11-04-2016 | On September 6, 2016 at 0827 EDT, with the reactor at approximately 91 percent core thermal power, operators manually scrammed the reactor when the benchmark for a reactor water level of +42 inches increasing was reached. Following the scram, all rods fully inserted and the Average Power Range Monitors were downscale, indicating the reactor was shut down. The Main Steam Isolation Valves closed on a Primary Containment Isolation Signal Group 1 isolation and were subsequently reopened to maintain reactor pressure.
The reason for the increasing reactor water level was the malfunction of Feedwater Regulating Valve 'A' (FRV 'A'). The reactor operator at the control panel placed FRV 'A' in remote manual in an attempt to stabilize the feedwater flow oscillations. This had no effect on the performance of FRV 'A'. The operators experienced feedwater flow oscillations from FRV 'A' that resulted in reactor water level high and low level alarms on the control panel. Shortly after this, the benchmark reactor water level of +42 inches increasing was reached and operators manually scrammed the reactor.
There was no impact to public health and safety. |
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Category:Letter
MONTHYEARML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status IR 05000293/20240022024-08-21021 August 2024 NRC Inspection Report No. 05000293/2024002 PNP 2024-030, Update Report for Holtec Decommissioning International Fleet Decommissioning Quality Assurance Program Rev. 3 and Palisades Transitioning Quality Assurance Plan, Rev 02024-08-0202 August 2024 Update Report for Holtec Decommissioning International Fleet Decommissioning Quality Assurance Program Rev. 3 and Palisades Transitioning Quality Assurance Plan, Rev 0 ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24129A1042024-05-26026 May 2024 Preapplication Readiness Assessment Plan for the Holtec Decommissioning International License Termination Plan ML24135A3212024-05-14014 May 2024 Annual Radioactive Effluent Release Report, January 1 Through December 31, 2023 ML24136A2382024-05-14014 May 2024 Annual Radiological Environmental Operating Report for 2023 IR 05000293/20240012024-05-0707 May 2024 NRC Inspection Report No. 05000293/2024001 L-24-009, HDI Annual Occupational Radiation Exposure Data Reports - 20232024-04-29029 April 2024 HDI Annual Occupational Radiation Exposure Data Reports - 2023 L-24-010, Request for Preapplication Readiness Assessment of the Draft License Termination Plan2024-04-22022 April 2024 Request for Preapplication Readiness Assessment of the Draft License Termination Plan L-24-007, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations – Holtec Decommissioning International, LLC (HDI)2024-03-29029 March 2024 Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations – Holtec Decommissioning International, LLC (HDI) IR 05000293/20230032024-02-29029 February 2024 NRC Inspection Report Nos. 05000293/2023003 and 05000293/2023004 L-24-002, Late LLRW Shipment Investigation Report Pursuant to 10 CFR 20, Appendix G2024-02-0202 February 2024 Late LLRW Shipment Investigation Report Pursuant to 10 CFR 20, Appendix G ML23342A1182024-01-0909 January 2024 Independent Spent Fuel Storage Installation Security Inspection Plan L-23-019, Proof of Financial Protection 10 CFR 140.152023-12-18018 December 2023 Proof of Financial Protection 10 CFR 140.15 ML23334A1822023-11-30030 November 2023 Biennial Report for the Defueled Safety Analysis Report Update, Technical Specification Bases Changes, 10 CFR 50.59 Evaluation Summary, and Regulatory Commitment Change Summary – November 2021 Through October 2023 L-23-012, Master Decommissioning Trust Agreement Changes for Indian Point Nuclear Generating Units 1, 2 and 3, Pilgrim Nuclear Power Station, Palisades Nuclear Plant and the Non-Qualified