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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000324/LER-1992-001, Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled1993-09-0202 September 1993 Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled 05000324/LER-1993-0081993-08-13013 August 1993 LER 93-008-00:on 930714,core Rated Thermal Power Exceeded Allowable Amount Due to Feedwater Flow Inaccuracy.Cause Believed to Be Due to Erosion/Corrosion of FW Flow Elements. FW Instrumentation recalibr.W/930812 Ltr 05000324/LER-1992-0101993-08-12012 August 1993 LER 92-010-01:on 921207,penetration Leakage Exceeded TS Allowable Limit Due to actuator-to-valve Alignment & disk-to-seat Alignment Problems.Line Bored Valve to Achieve concentricity.W/930812 Ltr 05000324/LER-1991-0191993-08-12012 August 1993 LER 91-019-01:on 911112,LLRT Failure of Two MSL Inboard & Outboard Isolation Valves Resulted in Condition Outside Design Basis.Root Cause Analysis in Process.Msls C & D Inboard & Outboard MSIVs Repairs complete.W/930812 Ltr 05000324/LER-1993-0031993-05-10010 May 1993 LER 93-003-00:on 930408,identified That Drywell Spray Outboard Isolation Valve Installed in Reverse Direction. Caused by Design & Installation Error.Appropriate Documents Will Be revised.W/930507 Ltr 05000324/LER-1988-0011990-08-0101 August 1990 LER 88-001-07:on 880102,manual Reactor Scram Occurred Due to Decreasing Main Condenser Vacuum.Reactor Power at 55% & Vacuum Decreased to 22 Inches Mercury.Caused by Leaks on Main Turbine Piping.Piping repaired.W/900801 Ltr 05000324/LER-1983-019, Updated LER 83-019/01T-2:on 830210,instrument Air Tubing to Safety Relief Valve/Automatic Depressurization Sys Valve Accumulator Inadequately Supported.Caused by Rerouted Tubing.Supports Installed1984-07-12012 July 1984 Updated LER 83-019/01T-2:on 830210,instrument Air Tubing to Safety Relief Valve/Automatic Depressurization Sys Valve Accumulator Inadequately Supported.Caused by Rerouted Tubing.Supports Installed 05000325/LER-1982-108, Updated LER 82-108/03L-1:on 821010 & 14,while Performing Automatic Depressurization Sys Valve Operability Test,Valves 1-B21-F013J & 1-B21-F013D & E Failed to Reclose.Caused by Faulty Spring.Valves Replaced1984-05-18018 May 1984 Updated LER 82-108/03L-1:on 821010 & 14,while Performing Automatic Depressurization Sys Valve Operability Test,Valves 1-B21-F013J & 1-B21-F013D & E Failed to Reclose.Caused by Faulty Spring.Valves Replaced 05000325/LER-1982-122, Supplemental LER 82-122/03L-1:on 821030 & 1104,reactor Recirculation Pump 1A Tripped.On 821101 & 04,reactor Recirculation Pump 1B Tripped.Caused by Spurious Action of ATWS Instrument B21-PS-N045C1984-04-0909 April 1984 Supplemental LER 82-122/03L-1:on 821030 & 1104,reactor Recirculation Pump 1A Tripped.On 821101 & 04,reactor Recirculation Pump 1B Tripped.Caused by Spurious Action of ATWS Instrument B21-PS-N045C 05000325/LER-1981-053, Updated LER 81-053/03L-1:on 810922,during Reactor Startup, Reactor Recirculation Pump 1B Tripped.Caused by Spurious Trip Signal from ATWS Low Water Level Instrument B21-LTM- NO24B-2.Instrument replaced.W/840329 Ltr1984-03-29029 March 1984 Updated LER 81-053/03L-1:on 810922,during Reactor Startup, Reactor Recirculation Pump 1B Tripped.Caused by Spurious Trip Signal from ATWS Low Water Level Instrument B21-LTM- NO24B-2.Instrument replaced.W/840329 Ltr 05000325/LER-1981-055, Updated LER 81-055/03L-1:on 820622,drywell Equipment Drain Flow Integrator 1-G16-FQ-K603 Continuously Indicated Dwed Sump Flow W/No Pumps Running.Caused by Water Being Introduced Into Pneumatic calibrator.W/840328 Ltr1984-03-28028 March 1984 Updated LER 81-055/03L-1:on 820622,drywell Equipment Drain Flow Integrator 1-G16-FQ-K603 Continuously Indicated Dwed Sump Flow W/No Pumps Running.Caused by Water Being Introduced Into Pneumatic calibrator.W/840328 Ltr 05000325/LER-1983-063, Updated LER 83-063/03L-1:on 831203,reactor Water Cleanup Sys (Rwcs) Differential Flow Indicator 1-G31-R615 Showed Erroneous Indication.On 831207,spurious Rwcs Alarm Annunciated.Caused by Air in Sensing lines.W/840222 Ltr1984-02-22022 February 1984 Updated LER 83-063/03L-1:on 831203,reactor Water Cleanup Sys (Rwcs) Differential Flow Indicator 1-G31-R615 Showed Erroneous Indication.On 831207,spurious Rwcs Alarm Annunciated.Caused by Air in Sensing lines.W/840222 Ltr 05000325/LER-1983-057, Updated LER 83-057/03L-1:on 831119,during Unit Power Performance,Temp Recorder TR-1258 Printed Erratically.Caused by Dirty Electrical Contacts in Control Board Timing Relay. Contacts Cleaned & Returned to svc.W/840222 Ltr1984-02-22022 February 1984 Updated LER 83-057/03L-1:on 