IR 05000220/2008005

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January 27, 2009

Mr. Keith Vice President Nine Mile Point Nine Mile Point Nuclear Station, LLC P.O. Box 63 Lycoming, NY 13093

SUBJECT: NINE MILE POINT NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000220/2008005 and 05000410/2008005

Dear Mr. Polson:

On December 31, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Nine Mile Point Nuclear Station, Units 1 and 2. The enclosed integrated inspection report documents the inspection results discussed on January 23, 2009, with you and members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents one NRC-identified finding of very low safety significance (Green) which was determined to involve a violation of NRC requirements. However, because of its very low safety significance and because it was entered into your corrective action program (CAP), the NRC is treating this violation as a non-cited violation (NCV) in accordance with Section VI.A.1 of the NRC's Enforcement Policy. If you contest the NCV noted in this report, you should provide a response with the basis for your denial, within 30 days of the date of this inspection report, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, D.C.

20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-001; and the NRC Senior Resident Inspector at Nine Mile Point Nuclear Station.

In accordance with 10 CFR Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/ Original Signed By: Glenn T. Dentel, Chief Projects Branch 1 Division of Reactor Projects

Docket No.: 50-220, 50-410 License No.: DPR-63, NPF-69

Enclosure:

Inspection Report 05000220/2008005 and 05000410/2008005

w/Attachment:

Supplemental Information cc w/encl:

M. Wallace, Vice - Chairman, Constellation Energy H. Barron, President, CEO & Chief Nuclear Officer, Constellation Energy Nuclear Group C. Fleming, Esquire, Senior Counsel, Nuclear Generation, Constellation Energy Group, LLC M. Wetterhahn, Esquire, Winston & Strawn T. Syrell, Director, Licensing, Nine Mile Point Nuclear Station P. Tonko, President and CEO, New York State Energy Research and Development Authority J. Spath, Program Director, New York State Energy Research and Development Authority P. Eddy, New York State Department of Public Service C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law Supervisor, Town of Scriba P. Church, Oswego County Administator T. Judson, Central NY Citizens Awareness Network D. Katz, Citizens Awareness Network G. Detter, Manager, Nuclear Safety and Security, Constellation Energy

SUMMARY OF FINDINGS

............................................................................................................ 3

REPORT DETAILS

........................................................................................................................

REACTOR SAFETY

...................................................................................................................... 4 1R01 Adverse Weather Protection ....................................................................................... 4 1R04 Equipment Alignment .................................................................................................. 5

1R05 Fire Protection

............................................................................................................ 6 1R11 Licensed Operator Requalification Program ................................................................ 6

1R12 Maintenance Effectiveness .......................................................................................... 8 1R13 Maintenance Risk Assessments and Emergent Work Control

.................................... 9 1R15 Operability Evaluations ............................................................................................. 12 1R18 Plant Modifications .................................................................................................... 13 1R19 Post Maintenance Testing ........................................................................................ 13 1R20 Refueling and Other Outage Activities ...................................................................... 14 1R22 Surveillance Testing

RADIATION SAFETY

.................................................................................................................. 16 2OS1 Access Control to Radiologically Significant Areas ................................................... 16 2OS2 ALARA Planning and Controls .................................................................................. 17 2OS3 Radiation Monitoring Instrumentation and Protective Equipment .............................. 17 2PS2 Radioactive Material Processing and Transportation

OTHER ACTIVITIES

................................................................................................................... 20

4OA1 Performance Indicator Verification

............................................................................ 20

4OA2 Identification and Resolution of Problems

................................................................. 21

4OA3 Followup of Events and Notices of Enforcement Discretion

...................................... 25

4OA5 Other Activities ........................................................................................................... 26 4OA6 Meetings, including Exit ............................................................................................. 26 ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

..................................................................................................... A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

......................................................... A-1

LIST OF DOCUMENTS REVIEWED

......................................................................................... A-1

LIST OF ACRONYMS

...... ......................................................................................................... A-9
3SUMMAR Y
OF [[]]
FINDIN [[]]

GS

IR 05000220/2008005, 05000410/2008005; 10/01/08 - 12/31/08; Nine Mile Point Nuclear Station,

Units 1 and 2; Maintenance Risk Assessments and Emergent Work Control.

The report covered a three-month period of inspection by resident inspectors and regional

specialist inspectors. One Green NCV was identified. The significance of most findings is

indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC)

0609, "Significance Determination Process (SDP)." Findings for which the SDP does not apply

may be Green or be assigned a severity level after

NRC management review. The

NRC's

program for overseeing the safe operation of commercial nuclear power reactors is described in

NUR [[]]
EG -1649, "Reactor Oversight Process," Revision 4, dated December 2006.
A. [[]]
NRC -Identified and Self-Revealing Findings Cornerstone: Initiating Events * Green. An
NRC -identified Green non-cited violation (
NCV ) of
10 CFR 50, Appendix B, Criterion

XVI, "Corrective Action," was identified on November 8, 2008 in that Nine

Mile Point Nuclear Station (NMPNS) did not take prompt action to verify that service

water (SW) pump performance had not been adversely affected following the

inadvertent introduction of a cleaning hose into the pump suction lines. This resulted

in delayed identification of two inoperable Unit 2 SW pumps due to fouling of the

impellers by foreign material that had been drawn into the pumps on November 4,

2008. As immediate corrective action, the affected pumps were disassembled and the

pieces of cleaning hose were removed. The finding was more than minor because it was associated with the equipment performance attribute of the Initiating Events cornerstone and affected the associated

cornerstone objective to limit the likelihood of those events that upset plant stability

and challenge critical safety functions during shutdown as well as power operations.

