ML20039C507

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LER 81-037/03L-0:on 811119,while Performing Diesel Generator Operability Surveillance,Diesel Generator Exhibited High Coolant Water Temp.Caused by Defective Discharge Check Valve on Diesel Generator Cooling Water Pump
ML20039C507
Person / Time
Site: Dresden Constellation icon.png
Issue date: 12/18/1981
From: Maxwell D
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20039C496 List:
References
LER-81-037-03L-02, LER-81-37-3L-2, NUDOCS 8112290416
Download: ML20039C507 (3)


Text

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LICENSEE EVENT REPORT CONTKOL BLOCK: l i

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(PLEASE PRINT CR TYPE ALL REQUIT.EO INFOXMATIONI M l Il8 9Ll DlLICENSEE 7

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7 8 61 EVENT OATE 74 OATE EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h I o l 2 J lDuring normal unit operation, while performing Unit 3 D/G operability surveillance, the l 4

go93l lD/G exhibited high coolant water temperature and was manually shutdown (T.S. 3.9.4.2). l lo ;4 l lThere was no effect on the health and safety of the public or plant personnel sinCe l g l Unit 2/3 D/G and all required ECCS's were operable. Previous occurrence: R0 81-33/01T, I l 0 l6 l l Docket 50- 249. _ g 10171 l l I o is I l I 80

  • IoI:'E CciE $08$OE COMPONENT CODE SL8 D'E S 3E gg lE lE l@ W@ lB l@ l V l A l L lV l E lX lh lC l@ W h 7 8 9 10 11 12 13 18 is 20

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44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l i l o j lCause of this event was a defective discharge check valve on the D/G cooline water mi-n. I ii ;i j l Valves on all three D/G cooling water niinps were insoected and replaced. Procedure I I i 12 I Irevision will be initiated to insure annual inspection of the check valves. I liial I l 11 141 l l 7 8 i 80 STAN  % POWER OTHER STATUS Qi Q RY OlSCOVERY DESCRIPTION li is I bj@ l 0 l 6 l 0 l@l N/A I La.J@l n,er, eor n - ,,4 -, 1 7 8 1 12 13 44 45 46 80 8tELEASED OFRELEASE AMOUNT OF ACTIVITY LoCAftoN OF RELEASE li is'I 'bj @ [2j@l N/A N/A l

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(T[T] lZ lhl N/A l 7 8 9 to PUBLICITY NRC USE ONLY ISSUED DESCRIPTION

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ATTACH W.I TO LICENSEE EVENT REPORT 81-037/03L-0 COM!!ONWEALTH EDISON COMPANY (CWE)

_L_RESDEN UNIT 3 (ILDRS 3)

DOCKET # 050-249 During normal' operation of Dresden Unit 3, while the Unit 3 Diesel Generator (D/G) was being run in preparation to taking the shared Unit 2/3 D/G out of service, the Unit 3 D/G was manually shutdown because of E. high coolant temperature condition that had developed (T.S. 3.9.A.2). There was no effect on public health or safety since the Unit 2/3 D/G and all required emergency core cooling systems were operable. Previous occurrence: R.O. 81-33/01T-0, Docket 050-249. ,,

The cause of this event was a defective check valve on the discharge side of the Unit 3 D/G cooling water pump. The valve was replaced and tested several times to prove its operability. The Unit 3 D/G and its cooling water system were declared operable. The discharge check valves for the Unit 2 and 2/3 D/G cooling water pumps were inspected and it was determined that ~

they also needed replacement since they were essentially in the same condition as the Unit 3 D/G cooling water pump check valve. The check valves were replaced, the systems satisfactorily tested, and placed back in service. A .

procedure revision will be initiated to inspect these valves annually to insure their operability.

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DEVIATION REPORT

  • DV R NO.

Commonwealth Ed.ison -

STA UNIT YEAR NO.

o 3 77 PART 11 TI TLE OF DEVI ATION OCCU RRED 11-19-81 0452 Unit 3 Diesel Generator Tnoparable cATE TIME SYSTEM AFFECTED 6600 PLANT CONDITIONS TESiiNG Diesel Generator Run p g 1509 g,g 464 YES NO DESCRiPitCN OF EVENT Unit 3 Diesel Generator (D/G.) was being run in preparation for taking 2/3 D/G out of service.

At 0452. Unit 3 D/G was .anually shutdown due to high temperature. /

4 .

DESCRIPTION OF GAUSE Lack of cooling water to D/G heat exchanger.

Tf7HCR APPLICABLE INFORMATION D/G cooline water cumn ran. but susoect it did not on-n suf#fcient varer to the. heat exchancer-EQUIPMENT YE5 DR N O. WR NO.

WM PM 1149-81 FAILURE O NO N/A D 17052 RESPONSISLE SUFF4 VISOR OA T E PART 2 l OPERATING ENGINEERS COMMENTS All required surveillances for the Unit 3 D/G were satisfactorily completed. The D/G cooline water pumo investicatine committee is actively reviewing the cause of the event. A -

chn4 n# the cooline water rumo suction line valvine disclosed no abnormalities. The 2/3 (over)

SAFETY-TYPE OF CEVI ATION EVENT OF POTENTI AL TECH SPEC NON-REPORTABLE ANNUAL RELATED REPORTABLE OCCURRENCE PUBLIC INTEREST VIOLATION OCCURRENCE REPGRTI NG WR ISSUED 14 DAY IOCFR21 YES YES y 30 DAY gCT6.l .glON NO NO

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l REPORTABLE CCCURRENCE ACTION ITEM NO. PROMPT ON-SI TE NOTIFICATION NUMBER R. M. Ragan 11-19-91 0600 I

m 81 - 37/03L-0 TITLE DATE TlME TITLE CATE TIME 24-HOUR NRC NOTIFICATION PROMPT OFF-SITE NOTIFICATION X TPH Tom Ton?ue 11-19-81 0730 F. Palmer 11-19-81 1059 REGION lli DATE TIME TI TLE DATE TIME TGM l REGION III & COL CATE TIME TITLE DATE TIME RESPONSI BLE COMP ANY O FFI CER INFOPMED OF 10CFR 21 CON 0 f TT ONS AND THEfR DEPO RT TO NPC + TITLE DATE T I M e.

REVI EW AND COMPLETED Michael Wricht 11-19-81 OPER ATING ENGa NetH OArg C A. BY STATION REVIEW ,J g g% --

DATE # N/ # 9 M -

RESOLUTION APPROVED AND / '

AUTHORIZED FOR DISTRIBUTlCN $7A N SUPERINTENOENT DATE es ss7e t o- 77 t_osu es sa-H_

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