831119,during Unit Power Performance,Temp Recorder TR-1258 Printed Erratically.Caused by Dirty Electrical Contacts in Control Board Timing Relay. Contacts Cleaned & Returned to svc.W/840222 Ltr 05000324/LER-1983-097, Updated LER 83-097/01T-1:on 831212,during Testing,Per IE Bulletin 83-02,crack Indications Discovered in 19 of 131 Welds in Reactor Recirculation & Reactor Water Cleanup Sys. Caused by Stress Corrosion Cracking1984-01-24024 January 1984 Updated LER 83-097/01T-1:on 831212,during Testing,Per IE Bulletin 83-02,crack Indications Discovered in 19 of 131 Welds in Reactor Recirculation & Reactor Water Cleanup Sys. Caused by Stress Corrosion Cracking 05000325/LER-1983-045, Updated LER 83-045/03L-2:on 830919 & 24,inboard PCIV Steam Supply Valve ES1-F007 to RCIC Sys Would Not Completely Reopen.Caused by Loose Limitorque Motor Operator Spring Pack1984-01-24024 January 1984 Updated LER 83-045/03L-2:on 830919 & 24,inboard PCIV Steam Supply Valve ES1-F007 to RCIC Sys Would Not Completely Reopen.Caused by Loose Limitorque Motor Operator Spring Pack 05000324/LER-1982-024, Updated LER 82-024/01T-1:on 820205,determined That Control Bldg Emergency Ventilation Sys Trains Will Not Isolate Upon Receipt of Chlorine Isolation Signal If Control Switch in on Position Due to Design Deficiency1983-11-14014 November 1983 Updated LER 82-024/01T-1:on 820205,determined That Control Bldg Emergency Ventilation Sys Trains Will Not Isolate Upon Receipt of Chlorine Isolation Signal If Control Switch in on Position Due to Design Deficiency 05000324/LER-1983-083, Updated LER 83-083/01T-1:on 830905,supply Valve 2-FP-V39 to Deluge Sys of Both Standby Gas Treatment Sys Discovered Shut.Caused by Operator Error.Valves Tagged for Identification.Auxiliary Operator Disciplined1983-09-23023 September 1983 Updated LER 83-083/01T-1:on 830905,supply Valve 2-FP-V39 to Deluge Sys of Both Standby Gas Treatment Sys Discovered Shut.Caused by Operator Error.Valves Tagged for Identification.Auxiliary Operator Disciplined 05000325/LER-1983-034, Updated LER 83-034/01T-1:on 830811,following Extended Maint & Refueling Outage,Instrument Isolation Valves to 1CAC-PDS-4222 & 4223 Discovered Closed.Caused by Cancelation of Equipment Clearance.Valves Reopened1983-09-12012 September 1983 Updated LER 83-034/01T-1:on 830811,following Extended Maint & Refueling Outage,Instrument Isolation Valves to 1CAC-PDS-4222 & 4223 Discovered Closed.Caused by Cancelation of Equipment Clearance.Valves Reopened 05000325/LER-1983-017, Updated LER 83-017/03L-1:on 830326-28 & 0402,listed Control Rods Had No Indications for Identified Positions.Caused by Loose Prototypic Inlet Piping Connectors Due to Undervessel Work.Connectors Will Be Properly Fastened1983-07-19019 July 1983 Updated LER 83-017/03L-1:on 830326-28 & 0402,listed Control Rods Had No Indications for Identified Positions.Caused by Loose Prototypic Inlet Piping Connectors Due to Undervessel Work.Connectors Will Be Properly Fastened 05000324/LER-1982-131, Supplemental LER 82-131/03L-1:on 821206,one-half Automatic Reactor Scram Signal Received Due to Instrument Downscale Signal from Main Steam Line Radiation Monitor D, 2-D12-RM-K603D.Caused by Disconnection of Instrument Cable1983-03-11011 March 1983 Supplemental LER 82-131/03L-1:on 821206,one-half Automatic Reactor Scram Signal Received Due to Instrument Downscale Signal from Main Steam Line Radiation Monitor D, 2-D12-RM-K603D.Caused by Disconnection of Instrument Cable 05000324/LER-1981-090, Updated LER 81-090/03L-3:on 810817 & 23,suppression Chamber Water Level Indicator 2-CAC-LI-2601-3 Indicated Lower Level & on 810820,indicated Higher Level than Other Indicator.Caused by Changes in Trickle Flow to Wet Ref Leg1983-01-28028 January 1983 Updated LER 81-090/03L-3:on 810817 & 23,suppression Chamber Water Level Indicator 2-CAC-LI-2601-3 Indicated Lower Level & on 810820,indicated Higher Level than Other Indicator.Caused by Changes in Trickle Flow to Wet Ref Leg 05000325/LER-1982-127, Updated LER 82-127/01T-1:on 821103,quick Start Testing of Diesel Generators 2,3 & 4 Not Performed for 12 H Period Per Tech Spec.Caused by Failure to Enter Requirement Into Daily Surveillance Rept on 821102.Testing Performed1982-12-23023 December 1982 Updated LER 82-127/01T-1:on 821103,quick Start Testing of Diesel Generators 2,3 & 4 Not Performed for 12 H Period Per Tech Spec.Caused by Failure to Enter Requirement Into Daily Surveillance Rept on 821102.Testing Performed 05000325/LER-1982-135, Supplemental LER 82-135/03L-1:on 821019,1.5-inch Discrepancy Noted Between Narrow & Wide Range Instruments.Caused by Inoperable RTGB Level Instruments.Plant Mod