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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000324/LER-1992-001, Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled1993-09-0202 September 1993 Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled 05000324/LER-1993-0081993-08-13013 August 1993 LER 93-008-00:on 930714,core Rated Thermal Power Exceeded Allowable Amount Due to Feedwater Flow Inaccuracy.Cause Believed to Be Due to Erosion/Corrosion of FW Flow Elements. FW Instrumentation recalibr.W/930812 Ltr 05000324/LER-1992-0101993-08-12012 August 1993 LER 92-010-01:on 921207,penetration Leakage Exceeded TS Allowable Limit Due to actuator-to-valve Alignment & disk-to-seat Alignment Problems.Line Bored Valve to Achieve concentricity.W/930812 Ltr 05000324/LER-1991-0191993-08-12012 August 1993 LER 91-019-01:on 911112,LLRT Failure of Two MSL Inboard & Outboard Isolation Valves Resulted in Condition Outside Design Basis.Root Cause Analysis in Process.Msls C & D Inboard & Outboard MSIVs Repairs complete.W/930812 Ltr 05000324/LER-1993-0031993-05-10010 May 1993 LER 93-003-00:on 930408,identified That Drywell Spray Outboard Isolation Valve Installed in Reverse Direction. Caused by Design & Installation Error.Appropriate Documents Will Be revised.W/930507 Ltr 05000324/LER-1988-0011990-08-0101 August 1990 LER 88-001-07:on 880102,manual Reactor Scram Occurred Due to Decreasing Main Condenser Vacuum.Reactor Power at 55% & Vacuum Decreased to 22 Inches Mercury.Caused by Leaks on Main Turbine Piping.Piping repaired.W/900801 Ltr 05000324/LER-1983-019, Updated LER 83-019/01T-2:on 830210,instrument Air Tubing to Safety Relief Valve/Automatic Depressurization Sys Valve Accumulator Inadequately Supported.Caused by Rerouted Tubing.Supports Installed1984-07-12012 July 1984 Updated LER 83-019/01T-2:on 830210,instrument Air Tubing to Safety Relief Valve/Automatic Depressurization Sys Valve Accumulator Inadequately Supported.Caused by Rerouted Tubing.Supports Installed 05000325/LER-1982-108, Updated LER 82-108/03L-1:on 821010 & 14,while Performing Automatic Depressurization Sys Valve Operability Test,Valves 1-B21-F013J & 1-B21-F013D & E Failed to Reclose.Caused by Faulty Spring.Valves Replaced1984-05-18018 May 1984 Updated LER 82-108/03L-1:on 821010 & 14,while Performing Automatic Depressurization Sys Valve Operability Test,Valves 1-B21-F013J & 1-B21-F013D & E Failed to Reclose.Caused by Faulty Spring.Valves Replaced 05000325/LER-1982-122, Supplemental LER 82-122/03L-1:on 821030 & 1104,reactor Recirculation Pump 1A Tripped.On 821101 & 04,reactor Recirculation Pump 1B Tripped.Caused by Spurious Action of ATWS Instrument B21-PS-N045C1984-04-0909 April 1984 Supplemental LER 82-122/03L-1:on 821030 & 1104,reactor Recirculation Pump 1A Tripped.On 821101 & 04,reactor Recirculation Pump 1B Tripped.Caused by Spurious Action of ATWS Instrument B21-PS-N045C 05000325/LER-1981-053, Updated LER 81-053/03L-1:on 810922,during Reactor Startup, Reactor Recirculation Pump 1B Tripped.Caused by Spurious Trip Signal from ATWS Low Water Level Instrument B21-LTM- NO24B-2.Instrument replaced.W/840329 Ltr1984-03-29029 March 1984 Updated LER 81-053/03L-1:on 810922,during Reactor Startup, Reactor Recirculation Pump 1B Tripped.Caused by Spurious Trip Signal from ATWS Low Water Level Instrument B21-LTM- NO24B-2.Instrument replaced.W/840329 Ltr 05000325/LER-1981-055, Updated LER 81-055/03L-1:on 820622,drywell Equipment Drain Flow Integrator 1-G16-FQ-K603 Continuously Indicated Dwed Sump Flow W/No Pumps Running.Caused by Water Being Introduced Into Pneumatic calibrator.W/840328 Ltr1984-03-28028 March 1984 Updated LER 81-055/03L-1:on 820622,drywell Equipment Drain Flow Integrator 1-G16-FQ-K603 Continuously Indicated Dwed Sump Flow W/No Pumps Running.Caused by Water Being Introduced Into Pneumatic calibrator.W/840328 Ltr 05000325/LER-1983-063, Updated LER 83-063/03L-1:on 831203,reactor Water Cleanup Sys (Rwcs) Differential Flow Indicator 1-G31-R615 Showed Erroneous Indication.On 831207,spurious Rwcs Alarm Annunciated.Caused by Air in Sensing lines.W/840222 Ltr1984-02-22022 February 1984 Updated LER 83-063/03L-1:on 831203,reactor Water Cleanup Sys (Rwcs) Differential Flow Indicator 1-G31-R615 Showed Erroneous Indication.On 831207,spurious Rwcs Alarm Annunciated.Caused by Air in Sensing lines.W/840222 Ltr 05000325/LER-1983-057, Updated LER 83-057/03L-1:on 831119,during Unit Power Performance,Temp Recorder TR-1258 Printed Erratically.Caused by Dirty Electrical Contacts in Control Board Timing Relay. Contacts Cleaned & Returned to svc.W/840222 