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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000254/LER-1993-0131993-08-27027 August 1993 LER 93-013-00:on 930729,identified Deviation from TS & Reg Guide 1.52 Requirements for Methyl Iodide Testing of Charcoal Sample Canisters.Caused by Failure to Implement Proper Canister Testing.Canisters Tested by Nucon 05000254/LER-1993-0121993-08-24024 August 1993 LER 93-012-00:on 930726,light Socket Shorted Out When Operator Reset HPCI Logic Power.Caused by Short Circuit in Light Socket.Light Socket & Blown Fuses replaced.W/930824 Ltr 05000254/LER-1993-0101993-08-19019 August 1993 LER 93-010-00:on 930720,HPCI Declared Inoperable & HPCI Outage Rept Qcos 2300-2 Initiated Because IST Flow Rate Fell in IST Required Action Range Due to New Procedure. Surveillance Procedure Will Be revised.W/930819 Ltr 05000254/LER-1993-0111993-08-18018 August 1993 LER 93-011-00:on 930721,discovered That 4kV Breaker 68 Feeding CS 1B Motor Pump Open & Discharged,Resulting in CS 1B Being Declared Inoperable.Wr Written to Investigate & repair.W/930813 Ltr 05000254/LER-1993-0091993-08-13013 August 1993 LER 93-009-00:on 930714,SBGT Methyl Iodide Test Failed Due to Age of Charcoal Combined W/Stringent Test Criteria. Replaced Charcoal Absorber in Both Trains of Sbgt. W/930806 Ltr 05000254/LER-1993-0081993-08-11011 August 1993 LER 93-008-00:on 930709,reactor Bldg Ventilation Radiation Monitor Setpoints Set non-conservatively Four Times in Five Yrs.Caused by Instrument Maint Program Error. New Computer Program developed.W/930805 Ltr 05000265/LER-1988-006, Errata to LER 88-006-02:on 880404,station Notified That Eleven Flued Head Anchors Did Not Meet Design Requirements. Caused by Misinterpretation of Scope & Design Structures.Mod Initiated to Revise Structure1992-06-0404 June 1992 Errata to LER 88-006-02:on 880404,station Notified That Eleven Flued Head Anchors Did Not Meet Design Requirements. Caused by Misinterpretation of Scope & Design Structures.Mod Initiated to Revise Structure 05000254/LER-1990-0131990-07-24024 July 1990 LER 90-013-00:on 900626,annunciators on Both Units & Reactor Recirculation Loop Sample Valve Closed.Caused by Actuation of Primary Containment Isolation Valve When Lightning Struck 345 Kv Line.Valve reopened.W/900724 Ltr 05000254/LER-1988-001, Sanitized Version of LER 88-001-00:on 880114,records Review Found Two Apparent Overexposures of Contractor Personnel During Fourth Quarter 1980.Caused by Inaccurate Secondary &/ or Primary Dosimetry.Dosimetry Sys Upgraded1988-01-28028 January 1988 Sanitized Version of LER 88-001-00:on 880114,records Review Found Two Apparent Overexposures of Contractor Personnel During Fourth Quarter 1980.Caused by Inaccurate Secondary &/ or Primary Dosimetry.Dosimetry Sys Upgraded ML20203L0281986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 05000254/LER-1984-018, :on 840922 & 24,reactor Bldg Fuel Pool Channel B Area Radiation Monitor 1705-16B Spiked High, Tripping Ventilation.Cause Unknown.Corrective Actions for Both Events Will Be Documented in Suppl to LER 84-0181984-10-11011 October 1984
- on 840922 & 24,reactor Bldg Fuel Pool Channel B Area Radiation Monitor 1705-16B Spiked High, Tripping Ventilation.Cause Unknown.Corrective Actions for Both Events Will Be Documented in Suppl to LER 84-018
