12-21-2017 | On 10/23/2017, during a walkdown of containment at the start of the Unit 3 refueling outage, a leak was identified in a socket weld for a 1-inch diameter instrument line. The line is connected to discharge piping for the 'B' recirculation pump and is part of the reactor coolant system pressure boundary. Because the leak was misting, the leakage rate could not be quantified. However, the reactor coolant system unidentified leakage prior to plant shutdown was 0.18 gpm. RCS pressure boundary leakage while in Mode 1 is a violation of Technical Specification 3.4.4 and is a reportable condition.
The cause of the event was a lack of fusion defect in the weld when it was done in the late 1980's. Normal vibration of the line since it was installed resulted in the crack initiating at the weld defect and propagating to the surface. The section of pipe and associated fitting were replaced, along with welds in similar sections of piping. There were no actual safety consequences as a result of this event. |
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Category:Letter
MONTHYEARIR 05000277/20244012024-10-17017 October 2024 Security Baseline Inspection Report 05000277/2024401 and 05000278/2024401 (Cover Letter Only) RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24284A2842024-10-10010 October 2024 (Wcgs), Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) ML24281A1012024-10-0707 October 2024 Senior Reactor and Reactor Operator Initial License Examinations ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24221A2582024-09-0606 September 2024 Response to Request for Re-Engagement Regarding the Subsequent License Renewal Environmental Review for Peach Bottom Atomic Power Station, Units 2 and 3 05000277/LER-2024-003, (Pbaps), Unit 2, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 (Pbaps), Unit 2, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum IR 05000277/20240022024-09-0404 September 2024 Reissued Integrated Inspection Report 05000277/2024002 and 05000278/2024002 IR 05000277/20240052024-08-29029 August 2024 Updated Inspection Plan for Peach Bottom Atomic Power Station, Units 2 and 3 (Report 05000277/2024005 and 05000278/2024005) IR 05000277/20240102024-08-23023 August 2024 Fire Protection Team Inspection Report 05000277/2024010 and 05000278/2024010 ML24235A0342024-08-23023 August 2024 U.S. Nuclear Regulatory Commission’S Analysis of Constellation Energy Generation’S Decommissioning Funding Status Report ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24227A5492024-08-14014 August 2024 Integrated Inspection Report 05000277/2024002 and 05000278/2024002 IR 05000482/20240052024-08-14014 August 2024 Updated Inspection Plan for Wolf Creek Generating Station (Report 05000482/2024005) ML24225A1692024-08-12012 August 2024 10 CFR 50.46 Annual Report ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24214A3232024-08-0101 August 2024 Response to Request for Additional Information - Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24206A1252024-07-24024 July 2024 Revision of Three Procedures and Two Forms That Implement the Radiological Emergency Response Plan (RERP) ML24191A0612024-07-0606 July 2024 Independent Spent Fuel Storage Installation (ISFSI) - Annual Radioactive Effluent Release Report ML24178A3672024-06-26026 June 2024 Correction to 2023 Annual Radioactive Effluent Release Report – Report 47 ML24178A4142024-06-26026 June 2024 Revision of One Procedure and One Form That Implement the Radiological Emergency Response Plan (RERP) ML24177A1512024-06-24024 June 2024 Post Accident Monitoring Instrumentation Report ML24166A1172024-06-20020 June 2024 Regulatory Audit Summary Regarding Proposed Alternative Schedule to Complete Decommissioning Beyond 60 Years RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations IR 05000277/20243012024-06-13013 June 2024 Initial Operator Licensing Examination Report 05000277/2024301 and 05000278/2024301 RS-24-058, Regarding Subsequent License Renewal Environmental Review2024-06-0505 June 2024 Regarding Subsequent License Renewal Environmental Review ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24150A2722024-05-29029 May 2024 Annual Radiological Environmental Operating Report 81, January 1, 2023 Through December 31, 2023 ML24150A0032024-05-28028 May 2024 Request for Exemptions from 10 CFR 50.82(a)(8)(i)(A) and 10 CFR 50.75(h)(1)(iv) and Proposed Amendment to the Decommissioning Trust Agreement ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000277/20240012024-05-13013 May 2024 Integrated Inspection Report 05000277/2024001 and 05000278/2024001 ML24134A1792024-05-13013 May 2024 Supplemental Information in Support of Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations IR 05000277/20245012024-05-0808 May 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000277/2024501 and 05000278/2024501 RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24121A1832024-04-30030 