Ltr1984-02-22022 February 1984 Updated LER 83-057/03L-1:on 831119,during Unit Power Performance,Temp Recorder TR-1258 Printed Erratically.Caused by Dirty Electrical Contacts in Control Board Timing Relay. Contacts Cleaned & Returned to svc.W/840222 Ltr 05000324/LER-1983-097, Updated LER 83-097/01T-1:on 831212,during Testing,Per IE Bulletin 83-02,crack Indications Discovered in 19 of 131 Welds in Reactor Recirculation & Reactor Water Cleanup Sys. Caused by Stress Corrosion Cracking1984-01-24024 January 1984 Updated LER 83-097/01T-1:on 831212,during Testing,Per IE Bulletin 83-02,crack Indications Discovered in 19 of 131 Welds in Reactor Recirculation & Reactor Water Cleanup Sys. Caused by Stress Corrosion Cracking 05000325/LER-1983-045, Updated LER 83-045/03L-2:on 830919 & 24,inboard PCIV Steam Supply Valve ES1-F007 to RCIC Sys Would Not Completely Reopen.Caused by Loose Limitorque Motor Operator Spring Pack1984-01-24024 January 1984 Updated LER 83-045/03L-2:on 830919 & 24,inboard PCIV Steam Supply Valve ES1-F007 to RCIC Sys Would Not Completely Reopen.Caused by Loose Limitorque Motor Operator Spring Pack 05000324/LER-1982-024, Updated LER 82-024/01T-1:on 820205,determined That Control Bldg Emergency Ventilation Sys Trains Will Not Isolate Upon Receipt of Chlorine Isolation Signal If Control Switch in on Position Due to Design Deficiency1983-11-14014 November 1983 Updated LER 82-024/01T-1:on 820205,determined That Control Bldg Emergency Ventilation Sys Trains Will Not Isolate Upon Receipt of Chlorine Isolation Signal If Control Switch in on Position Due to Design Deficiency 05000324/LER-1983-083, Updated LER 83-083/01T-1:on 830905,supply Valve 2-FP-V39 to Deluge Sys of Both Standby Gas Treatment Sys Discovered Shut.Caused by Operator Error.Valves Tagged for Identification.Auxiliary Operator Disciplined1983-09-23023 September 1983 Updated LER 83-083/01T-1:on 830905,supply Valve 2-FP-V39 to Deluge Sys of Both Standby Gas Treatment Sys Discovered Shut.Caused by Operator Error.Valves Tagged for Identification.Auxiliary Operator Disciplined 05000325/LER-1983-034, Updated LER 83-034/01T-1:on 830811,following Extended Maint & Refueling Outage,Instrument Isolation Valves to 1CAC-PDS-4222 & 4223 Discovered Closed.Caused by Cancelation of Equipment Clearance.Valves Reopened1983-09-12012 September 1983 Updated LER 83-034/01T-1:on 830811,following Extended Maint & Refueling Outage,Instrument Isolation Valves to 1CAC-PDS-4222 & 4223 Discovered Closed.Caused by Cancelation of Equipment Clearance.Valves Reopened 05000325/LER-1983-017, Updated LER 83-017/03L-1:on 830326-28 & 0402,listed Control Rods Had No Indications for Identified Positions.Caused by Loose Prototypic Inlet Piping Connectors Due to Undervessel Work.Connectors Will Be Properly Fastened1983-07-19019 July 1983 Updated LER 83-017/03L-1:on 830326-28 & 0402,listed Control Rods Had No Indications for Identified Positions.Caused by Loose Prototypic Inlet Piping Connectors Due to Undervessel Work.Connectors Will Be Properly Fastened 05000324/LER-1982-131, Supplemental LER 82-131/03L-1:on 821206,one-half Automatic Reactor Scram Signal Received Due to Instrument Downscale Signal from Main Steam Line Radiation Monitor D, 2-D12-RM-K603D.Caused by Disconnection of Instrument Cable1983-03-11011 March 1983 Supplemental LER 82-131/03L-1:on 821206,one-half Automatic Reactor Scram Signal Received Due to Instrument Downscale Signal from Main Steam Line Radiation Monitor D, 2-D12-RM-K603D.Caused by Disconnection of Instrument Cable 05000324/LER-1981-090, Updated LER 81-090/03L-3:on 810817 & 23,suppression Chamber Water Level Indicator 2-CAC-LI-2601-3 Indicated Lower Level & on 810820,indicated Higher Level than Other Indicator.Caused by Changes in Trickle Flow to Wet Ref Leg1983-01-28028 January 1983 Updated LER 81-090/03L-3:on 810817 & 23,suppression Chamber Water Level Indicator 2-CAC-LI-2601-3 Indicated Lower Level & on 810820,indicated Higher Level than Other Indicator.Caused by Changes in Trickle Flow to Wet Ref Leg 05000325/LER-1982-127, Updated LER 82-127/01T-1:on 821103,quick Start Testing of Diesel Generators 2,3 & 4 Not Performed for 12 H Period Per Tech Spec.Caused by Failure to Enter Requirement Into Daily Surveillance Rept on 821102.Testing Performed1982-12-23023 December 1982 Updated LER 82-127/01T-1:on 821103,quick Start Testing of Diesel Generators 2,3 & 4 Not Performed for 12 H Period Per Tech Spec.Caused by Failure to Enter Requirement Into Daily Surveillance Rept on 821102.Testing Performed 05000325/LER-1982-135, Supplemental LER 82-135/03L-1:on 821019,1.5-inch