ML031400561

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April 2003 Monthly Operating Report for Peach Bottom Units 2 & 3
ML031400561
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 05/02/2003
From: Stathes G
Exelon Nuclear
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
RG-10.001
Download: ML031400561 (13)


Text

ExelonSM Exelon Nuclear Peach Bottom Atomic Power Station Telephone 717.456.7014 www.exeloncorp.com Nuclear 1848 Lay Road Delta, PA 17314-9032 May 2, 2003 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Docket Nos. 50-277 and 50-278 Gentlemen:

Enclosed is the monthly operating report for Peach Bottom Units 2 and 3 for the month of April 2003 forwarded pursuant to Technical Specification 5.6.4 under the guidance of Regulatory Guide 10.1, Revision 4.

Sincerely, Director, Site Engineering Peach Bottom Atomic Power Station GLS/Pl3lVCSL:cmg Enclosures cc:

H. J. Miller, Administrator, Region I, USNRC A.C. McMurtray, USNRC, Senior Resident Inspector, PBAPS cen 03-14039 11---

Peach Bottom Atomic Power Station Unit 2 April 1 through April 30, 2003 Narrative Summary of Operating Experiences Unit 2 began the month of April at 100% power.

At 1847, on April 12k', Unit 2 automatically scrammed on high reactor pressure, due to an air line break on an outboard MSIV. This caused the MSIV to fail closed. Following repairs, the Unit was declared critical at 2259 on April 13 'h, and the turbine-generator was synchronized with the grid at 1150 on April 14th. The unit reached 3458 MWth (max rated without Caldon LEFM operable) at 0603 on April 15th. Following investigation and resolution of minor LEFM system anomalies, Unit 2 reached 3505 MWth (max rated with LEFM operable) by 2300 on April 16h.

At 2300 on April 3&, Unit 2 began a load drop to at first 60% power, and finally 30% power for power suppression testing, to identify a leaking fuel assembly. By 0000 on May 1I, the Unit had reduced power to approximately 80% rated. The Unit will return to 100% power in May, following completion of power suppression activities.

Unit 2 ended the month of April at 80% power.

Peach Bottom Atomic Power Station Unit 3 April 1 through April 30, 2003 Narrative Summary of Operating Experiences Unit 3 began the month of April at 100% power.

At 0920 on April 3 rd, Unit 3 reduced power by 5 MWe, for the planned installation of new Final Feedwater Temperature measurement software (AFTO). The Unit returned to 100% power by 1819 on April 3 rd At 2323 on April 16'h, Unit 3 reduced power to 88%, for HCU maintenance activities. The Unit returned to 100% power by 0230 on April 176'.

At 2320 on April 17th, Unit 3 reduced power to 87%, for follow-up scram timing of rods following maintenance on April 16h - 17'h. The Unit returned to 100% power by 0300 on April 18th.

Unit 3 ended the month of April at 100% power.

Attachment to Monthly Operating Report for April 2003 Page 1 UNIT 2 REFUELING INFORMATION

1. Name of facility:

Peach Bottom Unit 2

2. Scheduled date for next refueling shutdown:

Reload 15 is scheduled for September 22, 2004.

3. Scheduled date for restart following refueling:

Restart following refueling forecast for October 7, 2004.

4. Will refueling or resumption of operation there after require a technical specification change or other license amendment?

Yes If answer is yes, what, in general, will these be?

a. Potential Cycle 16 Safety Limit MCPR Change.
5. Scheduled date(s) for submitting proposed licensing action and supporting information:

Nothing to report for this period.

6. Important licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:

Nothing to report this period.

Docket No. 50-277 Attachment to Monthly Operating Report for April 2003 Page 2 UNIT 2 REFUELING INFORMATION (Continued)

7. The number of fuel assemblies (a) in the core, (b) in the spent fuel storage pool and (c) dry storage.

(a) ore - 764 Fuel Assemblies (b) Fuel Pool - 2908 Fuel Assemblies, 58 Fuel Rods (c) Interim Spent Fuel Storage Installation - 680 fuel assemblies

8. The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:

The spent fuel pool storage capacity has been relicensed for 3819 fuel assemblies.

9. The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present capacity:

Based on projected dry cask storage schedules and reload batch sizes, a full core discharge will remain available throughout plant life.

