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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000324/LER-1992-001, Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled1993-09-0202 September 1993 Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled 05000324/LER-1993-0081993-08-13013 August 1993 LER 93-008-00:on 930714,core Rated Thermal Power Exceeded Allowable Amount Due to Feedwater Flow Inaccuracy.Cause Believed to Be Due to Erosion/Corrosion of FW Flow Elements. FW Instrumentation recalibr.W/930812 Ltr 05000324/LER-1992-0101993-08-12012 August 1993 LER 92-010-01:on 921207,penetration Leakage Exceeded TS Allowable Limit Due to actuator-to-valve Alignment & disk-to-seat Alignment Problems.Line Bored Valve to Achieve concentricity.W/930812 Ltr 05000324/LER-1991-0191993-08-12012 August 1993 LER 91-019-01:on 911112,LLRT Failure of Two MSL Inboard & Outboard Isolation Valves Resulted in Condition Outside Design Basis.Root Cause Analysis in Process.Msls C & D Inboard & Outboard MSIVs Repairs complete.W/930812 Ltr 05000324/LER-1993-0031993-05-10010 May 1993 LER 93-003-00:on 930408,identified That Drywell Spray Outboard Isolation Valve Installed in Reverse Direction. Caused by Design & Installation Error.Appropriate Documents Will Be revised.W/930507 Ltr 05000324/LER-1988-0011990-08-0101 August 1990 LER 88-001-07:on 880102,manual Reactor Scram Occurred Due to Decreasing Main Condenser Vacuum.Reactor Power at 55% & Vacuum Decreased to 22 Inches Mercury.Caused by Leaks on Main Turbine Piping.Piping repaired.W/900801 Ltr 05000324/LER-1983-019, Updated LER 83-019/01T-2:on 830210,instrument Air Tubing to Safety Relief Valve/Automatic Depressurization Sys Valve Accumulator Inadequately Supported.Caused by Rerouted Tubing.Supports Installed1984-07-12012 July 1984 Updated LER 83-019/01T-2:on 830210,instrument Air Tubing to Safety Relief Valve/Automatic Depressurization Sys Valve Accumulator Inadequately Supported.Caused by Rerouted Tubing.Supports Installed 05000325/LER-1982-108, Updated LER 82-108/03L-1:on 821010 & 14,while Performing Automatic Depressurization Sys Valve Operability Test,Valves 1-B21-F013J & 1-B21-F013D & E Failed to Reclose.Caused by Faulty Spring.Valves Replaced1984-05-18018 May 1984 Updated LER 82-108/03L-1:on 821010 & 14,while Performing Automatic Depressurization Sys Valve Operability Test,Valves 1-B21-F013J & 1-B21-F013D & E Failed to Reclose.Caused by Faulty Spring.Valves Replaced 05000325/LER-1982-122, Supplemental LER 82-122/03L-1:on 821030 & 1104,reactor Recirculation Pump 1A Tripped.On 821101 & 04,reactor Recirculation Pump 1B Tripped.Caused by Spurious Action of ATWS Instrument B21-PS-N045C1984-04-0909 April 1984 Supplemental LER 82-122/03L-1:on 821030 & 1104,reactor Recirculation Pump 1A Tripped.On 821101 & 04,reactor Recirculation Pump 1B Tripped.Caused by Spurious Action of ATWS Instrument B21-PS-N045C 05000325/LER-1981-053, Updated LER 81-053/03L-1:on 810922,during Reactor Startup, Reactor Recirculation Pump 1B Tripped.Caused by Spurious Trip Signal from ATWS Low Water Level Instrument B21-LTM- NO24B-2.Instrument replaced.W/840329 Ltr1984-03-29029 March 1984 Updated LER 81-053/03L-1:on 810922,during Reactor Startup, Reactor Recirculation Pump 1B Tripped.Caused by Spurious Trip Signal from ATWS Low Water Level Instrument B21-LTM- NO24B-2.Instrument replaced.W/840329 Ltr 05000325/LER-1981-055, Updated LER 81-055/03L-1:on 820622,drywell Equipment Drain Flow Integrator 1-G16-FQ-K603 Continuously Indicated Dwed Sump Flow W/No Pumps Running.Caused by Water Being Introduced Into Pneumatic calibrator.W/840328 Ltr1984-03-28028 March 1984 Updated LER 81-055/03L-1:on 820622,drywell Equipment Drain Flow Integrator 1-G16-FQ-K603 Continuously Indicated Dwed Sump Flow W/No Pumps Running.Caused by Water Being Introduced Into Pneumatic calibrator.W/840328 Ltr 05000325/LER-1983-063, Updated LER 83-063/03L-1:on 831203,reactor Water Cleanup Sys (Rwcs) Differential Flow Indicator 1-G31-R615 Showed Erroneous Indication.On 831207,spurious Rwcs Alarm Annunciated.Caused by Air in Sensing lines.W/840222 Ltr1984-02-22022 February 1984 Updated LER 83-063/03L-1:on 831203,reactor Water Cleanup Sys (Rwcs) Differential Flow Indicator 1-G31-R615 Showed Erroneous Indication.On 831207,spurious Rwcs Alarm Annunciated.Caused by Air in Sensing lines.W/840222 Ltr 05000325/LER-1983-057, Updated LER 83-057/03L-1:on 831119,during Unit Power Performance,Temp Recorder TR-1258 Printed Erratically.Caused by Dirty Electrical Contacts in Control Board Timing Relay. Contacts Cleaned & Returned to svc.W/840222 Ltr1984-02-22022 February 1984 Updated LER 83-057/03L-1:on 831119,during Unit Power Performance,Temp Recorder TR-1258 Printed Erratically.Caused by Dirty Electrical Contacts in Control Board Timing Relay. Contacts