Package Developed to Increase Accuracy1982-12-23023 December 1982 Supplemental LER 82-135/03L-1:on 821019,1.5-inch Discrepancy Noted Between Narrow & Wide Range Instruments.Caused by Inoperable RTGB Level Instruments.Plant Mod Package Developed to Increase Accuracy 05000325/LER-1982-024, Supplemental LER 82-024/03L-2:on 820214,during Periodic Test,Discovered That Open Position Indication for Drywell to Suppression Vacuum Breaker X18H Could Not Be Achieved.Caused by Failure of Vacuum Breaker to Fully Stroke Open1982-10-13013 October 1982 Supplemental LER 82-024/03L-2:on 820214,during Periodic Test,Discovered That Open Position Indication for Drywell to Suppression Vacuum Breaker X18H Could Not Be Achieved.Caused by Failure of Vacuum Breaker to Fully Stroke Open ML20054L9761982-06-29029 June 1982 LER82-054/03L-0:on 820607,reactor Core Isolation Cooling Sys Turbine Automatically Started on Reactor Low Level,But Tripped Due to Closure of Control Valve 1-E51-V9.Caused by Lack of Turbine Speed Demand Signal Due to Governor Failure 05000325/LER-1982-0531982-06-29029 June 1982 LER 82-053/03L-0:on 820604,during startup,09 Position Found Superimposed on 00 RTGB Position Indication for Fully Inserted Control Rod 10-07.Caused by Defective Rod Position Reed Switch.Investigation Scheduled for 1982 Outage 05000325/LER-1981-092, Updated LER 81-092/01T-2:on 811226,action Statement 3.3.2b Not Entered When B21-LT-N017D-1 Instrument Failed Upscale. Caused by Failure of Operations Personnel to Recognize & Perform Required Action1982-06-21021 June 1982 Updated LER 81-092/01T-2:on 811226,action Statement 3.3.2b Not Entered When B21-LT-N017D-1 Instrument Failed Upscale. Caused by Failure of Operations Personnel to Recognize & Perform Required Action 05000325/LER-1981-093, Updated LER 81-093/01T-2:on 811226,reactor Protection Sys Vessel Low Level Trip instrument,1-B21-LT-NO17D-1,was Indicating Upscale.Caused by Personnel Failure to Recognize & Perform Tech Specs.Personnel Counseled1982-06-18018 June 1982 Updated LER 81-093/01T-2:on 811226,reactor Protection Sys Vessel Low Level Trip instrument,1-B21-LT-NO17D-1,was Indicating Upscale.Caused by Personnel Failure to Recognize & Perform Tech Specs.Personnel Counseled 05000325/LER-1982-038, Updated LER 82-038/03L-1:on 820419.Reactor Scrammed When Electrical Bus 1A-1 Dc de-energized.Caused by Operator Error in Opening 125-volt Dc Battery Charger Output Breaker for Battery 1A-1.Breaker Closed & Power Restored to Bus1982-06-0404 June 1982 Updated LER 82-038/03L-1:on 820419.Reactor Scrammed When Electrical Bus 1A-1 Dc de-energized.Caused by Operator Error in Opening 125-volt Dc Battery Charger Output Breaker for Battery 1A-1.Breaker Closed & Power Restored to Bus ML20062G3081978-12-21021 December 1978 /03L-0 on 781122:HPCI & RCIC Component Tests Were Overlooked Because Rescheduling Technique Provided No Clear Indication of Test Due Dates.Responsible Technician Reinstructed & Admin Operating Instruction AOI-5 Rev ML20064H8961978-12-19019 December 1978 /03L-0 on 781120:Senior Control Operator Did Not Have Completed Hatch Leak Rate Test Before Beginning Reactor Startup Due to Misunderstanding.Test completed.GP-1 Revised to Require Leak Test Verification by Control Operators ML20064H6181978-12-14014 December 1978 /03L-0 on 781114:torus Level of the HPCI Turbine Control Sys Was Slightly Above the Allowed 27 Inches.Proper Torus Level Restored to Normal.Torus Level Indicator Will Be More Clearly Marked ML20064H5971978-12-14014 December 1978 /03L-0 on 781114:Fire Hoses of Radwaste Bldg 3 Elevation Fire Stations Were Found Missing Due to Use by Personnel for Routine Radwaste Washdown.New Firehoses Installed & Mod Re Alternate Water Supply Is in Progress ML20064H5891978-12-14014 December 1978 /03L-0 on 781114:during Periodic Test 9.3.a the HPCI Egr Actuator Failed to Oper Properly Due to Water in Hydraulic Fluid Corroding Egr Actuator.Steam Leaking Past Seat of Valve HPCI E41-F001 Allowed Water Into Fluid ML20062F6781978-12-13013 December 1978 /03L-0 on 781112:reactor Steam Dome High Pressure Switch B32-PS-N018B Did Not Reset & Would Not Allow RHR Valve E11-F008 to Open for Shutdown Cooling at Reactor Pressure of 102psig.Caused by Sticking micro-switch ML20062F6681978-12-13013 December 1978 /03L-0 on 781117:while Reactor Was in Hot Shutdown Torus Level Increased .2 Above Tech Specs.Caused by Demineralized make-up Water Leakage Through Valves from RHR Keep-fill System Causing Torus Level to Rise ML20064G9301978-12-11011 December 1978 /03L-0 on 781109:Reactor Vessel Chemistry Exceeded Tech Spec Limits for Conductivity & Concentration Due to Presence of