08-03-2017 | On June 6, 2017, at 1357 [EDT] with the reactor at 100% core thermal power and steady state conditions, plant personnel were performing Ultrasonic testing ( UT) examination on Core Spray A high point piping in the A Residual Heat Removal Quad to ensure this piping was water solid, when they identified that the top of this horizontal pipe had an air void internally. A high point vent line with valves is located in the area of the UT exam.
It was found that the top 2 inches of the 10 inch core spray pump discharge line had accumulated an air void within the known inverted loop in Core Spray Loop-A discharge line. The system had been drained for maintenance during the Refueling Outage.
Pilgrim Nuclear Power Station is reporting this event pursuant to 10 CFR 50.73(a)(2)(i)(B), as a condition prohibited by Technical Specifications. Although upon discovery the proper Limiting Condition for Operation Action Statement was entered and the void was filled immediately to correct the issue, it is believed that this condition existed before the time of discovery for a period of time longer than that allowed by Technical Specifications.
This event posed no threat to public health and safety. |
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LER-2017-000, Air Accumulation Creates Small Void in Core Spray Discharge Piping |
Event date: |
06-07-2017 |
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Report date: |
08-03-2017 |
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Reporting criterion: |
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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2932017000R00 - NRC Website |
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Category:Letter
MONTHYEARML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status IR 05000293/20240022024-08-21021 August 2024 NRC Inspection Report No. 05000293/2024002 PNP 2024-030, Update Report for Holtec Decommissioning International Fleet Decommissioning Quality Assurance Program Rev. 3 and Palisades Transitioning Quality Assurance Plan, Rev 02024-08-0202 August 2024 Update Report for Holtec Decommissioning International Fleet Decommissioning Quality Assurance Program Rev. 3 and Palisades Transitioning Quality Assurance Plan, Rev 0 ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24129A1042024-05-26026 May 2024 Preapplication Readiness Assessment Plan for the Holtec Decommissioning International License Termination Plan ML24135A3212024-05-14014 May 2024 Annual Radioactive Effluent Release Report, January 1 Through December 31, 2023 ML24136A2382024-05-14014 May 2024 Annual Radiological Environmental Operating Report for 2023 IR 05000293/20240012024-05-0707 May 2024 NRC Inspection Report No. 05000293/2024001 L-24-009, HDI Annual Occupational Radiation Exposure Data Reports - 20232024-04-29029 April 2024 HDI Annual Occupational Radiation Exposure Data Reports - 2023 L-24-010, Request for Preapplication Readiness Assessment of the Draft License Termination Plan2024-04-22022 April 2024 Request for Preapplication Readiness Assessment of the Draft License Termination Plan L-24-007, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations – Holtec Decommissioning International, LLC (HDI)2024-03-29029 March 2024 Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations – Holtec Decommissioning International, LLC (HDI) IR 05000293/20230032024-02-29029 February 2024 NRC Inspection Report Nos. 05000293/2023003 and 05000293/2023004 L-24-002, Late LLRW Shipment Investigation Report Pursuant to 10 CFR 20, Appendix G2024-02-0202 February 2024 Late LLRW Shipment Investigation Report Pursuant to 10 CFR 20, Appendix G ML23342A1182024-01-0909 January 2024 Independent Spent Fuel Storage Installation Security Inspection Plan L-23-019, Proof of Financial Protection 10 CFR 140.152023-12-18018 December 2023 Proof of Financial Protection 10 CFR 140.15 ML23334A1822023-11-30030 November 2023 Biennial Report for the Defueled Safety Analysis Report Update, Technical Specification Bases Changes, 10 CFR 50.59 Evaluation Summary, and Regulatory Commitment Change Summary – November 2021 Through October 2023 L-23-012, Master Decommissioning Trust Agreement Changes for Indian Point Nuclear Generating Units 1, 2 and 3, Pilgrim Nuclear Power Station, Palisades Nuclear Plant and the Non-Qualified