05000265/LER-1983-021, Revised LER 83-021/01T-5:on 831028,ultrasonic Exams of Large Bore Stainless Steel Pipe Welds Identified 11 Welds W/Crack Indications.Caused by Intergranular Stress Corrosion Cracking.Weld Overlay Performed1984-02-28028 February 1984 Revised LER 83-021/01T-5:on 831028,ultrasonic Exams of Large Bore Stainless Steel Pipe Welds Identified 11 Welds W/Crack Indications.Caused by Intergranular Stress Corrosion Cracking.Weld Overlay Performed 05000265/LER-1983-018, Revised LER 83-018/01T-1:on 831011,discovered 1-1/4 Inch long,20% through-wall Linear Indication in Weld 12S-S27. Caused by Intergranular Stress Corrosion Cracking.New Welds & Elbow Installed1984-02-0202 February 1984 Revised LER 83-018/01T-1:on 831011,discovered 1-1/4 Inch long,20% through-wall Linear Indication in Weld 12S-S27. Caused by Intergranular Stress Corrosion Cracking.New Welds & Elbow Installed 05000265/LER-1983-020, Revised LER 83-020/01T-1:on 831028,weld 02B-S9,22-inch Pipe to Cap,Weld 02BS-S12,28-inch Elbow to Pipe & Weld 02BS-F14, 28-inch Pipe to Elbow Weld Had Circumferential Linear Indications1983-12-0909 December 1983 Revised LER 83-020/01T-1:on 831028,weld 02B-S9,22-inch Pipe to Cap,Weld 02BS-S12,28-inch Elbow to Pipe & Weld 02BS-F14, 28-inch Pipe to Elbow Weld Had Circumferential Linear Indications 05000265/LER-1982-018, Supplemental LER 82-018/03L-1:on 821006,emergency Diesel Generator Tripped on High Temp After Loading.Caused by Fouling of Diesel Generator Cooling Water Sys.Both HX Replaced1982-12-0101 December 1982 Supplemental LER 82-018/03L-1:on 821006,emergency Diesel Generator Tripped on High Temp After Loading.Caused by Fouling of Diesel Generator Cooling Water Sys.Both HX Replaced 05000254/LER-1982-022, Supplemental LER 82-022/03L-1:on 820816,maint Outage for 1/2B Diesel Fire Pump Exceeded 7-day Limit.Cause Not Stated. Diesel Pump Wear Rings Replaced1982-10-0707 October 1982 Supplemental LER 82-022/03L-1:on 820816,maint Outage for 1/2B Diesel Fire Pump Exceeded 7-day Limit.Cause Not Stated. Diesel Pump Wear Rings Replaced ML20150E1741978-11-20020 November 1978 /03L-0 on 781026:dual Position Indication Was Received for Supression Chamber to Drywell Vacuum Breaker, Valve 1-1601-33E.Caused by Position Indication Problem ML20062E6521978-11-15015 November 1978 /03L-0 on 781025:smoke Detectors Were Removed from Svc in Cable Spreading Room,Elec Equip Room & Control Room for Installation of New Fire Detection/Suppression Sys ML20062D5871978-10-25025 October 1978 /03L-1 on 780420:during Routine Hydraulic Snubber Surveillance Inspec,Snubber Mark 149 Was Found Inoper Due to Empty Fluid Reservoir & Mark 144 Was Found W/Missing Cotter Pin,Due to Component Failure ML20062D5161978-10-19019 October 1978 /03L-0 on 780920:A RHR Room Watertight Door Found Open.Caused by Contractor Personnel Ignorance. Personnel Admonished to Heed Procedures at All Times ML20084Q0021976-12-30030 December 1976 LER 017/03L-0:on 761203,Grinnell Corp Snubber 4755 on RCIC Steam Supply Piping Found to Have Empty Oil Reservoir. Caused by Leakage Through Reservoir End Gap Gaskets.Snubber Repaired & Reservoir Refilled w/oil.W/761230 Forwarding Ltr 05000265/LER-1976-012, Updated LER 76-012/03L-1 Correcting