|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000324/LER-1992-001, Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled1993-09-0202 September 1993 Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled 05000324/LER-1993-0081993-08-13013 August 1993 LER 93-008-00:on 930714,core Rated Thermal Power Exceeded Allowable Amount Due to Feedwater Flow Inaccuracy.Cause Believed to Be Due to Erosion/Corrosion of FW Flow Elements. FW Instrumentation recalibr.W/930812 Ltr 05000324/LER-1992-0101993-08-12012 August 1993 LER 92-010-01:on 921207,penetration Leakage Exceeded TS Allowable Limit Due to actuator-to-valve Alignment & disk-to-seat Alignment Problems.Line Bored Valve to Achieve concentricity.W/930812 Ltr 05000324/LER-1991-0191993-08-12012 August 1993 LER 91-019-01:on 911112,LLRT Failure of Two MSL Inboard & Outboard Isolation Valves Resulted in Condition Outside Design Basis.Root Cause Analysis in Process.Msls C & D Inboard & Outboard MSIVs Repairs complete.W/930812 Ltr 05000324/LER-1993-0031993-05-10010 May 1993 LER 93-003-00:on 930408,identified That Drywell Spray Outboard Isolation Valve Installed in Reverse Direction. Caused by Design & Installation Error.Appropriate Documents Will Be revised.W/930507 Ltr 05000324/LER-1988-0011990-08-0101 August 1990 LER 88-001-07:on 880102,manual Reactor Scram Occurred Due to Decreasing Main Condenser Vacuum.Reactor Power at 55% & Vacuum Decreased to 22 Inches Mercury.Caused by Leaks on Main Turbine Piping.Piping repaired.W/900801 Ltr 05000324/LER-1983-019, Updated LER 83-019/01T-2:on 830210,instrument Air Tubing to Safety Relief Valve/Automatic Depressurization Sys Valve Accumulator Inadequately Supported.Caused by Rerouted Tubing.Supports Installed1984-07-12012 July 1984 Updated LER 83-019/01T-2:on 830210,instrument Air Tubing to Safety Relief Valve/Automatic Depressurization Sys Valve Accumulator Inadequately Supported.Caused by Rerouted Tubing.Supports Installed 05000325/LER-1982-108, Updated LER 82-108/03L-1:on 821010 & 14,while Performing Automatic Depressurization Sys Valve Operability Test,Valves 1-B21-F013J & 1-B21-F013D & E Failed to Reclose.Caused by Faulty Spring.Valves Replaced1984-05-18018 May 1984 Updated LER 82-108/03L-1:on 821010 & 14,while Performing Automatic Depressurization Sys Valve Operability Test,Valves 1-B21-F013J & 1-B21-F013D & E Failed to Reclose.Caused by Faulty Spring.Valves Replaced 05000325/LER-1982-122, Supplemental LER 82-122/03L-1:on 821030 & 1104,reactor Recirculation Pump 1A Tripped.On 821101 & 04,reactor Recirculation Pump 1B Tripped.Caused by Spurious Action of ATWS Instrument B21-PS-N045C1984-04-0909 April 1984 Supplemental LER 82-122/03L-1:on 821030 & 1104,reactor Recirculation Pump 1A Tripped.On 821101 & 04,reactor Recirculation Pump 1B Tripped.Caused by Spurious Action of ATWS Instrument B21-PS-N045C 05000325/LER-1981-053, Updated LER 81-053/03L-1:on 810922,during Reactor Startup, Reactor Recirculation Pump 1B Tripped.Caused by Spurious Trip Signal from ATWS Low Water Level Instrument B21-LTM- NO24B-2.Instrument replaced.W/840329 Ltr1984-03-29029 March 1984 Updated LER 81-053/03L-1:on 810922,during Reactor Startup, Reactor Recirculation Pump 1B Tripped.Caused by Spurious Trip Signal from ATWS Low Water Level Instrument B21-LTM- NO24B-2.Instrument replaced.W/840329 Ltr 05000325/LER-1981-055, Updated LER 81-055/03L-1:on 820622,drywell Equipment Drain Flow Integrator 1-G16-FQ-K603 Continuously Indicated Dwed Sump Flow W/No Pumps Running.Caused by Water Being Introduced Into Pneumatic calibrator.W/840328 Ltr1984-03-28028 March 1984 Updated LER 81-055/03L-1:on 820622,drywell Equipment Drain Flow Integrator 1-G16-FQ-K603 Continuously Indicated Dwed Sump Flow W/No Pumps Running.Caused by Water Being Introduced Into Pneumatic calibrator.W/840328 Ltr 05000325/LER-1983-063, Updated LER 83-063/03L-1:on 831203,reactor Water Cleanup Sys (Rwcs) Differential Flow Indicator 1-G31-R615 Showed Erroneous Indication.On 831207,spurious Rwcs Alarm Annunciated.Caused by Air in Sensing lines.W/840222 Ltr1984-02-22022 February 1984 Updated LER 83-063/03L-1:on 831203,reactor Water Cleanup Sys (Rwcs) Differential Flow Indicator 1-G31-R615 Showed Erroneous Indication.On 831207,spurious Rwcs Alarm Annunciated.Caused by Air in Sensing lines.W/840222 Ltr 05000325/LER-1983-057, Updated LER 83-057/03L-1:on 831119,during Unit Power Performance,Temp Recorder TR-1258 Printed Erratically.Caused by Dirty Electrical Contacts in Control Board Timing Relay. Contacts Cleaned & Returned to svc.W/840222 Ltr1984-02-22022 February 1984 Updated LER 83-057/03L-1:on 831119,during Unit Power Performance,Temp Recorder TR-1258 Printed Erratically.Caused by Dirty Electrical Contacts in Control Board Timing Relay. Contacts Cleaned & Returned to svc.W/840222 Ltr 05000324/LER-1983-097, Updated LER 83-097/01T-1:on 831212,during Testing,Per IE Bulletin 83-02,crack Indications Discovered in 