Trust for Big Rock Point2023-11-13013 November 2023 Master Decommissioning Trust Agreement Changes for Indian Point Nuclear Generating Units 1, 2 and 3, Pilgrim Nuclear Power Station, Palisades Nuclear Plant and the Non-Qualified Trust for Big Rock Point ML23306A0992023-11-0202 November 2023 And Indian Point Energy Center, Notification of Changes in Schedule in Accordance with 10 CFR 50.82(a)(7) ML23300A0022023-10-27027 October 2023 10 CFR 72.48 Biennial Change Summary Report IR 05000293/20234012023-08-31031 August 2023 NRC Inspection Report No. 05000293/2023401 & 2023001 (Cover Letter Only) IR 05000293/20230022023-08-0404 August 2023 NRC Inspection Report No. 05000293/2023002 ML23143A0872023-05-23023 May 2023 Correction to Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations – Holtec Decommissioning International, LLC (HDI) ML23135A2152023-05-15015 May 2023 Annual Radioactive Effluent Release Report, January 1 Through December 31, 2022 ML23136A7792023-05-15015 May 2023 Annual Radiological Environmental Operating Report, January 1 Through December 31, 2022 L-23-004, HDI Annual Occupational Radiation Exposure Data Reports - 20222023-04-24024 April 2023 HDI Annual Occupational Radiation Exposure Data Reports - 2022 L-23-003, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2023-03-31031 March 2023 Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations ML23088A0382023-03-29029 March 2023 Stations 1, 2, & 3, Palisades Nuclear Plant, and Big Rock Point - Nuclear Onsite Property Damage Insurance ML23069A2782023-03-13013 March 2023 Request for Scoping Comments Concerning the Environmental Review of Monticello Nuclear Generating Plant, Unit 1 Subsequent License Renewal Application ML22361A1022023-02-24024 February 2023 Reactor Decommissioning Branch Project Management Changes for Some Decommissioning Facilities and Establishment of Backup Project Manager for All Decommissioning Facilities IR 05000293/20220042023-02-15015 February 2023 NRC Inspection Report No. 05000293/2022004 ML22356A0712023-01-31031 January 2023 Issuance of Exemption for Pilgrim Nuclear Power Station ISFSI Regarding Annual Radioactive Effluent Release Report - Cover Letter ML22347A2782022-12-21021 December 2022 Independent Spent Fuel Storage Installation Security Inspection Plan Dated December 21, 2022 L-22-042, Oyster, Pilgrim, Indian Point, Palisades and Big Rock Point - Proof of Financial Protection 10 CFR 140.152022-12-14014 December 2022 Oyster, Pilgrim, Indian Point, Palisades and Big Rock Point - Proof of Financial Protection 10 CFR 140.15 L-22-041, Supplemental Information to Enhance Exemption Request Detail for Pilgrim ISFSI Annual Radioactive Effluent Release Report Due Date Extension2022-12-0909 December 2022 Supplemental Information to Enhance Exemption Request Detail for Pilgrim ISFSI Annual Radioactive Effluent Release Report Due Date Extension IR 05000293/20220032022-11-18018 November 2022 NRC Inspection Report No. 05000293/2022003 ML22276A1762022-10-24024 October 2022 Decommissioning International Proposed Revisions to the Quality Assurance Program Approval Forms for Radioactive Material Packages ML22266A1922022-09-23023 September 2022 And Pilgrim Nuclear Power Station - Request to Withdraw Prior Submissions from NRC Consideration ML22272A0352022-09-22022 September 2022 S. Lynch-Benttinen Letter Regarding U.S. Citizen Intent to Sue U.S. Fish and Wildlife and NOAA Fisheries Representing the Endangered Species (Na Right Whale) Which Will Be Adversely Affected by Holtec International Potential Actions ML22269A4202022-09-22022 September 2022 Citizen Lawsuit ML22241A1122022-08-29029 August 2022 Request for Exemption from 10 CFR 72.212(a)(2), (b)(2), (b)(3), (b)(4), (B)(5)(i), (b)(11), and 72.214 for Pilgrim ISFSI Annual Radioactive Effluent Release Report IR 05000293/20220022022-08-12012 