ML20027D311

From kanterella
Revision as of 16:54, 20 February 2020 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 82-008/03L-0:on 820929,svc Water Pond Level Indication Not Verified for Modes 1,2,3 & 4 from 820922-29.Caused by Pond Level Entry Omitted from Operator Logs Due to Personnel Error.Logs Reviewed & Revised
ML20027D311
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 10/26/1982
From: Fields C
SOUTH CAROLINA ELECTRIC & GAS CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20027D305 List:
References
LER-82-008-03L, LER-82-8-3L, NUDOCS 8211040105
Download: ML20027D311 (1)


Text

f~  ?

$ N a C FEM 353 U.S. NUCL2A2 RCRULATSOY CCMM13SION APPAMV3D GY OMu LICENSEE EVENT REPORT E'O$$'s.ne a (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

CONTRCL BLOCK: l -- l l l l l l@

l o li l..l S l C T

l V l C l S l 1 l@l 0 l 0 l- l 0L.Cl 0EN lf E0Nb[MB0E lR 0 l - l 0 l 0 l@l 4 lLICENSE LICENSEE CODE .. .S .3 ..

1 l 0 TYPE l 0 l 0 l@l

3. 9, CAT l

5.

l@

CON'T l o li l ""0": l ..L l@l O l 5 l 0DOCKET l O NUMBER l 0 l 3 l 9 ] 5.. l@l 0 l 9EVENT l 2 Dl 9 l 8 l 2 l@l 1 ] 0R EPORT l 216 l 8 l 2..l@

y g ., .9 ATE ,. ,9 D ATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o2 lIthiin enine throuch initial plant startun and having recently entered Mode 4, l j o l3 l l Technical Specification 4.7.5 requires Service Water Pond level verification l lo l4 l l at least once every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. These readings were omitted from 9/22/82 to l lo ls l l 9/29/82. There were no adverse consequences since the plant had no inventory l 1o16ll of decav heat. Also, it was verified that the pond had not dropped below the l l o l 7 l l Technical Specification minimum level. l loistl l

, s ..

S Y ST E M CAUSE CAUSE COMP. VALVE CODE CODE SusCODE COMPONENT CODE SUSCODE SUSCODE lo l9 l l Zl Zl@ l Alh l l@ l Zl2lZ lZ l ZlZ l@ [Zj@ l Zl@

E,EN,, EAR  :::.":,""'.'

  • c """:"" "n "' "":.':.' "

@ 5,s.?R I aI 9Iu l, l lo l o I s I l/l l0l31 U,.J I-I

,, L..OJ

=~==  ::::::, ==" .URS .:: = . "'::. = -

S M:::::,=RS (j@l Gl@ lZl@ lZ l@ l0 l 0 l 010l 38 3. SS 3. 3,

@ :=W= @:lN l@ lZl@ l Zl 9l9 19 l

.. ., .. .3 .. .,

CAUSE DESORIPTION AND CORRECTIVE ACTIONS h 1110 l l The Operator Logs were recently revised. In the revision process, the Service l l i l 3 g j Water Pond level entry was omitted by personnel error. The Logs were revised y 1 2 l to include this surveillance. Also, the Logs were reviewed to ensure that all l l i l 3 l l required Tech. Spec. surveillances assigned to be covered on logs were infact l g,,,,l included.

No additional problems were discovered.

STAT S  % POW E R OTHER ST ATUS ISCOVER Y D.SCO VE R Y D E SCR.PT.ON l1l5ll. Bl @ l0 l 0 l 0 l@l N/A l l l@l NRC Resident Inspector l

, . i. i. ,, . . .

RELEASED RELEASE AMOUNT OF ACTIVITY LOC ATION OF R ELE ASE I 116. I, (_7J @ l,Z.j@l N/A l l N/A l NUMBER TVPE D E S C R IPT,0N Iil71l0l0l0l@lZl@l N/A l

PERSONNEL MJUR ES N/A I IilalI010l0IOL._

TYPE D E S C I.,P TIO N W102.6 l119l hl N/A h N CK 05000 l

8 NRC USE ONLY

..SU E T,""'n'S C ,,,PT.O N @

N/A I l lllllllllll l 12l OIL.nJ81 NAME OF PREPARER Curtis Fields pnong (803) 345-5209

/