05000325/LER-2020-001, Manual Reactor Scram During Startup Due to All Bypass Valves Fully Opening

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Manual Reactor Scram During Startup Due to All Bypass Valves Fully Opening
ML20141L763
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 05/20/2020
From: Krakuszeski J
Duke Energy Progress
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
RA-20-0111 LER 2020-001-00
Download: ML20141L763 (5)


LER-2020-001, Manual Reactor Scram During Startup Due to All Bypass Valves Fully Opening
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(i)
3252020001R00 - NRC Website

text

20

  1. DUKE

""' ENERGY May

, 2020 Serial: RA-20-0111 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555

Subject:

Brunswick Steam Electric Plant, Unit No. 1 Renewed Facility Operating License No. DPR-71 Docket No. 50-325 Licensee Event Report 1-2020-001 John A. Krakuszeski Vice President Brunswick Nuclear Plant 8470 River Rd SE Southport, NC 28461 o: 910.832.3698 10 CFR 50.73 In accordance with the Code of Federal Regulations, Title 10, Part 50.73, Duke Energy Progress, LLC, is submitting the enclosed Licensee Event Report (LER). This report fulfills the requirement for a written report within sixty (60) days of a reportable occurrence.

This document contains no regulatory commitments.

Please refer any questions regarding this submittal to Ms. Sabrina Salazar, Manager - Nuclear Support Services, at (910) 832-3207.

Sincerely, John A. Krakuszeski SBY/sby

Enclosure:

Licensee Event Report

U.S. Nuclear Regulatory Commission Page 2 of 2 cc (with enclosure):

Ms. Laura Dudes, NRC Regional Administrator, Region II Mr. Andrew Hon, NRC Project Manager Mr. Gale Smith, NRC Senior Resident Inspector Chair - North Carolina Utilities Commission

NRC FORM 366 (04-2020)

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (04-2020)

LICENSEE EVENT REPORT (LER)

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 04/30/2020

1. Facility Name Brunswick Steam Electric Plant (BSEP), Unit 1
2. Docket Number 05000325
3. Page 1 OF 3
4. Title Manual Reactor Scram During Startup due to all Bypass Valves Fully Opening
5. Event Date
6. LER Number
7. Report Date
8. Other Facilities Involved Month Day Year Year Sequential Number Rev No.

Month Day Year Facility Name Docket Number 05000 03 22 2020 2020

- 001 00 05 20 2020 Facility Name Docket Number 05000
9. Operating Mode
11. This Report is Submitted Pursuant to the Requirements of 10 CFR §: (Check all that apply) 2 20.2201(b) 20.2203(a)(3)(i) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A) 20.2201(d) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(iii) 50.73(a)(2)(ix)(A) 20.2203(a)(2)(i) 50.36(c)(1)(i)(A) 50.73(a)(2)(iv)(A) 50.73(a)(2)(x)
10. Power Level 20.2203(a)(2)(ii) 50.36(c)(1)(ii)(A) 50.73(a)(2)(v)(A) 73.71(a)(4) 002 20.2203(a)(2)(iii) 50.36(c)(2) 50.73(a)(2)(v)(B) 73.71(a)(5) 20.2203(a)(2)(iv) 50.46(a)(3)(ii) 50.73(a)(2)(v)(C) 73.77(a)(1) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(D) 73.77(a)(2)(i) 20.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(vii) 73.77(a)(2)(ii) 50.73(a)(2)(i)(C)

Other (Specify in Abstract below or in Page 3 of 3 In addition to the aforementioned completed corrective actions, the following corrective action is currently planned.

TCS adjustment training will be provided to appropriate Operations Department personnel. This action is scheduled to be completed by July 2, 2020.

Any changes to corrective actions or completion schedules will be made in accordance with the sites corrective action program.

Previous Similar Events

No events have occurred within the past three years in which vague procedure guidance and a lack of proficiency resulted in a LER.

Commitments

No regulatory commitments are contained in this report.