Discrepancy Noted Between Narrow & Wide Range Instruments.Caused by Inoperable RTGB Level Instruments.Plant Mod Package Developed to Increase Accuracy1982-12-23023 December 1982 Supplemental LER 82-135/03L-1:on 821019,1.5-inch Discrepancy Noted Between Narrow & Wide Range Instruments.Caused by Inoperable RTGB Level Instruments.Plant Mod Package Developed to Increase Accuracy 05000325/LER-1982-024, Supplemental LER 82-024/03L-2:on 820214,during Periodic Test,Discovered That Open Position Indication for Drywell to Suppression Vacuum Breaker X18H Could Not Be Achieved.Caused by Failure of Vacuum Breaker to Fully Stroke Open1982-10-13013 October 1982 Supplemental LER 82-024/03L-2:on 820214,during Periodic Test,Discovered That Open Position Indication for Drywell to Suppression Vacuum Breaker X18H Could Not Be Achieved.Caused by Failure of Vacuum Breaker to Fully Stroke Open ML20054L9761982-06-29029 June 1982 LER82-054/03L-0:on 820607,reactor Core Isolation Cooling Sys Turbine Automatically Started on Reactor Low Level,But Tripped Due to Closure of Control Valve 1-E51-V9.Caused by Lack of Turbine Speed Demand Signal Due to Governor Failure 05000325/LER-1982-0531982-06-29029 June 1982 LER 82-053/03L-0:on 820604,during startup,09 Position Found Superimposed on 00 RTGB Position Indication for Fully Inserted Control Rod 10-07.Caused by Defective Rod Position Reed Switch.Investigation Scheduled for 1982 Outage 05000325/LER-1981-092, Updated LER 81-092/01T-2:on 811226,action Statement 3.3.2b Not Entered When B21-LT-N017D-1 Instrument Failed Upscale. Caused by Failure of Operations Personnel to Recognize & Perform Required Action1982-06-21021 June 1982 Updated LER 81-092/01T-2:on 811226,action Statement 3.3.2b Not Entered When B21-LT-N017D-1 Instrument Failed Upscale. Caused by Failure of Operations Personnel to Recognize & Perform Required Action 05000325/LER-1981-093, Updated LER 81-093/01T-2:on 811226,reactor Protection Sys Vessel Low Level Trip instrument,1-B21-LT-NO17D-1,was Indicating Upscale.Caused by Personnel Failure to Recognize & Perform Tech Specs.Personnel Counseled1982-06-18018 June 1982 Updated LER 81-093/01T-2:on 811226,reactor Protection Sys Vessel Low Level Trip instrument,1-B21-LT-NO17D-1,was Indicating Upscale.Caused by Personnel Failure to Recognize & Perform Tech Specs.Personnel Counseled 05000325/LER-1982-038, Updated LER 82-038/03L-1:on 820419.Reactor Scrammed When Electrical Bus 1A-1 Dc de-energized.Caused by Operator Error in Opening 125-volt Dc Battery Charger Output Breaker for Battery 1A-1.Breaker Closed & Power Restored to Bus1982-06-0404 June 1982 Updated LER 82-038/03L-1:on 820419.Reactor Scrammed When Electrical Bus 1A-1 Dc de-energized.Caused by Operator Error in Opening 125-volt Dc Battery Charger Output Breaker for Battery 1A-1.Breaker Closed & Power Restored to Bus ML20062G3081978-12-21021 December 1978 /03L-0 on 781122:HPCI & RCIC Component Tests Were Overlooked Because Rescheduling Technique Provided No Clear Indication of Test Due Dates.Responsible Technician Reinstructed & Admin Operating Instruction AOI-5 Rev ML20064H8961978-12-19019 December 1978 /03L-0 on 781120:Senior Control Operator Did Not Have Completed Hatch Leak Rate Test Before Beginning Reactor Startup Due to Misunderstanding.Test completed.GP-1 Revised to Require Leak Test Verification by Control Operators ML20064H6181978-12-14014 December 1978 /03L-0 on 781114:torus Level of the HPCI Turbine Control Sys Was Slightly Above the Allowed 27 Inches.Proper Torus Level Restored to Normal.Torus Level Indicator Will Be More Clearly Marked ML20064H5971978-12-14014 December 1978 /03L-0 on 781114:Fire Hoses of Radwaste Bldg 3 Elevation Fire Stations Were Found Missing Due to Use by Personnel for Routine Radwaste Washdown.New Firehoses Installed & Mod Re Alternate Water Supply Is in Progress ML20064H5891978-12-14014 December 1978 /03L-0 on 781114:during Periodic Test 9.3.a the HPCI Egr Actuator Failed to Oper Properly Due to Water in Hydraulic Fluid Corroding Egr Actuator.Steam Leaking Past Seat of Valve HPCI E41-F001 Allowed Water Into Fluid ML20062F6781978-12-13013 December 1978 /03L-0 on 781112:reactor Steam Dome High Pressure Switch B32-PS-N018B Did Not Reset & Would Not Allow RHR Valve E11-F008 to Open for Shutdown Cooling at Reactor Pressure of 102psig.Caused by Sticking micro-switch ML20062F6681978-12-13013 December 1978 /03L-0 on 781117:while Reactor Was in Hot Shutdown Torus Level Increased .2 Above Tech Specs.Caused by Demineralized make-up Water Leakage Through Valves from RHR Keep-fill System Causing Torus Level to Rise