The finding was determined to be of very low safety significance in accordance with

Inspection Manual Chapter (IMC) 0609, Appendix A, "Determining the Significance of

Reactor Inspection Findings for At-Power Situations," based on a Phase 2 analysis

using the Nine Mile Point Unit 2 plant-specific Phase 2 pre-solved worksheets. The

finding had a cross-cutting aspect in the area of human performance because

NMP [[]]

NS did not use conservative assumptions in decision making, in that they did not

timely verify the assumption that the cleaning hose was fully retrieved and had not

impacted operability of the service water pumps (H.1.b per IMC 0305). (Section

1R13)

B. Licensee-Identified Violations None.
4REPORT [[]]

DETAILS Summary of Plant Status

Nine Mile Point Unit 1 began the inspection period at full rated thermal power (RTP). On October

10, power was reduced to 70 percent for power suppression testing to identify and suppress a

leaking fuel bundle. This was completed on October 12 and power escalation was commenced,

with full RTP being reached on October 13. On October 23, operators inserted a manual scram

due to failure of the electronic pressure regulator (EPR) that caused a loss of reactor pressure

control. Following repair, a reactor startup was performed on October 26 and full RTP was

achieved on October 28. On November 1, power was reduced to 80 percent for a control rod

pattern adjustment, and was restored to full RTP later that day. On December 20, power was

reduced to 82 percent for a control rod pattern adjustment and turbine valve testing. Power was

restored to full RTP later that day, and remained there for the rest of the inspection period.

Nine Mile Point Unit 2 began the inspection period at full RTP. On October 18, power was

reduced to 67 percent for a control rod sequence exchange and single control rod scram time

testing. Power was restored to full RTP the following day. On November 13, Unit 2 shut down

for planned outage to replace the 'B' reactor recirculation pump seal package. A reactor startup

was performed on November 16 and full RTP was achieved on November 18. On December 3,

power was reduced to 80 percent to remove the 'E' main condenser water box from service due

to a tube leak. Power was restored to full RTP later that day. On December 6, power was

reduced to 65 percent to swap steam jet air ejectors, plug leaking main condenser tubes, and

perform turbine and main steam isolation valve (MSIV) testing. Power was restored to full

RTP later that day and remained there for the rest of the inspection period. 1.
REACTO R

SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01 - Three samples) .1 Occurrences of Adverse Weather (One sample)

a. Inspection Scope On October 28, 2008, the inspectors reviewed

NMP [[]]

NS's actions in response to a storm in

the vicinity of the station with wind gusting to 50 miles per hour. The inspectors verified

that both units implemented actions specified in their respective adverse weather

procedures to minimize the potential impact of the storm on the station. Unit 1 arranged

for deferral of offsite maintenance on one of the two 115 kilovolt (kV) offsite power lines

(line 4) that had been planned for that day. Unit 2 postponed maintenance on the Division

emergency diesel generator (EDG) until the following day, and deferred diving

operations in the service water (SW) intake bay to allow the traveling screens to be placed

in service. The storm had no adverse affect on the operation of either unit. Documents

reviewed for each section are listed in the Attachment.

b. Findings No findings of significance were identified.

.2 Readiness for Seasonal Extreme Weather Conditions (Two samples)

a. Inspection Scope The inspectors verified the seasonal readiness for Unit 1 and Unit 2 in accordance with

NMPNS procedure

NAI-PSH-11, "Seasonal Readiness Program." The inspectors

reviewed and verified completion of the operations department cold weather preparation

checklists contained in procedures N1-OP-64 and N2-OP-102, "Meteorological

Monitoring," for Units 1 and 2, respectively. The inspectors toured selected areas at Unit

and Unit 2 to verify cold weather readiness. Additionally, the inspectors assessed the

readiness of the following risk significant systems that could be susceptible to the effects

of cold weather:

  • Unit
1 SW system; * Unit 1 containment spray raw water system; * Unit 2

EDGs; and * Unit 2 SW system. b. Findings No findings of significance were identified. 1R04 Equipment Alignment (71111.04 - Three samples) a. Inspection Scope The inspectors performed partial system walkdowns to verify risk-significant systems were

properly aligned for operation. The inspectors verified the operability and alignment of

these risk-significant systems while their redundant trains or systems were inoperable or

out of service for maintenance. The inspectors compared system lineups to system

operating procedures, system drawings, and the applicable chapters in the updated final

safety analysis report (UFSAR). The inspectors verified the operability of critical system

components by observing component material condition during the system walkdown.

The inspectors performed partial walkdowns of the following systems:

1 EDG while the Division 2

EDG was inoperable and unavailable; and * Unit 2 reactor core isolation cooling (RCIC) system due to it being a high safety significance single train system.

b. Findings No findings of significance were identified. 1R05 Fire Protection (71111.05Q - Five samples) a. Inspection Scope The inspectors toured areas important to reactor safety at

NMP [[]]

NS to evaluate the

station's control of transient combustibles and ignition sources, and to examine the

material condition, operational status, and operational lineup of fire protection systems including detection, suppression, and fire barriers. The inspectors evaluated fire

protection attributes using the criteria contained in Unit

1 UFS [[]]

AR Appendix 10A, "Fire

Hazards Analysis," and Unit 2 procedure N2-FPI-PFP-0201, "Unit 2 Pre-Fire Plans." The

areas inspected included:

  • Unit 1 screen house; * Unit 1 diesel fire pump room; * Unit 2 low pressure core spray pump room, north auxiliary bay 175 foot elevation; * Unit 2 Division 1 cable spreading room, control building (CB) 237 foot elevation; and * Unit 2 Division 1 switchgear room, CB 261 foot elevation.

b. Findings No findings of significance were identified. 1R11 Licensed Operator Requalification Program .1 Quarterly Review (71111.11Q - Two samples) a. Inspection Scope

The inspectors evaluated two simulator scenarios in the licensed operator requalification

training (LORT) program. The inspectors assessed the clarity and effectiveness of

communications, the implementation of appropriate actions in response to alarms, the

performance of timely control board operation, and the oversight and direction provided by

the shift manager. During the scenario, the inspectors also compared simulator

performance with actual plant performance in the control room. The following scenarios

were observed:

  • On November 4, 2008, the inspectors observed Unit
1 LO [[]]

RT to assess operator and instructor performance during a scenario involving loss of reactor protection system

motor generator 131, spurious opening of an emergency relief valve, and a steam leak

with failure of a torus-to-drywell vacuum breaker. The inspectors evaluated the

performance of risk significant operator actions including the use of special operating

procedures (SOPs) and emergency operating procedures (EOPs).