Cleaned & Returned to svc.W/840222 Ltr 05000324/LER-1983-097, Updated LER 83-097/01T-1:on 831212,during Testing,Per IE Bulletin 83-02,crack Indications Discovered in 19 of 131 Welds in Reactor Recirculation & Reactor Water Cleanup Sys. Caused by Stress Corrosion Cracking1984-01-24024 January 1984 Updated LER 83-097/01T-1:on 831212,during Testing,Per IE Bulletin 83-02,crack Indications Discovered in 19 of 131 Welds in Reactor Recirculation & Reactor Water Cleanup Sys. Caused by Stress Corrosion Cracking 05000325/LER-1983-045, Updated LER 83-045/03L-2:on 830919 & 24,inboard PCIV Steam Supply Valve ES1-F007 to RCIC Sys Would Not Completely Reopen.Caused by Loose Limitorque Motor Operator Spring Pack1984-01-24024 January 1984 Updated LER 83-045/03L-2:on 830919 & 24,inboard PCIV Steam Supply Valve ES1-F007 to RCIC Sys Would Not Completely Reopen.Caused by Loose Limitorque Motor Operator Spring Pack 05000324/LER-1982-024, Updated LER 82-024/01T-1:on 820205,determined That Control Bldg Emergency Ventilation Sys Trains Will Not Isolate Upon Receipt of Chlorine Isolation Signal If Control Switch in on Position Due to Design Deficiency1983-11-14014 November 1983 Updated LER 82-024/01T-1:on 820205,determined That Control Bldg Emergency Ventilation Sys Trains Will Not Isolate Upon Receipt of Chlorine Isolation Signal If Control Switch in on Position Due to Design Deficiency 05000324/LER-1983-083, Updated LER 83-083/01T-1:on 830905,supply Valve 2-FP-V39 to Deluge Sys of Both Standby Gas Treatment Sys Discovered Shut.Caused by Operator Error.Valves Tagged for Identification.Auxiliary Operator Disciplined1983-09-23023 September 1983 Updated LER 83-083/01T-1:on 830905,supply Valve 2-FP-V39 to Deluge Sys of Both Standby Gas Treatment Sys Discovered Shut.Caused by Operator Error.Valves Tagged for Identification.Auxiliary Operator Disciplined 05000325/LER-1983-034, Updated LER 83-034/01T-1:on 830811,following Extended Maint & Refueling Outage,Instrument Isolation Valves to 1CAC-PDS-4222 & 4223 Discovered Closed.Caused by Cancelation of Equipment Clearance.Valves Reopened1983-09-12012 September 1983 Updated LER 83-034/01T-1:on 830811,following Extended Maint & Refueling Outage,Instrument Isolation Valves to 1CAC-PDS-4222 & 4223 Discovered Closed.Caused by Cancelation of Equipment Clearance.Valves Reopened 05000325/LER-1983-017, Updated LER 83-017/03L-1:on 830326-28 & 0402,listed Control Rods Had No Indications for Identified Positions.Caused by Loose Prototypic Inlet Piping Connectors Due to Undervessel Work.Connectors Will Be Properly Fastened1983-07-19019 July 1983 Updated LER 83-017/03L-1:on 830326-28 & 0402,listed Control Rods Had No Indications for Identified Positions.Caused by Loose Prototypic Inlet Piping Connectors Due to Undervessel Work.Connectors Will Be Properly Fastened 05000324/LER-1982-131, Supplemental LER 82-131/03L-1:on 821206,one-half Automatic Reactor Scram Signal Received Due to Instrument Downscale Signal from Main Steam Line Radiation Monitor D, 2-D12-RM-K603D.Caused by Disconnection of Instrument Cable1983-03-11011 March 1983 Supplemental LER 82-131/03L-1:on 821206,one-half Automatic Reactor Scram Signal Received Due to Instrument Downscale Signal from Main Steam Line Radiation Monitor D, 2-D12-RM-K603D.Caused by Disconnection of Instrument Cable 05000324/LER-1981-090, Updated LER 81-090/03L-3:on 810817 & 23,suppression Chamber Water Level Indicator 2-CAC-LI-2601-3 Indicated Lower Level & on 810820,indicated Higher Level than Other Indicator.Caused by Changes in Trickle Flow to Wet Ref Leg1983-01-28028 January 1983 Updated LER 81-090/03L-3:on 810817 & 23,suppression Chamber Water Level Indicator 2-CAC-LI-2601-3 Indicated Lower Level & on 810820,indicated Higher Level than Other Indicator.Caused by Changes in Trickle Flow to Wet Ref Leg 05000325/LER-1982-127, Updated LER 82-127/01T-1:on 821103,quick Start Testing of Diesel Generators 2,3 & 4 Not Performed for 12 H Period Per Tech Spec.Caused by Failure to Enter Requirement Into Daily Surveillance Rept on 821102.Testing Performed1982-12-23023 December 1982 Updated LER 82-127/01T-1:on 821103,quick Start Testing of Diesel Generators 2,3 & 4 Not Performed for 12 H Period Per Tech Spec.Caused by Failure to Enter Requirement Into Daily Surveillance Rept on 821102.Testing Performed 05000325/LER-1982-135, Supplemental LER 82-135/03L-1:on 821019,1.5-inch Discrepancy Noted Between Narrow & Wide Range Instruments.Caused by Inoperable RTGB Level Instruments.Plant Mod Package Developed to Increase Accuracy1982-12-23023 December 1982 Supplemental LER 82-135/03L-1:on 821019,1.5-inch Discrepancy Noted Between Narrow & Wide Range Instruments.Caused by Inoperable RTGB Level Instruments.Plant Mod Package Developed to Increase Accuracy 05000325/LER-1982-024, Supplemental