ML20064G9301978-12-11011 December 1978 /03L-0 on 781109:Reactor Vessel Chemistry Exceeded Tech Spec Limits for Conductivity & Concentration Due to Presence of Organic Compounds in Condensate Sys.Organic Filtration & High Concentration of Ion Resin Cleanup Begun ML20062E4381978-11-30030 November 1978 /03L-0 on 781101:rod Block Monitor(Rbm) Channel a Was Found Out of Calibr During Testing Due to Setpoint Drift.Calibr Frequency Will Be Increased from Once to Twice Per Year ML20064E8001978-11-15015 November 1978 /03L-0 on 781017:reactor Bldg Radiat Exhaust Monitor D12-RM-N010B Failed Safe Causing Reactor Bldg Vent to Isolate,Due to Defective Transistor 2N1711 on 24V Pwr Supply ML20064E4581978-11-14014 November 1978 /01T-0 on 781101:util Was Informed by NRR of Nonconformance w/10CFR50 Append a Gen Design Criteria 54 & 56.Two Reactor bldg-to-torus Vacuum Breaker Lines Have Never Had Design Review by Nrc.Tech Spec Change Effective 781108 ML20064E3371978-11-0909 November 1978 /03L-0 on 781014:RCIC Turbine Was Tripped on Manual Overspeed for Training Purposes & Turbine control- Stop Valve E51-V8 Would Not Reset.Caused by Improperly Worn Adjusted Reset Lever ML20064E2921978-11-0909 November 1978 /03L-0 on 781011:torus Level Dropped Below Tech Spec Minimum While Water from Torus Was Being Pumped,Via Rgr to Radwaste in Efforts to Reduce Torus Water Level. Caused by Operator Being Distracted ML20064E3541978-11-0707 November 1978 /03L-0 on 781006:condensate Storage Tank Level Switch E41-LS-N003 Found Out of Calibration During Periodic Condensate Storage Tank Low Level Channel.Caused by Instru Drift ML20064E3491978-11-0606 November 1978 /03L-0 on 781105:Control Oper Received Control Rod Drift Alarm for Rod 10-31.When Rod Position Display Was Selected,A False 3 Was Superimposed on Actual Rod Position Due to Aground on the Rpls Probe ML20064D8211978-11-0202 November 1978 /03L-0 on 781004:pressure Switch E11-PS-NO16B Failed During Periods Plci Pump Discharges ADS Permissive Test,Due to Corrosion Buildup on Plunger of Switch ML20064C0151978-10-10010 October 1978 /03L-0 on 780911:during Monthly 1 Diesel Generator Load Test,It Was Found That 1 Cylinder Was Not Firing,Due to Faulty Fuel Pump ML20064C0011978-10-0909 October 1978 /03L-0 on 780911:Snubber SW-142SS164 Found Inoperable During Periodic Test.Caused by Seal Degradation & Resulting Loss of Fluid ML20147C9141978-10-0404 October 1978 /03L-0 on 780904:RCIC Isolation Channel a Tripped Momentarily,Causing RCIC Sys to Be Inoper,Due to Defective RX-2 Relay ML20062A0691978-10-0303 October 1978 /03L-0 on 780904:rod Block Monitor B Inoperative Trip Came on & Stayed on for 1/4 of the Control Rod Selection Matrix.Caused by Failed Integrated Circuit in Rod Block Monitor self-test Circuitry ML20064B7231978-10-0303 October 1978 /03L-0 on 780905:during Periodic Test,Radiat Monitor D12-RM-NO10B HI-HI Trip Point Drifted to Higher than Permitted Level.Monitor Recalibrated.Drift Appears to Be Isolated Incident;No Further Action Taken 1993-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N3271999-10-21021 October 1999 Part 21 Rept Re non-linear Oxygen Readings with Two (2) Model 225 CMA-X Containment Monitoring Sys at Bsep.Caused by High Gain Produced by 10K Resistor Across Second Stage Amplifier.Engineering Drawings Will Be Revised BSEP-99-0168, Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with ML20212D0431999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Brunswick Steam Electric Plant,Units 1 & 2 ML20210P9441999-08-10010 August 1999 Safety Evaluation Accepting Licensee Assessment of Impact on Operation of Plant,Unit 1,with Crack Indications of 2.11, 6.36 & 1.74 Inches in Three Separate Jet Pump Risers ML20210P9181999-08-10010 August 1999 Safety Evaluation Authorizing Request for Reliefs CIP-01,02, 06,07,08,09,10 & 11 (with Certain Exceptions) & 12-18,for Second 10-year ISI Interval.Request CIP-04 & 05 Would Result in hardship,CIP-03 Not Required & CIP-11 Denied in Part ML20210N2341999-08-0505 August 1999 SER Accepting Response to NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issues (USI) A-46 ML20210R1191999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Bsep,Units 1 & 2 ML20210R1311999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Bsep,Unit 2 BSEP-99-0118, Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with BSEP-99-0095, Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20210M8581999-05-14014 May 1999 B214R1 RPV Hydrotest Bolted Connection Corrective Action Evaluation, Rev 0 ML20211L3711999-05-10010 May 1999 Rev 0 to ESR 98-00333, Unit 2 Invessel