Event Type,Category & Rept type.W/761001 Forwarding Ltr1976-10-0101 October 1976 Updated LER 76-012/03L-1 Correcting Event Type,Category & Rept type.W/761001 Forwarding Ltr ML20084P4791976-08-25025 August 1976 LER 023/03L-0:on 760727,diesel Generator 1/2 Out of Svc for Monthly Insp for 55 Minutes Longer than Tech Spec Limit of 1.5 H.Caused by Maint Personnel Not Being Aware of Time Limit.Procedure to Be Changed ML20084Q0281976-05-27027 May 1976 LER 017/03L-0:on 760427,while Performing Low Reactor Water Level Functional Test,Level Indicating Switch LIS-1-263-58A Tripped,Exceeding Tech Specs.Caused by Instrument Drift. Switch recalibr.W/760527 Forwarding Ltr ML20084Q0511976-04-30030 April 1976 L-0:on 760427,while Performing MSIV Surveillance, Duel Indication Received for Valves AO 1-203-1B & AO 1-203-1D.Caused by Switches Being Out of Alignment.Minor Air Leak repaired.W/760430 Forwarding Ltr 05000254/LER-1976-002, Updated LER 76-002/03L Re Excessive Leakage from Double Gasketed Seal X-4.Initially Reported on 760202.Caused by Equipment Failure & Insufficient Compression.Hatch Bolts Tightened1976-03-0303 March 1976 Updated LER 76-002/03L Re Excessive Leakage from Double Gasketed Seal X-4.Initially Reported on 760202.Caused by Equipment Failure & Insufficient Compression.Hatch Bolts Tightened 1993-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30
[Table view] |
LER-2088-006, Errata to LER 88-006-02:on 880404,station Notified That Eleven Flued Head Anchors Did Not Meet Design Requirements. Caused by Misinterpretation of Scope & Design Structures.Mod Initiated to Revise Structure |
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[ 'N Commonwe:lth Edison
) oed C4tes Nut ear fwer Staton 22110 20S Aronue Nntth
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RLB-92-099 June 4, 1992 U.S. Nuclear Reguletory Commission Document Control Desk Washington, DC 20555
Reference:
Quad-Ctile! Nuclear Power Station Docket Number 50-265, DPR-30 Unit Two Enclosed is Licensee Event Report (LER)88-006, Revision 02, for Quad-Cities Nuclear _ Power Station. This revision provides additional information regarding flued head anchors.
This report is submitted in accordance with the requirements of the Code of Federal Regulations, Title 10, Part bO.73(a)(2)(11)(B), which requires the reporting of any event or condition that resulted in the nuclear power plant being in a condition that was outside the design basis of the plant.
Respectfully, COMMONHEALTH EDISON COMPANY '
QUAD-CITIES NUCLEAR POWER STATION
/
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- R. L. Bax Station Manager RLB/TB/pim Enclosure
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, OuAO:CitttijNC LLALPowuL 5]M10NJ1LIwo _0L5L9LDLollL6L5 ll_eiLLl1 T(tle-(4) UNIT Two FLUED HEAD ANCHOR $ Ovis!DE SAFE 1Y ANALYSIS des!GN REQUIREMENT $ DUE 10 ANALYS!$ DErlCitteCY
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THis REPORT is SUBMIT 1ED PUR$UANT TO THE REQUIREMENTS OF 10CFR 1(htd one or mRtt_DLiht_iQllD*_if01 (111 4 20.402(b) ___ 20.405(c) _' 50.73(a)(2)(iv) _ 73.71(b)
POWER _ 20.405(a)(1)(1) _ 50.36(c)(1) __ 50.73(a)(2)(v) _. 73.71(c)
LE/EL 20.405(a)(1)(li) 50.36(c)(2) 50.73(a)(2Hvii) Other (speci f y (101 0 l9 1_
.__ 20.405(a)(1)(lii)