LER 82-024/03L-2:on 820214,during Periodic Test,Discovered That Open Position Indication for Drywell to Suppression Vacuum Breaker X18H Could Not Be Achieved.Caused by Failure of Vacuum Breaker to Fully Stroke Open1982-10-13013 October 1982 Supplemental LER 82-024/03L-2:on 820214,during Periodic Test,Discovered That Open Position Indication for Drywell to Suppression Vacuum Breaker X18H Could Not Be Achieved.Caused by Failure of Vacuum Breaker to Fully Stroke Open ML20054L9761982-06-29029 June 1982 LER82-054/03L-0:on 820607,reactor Core Isolation Cooling Sys Turbine Automatically Started on Reactor Low Level,But Tripped Due to Closure of Control Valve 1-E51-V9.Caused by Lack of Turbine Speed Demand Signal Due to Governor Failure 05000325/LER-1982-0531982-06-29029 June 1982 LER 82-053/03L-0:on 820604,during startup,09 Position Found Superimposed on 00 RTGB Position Indication for Fully Inserted Control Rod 10-07.Caused by Defective Rod Position Reed Switch.Investigation Scheduled for 1982 Outage 05000325/LER-1981-092, Updated LER 81-092/01T-2:on 811226,action Statement 3.3.2b Not Entered When B21-LT-N017D-1 Instrument Failed Upscale. Caused by Failure of Operations Personnel to Recognize & Perform Required Action1982-06-21021 June 1982 Updated LER 81-092/01T-2:on 811226,action Statement 3.3.2b Not Entered When B21-LT-N017D-1 Instrument Failed Upscale. Caused by Failure of Operations Personnel to Recognize & Perform Required Action 05000325/LER-1981-093, Updated LER 81-093/01T-2:on 811226,reactor Protection Sys Vessel Low Level Trip instrument,1-B21-LT-NO17D-1,was Indicating Upscale.Caused by Personnel Failure to Recognize & Perform Tech Specs.Personnel Counseled1982-06-18018 June 1982 Updated LER 81-093/01T-2:on 811226,reactor Protection Sys Vessel Low Level Trip instrument,1-B21-LT-NO17D-1,was Indicating Upscale.Caused by Personnel Failure to Recognize & Perform Tech Specs.Personnel Counseled 05000325/LER-1982-038, Updated LER 82-038/03L-1:on 820419.Reactor Scrammed When Electrical Bus 1A-1 Dc de-energized.Caused by Operator Error in Opening 125-volt Dc Battery Charger Output Breaker for Battery 1A-1.Breaker Closed & Power Restored to Bus1982-06-0404 June 1982 Updated LER 82-038/03L-1:on 820419.Reactor Scrammed When Electrical Bus 1A-1 Dc de-energized.Caused by Operator Error in Opening 125-volt Dc Battery Charger Output Breaker for Battery 1A-1.Breaker Closed & Power Restored to Bus ML20062G3081978-12-21021 December 1978 /03L-0 on 781122:HPCI & RCIC Component Tests Were Overlooked Because Rescheduling Technique Provided No Clear Indication of Test Due Dates.Responsible Technician Reinstructed & Admin Operating Instruction AOI-5 Rev ML20064H8961978-12-19019 December 1978 /03L-0 on 781120:Senior Control Operator Did Not Have Completed Hatch Leak Rate Test Before Beginning Reactor Startup Due to Misunderstanding.Test completed.GP-1 Revised to Require Leak Test Verification by Control Operators ML20064H6181978-12-14014 December 1978 /03L-0 on 781114:torus Level of the HPCI Turbine Control Sys Was Slightly Above the Allowed 27 Inches.Proper Torus Level Restored to Normal.Torus Level Indicator Will Be More Clearly Marked ML20064H5971978-12-14014 December 1978 /03L-0 on 781114:Fire Hoses of Radwaste Bldg 3 Elevation Fire Stations Were Found Missing Due to Use by Personnel for Routine Radwaste Washdown.New Firehoses Installed & Mod Re Alternate Water Supply Is in Progress ML20064H5891978-12-14014 December 1978 /03L-0 on 781114:during Periodic Test 9.3.a the HPCI Egr Actuator Failed to Oper Properly Due to Water in Hydraulic Fluid Corroding Egr Actuator.Steam Leaking Past Seat of Valve HPCI E41-F001 Allowed Water Into Fluid ML20062F6781978-12-13013 December 1978 /03L-0 on 781112:reactor Steam Dome High Pressure Switch B32-PS-N018B Did Not Reset & Would Not Allow RHR Valve E11-F008 to Open for Shutdown Cooling at Reactor Pressure of 102psig.Caused by Sticking micro-switch ML20062F6681978-12-13013 December 1978 /03L-0 on 781117:while Reactor Was in Hot Shutdown Torus Level Increased .2 Above Tech Specs.Caused by Demineralized make-up Water Leakage Through Valves from RHR Keep-fill System Causing Torus Level to Rise ML20064G9301978-12-11011 December 1978 /03L-0 on 781109:Reactor Vessel Chemistry Exceeded Tech Spec Limits for Conductivity & Concentration Due to Presence of Organic Compounds in Condensate Sys.Organic Filtration & High Concentration of Ion Resin Cleanup Begun ML20062E4381978-11-30030 November 1978 /03L-0 on 781101:rod Block Monitor(Rbm) Channel a Was Found Out of Calibr During Testing Due to Setpoint Drift.Calibr Frequency Will Be Increased from Once to Twice Per Year ML20064E8001978-11-15015 November 1978 /03L-0 on 781017:reactor Bldg Radiat Exhaust Monitor D12-RM-N010B Failed Safe Causing