ML20198L923

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Insp Rept 50-293/97-05 on 970514-0828.Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Engineering
ML20198L923
Person / Time
Site: Pilgrim
Issue date: 10/21/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20198L921 List:
References
50-293-97-05, 50-293-97-5, NUDOCS 9710270233
Download: ML20198L923 (39)


See also: IR 05000293/1997005

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U.S. NUCLEAR' REGULATORY COMMISSION

REGION l .- -

Docket No. 50 293

Licensee No. DPR 35

Report No.- 97 05

Licensee: Boston Edison Company _

800 Boylston Street

Boston, Massachusetts 02199

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Facility: Pilgrim Nuclear Power Station :

Location: Plymouth, Massachusetts

Dates: May 14 August 28,1997

Inspectors: L. Prividy, Systems Engineering Branch

B. Higgins, Systems Engineering Branch

'S. K! din, Systems Engineering Branch

G. Morris, Electrical Engineering Branch

Approved by: Eugene M. Kelly, Chief, Systems Engineering Branch

Division of Reactor Projects

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9710270233 971021

PDR ADOCK 05u00293

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EXECUhVE SUMMARY

Pilgrim Nuclear Power Station

NRC SpecialInspection Report No. 50 293/97 05

May 14 August 28,1997

Several findings and observations from a BECo service water self assessment (SWSOPI)

conducted in January 1995 were not adequately evaluated or corrected. These issues

represented a pattern of inconsistencies and engineering weaknesses associated with

design control, corrective action and reportability.

Inadeouate Safety Evaluations (eel 97005 01)

  • Containment overpressure was credited in 1984 to demonstrate adequate net

positive suction head (NPSH) for the core spray and residual heat removal pumps

when considering the pressure drop due to insulation debris expected on newly-

Installed suction strainers. However, crediting overpressure was not part of the

Pilgrim licensing basis prior to July 3,1997, and therefore, represented an

unreviewed safety question. (Section E1.1)

Procedure 2.2.19.5, "RHR Modes of Operation for Transients," did not receive

written safety evaluations and yet resulted in changes to reactor building closed

loop cooling water (RBCCW) and RHR operation which differed from that described

in the Pilgrim FSAR and as approved in License Amendment No.173, and represent

potential unreviewed safety questions. (Sections E1.4 and E1.5)

Inconsistencies Between Plant Analyses and Operatina Procedures

Several examples involving the reactor building closed cooling water (RBCCW), residual

heat removal (RHR), and standby power systems were identified where plant analyses or

calculations of record were not consistent with nor properly translated into applicable

operating procedures. (eel 97005-02)

  • On several occasions in 1994 and 1995, the Pilgrim Station was operated with

RBCCW inlet temperature greater than the original licensing design basis value of

65 F. The NRC had not approved operation at temperatures above 65*F, which

was the value assumed for containment response in accident analyses, prior to

July 3,1997. (Section E1.2)

  • Design basis information regarding isolation of RBCCW system flow to nc,1 essential

loads and the establishment of an appropriate RHR flow rate was not correctly

translated into RHR Operating Procedure 2.2.19.5. (Sectiont E1.4 and 5)

PS-79 was not correctly translated into Standby AC Power System Operating

Procedure 2.2.8. (Section E1.6)

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Ineffective Corrective Action

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SeveralInstances from the January 1995 SWSOPl self assessment represent potentially

significant conditions adverse to quality which were not adequately identified, evaluated

and corrected in a timely manner. (eel 97005 03)

  • A single failure vulnerability was identified by the NRC which involved the

malfunction of a selector switch for the " swing" (or fifth) salt service water (SSW)

pump. The failure causes both headers to remain cross-tied fed by a single pump in

an unanalyzed potential runout condition, placing the plant outside the design basis.

(Section E1.3)

  • The lack of isolation of RBCCW flow to nonessential loads and discrepancies with

the diesel generator loading calculation had been initially identified (but not formally

entered in the PR process) during the January 1995 SWSOPl self assessment, but

had not yet been corrected or substantially addressed. (Sections E1.4, E1.6)

  • A long-standing question remained unresolved regarding the impact of ambient air

on diesel generator operation when exceeding the maximum design value of 88 F.

(Section E1.7)

Reportability

Several examples were identified where unanalyzed conditions outside the Pilgrim Station

design bases were not appropriately reported in accordance with the requirements of

10 CFR 50.72 and 73. (eel 97005-04)

  • No report was made regsirding exceedir.u the 65'F RBCCW inlet design temperature

on several occasions in 1994 and i995 (Section E1.2).

  • An untimely report was made regarding a single failure vulnerability which placed

the SSW system in a configuration with one pump supplying both headers, but in a

runout condition. (Section E1.3)

  • No report was made concerning the potential for operation outside the design basis

regarding isolation of RBCCW flow te nonessential loads. (Section E1.4)

  • An untimely report was made (and later retracted) regarding the potential for

operation significantly below and above the 5100 gallon per minute design basis

flow rate for RHR in the long-term containment heat removal mode. (Section E1.5).

  • For at least a seven-year period of December 1988 through March 1996, Pilgrim

Station was operated in a condition wherein, if a main steam line break were to

occur, drywell temperature profiles could have exceeded established environmental

qualification (EO) limits. Although identified by BECo in early 1996, this condition

(introduced by a modification to reduce drywell spray capability in 1987) was not

reported and apparently would have resulted in containment temperatures

approximately 35 degrees higher than the analyses of record, in apparent violation

of 10 CFR 50.49. (Section E1.8)

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TABLE OF CONTENTS

PAGE

EX EC UT IVE SU M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . II

El Conduct of Engineering ........................................ 1

E 1.1 Not Positive Suction Head (NPSH) Requirements (UNR 97 0103) ..... 1

E1.2 SSW System Design Inlet Temperature (UNR 9 5 21 -0 2) . . . . . . . . . . . . 5

E1.3 3 alt Service Water System Single Failure . . . . . . . . . . . . . . . . . . . . . . . 9

E1.4 Reactor Dullding Closed Cooling Water Flow Margir. . . . . . . . . . . . . . . 13

E1.5 Design Basis RHR Flow Range ............................. 15

E1.8 Diesel Generator Load Calculations . . . . . . . . . . . . . . . . . . . . . . . . . . 19

E1.7 Diesel Generator Ambient Temperature . . . . . . . . . . . . . . . . . . . . . . . 21

E1.8 Drywell Spray Flow Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

E1.9 SSW System inservice Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

E1.10 Automatic Starting of SSW and RBCCW Pumps during ECCS Testing . . 28

E1.11 Sea Water Levels Assumed in SSW System Ana'yses . . . . . . . . . . . . . 28

E1.12 Heat Transfer Capability of Safety Related Heat Exchangers . . . . . . . . 29

E1.13 SSW System Piping Through-Wall Leakage . . . . . . . . . . . . . . . . . . . . 31

E 1.14 Pla nt Walk downs . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32

E7 Ouality Assurance in Engineering Activities . . . . . . . . . . . . . . . . . . . . . . . . . 33

E7.1 Independent Oversight of SWSOPl Corrective Actions ............ 33

E8 Miscellaneous Engineering Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33

E8.1 Review of Updated Final Safety Analysis Report (UFS AR)

C o m m i tm e n t s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33

V. Management Meeting . . . . . . . . . . . . . . . . . . . . . . . . . . ................ 33

X1 Exit Me eting Sum m ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33

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111. Enaineerina

E1 Conduct of Engineering

Backnroyed

in January 1995 the Boston Edison Company (BECo) conducted a self assessment

of the Pilgrim safety related cooling water systems with the intent to meet the

objectives of NRC Temporary Instruction (TI) 2515/110 " Service Water System

Operational Performance Inspection (SWSOPI)." The NRC monitored these activities

as documented in NRC inspection Report 50 293/95 01. Thermal hydraulic margins

for the cooling water systems woro verified by BECo and subsequently

demonstrated by testing. Over 115 action items were created to followup on the

observations and recommendations from the SWSOPl report that required corrective

action.

The objective of this NRC inspection was to evaluate those corrective actions and

followup activities, including salt service water (SSW) system issues of significance

such as the design inlet temperature question (i.e.,65'F vs. 75'F). The inspection

also addressed existing NRC open items (namely 97-01 03,95 21 02).

E1.1 Not Positive Suction Head (NPSH) Reauirements (UNR 97-01 031

a. lDipaction Sqqpe (92903)

The inspector reviewed DECO nuclear safety evaluations, GE studies, the Pilgrim

UFSAR, and correspondence supporting BECo's use of containment overpressure to

satisfy emergency core cooling system (ECCS) pump NPSH requirements. BECo's

past reliance on crediting (,ontainment overpressure was determined by the NRC to

be an unreviewed safety question (USO), as documented in an attachment to

Inspection Report 97 01 issued on March 18,1997,

b. Observations and FindiDal

1@4 Desian Basu

BECo Nuclear Safety Evaluation (SE) No.1638, Revision 1, dated August 31,1984,

was performed to support changing all piping insulation in the drywell to a flexible

blanket type and the installation of enlarged ECCS suction strainers. The safety

evaluation cover sheet stated that ECCS pump NPSH margin was evaluated "...with

maximum debris loading on the strainer and no overpressure." However, the

licensee later concluded that SE-1638 was incorrect based on discussions with

Gerioral Electric (GE) representatives and in subsequent evaluations and analyses

performed by BECo. The licensee reasoned that results of analysis "...at a peak

supprossion pool temperature of 185*F indicated that the availablo NPSH at this

high temperature with torus overpressuto (calculated with containment sprays)

would be bounded by the NPSH available for a pool temperature of 130*F and a

torus pressure of 14.7 psia." It appears that this was also the rationale used to

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support the following statements (on ECCS NPSH)in Section 3.0 (page 17) of an

August 1984 GE report (AC-070-0884), " Effects of Fiberglass Insulation Debris on

Pilgrim ECCS Pump Performance":

"The lowest margins calculated, (i.e., the worst " clean screen" conditions)

for NPSH were 15 feet for the RHR pumps and 12 feet for the core spray

pumps, at 130*F pool temperature and atmospheric pressure. These

represent conservative marci ns since no credit is taken for torus

pressurization caused by heating of the air "

In discussiors with cognizant BECo staff and by review of GE written responses to

licensee questions, the inspector ascertained that several iterations of NPSH

calculations occurred in 1984. The GE San Jose design record file (DRFA00-

01713) which supports their study of debris loading effects on ECCS pump

performance was not available for review during this inspection; however, a copy

was being obtained for subsequent verification by the inspector. Nonetheless, GE

correspondence indicates that the final design of the newly installed strainers was

based on a worse caso debris formation (fiberglass) of 23 cubic feet, which was

then predicted to be distributed thrcughout the suppression pool and transported

circumferentially, eventually migrating onto the strainer screens in proportion to the

respective pump flow rates. Corresponding head (pressure) losses through the

shredded debris layer were estimated to be 14 feet for RHR and 6 feet for core

spray; both within the minimum available clean screen" NPSH margins quoted

above.

A key to understanding BECo's design bases and methods for calculating NPSH is

(former) FSAR Figure 14.510, "NPSH Availability for RHR and Core Spray System".

This figure existed in the Pilgrim FSAR for over 25 years, until recent revision.

Based on discussions with BECo staff, review of subsequent BECo safety

evaluations and calculations, RHR pump design information and the GE response to

specific questions posed in 1995, the inspector found that time-dependent NPSH

analyses have always been a part of the Pilgrim design bases. These analyses

explicitly depend upon suppression pool water temperature and containment leak

rate assumptions both ev donce of a consideration of overpressure in determining

NPSH margin. Most signifiaant (and the source of much confusion), the smallest

NPSH margin predicted in tne original (19711984) Pilgrim design was found to

occur relatively late in the containment accident response. FSAR Figure 14.510

illustrates where the limiting margin occurs, independent calculations by the

inspector show this point is at approximately 28 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br /> into the event, when the

containment pressure he reiurned to 14.7 psia (atmospheric) and suppression pool

water temperature has been cooled to approximately 130135 degrees.