19 of 131 Welds in Reactor Recirculation & Reactor Water Cleanup Sys. Caused by Stress Corrosion Cracking1984-01-24024 January 1984 Updated LER 83-097/01T-1:on 831212,during Testing,Per IE Bulletin 83-02,crack Indications Discovered in 19 of 131 Welds in Reactor Recirculation & Reactor Water Cleanup Sys. Caused by Stress Corrosion Cracking 05000325/LER-1983-045, Updated LER 83-045/03L-2:on 830919 & 24,inboard PCIV Steam Supply Valve ES1-F007 to RCIC Sys Would Not Completely Reopen.Caused by Loose Limitorque Motor Operator Spring Pack1984-01-24024 January 1984 Updated LER 83-045/03L-2:on 830919 & 24,inboard PCIV Steam Supply Valve ES1-F007 to RCIC Sys Would Not Completely Reopen.Caused by Loose Limitorque Motor Operator Spring Pack 05000324/LER-1982-024, Updated LER 82-024/01T-1:on 820205,determined That Control Bldg Emergency Ventilation Sys Trains Will Not Isolate Upon Receipt of Chlorine Isolation Signal If Control Switch in on Position Due to Design Deficiency1983-11-14014 November 1983 Updated LER 82-024/01T-1:on 820205,determined That Control Bldg Emergency Ventilation Sys Trains Will Not Isolate Upon Receipt of Chlorine Isolation Signal If Control Switch in on Position Due to Design Deficiency 05000324/LER-1983-083, Updated LER 83-083/01T-1:on 830905,supply Valve 2-FP-V39 to Deluge Sys of Both Standby Gas Treatment Sys Discovered Shut.Caused by Operator Error.Valves Tagged for Identification.Auxiliary Operator Disciplined1983-09-23023 September 1983 Updated LER 83-083/01T-1:on 830905,supply Valve 2-FP-V39 to Deluge Sys of Both Standby Gas Treatment Sys Discovered Shut.Caused by Operator Error.Valves Tagged for Identification.Auxiliary Operator Disciplined 05000325/LER-1983-034, Updated LER 83-034/01T-1:on 830811,following Extended Maint & Refueling Outage,Instrument Isolation Valves to 1CAC-PDS-4222 & 4223 Discovered Closed.Caused by Cancelation of Equipment Clearance.Valves Reopened1983-09-12012 September 1983 Updated LER 83-034/01T-1:on 830811,following Extended Maint & Refueling Outage,Instrument Isolation Valves to 1CAC-PDS-4222 & 4223 Discovered Closed.Caused by Cancelation of Equipment Clearance.Valves Reopened 05000325/LER-1983-017, Updated LER 83-017/03L-1:on 830326-28 & 0402,listed Control Rods Had No Indications for Identified Positions.Caused by Loose Prototypic Inlet Piping Connectors Due to Undervessel Work.Connectors Will Be Properly Fastened1983-07-19019 July 1983 Updated LER 83-017/03L-1:on 830326-28 & 0402,listed Control Rods Had No Indications for Identified Positions.Caused by Loose Prototypic Inlet Piping Connectors Due to Undervessel Work.Connectors Will Be Properly Fastened 05000324/LER-1982-131, Supplemental LER 82-131/03L-1:on 821206,one-half Automatic Reactor Scram Signal Received Due to Instrument Downscale Signal from Main Steam Line Radiation Monitor D, 2-D12-RM-K603D.Caused by Disconnection of Instrument Cable1983-03-11011 March 1983 Supplemental LER 82-131/03L-1:on 821206,one-half Automatic Reactor Scram Signal Received Due to Instrument Downscale Signal from Main Steam Line Radiation Monitor D, 2-D12-RM-K603D.Caused by Disconnection of Instrument Cable 05000324/LER-1981-090, Updated LER 81-090/03L-3:on 810817 & 23,suppression Chamber Water Level Indicator 2-CAC-LI-2601-3 Indicated Lower Level & on 810820,indicated Higher Level than Other Indicator.Caused by Changes in Trickle Flow to Wet Ref Leg1983-01-28028 January 1983 Updated LER 81-090/03L-3:on 810817 & 23,suppression Chamber Water Level Indicator 2-CAC-LI-2601-3 Indicated Lower Level & on 810820,indicated Higher Level than Other Indicator.Caused by Changes in Trickle Flow to Wet Ref Leg 05000325/LER-1982-127, Updated LER 82-127/01T-1:on 821103,quick Start Testing of Diesel Generators 2,3 & 4 Not Performed for 12 H Period Per Tech Spec.Caused by Failure to Enter Requirement Into Daily Surveillance Rept on 821102.Testing Performed1982-12-23023 December 1982 Updated LER 82-127/01T-1:on 821103,quick Start Testing of Diesel Generators 2,3 & 4 Not Performed for 12 H Period Per Tech Spec.Caused by Failure to Enter Requirement Into Daily Surveillance Rept on 821102.Testing Performed 05000325/LER-1982-135, Supplemental LER 82-135/03L-1:on 821019,1.5-inch Discrepancy Noted Between Narrow & Wide Range Instruments.Caused by Inoperable RTGB Level Instruments.Plant Mod Package Developed to Increase Accuracy1982-12-23023 December 1982 Supplemental LER 82-135/03L-1:on 821019,1.5-inch Discrepancy Noted Between Narrow & Wide Range Instruments.Caused by Inoperable RTGB Level Instruments.Plant Mod Package Developed to Increase Accuracy 05000325/LER-1982-024, Supplemental LER 82-024/03L-2:on 820214,during Periodic Test,Discovered That Open Position Indication for Drywell to Suppression Vacuum Breaker X18H Could Not Be Achieved.Caused by Failure of Vacuum Breaker to Fully Stroke Open1982-10-13013 October 1982 Supplemental LER 82-024/03L-2:on 820214,during