Reactor Bldg Vent to Isolate,Due to Defective Transistor 2N1711 on 24V Pwr Supply ML20064E4581978-11-14014 November 1978 /01T-0 on 781101:util Was Informed by NRR of Nonconformance w/10CFR50 Append a Gen Design Criteria 54 & 56.Two Reactor bldg-to-torus Vacuum Breaker Lines Have Never Had Design Review by Nrc.Tech Spec Change Effective 781108 ML20064E3371978-11-0909 November 1978 /03L-0 on 781014:RCIC Turbine Was Tripped on Manual Overspeed for Training Purposes & Turbine control- Stop Valve E51-V8 Would Not Reset.Caused by Improperly Worn Adjusted Reset Lever ML20064E2921978-11-0909 November 1978 /03L-0 on 781011:torus Level Dropped Below Tech Spec Minimum While Water from Torus Was Being Pumped,Via Rgr to Radwaste in Efforts to Reduce Torus Water Level. Caused by Operator Being Distracted ML20064E3541978-11-0707 November 1978 /03L-0 on 781006:condensate Storage Tank Level Switch E41-LS-N003 Found Out of Calibration During Periodic Condensate Storage Tank Low Level Channel.Caused by Instru Drift ML20064E3491978-11-0606 November 1978 /03L-0 on 781105:Control Oper Received Control Rod Drift Alarm for Rod 10-31.When Rod Position Display Was Selected,A False 3 Was Superimposed on Actual Rod Position Due to Aground on the Rpls Probe ML20064D8211978-11-0202 November 1978 /03L-0 on 781004:pressure Switch E11-PS-NO16B Failed During Periods Plci Pump Discharges ADS Permissive Test,Due to Corrosion Buildup on Plunger of Switch ML20064C0151978-10-10010 October 1978 /03L-0 on 780911:during Monthly 1 Diesel Generator Load Test,It Was Found That 1 Cylinder Was Not Firing,Due to Faulty Fuel Pump ML20064C0011978-10-0909 October 1978 /03L-0 on 780911:Snubber SW-142SS164 Found Inoperable During Periodic Test.Caused by Seal Degradation & Resulting Loss of Fluid ML20147C9141978-10-0404 October 1978 /03L-0 on 780904:RCIC Isolation Channel a Tripped Momentarily,Causing RCIC Sys to Be Inoper,Due to Defective RX-2 Relay ML20062A0691978-10-0303 October 1978 /03L-0 on 780904:rod Block Monitor B Inoperative Trip Came on & Stayed on for 1/4 of the Control Rod Selection Matrix.Caused by Failed Integrated Circuit in Rod Block Monitor self-test Circuitry ML20064B7231978-10-0303 October 1978 /03L-0 on 780905:during Periodic Test,Radiat Monitor D12-RM-NO10B HI-HI Trip Point Drifted to Higher than Permitted Level.Monitor Recalibrated.Drift Appears to Be Isolated Incident;No Further Action Taken 1993-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N3271999-10-21021 October 1999 Part 21 Rept Re non-linear Oxygen Readings with Two (2) Model 225 CMA-X Containment Monitoring Sys at Bsep.Caused by High Gain Produced by 10K Resistor Across Second Stage Amplifier.Engineering Drawings Will Be Revised BSEP-99-0168, Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with ML20212D0431999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Brunswick Steam Electric Plant,Units 1 & 2 ML20210P9441999-08-10010 August 1999 Safety Evaluation Accepting Licensee Assessment of Impact on Operation of Plant,Unit 1,with Crack Indications of 2.11, 6.36 & 1.74 Inches in Three Separate Jet Pump Risers ML20210P9181999-08-10010 August 1999 Safety Evaluation Authorizing Request for Reliefs CIP-01,02, 06,07,08,09,10 & 11 (with Certain Exceptions) & 12-18,for Second 10-year ISI Interval.Request CIP-04 & 05 Would Result in hardship,CIP-03 Not Required & CIP-11 Denied in Part ML20210N2341999-08-0505 August 1999 SER Accepting Response to NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issues (USI) A-46 ML20210R1191999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Bsep,Units 1 & 2 ML20210R1311999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Bsep,Unit 2 BSEP-99-0118, Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with BSEP-99-0095, Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20210M8581999-05-14014 May 1999 B214R1 RPV Hydrotest Bolted Connection Corrective Action Evaluation, Rev 0 ML20211L3711999-05-10010 May 1999 Rev 0 to ESR 98-00333, Unit 2 Invessel Feedwater Sparger Evaluation ML20206G1871999-05-0404 May 1999 Safety Evaluation Approving Third 10-year ISI Program Requests for Relief (RR) RR-08,RR-15 & RR-17 BSEP-99-0075, Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With ML20206N1791999-04-23023 April 1999 Rev 0 to 2B21-0554, Brunswick Unit 2,Cycle 14 Colr BSEP-99-0059, Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20205F9031999-03-30030 March 1999 Safety Evaluation Supporting Proposed Rev to BSEP RERP to Licenses DPR-62 & DPR-71,respectively ML20206N1831999-02-28028 February 1999 Rev 0 to Suppl Reload Licensing Rept for Bsep,Unit 2 Reload 13 Cycle 14 BSEP-99-0043, Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20203D7061999-02-0909 February 1999 SER Accepting Proposed Alternatives Contained in Relief Requests