Feedwater Sparger Evaluation ML20206G1871999-05-0404 May 1999 Safety Evaluation Approving Third 10-year ISI Program Requests for Relief (RR) RR-08,RR-15 & RR-17 BSEP-99-0075, Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With ML20206N1791999-04-23023 April 1999 Rev 0 to 2B21-0554, Brunswick Unit 2,Cycle 14 Colr BSEP-99-0059, Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20205F9031999-03-30030 March 1999 Safety Evaluation Supporting Proposed Rev to BSEP RERP to Licenses DPR-62 & DPR-71,respectively ML20206N1831999-02-28028 February 1999 Rev 0 to Suppl Reload Licensing Rept for Bsep,Unit 2 Reload 13 Cycle 14 BSEP-99-0043, Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20203D7061999-02-0909 February 1999 SER Accepting Proposed Alternatives Contained in Relief Requests PRR-04,VRR-04,VRR-13,PRR-01,PRR-03,VRR-01.VRR-07, VRR-08 & VRR-09 Denied BSEP-99-0005, Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0231, Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0218, Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with BSEP-98-0210, Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired1998-10-30030 October 1998 Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired ML20154P8151998-10-16016 October 1998 SER Accepting Revised Safety Analysis of Operational Transient of 920117,for Plant,Unit 1 ML20154P8591998-10-16016 October 1998 SER Accepting Equivalent Margins Analysis for N-16A/B Instrument Nozzles for Plant,Units 1 & 2 BSEP-98-0202, Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151Y6211998-09-14014 September 1998 BSEP Rept Describing Changes,Tests & Experiments, for Bsep,Units 1 & 2 ML20151Y6371998-09-14014 September 1998 Changes to QA Program, for Bsep,Units 1 & 2 BSEP-98-0185, Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151T5021998-08-0505 August 1998 Project Implementation Plan, Ngg Yr 2000 Readiness Program, Rev 2 BSEP-98-0164, Monthly Operating Repts for July 1998 for BSEP Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for BSEP Units 1 & 2 ML20236T1961998-07-0101 July 1998 Rev 1 to 2B21-0088, Brunswick Unit 2,Cycle 13 Colr ML20236T1921998-07-0101 July 1998 Rev 1 to 1B21-0537, Brunswick Unit 1,Cycle 12 Colr BSEP-98-0142, Monthly Operating Repts for June 1998 for BSEP Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for BSEP Units 1 & 2 ML20236T1971998-06-30030 June 1998 Rev 2 to 24A5412, Supplemental Reload Licensing Rept for Brunswick Steam Electric Plant Unit 2 Reload 12 Cycle 13 ML20249B9691998-06-11011 June 1998 Rev 1 to VC44.F02, Brunswick Steam Electric Plant,Units 1 & 2,ECCS Suction Strainers Replacement Project,Nrc Bulletin 96-003 Final Rept BSEP-98-0129, Monthly Operating Repts for May 1998 for Bsep,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Bsep,Units 1 & 2 ML20151S9041998-05-31031 May 1998 Revised Pages to Monthly Operating Rept for May 1998 for Brunswick Steam Electric Plant,Unit 1 BSEP-98-0104, Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 2 ML20151S8991998-04-30030 April 1998 Revised Pages to Monthly Operating Rept for Apr 1998 for Brunswick Steam Electric Plant,Unit 1 ML20247N7501998-04-30030 April 1998 Rev 0 to BSEP Unit 1,Cycle 12 Colr ML20247N7721998-04-30030 April 1998 Rev 0 to J1103244SRLR, Supplemental Reload Licensing Rept for BSEP Unit 1,Reload 11,Cycle 12 ML20217K8461998-04-24024 April 1998 Safety Evaluation Approving Proposed Use of Code Case N-535 at Brunswick Unit 1 During Second 10-yr Interval,Pursuant to 10CFR50.55a(a)(3)(i).Authorizes Use of Code Case N-535 Until Code Case Included in Future Rev of RG 1.147 ML20217K3941998-04-24024 April 1998 SER Approving Relief Request for Pump Vibration Monitoring, Brunswick Steam Electric Plant,Units 1 & 2 ML20217E6841998-04-23023 April 1998 Safety Evaluation Accepting Code Case N-547, Alternative Exam Requirements for Pressure Retaining Bolting of CRD Housings ML20217E7471998-04-21021 April 1998 Safety Evaluation Accepting Alternative to Insp of Reactor Pressure Vessel Circumferential Welds ML20217B5241998-04-20020 April 1998 SE Accepting Licensee Request for Approval to Use Alternative Exam Requirement for Brunswick,Unit 1,reactor Vessel Stud & Bushing During Second 10-yr ISI Interval Per 10CFR50.55a(a)(3)(ii) BSEP-98-0080, Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 2 ML20216B1041998-03-0404 March 1998 SER Approving Alternative to Insp of Reactor Pressure Vessel Circumferential Welds for Brunswick Steam Electric Plant, Unit 1 1999-09-30
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CD&L e'. m s a m . e , m.,m + _.o 1
Carolina Power a Light Company .