Trust for Big Rock Point2023-11-13013 November 2023 Master Decommissioning Trust Agreement Changes for Indian Point Nuclear Generating Units 1, 2 and 3, Pilgrim Nuclear Power Station, Palisades Nuclear Plant and the Non-Qualified Trust for Big Rock Point ML23306A0992023-11-0202 November 2023 And Indian Point Energy Center, Notification of Changes in Schedule in Accordance with 10 CFR 50.82(a)(7) ML23300A0022023-10-27027 October 2023 10 CFR 72.48 Biennial Change Summary Report IR 05000293/20234012023-08-31031 August 2023 NRC Inspection Report No. 05000293/2023401 & 2023001 (Cover Letter Only) IR 05000293/20230022023-08-0404 August 2023 NRC Inspection Report No. 05000293/2023002 ML23143A0872023-05-23023 May 2023 Correction to Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations – Holtec Decommissioning International, LLC (HDI) ML23135A2152023-05-15015 May 2023 Annual Radioactive Effluent Release Report, January 1 Through December 31, 2022 ML23136A7792023-05-15015 May 2023 Annual Radiological Environmental Operating Report, January 1 Through December 31, 2022 L-23-004, HDI Annual Occupational Radiation Exposure Data Reports - 20222023-04-24024 April 2023 HDI Annual Occupational Radiation Exposure Data Reports - 2022 L-23-003, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2023-03-31031 March 2023 Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations ML23088A0382023-03-29029 March 2023 Stations 1, 2, & 3, Palisades Nuclear Plant, and Big Rock Point - Nuclear Onsite Property Damage Insurance ML23069A2782023-03-13013 March 2023 Request for Scoping Comments Concerning the Environmental Review of Monticello Nuclear Generating Plant, Unit 1 Subsequent License Renewal Application ML22361A1022023-02-24024 February 2023 Reactor Decommissioning Branch Project Management Changes for Some Decommissioning Facilities and Establishment of Backup Project Manager for All Decommissioning Facilities IR 05000293/20220042023-02-15015 February 2023 NRC Inspection Report No. 05000293/2022004 ML22356A0712023-01-31031 January 2023 Issuance of Exemption for Pilgrim Nuclear Power Station ISFSI Regarding Annual Radioactive Effluent Release Report - Cover Letter ML22347A2782022-12-21021 December 2022 Independent Spent Fuel Storage Installation Security Inspection Plan Dated December 21, 2022 L-22-042, Oyster, Pilgrim, Indian Point, Palisades and Big Rock Point - Proof of Financial Protection 10 CFR 140.152022-12-14014 December 2022 Oyster, Pilgrim, Indian Point, Palisades and Big Rock Point - Proof of Financial Protection 10 CFR 140.15 L-22-041, Supplemental Information to Enhance Exemption Request Detail for Pilgrim ISFSI Annual Radioactive Effluent Release Report Due Date Extension2022-12-0909 December 2022 Supplemental Information to Enhance Exemption Request Detail for Pilgrim ISFSI Annual Radioactive Effluent Release Report Due Date Extension IR 05000293/20220032022-11-18018 November 2022 NRC Inspection Report No. 05000293/2022003 ML22276A1762022-10-24024 October 2022 Decommissioning International Proposed Revisions to the Quality Assurance Program Approval Forms for Radioactive Material Packages ML22266A1922022-09-23023 September 2022 And Pilgrim Nuclear Power Station - Request to Withdraw Prior Submissions from NRC Consideration ML22272A0352022-09-22022 September 2022 S. Lynch-Benttinen Letter Regarding U.S. Citizen Intent to Sue U.S. Fish and Wildlife and NOAA Fisheries Representing the Endangered Species (Na Right Whale) Which Will Be Adversely Affected by Holtec International Potential Actions ML22269A4202022-09-22022 September 2022 Citizen Lawsuit ML22241A1122022-08-29029 August 2022 Request for Exemption from 10 CFR 72.212(a)(2), (b)(2), (b)(3), (b)(4), (B)(5)(i), (b)(11), and 72.214 for Pilgrim ISFSI Annual Radioactive Effluent Release Report IR 05000293/20220022022-08-12012 August 2022 NRC Inspection Report No. 05000293/2022002 ML22215A1772022-08-0303 August 2022 Decommissioning International (HDI) Proposed Revisions to the Quality Assurance Program Approval Forms for Radioactive Material Packages ML22221A2592022-08-0101 August 2022 LTR-22-0217-1-NMSS - Town of Duxbury Letter Opposing the Irradiated Water Release from Pilgrim (Docket No. 05000293) ML22206A1512022-08-0101 August 2022 NRC Office of Investigations Case Nos. 1-2022-002 & 1-2022-006 ML22193A1662022-07-28028 