Docket No. 50-278 Attachment to Monthly Operating Report for April 2003 Page 1 UNIT 3 REFUELING INFORMATION

1. Name of facility:

Peach Bottom Unit 3

2. Scheduled date for next refueling shutdown:

Reload 14 is scheduled for September 21, 2003.

3. Scheduled date for restart following refueling Restart following refueling forecast for October 9, 2003.
4. Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?

Yes If answer is yes, what, in general, will these be?

a.) Potential Cycle 15 Safety Limit MCPR Change.

5. Scheduled date(s) for submitting proposed licensing action and supporting information.

a.) Submittal anticipated July 2003.

6. Important licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:

(a) The 3R14 reload will consist of approximately 288 GE-14 bundles. This will be the second reload of GE-14 fuel.

7. The number of fuel assemblies (a) in the core, (b) in the spent fuel storage pool and (c) dry storage.

(a) Core - 764 Fuel Assemblies (b) Fuel Pool - 2929 Fuel Assemblies, 6 Fuel Rods (c) Interim Spent Fuel Storage Installation - 408 fuel assemblies

8. The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:

The spent fuel pool storage capacity has been relicensed for 3819 fuel assemblies.

Attachment to Monthly Operating Report for April 2003 Page 2 UNIT 3 REFUELING INFORMATION (Continued)

9. The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present capacity:

Based on projected dry cask storage schedules and reload batch sizes, a full core discharge will remain available throughout plant life.

OPERATING DATA REPORT DOCKET NO. 50 - 277 DATE MAY 6, 2003 COMPLETED BY EXELON C. S. LEWIS PLANT ENGINEERING ENGINEERING DIVISION PEACH BOTTOM ATOMIC POWER STATION TELEPHONE (717) 456-3245 OPERATING STATUS

1. UNIT NAME: - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - PEACH BOTTOM UNIT 2
2. REPORTING PERIOD: - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - APRIL, 2003
3. DESIGN ELECTRICAL RATING (NET MWE): - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - _ 1143
4. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 1182
5. MAXIMUM DEPENDABLE CAPACITY (NET MWE): 1116 THIS MONTH YR-TO-DATE CUMULATIVE
6. NUMBER OF HOURS REACTOR WAS CRITICAL 690.8 2,850.8 184,116.3
7. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
8. HOURS GENERATOR ON-LINE 679.0 2,839.0 179,718.9
9. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
10. NET ELECTRICAL ENERGY GENERATED (MWH) 764,603 3,182,127 177,067,893

OPERATING DATA REPORT (CONTINUED)

DOCKET NO. 50- 277 DATE MAY 6, 2003 THIS MONTH YR-TO-DATE CUMULATIVE

11. UNIT SERVICE FACTOR 94.4 % 98.6 % 71.1 %
12. UNIT AVAILABILITY FACTOR 94.4 % 98.6 % 71.1 %
13. UNIT CAPACITY FACTOR (USING MDC NET) 95.3 % 99.0 % 65.0 %
14. UNIT CAPACITY FACTOR (USING DER NET) 93.0 % 96.7 % 63.9 %
15. UNIT FORCED OUTAGE RATE 5.6 % 1.4% 9.6 %
16. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE AND DURATION OF EACH):

(717) 456-4248

17. IF SHUTDOWN AT THE END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: (717) 456-4248
18. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATIONS): FORECAST ACHIEVED INITIAL CRITICALITY 09116/73 INITIAL ELECTRICITY 02/18/74 COMMERCIAL OPERATION 07/05/74 PAGE 2 OF 2

UNIT SHUTDOWNS DOCKET NO. 50 - 277 UNIT NAME PEACH BOTTOM UNIT 2 DATE MAY 6, 2003 COMPLETED BY EXELON C. S. LEWIS PLANT ENGINEERING ENGINEERING DIVISION PEACH BOTTOM ATOMIC POWER STATION REPORT MONTH APRIL, 2003 TELEPHONE (717) 456-3245 METHOD OF CAUSE AND CORRECTIVE TYPE DURATION REASON SHUTTING DOWN ACTION TO NO. DATE (1) (HOURS) (2) REACTOR (3) PREVENT RECURRENCE 1 030412 F 40.0 A 3 REACTOR POWER WAS REDUCED TO 0% DUE TO THE FAILURE OF THE D' OUTBOARD MSIV INSTRUMENT AIR LINE.

