05000272/LER-2078-016-03, Excessive Tilt Ratio of Quadrant Power
| ML19031B168 | |
| Person / Time | |
|---|---|
| Site: | Salem |
| Issue date: | 03/23/1978 |
| From: | Librizzi F Public Service Electric & Gas Co |
| To: | Grier B NRC/IE, NRC Region 1 |
| References | |
| LER 1978-016-03 | |
| Download: ML19031B168 (4) | |
| Event date: | |
|---|---|
| Report date: | |
| 2722078016R03 - NRC Website | |
text
- 0 PS~G Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 /622-7000 Mr. Boyce H. Grier Director of USNRC Off ice of Inspections and Enforcements Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406
Dear Mr. Grier:
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 78-16/03L March 23,
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a 1..N Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 78-16/03L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours, Original Signed f_. P. Librizzi F. P. Librizzi General Manager -
Electric Production CC:
Director, Office of Inspection and Enforcement (30 copies)
Director, Office of Management Information and Program Control 7809500:35 The Energy People
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Report Number: e I
Report Date:
78-16/03L J/23/78 2/23/78 j*
I Occurrence Date:
Facility:
Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Quadrant Power Tilt Ratio Greater than 1.02 CONDITIONS PRIOR TO OCCURRENCE:
Operational Mode 1 Reactor power decreased from 100% to 70%
DESCRIPTION OF OCCURRENCE:
At 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> following a.30% load reduction the Power Range Channel 1 deviation alarm was received in the Control Room.
Quadrant Power Tilt Ratio was determined to be 1.027 on N-41 upper.
Technical Specification 3.2.4 Action Statement a.2 was implemented.
At 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br /> Action Statement for LCO 3.2.4 was terminated with QPT calculation less than 1.02.
QPT calculations continued for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
All calculations were less than 1.02.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The cause of this occurrence was the load reduction which resulted in flux oscillations resulting in the Quadrant Power Tilt Ratio exceeding 1.02.
ANALYSIS. OF OCCURRENCE:
Technical Specification Action Statement for LCO 3.2.4 states that...
With the Quadrant Power Tilt Ratio determined to exceed 1.02 but< 1.09:
Within 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />s:
a)
Either reduce the Quadrant Power Tilt Ratio to within its limit, or b)
Reduce Thermal Power at least 3% from Rated Thermal Power for each 1% of indicated Quadrant Power Tilt Ratio in excess of 1.0 and similarly reduce the Power Range Neutron Flux-High Trip Setpoints within the next 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
Verify that the Quadrant Power Tilt Ratio is within its limit within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after exceeding the limit or reduce Thermal Power to less than 50% of Rated Thermal Power within the next 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and reduce the Power Range Neutron Flux-High Trip setpoints to < 55% of Rated Thermal Power within the next 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
LER 78-16/03L ~ Identify and correct the cause of the out of limit condition prior to increasing Thermal Power; subsequent Power Operation above 50%
of Rated Thermal power may proceed provided that the Quadrant Power Tilt Ratio is verified within its limit at least once per hour for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> or until verified acceptable at 95% or greater Rated Thermal Power.
The Quadrant Power Tilt Ratio was reduced to within its limits within thirty minutes therefore no further action was required.
CORRECTIVE ACTION
This occurrence is considered to be normal following a large load change.
No long term corrective action is planned.
FAILURE DATA:
N/A Prepared by T. L. Spencer Manage~ -
Salem Generating Station SORC Meeting No.*
14-78
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LICENSEE EVENT REPO.
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LICENSEE COOE 14 IS LICENSE NUMBER 25 26 LICENSE TYPE JO 57 C,o.T 58 CON'T [ill]
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REPORT DATE BO EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES @
!At 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> following a 30% loop reduction quadrant power tilt ratio [TIIJ I was determined to be 1. 027. Action Statements for LCD 3. 2. 4 implemented.!
[))3J !Action Statement terminated at 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br /> with QPT ratio less than 1.02.1 CIT!]
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. u:::m ]This occurrence was the result of a 30% load reduction which resulted CIIIJ !in QPT ratio exceeding 1. 02. This is an exvected occurrence and no o:JJJ 1corrective action is planned.
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