July 2022 LTR-22-0154-1 - Heather Govern, VP, Clean Air and Water Program, Et Al., Letter Regarding Radioactive Wastewater Disposal from the Pilgrim Nuclear Power Station (Docket No. 05000293) ML22175A1732022-07-28028 July 2022 LTR-22-0153-1 - Response Letter to D. Turco, Cape Downwinders, from A. Roberts, NRC, Regarding Holtec-Pilgrim Plans to Dump One Million Gallons of Radioactive Waste Into Cape Cod Bay ML22154A4882022-06-0101 June 2022 Letter from Conservation Law Foundation Regarding Irradiated Water Release from Pilgrim ML22154A1622022-05-26026 May 2022 Letter and Email from Save Our Bay/Diane Turco Regarding Irradiated Water Release from Pilgrim ML22136A2602022-05-16016 May 2022 Submittal of Annual Radiological Environmental Operating Report for January 1 Through December 31, 2021 ML22136A2572022-05-16016 May 2022 Submittal of Annual Radioactive Effluent Release Report for January 1 Through December 31, 2021 2024-09-18
[Table view] Category:Licensee Event Report (LER)
MONTHYEARML18179A1632018-06-21021 June 2018 Retraction of Licensee Event Report 2018-002-00, Diesel Generator a Inoperability, a Condition Prohibited by the Plant Technical Specifications 05000293/LER-2017-0132018-01-25025 January 2018 1 OF 4, LER 17-013-00 for Pilgrim Nuclear Power Station Regarding Reportable Conditions Involving Standby Gas Treatment System and Secondary Containment lnoperability Not Reported During the Previous Three Years 05000293/LER-2017-0122017-11-13013 November 2017 Start-Up Transformer Degraded Voltage Relay Found Outside Technical Specification Limit, LER 17-012-00 for Pilgrim Nuclear Power Station Regarding Start-Up Transformer Degraded Voltage Relay Found Outside Technical Specification Limit 05000293/LER-2017-0112017-08-15015 August 2017 Simultaneously Opened Reactor Building Airlock Doors Caused Loss of Secondary Containment, LER 17-011-00 for Pilgrim Nuclear Power Station Regarding Simultaneously Opened Reactor Building Airlock Doors Caused Loss of Secondary Containment 05000293/LER-2017-0102017-08-0707 August 2017 Air Accumulation Creates Small Void in Core Spray Discharge Piping, LER 17-010-00 for Pilgrim re Air Accumulation Creates Small Void in Core Spray Discharge Piping 05000293/LER-2017-0012017-07-17017 July 2017 Reactor Building Isolation Dampers Failed to Isolate, LER 17-001-01 for Pilgrim Nuclear Power Station Regarding Reactor Building Isolation Dampers Failed to Isolate 05000293/LER-2017-0092017-07-17017 July 2017 Supplement to Potential Primary Containment System Inoperability Due to Relay Concerns, LER 17-009-00 for Pilgrim Nuclear Power Station Regarding Potential Primary Containment System lnoperability Due to Relay Concerns 05000293/LER-2017-0082017-06-30030 June 2017 Supplement to 480V Bus B6 Auto Transfer Function Degraded Due to Time Delay Relay Failure, LER 17-008-00 for Pilgrim re 480V Bus B6 Auto Transfer Function Degraded Due to Time Delay Relay Failure 05000293/LER-2017-0072017-06-22022 June 2017 Supplement to Potential Inoperability of Safety Relief Valve 3A, LER 17-007-00 for Pilgrim Regarding Potential Inoperability of Safety Relief Valve 3A 05000293/LER-2016-0102017-06-14014 June 2017 MSIV Inoperability Led to a Condition Prohibited by the Plant s Technical Specifications, LER 16-010-01 for Pilgrim Nuclear Power Station re MSIV Inoperability 05000293/LER-2017-0062017-06-13013 June 2017 Source Range Monitor Inoperable During Fuel Movement, LER 17-006-00 for Pilgrim Nuclear Power Station Regarding Source Range Monitor Inoperable During Fuel Movement 05000293/LER-2017-0052017-06-0707 June 2017 10 CFR 50, Appendix J, Option B, Leak Rate Criteria Exceeded, LER 17-005-00 for Pilgrim Regarding 10 CFR 50, Appendix J, Option B, Leak Rate Criteria Exceeded 05000293/LER-2017-0042017-06-0202 June 2017 Secondary Containment Testing Led to Loss of Safety Function to Both Trains of Standby Gas Treatment System, LER 17-004-00 for Pilgrim Nuclear Power Station Regarding Secondary Containment Testing Led to Loss of Safety Function to Both Trains of Standby Gas Treatment System 05000293/LER-2017-0022017-05-25025 May 2017 Isolation of HPCI, LER 17-002-00 for Pilgrim Regarding Isolation of HPCI 05000293/LER-2017-0032017-05-25025 May 2017 Supplement to Suppression Pool Declared Inoperable Due to High Water Level, LER 17-003-00 for Pilgrim