Periodic Test,Discovered That Open Position Indication for Drywell to Suppression Vacuum Breaker X18H Could Not Be Achieved.Caused by Failure of Vacuum Breaker to Fully Stroke Open ML20054L9761982-06-29029 June 1982 LER82-054/03L-0:on 820607,reactor Core Isolation Cooling Sys Turbine Automatically Started on Reactor Low Level,But Tripped Due to Closure of Control Valve 1-E51-V9.Caused by Lack of Turbine Speed Demand Signal Due to Governor Failure 05000325/LER-1982-0531982-06-29029 June 1982 LER 82-053/03L-0:on 820604,during startup,09 Position Found Superimposed on 00 RTGB Position Indication for Fully Inserted Control Rod 10-07.Caused by Defective Rod Position Reed Switch.Investigation Scheduled for 1982 Outage 05000325/LER-1981-092, Updated LER 81-092/01T-2:on 811226,action Statement 3.3.2b Not Entered When B21-LT-N017D-1 Instrument Failed Upscale. Caused by Failure of Operations Personnel to Recognize & Perform Required Action1982-06-21021 June 1982 Updated LER 81-092/01T-2:on 811226,action Statement 3.3.2b Not Entered When B21-LT-N017D-1 Instrument Failed Upscale. Caused by Failure of Operations Personnel to Recognize & Perform Required Action 05000325/LER-1981-093, Updated LER 81-093/01T-2:on 811226,reactor Protection Sys Vessel Low Level Trip instrument,1-B21-LT-NO17D-1,was Indicating Upscale.Caused by Personnel Failure to Recognize & Perform Tech Specs.Personnel Counseled1982-06-18018 June 1982 Updated LER 81-093/01T-2:on 811226,reactor Protection Sys Vessel Low Level Trip instrument,1-B21-LT-NO17D-1,was Indicating Upscale.Caused by Personnel Failure to Recognize & Perform Tech Specs.Personnel Counseled 05000325/LER-1982-038, Updated LER 82-038/03L-1:on 820419.Reactor Scrammed When Electrical Bus 1A-1 Dc de-energized.Caused by Operator Error in Opening 125-volt Dc Battery Charger Output Breaker for Battery 1A-1.Breaker Closed & Power Restored to Bus1982-06-0404 June 1982 Updated LER 82-038/03L-1:on 820419.Reactor Scrammed When Electrical Bus 1A-1 Dc de-energized.Caused by Operator Error in Opening 125-volt Dc Battery Charger Output Breaker for Battery 1A-1.Breaker Closed & Power Restored to Bus ML20062G3081978-12-21021 December 1978 /03L-0 on 781122:HPCI & RCIC Component Tests Were Overlooked Because Rescheduling Technique Provided No Clear Indication of Test Due Dates.Responsible Technician Reinstructed & Admin Operating Instruction AOI-5 Rev ML20064H8961978-12-19019 December 1978 /03L-0 on 781120:Senior Control Operator Did Not Have Completed Hatch Leak Rate Test Before Beginning Reactor Startup Due to Misunderstanding.Test completed.GP-1 Revised to Require Leak Test Verification by Control Operators ML20064H6181978-12-14014 December 1978 /03L-0 on 781114:torus Level of the HPCI Turbine Control Sys Was Slightly Above the Allowed 27 Inches.Proper Torus Level Restored to Normal.Torus Level Indicator Will Be More Clearly Marked ML20064H5971978-12-14014 December 1978 /03L-0 on 781114:Fire Hoses of Radwaste Bldg 3 Elevation Fire Stations Were Found Missing Due to Use by Personnel for Routine Radwaste Washdown.New Firehoses Installed & Mod Re Alternate Water Supply Is in Progress ML20064H5891978-12-14014 December 1978 /03L-0 on 781114:during Periodic Test 9.3.a the HPCI Egr Actuator Failed to Oper Properly Due to Water in Hydraulic Fluid Corroding Egr Actuator.Steam Leaking Past Seat of Valve HPCI E41-F001 Allowed Water Into Fluid ML20062F6781978-12-13013 December 1978 /03L-0 on 781112:reactor Steam Dome High Pressure Switch B32-PS-N018B Did Not Reset & Would Not Allow RHR Valve E11-F008 to Open for Shutdown Cooling at Reactor Pressure of 102psig.Caused by Sticking micro-switch ML20062F6681978-12-13013 December 1978 /03L-0 on 781117:while Reactor Was in Hot Shutdown Torus Level Increased .2 Above Tech Specs.Caused by Demineralized make-up Water Leakage Through Valves from RHR Keep-fill System Causing Torus Level to Rise ML20064G9301978-12-11011 December 1978 /03L-0 on 781109:Reactor Vessel Chemistry Exceeded Tech Spec Limits for Conductivity & Concentration Due to Presence of Organic Compounds in Condensate Sys.Organic Filtration & High Concentration of Ion Resin Cleanup Begun ML20062E4381978-11-30030 November 1978 /03L-0 on 781101:rod Block Monitor(Rbm) Channel a Was Found Out of Calibr During Testing Due to Setpoint Drift.Calibr Frequency Will Be Increased from Once to Twice Per Year ML20064E8001978-11-15015 November 1978 /03L-0 on 781017:reactor Bldg Radiat Exhaust Monitor D12-RM-N010B Failed Safe Causing Reactor Bldg Vent to Isolate,Due to Defective Transistor 2N1711 on 24V Pwr Supply ML20064E4581978-11-14014 November 1978 /01T-0 on 781101:util Was Informed by NRR of Nonconformance w/10CFR50 Append a Gen Design Criteria 54 & 56.Two Reactor bldg-to-torus Vacuum Breaker Lines Have Never Had Design Review by Nrc.Tech Spec Change Effective 781108 ML20064E3371978-11-0909 November 1978 /03L-0 on 781014:RCIC Turbine