7* On October 14, 2008, the inspectors observed Unit

2 LO [[]]

RT to assess operator and instructor performance during a scenario involving a main turbine electro-hydraulic

control system pressure regulator malfunction that caused power to increase, a control

rod drifting out of the core, a loss of all reactor building closed loop cooling system

main pumps, and a failed-open safety relief valve with a break in the tailpiece above

the suppression chamber that required operators to perform a reactor pressure vessel

blowdown due to high drywell pressure. The inspectors evaluated the performance of

risk significant operator actions including the use of

SOP s and

EOPs.

b. Findings No findings of significance were identified.

.2 Biennial Review (71111.11B - One sample)

a. Inspection Scope The following inspection activities were performed using

NUR [[]]

EG 1021, "Operator

Licensing Examination Standards for Power Reactors," Revision 9, Supplement 1,

Inspection Procedure Attachment 71111.11, "Licensed Operator Requalification

Program," Appendix A, "Checklist for Evaluating Facility Testing Material," and Appendix B

"Suggested Interview Topics." A review was conducted of recent operating history documentation found in inspection

reports, licensee event reports (LERs), the licensee's corrective action program (CAP),

and the most recent NRC plant issues matrix. The inspectors also reviewed specific

events from the licensee's CAP which indicated possible training deficiencies, to verify that they had been appropriately addressed. The senior resident inspector was also

consulted for insights regarding licensed operators' performance. These reviews

indicated a potential area for improvement in recognizing off normal equipment status

below any alarm threshold. The operating and written tests for two of the six exam weeks were reviewed for quality

and performance. Compliance with overlap controls of the facility program was verified. On September 19, 2008, the results of the Unit 1 biennial written examination for 2008

and the annual operating tests for both units for 2008 were reviewed against the criteria of

NUR [[]]

EG-1021, "Operator Licensing Examination Standards for Power Reactors," Revision

9, Supplement 1, and NRC Manual Chapter 0609, Appendix I, "Operator Requalification

Human Performance SDP." The review verified the following:

For Unit 1 $ Crew pass rates were greater than 80% (Pass rate was 83.3%); $ Individual pass rates on the written exam were greater than 80% (Pass rate was 97.3%); $ Individual pass rates on the job performance measures (JPMs) of the operating exam were greater than 80% (Pass rate was 97.3%); and

8$ More than 75% of the individuals passed all portions of the exam (86.5% of the individuals passed all portions of the examination). For Unit 2 $ Crew pass rates were greater than 80% (Pass rate was 100%); $ No biennial written examination was administered this year; $ Individual pass rates on the

JPM [[s of the operating exam were greater than 80% (Pass rate was 98%); and $ More than 75% of the individuals passed all portions of the exam (90% of the individuals passed all portions of the examination). Observations were made of the dynamic simulator exams and]]

JPMs administered during

the week of the inspection. These observations included facility evaluations of crew and

individual performance during the dynamic simulator exams and individual performance of

five JPMs. The remediation plans for one crew operating test failure and four individual operating test

failures were reviewed to assess the effectiveness of the remedial training.

Operators, instructors and training/operations management were interviewed for feedback

on their training program and the quality of training received. Simulator performance and fidelity were reviewed for conformance to the reference plant

control room. A sample of administrative records was reviewed for compliance with license conditions,

including NRC regulations. This sample included one year of requalification attendance

records, two years of licensed operator watchstanding proficiency and license reactivation

records, and ten licensed operator medical records.

b. Findings No findings of significance were identified. 1R12 Maintenance Effectiveness (71111.12Q - Two samples) a. Inspection Scope The inspectors reviewed performance-based problems and the performance and

condition history of selected systems to assess the effectiveness of the maintenance

program. The inspectors reviewed the systems to ensure that the station's review

focused on proper maintenance rule scoping in accordance with 10 CFR Part 50.65,

characterization of reliability issues, tracking system and component unavailability, and 10

CFR Part 50.65 (a)(1) and (a)(2) classification. In addition, the inspectors reviewed the

site's ability to identify and address common cause failures and to trend key parameters.

The following maintenance rule inspection samples were reviewed:

9* Unit 1 emergency cooling system, based on repeat problems with main steam vent isolation valves; and * Unit

2 RC [[]]

IC system, based on repeated trip relay failures.

b. Findings No findings of significance were identified. 1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - Six samples) a. Inspection Scope The inspectors evaluated the effectiveness of the maintenance risk assessments required

by 10 CFR Part 50.65 (a)(4). The inspectors reviewed equipment logs, work schedules,

and performed plant tours to verify that actual plant configuration matched the assessed

configuration. Additionally, the inspectors verified that risk management actions for both

planned and emergent work were consistent with those described in station procedures.

The inspectors reviewed risk assessments for the activities listed below. Unit 1 * Week of October 6, which included containment spray 122 quarterly surveillance, EDG 103 monthly surveillance, and an emergent activity to perform power

suppression testing to identify and suppress a leaking fuel bundle. * Week of November 3, which included EDG 103 monthly surveillance, containment spray 121 quarterly surveillance and heat exchanger performance testing, an

extended maintenance period for 12 instrument air compressor, off-site 115 kV line 4

out of service for two days for off-site maintenance, and calibration of the average

power range monitoring system using the traversing in-core probe system. * Week of November 17, which included 111 and 121 core spray system quarterly surveillances, 111 containment spray heat exchanger performance testing, a three

day outage for

EDG 102 to clean the fuel oil storage tank, and

EDG 102 monthly

surveillance. Unit 2 * Week of October 13, which included

SW intake bay cleaning, Division 1

EDG monthly surveillance, a two day maintenance period for the Division 1 residual heat removal

(RHR) system, Division 1 RHR quarterly surveillance, a power reduction to 65 percent

for a control rod pattern exchange and single control rod scram time testing, and an

emergent issue to repair the 'B'

SW pump after failure of the outboard pump bearing. * Week of November 3, which included
RCIC system quarterly surveillances,
SW intake bay cleaning, and emergent maintenance to replace broken shear pins for the 'B'

SW

discharge strainer and to remove foreign material from the 'C' and 'F' SW pumps.