Nuclear Power Station Regarding Pressure Suppression Pool Declared Inoperable Due to High Water Level 05000293/LER-2016-0082016-12-0909 December 2016 Emergency Diesel Generator 'A' Past Inoperability, LER 16-008-00 for Pilgrim Nuclear Power Station Regarding Emergency Diesel Generator 'A' Past Inoperability 05000293/LER-2016-0072016-11-0404 November 2016 Manual Reactor Scram Due To Feedwater Regulating Valve Malfunction, LER 16-007-00 for Pilgrim Nuclear Power Station Regarding Manual Reactor Scram Due To Feedwater Regulating Valve Malfunction 05000293/LER-2016-0032016-07-11011 July 2016 Spent Fuel Storage Design Feature Exceeded, LER 16-003-00 for Pilgrim Nuclear Power Station Regarding Spent Fuel Storage Design Feature Exceeded 05000293/LER-2016-0042016-07-11011 July 2016 Salt Service Water Pump B Past Operability - Operation or Condition Prohibited by Technical Specifications, LER 16-004-00 for Pilgrim Nuclear Power Station Regarding Salt Service Water Pump B Past Operability - Operation or Condition Prohibited by Technical Specifications 05000293/LER-2016-0022016-06-20020 June 2016 Online Maintenance Test Configuration Prohibited By Technical Specifications, LER 16-002-00 for Pilgrim Nuclear Power Station Regarding Online Maintenance Test Configuration Prohibited By Technical Specifications 05000293/LER-2016-0012016-06-0909 June 2016 Both Emergency Diesel Generators Inoperable, LER 16-001-00 for Pilgrim Nuclear Power Station Regarding Both Emergency Diesel Generators Inoperable ML13149A1722013-05-26026 May 2013 E-mail from Micheal Mulligan to R.Guzman, Pilgrim Evacuation Plan Broken During Blizzard Nemo and Unenforced by the Nrc. ML0613706222006-05-11011 May 2006 LER 06-01-000, Pilgrim Re Manual Scram Due to High Offgas Recombiner Temperature Resulting from Inadequate Preventive Recombiner Preheater Pressure Control Valve Controller ML0416706152004-06-0808 June 2004 LER 99-008-01 for Pilgrim Regarding Automatic Scram at 100 Percent Power Due to Turbine Trip ML0207700612002-02-27027 February 2002 LER 99-003-01 for Pilgrim Nuclear Power Station Re Local Leak Rate Test Results Exceeding Allowable Technical Specification Leakage Rates 2018-06-21
[Table view] |
comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
Pilgrim Nuclear Power Station 05000-293 2017 - 00
BACKGROUND
Air/gas in discharge piping can be an indicator of potential back-leakage from high-pressure sources such as accumulators or the Reactor Coolant System, and the gas may have moved into the pumps and the pump suction piping. Such gas may have flowed through multiple closed in-series valves. For this reason, it is important to reassess air/gas accumulation conditions following system operations and valve manipulations.
(Reference NRC Generic Letter 2008-01).
EVENT DESCRIPTION
While performing Ultrasonic testing (UT) examination on Core Spray A high point piping in the A Residual Heat Removal Quad to ensure this piping was water solid, it was identified that the horizontal pipe had an air void internally. This piping goes through the concrete wall at this location and into the Torus room. A high point vent line with valves is located in the area of the UT exam. It was found that the top 2 inches of the 10 inch core spray pump discharge line had accumulated an air void within the known inverted loop in Core Spray Loop-A discharge line.
CAUSE OF THE EVENT
The air volume was likely introduced into the system as a consequence of inadequate guidance in procedure 2.2.20, Core Spray, which does not provide task specific directions for fill and vent of the Core Spray system to restore from a draindown.
The information for filling and venting the system was contained in one Section of the procedure and in two Attachments, but it was not compiled in one place that was readily accessible to the Operator performing the procedure. The lack of guidance provided an error trap when system restoration was being performed.
CORRECTIVE ACTIONS
The immediate corrective action was to vent the air from the 10 inch Core Spray Pump discharge line that had accumulated an air void within the known inverted loop in Core Spray Loop-A Discharge Line.
The follow-up UT exam was performed and determined that the Core Spray Loop-A discharge piping was water solid with no evidence of air present. Core Spray Loop-A is OPERABLE.