Was Tripped on Manual Overspeed for Training Purposes & Turbine control- Stop Valve E51-V8 Would Not Reset.Caused by Improperly Worn Adjusted Reset Lever ML20064E2921978-11-0909 November 1978 /03L-0 on 781011:torus Level Dropped Below Tech Spec Minimum While Water from Torus Was Being Pumped,Via Rgr to Radwaste in Efforts to Reduce Torus Water Level. Caused by Operator Being Distracted ML20064E3541978-11-0707 November 1978 /03L-0 on 781006:condensate Storage Tank Level Switch E41-LS-N003 Found Out of Calibration During Periodic Condensate Storage Tank Low Level Channel.Caused by Instru Drift ML20064E3491978-11-0606 November 1978 /03L-0 on 781105:Control Oper Received Control Rod Drift Alarm for Rod 10-31.When Rod Position Display Was Selected,A False 3 Was Superimposed on Actual Rod Position Due to Aground on the Rpls Probe ML20064D8211978-11-0202 November 1978 /03L-0 on 781004:pressure Switch E11-PS-NO16B Failed During Periods Plci Pump Discharges ADS Permissive Test,Due to Corrosion Buildup on Plunger of Switch ML20064C0151978-10-10010 October 1978 /03L-0 on 780911:during Monthly 1 Diesel Generator Load Test,It Was Found That 1 Cylinder Was Not Firing,Due to Faulty Fuel Pump ML20064C0011978-10-0909 October 1978 /03L-0 on 780911:Snubber SW-142SS164 Found Inoperable During Periodic Test.Caused by Seal Degradation & Resulting Loss of Fluid ML20147C9141978-10-0404 October 1978 /03L-0 on 780904:RCIC Isolation Channel a Tripped Momentarily,Causing RCIC Sys to Be Inoper,Due to Defective RX-2 Relay ML20062A0691978-10-0303 October 1978 /03L-0 on 780904:rod Block Monitor B Inoperative Trip Came on & Stayed on for 1/4 of the Control Rod Selection Matrix.Caused by Failed Integrated Circuit in Rod Block Monitor self-test Circuitry ML20064B7231978-10-0303 October 1978 /03L-0 on 780905:during Periodic Test,Radiat Monitor D12-RM-NO10B HI-HI Trip Point Drifted to Higher than Permitted Level.Monitor Recalibrated.Drift Appears to Be Isolated Incident;No Further Action Taken 1993-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N3271999-10-21021 October 1999 Part 21 Rept Re non-linear Oxygen Readings with Two (2) Model 225 CMA-X Containment Monitoring Sys at Bsep.Caused by High Gain Produced by 10K Resistor Across Second Stage Amplifier.Engineering Drawings Will Be Revised BSEP-99-0168, Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with ML20212D0431999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Brunswick Steam Electric Plant,Units 1 & 2 ML20210P9441999-08-10010 August 1999 Safety Evaluation Accepting Licensee Assessment of Impact on Operation of Plant,Unit 1,with Crack Indications of 2.11, 6.36 & 1.74 Inches in Three Separate Jet Pump Risers ML20210P9181999-08-10010 August 1999 Safety Evaluation Authorizing Request for Reliefs CIP-01,02, 06,07,08,09,10 & 11 (with Certain Exceptions) & 12-18,for Second 10-year ISI Interval.Request CIP-04 & 05 Would Result in hardship,CIP-03 Not Required & CIP-11 Denied in Part ML20210N2341999-08-0505 August 1999 SER Accepting Response to NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issues (USI) A-46 ML20210R1191999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Bsep,Units 1 & 2 ML20210R1311999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Bsep,Unit 2 BSEP-99-0118, Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with BSEP-99-0095, Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20210M8581999-05-14014 May 1999 B214R1 RPV Hydrotest Bolted Connection Corrective Action Evaluation, Rev 0 ML20211L3711999-05-10010 May 1999 Rev 0 to ESR 98-00333, Unit 2 Invessel Feedwater Sparger Evaluation ML20206G1871999-05-0404 May 1999 Safety Evaluation Approving Third 10-year ISI Program Requests for Relief (RR) RR-08,RR-15 & RR-17 BSEP-99-0075, Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With ML20206N1791999-04-23023 April 1999 Rev 0 to 2B21-0554, Brunswick Unit 2,Cycle 14 Colr BSEP-99-0059, Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20205F9031999-03-30030 March 1999 Safety Evaluation Supporting Proposed Rev to BSEP RERP to Licenses DPR-62 & DPR-71,respectively ML20206N1831999-02-28028 February 1999 Rev 0 to Suppl Reload Licensing Rept for Bsep,Unit 2 Reload 13 Cycle 14 BSEP-99-0043, Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20203D7061999-02-0909 February 1999 SER Accepting Proposed Alternatives Contained in Relief Requests PRR-04,VRR-04,VRR-13,PRR-01,PRR-03,VRR-01.VRR-07, VRR-08 & VRR-09 Denied BSEP-99-0005, Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0231, Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0218, Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with BSEP-98-0210, Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired1998-10-30030 October 1998 Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired ML20154P8151998-10-16016 October 1998 SER Accepting Revised Safety Analysis of Operational Transient of 920117,for Plant,Unit 