This is a!ao consistent with eaily GE design guidance (SCER 109) which would

typically evaluate minimum NPSH available for pumps taking suction off the

suppression pool based on 130*F pool water totnperature and atmospheric pressure

ever the pool, Also, the type of pumps provided by GE (e.g., Pilgrim uses single-

stage cast models) provides insight to the design. The inspector noted that this

could easily be miscont, trued at. an assumption of no containment overpressure; to

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the contrary, it represents the endpoint in a time and temperature-dependent

analysis of NPSH which explicitly requires consideration of subcooling and hence

overpressure. In fact, at the tirne of peak predicted torus water temperature (166'F

originally) approximately 10 foot of margin was shown, about 80% of which is

attributable to containment pressure above atmospheric.

Therefore, while the minimum " clean screen" NPSH margin used in the 1984 design

is referenced at torus conditions of 130'F and 14.7 psia, the torus airspace

pressurization predicted at times earlier in the design basis event was both credited

and necessarv in overcoming the debris loading head lossos. A separate and

independent calculation by the inspector shows that, for torus water temperature

greater than approximately 130'F, containment overpressure (above 14.7 psia) was

required (from August 1984 until April 1997) for the RHR pump to ovwcome the

predicted debris loading on its strainer. Lastly, even at a 130*F/14.7 psia

condition, the subcooled nature of the torus water and consideration of the

"prossure term" in the NPSH calculation still contribute over 12 psi or approximately

29 foot of hood (although not necessarily overpressure) which is factored into the

1984 margin ovaluation.

In a GE Heport (NEDC 30915) performed in 1985 entitled " Pilgrim Decay Heat

Removal Capability", NPSH margins were quoted that are consistent with the 1984

strainer modification. The assumptions and inputs associated with this GE

evaluation woro not consistent with the Pilgrim licensing basis described in UFSAR

Section 14.5 (which was, itself inaccurate). However, with respect to the

consideration of overpressure in the design, the report (Section 5 and Figure 51)

refers to the minimum margin as ".. occurring at a lo'v pool temperature...but as

pool temperature increases, the available NPSH incraases due to wetwell

pressurization". The inspector considered this statement to further corroborate the

use (and necessity) of containment overpressure in the design.

The inspector concluded that a USO was introduced in 1984 but, because SE 1638

was unclear and poorly documented, the explicit credit from that timo forward for

overpressure was not obvious. And, inconsistencies existed (in 1984) between a

number of GE evaluations and several revisions (in April, Juno and August 1984) to

SE 1638. The inspector found that analyses and evaluations at that time were

unclear, and lacked the clarity and rigor nooded to unambiguously conclude what

the design and licensing bases were with respect to NPSH. This was later

corroborated by the independent opinions of outside reviewers engaged by BECo to

review the issue, and ultimately by the NRC in February 1997. Finally, Pilgrim

UFSAR Section 14.5 was never appropriately updated between 1984 and 1996 to

reflect the design during that period, representing an apparent violation of 10 CFR

50.71(c)(4), (eel 9700510)

! 1996 Safetv Evaluations

A now SE 2971 was approved on March 25,1996 to correct SE 1638. This 1996

, evaluation supported the previous replacement of all piping thermalinsulation in the

drywell with Owens Corning NUKON fiberglass blanket, and once again concluded

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that the 1984 plant modification did not constitute a USQ. Although SE 2971 did

not specifically address the issue of crediting containment overpressure, it refers (in

Section F.4, page 9) to an NPSH margin discussion contained in the original Pilgrim

FSAR. The SE states (original) FSAR Figure 14.513 shows that the containment

remains at or above atmospheric pressure (even in the case of continuous spray).

Still another SE 2983 was approved on March 25,1996, and was characterized as

a " design verification of the plant safety analysis design basis...at 75'F".

However, SE 2983 incorrectly concluded that no unreviewed safety question

existed. The inspector reasoned that this was incorrect because not only was the

use of overpressure (at 65'F) considered to be a USO, but additional amounts of

containment pressure and different assumptions were necessary to justify operation

at 75'F. In a more recent letter (#2.97 004), dated January 20,1997, DECO

requested NRC review and approval for including containment pressure as a

component of NPSH margin in the Pilgrim licensing basis.

ADdenendent Reviewg

The licensee undertook severalindependent reviews of this issue. The inspector

reviewed portions of the following reports summarizing these studies:

1. Once identified by BECo as part of the 1995 SWSOPl self assessment,

Problem Report (PR) 95.9417 was initiated. A BECo Memorandum, dated

March 7,1996, documented the results of a BECo Quality Assurance (QA)

review related to PR 95.9417. That review identified several observations

considered by the OA Department to be " key contributors in allowing the

NPSH condition (viz. the invalid use of overpressure) to go undetected and

create an operability question." For example, the review of vendor design

information (numerous GE evaluations) was cited as a suggested area in

need of assessment.

2. Fauske & Associates performed a review of BECo documentation related to

the design criteria for evaluating NPSH for the RHR and core spray systerns.

The review was performed to assess the technical basis associated with the

available NPSH. The report, dated March 6,1996, concluded that the BECo

evaluations *were performed in a credible manner using available information

in a consistent way."

3. An independent review was also performed by Yankee Atomic Electric

Company, and the results reported in a letter to BECo, dated June 5 1996.

This assessment concluded that containment overpressure was not credited

in the Pilgrim licensing basis. The conclusion was based on the fact that

BECo smendments to the final safety analysis report related to NPSH did not

clearly state reliance on overpressure, and there was no BECo response or

challenge to the AEC's Safety Evaluation which acknowledged that a

positive NPSH margin would be available without requiring overpressure.

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c. Conclusions

Crediting containment overpressure prior to July 1997 was not in accordance with

the Pilgrim licensing basis, and therefore, constitutoo a USO. This represents the

first of four examples of an apparent violation of 10 CFR 50.59 (eel 97005 01)

The Pilgrim design for ECCS pump NPSH, particularly its reliance upon containment

overpressure, was not adequately described after 1984 in the UFSAR .

The design initially submitted to the NRC by BECo explicitly referred to the presence

of containment pressure in evaluating the NPSH margin avellable, as depicted in

FSAR Figure 14.510. Positive NPSH margin was originally ohown to be available

for the entire course of the event, including points where the containment is

predicted to return to atmospheric pressure (14.7 psla). The NRC, however,

established an originallicensing basis in the August 1971 Safety Evaluation Report,

which was judged acceptable on the basis of margin without requiring containment

overpressure even, as later evaluated, if containment spray was utilized.

A modification to the ECCS pump strainers in 1984 was supported by NPSH

= calculations that required credit for containment overpressure to accommodate

debris loading, but were ambiguously described in terms of where the limiting

design margin occurred. The condition selected (130*F and atmospheric pressure

in the suppression pool) was neither clearly explained nor adequately justifled; the

1984 design was, therefore, not strictly based upon calculations that used

overpressure. However, by extension of the analysis (beyond what's documented

in 1984 evaluations), overpressure was clearly required for the RHR pump at

suppression pool temperatures above 139'F. The statement in BECo evaluations

and GE studies at that time, that this was a " conservative margin", is misleading

and requires speculation to ascertain whether the condition occurs early (i.e., initial

10 20 minuter) or late (beyond 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />) in the design basis event. In either case,

an overpressure is needed for rollable ECCS pump performance between those

timos, particularly at the point of peak torus water temperature. It is notable that,

with Pilgrim operation at SSW temperatures in excess of 65aF, and correspondingly

higher peak torus water temperaturos, the overpressure required for the 1984 1997

strainer design was about twice that currently approved by Amendment No.173.

The NRC has sinco approved a more current licensing basis for Pilgrim in Uconse

Amendment No.173 (NRC letter to BECo, dated July 3,1997), allowing credit for a

specific amount of containment overpressure (1.9 psig from 20-100 minutes, and

2.5 psig thereafter) in determining available NPSH for the core spray and RHR

pumps.

E1.2 SSW System Dosinn inlet Temperature (UNR 95 21 02)

a. Inspection Scope f92903)

in Inspection Report (IR) 95 21, the NRC identified an unresolved item related to

elevated SSW inlet temperatures. The inspector reviewed related correspondence

and DECO Safety Evaluation No. 2983, dated March 25,1996.

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b. Observations and Findinas

In February 1990, the NRC questioned the Pilgrim licensing and design bases for the

ultimate heat sink in two regards:

1. The original licensing design basis temperature established for the Pilgrim

ultimate heat sink (UHS).

2, T% method used to measure and establish SSW inlet temperature during

ns mial plant operation.

The NRC's poaltion, established in February 1996, was that since 65'F was

assumed in UFSAR Chapter 14 accident analyses, that number was considered to

be part of the Pilgrim licensing design basis Consequently, whenever the RBCCW

heat exchanger inlet temperature exceeded 65'F, the plant should have been

considered outside its design basis, in addressing the method of measurement,

DECO's past practice of using a 30 day " rolling average" to establish a temperature

(for comparison against the 65'F design basis) was considered by the NRC to be

inconsistbnt with good engineering practice and, therefore, unacceptable. For

instance, inspection guidance has existed since 1988 (e.g, Manual Chapter

9900,STS 3.7.5) which cautions against the use of a time average to effectively

"... dampen peak values occurring due to higher daytime temperatures or tidal

effects;" otherwise, temperature could significantly exceed that assumed in

accident analyses. Existing (" instantaneous") temperature was more appropriate in

determining if the plant is operating within its design basis. These issues were

discussed with the licensee in a management meeting held on February 22,1996.

Orlainal DosinD_ Considerations

During the February 22,1996 meeting, BECo presented background information

associated with an October 1968 ocean water temperature study which formed the

basis for UFSAR Figure 2.4 2, " Maximum, Minimum, and Mean Temperatures for

Cape Cod Bay and Boston Tide Stations." The licensee argued that a peak

temperature of 75'F and a monthly mean (during August) of 65*F were " carried

forward into the design," and were considered as conservative since the Pilgrim site

l was shown to be approximately five degrees cooler, But, from 1968 until issuance

of the Pilgrim operating license on September 15,1972, the licensee maintained -

that various temperatures (55'F,65'F,75'F) were used to evaluate the RHR

RBCCW and TBCCW heat exchangers (for shutdown cooling, accident and normal

operation, respectively). However, containment heat removal capability was

l analyzed using 65 F, and this was consistently described in the UFSAR.

Nonetheless, the licenseo concluded that 65'F was only a design input, based on

l historical monthly mean seawater temperature, and that "... excursions to

75*F...were identified in' site characterization studies."

Proposed changes to the Pilgrim operating license had been previously considered

by BECo in 1984 and 1985, but were not completed. Similarly, in a review of NRC

Information Notice 87 65, the issue of operating in excess of 65 F was again

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evaluated by the licensee. The more recent BECo position indicates a i

misunderstanding of the Pilgrim licensing basis. The NRC views the temperatures ,

presented and discussed in UFSAR Section 2 as data used by BECo to support a 65

degree SSW design inlet temperature. Although the historical data presented did

not preclude the use of a higher ternperature, BECo elected to establish 65'F as the  ;

licensing and design basis for Pilgrim. Viewing the 65'F temperature as merely a

design input was inconsistent with UFSAR Chapter _14 accident analyses which

had, since original licensing, been reviewed and approved (by the NRC) for 65'F.

Rollina Averaae.g ,

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By late 1995, BECo justified the operation of the plant above 65'F using what they i

termed a " risk averaged" approach Citing the original site studies of environmental

conditions in the Cape Cod / Boston area (viz. FSAR Chapter 2), the licensee ,

reasoned that exceeding 65'F seawater temperature "did not violate the Pilgrim  !

licensing basis...and that all water temperatures within the range of values

contained in UFSAR Section 2.4.2 are within the licensing basis (i.e., .175'F)."