PRR-04,VRR-04,VRR-13,PRR-01,PRR-03,VRR-01.VRR-07, VRR-08 & VRR-09 Denied BSEP-99-0005, Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0231, Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0218, Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with BSEP-98-0210, Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired1998-10-30030 October 1998 Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired ML20154P8151998-10-16016 October 1998 SER Accepting Revised Safety Analysis of Operational Transient of 920117,for Plant,Unit 1 ML20154P8591998-10-16016 October 1998 SER Accepting Equivalent Margins Analysis for N-16A/B Instrument Nozzles for Plant,Units 1 & 2 BSEP-98-0202, Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151Y6211998-09-14014 September 1998 BSEP Rept Describing Changes,Tests & Experiments, for Bsep,Units 1 & 2 ML20151Y6371998-09-14014 September 1998 Changes to QA Program, for Bsep,Units 1 & 2 BSEP-98-0185, Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151T5021998-08-0505 August 1998 Project Implementation Plan, Ngg Yr 2000 Readiness Program, Rev 2 BSEP-98-0164, Monthly Operating Repts for July 1998 for BSEP Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for BSEP Units 1 & 2 ML20236T1961998-07-0101 July 1998 Rev 1 to 2B21-0088, Brunswick Unit 2,Cycle 13 Colr ML20236T1921998-07-0101 July 1998 Rev 1 to 1B21-0537, Brunswick Unit 1,Cycle 12 Colr BSEP-98-0142, Monthly Operating Repts for June 1998 for BSEP Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for BSEP Units 1 & 2 ML20236T1971998-06-30030 June 1998 Rev 2 to 24A5412, Supplemental Reload Licensing Rept for Brunswick Steam Electric Plant Unit 2 Reload 12 Cycle 13 ML20249B9691998-06-11011 June 1998 Rev 1 to VC44.F02, Brunswick Steam Electric Plant,Units 1 & 2,ECCS Suction Strainers Replacement Project,Nrc Bulletin 96-003 Final Rept BSEP-98-0129, Monthly Operating Repts for May 1998 for Bsep,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Bsep,Units 1 & 2 ML20151S9041998-05-31031 May 1998 Revised Pages to Monthly Operating Rept for May 1998 for Brunswick Steam Electric Plant,Unit 1 BSEP-98-0104, Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 2 ML20151S8991998-04-30030 April 1998 Revised Pages to Monthly Operating Rept for Apr 1998 for Brunswick Steam Electric Plant,Unit 1 ML20247N7501998-04-30030 April 1998 Rev 0 to BSEP Unit 1,Cycle 12 Colr ML20247N7721998-04-30030 April 1998 Rev 0 to J1103244SRLR, Supplemental Reload Licensing Rept for BSEP Unit 1,Reload 11,Cycle 12 ML20217K8461998-04-24024 April 1998 Safety Evaluation Approving Proposed Use of Code Case N-535 at Brunswick Unit 1 During Second 10-yr Interval,Pursuant to 10CFR50.55a(a)(3)(i).Authorizes Use of Code Case N-535 Until Code Case Included in Future Rev of RG 1.147 ML20217K3941998-04-24024 April 1998 SER Approving Relief Request for Pump Vibration Monitoring, Brunswick Steam Electric Plant,Units 1 & 2 ML20217E6841998-04-23023 April 1998 Safety Evaluation Accepting Code Case N-547, Alternative Exam Requirements for Pressure Retaining Bolting of CRD Housings ML20217E7471998-04-21021 April 1998 Safety Evaluation Accepting Alternative to Insp of Reactor Pressure Vessel Circumferential Welds ML20217B5241998-04-20020 April 1998 SE Accepting Licensee Request for Approval to Use Alternative Exam Requirement for Brunswick,Unit 1,reactor Vessel Stud & Bushing During Second 10-yr ISI Interval Per 10CFR50.55a(a)(3)(ii) BSEP-98-0080, Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 2 ML20216B1041998-03-0404 March 1998 SER Approving Alternative to Insp of Reactor Pressure Vessel Circumferential Welds for Brunswick Steam Electric Plant, Unit 1 1999-09-30
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LER-2092-001, Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled |
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FBE227amaT2:CLh"*J:NEDLTIM Carolina Power & Ught Company
%Mciz:nzmaaxn,TmuczTa Brunswick Nuclear Plant P. O. Box 10429 Southport, N.C. 28461-0429 September 3, 1993 FILE: B09-13510C 10CFR50.73 SERIAL: BSEP-93-0137 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 BRUNSWICK NUCLEAR PLANT UNIT 2 DOCKET NO. 50-324 LICENSE NO. DRP-62 SUPPLEMENTAL LICENSEE EVENT REPORT 2-92-001-01 Gentlemen:
In accordance with Title 10 of the Code of Federal Regulations, the enclosed Supplemental Licensee Event Report is submitted. The original report fulfilled the requirement for a written report within thirty (30) days of a reportable occurrence and was submitted in accordance with the format set forth in NUREG-1022, September 1983.
Supplemental Licensee Event Report 2-92-001-01 was mailed en September 1, 1993. Due to the inadvertent omission of the report date on form OMB 3150-0104 please disregard that report and replace it with this supplement.