1 ML20154P8591998-10-16016 October 1998 SER Accepting Equivalent Margins Analysis for N-16A/B Instrument Nozzles for Plant,Units 1 & 2 BSEP-98-0202, Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151Y6211998-09-14014 September 1998 BSEP Rept Describing Changes,Tests & Experiments, for Bsep,Units 1 & 2 ML20151Y6371998-09-14014 September 1998 Changes to QA Program, for Bsep,Units 1 & 2 BSEP-98-0185, Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151T5021998-08-0505 August 1998 Project Implementation Plan, Ngg Yr 2000 Readiness Program, Rev 2 BSEP-98-0164, Monthly Operating Repts for July 1998 for BSEP Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for BSEP Units 1 & 2 ML20236T1961998-07-0101 July 1998 Rev 1 to 2B21-0088, Brunswick Unit 2,Cycle 13 Colr ML20236T1921998-07-0101 July 1998 Rev 1 to 1B21-0537, Brunswick Unit 1,Cycle 12 Colr BSEP-98-0142, Monthly Operating Repts for June 1998 for BSEP Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for BSEP Units 1 & 2 ML20236T1971998-06-30030 June 1998 Rev 2 to 24A5412, Supplemental Reload Licensing Rept for Brunswick Steam Electric Plant Unit 2 Reload 12 Cycle 13 ML20249B9691998-06-11011 June 1998 Rev 1 to VC44.F02, Brunswick Steam Electric Plant,Units 1 & 2,ECCS Suction Strainers Replacement Project,Nrc Bulletin 96-003 Final Rept BSEP-98-0129, Monthly Operating Repts for May 1998 for Bsep,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Bsep,Units 1 & 2 ML20151S9041998-05-31031 May 1998 Revised Pages to Monthly Operating Rept for May 1998 for Brunswick Steam Electric Plant,Unit 1 BSEP-98-0104, Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 2 ML20151S8991998-04-30030 April 1998 Revised Pages to Monthly Operating Rept for Apr 1998 for Brunswick Steam Electric Plant,Unit 1 ML20247N7501998-04-30030 April 1998 Rev 0 to BSEP Unit 1,Cycle 12 Colr ML20247N7721998-04-30030 April 1998 Rev 0 to J1103244SRLR, Supplemental Reload Licensing Rept for BSEP Unit 1,Reload 11,Cycle 12 ML20217K8461998-04-24024 April 1998 Safety Evaluation Approving Proposed Use of Code Case N-535 at Brunswick Unit 1 During Second 10-yr Interval,Pursuant to 10CFR50.55a(a)(3)(i).Authorizes Use of Code Case N-535 Until Code Case Included in Future Rev of RG 1.147 ML20217K3941998-04-24024 April 1998 SER Approving Relief Request for Pump Vibration Monitoring, Brunswick Steam Electric Plant,Units 1 & 2 ML20217E6841998-04-23023 April 1998 Safety Evaluation Accepting Code Case N-547, Alternative Exam Requirements for Pressure Retaining Bolting of CRD Housings ML20217E7471998-04-21021 April 1998 Safety Evaluation Accepting Alternative to Insp of Reactor Pressure Vessel Circumferential Welds ML20217B5241998-04-20020 April 1998 SE Accepting Licensee Request for Approval to Use Alternative Exam Requirement for Brunswick,Unit 1,reactor Vessel Stud & Bushing During Second 10-yr ISI Interval Per 10CFR50.55a(a)(3)(ii) BSEP-98-0080, Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 2 ML20216B1041998-03-0404 March 1998 SER Approving Alternative to Insp of Reactor Pressure Vessel Circumferential Welds for Brunswick Steam Electric Plant, Unit 1 1999-09-30
[Table view] |
LER-2091-019, |
Event date: |
|
---|
Report date: |
|
---|
3242091019R00 - NRC Website |
|
text
. , . ,?)
-i gy .- symm- m ;
Carolina Power & Light Company
- E;acntrariawamimmante Brunswick Nuclear Plant P. O. Box 10429 Southport, N.C. 28461-0429 August 12, 1993 FILE: B09-13510C 10CFR50.73 SERIAL: BSEP-93-0128 i
U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 i
BRUNSWICK NUCLEAR PLANT UNIT 2 ,
DOCKET NO. 50-324 LICENSE NO. DRP-62 SUPPLEMENTAL LICENSEE EVENT REPORT 2-91-019-01 Gentlemen: Y In accordance with Title 10 of the Code of Federal Regulations, the enclosed -l '
Supplemental Licensee Event Report is submitted. The original report fulfilled the requirement for a written report within thirty (30) days of a reportable occurrence and was submitted in accordance with the format set forth in NUREG-1022, Septenber 1983.
Very truly yours, ,
M Wm ;
M. Brown, Plant Manager - Unit 1 )
Brunswick Nuclear Plant l l
TMJ/ ,
a Enclosure l cc: Mr. S. D. Ebneter Mr. P. D. Milano BSEP NRC Resident Office _]
l I
i 170038 .
9308170190 DR 930812
A
NRC FORM Y6 U S NUCLEAR REGULATORY COMM$SION APPROVED OMB NO 315D-0104
- EXPIRES 4/3^#92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH TH!$ INFORMATION COLLECTION REQUEST. 50 0 HRS FORWARD COMMENTS REGARDING BUR EN ESMME T THE RECORDS AND REPORTS MANAGEMENT BRANCH LICENSEE EVENT REPORT (LER) (P-630) U S NUCf. EAR REGUt ATORY COMM!SSiON, WASHINGTON, DC 20555, AND TO THE PAPERVN i:iEDUCTICN PROJECT (3150 01G4). OFFICE oF MANAGE' MENT AND BUDGET. WASHINGTON. DC 23503 F ACILITY NAME (1) Brunswick Steam Electric Plant D@C NUMMR Q PAGE (3)
Unit 2 05000324 1
mLE f4i LLRT Failure of Two Main Steam Lines' Inboard and Outboard Isolation Valves Resulting in a Condition Outside the Plant Design Basis.
