ML18139B213

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Updated LER 80-010/01X-1:on 800131,overstress on 18-inch Line CC-9-121,unit 2 Supply to RHR Exchanger,Found During Pipe Stress Reanalysis on Show Cause Lines.Caused by Supports Installed to Prevent Overstress During DBE
ML18139B213
Person / Time
Site: Surry Dominion icon.png
Issue date: 03/27/1981
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139B212 List:
References
LER-80-010-01X-01, LER-80-10-1X-1, NUDOCS 8104020621
Download: ML18139B213 (2)


Text

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l Ii' _..._-:.6 \.!./ (PL.EASE PRiNT OF! TYPE AL.L REOUIREO INFORMATION! [IE] I V l A I S I P I S I 1 IQ)l O I Ol - I 0 l 01 01 01 01 -I Ol O l(Dl 4 11 11 1111101 ' I© 7 S 9 ~ICENSES COOE 14 is LICENSE NUMBER . 2S . 2S LICENSE TYPE JO 57 CAT 58 CON~ 1o i 1 6: ~;~~~~  !!!.J© I o I s l o I o I oI 60 61 OOCKET NUMBER 21 s I o 66 101 o I 1 I 3 69 11 EVENi OAT! I s l o.74I© I7SO 13 REPORT 12 l CA,7JE s f1 80 I© EVENT OESCi:IIPTlON ANO PROBABLE CONSEQUENCES@ l Pipe stress reanalysis on show cause liries outside cont*ainment has **t-eV'ealed an over- [[ID I stress on line 18"-CC-9-121, Unit No~ 2 supply to the "A" Residual Heat Removal .[[E) J Exchanger. This event is reportable in accordance with. the NRC- order lifting susp~ri- []J]J lsion of facility operation dated August 22,1979 and Technical Specification 6.6.2.a.9.J

 ~ ]The health and safety of the public were not affected since the redundant train was

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[II§] JStress calculations revealed that the installed supports would riot prevent an oyer-o::::o:::J 1stressed condition on the affected line during a Design Basis Earthguake. Modifics1,tjorl o:II] !was initiated in accordance with preliminary design drawings and completed priori~ to [il]J !the final stress calculation.

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e SURRY POWER STATION, UNIT 1 DOCKET NO: 50-280 REPORT NO: 80-010/0lX-l EVENT DATE: 01-31-80 TITLE OF REPORT: EXCESSIVE STRESS ON PIPE 18"-CC-9-121

1. DESCRIPTION OF EVENT:

During progress of the pipe stress reanalysis effort, it was determined that line 18"-CC-9-121 would have been overstressed (exceeding 50 percent ultimate capacity) in the event of a Design Basis Earthquake. The affected line feeds the Unit No.2 "A" RHR. Heat Exchanger. This event is reportable in accordance:JWith the NRC order lifting suspension of unit operation dated August 22,1979 and Tech. Spec. 6.6.2.a.9.

2. PROBABLE CONSEQUENCES AND STATUS OF REDUNDANT SYSTEMS:

Since the redundant train was operable and isolation capability, for the affected line was available, the health and safety of the public were not affected.

3. CAUSE:

The problem was disclosed when the architect engineer, who is conducting the pipe stress reanalysis required by the NRC Show Cause Order, discovered the overstress condition.

4. IMMEDIATE CORRECTIVE ACTION:

The overstressed condition was relieved by installing a constraint in accordance with preliminary design drawings.

5. SUBSEQUENT CORRECTIVE ACTION:

No subsequent action is required since the overstressed :condition has been rectified.

6. FUTURE CORRECTIVE ACTION:

None required.

7. GENERIC IMPLICATIONS:

The reanalysis has been directed towards all Show Cause Lines. As overstressed conditions arise*, the appropriate corrective actions are implemented.}}