__._ 50.73(a)(2)(i)
__ 50.73(a)(2)(viii)(A) in Abstract below
/ / / // / / / / / / / / / / / /,/ /, /,/ /, /, / /,/, _ 20.405(a)(1)(iv) JL 50.73(a)(2)(it) __ 50.73(a)(2)(vitt)(B) and in Teat)
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j __ 20.405(a)(1)(v) __ 50.73(a)(2)(iii) _ 50.73(a)(C)(n) 11CD11LLCONIACT FOR T111LLER t12)
Name T[([ff!QNL}f)MBER AREA EODE Dayejiuntsn. Technical staf f EnalattL13G67 31019 _61._5141 -LZLZLilt COMPLETE ONE LINE TOR EACH (0.MSNLML{ALLURLQLiCRID1Q_lN_THis REEORT (13)
CAusE SYSTEM COMPONENT IW NFAC- REPORTABLE / cAusE SYSTEM COMPONENT MAPUF AC- REPORTABLE TURER TO NPRDS / TURLR _lLNP_ PAL i 11l- 1 I L / __ ____1 lI l_ J_LL l l l l 1 l l : / 1 l l l_ __,j l l SUF_PLEMEt(LAL _ REPORT r.EELCILD_Ll41 Expected tigDitLLD3L.l Jt1E submissia
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lyes lif_yg1 M ete EXPECTED sUBMIl$10N DATE) _X_1 NO 1 ll l ABsTRNst (Limit to 100 spaces, i.e. approximately fif teen single-sp.ce typewritten lines) (16)
On April 4, 1988, Quad-Cities Unit Two was in the RUN mode at 93 percent thermal power. At 1410 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.36505e-4 months <br />, the Station wLs notified by d e BWR Engineering Department that eleven flued head anchors did not meet the at: bn rep (rements of the Final '
Safety-Analysis Report (FSAR). _ NRC notification of__this condition was completed at 1423 hours0.0165 days <br />0.395 hours <br />0.00235 weeks <br />5.414515e-4 months <br /> to satisfy 10 CFR 50.72. A subsequent inspection found that there was also a pin missing from one of the affected flued head anchors. The missing pin was avaluated and the flued head anchor was considered operable.
.The cause f_or this condition was due to misinterpretation of scope in that these strut.tures were not reassessed for design base requirements based on IE Bulletin 79-02 and 79-14 programs. The cause for the missing piii could not be determined.
Modification 04-02-88-0;7 has been initiated to revise the structures to comply with FSAR requirements. A program is in place to analy2e the Unit One structures in a similar manner.
This report is provided to comply with the requirements of 10 CFR 50.73(a)(2)(11)(B).
DVR-107 I
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UAEN$1EYitfl JtEPDRT (LER1 TEXT CQ!illMjAJJ91
.FAcigt?Y NAME (1) DOCKET NUMBER (2) LER HUtgER,_t6) Page 131 ,
Year ! jj/j/
/ sequential //jj/ Revision
- f uL...Nwiel tr ul _!fu!!*tr_
_ Qual Cliitt unit Two 0 i 5_LA_Lo_Lo_L2161- s s18 -
o LoJ_6_. _ o12- alz or sit TExV PLANT AND SYSTEM IDERIlflCATIO11 General Electric - Bolling Water Reactor - 2511 MHt rated core thermal power. Energy fndustry Identification System (EIIS) codes are identified in the text as [XX).
EVENT IDENTIFICATION:
Eleven Unit Two flued head anchors do not meet the design requirements due to analysis deficiency. ,
A. CONDITIONS PRIOR TO EVIRIl Unit: Two Event Date: April 4, 1988 Event Time: 1410 '
Reactor Mode; 4 Mode Name: RUN Power Level: 93% .
This report was initiated by Deviation Report D-4-2-88-017
- RUN Mode (4) - In this position the reactor system pressure is at or above 825 psig, l and the reactor protection system is energized, with APRM protection and RBM I interlocks in service (excluding the 15% high flux scram). ..