Organic Compounds in Condensate Sys.Organic Filtration & High Concentration of Ion Resin Cleanup Begun ML20062E4381978-11-30030 November 1978 /03L-0 on 781101:rod Block Monitor(Rbm) Channel a Was Found Out of Calibr During Testing Due to Setpoint Drift.Calibr Frequency Will Be Increased from Once to Twice Per Year ML20064E8001978-11-15015 November 1978 /03L-0 on 781017:reactor Bldg Radiat Exhaust Monitor D12-RM-N010B Failed Safe Causing Reactor Bldg Vent to Isolate,Due to Defective Transistor 2N1711 on 24V Pwr Supply ML20064E4581978-11-14014 November 1978 /01T-0 on 781101:util Was Informed by NRR of Nonconformance w/10CFR50 Append a Gen Design Criteria 54 & 56.Two Reactor bldg-to-torus Vacuum Breaker Lines Have Never Had Design Review by Nrc.Tech Spec Change Effective 781108 ML20064E3371978-11-0909 November 1978 /03L-0 on 781014:RCIC Turbine Was Tripped on Manual Overspeed for Training Purposes & Turbine control- Stop Valve E51-V8 Would Not Reset.Caused by Improperly Worn Adjusted Reset Lever ML20064E2921978-11-0909 November 1978 /03L-0 on 781011:torus Level Dropped Below Tech Spec Minimum While Water from Torus Was Being Pumped,Via Rgr to Radwaste in Efforts to Reduce Torus Water Level. Caused by Operator Being Distracted ML20064E3541978-11-0707 November 1978 /03L-0 on 781006:condensate Storage Tank Level Switch E41-LS-N003 Found Out of Calibration During Periodic Condensate Storage Tank Low Level Channel.Caused by Instru Drift ML20064E3491978-11-0606 November 1978 /03L-0 on 781105:Control Oper Received Control Rod Drift Alarm for Rod 10-31.When Rod Position Display Was Selected,A False 3 Was Superimposed on Actual Rod Position Due to Aground on the Rpls Probe ML20064D8211978-11-0202 November 1978 /03L-0 on 781004:pressure Switch E11-PS-NO16B Failed During Periods Plci Pump Discharges ADS Permissive Test,Due to Corrosion Buildup on Plunger of Switch ML20064C0151978-10-10010 October 1978 /03L-0 on 780911:during Monthly 1 Diesel Generator Load Test,It Was Found That 1 Cylinder Was Not Firing,Due to Faulty Fuel Pump ML20064C0011978-10-0909 October 1978 /03L-0 on 780911:Snubber SW-142SS164 Found Inoperable During Periodic Test.Caused by Seal Degradation & Resulting Loss of Fluid ML20147C9141978-10-0404 October 1978 /03L-0 on 780904:RCIC Isolation Channel a Tripped Momentarily,Causing RCIC Sys to Be Inoper,Due to Defective RX-2 Relay ML20062A0691978-10-0303 October 1978 /03L-0 on 780904:rod Block Monitor B Inoperative Trip Came on & Stayed on for 1/4 of the Control Rod Selection Matrix.Caused by Failed Integrated Circuit in Rod Block Monitor self-test Circuitry ML20064B7231978-10-0303 October 1978 /03L-0 on 780905:during Periodic Test,Radiat Monitor D12-RM-NO10B HI-HI Trip Point Drifted to Higher than Permitted Level.Monitor Recalibrated.Drift Appears to Be Isolated Incident;No Further Action Taken 1993-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N3271999-10-21021 October 1999 Part 21 Rept Re non-linear Oxygen Readings with Two (2) Model 225 CMA-X Containment Monitoring Sys at Bsep.Caused by High Gain Produced by 10K Resistor Across Second Stage Amplifier.Engineering Drawings Will Be Revised BSEP-99-0168, Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with ML20212D0431999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Brunswick Steam Electric Plant,Units 1 & 2 ML20210P9441999-08-10010 August 1999 Safety Evaluation Accepting Licensee Assessment of Impact on Operation of Plant,Unit 1,with Crack Indications of 2.11, 6.36 & 1.74 Inches in Three Separate Jet Pump Risers ML20210P9181999-08-10010 August 1999 Safety Evaluation Authorizing Request for Reliefs CIP-01,02, 06,07,08,09,10 & 11 (with Certain Exceptions) & 12-18,for Second 10-year ISI Interval.Request CIP-04 & 05 Would Result in hardship,CIP-03 Not Required & CIP-11 Denied in Part ML20210N2341999-08-0505 August 1999 SER Accepting Response to NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issues (USI) A-46 ML20210R1191999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Bsep,Units 1 & 2 ML20210R1311999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Bsep,Unit 2 BSEP-99-0118, Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with BSEP-99-0095, Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20210M8581999-05-14014 May 1999 B214R1 RPV Hydrotest Bolted Connection Corrective Action Evaluation, Rev 0 ML20211L3711999-05-10010 May 1999 Rev 0 to ESR 98-00333, Unit 2 Invessel Feedwater Sparger Evaluation ML20206G1871999-05-0404 May 1999 Safety Evaluation Approving Third 10-year ISI Program Requests for Relief (RR) RR-08,RR-15 & RR-17 BSEP-99-0075, Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With