This rationale formed the basis for use of a " rolling average" of SSW inlet

temperatures which is inconsistent with acceptable engineering methods of

establishing an ultimate heat sink design temperature.

In NRC Inspection Report 50 293/95 22 (Section 4.1.3), a chronology of events

related to elevated SSW temperature are presented that demonstrate a

misunderstanding of the Pilgrim licensing bases and a reluctance by BECo to

recognize 65'F as an operating limit, such that the plant had been operating'outside

its NRC approved licensing design basis on several occasions. These events are

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briefly summarized below:

Qalft Document Eymt

July 7,1994 PR 94.9297 SSW inlet reaches 07'F; Onsite

Review Committee concludes

RBCCW is operable at

temperatures up to 75*F.

Feb. 23,1995 Procedure 2.2.32 Administrative limit included in

Revision 35 of procedure to allow

RBCCW operation with a SSW

inlet temperaturo up to 75'F.

Aug.3,1995 Engineering memo Approved SSW excursions above

65'F and use of avmge monthly

temperature (" rolling" 30 day

average).

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Aug.7,1995 Engineering memo Established rolling eight hour

average of 75'F for SSW inlet

temperature in the short term with

specific instructions included in

Operations Standing Order 95 09.

Sept. 4,1995 30 day average exceeded (67'F).

Sept.14,1995 Engineering memo New 30 day " rolling" average limit

established at 67*F.

November 1995 BECo Licensing "PNPS Seawater Temperature

Document Licensing Basis" descrloes a

risk average approach

Qperatinn Procedures

Historically, Cape Code bay water temperatures were known to exceed 65'F during

the months of July September. The licensoo performed a statistical study in March

1996 of SSW temperatures over the 20 year period of 1976 1995, calculating an

average number of hours above 65'F for each year; the mean time for the 20 year

period was 108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br /> (above 65'F). The " hottest" summers (based on a maximum

average for 24 hoor periods) occurred in 1981 (69*F),1990 (71.7'F) and 1995

(70.8'F). The worst case recorded period was during the summer of 1995. In the

11 day period of August 17 29,1995,65'F was continucIly exceeded. The peak

recorded value in that period occurred on August 10 at 73.7*F, lasting about 11

hours above 70"F. Several days in that period occurred wherein SSW temperature

remalnad above 70*F for approximately an 810 hour0.00938 days <br />0.225 hours <br />0.00134 weeks <br />3.08205e-4 months <br /> duration.

Notably, no safety evaluation was completed when SSW temperatures exceeded

65'F. As previously discussed in NRC Inspection Report 50 293/95 22, SSW

Operating Procedure 2.2.32 contained an administrative limit in the Section 5.0

precautions and limitations stating that the RBCCW system remains operable with

SSW inlet temperatures up to 75*F. The inspectors considered the lack of a

written safety evaluation to address operation of the RBCCW system at temper-

atures above 65'F to be inconsistent with the Pilgrim licensing basis at that time

(i.e., FSAR 14.5.3) and the second of four examples of an apparent violation of 10

CFR 50.59. (eel 97005 01)

The limit of 75 F was added on February 23,1995 as part of procedura revision

35. However, at that time, no formalized analysis existed to support plant

,

operation above 65'F. Boston Edison Quality Assurance Manual, " Design Control",

requires that engineering and design activities associated with plant design changes

and modifications of nuclear safety related structures...aro accomplished according

I

to ANSI Standard N45.2.11 1974, and BECo Nuclear Engineering Services Group

l Proceduto No. 3.05, " Design Calculations", applies to all safety-related design

analyses.This represents a failure to assure that design basis information (65'F

1: censing design basis SSW inlet temperature) was correctly translated into

_

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_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ - _ _ _ _ - _ _ _ _ _ _ _ _ .

.

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9

operating proceduros (Pilgrim Proceduro 2.2.32) and is one of four examples of an

apparent violation of 10 CFR 50, Appendix B, Critorion Ill, Design Control.

(eel 97005 02)

Moreover, NRC approval of the use of containment overprossure would have boon

required at that time to permit operation up to 75'F (see Section E1.1 above).

Consequently, during the times when Pilgrim Station was operating at SSW

temperatures abovo OS*F, the plant was (until Mar:h 1990) in an unanalyrod

condition with respect to containment heat removal, ECCS pump performance, EDG

electricalload profilos, and environmental qualification that significantly

compromised plant safety and was (until July 3,1997) outsido its design basis, but,

no report was medo to the NRC. This is one of six examples of an apparent

violation of 10 CFR 50.72 and 50.73. (eel 97005 04)

This issue was eventually resolved when, on May 14,1997, BECo requested NRC

approval for Pilgrim operation up to a UHS temperature of 75'F in conjunction with

a licenso amendment to permit crediting containment overpressure for ECCS pump

NPSH requirements. This request was based, in part, on DECO Safety Evaluation

SE-2983 which DECO charactorized as a " design verification for safety related

cooling systems using a 75'F maximum SSW temperature." On July 3,1997, the

NRC approved Amendment No.173, permitting Pilgrim operation up to a UHS

temperature of 75'F.

c. Concludo.na

DECO used " rolling averages" and other relatively informal means (e.g., engineering

memoranda) to address or reconcile operation with SSW abovo 05'F. On numerous

occasions, particularly the suminer of 1995, the Pilgrim Station was operated

outsido the NRC approved design. In contrast, the licensoo established operating

instructions to permit plant operation at inlet temperatures up to 75'F without a

formally approved safety ovaluation.

E1.3 Salt Servico Water System Sinato Failure

a. IDinoction Sconol029321

The 1995 BECo SWSOPl self assessment team questioned the SSW system design

with respect to single activo failures, with an observation that plant personnel did

not always recognize the safety significance of the SSW system pressure switches.

The pressure switches fulfill a safety related function to start standby pumps in the

event that header pressuro is reduced below a sotpoint of 3.3 psig. Separato

pressure switches exist for each of the SSW headers. If the header pressure is

greater than 3.3 psig and increasing, the switch is satisfied, (i.e., additional

automatic SSW pump starts will not nceur).

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!

Three specific maintenance and test observations were made by the team:

  • A recent examplo regarding the plugging of a pressure switch impulse lino

had not been ovaluated for potential common modo f ailure.

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1. __ .. . - _. - -- . --. - .-

______ _____________________-__ _ - _ _ _______ ______ _ ___ ____ _ _ ________ _ _ _ _

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10

  • Air accumulation in tne CSW pump discharge pressure indicators did not

prompt an evaluation of the potential for air accumulation in the header

pressure switches.

  • All consequences of jumpering the SSW pressure switches were not

recognized during maintenance activltios.

At the timo of this inspection, BEco considered any SWSOPI related pressure

switch issues to be closed. The inspector reviewed the various corrective actions

that had been completed to address the above observations. This review included

the function (s) of the pressure switch within the context of overall SSW system

design after postulating cortain single f ailures,

b. Qbservations and Findinas

Based on reviews of plant records and interviews with instrumentation and control

(l&C) personnel who were responsible for maintaining the pressure switches,

adequate correctivo actions were found to have been taken regarding plurging and

venting of the pressure switch impulse lines. Procedure 8.E.29.1, "SSW

Instrumentation Calibration and Functional Test," performed annually to calibrato

the pressure switches, had been revised after the 1995 SWSOPl to formally include

stops to flush and vont the instrument lines. l&C personnel indicated that the past

plant practice had been to flush and vent these lines upon restoring the instrument

to service, even though the procedure did not specifically require it. The inspector

also discussed the impulso line plugging question with soverallicensee personnel

(l&C technician and l&C engineer) who stated that this has been the only known

occurrence of this kind in a pressure switch sensing line, supporting their conclusion

that it was apparently an isolated occurrence.

Desian Bases

The SSW system consists of five pumps, one of which is considered an additional

' swing" pump. The swing pump is arranged to permit operation on either SSW

header according to the position of two normally open DC powered motor operated

valves (MO 3808 and 3813)in a common section of discharge piping. One of

those valvos is designed to close upon a loss of offsite power (LOOP) based on a

preset position of the Loop Select switch, effectively dividing the SSW system into

two independent loops which is consistent with Updated Final Safety Analysis

Report (UFSAR) Section 10.7.5. In a design basis loss of coolant accident (LOCA)

coincident with a LOOP, the emergency diesel generator (EDG) load sequencer

establishes the automatic start of one SSW pump in each loop. The pressure

switches located in each loop would automatically start additional pumps (af ter

established timo delays) if header pressure is less than 3.3 psig. The switches ,

therefore, control sequenced addition of SSW pumps, for EDG load considerations.

. - _-.

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11

1995 SWSOPl Guestions

A separate Problem Report 97.9408 was issued on July 1,1997, to establish

whether failures in the DC power system should have been considered in the SSW

system single failure analysis in response to Generic Letter (GL) 8913. The

licensoo initially performed a fallste modes and offects analysis via a

January 11,1990 contract study to address GL 8913. The 1995 SWSOPl team,

however, found several weaknesses associated with the licensee's original

evaluations and, could not conclude that all single active failures had been

appropriately evaluated for the SSW system. While the team independently

examined what it termed "significant vulnerabilit4s" and reasoned that any

additional unidentified failures "wouldn't Jeopardize SSW function," they

nonetheless concluded that BECo's analyses performed at that point were

incomplete. In fact, this specific failure was questioned (MECH-03, Page 3)in the

final SWSOPl report issued on April 25,1995. BECo opened SWSOPl Action item

SW95.003.01 to address this question. BECo later resolved the single failure item

on April 29,1997, as documented in a specir.1 report S&SA9712. However, the

DC power failure in question had not been included in Report S&SA 97-12.

Los9 of DC Power / Selector Switch (Problem Reoorts)

Based on discussions between the inspector and DECO staff during the first two

weeks of the inspection, a system single failuro vulnerability that represented

operation outside the plant design basis was identified. The condition involves a

loss of DC power during a design basis event at specific tidal conditions and Cape

Cod Bay water temperatures. An assumed DC power failure for the train opposite

to which the swing pump is selected to align, results in the expected loss of an

associated EDG and the related SSW pumps. However, both header isolation valves

(MO 3808 and 3813) remain open, and the headers are not split".

BECo issued Problem Report 97.2040 on June 8,1997, to evaluate the problem.

Hydraulic calculations for both a design high tido of + 13.5 ft. (water levelin intake

I

structure above pump suction) and a design low tide of -7.1 ft. were performed

I

using the existing pressure switch setpoint of 3.3 psig. The results for the high tide

case indicated that the automatic sequenced start of a single SSW pump would

alone satisfy the pressure switch. Therefore, both SSW loops would remain cross-

tied with one pump supplying flow to both headers. The resultant flow was higher

l

than normal and beyond the existing pump curve (approximately 5155 gpm), and in

l an apparent runout condition. However, BECo estimated that pump cavitation

would not be expected since sufficient net positive suction head (NPSH: was

, available although the licensee had to extrapolate to make that conclusion, The

l results of the low tide case indicated that a second SSW pump in the same loop

(predicted to be cavitating briefly) would need to be started by the pressure switch

logic after a 30-second time delay, since tho header pressure would remain less

than 3.3 psig. However, BECo recognized that, at other intermediate tide levels (a)

there could be conditions under which one only pump would remain operating, in a

runout condition; (b) with the SSW headers cross-connected; and (c) insufficient

NPSH. The pump would likely experience cavitation until operator action was

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_- . - .- -- - . .__ .-_- - -- - - -- .- . - . - - .. .. .