EVE NT DATF (E) LER NUMBER 46) REPORT DATE (7) CTHER FACluTIES INVOLVED 19)
MONTH DAY YEAR VF AR SEQ REV NQ MONTH DAY YEAR FACILITV NAME DOCKET NUMBER NO 11 12 91 91 -
019 -
01 08 12 93 THis REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR g (Check one or mme of the followmg) (11)
OPfliATfNG MODE (9) S 20 do2?tu 20 doHci 50 73talmim) 73 71(el b
POWC R 20 4h(1gi) 50 36(n)(1) g 50 73(a) A(v) 73 71(c) }
ttvEt (10j ooo 20 4%@M SD 36(c)Q SO 73(a)Q(vu) OTHER (Specify m Abstract and Tert) 20 415[an1)(m) 50 73tajmp) $0 73(alm (vmHA)
/
20 43$(a)(1)(w) y SC 73(sjm(n) 50 73(a)Atvm)(B)
?O 4DStan(inv) 50 73(ejf2)(ni) 50 73(almb)
UCENSEE CONTACT FOR THIS LER (12)
MME Theresa M. Jones, Regulatory Compliance Specialist TELEPHONE NUMBER (919) 457-2039 COMPLETE ONE LINE FOR EACH COMPONENT F AILURE DESCRIBED IN THis REPORT (13)
GAUM SY ST EM COMPONENT MANurACTURER REPORTABLE CAUSE EYSTEM COMPONENT MANUFACTURER REPORTABLE +
TO NPRDS TO NPRDS X SB ISV R344 Y SUPPLEMENTAL PEPORT EXPECTED (14) EXPECTED MONTH DAY YEAR SUBMISSION YES pf yas cuee E@LCTED SubMtS$10N DATE)
NO DATE !
X (15) l l
ABSTRACT {Le to 1470 wees i e awmommer feean w@e um typwen imey (16) l On November 12, 1991, the Unit 2 reactor was shutdown in refuel / maintenance outage. i Local leak rate testing (LLRT) of the main steam isolation _ valves (MSIVs) had been performed. The results of testing indicated that MSIV leakage on main steam lines l (MSLs) C and D had exceeded the Technical Specification (TS) limit of 11.5 standard cubic feet per hour (scfh), but the actual amount of leakage could not be determined. MSL C outboard MSIV leakage was caused by an indication across the in-body seat. It is believed the indication resulted from the disk closing on a piece of metal that had spalled off the body bore during a previous closure. MSL C inboard MSIV leakage resulted from poor disk to in-body seat contact caused by low spots. Low spots are generally the result of in-body seat deformation from thennal expansion and contraction. It was believed that MSL D outboard MSIV leakage resulted from the disk not seating completely against the in-body seat. The disk outside diameter was contacting a raised lip (tooling mark) on the in-body seat surface. It was believed that low spots also caused leakage of the MSL D inboard valve. MSLs C and D MSIVs repairs were completed and a repeat of the testing revealed zero leakage in both MSLs (ies MSL C = 0.173 scfh and MSL D = 0.266 scfh) .
This event is considered potentially safety significant based on the inability to determine the amount of leakage. A previous failure of two MSIVs to meet the TS required 11.5 scfh leakage requirement has been reported in LER 1* SS-025, That LER involved the outboard MSIV on two separate MSLs. On December 7, 1932, the results 1 of testing indicated that MSIV leakage on MSL D had again exceeded Technical l Specification limits (LER 2-92-010).
~
NRC FORM Sf4A U S NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150 0100
' EXP!RES: 630/02 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INWRMAN CMECM REWESt M O HRS FORWARD COMEMS LICENSEE EVENT REPORT (LER) REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS TEXT CONTINUATION MANAGEEM WNCH F53% U S NUCLEAR REGULATORY COMMISStON, WASHINGTON, DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104L OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC 20 sos IActuTV NAME (1) DOCKET NUMBER c) LER NUMBER (0) PAGE (3)
Brunswick Steam Electric Plant 05000324 vEAR SEQ REV 2 Unit 2 NO. NO 91 019 01 TExr e mm. .p.c. . r.92n.a us. .Hhonal NRC Form 3fMiA s) (17)
Title:
LLRT Failure of Two Main Steam Lines' Inboard and Outboard Isolation Valves Reeultina in a Condition Outside the Plant Desion Basis.
INITIAL CONDITIONS On Novenber 12, 1991, the Unit 2 reactor was shutdown in day 62 of the 1991 refuel / maintenance outage. Local leak rate testing (LLRT) of the main steam isolation valves (MSIVs) had been performed to satisfy technical specification (TS) primary containment leakage rate surveillance requirements. The referenced TS requires that the primary containment leakage rate be limited to less than or equal to 11.5 standard cubic feet per hour (scfh) for any one main steam line (MSL) isolation valve when tested at 25 psig.
EVENT NARRATIVE The ref erenced testing is accomplished by draining the MSL, closing the inboard and outboard MSIVs, prcasurizing the space between them to 25 psig with air while providing a vent path for any leakage, and measuring the leakage rate. In the event of a leakage rate equal to or-greater than 11.5 scfh the test procedure directs that the associated MSL be filled with water between the reactor vessel and the inboard MSIV to seal any leakage past the inboard MSIV. The space between the MSIVs is again air pressurized and the leakage rate resulting from leakage past the outboard MSIV is measured. This method of testing indicates the total MSL leakage, the leakage associated with the outbourd MSIV and, by subtraction, the leakage associated with the inboard MSIV.
The MSIVs are Rockwell Model 1612, 24", Y-type globe velves.
