections for damage after cutting operations are performed. This action is expected to be completed by June 30, 2016.
  • The procedure and work instructions for inspecting and cleaning the non-segregated busses will be revised to eliminate the root causes of the water intrusion. This action is expected to be completed by August 25, 2016.
  • An improved cable testing methodology will be specified in appropriate maintenance procedures.

This action is expected to be completed by June 30, 2016.

  • The non-segregated bus housing design will be presented for action by the site's Modification Review and Prioritization Team (MRPT) for scheduling and design work. This action is expected to be completed by June 30, 2016.

Previous Similar Events

A review of LERs and the site's corrective action program for the past three years did not identify any previous similar occurrences involving significant electrical faults or LOOP conditions.

Commitments

No regulatory commitments are contained in this report.

2. DOCKET NUMBER YEAR 05000-325 2016 -

Energy Industry Identification System (EllS) codes are identified in the text as [XX].

Background

Initial conditions

3. LER NUMBER SEQUENTIAL NUMBER 001 REV NO.

000 On February 7, 2016, at 1312 Eastern Standard Time (EST), Unit 1 was in Mode 1 (i.e., Run) at a power level of 88 percent of rated thermal power in end-of-cycle coastdown. No out-of-service equipment contributed to, or affected the course of, this event.

Reportability Criteria This event is being reported in accordance with 1 O CFR 50.73(a)(2)(iv)(A) because it involved actuations of systems listed in 1 O CFR 50.73(a)(2)(iv)(B). Specific actuations included:

  • Several Primary Containment Isolation Valves (PCIVs) [JM] automatically closed per design in response to either loss of control logic power or reactor water level changes that resulted from the reactor scram.

The NRC was notified of the event, including the emergency declaration, per 1 o CFR 50.72(a)(1 )(i),

10 CFR 50.72(b)(2)(iv)(B), and 10 CFR 50.72(b)(3)(iv)(A) via Event Notification 51715 at 13:46 EST on February 7, 2016.

Event Description

On February 7, 2016, at 1312 EST, BSEP Unit 1 was in Mode 1 during end-of-cycle coastdown. Two arc flashes occurred in a 4160-volt electrical system which resulted in two phases of the system faulting to ground, which also constituted a phase-to-phase fault. The high differential current actuated the lockout on the Unit 1 Startup Auxiliary Transformer (SAT) [EA], which started all four emergency diesel generators. The loss of power to equipment fed from the SAT resulted in shutdown of both Reactor Recirculation system pumps. With both pumps not operating, station procedures require licensed personnel to insert a manual scram. This was performed immediately, and all control rods,[AA] fully inserted into the core per design.

The manual scram automatically shut down the main turbine [TA] and main generator [EL] per design.

With the main generator offline, the power circuit breakers for the Unit Auxiliary Transformer (UAT) [EA]

05000-325 YEAR 2016 -

SEQUENTIAL NUMBER 001 REV NO.

000 opened per design and deenergized the UAT. This interrupted power to emergency busses E1 and E2.

Since the SAT was already locked out, the power source for busses E1 and E2 could not transfer to the SAT. Therefore, a LOOP condition existed on emergency electrical busses E1 and E2. EDG1 and EDG2 were already running and automatically tied to their respective busses, E1 and E2. On Unit 2, EDG3 and EDG4 started per design, but did not connect to their busses because the LOOP condition did not exist on Unit 2.

Following shutdown of the main turbine, reactor pressure was initially controlled by opening safety/relief valves [SB]. When pressure was stable, licensed personnel manually started the HPCI system and maintained control of reactor pressure, and they started the RCIC system for the purpose of maintaining reactor water level. After the manual scram, reactor water level decreased below Low Level 1 per the normal, expected water level shrinkage that follows a reactor scram. The low water level resulted in additional, redundant RPS actuation signals being received, and Group 2 and Group 6 PCIVs received an auto closure signal. The momentary loss of power that occurred between the LOOP and energizing the busses via the EDGs also resulted in Group 1, Group 3, and Group 1 O PCIVs receiving a closure signal.

All affected PCIVs closed per design.

Standby Gas Treatment System (SBGT) [BH] fans started due to the LOOP condition. However, associated Secondary Containment dampers [VA] did not reposition because the relays in the damper control logic are not designed to seal in, and the duration of the transient when the bus was depowered was too brief for the dampers to physically complete their movement before the EDGs repowered the busses and the signal cleared.