ML20206N1791999-04-23023 April 1999 Rev 0 to 2B21-0554, Brunswick Unit 2,Cycle 14 Colr BSEP-99-0059, Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20205F9031999-03-30030 March 1999 Safety Evaluation Supporting Proposed Rev to BSEP RERP to Licenses DPR-62 & DPR-71,respectively ML20206N1831999-02-28028 February 1999 Rev 0 to Suppl Reload Licensing Rept for Bsep,Unit 2 Reload 13 Cycle 14 BSEP-99-0043, Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20203D7061999-02-0909 February 1999 SER Accepting Proposed Alternatives Contained in Relief Requests PRR-04,VRR-04,VRR-13,PRR-01,PRR-03,VRR-01.VRR-07, VRR-08 & VRR-09 Denied BSEP-99-0005, Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0231, Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0218, Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with BSEP-98-0210, Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired1998-10-30030 October 1998 Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired ML20154P8151998-10-16016 October 1998 SER Accepting Revised Safety Analysis of Operational Transient of 920117,for Plant,Unit 1 ML20154P8591998-10-16016 October 1998 SER Accepting Equivalent Margins Analysis for N-16A/B Instrument Nozzles for Plant,Units 1 & 2 BSEP-98-0202, Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151Y6211998-09-14014 September 1998 BSEP Rept Describing Changes,Tests & Experiments, for Bsep,Units 1 & 2 ML20151Y6371998-09-14014 September 1998 Changes to QA Program, for Bsep,Units 1 & 2 BSEP-98-0185, Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151T5021998-08-0505 August 1998 Project Implementation Plan, Ngg Yr 2000 Readiness Program, Rev 2 BSEP-98-0164, Monthly Operating Repts for July 1998 for BSEP Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for BSEP Units 1 & 2 ML20236T1961998-07-0101 July 1998 Rev 1 to 2B21-0088, Brunswick Unit 2,Cycle 13 Colr ML20236T1921998-07-0101 July 1998 Rev 1 to 1B21-0537, Brunswick Unit 1,Cycle 12 Colr BSEP-98-0142, Monthly Operating Repts for June 1998 for BSEP Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for BSEP Units 1 & 2 ML20236T1971998-06-30030 June 1998 Rev 2 to 24A5412, Supplemental Reload Licensing Rept for Brunswick Steam Electric Plant Unit 2 Reload 12 Cycle 13 ML20249B9691998-06-11011 June 1998 Rev 1 to VC44.F02, Brunswick Steam Electric Plant,Units 1 & 2,ECCS Suction Strainers Replacement Project,Nrc Bulletin 96-003 Final Rept BSEP-98-0129, Monthly Operating Repts for May 1998 for Bsep,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Bsep,Units 1 & 2 ML20151S9041998-05-31031 May 1998 Revised Pages to Monthly Operating Rept for May 1998 for Brunswick Steam Electric Plant,Unit 1 BSEP-98-0104, Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 2 ML20151S8991998-04-30030 April 1998 Revised Pages to Monthly Operating Rept for Apr 1998 for Brunswick Steam Electric Plant,Unit 1 ML20247N7501998-04-30030 April 1998 Rev 0 to BSEP Unit 1,Cycle 12 Colr ML20247N7721998-04-30030 April 1998 Rev 0 to J1103244SRLR, Supplemental Reload Licensing Rept for BSEP Unit 1,Reload 11,Cycle 12 ML20217K8461998-04-24024 April 1998 Safety Evaluation Approving Proposed Use of Code Case N-535 at Brunswick Unit 1 During Second 10-yr Interval,Pursuant to 10CFR50.55a(a)(3)(i).Authorizes Use of Code Case N-535 Until Code Case Included in Future Rev of RG 1.147 ML20217K3941998-04-24024 April 1998 SER Approving Relief Request for Pump Vibration Monitoring, Brunswick Steam Electric Plant,Units 1 & 2 ML20217E6841998-04-23023 April 1998 Safety Evaluation Accepting Code Case N-547, Alternative Exam Requirements for Pressure Retaining Bolting of CRD Housings ML20217E7471998-04-21021 April 1998 Safety Evaluation Accepting Alternative to Insp of Reactor Pressure Vessel Circumferential Welds ML20217B5241998-04-20020 April 1998 SE Accepting Licensee Request for Approval to Use Alternative Exam Requirement for Brunswick,Unit 1,reactor Vessel Stud & Bushing During Second 10-yr ISI Interval Per 10CFR50.55a(a)(3)(ii) BSEP-98-0080, Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 2 ML20216B1041998-03-0404 March 1998 SER Approving Alternative to Insp of Reactor Pressure Vessel Circumferential Welds for Brunswick Steam Electric Plant, Unit 1 1999-09-30
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Carolina Poveer & Light Company $
armmesweremzmmmermawam Company Correspondence '
P. O. Box 10429 Southport, N.C. 28461-0429 MAY 071993 l
'i FILE: B09-13510C 10CFR50.73 Serial Not BSEP 93-0070 ,
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U.S. Nuclear Regulatory Commission {
ATTN Document Control Desk Washington, D. C. 20555
.)