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12

taken. Such cavitation conditions had to be assumed to persist for ten minutes,  !

baced on no operator action to start additional pumps or close a header isolation

valve, and would have to be evaluated for impact on SSW pump and system ,

operability,

based on engineering judgment and discussions with the pump vendor, and on the-

adequacy of existing procedures and training, BECo concluded on June 27,1997,

that the SSW system was operable. Disposition of PR97.2040 also relied on the

assumption that operators woutJ recognize and diagnose the failure condition, such

that the headers would be manually isolated and/or an additional pump started soon

after the 10 minute mark. BECo concluded that this conditicn was not reportable,

but also intended to confirm their engineering judgment in this matter by performing '

a special pump test at the postulated runout condition.

Banortability

The single failure deficiency represented ineffectiva corrective action for a problem

first identified during the original 1995 SWSOPl, and for which several opportunities

to resolve it were missed in the subsequent 30 months. The inspectors considered

that this significant condition adverse to quality was the first of five examples of an

apparert violation of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action. ,

(eel 97005 03)

A 10 CFR 50.72 report was made on July 18,1997, stating that the plant had been

operated beyond its design basis in light of this single failure vulnerability. BECo

implemented a temporary modification to shut one of the header isolation valves to

remove the vulnerability. Since the issue regarding system design and reportability

appeared to be sufficiently understood by early June 1997, the inspector considered

that this report was untimely and the second example of an apparent violation of 10

CFR 50.72. BECo later submitted Licensee Event Report 97 01100, " Service

Water System Single Fanure Vulnerability", to the NRC on August 1,1997.

Still ano'her Problern Report 97.9413 was issued on July 3,1997, to clarify an

inconsistency in the plant design information submitted in support of the original

(NRC) SER for Pilgrim. While reviewing the UFSAR and associated documents in

response to PR 97.9408, BECo noted that SER Section 7.4, Salt Service Water

System, stated "On loss of AC power the loops are automatically isolated by

redundant valvss." This would imply that both header isolation valves (MO 3808

and 3813) closo, which differs from the current design where the selective isolation

. of only one valve occurs upon loss of AC power. This is also inconsistent with

~

UFSAR Section 10.7. The inspectors' questioned whether this apparent lack of

redundancy was merely an administrative oversight or a legitimate design

,

deficiency, and this therefore will remain open pending the disposition of

I

PR 97-9413. (URI 97005 06)

_._,,Lm. .,. . . '- ,y y -.- ,m.. ,,., , . - . , ..

_ _ __ . m _ . _ _ . _ __ ___ __ . . .- __ _ . _ _ ___

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c. Conclusions

A new SSW system single failure vulnerability was identified representing operation

.

(ptlor to July 1997)in a enndition outside the Pilgrim Station design basis. This

problem was not reported in a timely manner in accordance with 10 CFR w0.72, and

was also viewed as an example of ineffective corrective action associated with

questions first raised during the 1995 SWSOPl. Once the new single failure i

vulnerability was identified, BECo engineering personnel provided a comprehensive .

i

technical response with a bounding analysis of tidal conditions, and took

- appropriate actions to isolate the SSW headers. An inconsistency in the licensing  ;

basis for the SSW header independence, specifically the redundancy of the cross-

connect valves, remains unresolved.  ;

E1.4 Reactor Buildina Qlosed Coolina Water Flow Marain  ;

a. Inspection Scone (92903)

- The 1995 SWSOPl self assessment identified several weaknesses related to the

reactor building closed cooling water RBCCW flow model, including some

components where the model predicted little or no flow margin. The inspector

reviewed the revised flow model and hydraulic analysis (SUDDS/RF 95 74),

Calculation lAs364, " Containment Heat Removal," RECCW Pump Test Procedure

8.1.11.19, and RHR Operating Procedure 2.2.19.5.

b. Observations and Findinas

RBCCW Flow Model

The revised analysis (model) Vedicted flows supplied to various plant components

for several modes of operation including design basis (accident) conditions with

" degraded" RBCCW pumps. The latter case assumed that the pumps performed

32.3% lower than their design (pump curve) values at all flow rates. This reduction

accounts for the degradation permitted by Pilgrim Technical Specification 4.5,

associated with pump surveillance testing.

The 1995 SWSOPl had noted little or no flow margin existed for some components,

especially low flow " users" such as pump seal water and motor oil coolers. The

inspector was concerned that the high resistance presented to the system by the

low flow users may require significantly higher pump head to supply adequate flow

to those components. The hspector confirmed that flow model results were -

aopropriately used as inputs to Calculation No. M-664,' Revision 0, " Containment

Heat Removal" approved on March 25,1996. Calculation M 664 demonstrated

that the RBCCW system is capable of adequate heat removal, assuming SSW inlet

temperatures up to 75"F and using RBCCW flows predicted by the hydraulic

analysis. The inspector noted that the existing RBCCW pump performance exceeds

I

the minimum Technical Specification 4.5 B requirement of 1700 gpm at 70 feet of

- head. This would result in higher actual flows than those used in the containment

i

heat removal analysis and, therefore, additional flow margin. ,

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_

  • w --v-T-ivwr-re*9-gw-,ry--i'9 pgy,-q,,.--gyv-g gy-_ awn-.mg,*wgy -

y,,-gya-9- y 9y-yyir-i- ,g_.. .py- 9 g n_p-. i yf7.p ,

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14

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BEco Design Engineering personnel stated that Test Procedure No. 8.l.11.19 did

not account for instrument uncertainties. Further, although some field testing has

been initiated (in response to a SWSOPl observation), testing has not yet been

completed as of this inspection to validate the flow model. The completion of field

testing, v .ildation of the flow model, accounting for instrument uncertainties, and

any additional analysis to quantify flow margin remains unresolved. (URI 97005 07)

bolation of Flow to Non Safetv Related Loads

The 1995 SWSOPl self assessment team noted that the RBCCW hydraulic analysis

assumed that flow to nonessential loads was isoldied during design basis

conditions, but there was no guidance provided to operators to isolate these

components (e.g., in Pilgrim Operating Procedure No. 2.2.19.5, "RHR Modes of

Operation for Transients"). Without specific guidance or instructions to operators,

flows to nonessential loads may not be isolated; consequently, RBCCW could be  !

diverted from safety related components. This issue was tracked as an open item

on an informal SWSOPl database (IADB ID SW95.0002.05), but had not yet been

addressed at the time of this inspection. The inspector considered this as a second

example of untimely and inadequate corrective action for a potentially significant

condition adverse to quality, and an apparent violation of 10 CFR Appendix 8, .

Criterion XVI. (eel 97005 03)

There are no formal analyses to dernonstrate or quantify adequate RBCCW flow if

non-essential loads were not isolated. in response to the inspector's questions on

this issue, the licensee revised Procedure No. 2.2.19.5 in July 1997. The inspector

reviewed the approved Revision 2 and found that the procedure change had not

received a written safety evaluation, and was stilllacking in that it would not

require isolation of nonessential luads if suppression pool temperature remained

below 130*F. It was not clear that suppression pool temperatures would remain

below 130 degrees for all design basis scenarios of interest; and, in those

instances, flow to the nonessential loads may still not be isolated. Flow could

therefore still be diverted from so-called "small um " enfety related components,

such as area coolers, RHR pump seal water coolers, cod the core spray pump

bearing cooler which is calculated to recolve 1012 gpm in order to adequately cool

the upper motor thrust bearings. (URI 97005 08)

The inspector concluded that the unisolated nonessential loads constitute a different

case than those analyzed in the RBCCW flow analysis, and is not bounded by the

design basis calculations of record. Similar to the 75'F SSW temperature issue

(Section E1.2), the Boston Edison Quality Assurance Manual, " Design Cnntrol,

requires that enginccring and design activites associated with plant design changes

and modification of nuclear safety-related structuru...are accomplished according to

ANSI N45.2.11 1974, and DECO Nuclear Engineering Services Group Procedure No.

3.05, " Design Calculations", applies to all safety re'ated design analysis, in spite of

the revision to Procedure 2.2.19.5 in July 1997, no formal analyses exist to confirm

that sufficient RBCCW flow will be supplied to the core spray pump bearing cooler

during all design basis conditions. The failure to have an adequata basis for not

isolating nonessential loads as well as to assure that design basis information is

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correctly translated into Operating Procedure 2.2.19.5 is the second example of an

apparent violation of 10 CFR Part 50, Appendix B, Criterion Ill, Design Control j

(eel 97005 02).Further compounding this issue, the inspector noted that Pilgrim  ;

FSAR Section 10.5.5.3, " Accident and Transient Operations," describes the design  !

'

basis operation of RBCCW At 600 seconds, operators manually initiate cooling for

the RHR heat exchanger by starting a second RBCCW pump, valving in flow, and

"

... isolating the nonessential loads on each loop" (page 10.5 3). Therefore, the  !

licensing basis of RBCCW described in FSAR Section 10.5.3 lb also inconsistent  !

with Operating Procedure 2.2.19.5, and represents the third example of an apparent

violation of 10 CFR 50.59. (eel 97005 01)

c. Conclusions

The evaluation of flows supplied using reduced RBCCW pump capability (32.3%)

adequately addressed the degradation issue raised during the 1995 SWSOPl self  !

assessment. The potential for RBCCW flow diversion because of flow supplied to i

nonessential loads represents operation in an unanalyzed cendition outside of the

Pilgrim Station design bases, and represents the third example of an apparent r

'

violation of 10 CFR 50.72 and 73. (eel 97005 04)

E1.5 Desian Basis RHR Flow Ranae

a. JDinaction Scope (92903)

The inspector reviewed Calculation M 664, Revision 0, dated March 25,1996, ,

" Containment Heat Removal," '"-h recalculated the design basis containment heat

transfer and pressure / temperature n...Jonse. Calculation M 664 utilizes input from

.

GE accident analyses, including the suppression pool temperature profile. The

calculation uses a so-called "K" factor to model heat exchanger performance as well

as overall system heat transfer,

b. Observations and Findinag

i

An RHR design flow rate of 5100 gallons per minute (gpm) is assumed in

Calculadon M 664. How:,ver, revisions prior to July 1997 of Pilgrim Operating

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'

Procedure 2.2.19.5, directed operators to throttle RHR flow in a range of 4800-

5100 gpm for containment cooling during design basis conditions. In addition to

procedurally allowing flow loss than design, the inspector found that neither the

procedure nor the calculation account for instrument uncertainty at either extreme.

Consequently, the actual flow supplied to the RHR heat exchanger could be higher

than 5100 gpm, or lower than 4B00 gpm. There was no formal documented

analysis to confirrn that adequate heat removalis provided at the lower flow, *

Including the effects of instrument error. Further, flows greater than 5100 gpm

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-- _ _ --.

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10

may exceed design limits for the heat exchanger, affecting tube vibration and

structural loading.

Probiern Report 97.9363

in response to these issues, Problem Report (PR) No. 97.9363 was issued which

judged RHR to be operable based on engineering judgement "... demonstrating

conservative assumptions in the containment heat removal aneiysis." The inspector

observed that the initial reportability screening review for PR 97.9363 did not

require an evaluation in accordance with 10 CFR 50.72. The licensee revised

Operating Procedure 2.2.19.5 to stipulate that RHR pump flow not exceed 5000

gpm when suppression pool temperature exceeds 130'F and one loop of

containment cooling is used during torus cooling. The licensee contemporaneously

developed analyses (SUDDS/RF# 97 84, Revision 0, July 14,1997, " Evaluation of

RHR Heat Exchanger at 5600 gpm") to confirm that the RHR heat exchanger can be  ;

operated at shell side flow rates up to 5600 gpm without affecting structural

integrity.

On July 18,1997, the licensee notified the NRC that plant operating procedures

specified RHR system operation in the emergency mode that was contrary to that

assumed in design basis accident analyses. However, BECo retracted this

notification on September 12,1997, based on an evaluation (using engineering

judgement) to affirm acceptable RHR performance.

