RA22-060, Regulatory Commitment Change Summary Report

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Regulatory Commitment Change Summary Report
ML22334A060
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 11/30/2022
From: Van-Fleet J
Constellation Energy Generation
To:
Office of Nuclear Reactor Regulation, Document Control Desk
References
RA22-060
Download: ML22334A060 (1)


Text

LaSalle County Station Constellation 2601 North 21 " Road Marseilles, IL 61341 815-415-2000 Telephone RA22-060 10 CFR 50.4 November 30, 2022 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555-0001 LaSalle County Station, Units 1 and 2 Renewed Facility Operating License Nos. NPF-11 and NPF-18 NRC Docket Nos. 50-373 and 50-374

Subject:

2021 Regulatory Commitment Change Summary Report The purpose of this report is to provide the Constellation Energy Generation, LLC (CEG), "2021 Regulatory Commitment Change Summary Report," for LaSalle County Station commitment changes processed during the period of January 1, 2021 through December 31, 2021. Based on a review of commitment tracking documentation, it was determined that commitment changes were processed and implemented during the calendar year 2021 in accordance with Nuclear Energy lnstitute's (NEI) 99-04, "Guidelines for Managing NRC Commitment Changes,"

Revision 0, dated July 1999.

The enclosed commitment changes were found to meet the criteria for inclusion in the annual Commitment Change Summary Report. There are no new regulatory commitments established by this correspondence.

Should you have any questions concerning this letter, please contact Mr. Daniel Mearhoff, Regulatory Assurance Manager, at (815) 415-2800.

Respectfully, Jo~l~efkr Plant Manager LaSalle County Station

Enclosure:

2021 Regulatory Commitment Change Summary Report cc: Regional Administrator - NRC Region Ill NRC Senior Resident Inspector - LaSalle County Station

RA22-060 2021 Regulatory Commitment Change Summary Report Commitment Date of Original Document Original Commitment Changed Commitment Basis for Change Change Commitment Trackina No. Chanae 21-001 03/19/2021 Letter from W. J. Category B MOV to be Repair of valve 2G33-F001, Deferring the repair Trafton (Exelon repaired at the LaSalle Reactor Water Cleanup of the 2G33-F001 Generation Generating Station, Unit 2 Inboard Isolation Valve, will valve will allow Company, LLC) to be performed in refueling additional controls to U.S. NRC, Valve Outage (Year) outage L2R19 scheduled for reduce risk including "Commitments for 2G33-F001 L2R17 (2019) Spring 2023. Water Inventory Resolution of Control (WIC)

Anchor Darling Category B MOV to be impacts. The Double Disc Gate repaired at the LaSalle deferral is supported Valve Part 21 Generating Station, Unit 2 by engineering Issues," dated June evaluation and 2,2017 Valve Outage (Year) results of diagnostic 2G33-F001 L2R19 (2023) testing.

Letter from James Barstow (Exelon Generation Company, LLC) to U.S. NRC, "Commitments for Resolution of Anchor Darling Double Disc Gate Valve Part 21 Issues," dated December 19, 2017