i BRUNSWICK STEAM ELECTRIC PLANT UNIT 2 DOCKET NO. 50-324 j LICENSE NO. DPR-62 l LICENSEE EVENT REPORT 2-93-03 .. j n
Gentlemen:
p In accordance with Title 10 of the Code of Federal Regulations, the enclosed' [
Licensee Event Report is submitted. This report fulfills the requirement for.a : l t
written report within thirty (30) days of a reportable occurrence' and is !
submitted in accordance with the format set forth in NUREG-1022,L September 1983. !
Very truly yours, f 1
. M. Brown, Plant Manager - Unit'l '
Brunswick Nuclear Plant :
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Enclosure cc: Mr. S. D. Ebneter -]
Mr. P. D.~Milano. ;
i BSEP NRC Resident-Office l
J g5110313930510 !
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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROtfED OMB NO. 3150-0104
, (S/92) EXPIRES: 5/31/95 E STIMATED BURDEN PER RE SPONSE TO COMPLY WITH THIS INFORM ATION COLLECT 80N REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REr,ARD,NG URDEN EST, MATE To THt iNFoRuATioN AND PICDHDS MANAGEMENT BRANCH (MNBR 77141. U.S. NUCLE AR RE GULATORY COMMISSION. W ASHINGTON. DC PO555-DOO1, AND TO THE PAPERWORK REDUCTION PROJECT t3150 0104), OFFICE OF j MANAGEMENT AND BUDGET. WASHrNGTON, DC 20503.
FACILITY NAME (1) DOCKET NUVBER (2) PAGE{3l Brunswick Steam Electric Plant, Unit 2 05000324 1 of 5 TITLE d41 MISSED PRIMARY CONTAINMENT INTEGRITY SURVEILLANCE ON A BODY DRAIN VALVE FOR THE DRYWELL SPRAY OUTBOARD ISCLATION VALVE.
EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
M ONTH DAY YEAR YEAR M ONTH DAY YEAR NUMBER NJMBE R 05000 04 08 93 93 00 05 10 93 Faaun saut DOCKET NUMBER 05000 OPERATING THl3 REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 1: (Check one or more of the followingM11)
E MODE (9) 20 402M 20.405tc) 50.73(a)(2Hav) 73.71(b)
POWER l LEVEL (10) 000 50.as(cH2) 20.405(aH1 Hii) So.73ta)(2Hvii) OTHER 20 405(aH1Hiii) X 50.73taH2Hil 50.73(aH2HviiiHA) (Specify in Abstract 5
20.405(aH1Hiv) 50.73(aH2Hii) 50.73(aH2HviiiHB)
. 20.405taH1 Hv) 50 73(aH2Heiil 50.73(a)(2Hx)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER Theresa M. Jones, Regulatory Compliance Specialist (919) 457-2039 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
C A USE SYSTEM COMPONENT M ANUF A CTURE R CAUSE SYS EM COMPDNE NT MANUF ACTURER D O PD -
t SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED SUBMISSION ,
YES ire v. compiet. E APE CTED susMisS10N DATEi z
No DATE (15) !
ABSTRACT (Umst to 1400 spaces,i e. approximately fatteen single space typewritten lines) (16)
On April 8, 1993, with both units i- 'd shutdown, an engineering field inspection -
resulting from NRC concerns invol- t e surveillance of Primary Containment System Isolation (PCIS) valve vent and c .alves identified that the 2-E11-F016B, Drywell Spray Outboard Isolation Valve, was installed in the reverse direction. This ,
configuration exposed the associated body drain valve, 2-E11-V125, to primary containment pressure and thereby requires the valve to be periodically tested in accordance with the requirements of the Technical Specification. Because the installation configuration was not incorporated in the appropriate design documents, the 2-E11-V125 valve was not included in the PCIS valve surveillance program. Corrective actions include appropriate revisions to plant documentation to ensure the prcper classification and surveillance testing of the 2-E11-V125 valve and an examination of other plant installed PCIS throttle valves to ensure proper installation configuration.
1 The present configuration of the 2-E11-F016B resulted in the 2-E11-V125 being within the ;
Appendix "J" test boundary-. Testing of the 2-E11-F016B valve verified that any observed !
leakage was within the acceptance criteria and was included within the Primary l Containment Leakage total. Therefore, the installed configuration of the 2-E11-F016B does not create the potential for increased dose to the public.
i The cause classification for this event per the criteria of NUREG-1022 is (B) Design, '
Manufacturing, Construction / Installation.