Dulan Bases

The inspectors expressed concern for the effects of flow rates at both ends of the

range. The inspectors considered the basis for the operating range of 4800 5100

gpm to be principally anecdotal, considering normal operation rather than design

basis. The range was selected with consideration of the fact that the

instrumentation used to throttle RHR (full range of 0 20,000 gpm) would be at the

low end of indicated flow. More rigorous evaluation after this inspection --

quantified instrument inaccuracy et 2.8% (of full scale) or approximately .t.560 gpm

in the range of interest.

Using procedures in place prior to July 1997, RHR flow with one pump operation

could therefore have been as low as 4,240 gpm, which is more than 15% below

that assumed in the design basis calculation of record (M-664). Although not

verified during this inspection, the licensee later indicated that the overall K-f actor

utilized in determining containment response would decrease by about 5%,

affecting the predicted torus water temperatures and heat removal from the

containment. While the containment apparently remains operable (bases for

Technical Specification 3.5.8 unchanged at 64 million BTU /hr), the inspectors found

that the design margins would have been reduced. On the upper end, an indicated

flow of 5100 gpm could be as high as 5660 gpm which exceeds structuralintegrity

limits for the RHR heat exchanger. The failure to assure that design basis

information (i.e., appropriate RHR flow range) was correctly translated into

operating procedures (Pilgrim Procedure 2.2.19.5)is the third example of an

-. _ _ _ _ - - - - . - . . -

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17

apparent violation of 10 CFR Part 50, Appendix B, Criterion Ill, Design Control. (eel

97005 02)

Current Licensina Basla

The inspectors also noted that the licensing basis (prior to Amendment No.173)

described in the P;lgrim UFSAR was inconsistent with respect to RHR operating

procedures. Specifically, FSAR Ssetion 4.8.5.4.1, "LPCl with Heat Hejection,"

states (Revicion 20, February 1997, Pago 4.8 0) that rated heet removal from the

containment by removal of one RHR pump from LPCI service, closure of the RHR

heat exchanger bypass valve, and "... valve adjustments as necessary to establish

5100 gpm through the RHR heat exchanger."

Further, in FSAR Chapter 14.5.3, the design basis containment response end core

standby cooling system NPSH analyses are described. Design margins are

determined for maximum suppression pool water temperature (page 14.611) and

RHR pump NPSH required (page 14.512a) based on establisliing a maximum flow

rate of 5100 gpm. Specifically, FSAR Section 14.5.3.1.2, " Containment Response"

(Revision 20, February 1997) describes the transition at two hours after an accident

to a one pump LPCI Heat Rejection Mode to "... provide lated heat removal from the

containment." Similar to other FSAR descriptions, valve adjustments establish

5100 gpm flow through the RHR heat exchanger, and this modo is assumed to

"...run continuously throughout the remainder of the accident response" voth a

peak suppression pool temperature predicted to occur at 5 to 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> af ter the

accident begins. This flow rate is also summarized in FSAR Tobie 14.5 6.

With approval of Amendment No.173 on July 3,1997, the peak suppression pool

water temperature is higher as a result of 75 F SSW and oth-r considerations

including increased decay heat assumptions imposed as a condition to the

amendmont. RHR pump NPSH is calculated based on 185'F pool water

temperature and 5100 gpm; at an increased flow up to 5000 9pm, frictional losses

and required NPSH (extrapolated at 27 feet) would change, thereby decreasing the

margin availablo and placing more importance on the existence of an ovespressure

to compensate for the deficit in suction head. More significantly, following either

Step 9 (page 15 of 26) or Step 10 (page 22 of 26) in Procedure 2.2.19.5

establishes flow at essentially a runout condition and potentially beyond vendor-

certified test data for both flow and required NPSH.

Oneistina Procedures

The inspectors found that revisions to Operating Procedure 2.2.19.5 in effect prior

to July 1997 contained guidanco to operators which was inconsistent with the

design basis calculation (M 664) of record as well as the licensing design basis

described in the Pilgrim FSAR. While steps woro taken to correct the operating

procedure during this inspection, it remains inconsistent with the FSAR as of

October 3,1997. Operators are now instructed to throttle open either the LPCI

(28A/B) or the RHR torus test return valve (36A/B), "...to achieve loop flow at

maximum RHR pump capacity not to exceed 5600 gpm." The licensee contends

. __.

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18  :

that this step will ensure flows in excess of 5100 but loss than 5600 gpm. While

the Inspectors did not review the revised calculations to ensure desired flows

remained between 5100 5600 gpm, the inspectors did note that this represents a

change to the facility as described in FSAR Sections 4.8.5.4 and 14.5.3. Sinco no

safety evaluation was performed to reflect those design changes (i.e., higher system

maximum flow rates hbovo 5100 and up to 5600 gpm), this was considered as the

fourth example of an apparent violation of 10 CFR 50.b9. (eel 97005 01)

Further, the ins;)octors were concerned that if the margins for suppression pool

water temperature or EC/;S pump NPSH associated with Pilgrim Amendment No.

173 were decreased, then this problem may also represent a potential USO.

Amendment No.173 was based upon RHR flow of 5100 gpm which required 23

feet of NPSH and affects head losses, EDG loadings, and strainer pressure drop.

Calculations of record, which support the approved (and current) licensing basis,

show that while the core spray pumps are moro limiting with respect to NPSH, the

'

RHR pumps also require a small amount of containment overpressure (approximately

0.04 psig). With the approval of 2.5 psig of overpressure beyond 100 minutes in

Amendment No.173, the RHR pumps are predicted (and licenced) to have about six

foot of suction head margin at R100 ppm. However, at the increased flow of 5600

gpm this margin is reduced to about four feet but, more significantly, a near runout

condition is created, thereby affecting the long term reliability of the pump and

increasing the likelihood of pump failure. Lastly, considering both the uncertainty

with measured flow and certified pump performance at flows in excess of 55;')

opm, RHR heat exchanger structural integrity and the potential for component

failure is similarly in question.

ReportoMity

Regarding the adequacy of containment heat removal at RHR flows lower than 5100

gpm prior to July 1997, the inspectors considered the potentit.Ily higher peak

suppression pool temperature to be significant. While the FSAR value reported on

, page 14.511 of 178'F was changed after July 3,1997, by Amendment No.173

(and is in fact also affected by assumptions regarding CSW temperature,

containmont overpressure, and ECCS strainer design), the inspectors considered the

lower flow case to be an unanalyzed condition that significantly compromised plant

safety, as well as a facility change outsido the Pilgrim design basis, not

appropriately evaluated in accordance with 10 CFR 50.59.

In reviewing the NRC staffs' safety evaluation associated with Amendment No.173

(Section 3.1.2, page 5 and 6), the peak calculated pool temperature with 65'F

SSW had been 166'F, prior to July 1997. The inspectors concluded that - if 75'F

SSW and credit for overpressure were invalid prior to July 1997 -- the possibility of

RHR flow in the long term heat removal mode with one pump potentially as low as

4240 opm or as high as 5660 gpm (particularly for long periods of time) similairly

represent operation in an unanalyzed condition outside of the design basis.

Therefore, the retraction on September 12,1997 (two months after an ENS report,

but with no LER issued), is the fourth example of an apparent violation of 10 CFR

50.72 and 50.73. (eel 97005-04)

_ , _

_ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ___ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ . _ _ - _ _ - _ _ _ _ _ _ _ _ _

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10

c. Conclusions

Prior to July 1997, Operating Procedure 2.2.19.5 permitted operation of the RHR

system at flows both above and below design basis, without a rigorous and '

formalized analysis of the effects on not only component performance but overall

containment response. Operation at RHR flows substantially higher or lower than

5100 gpm would be outside the Pilgrim design basis, and presents problems to

operators because of f.560 gpm uncertainty in measured RHR flow. This issue

reflects problems rogarding design control, reportability and safety evaluations that

were (and still are) not accurately reflected in the Pilgrim UFSAR.

E1.6 Diesel Generator load Calculations

a. Scoco of insocction

The 1995 SWSOPl self assessment questioned diesel generator (EDG) loading,

assuming various single failures r,uch as the failure of the SWS header pressure

switches or the failure of the EDG load shed circuitry. The inspector reviewed

BECo's response to this ope, item including related calculations and operating

procedures,

b. Observations and Findinos

The inspector reviewod ceiculation PS 79, " Emergency Diesel Generator Loading,"

Rev. 4, dated January 19,1996, and calculation comment sheets outstanding

against PS 79 up to comment sheet PS 7019. The inspector confirmed that the

calculation addressed all the loading combinations questioned during BECo's 1995

self assessment. The inspector confirmed that the calculation resulted in

demonstrating a worst case or smallest margin of 01 kilowatts (kW) below the

2000 hour0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> limit (i.e. 2750 kW). This case was based on operator actions (beyond

10 i.11nutes) to remove certain loads and in the event of the failure of a SSW

pressure switch.

During the review of the calculation, the inspector noted two additional deficiencies.

The 250 Volt de battery charger did not include the power drawn during current

limit operation similar to what had been included for the 125 Volt de battery

chargers, in response to the inspector's question, the licensee estimated that this

could amount to an additional 6.4 kW for each 250 Volt battery charger with a

110% current limit. Also, the calculation did not address the effect on generator

load by the motor driven pqmps frequency variation from a nominal 60 Hertz.

Motor speed, and therefore pump speed, varies with frequency; pump speed, in

turn, affects flow and power drawn by the pump. BECo initiated Problem Report

(PR) 97.9541 to address the frequency variation, but did not expect substantial

changen in calculation results based on a tight governor control of diesel speed to

+ /. 0.2 5 E

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The inspector also noted the cuver sheet to calculation PS 79 indicated the analytls

did not require revision to affected d6 sign documents. BECo acknowledged that l

they did not have a cross reference list of documents affected by this calculation.  !

Calculation comment sheet PS 7912 had already identified the fuel capacity

calculation as an affected document prior to this inspection. The inspector further

noted that the cover sheet did not address other documents such as operation and

surveillance procedures.

The inspector comparret the diesel generator loads documented in design basis

calculation PS 79 to Operating Procedure 2.2.8, " Standby AC Power System", Rev.

42, dated August 8,1997. Attachment 5 to this procedure, Diesel Generator

Loa-fing Table, is a twelve page guide uhsd by the operators when they must

remove Partain loads (in the licensing bases beyond 10 minutes). The inspector

found eiumerous discrepancies betw9en thic table and calculation PS 79; six out of '

ten l>sds an page one of the procedure were wrong. The discrepancies found in

calculation PS 79 would not necessarily result in an automatically applied calculated

dieselload above the 2000 hour0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> ratlhg. BECo indicated that they had known about

the inconsistencies since the 1995 SWSOPI, and had issued tracking item SW l

95.0029.04 to revise Procedure 2.2.8.

However both calculation PS 79 Revision i 4) and Procedure 2.2.8 have since been

revised Revision 42), but without ensuring consistency. The inspector found that '

Engineer ng staff had not issued any Interim instructions to Operations cautioning

them ab eut this discrepancy. BECo indicated that following a start of the diesel

gJneratf/, operators Would be dispatded locally to monitor its operation, including

engine temperature; therefore, it was believed that they would not overload the

diesel. The inspector noted that not only was the tracking item still open, but it

was not included or entered as part of the formal P;lgrim corrective action process.

Knowledge of the discrepancy iIso apparently pre dated the 1995 SWOOPl

observation (i.e., PCAO 88 506). Moreover, the inspector noted that proper

removal of loads is critical to not exceeding the 2750 kW design limit.