April 2024 Pre-Submittal Meeting Presentation Material Peach Bottom ECCS Compensated Level System Replacement Project ML24118A0032024-04-27027 April 2024 2023 Annual Radioactive Effluent Release Report - Report 47 ML24120A2762024-04-23023 April 2024 Independent Spent Fuel Storage Installation (ISFSI) Facility - Annual Radioactive Effluent Release Report 66 January 1, 2023 Through December 31, 2023 CNL-24-033, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-04-17017 April 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24107A2462024-04-15015 April 2024 Submittal of Changes to Technical Specifications Bases ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24102A0472024-04-11011 April 2024 Operator Licensing Examination Approval ML24099A0012024-04-0808 April 2024 (PBAPS) Units 2 and 3, Uncoordinated DC Circuits Cause Unanalyzed Condition RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report RS-24-023, Report on Status of Decommissioning Funding.2024-03-22022 March 2024 Report on Status of Decommissioning Funding. 05000277/LER-2024-001, Submittal of LER 2024-001-00 for Peach Bottom Atomic Power Station (PBAPS) Unit 2, Automatic Reactor Scram Due to an Invalid Generator Lockout2024-03-21021 March 2024 Submittal of LER 2024-001-00 for Peach Bottom Atomic Power Station (PBAPS) Unit 2, Automatic Reactor Scram Due to an Invalid Generator Lockout IR 05000277/20244022024-03-12012 March 2024 Cybersecurity Inspection Report 05000277/2024402 and 05000278/2024402 (Cover Letter Only) 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000277/LER-2024-003, (Pbaps), Unit 2, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 (Pbaps), Unit 2, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum ML24099A0012024-04-0808 April 2024 (PBAPS) Units 2 and 3, Uncoordinated DC Circuits Cause Unanalyzed Condition ML24081A1212024-03-21021 March 2024 Automatic Reactor Scram Due to an Invalid Generator Lockout ML21196A4852021-07-16016 July 2021 LER 2-2021-002-00 for Peach Bottom Atomic Power Station, Unit 2, Safety Relief Valve Inoperability Due to Nitrogen Leakage from Braided Hose Wear 05000278/LER-2017-0012017-12-20020 December 2017 Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line, LER 17-001-00 for Peach Bottom Atomic Power Station (PBAPS), Unit 3 Regarding Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line 05000277/LER-2017-0012017-03-0808 March 2017 Emergency Diesel Generator Exhaust Stacks Nonconforming Design for Tornado Missile Protection, LER 17-001-00 for Peach Bottom Atomic Power Station (PBAPS), Unit 2 Regarding Emergency Diesel Generator Exhaust Stacks Nonconforming Design for Tornado Missile Protection 05000278/LER-2016-0012016-11-22022 November 2016 Leak in High Pressure Coolant Injection Drain Pipe Results in a Loss of Safety Function, LER 16-001-00 for Peach Bottom, Unit 3, Regarding Leak in High Pressure Coolant Injection Drain Pipe Results in a Loss of Safety Function 05000277/LER-2016-0012016-11-11011 November 2016 Leak in High Pressure Service Water Pipe Results in Condition Prohibited by Technical Specifications, LER 16-001-00 for Peach Bottom, Unit 2, Regarding Leak in High Pressure Service Water Pipe Results in Condition Prohibited by Technical Specifications 05000278/LER-2015-0012016-02-26026 February 2016 Loss of High Pressure Coolant Injection System Function as a Result of Failed Flow Controller Signal Converter, LER 15-001-00 for Peach Bottom, Unit 3, Regarding Loss of High Pressure Coolant Injection System Function as a Result of Failed Flow Controller Signal Converter ML13058A0432013-02-22022 February 2013 Submittal of Independent Spent Fuel Storage Installation (ISFSI) Cask Event Report ML1007702362010-03-12012 March 2010 60-Day Security Event Report 2-10-S01 ML0927401622009-09-30030 September 2009 LER 09-S01-00 for Peach Bottom, Units 2 & 3 Regarding Unescorted Access Granted to Contract Worker Who Did Not Provide Complete Work History Information ML1015505682009-07-10010 July 2009 Event Notification for Peach Bottom on Elevated Tritium Levels Found in On-Site Well ML0434503772004-12-10010 December 2004 LER-04-S01-00 for Peach Bottom Atomic Power Station (PBAPS) Unit 2 and Unit 3, 60 Day Security Event Report 2-04-S01 ML19095A7391976-12-0505 December 1976 Reporting Abnormal Occurrence No. 50-278-74-33 at Peach Bottom Atomic Power Station for Failure of Main Steam Line High Flow Switch dPIS-3-2-116C to Trip During Surveillance Test 2024-09-05
[Table view] |
comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2017 - 00 001 Unit Conditions Prior to Discovery of the Event Unit 3 was in Mode 3, Hot Shutdown, when the condition was discovered on 10/23/2017 at approximately 4:00 am. The unit entered Mode 3 at 1:08 am in preparation for the planned refueling outage. There were no structures, systems, or components out of service that contributed to this event.