teemmeswomammaawnwa ;
Brunswick Nuclear Plant f P. O. Box 10429 ;
Southport, N.C. 28461-0429- -j August 12, 1993 :
i FILE: B09-13510C 1 0CFR50.73 i I
SERIAL: BSEP-93-0129 i
U.S. Nuclear Regulatory Commission ATTN: Document Control Desk .:
Wasl.ington, D. C-. 20555 BRUNSWICK NUCLEAR' PLANT UNIT 2 f DOCKET'NO. 50-324 >
LICENSE NO. DRP-62 l' SUPPLEMENTAL LICENSEE EVENT REPORT 2-92-010-01 Gentlemen:
i In accordance with Title 10 of the Code of Federal Regulations, the enclosed l Supplemental Licensee Event Report is submitted. The original report fulfilled :
the requirement for a written report within thirty (30) days of a reportable !
occurrence and was submitted in accordance with the format set forth in NUREG-1022, Septenber 1983.
Very truly yours, )
'. M. Brown, Plant Manager - Unit 1 8runswick Nut: lear Plant TMJ/
Enclosure cc: Mr. S. D. Ebneter Mr. P. D. Milano BSEP NRC Resident Office i
I u
l 170037 93081702o4 930812
. DR ADOCK 05000324 /)
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1 NRC FORM 366 U.S. NUCLEAR REGULAVORY COMMISSION APPROt/ED OMB NO. 3150-0104
. (5/92f EXPIRES: 5/31/95 ESTIMATED BURDEN PER HISPONSE TO COMPty WITH THIS d INF0FtM ATION COLL.E CTlDN RE QUE ST: 60.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMutmS REGARoma BURDEN ESTum ,0 THE ,NFORuATiON AND FIECORDS MANAGEMENT BRANCH [MNBB 7714L U.S. NUCLEAR REGUL ATORY COMMISSION, W ASHINGTON, DC 205$6 0D01. AND TO THC F APERWORK REDUCTION PROJECT (3150 c104L OFFICE OF '
MANAGEMINT AND BUDOET, WASHINGTON, DC 20503.
F ACIUTV NAME (1) DOCEET NVMEiER (2) P AGE (3)
Brunswick Steam Electric Plant, Unit 2 '
05000324 1 of 4 TITLE (4l PENETRATION LEAKAGE IN EXCESS OF TECHNICAL SPECIFICATION ALLOWABLE LIMIT DURING LOCAL l LEAK RATE TEST 1hu EVENT DATE (5) LER NUMBER (6) REPORT D ATE (7) OTHER FACILITIES INVOLVED (8) l MONTH DAY VEAR YEAR MONTH DAY YEAR NUVDER NUM bER 05000 12 07 92 92 - 010 - 01 OB 12 93 FACW NAME DOCF ET NVVBER 05000 ,
OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 8: (Check one or rnore of the followingM11) 4 MODE (9) 20.402(bl 20 405tcl 50.731aH2Hivl 73.71(b) )
20.405 taH1 % 50.36(cH1) X 50.73taH2Hvi 73.71 tc)
LEVEL (10) 000 20 405(aH11tM 50 36(cH2) 50.731aH2)fvii) OTHER
- 0 405taH1Hiid so 73(aH2Ha 50.73(aH2HviiiHA) (Specify in Abstract 1 20 405taH1Hrv) 50 73(aH2Hi0 50.73(aH2HvnilfB) and Tert) 20 405taH1Hv1 EO 73faH2Hsd j 50 73talt2Hz) !
I LICENSEE CONTACT FOR THIS LER (12)
NAME TELEFHONE NUMBIR Theresa M. Jones, Regulatory Compliance Specialist (919) 457-2039 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
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CAUSE SYSTEM C OMPONI NT M A NUf ACTURER CAUSE SYSTEM C OMPONE NT M ANUF ACTURE R X SB ISV R344 Y SUPPLEMENTAL REPORT EXPECTED (14) M NTH DAY YtAR EXPECTED SUBMISSION E DATE (15) nf yes r,smoieve E ME CTf D SUBM!sDON CATE)
ABSTRACT (Umst to 1400 spaces, i e. appmximately fifteen single space typewntten knes) (10)
On December 7, 1992, the Unit 2 reactor was shutdown in day 230 of an outage. Local leak rate testing 'LLRT) of tha min steam isolation valves (MSIVs) had been performed. The results of testing indicated that MSIV leakage on main steam line iMSL) D was 54 standard cubic feet per hour (s ef h) , exceeding the technical specification limit of 11.5 scfh.
