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LER-2078-044, Inoperability of No. 11 S/G Feedwater Flow Channel 2 |
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| 2722078044R03 - NRC Website |
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~~~~{£1f f~t~ ~~~w Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201/622-7000 Mr. Boyce H. Grier Director of USNRC August 24, 1978 Office of Inspections and Enforcements Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406
Dear Mr. Grier:
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 78-44/03L
... _1 Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1.9.a, we are submitting Licensee Event Report for Reportable Occurrence 78-44/03L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours, F. P. Librizzi General Manager -
Electric Production CC:
Director, Office of Inspection and Enforcement (30 copies)
Director, Office of Management Information and Program Control (3 copies) ri ~
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e Report Number:
78-44/03;L Report Date:
8/24/78 Occurrence Date:
8/9/78 Facility:
Salem Generating Station Public Service Electric & Gas Company Hancocks Bridge, New. Jersey 08038 IDENTIFICATION OF OCCURRENCE:
No. 11 Steam Generator Feedwater Flow Channel II Inoperable CONDITIONS PRIOR TO OCCURRENCE:
Operational Mode 1, Reactor Power 99%
DESCRIPTION OF OCCURRENCE:
At 2040 hours0.0236 days <br />0.567 hours <br />0.00337 weeks <br />7.7622e-4 months <br />, during functional testing, No. 11 Steam Generator Feed-water Flow Channel II was declared inoperable due to the trip point being above the.Technical Specification limit.
Action Statement No. 7 for LCO 3.3.1.1 was implemented and at 2335 hours0.027 days <br />0.649 hours <br />0.00386 weeks <br />8.884675e-4 months <br />, instrumentation per-sonnel returned the channel to operable status.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
This occurrence was the result of a failed operational amplifier in the dual comparator which resulted in the trip setpoint being above
- the Technical Specification limit.
ANALYSTS OF OCCURRENCE:
~echnical Specification 3.3.1.1, Action Statement No. 7, states that "with the number of operable channels one less.than the total number of channels, startup and/or power operation may proceed until perform-ance of the next required channel functional test provided the inoperable channel is placed in the tripped condition within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />".
No. 11 Steain Generator Feedwater Flow Channel II was placed in the tripped con_dition with-in 1 -hour* and remained in that condition until
'it ~as returned to operable status.
CORRECTIVE ACTION
.Four operational amplifiers were replaced in the Hagan Dual Output Comparator.
The comparator was then replaced.
The functional test
- - _was then completed to confirm operability.
LER 78-44/03L FAILURE DATA:
Dual Output Comparator-Manufacturer:
Model:
Hagan Controls Orville, Ohio 4111082-002 Prepared by T. L. Spencer
~~~~~--=~~~~~~~-
SORC Meeting No.
51-78
~~~~~~~~~~-
1 Manager l_ s!iem Generating Static
U.S. NUCLEAR REGULATURY COMMISSION 11.n1 e
LICENSEE EVENT REPORT
- CONTROL BLOCK: I I I 1 G) 1 6
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION!
~
I N IJ I s I G I s I 1 101 o I o 1-I o I o I o I o I o I - I o I o 101 4 I 1 I 1 I 1 I l 101 I I 0 7
8 9
LICENSEE CODE 14
- s LICENSE NUMBER 25 26 LICENSE TYPE
- JO Si CAT 58 CON'T [2TI
~:~~~ LlJ© I o I s I o I o I o I 2 I 7 I 2 101 o I s I o I 9 I 7 I s I© I o I a I 2 I 4 I 7 I a 10 7
8 60 61 DOCKET NUMBER 68 69 EVENT CATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
CQID I During functional testing, No. 11 S/G Feedwater Flow Channel 2 was J
!TID declared inoperable due to the bistable setpoint being above T.S.
limit~
All remaining channels were operable.
This is the fifth occurrence of J CQli)
C£ID lil2J
[§J]J this type.
1 8 9 SYSTEM CODE I IIAI@
9 10
~
LER *Ro LvENT YEAR I.:,:) REPOl'IT
. I 7 I 8 I NUMBER
- ?l.
22.
CAUSE
CAUSE
CODE SUBCODE COMPONENT CODE w@ w@ 1r1N1s1T1R1u1e 11 12 1J 18 SEQUENTIAL OCCUR REN CE REPORT NO.
CODE COMP.
SUB CODE
~@
19 REPORT TYPE VALVE SUBCODE w@
20 I I I o I 4 I 4 I I /I I o I 3 I LiJ l=l 2J 24 26 27 28 29 JO 31 REVISION NC. w J2 80
. ACTION FUTURE
~ ATTACHMENT NPRD4 PRIME COMP.
TAKEN ACTION ON PL.ANT METHOD HOURS ~ SUBMITTED FORM ~UB.
SUPPLIER COMPONENT MANUFAC7URER
~@W@ W@ W Io I 010101 L!J@
LJ!,J@)
JJ 34 JS 36 37 40 41 42
- 4J CAUSE DESC.RIPTION ANO CORRECTIVE ACTIONS @
IHI 0 I 2 I 0 I@
44 47 DJ)) I The* cause of this occurrence was failed operational amplifier in the dual comparator module which resulted in the setpoint being above T.S.
ITJ]J limits.
Operational amplifiers were replaced and functional test completed.
OEl 1
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FACILITY tJo'I STATUS
% POWER OTHER STATUS \\.:::::J ITTIJ W@ I 01 91 9 l@I.... __
N
..... /_,_A...._ __
8 9
10 12 11 ACTIVITY CONTENT r.:;;;...
RELEASED OF RELEASE AMOUNT OF ACTIVITY ITE1 W@ W@I N/A 1
8.9 10 11 PERSONNEL EXPOSURES t:::::\\
NUMBER
(.;;\\TYPE~ DESCRIPTION ~
!IE] I o I o I o k~W
....... __ N_/_A ______________________
80 7
METHOD OF
(.;:;\\
DISCOVERY DISCOVERY OESCRIPTION ~
llLJ~I Functional TBsting 45 46 80 44 44
.. LOCATION OF RELEASc@
N/A 80 1
a 9 11 12 1:1 80 PERSONNEL INJURIES
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NUMBER DESCRIPTION~
~I ol ol ol@).__ _______
N~A=-------------------------------------------------------------'
8 9
11 12 80 LOSS OF OR DAMAGE TO FACILITY t4:j\\
TYPE
DESCRIPTION
~
[2liJ W@
NA 7
B 910
-~--~----~------....... ----~~------~----------------------------------------------8~0 ISSU;~~~~CRIPTION@
NRC USE ONLY 0
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0 N.... /_A _______________
II I I I I I I I I I I I t sa 69 ao ;
(609)365-7000 Salem Ext.~
528 NAMEOFPRE?ARER~~--T"-"-.-=L~-.._-s.o~e~n-c.;;..;::e~r.._ __________ __
PHONE:
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