Very truly yours, M13w C. Warren, P ant Manager Unit 2 Brunswick Nuclear Plant JFM/jfm Enclosure cc: Mr. S. D. Ebneter Mr. P. D. Milano BNP NRC Resident Office 080r+
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NRC FORM 306 U.S. NUCLEAR REGULATORY COWtSSION APPROVED OMB NO. 3150-0104 (5/92) WPIRES: 5/31/95 LST1M Alf D BURDEN AR RTEPONSE TO COMPLY WITH T HIS INF ORV AnDN CD11.lCTIDN REOVtST 50 D HR5 5 05hN ARD LICENSEE EVENT REPORT (LER) COMMus R,GiRDe euRDtN i5num iO ,He i~,ORunON AND Rt CORDS MANAGIM(NT !! RANCH lMNE4B 7714t U $ NUCLi AR fit GULATORY C OMMf55sDN. WA$mNGTON. DC 205% DOO1 ANDTO THE FAPERWORK RE DUCTION PROJf CT (3150 0104L OrnCE OF Mr NAC,lMINT A,ND fluDGET. W ASHilicTON. DC 20503 f AC IWV NAMI 1i DOC k iT NUVE4[ R (2} J%[ (3)
Brunswick Steam Electric Plant, Unit 2 05000324 l 1 of 4 1Ill F .4 <
UNIT 2 SCRIJ4 DURING MAIN TURBINE CONTROL VALVE TESTING f
EVENT DATE (5i LER NUMBER t61 REPORT DATE 17} OTHER FACILITIES INVOLVED (8)
SE OUf_NT l At Rf VI5!ON f ACllllV N AM[ DOCF f Y NUMBER MON ' H DAY ilAR %fAR MONT H DM Y{AR Naua n NuMn R 05000 02 02 92 92 - 001 - 01 09 02 93 ' ACUT Y hAMI DOC S ET NUMDE R 05000 gp , , TH S RE PORT IS SUBMITTE D PURSUANT TO THE REQUIREMENTS OF 10 CFR 6. (Ched one or more of the fobowmgul t)
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LICENSEE CONTACT FOR THIS LER (12)
NAMI it'i['PHONf NUMt i R Jeanne F McGowan, Regulatory Compliance Specialist (919) 457-2136 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DrSCRIBED IN THIS REPORT (13) m POni Ante l mr onT ABLE t Auti su u M ct w oN!Ni M Anes tum a ( AL8f SYSTLM COMPONE N T MANJF ACTUkFR
,g w g B TG IsCC/ SEAL P070 Y SUPPL EMENTAL REPORT EXPECTED (141 I EXPECTED
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SUBMISSION vi s X NO e m - - eninTroSunuisuoNCnt, DATE(15)
/ b TF2 - ..mt t ;4C0 rpaces, 2 .e. apprcximatel) fifteen single space t ypewritten lines) (26) t i Jar a:y 9, 19 s , '
ut ; wa< geratir3 at apprcximately 100% steady state power. An
- c nc:ater icr .cw electittydraul:c (EH3 fluid pressure was receised. EHC pressure cwings cu*
- re.g t< pr wr rety i t' abcut a power to c1tse #4 turbine control valve (TCV) w:,ch Ic: ac"d t !a EC p r + < ni . E w;n: r .
'n Februar, ., I H2, reactor power was reduced to
- qprcx mately ~A M T~J t esting bega During #2 TCV testing, the Centrol Operator (CO) did m:t havt .
> t' reter t re scram log:c for trv 'F: trip (Ieceived as expected) before the 'Al' tz:p gnal wu :ac" ved cam og a reactcr scram. Follcwing the r ea ct c r scram, ECIC aatr , . call 3 : nit l at e d a nf .n3 ect ed . EPCl initiated but level recovered prior to iniectien.
T% cause cf this er"nt war nit 2 oyn t rapped in the Turbira Control Valve Fast Closure (TCVFC) 12 9 c: cat.ng 2 pretsute pel t ar t at icn m 3 the TCVFC Frersure Switch #1 (2-EHC-PSL-1756) causing it t o tr;p The gas s
- i an EHC accun ulat or was f ound t m be salid with EHC f luid. It is bel 2esed that a seal failure cf t h. accumulatcro arsociat ed with t his line allowed nitrogen t o ent er t h< EHC flu d. ~ne accrul at er seal failure is attributed to excessive cycling which began atter ir talle icm cf t he part ial are conve rsion modif ication during the last Unit 2 refueling outa ? '3e; 3 r a l Elm tr:c and Carolina Fowor & Light are investigating the cause and developing a
! plan fer arr ect A ve actic t til rplementation of the corrective action, reactor power was j ' enced 'O dnt: ore the EHF fyrtom crrillatirns. The EH2 accumulatorr. were rebuilt. During t he I m. 1-cevary +he CC was unaria to :ere* the 'A' Eeactor Feed Pump (EFP) t urbine due t o a failed ie et :% ay c eli 2 n t he F TP I t ' - logic. The 'IP RFP also had a bound pcmp shaft assembly due t o failure "f wer r: JT cap screwr The rafety significance of this event war minimal. Safety ryt t rw f r_* .- -d as esigmd. U-th I cimilar event was repcrted :n H R 017 (SCPJN during TCV /Tr' tes .ng du to p:oceduta] c d rwitch problems).
T' ause cl as s i f : cat ic.n fc: t his event per tr.a criteria cf NUE E ;- 1;22 is Design, Manufacturing, C nstrn~t cn/I <tallataen.
63RC FORM 366A U. S. FJUCLEAA REGULATORY COMMISSION APPROtfED OMB NO. 3150-0104 (5/92) EXPlRES: 5/31/95 ESTIMATED BURDEN PER RISPONSE TO COMPL Y WTTH TNS INFORMATION COLLECTION 84EQUEST: 50 0 HRS. FORWARC LICENSEE EVENT REPORT (LER) COMMcNT3 rec,ARo,No ,URnEN EsT,M A1E T O TNE ,N ORM AT,0N ANo TEXT CONTINUATION RECORDS MANAGEMENT BRANCH (MNBB 7714), U .S . WLEAR REGULATORY COMMISSION. WA9ttNGTON. DC20555-000L AND TO THE PAPERWORK REDUCTION PROJE CT (3160 0104). OFHCE OF MANAGEMENT AND BUDGET, WA$HINGTON, DC 20503.