l MSLs A, B, and C tested satisfactory. It was determined that the Inboard MSIV leakage was caused by an a ct uator- t o- valve alignment problem. The actuator guide tube feet faces (which bolt to the bonnet; were found to have excessive run-out resulting in actuator-to-valve stem misalignment of 0.290 inches. Leakage of the outboard MSIV was caused by a disk-to-seat alignment problem. Inspections revealed that the seat bore and body bore were not concentric and that disk-to-guide clearances were excessive. Bonnet r egister-to-valve clearances were also found Lv be ej.cessi w. The inboard MOIV actuatcr guide tube feet faces were machined flat reducing actuator-to-valve stem misalignment to less than half (0.125) of the as-found readings, The outboard and inhoard MSIV were line-bored to obtain concentricity. On January 27, 1993, post-maintenance testing was performed twice (for repeatability) with satisf actory results (i.e., MSL D leakage measured 4.013 scfh in both tests). Troubleshooting ef f orts were applied in determining the cause of leakage since this was a repeat event for MSL D. The safety significance of this event is considered minimal. Previous similar events involving MSIVs not meeting the technical specification leakage requirements are re;)orted in LERs 1-B8-025 and 2-91-019.
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i NRC FORM 366A U. S. NUCLEAR REGULATORY COMMISSloN APPROVED OMB NO. 3150-0104 (5/92) EXPIRES: 5/31/95 E STIM ATED BURDE N PER RE SPONSE TO COMPLY WITH THIS j INFORMATION COLLECTION REQUEST: . 50.0 HRS. FORWARD UCENSEE EVENT REPORT (LER) COMMEuTS nEcARoiNo Bv4 DEN ESTIMATE To THE iNronMATiON ANo
. TEXT CONTINUATION RECORDS M AN AGEME NT BRANCH IMNBB 7714L U.S. NUCLE AR REGULATORY COMMISSION, W ASHINGTON. DC206500001. AND TO THE PAPERWORK REDUCTION PROJECT (3160-0104), OfTICE OF M AhAGEMf NT AND BUDGET. WASHINGTON, DC 205C3. )
l FACILfTY NAME {11 DOCKET NUMBER (2) LER NUMBER 16) PAGE (3)
Sf QUENTIAL REVISION B swick Steam Electric Plant """"" ""
05000324 2 of 4 92 - 010 - 1 TEXT I!f more space as requireri, use additionalNRC Form 366Nsl (17>
TITLE PENETRATION LEAKAGE IN EXCESS OF TECHNICAL SPECIFICATION ALLOWAELE LIMIT DURING LOCAL LEAK RATE TESTING SUPPLEMENTAL INFORMATION INITIAL OONDITIONS ,
On December 07, 1992, the Unit 2 reactor was shutdown in day 230 of the 1992 outage resulting from structural concerns with the emergency diesel generator building walls.
Local leak rate testing (LLRT) of the main steam isolation valves (MSIVs) had been i performed to satisfy technical specification primary containment leakage rate surveillance l requirements. Technical specifications require that the primary containment leakage rate be limited to less than or equal to 11.5 standard cubic feet per hour (scfh) for any one- i main steam line (MSL) isolation valve when tested at 25 psig.
The MSIVs are Rockwell Model 1612, 24", Y-type globe valves. l F
EVENT NARRATIVE The LLRT is accomplished by draining the MSL, closing the inboard and outboard MSIVs, pressurizing the space between them to 25 psig with air while providing a vent path for any leakage, and measuring the leakage rate. In the event of a leakage rate equal to or greater than I1.5 scfh, the test procedure directs that the associated MSL be filled with ,
water between the reactor vessel and the inboard MSIV to seal any leakage past the inboard l MSIV. The space between the MSiVs is again air pressurized and the leakage rate resulting '
from leakage past the outboard MSIV is measured. This method of testing indicates the total MSL leakage, the leakage associated with the outhcard MSIV and, by substraction, the leakage associated with the inboard MSIV.
On November 29, 1992, leakage testing of MSL D commenced. Testing was initially performed by closing the inboard and outboard MSIVs and attempting to pressurize the space between them; however, test pressure was not obtainable. Subsequent testing, af ter stroking the outboard MSIV, was accomplished by raising reactor vessel level and filling the MSL unti]
a static water head of 25 psig was reached at the inboard MSIV. Leakage past the outboard MSIV was found to be 105 scfh. A retest was performed, af ter draining the water from MSL D and a leakage rate of 159 scfh was obtained. This indicates an inboard MSIV leakage rate Of M ccfh. Therefore. leakege through W L D inhnard and outboard MSIVs was limited to 54 scfh. The inboard and outboard MSIVs were repaired after determining the cause of 1 % r.a ge and, on January 27, 1993, post-maintenance testing was performed twice (for repeatability) with satisfactory results (i .e. , MSL D leakage measured 4.013 scfh in both tests). Troubleshooting efforts were applied in determining the cause of leakage since this was a repeat event for MSL D.
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NRC EORM 366A U. S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104
, (5/92) EXPIRES: 5/31/95 ISTIM ATED BifRDE N PER RE SPONSE TO COMPLY wtTH THl5 (NFORMATION COLLECTION RE QUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COuurNTs REcARn No euRoEN tsTiu*TE TO TwE iNrORu ATiON ANo
. TEXT CONTINUATION RECORos uANacEusNT eRANCH ruses 7714), u.s. NoCLE AR REGOLATORY COMMISS80N. WASHINGTON, DC20555-000), AND TO THE FAPERWORK REDUCTION PROJECT (3150-C104L OFFICE OF MANAGEMENT AND SUDGET, WASHINGTON, DC 20503.