Section 5.3 of Procedure 2.2.8, Precautions, notes that the connected load is

reduced to less than 2750 kW after 10 minutes. This is the 2000 hour0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> rating for

the diesel but does not account for the accuracy of the kW meter. BECo issued i

Problem Report PR 97.9559 on September 5,1997 to address this issue. BECo

indicated that any inaccurar e in the meter would be less than the 10% overload

capablilty of the niachine, and would be correc,tod by the operators dir atchnd to  :

- the diesel prior tr. reaching the t.vo hour (in 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />) overload limit,

c. Conclustom

The failure t1 correctly translate the dasign baals results of calculation PS 79 into

the loading table in Procedure 2.i',8 and the lack of consideration of the accuracy of

the kW meter constitute the fourth exemnle of an apparent violation of 10 CFR 50,

Aogr h B, Criterion 'll, Design Control. (eel 97005 02)

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, y, _ y.,my...-_,.~,,. . . , . , . . ~ .r,.,,. . ,.,._.-,,_m--- y-.,.,...,._,m.y

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Similar to the finding related to the SSW pressure switches (refer to Section E1.3),

the question related to EDG loading calculations was an example wherein the single

failure analysis committed to under Generic Letter 8913 had been found to be

lackmg. But more than two years after the SWSOPl team's concern for what had

been characterized as a weakness (one of seven observed) in the procedural

guidance provided to operators regarding EDG loading (particularly SSW and

RBCCW pumps), numerous inconsistencies between calculation PS 79 and

Operating Procedure 2.2.8 persisted. Failure to ensure consistency between the

design basis EDG loading calculation and the operating procedure represented a

potentialiy significant condition adverse to quality, indicative of untimely and

inadequate corrective action and the third example of an apparent violation of 10

CFR 50, Appendix B, Criterion XVI. (eel 97005 03)

E1.7 Diesel Generator Ambient Temocrature

a. Scone of insocction

One of the open items from DECO's 1995 SWSOPl self assessment was a question

of the maximum allowable ambient temperature for the diesel generator and ita

offect on engine operation. The SWSOPl team noted the specified maximum

ambient temperature of 80'F had been exceeded in the past, but the consequences

for engine cooling and combustion air were not thoroughly addressed. The

inspector evaluated DECO's progress on resolution of this problem, and reviewed the

Pilgrim FSAR, Coltec studies and Operating Procedure 2.2.8.

b. Qhpervations and FindiDDI

8ECo initially addressed the problem of operating the diesel beyond its specified

maximum ambient temperature by attempting to take advantage of any built-in

margin in Jacket water or lube oil temperature limits. BECo did not place any interim

limits on dieselloading when operating above an 88'F ambient until Revision 42 of

Procedure 8.9.1 (" Emergency Diesel Generator and Associated Emergency Bus

! Surveillance") was issued on June 20,1997. Jacket water coolant was changed

'

from a 50/50 glycol mix to pure water in June 1997 to take advantage of the

increased heat capacity and thermal conductivity.

Maximum Deslan Basis Ambient Temoerature

i

Historical data for the years 1994,1995,1996 and 1997 indicate that the ambient

temperature exceeded 88'F in each year, prior to the switch to 100% water

coolant. FSAR Table 2.315, " Temperatures - Plymouth, Mass," indicates " extreme

maximum" temperatures above 88'F; the highest temperature recorded in this table

is 102*F for the months of June, July, and August. The 88 cogree value is

apparently a "1% ASHRAE exceedance rate"; nonetheless, the EDG design

specification performance ratings are based on this number.

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22

BECo had not performed an operability evaluation until the time of this inspection,

when problem report PR 97.9303 was initiated. The inspector was concerned that

this evaluation was based upon oreliminarv information obtained from the diesel

supplier, Coltec, on Novembei 8,1996 (Report R 6.00-0260). Coltec's evaluation

did not unilaterally endorse operations above 80'F ambient, nor change established

operating limits. Therefore, at temperatures in excess of 95'F, the diesel generator

and other components ins!de the room could have been subjected to temperatures

beyond their design if the closels had been called upon to operate in a design basis

event. This represented operation in an unanalyzed condition prior to June 1997

significantly compromised plant safety, outside of the Pilgrim design basis of 88'F

ambient fur rated EDG performanco, and is the fifth example of an apparent

violation of 10 CFR 50.72 and 50.73. (eel 97005 04)

June 1997 Desinn Channe

The inspector found that ambient temperature has exceeded 88'F during the

summer months. Worst case recent data from Met Tower readings indicate e

maximum ambient of 97'F reached between 1:00 to 2:00 P.M. on July 14,1995

and May 21,1996. Temperatutes at lower ground elevations -where outside air

enters the EDG Duilding and is mixed with room air--are expected to be higher (e.g.,

heating off of black top and surface effects). The inspector independently used the

predictions of the Coltec Analysis to make the case that the ability of both EDG's to

achieve rated 2750 kW output was in question during past instances where ambient

temperature exceeded 95'F. At temperatures in excess of 95*F, this condition

could result in derated engine performance, even with the "new" predict;ons for a

50/50 mix.

Nonetheless, the results of the preliminary Coltec evaluation were used as part of a

Pilgrim Design Change (PDC 9715) approved on June 17,1997, to permit EDG

operation at outdoor temperatures up to 93'F with a 50% jacket water / glycol

mixture, and up to 102'F with a 100% water mixture. These limits were formally

instituted within Procedure 2.2.8, " Standby AC Power System," Section 5.2,

Administrative Limits. The die.els were operated with the 100% water coolant (for

the first time) during the summer of 1997. BECo attempted to verify the predicted

jacket water temperature in the Coltec evaluation by testing at 2000 kW load and

one hour runs during the months of June, July and August 1997. The expected ten

degree drop in Jacket water temperature did not occur, and the change was

ultimately considered indeterminent because it did not produce the results predicted;

the licensee subsequently initiated atiother problem report PR 97.9536 on August

25,1997 and replaced the 100% water with the 50/50 glycol mix in early October

1997.

HQnertobility Evaluation

The EDG design needed to be modified to accommodate operation above the 88'F

design basis, yet the licenseo maintained in an August 16,1997 evaluation that this

was not reportable since it is...a nominal design parameter... not a station operating

or licensing limit... it is a component limit." The inspector disagreed with the

. __ _ _ _ _ _ _ .

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evaluation, noting not only that the design needed to be thanaed in sune 1997 but  :

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also that FSAR Section 10.9.3.9 and FSAR Table 10.9 2 require revision to address

the 88'F outdoor ambient and related engine coolant (i.e., antifreete). Since both ,

EDG's would be potentially affected in a common mode sense by high temperature,  ;

the inspector considered the functionalMy issue as significant. The engineering  !

evaluation associated with PR 97.9383 condudec; operability based on 93'F l

ambient air with a 50/50 glycol mix; this remilns inconsistent with past Station

experience at outside air in excess of 93*F, even af ter the June 1997 change was ,

later found to be not well founded.

in fact, the evaluation of reportability was delayed, and dispositioned eight weeks

ofter the operability determinations, suggesting a flaw in the reportability process, .

and an emphasis upon operability in contrast to design basis focus. l

!

Safety Evaluations -!

The common mode failure of both EDG's represents a risk significant implication.

The inspector therefore questioned the scope of the licensee's evaluation of high .

ambient temperature and suggested that the diesel room could possibly experience

an even hotter temperature when the outside ambient exceeds 88'F. The inspector

found that the generator was rated for 2600 kW in a 40*C (104'F) ambient. The ,

diesel generator specification (6498-M 0, Rev.1, dated September ^,1969) l

Indicated that the room design temperature was 105'F. BECo responded by issuing

problem report PR 97.9540 on August 28,1997, which indicated the room

temperature could possibly reach 13 degrees above outside ambient during diesel

operation. Therefore the room temperature could reach 115'F.

During the evaluation stage for this problem report, BECo administratively limited

the operation of the diescis at 88'F outside air temperature. The safety evaluations

for both the June 1997 change to 100% water and the August change back to a

50/50 mir. of glycol did not address highor air temperature effects on key engine

performance characteristics such as fuel consumption rate. Further, the overall

impact on accelerated engine wear and the possible engine power de rating which

90100*F ambient air would conceivably have, were also not addressed in either

SE 3102 (in June) or SE 3110 (in late August). The evaluations were concluded to

be narrowly focused (again upon operability, similar to the design work), and were

not critical of the more safety significant aspects of the issue.

The inspector found that safety evaluations, 3102 and 3114, (upon which Revision

41 to procedure 2.2.8 was based), were not comprehensive and-in retrospect-

'

technically incorrect. _ Further, the evaluations were generally qualitative in nature ,

and based on preliminary input not properly validaied. Even when post modification

tests in June did not achieve the expected results, the engines were considered

operable through the next four months. The testing did not conclusively

demonstrate design basis EDG function above 88'F ambient; therefore, operability

with water / glycol mixturo above that temperature remained questionable,

_ ._ . _ . _ _ ,_ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ __ . _ . , , __

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24

c. Conclu'dQa!

DECO's corrective actions, for the realistic likelihood of operating bo h diesel

generators above their specified design outdoor ambient maximum temperature of  !

88'F, were untimely and narrowly focused. This issue, which pre-dated the 1995

SWSOPI, also presents a concern for 'perability prior to summer 1997 with 50/50

Olycol Jacket water coolant when amt nt exceeded 95'F on occasion. This is the

fourth example of a significant condition adverse to quality which has not been

appropriately resolved and an apparent violation of 10 CFR 50 Appendix B, Criterion

XVI, Correctivo Action. (eel 97005 03)

E1.8 Drvwell Sorav Flow Modifications

a. Inspection Engno.122R_Q21

The inspector reviewed portions of several Problem Reports (PR), a past

modification of the RHR spray header caps to reduce drywell spray capability,

related Safety Evaluations 2133 and 3090, and a more recent chango to increar,e

drywell spray flow to 1245 gpm. Desien Change PDC 86 52A was engineered in

1987 to replace the existing upper and lower drywell header spray caps with

assemblies having six of seven nozzlos capped. The resulting lower spray flow rate

reduced the risk of structural damage from an inadvertent spray Initiation in a hot

dry atmosphere, and allowed for a beyond design 5 asis alternate spray configuration

in certain risk significant scenarios. However, the reduced spray capability

impacted the limiting containment temperature profile used for environmental

qualification (EO).

b. Observations and Findinas

1987 Sorav Modification

BECo determined (based on a 1987 GE study) that a spray flow of 300 gpm was

sufficient to maintain the drywell airspace temperature to less than 340 degrees as

well as below the drywell liner structural design limit of 281'F. The calculation

(M6601, Revision 0) predicted a flow rate of 720 opm for the maximum det an

spray capability from December 1988 through May 1997.

DE Model Errors

in January 1996, BECo identified a question related to the development of new

drywell temperature profiles associated with higher (75'F) SSW inlet conditions.

BECo found that the preliminary profiles were not similar to the analysis of record.

The computer modelling error involved certain small break sizes and an incorrect

" simplifying" aswmption that drywell temperature was equal to the reactor vessel

temperature. Consequently, a slightly higher peak temperature (334*F versus

330 F) was predicted and from one hour to ap roximately 220 hours0.00255 days <br />0.0611 hours <br />3.637566e-4 weeks <br />8.371e-5 months <br /> after the

l

event, substantially higher drywell temperature (averaged approximately 35 degrees

higher) than the analysis of record since 1987 (SUDDS/RF 87 917, dated

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25

September 2,1987, "Drywell Temperature Analysis"), representing an apparent

violation of 10 CFR 50.49(o)(1). (eel 97005 05).

A problem report was generated to assess operability after the model error was

discovered. New (corrected) EO profiles were produced- both for 65'F and 75'F

SSW- and five motor operated valses (located insido the drywell) were identified as

having position indice.tlon not fully qualified. The evaluation at that time considered

the position indicators for the five containment isolation val'" in question to be

able to "... survive the 30-day mission time with the higher drywell temperature,"

but this was based upon engineering judgement and required later re testing to

demonstrate they woro "qualifiable."