10 * Week of December 1, which included Division 2 standby liquid control system valve maintenance and quarterly surveillance, Division 2 SW pumps quarterly surveillance,

Division 2 EDG annual 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run surveillance, and emergent maintenance to repair

the 'E' SW discharge strainer. In addition, the week included the identification of lake

water inleakage to the condensate system which led to a 20 percent power reduction

to remove the 'E' main condenser waterbox from service, and a subsequent power

reduction to 65 percent to conduct repairs and swap steam jet air ejectors.

b. Findings

Introduction. An

NRC -identified Green
NCV of
10 CFR 50, Appendix B, Criterion
XVI , "Corrective Action," was identified on November 8, 2008 in that
NMP [[]]

NS did not take

prompt action to verify that SW pump performance had not been adversely affected

following the inadvertent introduction of a cleaning hose into the pump suction lines. This

resulted in delayed identification of two inoperable Unit 2 SW pumps due to fouling of the

impellers by foreign material that had been drawn into the pumps on November 4, 2008. Description. The Unit 2 SW system has six pumps (A-F), with three in each of the two Divisional subsystems (A, C, and E in Division 1, and B, D, and F in Division 2). The

subsystems are normally cross-connected, with two pumps operating in each subsystem. On the morning of November 4, 2008, divers were cleaning the Unit 2 SW intake bay

using a vacuum device that was connected to a six inch diameter plastic hose. At 11:43

a.m., operators in the control room received an alarm that indicated low suction pressure

for the Division

1 SW pumps, and observed decreased discharge flow from the 'C'

SW

pump. The control room operators contacted the diving supervisor, who informed them

that the cleaning vacuum hose had inadvertently been drawn into the suction pipe for the

'C'

SW pump. The 'E'

SW pump was started to allow the 'C' SW pump to be secured, and

the hose was withdrawn. At about 12:45 p.m., a similar event occurred with the 'F'

SW pump; the 'C'
SW pump was started, the 'F'

SW pump was secured, and the hose was

withdrawn. Cleaning operations were secured and the cleaning vacuum hose was

removed from the water. Although the end of the hose had broken into several pieces,

NMPNS determined incorrectly that all of the hose had been retrieved. Later on November 4, the inspectors noted that the discharge flow for the 'C'

SW pump

appeared to be lower than normal. The control room operators responded that the lower

flow was normal for the existing pump combination. On November 7, 2008, the 'F' SW pump was started as part of a planned pump swap.

This was the first time that the pump had been operated since it had been secured on

November 4 to allow removal of the cleaning vacuum hose. An operator reported that the

pump had made an abnormal noise just after it had been started, and control room

operators observed abnormally low discharge flow. The 'F' SW pump was secured and

declared inoperable. Disassembly of the pump revealed that approximately five feet of

cleaning vacuum hose was lodged in the pump casing and impeller. The 'F' SW pump

was restored to a functional status on November 8 at 5:31 p.m.

11Because the November 7 issue with the 'F' SW pump confirmed that all of the cleaning vacuum hose had not actually been retrieved on November 4, the inspectors questioned

whether additional action would be taken to verify that the 'C' SW pump had not been

similarly impacted.

NMPNS indicated that the

SW pump quarterly surveillance would be

performed to verify the operability of all of the remaining SW pumps. During this test,

operators were unable to achieve the required parameters for the 'C' SW pump, and the

pump was declared inoperable. Test results for the remaining SW pumps were

satisfactory. On November 9 at 2:54 a.m., the 'C' SW pump was declared unavailable to

support disassembly; approximately one foot of cleaning suction hose was found lodged

in the impeller. The 'C' SW pump was returned to a functional status at 5:45 p.m. on

November 9.

NMPNS engineering subsequently determined that the 'C'

SW pump had been functional

between November 4, when the hose had been sucked into the pump, and November 9,

when the pump was declared inoperable and disassembled. The inspector agreed with

this determination, because, while the pump was inoperable (pump differential pressure

degraded below the in-service test requirement), it still would have supported SW system

operability in combination with any of the remaining operable SW pumps. As immediate corrective action for this event, the affected pumps were disassembled and

the foreign material was removed. These issues were entered into the CAP as condition

report (CR) 2008-8430 for the 'F'

SW pump and
CR 2008-8444 for the 'C'
SW pump. The performance deficiency associated with this event was that

NMPNS did not promptly

verify that ingestion of the cleaning vacuum hose into the 'C' and 'F' SW pump suction

lines had not adversely affected the performance of the pumps. Corrective action to

address the failure to promptly verify

SW pump operability is being addressed by

CR

2008-8492. Analysis. The finding is more than minor because it is associated with the equipment performance attribute of the Initiating Events cornerstone and affects the associated

cornerstone objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. Per

inspection manual chapter (IMC) 0609, Attachment 0609.04, "Initial Screening and

Characterization of Findings," the inspectors conducted a Phase 1 screening and

determined that this finding required a Phase 2 analysis because the finding contributed

to both the likelihood of a reactor trip and the likelihood that mitigation equipment

functions would not be available. The inspectors determined that the finding was of very low safety significance (Green)

using the Unit 2 plant-specific Phase 2 pre-solved worksheets, which include large early

release frequency and external events, in accordance with IMC 0609, Appendix A,

"Determining the Significance of Reactor Inspection Findings for At-Power Situations."

The following assumptions were made during the evaluation: 1) the reactor was operating

at full power; 2) the 'C'

SW pump was functional while the 'F'

SW pump was not

functional; 3) the 'F' SW pump was unavailable for greater than three days but less than

days (approximately 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> from when the hose was drawn into the suction pipe

and the pump was secured on November 4 until it was restored to available status on

2November 8); and 4) the approximately 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> that the 'C' SW pump was not functional (November 9, while the pump was disassembled), would not add significantly to the result.