B. DESCRIPTION OF EVENT:
On Apr11-4, 1988, Quad-Cities Unit Two was in the RUN mode at 93 per cent of rated
, core thermal power. At 1410 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.36505e-4 months <br />, the Station was notified by the Bolling Water Reactor Engineering Department (BHRED) that eleven (11) flued head anchors [SPT] did not meet the design requirements specified in the Ouad-Cities Final Safety Analysis l Report (FSAR). All of the Unit Two flued head anchers were rev,lewed and the ones j in question are located at the following penetrations:
1 I
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kl(LNSEE E' ANT REP 0tI_(1LRL1LXLCONI2fMIIE i 6 ,FAc!LITY NAhl (1) D0cKE! NUMetR (2) ' LLILIMH)LILihL
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/p//j/,/,,_Humbs t QUAL (ities UniLIro 0 l 5 l 0_l_01012}_6]Ji _f}_lk _0_j_Ad_Q -
L}_ L .QjL._0L_OlL TEXT EeJ19.tnitoILRumbn associatesLSystem
- 1. X.11 High Pressure Coolant Injection [B)) Steam Supply
- 2. X-13A Residual Heat Removal (RHR)/ Low Pressure Coolant Injection (LPCI) injection [BO)
- 3. X-13B RHR/LPCI Injection
- 4. X-16A Core Spray [BM) Injection S. X-16B Core Spray Injection
- 6. X-23 Reactor Building Closed Cooling Water (RBCCH)
(CC) Supply
- 7. X-24 RBCCH Return
- 8. X-36 Control Rod Drive (CRD) [AA) Return
- 9. X-47 . Standby Liquid Control [BR) Injection
- 10. X-8 Main Steamline Drains [SB)
- 11. X-7A, B, C, D Hain Steam X-9A, B Feedwater [SJ)
X-10 Reactor Core Isolation Cooling [BN) Steam Supply X-12 Shutdown Cooling Suction [BO)
X-17 RHR Head Spray [BO)
' Gang Anchor The NRC, via the Emergency Notification System (ENS), was notified of this condition at 1423 hours0.0165 days <br />0.395 hours <br />0.00235 weeks <br />5.414515e-4 months <br />, to satisfy the requirements of 10 CFR 50.72. The design concern for the eleven (11) flued head assemblies was the result of a concern identified at Dresden Station. It was identified duri.19 the Dresden review that the flued head anchor structures at Dresden and Quad-Cities were not included under the I.E.
Bulletins No. 79-14 and 79-02 scope of work.
The flued head anchors in question were assessed for considerat' ion of continued
. operability. The results of the assessment concluded that the flued head anchors aill perform their intended functions, thereby, establishing an acceptable operability basis.
Subsequent to the initial submittal of this LER, it was discovered that one shear pin was missing.from the Flued Head Anchor structure at penetration X-16A. Thii specific concern was assessed by Boiling Hater Reactor Engineering Department tnd the anchor was considered operable without the pin. It was recommended, however, to install a pin in order to fulfill the FSAR reautrements.
DVR 107
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.FAc!LITY NAMc (1) DOCKil NUMBLR (2) _LR jut 0LR_iffj .PAgt_t31 Year /// sequential ff//j/ Revision ff UL, Mudu-- UL -_hntL
_Dantiille13 bill s .0_L11LLLlJL12LtLLeLL._ JLL9_LL - o_ ILc1L_0Lolt TEXT C. AEEAREtLLCAUSE OF EVI!R1 This report is submitted to comply with the requirements of 10 CFR 50.73(a)(2)(11)(B), which requires the reporting of any event or condition that resulted in the nuclear power plant being in a condition that was outside the design basis of the plant.
The exclusion of the structures in the 79-02 and 79-14 programs was due to misinterpretation of the scope requirements. Therefore, analysis for these ~
structures was not reassessed for design base requirements. Although the eleven (ll)-flued head anchors did not meet FSAR design requirements, these flued head anchors were considered operable as determined by an analysis in January 1988.
The cause of the missing pin for the structure at penetration X-16A could not be determined.