NRC FORM 366A U. S. NUCLEAR REOULATORY COMMISSION APPROVED OMB NO. 3150-0104
, (5/92) EXP!RES: 5/31/95 E STIM ATED BURDEN PER RESPONSE TO COMPLY WITH THt$
INF ORM ATION COLLE CTION RE QUE ST: 60.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARomG euRoEN EsT,u ATE TO THE mFonMAnouNo TEXT CONTINUATION RE CORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAP RIGULATORY COMMISSION, WASHINGTON. DC 20555-0D01, AND TO THE PAPERWORK REDUCTlDN PROJECT (3150-01046, OFFICE OF M ANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (31 :
SE QUE NTIAL REVISION Brunswick Steam Electric Plant """ "" "
05000324 2 of 5' Unit 2 93 00 ,
A: .i
'EKT (1f rnare space is required, use additional NRC Form 366A's] (17)
TITLE MISSED PRIMARY CONTAINMENT INTEGRITY SURVEILLANCE ON A BODY DRAIN VALVE FOR THE DRYWELL SPRAY OUTBOARD ISOLATION VALVE. !
r INITIAL CONDITIONS Unit 2 was in COLD SHUTDOWN in day 352 of a dual unit outage. An NRC Operational Readiness Assessment Team (ORAT) was on site. A member of the NRC team questioned why certain vent and drain valves on valves which are part of ' the primary .
containment boundary are not included in Periodic Test (PT) 02.2.4a, Primary !
Containment Integrity Verification - Containment External.
PT-02.2.4a satisfies the PRIMARY CONTAINMENT INTEGRITY Technical Specification Surveillance 4.6.1.1.a . Technical Specification 4.6.1.1.a requires that integrity be demonstrated: ,
At least once per 31 days by verifying that all primary containment penetrations
- not capable of being closed by OPERABLE containment automatic -
isolation valves and required to be closed during accident conditions are closed by valves, blind flanges, or deactivated automatic valves secured in position, ...
The (*) allows certain valves, blind flanges and deactivated automatic valves which ,
are locked, sealed, or otherwise secured in the closed position in inaccessible areas, to be excepted from the 31 day verification and verified during each COLD ,
SHUTDOWh.
EVENT NARRATIVE ,
During a field inspection while responding to the NRC CRAT team member's question, ,
the System Engineer noted that the .2-E11-F016B, Drywell Spray Outboard Isolation l Valve, was installed in the reverse direction. This exposes the associated body i drain valve, 2-E11-V125, to primary containment pressure thereby requiring it to
.be verified in accordance with Technical Specification 4.6.1.1.a. On April 22, ;
1993, PT-02.2.4a was revised to include a surveillance of the 2-E11-V125. ;
The valves in question are globe valves. The design of globe valves results in the !
body drain valves for outboard globe valves being outside the primary containment ,
pressure boundary. Therefore, the body drain valves are not required to maintain ;
primary containment integrity and are not required to be tested in accordance with Technical Specification 4.6.1.1.a.
On June 21, 1974, the System Description, SD-12, Primary Containment Isolation ,
System, revision 00 was approved. The SD did not include the E11-V125. l On Septenber 9, 1974, a letter from United Engineers and Constructors Inc. (UE&C) was generated stating: l l
that valve 2-E11-F016B was installed so that normal flow is on top of i the valve disc instead of under the disc. . . contrary to that 1 prescribed by Anchor Valve Co. ... UE&C was requested to review this j problem and make recommendations... UE&C determined that ...
technically the valve will crerate creceriv and provide the thrcttlino
NRC FORM 366A U. S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104
, (5/92) EXPIRES: 5/31/95 E STIM ATED ttuRDEN PER RESPONSE TO COMPLY WITH THl$
INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMEWS uGA ,NG BUetN EST,M ATE 10 Tm ,,ORMolOuNo TEXT CONTINUATION M CO@S MANAGNEW BRANCH (MNEtB 77141. U.S. NUCLE AR P.iGULATOMY COMMISSION, WASHINGTON. DC 20$b5 0001, AND TO THE FAPERWORK REDUCTION PROJECT (3150-0104;. OFFICE OF MANAGEMENT AND BUDGET. % ASHINGTON. DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER 16) PAGE (3)
SE QUE NTIAL REVISION Brunswick Steam Electric Plant " " " " """
05000324 3 of 5 Unit 2 93 00
' EXT Uf more space is required, use additionalNRC Form 366A's) (17) capabilities required... Should it be required that the installation ,
of valve 2-E11-F016B be changed at this time, it could have a substantial schedule impact; therefore, UE&C recommends that valve 2-E11-F016B remain installed "as is".
The as installed valve configuration was not incorporated into design documents for future reference.
On January 13, 1980, PT-02.2.4, Primary Containment Isolation Valve verification, revision 00, was approved. This test included accessible and inaccessible valves and allowed for valves which were in ccessible during power operations to be marked "N/A". The test did not include a surveillance of 2-E11-V125.
On September 10, 1982, PT-02.2.4a, Primary Containment Integrity Verification -
Containment External, revision 00, was approved. The 2-E11-V125 valve was included for surveillance.
On September 14, 1982, The Report en the Accentability of the Primary Containment Isol ation Valves was approved. The report listed the 2-E11-V125 as a PCIS valve based on a conservative approach that generically incorporated body drain valves.
A revision to PT-02.2.4, revision 06, incorporated the report information and deleted the " accessible" (i.e. , external /31 day surveillance required) containment checks which the new PT-02.2.4a incorporated. ,
On August 24, 1983, SD-12, revision 04, was approved to incorporate the report information, including the determination that the 2-E11-V125 was considered a PCIS valve.
