ML20041E681

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LER 82-012/03L-0:on 820204,drywell & Torus Purge Sys Valve 3-1601-21 Found to Leak.Caused by Failure of Resilient Seating Matl to Maintain Proper Seal to Valve Butterfly Disc.Valve Will Be Replaced
ML20041E681
Person / Time
Site: Dresden Constellation icon.png
Issue date: 03/03/1982
From: Whalen R
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20041E677 List:
References
LER-82-012-03L, LER-82-12-3L, NUDOCS 8203110239
Download: ML20041E681 (2)


Text

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l.lCENSEE EVENT REPORT CONTROL BLOCK: l l l l 1 l 6

(PLgAsa PMINT OR TYPE ALL REQUIRED INFORMATION)

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l 7 4 7 UCENSEE Co0E 14 15 UCENSENVMSER 28 TYPE 40 i CCN'T loI1I

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60 4 DocxET NUMS E R 68 69 EVENT DATg to 75 REPoRTQATE 80 EVENT CESCRIPTION AND PROBA8LE CONSEQUENCES h l o l 2 I l During a refueling outage, local leak rate testing of primary containment isolation [

g ; valves was being performed in accordance with procedure DTS 1600-1. Drywell and torus  ;

,, ,, , purge system valve 3-1601-21 was found to leak at a rate of 4585.8 SCFH in violation of g

, the T.S. 4.7.1 limit of 28.38 SCFH. No danger to the public health and safety since pri g mary containment integrity was maintained by the 3-1601-22 and 3-1601-56 v'alves. Last previous occurrence on this system reported by R.O. 82-04 on Docket 50-249.

Io#aII I 7 ee s0 ceSE To"c'! suNSE COMPONENT CoOE $1,8 o'O'E $U E loisi 7 8 l s In l@ L;j@ La j@ I v l a I t lv !v Iv l@ U@ Laj @

9 10 11 12 13 18 19 10

,,, SECUENTIAL OCCURRENCE REPORT AEVISloN LER/Ro EV ENT YEAR REPORT No. Coot TYPE No.

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42 43 44 CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS I i t o l l The leakage was caused by failure of the resilient seating material to maintain a proper l l seal to the valve butterfly disc when in the closed position. The valve will be replaced l

,and the test rerun prior to reactor startup; any leakage in excess of the Tech. Specs. ,

, g will be reported at that time. This type of occurrence is under engineering review. l IiI4l l I 7 g g 80 A  % POWER oTHER STATUS oEY DISCOVERY CESCRIPT1oM

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7 ag l0l0l0l@l ig 22 11 N/A l 44 lde3 l@las Local Leak Rate Testine so l

r:ELEAsEo PRELEAsE LoCAT1oM op RELEASE @

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  1. ERSoNNEL EXPOSURES NUM6ER TYPE DESCRIPT1oM l 1 l 71 l 0 l 0 l 0 l@]@l N/A l
  • EmsoNNEL INJV IES N

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8203110239 820302 ** " ' "

  • PDR ADOCK 05000249 .obert Whalen pyoug: DON FE 2 j,

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k DEVIATION REPORT Ur g Commonwealth E:" son DvR NO. 12 - 3 -

82 - 16 x ,/ STA UNIT YEAR NO.

PART Il TI TLE OF DEVI ATION CCCuRRE Failure of Drywell and Torus Purge System Valve 3-1601-21 to Pass LLRT 2-4-82 1800 I 3y , , .y

, PLANT STATUS AT TIME OF EVENT TESTfNG SYSTEM AFFECTED 1600 Containment MODE Rafnel . PnR(M4T) 0 . LOAD (M*E) 0 y ,

otsCRIPTIGN OF EVENT While performing DTS 1601-1, Local Leak Rate Testing of Primary Ieolation Valves, the N2 Inerting and Containment System failed to pass the local leak rate test.

It was determined that the butterfly valve A0 3-1601-21 was leaking at a rate of 4585.8 SCFH, exceeding the Tech. Spec. 4.7.1 limit of 29.38 SCFH.

l 10 CFR50.72 NRC RED PHONE O 5 NOTIF eC ATION MADE ,,

YES NO EQU4PMENT FAILURE D18579 -

OVES O NO =0Rx REOUESr No. Resp 0NSistF supervisor Ed Rowley cart 2-5-82 P ART 2 l 0PERATING ENGINEER'S C0hNENTS Local leak rate testing determined that the leakage is through the A0 3-1601-21 valve, meaning that no through leakage had occurred. The valve will be repaired and the volume retested prior to startup from the refueling outage.

O EVENT OF PUBLIC INTEREST 24-HOUR NRC NOTI F I CATI ON REQ'O TECH. SPEC. VIOLATION TELEPH Tom Tongue (courtesv) 2-5-82 1330 REGION 11i OATE TIME O NON REPORTABLE OCCURRENCE TELE GA/ TEL ECOPY I4 DAY REPO RTA BLE/ T. S. REGION 111 DATE TIME O 30 oAY RE*0R TA BL E/ T. S.6. 6. B . 2. d CECG CORPORATE NOTIFICATION MADE ANNUAL /$PECL REPORT REQ'D IF ABOVE NOTIFICATION IS PER 10CFR21 A.I.R. . 12-82-13 5 D AY WRI TTEN REPORT REQ'D PER 10CFR21 t.g R, , 82-12/03L-0 TELEPH

. . a er MM UM CECO CORPORATE OFFICER DATE TIME PRELIMINARY REPORT COMPLETED AND REVIE4ED Michael Wright 2-5-82 GPERATING ENGINEER _a i DAFE./!

INb ESTI GATED REPORT & RESOLUTICN  ! '

ACCEPTED BY STATION REVIEW A. =_- - ff ()hV /y N )/

// f.f 313 \ r2-. L3-iTW ,

RESOLUTION APPROVED AND AUTHOR I ZED FOR DI STR I BUTION jK g% h 3 M p

86 5176 4FORU 15-52 1) 10 31