The risk increase was dominated by the internal core damage frequency increase which

was conservatively estimated to be in the mid E-7/year range. The dominate core

damage sequence was based on the increased frequency of a loss of SW initiating event,

due to loss of SW pump redundancy, and included the failure of containment heat

removal, failure to vent the containment, and failure of low pressure injection sources

following containment failure. The finding had a cross-cutting aspect in the area of human performance because

NMP [[]]

NS did not use conservative assumptions in decision making, in that they did not

timely verify the assumption that the cleaning hose was fully retrieved and had not

impacted operability of the service water pumps (H.1.b per

IMC 0305). Enforcement. 10

CFR 50, Appendix B, Criterion XVI, "Corrective Action," states, in part, "Measures shall be established to assure that conditions adverse to quality, such as

failures, malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformance are promptly identified and corrected." Contrary to the above, on

November 4 until November 8, 2008,

NMP [[]]

NS did not promptly identify that introduction of

foreign material into the 'C' and 'F'

SW pump suction lines had degraded the 'C' and 'F'
SW pumps. This resulted in inoperability of the pumps. Because this noncompliance is of very low safety significance and was entered into the

CAP as CRs 2008-8430, 2008-

8444, and 2008-8492, this violation is being treated as an

NCV , consistent with Section
VI.A. 1 of the
NRC Enforcement Policy. (

NCV 05000410/2008005-01, Untimely Corrective Action for Degraded Service Water Pumps) 1R15 Operability Evaluations (71111.15 - Five samples) a. Inspection Scope The inspectors evaluated the acceptability of operability evaluations, the use and control

of compensatory measures, and compliance with technical specifications (TSs). The

evaluations were reviewed using criteria specified in NRC Regulatory Issue Summary

2005-20, "Revision to Guidance Formerly Contained in NRC Generic Letter 91-18,

'Information to Licensees Regarding Two NRC Inspection Manual Sections on Resolution

of Degraded and Nonconforming Conditions and on Operability'," and Inspection Manual

Part 9900, "Operability Determinations and Functionality Assessments for Resolution of

Degraded or Nonconforming Conditions Adverse to Quality or Safety." The inspectors'

review included verification that the operability determinations were made as specified by

Procedure

CNG -

OP-1.01-1002, "Conduct of Operability Determinations / Functionality

Assessments." The technical adequacy of the determinations was reviewed and

compared to the

TS s,

UFSAR, and associated design basis documents (DBDs).

The following evaluations were reviewed:

  • CR 2008-8383 concerning the post-accident monitoring reliability of Unit 1 drywell pressure instruments following a postulated fuel failure and design basis loss of

coolant accident;

13*

CR 2008-8680 concerning Unit 1
EDG 102 fuel oil storage tank wall pitting; *
CR 2008-7690 concerning divergence of two channels of the Unit 2 leak detection system differential temperature monitors for the main steam tunnel; *
CR 2008-8405 concerning the continued operability of the 'B'
SW pump without strainer backwash in service due to broken shear pins in the rotating mechanism; and *

CR 2008-8518 concerning the Unit 2 TS-required determination of acceptability for continued operation of the reactor coolant system following a cooldown of greater than

100 degrees Fahrenheit (F) in a one hour period.

b. Findings No findings of significance were identified.

1R18 Plant Modifications (71111.18 - One sample) a. Inspection Scope The inspectors reviewed a Unit 2 temporary modification that installed a blowdown valve

at a low point of the instrument air system for removal of condensation in the system. It

was installed to reduce air moisture content and prevent condensation in air operated

components that could result in component malfunction. The inspectors reviewed the

modification package and discussed its installation with mechanical engineering

personnel. The inspectors evaluated the modification against the system design

attributes listed in Unit

2 UFS [[]]

AR Section 9.3.1.1, "Instrument Air System."

b. Findings No findings of significance were identified. 1R19 Post Maintenance Testing (71111.19 - Four samples) a. Inspection Scope The inspectors reviewed the post maintenance tests (PMTs) listed below to verify that

procedures and test activities ensured system operability and functional capability. The

inspectors reviewed the test procedure to verify that the procedure adequately tested the

safety functions that may have been affected by the maintenance activity, that the

acceptance criteria in the procedure were consistent with information in the applicable

licensing basis and/or DBDs, and that the procedure had been properly reviewed and

approved. The inspectors also witnessed the test or reviewed test data, to verify that the

test results adequately demonstrated restoration of the affected safety functions. * Unit 1, Work Order (WO) 08-01313-00 to replace solenoid operated valves 113-273 and 113-274 for air operated valves 44.2-18 and 44.2-15 that control the vent and

drain valves for the scram discharge volume, due to slow closure time after the

October 23 scram. The PMT was to stroke time the vent and drain valves open and

closed, in accordance with the WO step text.

14 * Unit 1,

WO 07-03553-00 for preventive maintenance on drywell nitrogen containment isolation valve air regulators. The

PMT was to exercise the valves in accordance with

procedure N1-ST-Q5, "Primary Containment Isolation Valves Operability Test." * Unit 2,

WO 08-18322-00 to replace solenoid valves 2
MSS *SOV7C-1, -2, and -3 for
MSIV 2
MSS *7C, due to the
MS [[]]

IV having cycled without operator action following slow

closure. The

PMT was to perform 2

MSS*7C fast closure stroke timing in accordance

with N2-OSP-MSS-CS001, "MSIV Operability Test," perform 2MSS*7C slow closure in

accordance with N2-OP-1, "Main Steam System," and verify proper solenoid operating

currents in accordance with N2-OSP-LOG-W001, "Weekly Checks." * Unit 2,

WO 08-10810-00 to recondition or replace Division 1 standby liquid control pump suction and discharge valves in accordance with N2-

MPM-SLS-V143, "Standby

Liquid Control Pumps

PM and Overhaul." The

PMT was to operate the pump at

normal flow and test pressure in accordance with N2-OSP-SLS-Q001, "Standby Liquid

Control Pump, Check Valve, Relief Valve Operability Test and

ASME [[]]

XI Pressure

Test."

b. Findings No findings of significance were identified.

1R20 Refueling and Other Outage Activities (71111.20 - Two samples)

.1 Unit 1 Forced Outage

a. Inspection Scope

The inspectors observed and reviewed the following activities during the Unit 1 forced

outage from October 23 to October 26, 2008.

The inspectors observed portions of the plant shutdown and cooldown and verified that

the TS cooldown rate limits were satisfied. The inspector reviewed outage schedules and

procedures, and verified that TS specified safety system availability was maintained and

that shutdown risk was considered.

The inspectors observed portions of the reactor startup following the outage, and verified

through control room observations, discussions with personnel, and log reviews that

safety-related equipment specified for mode change was operable.

b. Findings No findings of significance were identified.