The safety function of containment isolation was deemed fully operable, because of

tho short active mission period (to close) and the subsequent time nooded using

position indication for operators to verify the change of state of the valves. As part

of the corrective action associated with PR 96.9028 initleted on January 26,1996,

BECo recommended that a requirernent be added to Nuclear Engineering Procedure

3.01, " Review, Evaluation and Accoptance of Supplier Design Documents". to

review inputs and assumptions used by suppliers in safety related analysos to the

extent practical. The inspector noted that this procedure had not been changed,

representing the fifth example of untimely / inadequate corroJive action and an

appars.nt violation of 10 CFR 50, Appendix B, Criterion XVI. (eel 97005 03)

BECo representativos stated that a reportability evaluation had been conducted in

1996, in which the condition was fourid not to be reportable, in response to NRC

questions, BECo completed another reportability evaluation on September 5,1997,

which (onco again) concluded that the condition was not reportable. The inspector

disagrood with this determination on the basis that the drywell temperature profilos,

which constitute the analyses of record for EQ purposes, establish a design basis

condition for the plant. And, between 1987 and 1996, the drywell temperature

profiles of record could have been exceeded during postulated main steamlino break

(MSLB) accidents. Hence, this condition represented an unanalyned condit on that8

significantly compromised plant safety, and which was outside of the plant design

basis and the sixth examplo of an apperent violation of 10 CFR 50.72 and 73.

(eel 97005 04).

Further Nonconservatism

Problem Report 97.9101 originated on February 12,1997, identified two concerns

related to the drywell spray flow: (1) the now (proposed) drywell temperature profile

based on a 75*F ultimato heat sink temperature assumed design RHR pump

performance, as opposed to the minimum pump performance permitted by Technical

Specifications; and (2) the analysis was based on a hydraulic calculation that

underestimated the difference in elevation between the minimum torus water level

and the uppJr drywell spray header. The engineering evaluation associated with PR

97.9101 determined that the affected equipment was operable if existing RHR

pump performance was considered. The inspector noted that these errors resulted

in reduced spray flow capability, below the 720 gpm value upon which EQ profiles

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and containment response were based. Also notable was that the EO calculations

of record throughout this entire period in question (19881997) were based on

65'F SSW, which had been exceeded on many occasions.

Increased Sorav Caoability

l

In conjunction with Pilgrim Amendment No.173, the NRC required further analysis

using a higher decay heat input, which results in higher predicted drywell

temperatures. To offset the resulting temperature increase, a modification was

instituted during the May 1997 outage (PDC 97 06) increasing the number of spray '

nozzles on the upper drywell spray header from 104 to 208, and from 104 to 196

on the lower header. The resulting spray flow :apability was increased to 1245

gpm. BECo concluded in Safety Evaluation No. 3090 that the increase in flow rate

offset the drywell temperature increase that would otherwise result from the higher

dacay heat input.

c. Conclusio.D1

from 1988 until early 1996, Pilgrim was operated in a condition where design basis '

drywell temperature profiles could have exceeded established Environmemal

Oualification design temperature limits for equipment exposed to this environment

during a postulated (MSLB) accident. While the 1987 computer modelling error was

a subtle problem not easily identified, it represented a violation of 10 CFR 50.49 not

reported to the NRC, and for which appropriate corrective action (under PR

96.9028) has not been instituted.

i

E1.9 SSW Svstem Inservice Testina

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a. Inspection Ergp1(92903)

The 1995 SWSOPl self assessmont team identified a SSW system testing weakness

regarding flow measurements. The ultrasonic flow instruments installed by plant

design change (PDC) 91 10 to support inservice testing (IST) were not reliable or

formally incorporated into IST program by Relief Request RP 5. The inspector

reviewed plant records and had discussions with plant personnet regard
ng the

licensoe's IST program and its irnplementation, including the use of ultrasonic flow

instruments in periodic SSW pump tests. The inspector also reviewed the

licensee's actions regarding LER 9510 which involved an erroneous reportability

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determination rendered in 1994 regarding the past operability of the SSW pumps,

b. Observations and Findinas ,

l -Relief Reauest RP 5

Procedure 8 l.1,1, inservice Pump and Valve Test Program, Revision 8, dated

March 11,1997, was in effect at Pilgrim for defining IST program requirements.

The basis of Relief Request RP 5 indicated that the flow measurement requirement

during the SSW pump test was not achievable due to lack of instrumentation.

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DECO's basis for relief stated that while shutoff head testing would still bs used,

ultrasonic flow instruments would also be used during a proving period to determine

their reliability and accuracy to support SSW pump fu4 flow testing.

Full flow quarteriv testing with ultrasonic flow instruments in accordance with

Procedure 8.5.3.2.1, SSW System Pump and Valve Operability Tests with Full Flow

Test Conditions, began in 1996. Prior to this time, BECo had taken measures to

properly calibrate the ultrastnic flow measurement equipment to ensure that the

ASME Code accuracy requirements would be met when using the equipment for

official IST tests. The celibration work was done at A's' t. abs with the 22. inch

titanium piping spool representative of the Pilgrim Sh f.pmg. The ultrasonic flow

equipment was installed so as to match the results against the Alden Lab

instrumentation which had been calibrated to the NationalInstitute of Standards and

Technology.

BECo adopted the use of the ultrasonic flow instrumentation for SSW pump

inservice testing per Procedure 8.5.3.2.1 in October 1996. The inspector verified

that BECo had taken appropriate measures to ensure that the flow instrument

accuracy requirements were properly accounted for during testing and that

adequate instructions were included in the Procedure 8.5.3.2.1 for operating the

flow measurement equipment. BECo was preparing Revis;on 9 of the IST program

to retract Relief R squest RP-5 since they were now conforming to the ASME code

requirement for ficw measurement.

LER 9510

During a previous inspection (NRC Inspection Report 95 22), the inspector identified

an erronooJa reportability determination made by the licensee regarding several

degraded SSW pumps. This item was documented as part of Unresolved item 95-

2102. This determination was the result of a reportability evaluation conducted in

conjunction with Problem Report 94.9385. The PD, in turn, was written to

document a discrepancy between Technical Specification (TS) requirements for a

SSW pump head (2700 gpm at 55 feet TDH) versus a SSW system calculatun that

concluded a SSW pump should delivu. 2700 gpm at 87.5 feet TDH. Upon further

review of the reportability evaluation, the licensee determined instances where SSW

pumps were inoperable due to fa: lure to meet the TS requirement and hence

reportable in accordance with 10 CFR 50.72. This development caused the

issuance of LER 9510.

The inspector evaluated the effectiveness of the corrective acticas taken to

determine if similar erroneous reportability determinations may have been made

regarding other issues. The licensee had conductcd a 3 Jerson review of about

25% of the reportability evaluations conducted in the sa'ne 1 year period. The

licensee concluded in LER 9510 that the erroneous tor ortability determination was

an isolated occurrence. However, the inspector noted that this conclusion was (in

retrospect) not well supported based on the findings from this current NRC

inspection, specifically considering the numerous examples regarding licensee's

f ailure to adhere to the reporting requirements of 10 CFR 50.72.

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28

c. CRD_qlusloas

BECo has adequately implemented quarterly full flow testing of SSW pumps using

ultrasonic flow instruments in accordance with the ASME Code requirements for

flow measurement. The conclusion in LER 9510, that a past erroneous

reportability determination was an isolated occurrence, is not well sue . 4rted Lased

on other examples of reportability problems in this report,

i

E1.10 Automatic Startina of SS$ and RBCCW Pumos durina ECCS Testina

a. Insoection Scoce (92903)

The 1995 SWSOPl self assessment team observed a testing weakness in regarding

technical specification ECCS testing. These tests are performed every refueling

outage to confirm that the emergency diesel generator adequately accepts

emergency loads, but did not confirm the start of smaller loads such as the SSW,

RBCCW, er TBCCW pumps. The inspector reviewed the applicable procedures and

discussed them with cognizant Engineering and Operations personnel,

b. Observations and Findinas

The applicable plant procedure that describes ECCS testing is Procedure 8 M.3.1,

"Special Test for Automatic ECCS Lo,ad Sequencing of Diesels and Shutdown

Transformer with Simulated Loss of Off Site Power". The inspector confirmed that

this procedure had been revised to include specific steps to record the automatic

ctart of the SSW, RBCCW, and TBCCW pumps which adequately resolved the 1995

SWSOPi comment. The inspector also reviewed the results of the most recent

special ECCS test conducted in April 1997. The inspector verified that one SSW,

one RBCCW, and one TSCCW oump automatically started durir1 this planned ECCS

test.

-

c. Conclusions

BECo adequately vm t +he 1995 SWSOPl self assessment observation regarding

the confirmation of v.tallloads starting during ECCS testing.

E1.11 Sea Water Levels Assumed in SSW System Analyses

-

c. Inspectior. 3cooe (92903)

The inspector reviewe! severallicensee documents to understand the sea water

- levels used to deterrt ie SSW system flows for assessing RBCCW heat exchanger -

performance. The documents included appropriate sections of the UFSAR and

BECo Safety Evaluation (SE) 2982 which reduced the minimum required SSW flow

rate to the RBCCW heat exchanger from 5000 gpm to 4500 gpm during accident

'

conditions,

,

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - ______I____________________ .

.

4

29

b. Observations and Findinas

The inspector noted that BECo SE 2982 and Section 10.7.S. Sa:t Service Water

System Description, included a tide level of 8.3 feet as a parameter int the SSW

pump's required performance of 2700 gpm at 87.5 feet TDH actr.ss 'he pump's

impeller. The inspector further noted that this tide level wu not consisMnt with

7.1 feet minimum tide level used in the analysis to evaluate the new single 'ailure

vulnerability discussed in Section E.1.3 A third tide level vrdue of - 13 feet,9

inches related to SSW pump performance is also included in Section 2.4.4.2 of the

FSAR defined as "the minimum sea water level at which the service water pumps

maintain design conditions." The inspector discussed this information with th6

cognizant design engineer and obtained the following clarification.

1. The tido level used in accident analysis calculations was - 7.1 feet which is

the yearly astronomical minimum low tide. This value is used to determine

minimum SSW system performance required to perform the emergency

containment cooling function.

2. The basis for the tide level of - 8.3 feet previously referenced in SE 2982

and the UFSAR could not be substantiated and will be removed from the

UFSAR.

3. The rated performance of a SSW system pump is 2700 gpm while

developing 95 feet TDH across the pump's impeller. The minimum sea water

level for the SSW pump maintaining this design performance is - 13 feet,9

inches.

'To inspector verified that the cognizant engineer had submitted an UFSAR change

raquest in June 1997 (for the next annual UFSAR update) to the BECo Licensing

Department to clarify the sea water level requirements applicable to SSW pump

performance, as discussed above,

c. Conclusions

The inspector obtained and was satisfied with the clarification of the sea water

levels applicable to SSW performance to support accident requirements. BECo was

processing a change to the UFSAR to clarify this sea water levelinformation.

E1.12 Heat Transfer Capability of Safety Related Heat Exchanaers

a. insoection Scoce (92903)

lne inspector reviewed a number of activities concerning the performance of safety

related heat exchangers. This included procedures for periodic heat exchanger

thermal performance tests, periodic SSW system full flow tests for the RBCCW heat

exchangers, and recent replacement of the etBCCW heat exchanger heads.

l

. _ _ _ _ _ _ _ _ _ _ _ - _ - _ _ _ _ _ _ _ _ _ -

_

!

!

.

30

b. Observations and F;ndinos

During the recent refueling outage, the licensee modify the heads of both RBCCW

heat exchangers to prc, vide a long term resolution of por head cracks. The most

recent head problem, which was reported in LER 96 008, was a through-wall crack

in the channel cylinder of the "B" RBCCW heat exchanger due to fatigue caused by

cyclic loading of the attached lower partition plate. The original heat exchangers

wem under designed such that the channel partition plates and channel heads were

thinner. With the increased cylinder shell and partition plate thickness and some

changes to the tube inlet flow pattem, the inspector was initially concerned that the

hydraulic loss in the new head might significantly increase and hence have a

negative impact on prior SSW system calculations. However, after discussion with

the cognizant engineer responsible for the modifiention, the inspector loamed that

this potential problem area had been reviewed with the heat exchanger vendor who

concluded that the increase in the hydraulic losses in the new head would be

insignificant. The inspector had no further comments.