FACILITY NAME (1) DOOKET NUMBER W LER NUMBER IE9 PAGE (3)
$FOUENTIAL REVISION Brunswick Steam Electric Plant ""'" """""
05000324 2 of 4 Unit 2 92 - 001 - 01 1
TEXT Uf more space os required, use additwat NRC form 366A %I (1h I 1
TITLE l l
UNIT 2 SCRAM DURING MAIN TURBINE CONTROL VALVE TESTING l
l INITIAL CONDITIONS !
On February 1, 1992, Unit 2 was operating at 87% power. Periodic Test (PT) 4 0. 2. 5, Turbine Control Valve and Extraction Steam Stop Valve Testing, was scheduled to be performed during the shift. On February 2, 1992, at 0313 hours0.00362 days <br />0.0869 hours <br />5.175265e-4 weeks <br />1.190965e-4 months <br />, the Control Operator commenced a power reduction to 00% to perform the weekly valve testing. A briefing was held and at 0345 !
hours the valve testing commenced. The High Pressure Coolant Injection System (HPCI) and '
the Reactor Core Isolation Cooling System (RCIC) were operable and in standby.
EVENT NARRATIVE On January 29, 1992, Unit 2 was operating at approximately 100% power. An annunciator for low EHC 11uid pressure was received. EHC pressure swings occurred and reactor power was reduced to approximately 85% to close #4 TCV which reduced the EHC pressure swings.
The 4 TCVs had experienced oscillations during power ascension to 100% after the Unit 2 refueling outage. A plant modification had been installed to convert the Unit 2 High Pressure (HP) turbine from a full arc to a partial arc valve admission. During the investigation of the ccntrol valve oscillations, the lead / lag potentiometers in the pressure regulator control loops were found at zero (0). The system was aligned after installation of the Partial Arc Conversion Modification. Per the lineup instructions, lead / lag potentiometers are moved to zero (0) from their operational settings at the start of pressure control adjustments. Upon completion of the pressure control adjustments they are to be returned to their "as-found" settings. The lead / lag potentiometers were not returned to the required "as-found" positions upon completion of the pressure control section of the line-up instructions. Unit 2 was shutdown to correct the potentiometer settings. The unit was returned to 100% power after the adjustments were made.
Af ter restart, the valves continued to oscillate causing steam line pressure swings. The EHC pressure regulators began to alternately control the valve demand signals due to the pressure swings. Reactor power was reduced due to scram potential of the unstable pressure regulators. Based on the manufacturers recommendations, a bias adjustment was made to separate the control functions of the pressure regulators, allowing the backup pressure I regulator to control the valve demand signals. This did provide better valve stability: j h w ver, after approximately seven days of 100% power operation the valve oscillations j becaue larger and the EHC hydraulic pressure was observed to be moving greater than 150 )
psi. Reactor power was reduced to 85% while a root cause determination was made. Based ;
on a recommendation from the manufacturer, the hydraulic accumulators were tested and it !
was discovered that leakage past the seals had resulted in the accumulators being filled j with EHC fluid. The reduction in mechanical dampening from the leakage into the gas end of the accumulators was corrected by depressurizing the gas end and recharging it to the correct p1 tssure in accordance with PT 33.1, EHC Accumulator Precharge Check, on February 1, 1992. The unit was expected to return to 100% power after performing control valve testing to assure correct mechanical response of the accumulators.
, On February 2, 1992, at 0313 hours0.00362 days <br />0.0869 hours <br />5.175265e-4 weeks <br />1.190965e-4 months <br />, the Control Operator commenced reactor power reduction to 80% to perform PT 40.2.5, Turbine Control Valve and Extraction Steam Stop Valve Testing.
A briefing was held and at 0345 hours0.00399 days <br />0.0958 hours <br />5.704365e-4 weeks <br />1.312725e-4 months <br />. the valve testing commenced. At 0509 hours0.00589 days <br />0.141 hours <br />8.416005e-4 weeks <br />1.936745e-4 months <br />, while
I r---- -= . j NRC FORM 366A U. S. f60 CLEAR REGULATORY COMNtSSIOM APPROVED OMB NO. 3150-0104 j
{5/92)
EXP!RES: 5/31/9b
( STIM AT E D BURDEN PE R RE SPONSE TO COMPL Y WITH THIS INf DHMATION COLLE CTION RIOUf 5T: f.O.0 HRS F ORW ARD !
. LICENSEE EVENT REPORT (LER) COMME Nis RtGAnn,NG BURotN tsTiMATr TO THc ,NroRiaAT,oN ANo TEXT CONTINUATION RICORDS MWAGEMINT BRWCH NNbB M O. U S. NUCLI AR REGULATORY COMMISSION. WASHINGTON, DC 20f 55 0001. AND TO i THE P APf. RWORK Rf, DUCTION PROJECT 0160 0100 Of rice Of l i
MANAGEMLNT AND BUDGLT, WALHINGTON, DC 20t.03 I
f ACPJTY NAME M) DOCKET NUMBER G) LE R NUMBER (C) PACE (3)
LIQUINTIAL REVISION Brunswick Steam Electric Plant " " " * "
05000324 3 of 4 Unit 2 92 - 001 - 01 ;
TVKT Uf mue space is requeed. use addaronalIVRC form 366Ks! O h testing the #2 TCV, a reactor scram occurred due to the actuation of an EHC Reactor ,
Protection System (RPS) pressure switch (2-EHC-PSL-1756). Following the reactor scram, l ECIC automatically initiated and injected. HPCI initiated but level recovered prior to j allowing injection.