Procedure 2.2.20, Core Spray, will be revised to provide specific guidance to fill and vent the Core Spray system following maintenance requiring a system draindown, or any activity requiring a system breach.
- 010 comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
Pilgrim Nuclear Power Station 05000-293 2017 - 00 - 010
SAFETY CONSEQUENCES
There were no consequences to the safety of the general public, nuclear safety, industrial safety, or radiological safety due to this event. For the purpose of evaluating the potential consequences of the as-found void volume, the measured void volume was compared to the Maximum Allowable Void Criteria that was established for this purpose. These criteria are used only for functionality determinations if voids are detected. The void volume did not exceed the maximum allowable void criteria. Therefore, the Core Spray system would have been capable of performing all of it specified safety functions.
No actions to reduce the frequency or consequence are necessary.
REPORTABILITY
Pilgrim Nuclear Power Station (PNPS) is reporting this event pursuant to 10 CFR 50.73(a)(2)(i)(B), as a condition prohibited by Technical Specifications (TS). Although upon discovery the proper Limiting Condition for Operation Action Statement was entered and the void was filled immediately to correct the issue, it is believed that this condition existed before the time of discovery for a period of time longer than that allowed by TS.
PREVIOUS EVENTS
A review of PNPS LERs since NRC Generic Letter 2008-01 was issued did not identify any other LERs that have been written regarding line voids of air or gas accumulation in discharge piping.
REFERENCES
CR- PNP-2017-06029
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05000293/LER-2017-010 | Air Accumulation Creates Small Void in Core Spray Discharge Piping LER 17-010-00 for Pilgrim re Air Accumulation Creates Small Void in Core Spray Discharge Piping | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2017-011 | Simultaneously Opened Reactor Building Airlock Doors Caused Loss of Secondary Containment LER 17-011-00 for Pilgrim Nuclear Power Station Regarding Simultaneously Opened Reactor Building Airlock Doors Caused Loss of Secondary Containment | | 05000293/LER-2017-001 | Reactor Building Isolation Dampers Failed to Isolate LER 17-001-01 for Pilgrim Nuclear Power Station Regarding Reactor Building Isolation Dampers Failed to Isolate | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2017-012 | Start-Up Transformer Degraded Voltage Relay Found Outside Technical Specification Limit LER 17-012-00 for Pilgrim Nuclear Power Station Regarding Start-Up Transformer Degraded Voltage Relay Found Outside Technical Specification Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2017-002 | Isolation of HPCI LER 17-002-00 for Pilgrim Regarding Isolation of HPCI | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000293/LER-2017-013 | 1 OF 4 LER 17-013-00 for Pilgrim Nuclear Power Station Regarding Reportable Conditions Involving Standby Gas Treatment System and Secondary Containment lnoperability Not Reported During the Previous Three Years | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000293/LER-2017-003 | Supplement to Suppression Pool Declared Inoperable Due to High Water Level LER 17-003-00 for Pilgrim Nuclear Power Station Regarding Pressure Suppression Pool Declared Inoperable Due to High Water Level | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2017-004 | Secondary Containment Testing Led to Loss of Safety Function to Both Trains of Standby Gas Treatment System LER 17-004-00 for Pilgrim Nuclear Power Station Regarding Secondary Containment Testing Led to Loss of Safety Function to Both Trains of Standby Gas Treatment System | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000293/LER-2017-005 | 10 CFR 50, Appendix J, Option B, Leak Rate Criteria Exceeded LER 17-005-00 for Pilgrim Regarding 10 CFR 50, Appendix J, Option B, Leak Rate Criteria Exceeded | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000293/LER-2017-006 | Source Range Monitor Inoperable During Fuel Movement LER 17-006-00 for Pilgrim Nuclear Power Station Regarding Source Range Monitor Inoperable During Fuel Movement | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2017-007 | Supplement to Potential Inoperability of Safety Relief Valve 3A LER 17-007-00 for Pilgrim Regarding Potential Inoperability of Safety Relief Valve 3A | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2017-008 | Supplement to 480V Bus B6 Auto Transfer Function Degraded Due to Time Delay Relay Failure LER 17-008-00 for Pilgrim re 480V Bus B6 Auto Transfer Function Degraded Due to Time Delay Relay Failure | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-2017-009 | Supplement to Potential Primary Containment System Inoperability Due to Relay Concerns LER 17-009-00 for Pilgrim Nuclear Power Station Regarding Potential Primary Containment System lnoperability Due to Relay Concerns | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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