1 FACluTY NAME (1) DOCKET NUMBER (2) tER NUME.ER 16) PAGE (3) !
tiEQUENTIAL REVISION 4 Brunswick Steam Electric Plant "" "#"'"
05000324 3 of-4 Unit 2 92 -- 010 - 1
- TEXT Uf mwe space is required, use additwroalNRC form 366A'st (17) i CAUSE OF EVENT J
MSL D INBOARD MSIV Leakage of the inboard MSIV was caused by an actuator-to-valve alignment problem. This ,
was confirmed during initial cause and ef fect troubleshooting when a satisf actory leakage >
rate was obtained utilizing temporary rigging to correct the misalignment. Thrust measurements were taken and found to be satisfactory with and without actuator to valve misalignment. The actuator guide tube feet faces (which bolt to the bonnet) were found to have run-out readings as much as 0.060 inches on one foot and 0.040 inches on another, {
resulting in a actuater-to-valve stem misalignment of 0.290 inches. Further evidencing j an actuator-to-valve alignment problem were a scored, or galled, valve stem and bonnet l spacer ring. Possibly contributing to the leakage was a disk-to-seat alignment problem i caused by the body bore, seat joint, and seat bore not being concentric. i l
MSL D OUTBOARD MSIV Leakage of the outboard MSIV was caused by a disk-to-seat alignment prcblems. Inspections revealed that the seat bore and body bore were not concentric and that disk-to-guide l clearances were excessive. Bonnet register-to-valve bore clearances were also found to j be excessive. d i
CORRECTIVE ACTICNS MSL D INBOARD MSIV The irboard MSIV actuator guide tube feet Iaces were machined flat reducing actuator-to-valve stem misalignment to less than half (0.125 inches) of the as-found readings.
Additionally, the valve was line bored to achieve concentricity. This was done as a conservative measure even thour.1 the vendor field service representative did not feel valve bore run-out was excessive . Because the valve bore was slightly oversized after line boring, a new oversized disk was required to be installed to maintain proper disk-to-bore and disk-to-guide rib clearances. A new stem and spacer ring was installed.
MSL D OUTBOARD MSIV The outboard MSIV was line-bored to obtain concentricity between the seat bore and body bcre. The disk was oversized to achieve manufacturer recommended clearances between the disk outside diameter and body guides, and weld build-up to the bonnet register was performed to maintain proper clearancca with the new valve bore dimensions.
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l' NRC EORM 366A (3/92)
U. S. NUCLEAR REGULATORY COMMISSION APPROVED OMB No. 3150 0104 ,
l ,, EXPIRES: 5/31/95 i
} ES*lMATED BURDEN PER RESPONSE TO COMPLY WIT H THIS ;
I INFD*1M ATION COLLECTION REQUESTS SD.0 HRS. FORWARD i
LICENSEE EVENT REPORT (LER) CoMMtN1S nloARa,No ,UnoEN Es1,M ATE To rst ,N,onM ATioN ANo >
. TEXT CONTINUATION RECORDS MANAGEMENT BRANCH (MNBB 7714L U.S. NUCLEAR REGULATORY COMMIS$10N. WASHINGTON, DC 20555-D001, AND 10 T HE PAPERWORK Rf DUCTION PROJE CT 0150-01041, OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON. DC 205C3.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) f l
SE QUENTIAL REVISION i l
Brunswick Steam Electric Plant "*"'" * * *'"
Unit 2 05000324 4 of 4 1 92 - 010 - 1 j
TEXT (If rnore space is required, use additional n/RC Forrn 36&A 's! l17) -
i BUTY ASSESSMENT ;
Primary containment integrity ensures that the release of radioactive materials from the ;
containment atmosphere will be restricted to those leakage paths and associated leak rates !
assumed in the accident analyses. This restriction, in conjunction with the leakage rate l limitations, will limit the site boundary radiation doses to within the litnits of 10CFR100 during accident conditions. Technical specifications require that primary containment !
leakage rates be limited to less than or equal to 11.5 scfh for any one MSL isolation valve I
tested at 25 psig. '
The safety significance of this event is considered minimal. Although the technical ,
specification limits were exceeded, a MSL leakage rate of 54 scfh would have not resulted t in the 10CFR100 off-site dose limits being exceeded during a design basis accident. This ;
assessment is based upon dose calculations recently completed for Brunswick Units 1 and !
2 by General Electric (GE letter OG-91-1063-09, dated Decenter 17, 1991) , using the Boiling t Water Reactor Owners Group (Bh70G) methodology at 100 scfh per steam line.
PREVIOUS SIMILAR EVENTS Past f ailures of MSIVs to meet the TS required 11.5 scfh leakage requirements were reported in LERs 1-88-025 and 2-91-019. LER 1-88-025 involved the outboard MSIV on two separate !
l MSLs. On November 12, 1991, LER 2-91-019 reported the failure of both MSLs C and D. The }
l associated MSIVs were repaired and the unit was. returned to service in January,1992 until l April 21, 1992, when it was shutdown for an outage.
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ETIS COMPONENT IDENTIFICATION l
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l System / Component ETIS Cod 2 l
l MSIv Ss/ISV l I
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