Preliminary investigation into this event revealed that the accumulator piston seals were !
subjected to excessive cyclic wear due to the hydraulic occillations in the EHC system.
The EHC Accumulators were rebuilt and placed back in cervice. The unit was returned to 82% power and evaluations of the accumulator seal failure continued. The unit was to (
remain at 82% power to minimize control valve oscillations and until the root cause could l be determined and the corrective acticna implemented. The unit remained at 82% power until both undts were shutdown in April due to Diesel Generator Building seismic concerns. ;
i CAUSE OF EVENT The cause of the event was the excessive cycling of the turbine control valves. This caused the failure of the EHC Accumulator seals. The seal failure allowed nitrogen into the EHC lines, causing a pressure perturbation on the TCVFC Pressure Switch No. 1 (2-EHC-PSL-1756). This perturbation caus M the opening of the TCVFC Pressure Switch No.1 during testing of TCV #2. Extensive benc;. 7 sting of the TCVFC Pressure Switch No. 1 showed no 4 defects or unusual sensitivity to pressure perturbations. It was concluded that the pressure seen by the switch did drop into the trip setpoint range and the switch did react to that pressure by opening.
Following the scram on February 2, 1992, both of the EHC Accumulators were disassembled.
Removal of the piston revealed that the piston seal in both accumulators had f ailed. Both ,
seals had significant deterioration as indicated by excessive pitting. The f ailure of the seu s were due to the precoure oscillations during the period from January 5 to February 2, 1992. This was due to the instability experienced in the EHC system pressure regulator ,
as seen after the conversicn from full arc-1 admission to partial arc-2 admission. l Initially, hydraulic pressure oscillations in the order of apprcximately 70-100 psi were a seen. After electrcnic adjustment to the pressure regulator, hydraulic pressure ,
oscillations of approximately 25-50 psi were seen. The frequency range of these oscillations was 0.5 - 1.0 Hz. Typical hydraulic accumulator piston seals have a life of ;
I - 2 x 10' cycles. Based on the time period and frequency of the hydraulic pressure oscillations, the EHC accumulators experienced in excess of 1 x 10' cycles.
4 As part of the Partial Arc Conversion Modification, new valve curves were used to pennit !
operation f or partial are - 2 admission. The investigation of the failed EHC Accumulator j seals revealed that the valve curves were designed f or a reactor output of 105% . The power i uprate modification on the reactor had not been performed and the reactor output was 100%
rather than 105%. This caused the new valve curves to be inaccurate for the present ,
reactor operation. The resulting turbine instability caused turbine control valve oscillations and the EHC Ac.;umulator seal failure.
i COPRFCTIVE ACTIONS <
Corrective actions included the following: ,
l
- 1. The EHC hydraulic accumulators A and B were disassembled. The inner cylinder walls were checked for nicks and light scoring and any indications were removed with crocus cloth. All *O* rings, teflon rings, and piston seals were replaced. The
i lNRC FORM 366A U. S. NUCLEAR REGULATORY COISMISSIORI APPROVED OMB NO. 3150-0104 (5/92) EXPIRES: 5/31/95
, F STIM ATID 11URDEN PLA RfLPONSE TO COMPL Y WITH THIS INFORMATION COLLICTION RtOUEST: 50.0 HRS. F ORWARD
' LICENSEE EVENT REPO T L g r COMMINTS Rt GARDJNG BURDEN tSTIM ATE TO THE INF ORM A1 ION AND TEXT CONTINUATION RECORDS MANAGEMENT BRANCH (MNt!B 77141 US NUCLE AR
, REGULATORY COMMISSION, W ASHINGTON, DC 20b05 0001. AND TO THE PAPE RWORK REDUCT ION PROJECT (3160 01041, Of f sCE OF M ANAGI ME NT AND HUDGEI. WASHINGTON DC 20503.
i FACILITY NAME (1) DOCKET NUMBER (21 LER NUMBER 16) PAGE (3)
SL OUfNTIAL R[ VISION Brunswick Steam Electric Plant """"'" " " '"
05000324 4 of 4 Unit 2 92 - 001 - 01 TEXT W mcne space as re.7uked, use addmonalNRC form 366A's) (17) accumulators were reassen. bled and placed back in operation.
- 2. The accumulator testing frequency was increased to verify accumulator integrity.
l The increased frequency continued until the unit was shutdown in April, 1992.
- 3. Reactor power remained at a lower level to prevent the opening of TCv #4 which resulted in stable unit operation and eliminated abnormal EHC pressure oscillations.
The reduced power level continued until the unit was shutdown in April, 1992.
- 4. The causes f or errors made during the design and installation phases of the partial arc conversion modification were studied. Lessons learned were incorporated into redesign and repair activity. Af ter the April 1992 shutdown, the decision was made by plant management to return the Turbine to partial arc - 3 admission. This decision was based on the Stable operation of the unit during the first ten years when the unit was in partial arc -3 admission turbina operation. The modification was performed and the unit was able to achieve 100% operation without the previous oscillations experienced in partial arc - 2 admission.
SAFETY ASSESSMENT The saf ety significance of this event was minimal . Safety systems functioned as designed.
HPCI and RCIC initiated as required with RCIC injecting to restore vessel inventory. HPCI did not inject due to level recovery prior to the HPCI injection valve receiving an open signal.
PEEVIOUS SIMILAR EVENTS A previous similar event was reported in LER 1-90-017, Scram during TCV/TSV testing due to procedural and switch problems.
EIIS COMPONENT IDENTIFICATION System / Component EIIS Code ELECTROHYDRAULIC SYSTEM TG ACCUMULisTOR / SEAL ACC/ SEAL 3
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