In reviewing the plant records that documented the replacement of the RBCCW heat

exchanger heads, the inspector noted that BECo had performed a SSW system full

flow test on each heat exchanger in accordance with Procedure 8.5.3.14, SSW

Flow Rate Operability Test, prior to returning it to service. Procedure 8.ti.3.14

provides a method of demonstrating that each SSW system loop can provide 4500

gpm to its respective RBCCW heat exchanger without exceeding the heat

exchanger's design basis pressure drop. Plant records indicated that the "B"

RBCCW heat exchanger modification had been completed in March 1997 with a

satisfactory retest per Procedure 8.5.3.14. However, on April 3 and 4,1997, with

the plant shutdown, the "B" RBCCW heat exchanger f ailed to meet the procedure's

pressure drop acceptance criteria. The heat exchanger was declared inoperable and

immediate corrective actions were taken to backflush it repeatedly.

The inspector reviewed the associated Problem Report 97.9261 wherein BECo

concluded that the direct cause was attributed to macrofouling from a severe

northeaster storm of April 1,1997. This Problem Report had been closed and the

inspector questioned the thoroughness of the licensee's corrective actions as

follows:

1. Were BECo's corrective actions appropriate knowing that the "A" RBCCW

heat exchanger was undergoing modification at the time and not available for

cooling?

2. Were lessons teamed from this problem such that existing storm readiness

procedures could be improved?

During subsequent discussions the inspector determined that BECo had acted

appropriately to correct the flow blockage of the "B" RBCCW heat exchanger.

However, regarding lessons leamed from the problem, BECo agreed to improve

Procedure No. 2.1.37, Coastal Storm - Preparations and Actions. Provisions would

be included to check for potential safety system degradations, such as macrofouling

i

1

. _ __ _ _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ _ _ _ _ - _ _ _ - __

'

1

1

.

31

in portions of the SSW system, after a storm. This procedure change would result

in a proactive rather than a reactive approach to the effects of a storm. The

inspector had no further comments.

BECo had compiled Procedure No. 8.5.3.14.1, RBCCW Heat Exchanger Thermal

Performance Test, and used this new procedure to test the "A" RBCCW heat

exchanger during the 1997 outage. The "B" RBCCW heat exchanger will be tested

during the next outage. The procedure clearly presented the acceptance criteria

which included appropriate allowances for uncertainty of the test results. The test

results showed fouling factors well below allowable values,

c.- Conclusions

BECo has been adequately testing the RBCCW heat exchangers at full flow

conditions, demonstrating design basis capability. The new test exchanger thermal

performance test procedure contained clear acceptance criteria.'

E1.13 SSW System Pioinn Throuch Wall Leakaae

a. Insoection Scone (92903)

The inspector discussed the long term corrective actions being taken regarding a

recent through wallleak in a section of SSW system piping,

b. Observations and Findinas

On June 23,1997, a through wallleak (3 places) developed in the SSW outlet

piping of the "B" RBCCW heat exchanger near the downstream flange of a butterfly

valve, MOV 3806. BECo developed a corrective action p!an to effect short term ,

repairs of the affected piping. The NRC reviewed this matter as discussed in NRC

Inspection Report 50-293/97-07. The inspector was also concerned about BECo's

long term corrective actions, including the root cause analysis, since this problem is

intimately related to recommended action ill of Generic Letter 89-13 regarding the

need for a routine inspection and maintenance program for open-cycle service water

system piping to ensure that erosion and corrosion cannot degrade the system

performance.

BECo issued Problem Report 97.9399 on June 24,1997, to address the problem.

The defective carbon steel piping spool was determined to be part of the original

SSW system piping. Initial evaluations attributed the cause to a localized loss of

rubber lining and subsequent erosion / corrosion of the carbon steel pipe. The

inspector discussed the long term corrective action plans with the cognizan* deign

engineer who also was involved in the pipe patch implemented for the short term

repairs. Several engineers were assigned to perform a root cause analysis which

would not be finalized until the section of piping was removed for analysis (probably

the next refueling outage). An inspector followup item will be opened to review the

results of the final root cause analysis of the through wall piping leak near MOV-

3806 (IFl 97005 03).

_ - _ - - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - -

- . _ - . - = - - . _ - - . . . _---- - - - -.-- - -.

.

-9

32

c. - Conclusions

BECo took adequate corrective actions to effect short term repairs of the SSW

piping through-wall leaks. The root cause analysis of the piping leaks has not been

finalized, pending the removal and inspection of the pipe section during the next

outage.

E1.14 Plant Walkdowns

b

a. Inspection Scooe (92903)

The inspector observed the mat 6 rial condition of various SSW and RBCCW system

equipment during plant walkdowns. The inspector discussed these observations

with BECo personnel.

'

b. Observations and Findinos

The inspector noted tha modifications (Plant Design Changes 94-29 and 94 31) that

had been implemented to upgrade the screen wash system piping and strainers and

the screenwelllevel instruments. During a walkdown in the reactor building, the

inspector questioned the preventive maintenance measures applicabie to the

equipment hoses that connect the RBCCW piping to the ECCS pump area coolers.

BECo confirmed that these hoses were original plant equipment. While the exterior

of thest. hoses were periodically inspected, the licensee could not confirm the

condition of the interior of the hoses, and decided to issue maintenance work

>

requests for replacement. The inspector had no further comments.

During a plant walkdown in the intake structure, the inspector questioned the SSW

system pressure switch tubing's ability to withstand seismic interaction with

adjacent SSW discharge piping in two pipe floor sleeve locations.1he licensee's

civil / structural engineer confirmed that restraints were in place at both sleeve

locations to protect the tubing from the potential interaction. The inspector found

this resolution to be acceptable,

c. Conclusions

Material condition in the areas toured and for the equipment observed was

acceptable. Several walkdown observations that were noted by the inspector were

satisfactorily resolved.

_ , _

. __ . . _ . . _ . .-. _ _ _ _ . _ . _ _ . _ _ - . _ .. . _

.

.

33

'

E7- Quality Assurance in Engineering Activities

E7.1 independent Overslaht of SWSOPl Corrective Actions

a. _ Inspection Scope

- The inspector met with BECo quality assurance (QA) management representatives

to understand the QA Department's effo.ts taken in the past two years regarding

BECo's corrective actions for the 1995 SWSOPl self assessment.

b. - Observations and Findinas

Although there was a OA department review conducted regarding the use of

containment overpressure in calculating the NPSH available for the ECCS pumps *

(see Section_ E1.1), there did not appear to be any other substantial QA effort

regarding the corrective actions associated with the 1995 SWSOPl self assessment _

findings. A QA finding in December 1995 indicated that the action items in the

corrective action tracking system related to_the SWSOPl findings were not being

maintained, and many of the items were still(at that time) open,

c. Conclusions

Oversight by the QA Department regarding _1995 SWSOPlissues was limited and,

ultimately ineffective with respect to bringing forward the Criteria XVI findings from

this NRC inspection.

E8 Miocellaneous Engineering issues

E8.1 Review of Updated Final Safety Analvsis Report (UFSAR) Commitments

A recent discovery of a hcensee operating their facility in a manner contrary to the

FSAR oescription highlighted the need for a special focused review that compares

plant practices, procedures, and/or parameters to the UFSAR descriptions. While

performing the inspections documented in this report, the inspector reviewed the

applicable portions of the UFSAR that related to the areas inspected and verified

that it was consistent with observed plant practices, procedures, and/or parameters

except as noted in Sections E1.2, E1.3, and E1.11.

4

V. Manaaement Meeting

X1 Exit Meeting Summary

The inspector' discussed the findings with the licensee staff and management at the end of

each weekly visit, such as the substantial exit meeting of July 18,1997 A final exit

meeting was held on August 28,1997. The licensee acknowledged the findings

presented. No proprietary materials were knowingly retained by the inspectors or disclosed

in this inspection report.

e

a,

, - . - , , . - -

. , , , + + ,-

4

.

34

PARTIAL LIST OF PERSONS CONTACTED

Boston Edison Comoany

E. Boulette Senior Vice President, Nuclear

P. Harizi Mechanical Engineer

J. Alexander QA Manager

H. Oheim General Manager, Technical Section

T. White Mechanical Engineering Manager

T. Trepanier Acting Plant Manager

N. Desmond Regulatory Relations Group Manager

R. Haladyna Regulatory Affairs Engineer

P. Kahler Regulatory Affairs Engineer

M. Jacobs Operations Manager

J. Keene Regulatory Affairs Manager

B. Chenard Electrical Engineering Manager

J. Coughlin Electrical Engineer

Nuclear Reautatory CommissigD

E. Kelly DRS Systems Engineering Branch Chief

R. Laura Senior Resident inspector, Pilgrim

R. Arrighi Resident inspector, Pilgrim

INSPECTION PROCEDURES USED

IP 92903 Followup - Engineering

'

ITEMS OPENED, CLOSED, AND DISCUSSED

Ooened

Safetv Evaluation

97-05 01 eel Unreviewed safety question on NPSH issue for ECCS pumps

97-05-01 eel No safety evaluation to address operation of RBCCW above 65"F

97-05 01 eel Licensing Basis of RBCCW inconsistent with operating procedure

97-05-01 eel No safety evaluating for design change of RHR ilow

Desian Control-

97-05-02 eel Design control issue re operation above SSW design inlet temperature

97-05-02 eel Failure to have adequate basis for not isolating nonessential loads and

assuring design basis information

97-05-02 eel Design control issue f ailure to translate design basis information (EDG

loading calculations) into standby AC power system procedure and

accounting for kW meter accuracy

-- - - - - - -- - -- - - - - - - - - - - - -

. - - - - -.

e

35

97 05-02 eel Design control issue on failure to assure design basis info (appropriate

RHR flow range) was correctly translated into operating procedures

Corrective Action

97 05-03 eel Inadequate corrective action regarding single failure analysis

performed in response to GL 8913

97-05-03 eel inadequate corrective action regarding SWSOPl finding of

discrepancies between Standby AC Power System Procedure and the

diesel generator loading calculation

97-05-03 eel Inadequate corrective action regarding SWSOPl finding of

inconsistency between operating procedures and design basis info

(assumed isolation of nonessential loads)

97 05 03 eel Inadequate corrective action taken to assure that the design basis

maximum ambient temperature of 88'F for the emergency diesel

generators was controlled properly

97-05-03 eel Nuclear Engineer Procedure not revised as part of corrective action

from PR 96.9028

Reportability

97-05-04 eel Failure to report operation beyond design basis SSW design inlet

temperature

97-05-04 eel Untimely report filed re new single failure vulnerability

97-05-04 eel Failure to report possibility of being outside design basis since

procedures did not require isolation of RBCCW flow to nonessential

loads

97 05-04 eel Failure to report possibility of operation outside design basis at RHR

flows at or below 5100 gpm

97-05-04 eel Failure to report a condition outside the plant design basis regarding

an adverse drywell temperature profile

, 97-05-04 eel Diesel generator ambient temperatures resulting in components

!

potentially subjected to temperatures beyond their design

97 05-05 eel Drywell temperature averaged approximately 35*F higher than

analysis of record since 198710 CFR 50.49(e)(1)

97-05-06 URI lsolation redundancy for salt service water valves

97 05 07 IFl Complete benchmark testing of RBCCW system to validate flow

I

model

97-05-08 URI Confirm that adequate RBCCW flow provided to core spray pump

when flow is not isolated to nonessential loads

l 97-05-09 IFl Understand the final root cause analysis of the SSW system through

wall piping leaks

l 97-05 10 eel Failure to Update FSAR

l

l Closed

50-293/97-01-03 URI Unreviewed safety question on NPSH issue for ECCS pumps

50-293/95-21-02 URI Elevated SSW inlet temperature at Pilgrim