In 1989 a review of primary containment penetrations was conducted by System ,
Engineering to eliminate testing of valves which do not meet the PCIS valve criteria utilizing piping and instrument diagrams (P&ID). On December 29, 1989, s PT-02.2.4a. revision 17 was approved. The 2-E11-V125 was deleted from the procedure as a PCIS valve.
On March 27, 1990, SD-12, revision 14, was approved to incorporate the results of ;
the 1989 penetration review.
During the first quarter of 1991, a cross check of the Equipment Database System (EDBS) listing of PCIS valves and SD-12 was performed to support the addition of the PCIS valves to Regulatcry Compliance Instruction (RCI) 02.6, Cross Reference to Technical Specifications. The PCIS designator for 2-E11-V125 in EDBS was removed based on the fact that it was a body drain valve for a globe valve.
On April 15, 1993, an Engineering Work. Request (EWR) #12141 evaluating operability (
of the 2-E11-F016B configuration was approved. The EWR considered that 2-E11-F016B !
is a 10CFR50 Appendix "J" valve and is tested per the refueling /24 month cycle. ;
In its present configuration the 2-E11-V125 is a part of the test boundary. During ;
testing both valves are subjected to simulated accident pressures of 49 psig. The testing method used ensures. that any observed leakage is verified to meet the acceptance criteria and is included in the Primary Containment leakage total.
The Mechanical Analysis and Calculation for torque switch setting and seating thrust of the 2-E11-F016B has been revised to include the present installed configuration of the valve. Results of the VOTES testing performed this outage were reviewed against the newly revised calculations and the as left data was I determined to be within the rances specified in the calculation.
I
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NRC FORM 366A U. S, NUCLEAR REGULATORY COMMISSION APPROVED OMG NO. 3150-0104 (5/92) EXPIRES: 5/31/95 y ESTIMATED BURDEN PER RESPONSE TD C OMPLY WITH THIS INFORMATION COLLE CTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) cOMMtNTs RE o ARDiNo eURoE N ESTluATE TO THE iNFORu avion ANo RE C ORDS MANAGEMENT BRANCH IMNBB 7714), U.S. NUCLE AP TEXT CONTINUATION REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, W ASHINGTON, DC 20503.
FACIUTY NAME (1) DOCKET NUMBER th LER NUMBER 16) PAGE 13)
SE QUE NTIAL REVISION Brunswick Steam Electric Plant """"" """""
05000324 4 of 5 Unit 2 ,
93 00
' EXT (If enore space is required, use additionalNRC form 366A'sl (1h The present hydraulic characteristics were determined to be bounded by the original hydraulic calculation.
The ENR concluded that direction of flow through the subject valve has no significant effect on the valve's ability to perform its intended function and that the 2-E11-F016B and 2-E11-V125 should be considered operable.
On April 22, 19 9 3, PT- 02. 2 . 4 a , revision 27, was approved to incorporated the 2-E11-V125 for surveillance.
CAUSE OF EVENT The cause of this event is failure to incorporate the installation configuration in the appropriate design documents for future reference.
CORRECTIVE ACTIONS On April 22, 1993, PT-02.2.4a was revised to include a surveillance of the 2-E11-V125.
The appropriate plant documents will be revised to incorporate the 2-Ell-V125 as a PCIS valve by December 1, 1993.
The 1989 penetration review deleted outboard PCIS globe valve body drain valves from surveillance testing based on the assumption that the globe valve are installed with the designed orientation. The reverse installation of the 2-E11-F016B invalidated that assumption. Therefore, to revalidate the penetration review an examination of the Unit 1 and Unit 2 PCIS globe valves was performed. The results of this examination did not reveal any deficiencies.
SAFETY ASSESSMENT The present configuration of the 2-E11-F016B resulted in the 2-E11-V125 being within the Appendix 'J" test boundary. Testing of the 2-E11-F016B valve verified that any observed leakage was within the acceptance criteria and was included within the Primary Containment Leakage total. Therefore, the installed configuration of the 2-E11-F016B does not create the potential for increased dose to the public.
PREVIOUS SIMILAR EVENTS This is considered an isolated event, design information related to original improper design installation was not properly documented.
EIIS COMPONENT IDENTIFICATION Sys t em /Comoonqqt;. EIIS Code Containment Leakage Control System (PCIS) BD
. iNRp[ORM 300A - U. S. NUCLEAR REGULATORY COMMISSION ; APPROVED OME NO. 3150-0104
!15 '9 3 EAPIRES: 5/31/95
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' EXT tlf truire space os requerd. use additionalNRC form 36CA's! (17)
AT'ACHMENT 1 Globe Valve, Rising Stem Type >
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05000324/LER-1993-003 | LER 93-003-00:on 930408,identified That Drywell Spray Outboard Isolation Valve Installed in Reverse Direction. Caused by Design & Installation Error.Appropriate Documents Will Be revised.W/930507 Ltr | | 05000324/LER-1993-008 | LER 93-008-00:on 930714,core Rated Thermal Power Exceeded Allowable Amount Due to Feedwater Flow Inaccuracy.Cause Believed to Be Due to Erosion/Corrosion of FW Flow Elements. FW Instrumentation recalibr.W/930812 Ltr | |
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