Description of the Event
On 10/23/2017, with the Unit in Mode 3, at the beginning of a refueling outage, personnel entered the drywell to perform an inspection. At approximately 4:00 am, leakage was identified on a one-inch diameter instrument line socket (EIIS:PSF) weld. The instrument line is for a pressure transmitter from the 'B' Recirculation Pump (EIIS:AD) discharge. Because the leak was misting, the leakage rate could not be quantified. However, the reactor coolant system unidentified leakage prior to plant shutdown was 0.18 gpm.
This line is part of the ASME Class 1 primary coolant pressure boundary. Technical Specification (TS) 3.4.4 does not allow any pressure boundary leakage in Modes 1, 2 or 3. As a result, TS 3.4.4 Condition C was entered, which requires the plant to be in Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Mode 4 in 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. The plant was in Mode 3 at the time of discovery and entered Mode 4, Cold Shutdown, at 12:54 pm on 10/23/2017 (approximately 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> after time of discovery).
Prompt notification to the NRC was made in accordance with 10 CFR 50.72(b)(3)(ii)(A) on 10/23/2017 at 9:35 am (Event Notification #53031).
Analysis of the Event
The leak was determined to be from a crack in the weld connecting the pipe to a tee fitting. The crack extended approximately 60 degrees around the circumference of the weld. Although it could not be determined when the crack developed, it is assumed it existed while operating in Mode 1, prior to shutdown. During such time, the leakage would have been contributing to the total unidentified leakage of 0.18 gpm. This is well below the 5 gpm limit for unidentified leakage as stated in TS 3.4.4.
This event is being reported in accordance with the following:
1. 10 CFR 50.73(a)(2)(i)(B) — Conditions Prohibited by Technical Specifications - TS Limiting Condition for Operation (LCO) 3.4.4 requires there to be no RCS pressure boundary leakage while in Modes 1, 2 and 3. If leakage exists, TS 3.4.4 Condition C requires the unit to be in Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Mode 4 in 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Since the leak existed while in Mode 1 for greater than 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />, a condition prohibited by TS existed.
comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Infocollects.Flesource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (31500104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2017 - 00 001 2. 10 CFR 50.73(a)(2)(ii)(A) — Degradation of the RCS — Because of the RCS pressure boundary leakage, one of the principal safety barriers of the plant was degraded.
Cause of the Event
The section of the one-inch pipe containing the cracked socket weld was sent to an offsite laboratory for analysis. The pipe was sectioned and lack of fusion defects were identified at the root of the weld. The crack initiated at the location of these defects. The defects would have occurred when the weld was performed during a recirculation system pipe replacement in the late 1980's. It is unknown when the crack began, but normal vibration for the piping likely caused it to propagate to the surface of the weld, resulting in the identified leak.
Corrective Actions
The section of pipe and the associated fitting were replaced. Instrument lines connected to the suction and discharge lines for both of the recirculation pumps with similar configuration and subject to vibration were also replaced during the refueling outage. The new welds were performed with a 2:1 profile, which reduces their susceptibility to vibration-induced failures.
Previous Similar Occurrences A similar event occurred in September of 2005. A crack in a socket weld caused by a lack of fusion defect resulted in a 1 gpm leak in a one-inch equalizing line for a check valve on the 'A' Residual Heat Removal (RHR) injection line. The event is documented in LER 2005-003, dated 10/28/2005. Additional information on this previous occurrence is contained in the corrective action program.