15.2 Unit 2 Planned Outage

a. Inspection Scope The inspectors observed and reviewed the following activities during the Unit 2 planned

outage from November 13 to November 16, 2008.

The inspectors observed portions of the plant shutdown and cooldown. The inspectors

reviewed outage schedules and procedures, and verified that TS specified safety system

availability was maintained and that shutdown risk was considered.

The inspectors performed a walkdown of accessible areas of the drywell to identify

evidence of reactor coolant system leakage, and verify the condition of drywell coatings,

structures, valves, piping, supports, and other equipment.

The inspectors observed portions of the reactor startup following the outage, and verified

through control room observations, discussions with personnel, and log reviews that

safety-related equipment specified for mode change was operable.

b. Findings No findings of significance were identified. 1R22 Surveillance Testing (71111.22 - Four samples) a. Inspection Scope The inspectors witnessed performance of and/or reviewed test data for risk-significant

surveillance tests to assess whether the components and systems tested satisfied design

and licensing basis requirements. The inspectors verified that test acceptance criteria

were clear, demonstrated operational readiness and were consistent with the DBDs; that

test instrumentation had current calibrations and the range and accuracy for the

application; and that tests were performed, as written, with applicable prerequisites

satisfied. Upon test completion, the inspectors verified that equipment was returned to

the status specified to perform its safety function.

The following surveillance tests were reviewed:

  • N1-SST-Q6D, "Containment Spray System Loop 122 Quarterly Operability Test;" * N1-ST-M1A, "Liquid Poison Pump 11 Operability Test;" * N2-OSP-RHS-Q@006, "RHR System Loop C Pump and Valve Operability Test and System Integrity Test;" and * N2-ESP-ENS-Q731, "Quarterly Channel Functional Test of
LPCS /

LPCI [low pressure core spray/low pressure coolant injection] Pumps A, B, and C (Normal and Emergency

Power) Auto Start Time Delay Relays."

16 b. Findings No findings of significance were identified. 2.

RADIAT [[]]
ION [[]]
SAFETY 2

OS1 Access Control to Radiologically Significant Areas (71121.01 - Seven samples)

a. Inspection Scope The inspectors reviewed all licensee performance indicators (PIs) for the occupational

radiation safety cornerstone for follow-up. The inspectors reviewed the licensee's self assessments, audits, LERs, and Special

Reports related to the access control program since the last inspection. The inspectors

verified that identified problems were entered into the CAP for resolution. The inspectors reviewed corrective action reports related to access controls. The

inspectors interviewed staff and reviewed documents to determine if the activities are

being conducted in an effective and timely manner commensurate with their importance to

safety and risk:

  • Initial problem identification, characterization, and tracking; * Disposition of operability/reportability issues; * Evaluation of safety significance/risk and priority for resolution; * Identification of repetitive problems; * Identification of contributing causes; * Identification and implementation of effective corrective actions; * Resolution of NCVs tracked in the corrective action system; and * Implementation/consideration of risk significant operational experience feedback.

For repetitive deficiencies or significant individual deficiencies in problem

identification and resolution identified above, the inspectors determined if the licensee's

self-assessment activities were also identifying and addressing these deficiencies. The inspectors reviewed licensee documentation packages for all PI events occurring

since the last inspection. The inspectors determined if any of these PI events involved

dose rates >25 rad per hour (R/hr) at 30 centimeters or >500 R/hr at 1 meter. If so, the

inspectors determined what barriers had failed and if there were any barriers left to

prevent personnel access. For unintended exposures >100 millirem (mrem) total effective

dose equivalent (TEDE) (or >5 rem skin dose equivalent (SDE) or >1.5 rem lens dose

equivalent (LDE)), the inspectors determined if there were any overexposures or

substantial potential for overexposure. The inspectors reviewed any radiological problem reports since the last inspection which

were attributed to radiation worker errors. The inspectors evaluated whether there was an

17observable pattern traceable to a similar cause. The inspectors determined if this perspective matched the corrective action approach taken by the licensee to resolve the

reported problems. The inspectors discussed with the radiation protection manager any

problems with the correction actions planned or taken. The inspectors reviewed any radiological problem reports since the last inspection

which were attributed to radiation protection technician errors. The inspectors determined

if there was an observable pattern traceable to a similar cause. The inspectors

determined if this perspective matched the corrective action approach taken by the

licensee to resolve the reported problems.

The inspectors evaluated licensee performance against the requirements contained in

CFR 20, Unit 1

TS 6.7 and Unit 2 TS 5.7.

b. Findings No findings of significance were identified.

2OS 2

ALARA Planning and Controls (71121.02 - Two samples)

a. Inspection Scope The inspectors reviewed the licensee's self assessments, audits, and Special Reports

related to the as low as reasonably achievable (ALARA) program since the last inspection.

The inspectors determined if the licensee's overall audit program's scope and frequency

(for all applicable areas under the Occupational Radiation Safety Cornerstone) met the

requirements of 10 CFR 20.1101(c). For repetitive deficiencies or significant individual deficiencies in problem

identification and resolution identified above, the inspectors determined if the licensee's

self-assessment activities were also identifying and addressing these deficiencies.

The inspectors evaluated licensee performance against the requirements contained in

CFR 20.1101.

b. Findings No findings of significance were identified.

2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03 - Two samples)

a. Inspection Scope The inspectors reviewed CAP reports related to exposure significant radiological incidents

that involved radiation monitoring instrument deficiencies since the last inspection in this

area. The inspectors interviewed staff and reviewed documents to determine if the

following activities were being conducted in an effective and timely manner commensurate

18with their importance to safety and risk: * Initial problem identification, characterization, and tracking; * Disposition of operability/reportability issues; * Evaluation of safety significance/risk and priority for resolution; * Identification of repetitive problems; * Identification of contributing causes; * Identification and implementation of corrective actions which will achieve lasting results; * Resolution of NCVs tracked in corrective action system(s); and * Implementation/consideration of risk significant operational experience feedback. For repetitive deficiencies or significant individual deficiencies in problem identification and resolution identified above, the inspectors determined if the licensee's self-assessment

activities are also identifying and addressing these deficiencies.