August 2022 NRC Inspection Report No. 05000293/2022002 ML22215A1772022-08-0303 August 2022 Decommissioning International (HDI) Proposed Revisions to the Quality Assurance Program Approval Forms for Radioactive Material Packages ML22221A2592022-08-0101 August 2022 LTR-22-0217-1-NMSS - Town of Duxbury Letter Opposing the Irradiated Water Release from Pilgrim (Docket No. 05000293) ML22206A1512022-08-0101 August 2022 NRC Office of Investigations Case Nos. 1-2022-002 & 1-2022-006 ML22193A1662022-07-28028 July 2022 LTR-22-0154-1 - Heather Govern, VP, Clean Air and Water Program, Et Al., Letter Regarding Radioactive Wastewater Disposal from the Pilgrim Nuclear Power Station (Docket No. 05000293) ML22175A1732022-07-28028 July 2022 LTR-22-0153-1 - Response Letter to D. Turco, Cape Downwinders, from A. Roberts, NRC, Regarding Holtec-Pilgrim Plans to Dump One Million Gallons of Radioactive Waste Into Cape Cod Bay ML22154A4882022-06-0101 June 2022 Letter from Conservation Law Foundation Regarding Irradiated Water Release from Pilgrim ML22154A1622022-05-26026 May 2022 Letter and Email from Save Our Bay/Diane Turco Regarding Irradiated Water Release from Pilgrim ML22136A2602022-05-16016 May 2022 Submittal of Annual Radiological Environmental Operating Report for January 1 Through December 31, 2021 ML22136A2572022-05-16016 May 2022 Submittal of Annual Radioactive Effluent Release Report for January 1 Through December 31, 2021 2024-09-18
[Table view] Category:Licensee Event Report (LER)
MONTHYEARML18179A1632018-06-21021 June 2018 Retraction of Licensee Event Report 2018-002-00, Diesel Generator a Inoperability, a Condition Prohibited by the Plant Technical Specifications 05000293/LER-2017-0132018-01-25025 January 2018 1 OF 4, LER 17-013-00 for Pilgrim Nuclear Power Station Regarding Reportable Conditions Involving Standby Gas Treatment System and Secondary Containment lnoperability Not Reported During the Previous Three Years 05000293/LER-2017-0122017-11-13013 November 2017 Start-Up Transformer Degraded Voltage Relay Found Outside Technical Specification Limit, LER 17-012-00 for Pilgrim Nuclear Power Station Regarding Start-Up Transformer Degraded Voltage Relay Found Outside Technical Specification Limit 05000293/LER-2017-0112017-08-15015 August 2017 Simultaneously Opened Reactor Building Airlock Doors Caused Loss of Secondary Containment, LER 17-011-00 for Pilgrim Nuclear Power Station Regarding Simultaneously Opened Reactor Building Airlock Doors Caused Loss of Secondary Containment 05000293/LER-2017-0102017-08-0707 August 2017 Air Accumulation Creates Small Void in Core Spray Discharge Piping, LER 17-010-00 for Pilgrim re Air Accumulation Creates Small Void in Core Spray Discharge Piping 05000293/LER-2017-0012017-07-17017 July 2017 Reactor Building Isolation Dampers Failed to Isolate, LER 17-001-01 for Pilgrim Nuclear Power Station Regarding Reactor Building Isolation Dampers Failed to Isolate 05000293/LER-2017-0092017-07-17017 July 2017 Supplement to Potential Primary Containment System Inoperability Due to Relay Concerns, LER 17-009-00 for Pilgrim Nuclear Power Station Regarding Potential Primary Containment System lnoperability Due to Relay Concerns 05000293/LER-2017-0082017-06-30030 June 2017 Supplement to 480V Bus B6 Auto Transfer Function Degraded Due to Time Delay Relay Failure, LER 17-008-00 for Pilgrim re 480V Bus B6 Auto Transfer Function Degraded Due to Time Delay Relay Failure 05000293/LER-2017-0072017-06-22022 June 2017 Supplement to Potential Inoperability of Safety Relief Valve 3A, LER 17-007-00 for Pilgrim Regarding Potential Inoperability of Safety Relief Valve 3A 05000293/LER-2016-0102017-06-14014 June 2017 MSIV Inoperability Led to a Condition Prohibited by the Plant s Technical Specifications, LER 16-010-01 for Pilgrim Nuclear Power Station re MSIV Inoperability 