3 D. SAFETY ANALYSIS _OF EVENT:
Os .iealth and safety of the public and of plant personnel was not adversely affected by this event. Since the anchor assemblies were analyzed and considered operable, the associated safety significance is minimal.
The concerns '.dentified are to be resolved to comply with the necessary FSAR requirements.
E. CORRECTIVE ACTIONS:
When the flued head anchor assembly concerns were initiated Co'mmonwealth Edison ~
(CECO) reviewed the basis-for the exclusion of the assemblies under the IE Bulletin No. 79-14 and 79-02 scope of work. Subsequently, CECO presented justification for the operability criteria as well as the basis for the exclusion in relation to IEB 79-14 and 79-02. The NRC has disagreed with this exclesion basis, hence, CECO has initiated a comprehensive program to demonstrate the adequacy of the aforementioned flued head anchor structures. An engineering walkdown was conductet during the ongoing Quad-Cities Unit Two refueling outage.
The eleven (11) Unit Two structures were reviewed and Engineering Change Notices were issued. -Modification (M-4-2-88-017) has been initiated to revise the structures to a condition that compiles with FSAR design requirements. The eleven (11) flued head anchors are complete and the anchors meet the required FSAR design requirements. In general, the modification involved the addition of structure baseplates and anchors, the welding of some minor support additions, and changeout of certain concrete expansion anchors (Nuclear Tracking System 2652008801701).
DvR 107 1
__ ---=_ --- - .. - . - . -
A LICLMSELLYLMIJLIML11LRLILELIMIMJAll0F
. roc!LITY NAME (1) D0cKET NUMBER (2) _ LLR d *f LR J 61 faseJ21 1 Year // sequential ///
jf Revision
' /,/jI /, NumbtL_ ///j _l!VrbtL JusLLillesaniLIvo LLL13 I o I o i 2LeLLaLL . _JJJJ_L-_LL2_ all JL J1L TEXT In regald to the missing pin, a new pin was installed and a keeper tab was welded to hold the pin in place. Th', should prevent recurrence.
Further analys b of Unit One flued head anchor assemblies showed that assemblies located at the X-11, X-13A, X-13B, X-16A, X-16B, X-23, X-24, X-36, X-47, X-7A, X-78, X-7C, X-7D, X-8, X-9A, X-9B, X-10, X-12 and X-17 penetrations did not meet FSAR .
design requirements. The station implemented modification H-4-1-88-017 to resolve any FSAR design requirement deficiencies. Modification H-4-1-88-017 was completed during the Q1R10 refur. ling outage and authorized for operation on 11-22-89. Under this modification piping to the X-36 penetration was cut and capped at both ends.
This reduced the pipe load to zero and eliminated the need to modify the anchor.
F. EREyl00S EVENTit l
LERJ2BEB TIILE 254/86-022 Containment Atmospheric Monitoring [IL) Line does not meet code allowable stress limits.
254/86-024 U-1 and U-2 Residual Heat Removal Service Hater (80)
Piping Supports exceeded code stress allowable limits.
254/86-025 Torus attached Small Bore Piping does not meet Code Allowable Limits 254/87-008 1C Residual Heat Removal Service Water Pump [P) piping in excess of allowable stress due to sheared anchor bolts.
254/87-011 Residual Heat Removal Support Embedment Pla'te in excess of allowable stress due to improper anchor strap spacing.
254/87-026 Piping Supports Outside Compliance with Safety Analysis Report due to Desigh/ Construction Errcr.
254/87-030 Anticipated Transient Without Scram [JC] Instrument Sensing Lines Inadequately Supported due to Personnel Error and Inadequate Design.
265/87-019 Piping Supports Outside Compliance With Safety Analysis Report due to Design Error.
254/88-004 Reactor Head Vent Line outside Safety Analysis Criteria for Allowable Stress due to Design Error.
l i
l DVR.107
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TEXT G. COMP 0HEELIAlLURE DATA:
Since the structures are not considered inoperable, no component failure is identified in this event.
DVR 107
.