The inspectors evaluated licensee performance against the requirements contained in

CFR 20.1501, 10

CFR 20.1703 and 10 CFR 20.1704.

b. Findings No findings of significance were identified.

2PS2 Radioactive Material Processing and Transportation (71122.02 - Six samples)

a. Inspection Scope The inspectors reviewed the solid radioactive waste system description in the

UFS [[]]

AR and

the recent radiological effluent release report for information on the types and amounts of

radioactive waste disposed. The inspectors reviewed the scope of the licensee's audit

program to verify that it meets the requirements of 10 CFR 20.1101(c). The inspectors walked-down the liquid and solid radioactive waste processing systems to

verify and assess that the current system configuration and operation agree with the

descriptions contained in the

UFSAR and in the Process Control Program (

PCP). The

inspectors reviewed the status of any radioactive waste process equipment that was not

operational and/or was abandoned in place. The inspectors reviewed the licensee's

administrative and physical controls to ensure that the equipment will not contribute to an

unmonitored release path and/or affect operating systems or be a source of unnecessary

personnel exposure.

The inspectors reviewed the adequacy of any changes made to the radioactive waste

processing systems since the last inspection. The inspectors verified that the changes

were reviewed and documented in accordance with 10 CFR 50.59, as appropriate. The

inspectors reviewed the impact, if any, to radiation doses to members of the public. The

inspectors reviewed current processes for transferring radioactive waste resin and sludge

discharges into shipping/disposal containers to determine if appropriate waste stream

19mixing and/or sampling procedures, and methodology for waste concentration averaging, provide representative samples of the waste product for the purposes of waste

classification as specified in 10 CFR 61.55 for waste disposal. The inspectors reviewed the radio-chemical sample analysis results for each of the

licensee's radioactive waste streams. The inspectors reviewed the licensee's use of

scaling factors and calculations used to account for difficult-to-measure radionuclides.

The inspectors verified that the licensee's program assures compliance with

10 CFR 61.55 and
10 CFR 61.56 as required by Appendix G of 10

CFR Part 20. The inspectors

reviewed the licensee's program to ensure that the waste stream composition data

accounts for changing operational parameters and thus remains valid between the annual

or biennial sample analysis update.

The inspectors observed shipment packaging, surveying, labeling, marking, placarding,

vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and licensee verification of shipment readiness. The inspectors verified that

the requirements of any applicable transport cask Certificate of Compliance had been

met. The inspectors verified that the receiving licensee is authorized to receive the

shipment packages. The inspectors observed radiation workers during the conduct of

radioactive waste processing and radioactive material shipment preparation activities.

The inspectors determined if the shippers were knowledgeable of the shipping regulations

and whether shipping personnel demonstrated adequate skills to accomplish the package

preparation requirements for public transport with respect to NRC Bulletin 79-19 and 49

CFR Part 172 Subpart H. The inspectors verified that the licensee's training program

provided training to personnel responsible for the conduct of radioactive waste processing

and radioactive material shipment preparation activities. The inspectors sampled non-excepted package shipment records. The inspectors

reviewed these records for compliance with NRC and Department of Transportation

(DOT) requirements. The inspectors reviewed the licensee's LERs, Special Reports, audits, State agency

reports, and self assessments related to the radioactive material and transportation

programs performed since the last inspection. The inspectors determined if identified

problems are entered into the CAP for resolution. The inspectors reviewed corrective

action reports written against the radioactive material and shipping programs since the

previous inspection. The inspectors interviewed staff and reviewed documents to determine if the following

activities were being conducted in an effective and timely manner commensurate with

their importance to safety and risk:

  • Initial problem identification, characterization, and tracking; * Disposition of operability/reportability issues; * Evaluation of safety significance/risk and priority for resolution; * Identification of repetitive problems; * Identification of contributing cause;

20* Identification and implementation of effective corrective actions; * Resolution of NCVs tracked in corrective action system(s); and * Implementation/consideration of risk significant operational experience feedback. For repetitive deficiencies or significant individual deficiencies in problem

identification and resolution identified above, the inspectors determined if the licensee's

self-assessment activities were also identifying and addressing these deficiencies.

b. Findings No findings of significance were identified. 4.

OTHER [[]]
ACTIVI TIES
4OA 1 Performance Indicator Verification (71151 - Twelve samples) a. Inspection Scope The inspectors sampled

NMPNS submittals for the PIs listed below. To verify the

accuracy of the

PI data reported during that period, the

PI definition guidance contained in

Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Performance Indicator

Guideline," Revision 5, was used to verify the basis in reporting for each data element.

Cornerstone: Mitigating Systems

The inspectors reviewed

NMP [[]]

NS's submittals for the Mitigating System Performance

Indicators (MSPIs) listed below to determine the accuracy and completeness of the

reported data. The review was accomplished by comparing the reported PI data to plant

records and information available in plant logs,

CR s, system health reports, the respective
MSPI Basis Documents, and

NRC inspection reports. The definitions and guidance in

NEI 99-02, formed the basis for the review. The results were discussed with the

cognizant engineering and licensing personnel. Operating data for the period of October

2007 through September 2008 were reviewed to complete this inspection.

  • Unit 1 emergency alternating current (AC) power system; * Unit 1 high pressure injection system; * Unit 1 heat removal system; * Unit
1 RHR system; * Unit 1 cooling water systems; * Unit 2 emergency

AC power system; * Unit 2 high pressure injection system; * Unit 2 heat removal system; * Unit 2 RHR system; and * Unit 2 cooling water systems.

21Cornerstone: Occupational Radiation Safety

The inspectors reviewed all licensee PIs for the Occupational Radiation Safety

Cornerstone for follow-up. The inspectors reviewed a listing of licensee action reports for

the period January 1, 2008, through November 17, 2008, for issues related to the

Occupational Radiation Safety

PI , which measures non-conformances with high radiation areas greater than 1R/hr and unplanned personnel exposures greater than 100 mrem
TEDE , 5 rem
SDE , 1.5 rem
LDE , or 100 mrem to the unborn child. The inspectors determined if any of these

PI events involved dose rates >25 R/hr at

centimeters or >500 R/hr at 1 meter. If so, the inspector determined what barriers had

failed and if there were any barriers left to prevent personnel access. For unintended

exposures >100 mrem

TEDE [[(or >5 rem]]

SDE or >1.5 rem LDE), the inspector determined

if there were any overexposures or substantial potential for overexposure. The inspectors

compared the results with the reported data.