05000293/LER-2017-0062017-06-13013 June 2017 Source Range Monitor Inoperable During Fuel Movement, LER 17-006-00 for Pilgrim Nuclear Power Station Regarding Source Range Monitor Inoperable During Fuel Movement 05000293/LER-2017-0052017-06-0707 June 2017 10 CFR 50, Appendix J, Option B, Leak Rate Criteria Exceeded, LER 17-005-00 for Pilgrim Regarding 10 CFR 50, Appendix J, Option B, Leak Rate Criteria Exceeded 05000293/LER-2017-0042017-06-0202 June 2017 Secondary Containment Testing Led to Loss of Safety Function to Both Trains of Standby Gas Treatment System, LER 17-004-00 for Pilgrim Nuclear Power Station Regarding Secondary Containment Testing Led to Loss of Safety Function to Both Trains of Standby Gas Treatment System 05000293/LER-2017-0022017-05-25025 May 2017 Isolation of HPCI, LER 17-002-00 for Pilgrim Regarding Isolation of HPCI 05000293/LER-2017-0032017-05-25025 May 2017 Supplement to Suppression Pool Declared Inoperable Due to High Water Level, LER 17-003-00 for Pilgrim Nuclear Power Station Regarding Pressure Suppression Pool Declared Inoperable Due to High Water Level 05000293/LER-2016-0082016-12-0909 December 2016 Emergency Diesel Generator 'A' Past Inoperability, LER 16-008-00 for Pilgrim Nuclear Power Station Regarding Emergency Diesel Generator 'A' Past Inoperability 05000293/LER-2016-0072016-11-0404 November 2016 Manual Reactor Scram Due To Feedwater Regulating Valve Malfunction, LER 16-007-00 for Pilgrim Nuclear Power Station Regarding Manual Reactor Scram Due To Feedwater Regulating Valve Malfunction 05000293/LER-2016-0032016-07-11011 July 2016 Spent Fuel Storage Design Feature Exceeded, LER 16-003-00 for Pilgrim Nuclear Power Station Regarding Spent Fuel Storage Design Feature Exceeded 05000293/LER-2016-0042016-07-11011 July 2016 Salt Service Water Pump B Past Operability - Operation or Condition Prohibited by Technical Specifications, LER 16-004-00 for Pilgrim Nuclear Power Station Regarding Salt Service Water Pump B Past Operability - Operation or Condition Prohibited by Technical Specifications 05000293/LER-2016-0022016-06-20020 June 2016 Online Maintenance Test Configuration Prohibited By Technical Specifications, LER 16-002-00 for Pilgrim Nuclear Power Station Regarding Online Maintenance Test Configuration Prohibited By Technical Specifications 05000293/LER-2016-0012016-06-0909 June 2016 Both Emergency Diesel Generators Inoperable, LER 16-001-00 for Pilgrim Nuclear Power Station Regarding Both Emergency Diesel Generators Inoperable ML13149A1722013-05-26026 May 2013 E-mail from Micheal Mulligan to R.Guzman, Pilgrim Evacuation Plan Broken During Blizzard Nemo and Unenforced by the Nrc. ML0613706222006-05-11011 May 2006 LER 06-01-000, Pilgrim Re Manual Scram Due to High Offgas Recombiner Temperature Resulting from Inadequate Preventive Recombiner Preheater Pressure Control Valve Controller ML0416706152004-06-0808 June 2004 LER 99-008-01 for Pilgrim Regarding Automatic Scram at 100 Percent Power Due to Turbine Trip ML0207700612002-02-27027 February 2002 LER 99-003-01 for Pilgrim Nuclear Power Station Re Local Leak Rate Test Results Exceeding Allowable Technical Specification Leakage Rates 2018-06-21
[Table view] |
The purpose of the feedwater level control system (FWLC) is to automatically control feedwater flow to the reactor vessel, maintaining vessel water level within a small range during all operating modes. During power generation, the FWLC system regulates feedwater flow maintaining proper water level in the reactor vessel according to the requirements for steam separator carryover and carry under through the entire reactor operating range. The FWLC system ensures sufficient sub-cooled water to the reactor vessel for jet pump and recirculation pump net positive suction head (NPSH) and to maintain normal operating temperatures during power operation.