Operations personnel promptly performed a walkdown of plant equipment and noted evidence that an arc flash had occurred in a balance of plant 4160-volt circuit breaker cubicle which supplies the 18 Reactor Recirculation Pump Variable Frequency Drive (VFD) unit. The breaker cubicle showed evidence of an electrical* explosion; that is, the cubicle door was deformed. Per Emergency Action Level HA2.1, evidence of an explosion in an area affecting safe shutdown equipment requires entry into an Alert. Thus, the Alert was declared at 1326 EST.

At 1628 EST on February 7, 2016, offsite power was restored to electrical busses E1 and E2 by connecting the UAT to the grid and supplying power to the busses from the UAT, which is their normal source. At 1751 EST, the emergency classification was downgraded to an Unusual Event (UE) because the plant no longer met the criteria for an Alert, since the source of the explosion was determined not to have affected safe shutdown equipment. The UE emergency declaration was terminated at 1814 EST.

Event Causes The initiating event was two arc flashes that occurred in a non-segregated bus (i.e., a bus in which all three phases lie within a single housing) and in a circuit breaker cubicle which powers the 18 VFD for a Reactor Recirculation system pump. The first arc flash occurred in an area of the bus housing outdoors where water had accumulated. The fault created a voltage imbalance which led to the second arc flash which occurred in the breaker cubicle where cable insulation was found to be degraded.

05000-325 YEAR 2016 -

SEQUENTIAL NUMBER 001 REV NO.

000 Water entered the non-segregated bus housing through a degraded seal and an area that had previously been repaired. The water created the conditions conducive to an arc flash.

In the breaker cubicle for the 1 B VFD, it was found that during installation in 201 O of electrical stress-relieving insulation (i.e., "stress cones"), the dielectric insulation on a cable jacket had been damaged when a piece of semiconducting material was being removed. The arc flash occurred at the point where the cable insulation had been damaged.

The root cause of the moisture intrusion into the non-segregated bus was inspection procedures did not contain sufficient specific detail based on highest risk locations (i.e., specifically, horizontal surfaces through which bars penetrate) to ensure that deficiencies that can lead to water intrusion are identified and corrected during its implementation. A contributing cause was that the design of the bus housing is not optimum for the application because it is susceptible to corrosion leading to water intrusion.

The root cause of the damaged cable insulation was failure to specify and use a depth-limiting cutting tool for removing semiconducting material from cable insulation. When workers removed semiconducting material from the cable during initial installation of the cable termination stress cone, the underlying cable dielectric insulation was scored, reducing its insulating effectiveness. This contributed to conditions which led to an arc fault in the affected 4160-volt cable. A contributing cause was lack of a post-installation test method which would be adequate to detect insulation deficiencies.

Safety Assessment

In this event, a LOOP occurred on Unit 1 emergency busses E1 and E2 due to lockout of the SAT and interruption of power to the UAT. The reactor was immediately and safely shut down by manual scram in accordance with station operating procedures. The RCIC system and HPCI system operated as designed and controlled reactor water level and pressure, respectively. All four station EDGs started as expected, and EDGs 1 and 2 supplied power to affected emergency busses E1 and E2. Unit 2 busses E3 and E4 were not affected by the event, and they remained powered by their normal, offsite sources. In addition, the site's supplemental diesel generator was available and could have been used if necessary to mitigate the event. The SAT was not damaged by the event. The UAT remained available for backfeed, and backfeed was implemented per procedure during the event. All safety systems operated per design in response to the event.

Based on the foregoing analysis, it's concluded that this event had no adverse impact on the health and safety of the public.

Corrective Actions

05000-325 YEAR 2016 -

SEQUENTIAL NUMBER 001 Any changes to the corrective actions and schedules noted below will be made in accordance with the site's corrective action program.

REV NO.

000

  • Affected equipment related to the event has been repaired, including the affected non-segregated bus housing, conductors and stress cones, and circuit breaker. These actions are completed.
  • The procedure for splicing and terminating wires and cables will be revised to include lessons learned from this event, including the use of depth-limiting cutting tools and inspections for damage after cutting operations are performed. This action is expected to be completed by June 30, 2016.
  • The procedure and work instructions for inspecting and cleaning the non-segregated busses will be revised to eliminate the root causes of the water intrusion. This action is expected to be completed by August 25, 2016.
  • An improved cable testing methodology will be specified in appropriate maintenance procedures.

This action is expected to be completed by June 30, 2016.

  • The non-segregated bus housing design will be presented for action by the site's Modification Review and Prioritization Team (MRPT) for scheduling and design work. This action is expected to be completed by June 30, 2016.

Previous Similar Events

A review of LERs and the site's corrective action program for the past three years did not identify any previous similar occurrences involving significant electrical faults or LOOP conditions.

Commitments

No regulatory commitments are contained in this report.