TOTAL HOURS 40.0 (1) (2) (3)

F-FORCED REASON METHOD S - SCHEDULED A- EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL B - MAINTENANCE OR TEST 2 - MANUAL SCRAM C - REFUELING 3 - AUTOMATIC SCRAM D - REGULATORY RESTRICTION 4 - OTHER (EXPLAIN)

E - OPERATOR TRAINING +LICENSE EXAMINATION F - ADMINISTRATIVE G - OPERATIONAL ERROR (EXPLAIN)

H - OTHER (EXPLAIN)

OPERATING DATA REPORT DOCKET NO. 50 - 278 DATE MAY 6, 2003 COMPLETED BY EXELON C. S. LEWIS PLANT ENGINEERING ENGINEERING DIVISION PEACH BOTTOM ATOMIC POWER STATION TELEPHONE (717) 456-3245 OPERATING STATUS

1. UNIT NAME: _ _ _ - - - - - - - - - - - - - - - - - - - - - _PEACH BOTTOM UNIT 3
2. REPORTING PERIOD: - _- _- - - - - - - - - - - -_ - - __ APRIL_2003
3. DESIGN ELECTRICAL RATING (NET MWE): - - - - - _- - - - - - - - - - - - - - - - - - - _- - - - - - - - - - - _ 1119
4. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - _ 1159
5. MAXIMUM DEPENDABLE CAPACITY (NET MWE): - - - - - - - - - - - - - - - - - - - - - - _ - - - - - - - - - - - - - - - _1093 THIS MONTH YR-TO-DATE CUMULATIVE
6. NUMBER OF HOURS REACTOR WAS CRITICAL 719.0 2,879.0 183,018.5
7. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
8. HOURS GENERATOR ON-LINE 719.0 2,879.0 179,112.8
9. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
10. NET ELECTRICAL ENERGY GENERATED (MWH) 803,953 3,218,038 175,334,003

OPERATING DATA REPORT (CONTINUED)

DOCKET NO. 50 - 278 DATE MAY 6, 2003 THIS MONTH YR-TO-DATE CUMULATIVE

11. UNIT SERVICE FACTOR 100.0 % 100.0 % 72.1 %
12. UNIT AVAILABILITY FACTOR 100.0 % 100.0 % 72.1 %
13. UNIT CAPACITY FACTOR (USING MDC NET) 102.3 % 102.3 % 66.8 %
14. UNIT CAPACITY FACTOR (USING DER NET) 99.9 % 99.9 % 65.0 %
15. UNIT FORCED OUTAGE RATE .0 % .0% 8.2 %
16. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE AND DURATION OF EACH):

(717) 456-4248

17. IF SHUTDOWN AT THE END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: (717) 456-4248
18. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATIONS): FORECAST ACHIEVED INITIAL CRITICALITY 08/07/74 INITIAL ELECTRICITY 09/01/74 COMMERCIAL OPERATION 12/23/74 PAGE 2 OF 2

UNIT SHUTDOWNS DOCKET NO. 50 - 278 UNIT NAME PEACH BOTTOM UNIT 3 DATE MAY 6, 2003 COMPLETED BY EXELON C. S. LEWIS PLANT ENGINEERING ENGINEERING DIVISION PEACH BOTTOM ATOMIC POWER STATION REPORT MONTH APRIL, 2003 TELEPHONE (717) 456-3245 METHOD OF CAUSE AND CORRECTIVE TYPE DURATION REASON SHUTTING DOWN ACTION TO NO. DATE (1) (HOURS) (2) REACTOR (3) PREVENT RECURRENCE TOTAL HOURS (1) (2) (3)

F-FORCED REASON. METHOD S - SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL B - MAINTENANCE OR TEST 2 - MANUAL SCRAM C - REFUELING 3 -AUTOMATIC SCRAM D - REGULATORY RESTRICTION 4 - OTHER (EXPLAIN)

E - OPERATOR TRAINING + LICENSE EXAMINATION F - ADMINISTRATIVE G - OPERATIONAL ERROR (EXPLAIN)

H - OTHER (EXPLAIN)