The primary FWLC system purpose is to maintain reactor vessel water level within a small range during all operational modes. FWLC instrumentation measures reactor vessel water level, feedwater flowrate and exit steam flowrate. During automatic operation these three measurements are used to control feedwater flow.
The ability to maintain vessel level within a small range during load changes is accomplished by the three- element control signal. The total steam flow signal and the total feedwater flow signal are fed into a proportional amplifier. The output from this amplifier is the mismatch between the input signals (steam flow-feedwater flow error signal). If steam flow is greater than feedwater flow, the amplifier output is increased from its normal value, causing the system to increase feed flow to balance with steam flow. This amplifier output is fed to a second proportional amplifier that also receives a reactor vessel water level signal. Adding the reactor vessel water level signal to the steam flow-feedwater flow error signal results in a three-element control signal, which is fed to the level controller.
In May of 2015, during the refueling outage, new connectors on the encoder were installed. The new connectors were crimped onto the existing wires and inserted into the connection on the encoder. The valve was successfully post-work tested and returned to service. During the refueling outage, valve testing on the FRV 'A' was completed, including a pressure drop test on the actuator. However, due to a poorly written test procedure, anomalies were not properly identified or addressed as described below.
During a reactor downpower on October 20 and 21, 2015, a packing leak was identified on FRV 'A'. This resulted in exposing the valve manual locking device to unfavorable conditions which eventually led to degradation of the valve locking mechanism couplings and bearings. The valve packing was adjusted to reduce the packing leak.
EVENT DESCRIPTION
At 07:55 on September 6, 2016, the control room received an instantaneous core thermal power (CTP) blinking annunciator light. This was the first indication to the control room operators that there was a problem.
At 08:00 operations received an alarm for thermal power due to suspect value (feedwater flow).
At 08:10 operators placed FRV 'A' in remote manual. Three unsuccessful attempts were made to manually control the valve.
At 08:14 operators were dispatched to the Condenser Bay to lockup FRV 'A' in accordance with procedure. The control room operators established scram benchmarks of +15 inches lowering, +42 inches increasing reactor At 08:20 an operator at the local digital control panel identified Error message for Friction Warnings and proceeds to FRV 'A' to lockup the valve.
At 08:21 operators at FRV `A' cannot operate the mechanical operator due to degraded condition of the actuator.
At 08:25 FRV 'A' goes full open while operators are located at the valve.
At 08:26:12, a "Friction Failure" error message was received at the local digital control panel.
At 08:26:28 operators in the control room received an alarm for reactor water level high.
At 08:27 operators manually scrammed the reactor at a water level of +42 inches increasing and received APRM downscale with all rods in.
CAUSE OF THE EVENT
The direct cause of this event is the neutral common wire lost connection to the encoder stab on the stepper motor resulting in a loss of feedback to the control system for the valve.
The causes of the event are that the work package quality standards for critical maintenance work order package planning were not known or understood by some planning personnel. This resulted in the inadequate installation, during the May 2015 refueling outage, of the neutral common wire that became loose and lost connection between the encoder and the digital controller. In addition, the air operated valve testing procedure for the FRVs did not contain criteria for valve packing friction or stem load evaluation. This resulted in a missed opportunity to identify and correct the valve packing leakage condition and the degraded condition of the mechanical locking device prior to the event.
CORRECTIVE ACTIONS
The following corrective actions were performed:
1) Replaced the FRV 'A' valve stem 2) Replaced the FRV 'A' and FRV B' valve packing 3) Refurbished the FRV `A' manual actuator 4) Reassembled the encoder electrical connector 5) Performed a pull test of each individual wire in the encoder electrical connection satisfactorily before the connector was reinstalled and sealed in place for both FRV 'A' and T3'.