On September 17, 1991, the initial leakage testing of main steam lines (MSLs) C and D was conducted. In each case the line would not pressurize to the required air pressure; therefore, the amount of leakage past the outboard MSIV was nonquantifiable. Specifically, MSL C could only be pressurized to 21 psig and MSL D could not be pressurized above 3 psig.
During the testing, the test volume in MSL C experienced water intrusion but the volume in MSL D did not, indicating possible leakage of the MSL C inboard MSIV. Work requests were initiated to repair the outboard MSIVs on MSLs C and D. Inspection of the valves revealed the following:
MSL C outboard MSIV
- 1. Galled stem.
- 2. Indication on in-body seat.
- 3. Raised " lip" on in-body seat face.
- 4. Bonnet backseat deformation (indented contact pattern).
- 5. Raised metal on body bore.
MSL D outboard MSIV
- 1. Poor disk to in-body seat contact.
- 2. Disk outside diameter contacting raised " lip" on seat face above in-body seat.
- 3. Indented cont act pattern on bonnet backseat.
- 4. Steam cuts exhibited on inside diameter of packing gland / follower piece. j
.A second leakage test was performed on November 12, 1991, following repair of the MSLs C and l D outboard MSIVs. The results of these tests indicated that both outboard MSIVs were no I
1
)
-)
NRO FORM 3DCA U S f(JCLEAR REGULATORY COMM$SION APPRCNED OME NO. 3150-0134 EKPIPES 413'vD2 ESTIMATED BURDEN PER RESPONSE TO COMPtY 1MTH THIS M RMAD N NECD N RE UEST. SH HRS F RWAR C MMENTS LICENSEE EVENT REPORT (LER) REGARD!NG BURDEN ESTIMATE TO THE RECORDS AND REPORTS TEXT CONTINUATION u^o^ocut"T SRAucH (R430i. u s NUCtEAR eeoutaTOR< COMM>SsiON.
WASHINGTON DC 20%5, AND TO THE PAPERWORK REDUCTION PROJECT (31500104J OFFICE OF MANAGEMENT AND BUD 3ET, WASHINGTON, DC 20503 i ActuTY NAME (1) DOCEET NUMDER (2) LER NUMBER (5) PAGE (%
Brunswick Steam Electric Plant 05000324 YEAR SEO REV 3 No- NO Unit .2 ,
91 ,
019 01 T E n %. . . . .... - -~., NRC - w .m ,
longer leaking. Given that the outboard leakage was eliminated the testing revealed that both MSLs C and D inboard MSIVs exhibited leakage. MSL C inboard MSIV was determined to have a leakage rate of 32.47 scfh. The leakage rate associated with the MSL D inboard MSIV is nonquantifiable because the test volume would not pressurize. Work requests were initiated to repair MSLs C and D inboard MSIVs. Inspection of the valves indicated the following:
fML C inboard MSIV
- 1. In-body seat showed inadequate contact with disk.
- 2. In-body seat had two small pin holes.
- 3. Contact indications on outside diameter of disk. t
- 4. Slight gall marks in body bore.
- 5. Indications on bonnet backseat.
MSL D inboard MSIV
- 1. In-body seat has two " low spots".
- 2. Gall marks on body bore.
- 3. Bonnet backseat had slight indention marks.
The MSLs C and D inboard MSIVs repairs were completed and a subsequent repeat of the testing revealed zero leakage in both MSLs (ie: MSL C = 0.173 scfh and MSL D - 0.266 scfh).
GhUSE OF EVENT A Ioot cause analysis is in progrecs and the results will be provided in a supplement to this '
report.
CORRECTIVE ACTIONS 1 MSLs C and D inboard and outboard MSIVs repairs are complete. Additional corrective actions resulting from the root cause determination will be reported in the supplement to this report.
l SAFETY ASSESSMENT This event is outside the current design basis of Unit 2. A safety assessment of this event has not been completed at this time. Available data indicates that. it is not reasonable to assume a loss of MSL or condenser integrity during a LOCA or an earthquake, therefore the MSLs and the condenser would delay the release of MSIV 3eakage. However, given that the amount of leakage which would have eccurred through MSL D MSIVs has not been quantified, the degree to which the radiological limits of 10CFR100 would have been approached during a design basis accident bas not been determined. The assessment of this event will continue and will be reported in the supplement to this report.
PREVIOUS SIMILAR EVENTS A past failure of two MSIVs to meet the TS required 11.5 scfh leakage requirement has been reported in LER 1-88-025. That LER involved the outboard MSIV on two separate MSLs.
EIIS COMPONENT IDENTIFICATION Sys t ern /Comrenent FIIS Code ;
MSIV SB/ISV l
NRCFORM 3904 U $ NUCLEAR REGULATORY COMMIS$0N APPROVED OMB NO. 31$04100 .
' EXPIRES' &sof02 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INF RMATCN C LLECTON MEST; $0.0 HRSJORWARD COMMEMS LICENSEE F. VENT REPORT (LER) REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS TEXT CONTINUATION MANWENT BRANCH N U S. NUCLEAR REGULATORY COMM:SSON, WASHlNGTON DC 205S5, AND TO THE PAPERWORK REDUCTION PROJECT (3150-01ML OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503 F ACILITY NAME tt) DOCKET NUMBER (2) LER NUMBER (e) PAGE(3)
Brunswick Steam Electric Plant 05000324 YEAR SEQ PEV 4 Unit 2 NO NO.
91 019 01 TEXT (if mme spne a reautred tme addtanal NRC Fo'm 366A e) (17)
SUPPLEMENTAL CAUSE/ CORRECTIVE ACTION ,
Q MSL C OUTBOARD MSIV The leakage of the MSL C outboard MSIV resulted from the indication across the in-body seat.