The following corrective actions are currently planned to be performed:
1) Generate a maintenance planning standards checklist for critical maintenance work package quality and train maintenance planners on use of the new checklist.
2) Train station personnel in problem identification and resolution.
3) Train operating crews and station leadership on the event, causes and corrective actions. '
SAFETY CONSEQUENCES
The actual consequences were a loss of ability to control FRV 'A' which resulted in increasing reactor water level and an operator-initiated manual scram. There were no other actual consequences to general safety of the public, nuclear safety, industrial safety, and radiological safety for this event.
The potential consequences to general safety of the public, nuclear safety, industrial safety, and radiological safety of this event if the operator-initiated manual scram did not occur were minimal. Had the manual scram not been initiated, in a short time there would have been an automatic turbine trip, feedwater pump trip, and Primary Containment Isolation Signal Group 1 isolation from the high reactor water level condition. These automatic actions would have immediately caused an automatic reactor Scram.
The conditional core damage probability of this event has been estimated to be 3.49E-06. This is the value associated with a Main Steam Isolation Valve (MSIV) isolation initiator. The risk from the actual event was less than this calculated value because the Scram was manually initiated prior to the turbine trip and other automatic actions. The scram was considered uncomplicated as defined in Nuclear Energy Institute 99-02.
Therefore, based on the above there was no adverse impact on the public health or safety.
REPORTABILITY
This report is submitted in accordance with 10 CFR 50.73(a)(2)(iv)(A). Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B) of this section including 50.73(a)(2)(iv)(B)(2), general containment isolation signals affecting containment isolation valves in more than one system or multiple MSIVs.
PREVIOUS EVENTS
A review of Pilgrim Nuclear Power Station Licensee Event Reports for the past five years did not identify any similar occurrences of manual scrams being initiated by feedwater oscillations.
ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES The EIIS codes for Components and Systems referenced in this report are as follows:
SYSTEMS CODES
Feedwater System SJ
REFERENCES:
CR-PNP-2016-6635
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05000293/LER-2016-010 | MSIV Inoperability Led to a Condition Prohibited by the Plant s Technical Specifications LER 16-010-01 for Pilgrim Nuclear Power Station re MSIV Inoperability | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000293/LER-2016-001 | Both Emergency Diesel Generators Inoperable LER 16-001-00 for Pilgrim Nuclear Power Station Regarding Both Emergency Diesel Generators Inoperable | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | 05000293/LER-2016-002 | Online Maintenance Test Configuration Prohibited By Technical Specifications LER 16-002-00 for Pilgrim Nuclear Power Station Regarding Online Maintenance Test Configuration Prohibited By Technical Specifications | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System | 05000293/LER-2016-003 | Spent Fuel Storage Design Feature Exceeded LER 16-003-00 for Pilgrim Nuclear Power Station Regarding Spent Fuel Storage Design Feature Exceeded | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000293/LER-2016-004 | Salt Service Water Pump B Past Operability - Operation or Condition Prohibited by Technical Specifications LER 16-004-00 for Pilgrim Nuclear Power Station Regarding Salt Service Water Pump B Past Operability - Operation or Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2016-005 | Ultimate Heat Sink and Salt Service Water System Declared Inoperable | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000293/LER-2016-006 | 1 OF 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2016-007 | Manual Reactor Scram Due To Feedwater Regulating Valve Malfunction LER 16-007-00 for Pilgrim Nuclear Power Station Regarding Manual Reactor Scram Due To Feedwater Regulating Valve Malfunction | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000293/LER-2016-008 | Emergency Diesel Generator 'A' Past Inoperability LER 16-008-00 for Pilgrim Nuclear Power Station Regarding Emergency Diesel Generator 'A' Past Inoperability | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2016-009 | HPCI Declared Inoperable Due to Failure of 1ST Surveillance Test | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident |
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