Although no foreign material was found during the inspection, it is believed the indication was caused by the disk (main disk or poppet) closing on a piece of metal that had spalled off
-the body bore during a previous closure. This conclusion was substantiated by the raised metal on the body bore. Body bore-to-disk galling is a common problem with this type of valve. Corrective actions included lapping the in-body seat to remove the indication, removing the raised lip, and honing the body bore to remove the raised metal. The bonnet backseat surface was " skim cut" to remove the deformation (indented contact pattern). The ,
raised lip on the in-body seat was determined to be a tooling mark interjected during a previous seat repair, and is not suspected to have affected valve closure. A new (lighter) disk was also installed. Installation of the lighter disk is recommended by the vendor to minimize or eliminate galling. New and improved parts (disk, stem, stem-disk, and disk-piston) being supplied by the vendor as replacements for discontinued parts are being used ,
whenever an MSIV is required to be rebuilt. Other corrective actions included installing a new stem and increasing the bonnet backseat bore inside diameter to achieve greater clearance between the stem and backseat bore. This reduces the propensity of the stem contacting the bonnet backseat during valve stroking. Also, taller spacer rings have been installed.
Taller spacer rings are less likely to become cocked and cause galling.
A possible contributor could have been leakage of the stem-disk (pilot disk) to disk-piston ,
seat due to alignment. Stem misalignment is caused by a lack of valve actuator support I resulting in actuator deflection. The vendor states that a certain amount of misalignment 2s not detrimental to the actuator performance, however it is not advisable because it may cause galling of the stem and cocking of the stem-disk. Brunswick has installed taller i spacer rings to provide additional stem support and increased the bonnet backseat bore '
internal diameter to reduce the chance of stem galling.
MSL D OUTBOARD MSIV It is believed that leakage of the MSL D outboard MSIV resulted from the disk not seating completely against the in-body seat due to the disk outside diameter coming into contact with a raised lip (tooling mark) on the in-body seat face. This was evidenced by the disk O.D.
showing signs of contacting the raised lip. Finding no indications / imperfections on either the in-body or disk seating surfaces further substantiated this analysis. The in-body seat was lapped and the tooling mark removed. A " skim cut" was performed on the bonnet backseat to remove the def ormation and the packing gland / follower was replaced. The disk was replaced and the bcnnet backseat insida diameter was enlarged. A taller spacer ring was installed.
MSL C TNPOARD M91V Leakage of the MSL C inboard MSIV is attributed to poor disk to in-body seat. contact caused by low spots. Poor or no contact in certain areas due to low spots is considered typical and a primary cause of leakage in valves. These low spots are generally the result of in-body seat deformation caused by thermal expansion and contraction. The pin holes or pits noted were not.large enough in diameter (approximately 1/32") to cause leakage. The in-body seat was lapped to a satisf actory sealing surf ace. Additional corrective actions included honing the gall marks smooth and taking a " skim cut" on the bonnet backseat to remove the indication. The disk was replaced and the bonnet backseat inside diameter enlarged. A taller spacer ring was installed.
MSL D INBOARD MSIV
, HRC FORM yiCA U 5 NOCLEAR REGULATORf COMMISSON APPROVED C#B NO 3150-0104 o . .
- EXP*ES 4!30/B2 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS
'"F RMAEN MCTON REMST W HR$3ORWARD COMMENTS LICENSEE EVENT REPORT. (LER) REGARDING BUPDEN ESTIMATE TO THE RECORDS AND REPORTS TEXT CONTINUATION MANAGEMENT DRANCH (P430), U $ NUCLEAR REGULATORY COMMlSSION.
WASHINGTON DC 20%5 AND TO THE PAPERWORK REDUCTON PROJECT I (3150 010 4 OFFICE OF MANAGEMEPlf AND BUDGET, WASHINGTON, DC i "3
F AOUTY NA " - (1) DOCKET NUMBER c) LER NUMBER (6) PAGE (3)
Brunswick Steam Electric Plant 05000324 YEAR SEQ REV 5 Unit 2 NO NO 91 019 01 TEXT p ,w. we. . q,.o . . sone.:NaC rorm 3 sea .) (37; It is believed that low spots also caused leakage of the MSL D inboard valve. A loose stem-disk may have contributed to the leakage in that the disk could have cocked enough to prevent proper fit-up to the disk-piston seat. The loose stem-disk was determined to be caused by vibration loosening the locking pin (i.e., locking pin was found " wallowed outa). The in-body seat was lapped to a satisf actory sealing surf ace. The gall marks were honed smooth and .;
a " skim cut" taken to remove the indention marks from the bonnet backseat. Additionally, the' '
disk was replaced and the bonnet backseat inside diameter enlarged. A taller spacer ring was installed.
SUPPLEMENTAL SAFETY ASSESSMENT
- This event is considered potentially safety significant based on the possibility- for exceeding the 10CFR100 dose limits during a design basis accident. A dose analysis was l performed by first calculating the maximum allowable leakage without exceeding the limits and '
then the equivalent orifice necessary to produce this leakage. If the MSIV with the smallest ;
leak was more than 0.01 percent open, the offsite dose limit may have been exceeded. !
However, since the percent open la not known, the degree to which the radiological limits '
may have been approached can not be determined.
ADDITIONAL SUPPLEMENTAL INFORMATION .
t On December 7, 1992, the results of local leak rate testing indicated that MSIV leakage on MSL D again had exceeded the Techn;_al Specification limit of 11.5 scfh. Preliminary investigation indicated that the outboard MSIV appeared to have had excessive disk piston to valve bore clearance and an alignment problem (ie., the disk was not guiding properly into the in-body seat). MSLs A, B, and C tested satisfactorily. See LER 2-92-010.
i f
i i
1 I
1 i
I