Cornerstone: Public Radiation Safety The inspectors reviewed a listing of licensee action reports for the period January 1, 2008

through December 8, 2008 for issues related to the public radiation safety PI, which

measures radiological effluent release occurrences per site that exceed 1.5 mrem/quarter

(qtr) whole body or 5 mrem/qtr organ dose for liquid effluents; or 5 mrads/qtr gamma air

dose, 10 mrads/qtr beta air dose; or 7.5 mrems/qtr organ doses from I-131, I-133, H-3

and particulates for gaseous effluents. The inspectors compared the results with the

reported data.

b. Findings No findings of significance were identified.

4OA 2 Identification and Resolution of Problems (71152 - Four samples) .1 Review of Items Entered into the

CAP

a. Inspection Scope As specified by Inspection Procedure 71152, "Identification and Resolution of Problems,"

and in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a daily screening of items entered into

NMPNS 's

CAP. In accordance with the baseline inspection procedures, the inspectors

also identified selected CAP items across the initiating events, mitigating systems, and

barrier integrity cornerstones for additional follow-up and review. The inspectors

assessed the threshold for problem identification, the adequacy of the cause analyses,

extent of condition review, operability determinations, and the timeliness of the specified

corrective actions.

2 b. Findings No findings of significance were identified.

.2 Semi-Annual Review to Identify Trends (One sample)

a. Inspection Scope As specified by Inspection Procedure 71152, "Identification and Resolution of Problems,"

the inspectors reviewed

NMPNS 's

CAP and associated documents to identify trends that

could indicate significant safety issues and/or low level trends before they become

significant. The inspectors' review focused on repetitive equipment and corrective

maintenance issues, and considered the results of the daily inspector CAP item

screening. The review included issues documented outside of the normal CAP, such as

system health reports, quality performance reports, quality assurance assessment

reports, maintenance rule status reports, operator workaround lists, and the governing

procedure. The inspectors' review considered the period of June through November

2008.

b. Assessments and Observations No findings of significance were identified. The inspectors did not identify any equipment

or performance trends that had not already been noted in departmental quarterly

assessments.

NMPNS had a low threshold for the identification of items in the

CAP,

which allowed for the identification of low-level trends before the issue became significant.

.3 Annual Sample - Unit 1 Operator Workarounds (One sample) a. Inspection Scope The inspectors reviewed the Unit 1 operator workarounds, operator burdens, and

operations items of interest, defeated annunciators, control room deficiencies, and open

operability determinations. The review focused on the reliability and availability of

mitigating systems with particular focus on issues that had the potential to affect the ability

of operators to respond to plant transients and events. Also, the inspectors reviewed the

governing procedure,

NAI -

REL-02, "Control of Operator Workarounds, Burdens, and

Interests." The inspectors interviewed operations personnel on their knowledge of

selected workarounds and the associated compensatory actions. In addition, the

inspectors discussed with engineering and operations management the planned

corrective actions for restoration of some of the degraded systems. b. Assessment and Observations No findings of significance were identified. None of the identified issues, individually or in the aggregate, appear to have a negative impact on the ability of the operators to

complete actions in procedures, or to significantly affect the timeliness of those actions.

The inspectors identified one issue which had been removed from the workaround list

without adequate corrective actions being taken. Specifically, the inspectors identified

23that the Unit 1 Shutdown Cooling System outboard isolation valve (SDC IV-38-02), which was placed on the list in August 2004, was removed from the Operator Workaround List

because the nonconforming condition was "accepted-as-is."

Nine Mile Point administrative instruction

NAI -

REL-02, "Control of Operator Workarounds,

Burdens, and Interests," Section 3.5.2, states: "A workaround / burden can be resolved

as an 'Accept-As-Is' condition. In this case the Operations Manager must approve the

'Accept-As-Is' resolution." Section 3.5.3 states, in part, "If a workaround will be resolved

by an 'Accept-As-Is' condition . . . Confirm that any compensatory/manual measures have

been appropriately . . . proceduralized."

The issue was first documented in

CR -2004-3921, dated August 30, 2004. The

CR noted

that the breaker for IV-38-02 tripped while trying to open the valve from the control room.

The cause was determined to be thermal binding; the valve has a solid wedge disc which

is sensitive to temperature differentials between the valve body and disc. One of the

corrective actions was to revise N1-OP-4, "Shutdown Cooling System," to manually open

the valve off the valve seat with a torque wrench, and then complete opening the valve

from the control room. As part of the procedure change process,

NMP [[]]

NS completed a 10

CFR 50.59 Screening Form but failed to recognize/identify that the system operation was

described in the Unit

1 UFSAR. The

UFSAR,Section X.A.2, states that the shutdown

cooling system may be manually actuated from the main control room. The consequence

of the valve failing to open from the control room is a delay in the ability to place shutdown

cooling in service by the normal means. Because the valve is not able to function as

described in the

UFS [[]]

AR, the system is degraded; however, there is no affect on the

safety-related function of the valve, which is to close automatically for containment

isolation.

The failure to identify during the 10 CFR 50.59 screening process for a procedure change

to N1-OP-04 that the change was not consistent with the Unit

1 UFS [[]]

AR is considered a

violation of minor significance. As such, this issue is not subject to enforcement action, in

accordance with the NRC's Enforcement Policy.

.4 Annual Sample - Unit 2 Operator Workarounds (One sample) a. Inspection Scope The inspectors reviewed the Unit 2 operator workarounds, operator burdens, and

operations items of interest, defeated annunciators, control room deficiencies, and open

operability determinations. The review focused on the reliability and availability of

mitigating systems with particular focus on issues that had the potential to affect the ability

of operators to respond to plant transients and events. Also, the inspectors reviewed the

governing procedure,

NAI -

REL-02, "Control of Operator Workarounds, Burdens, and

Interests." The inspectors interviewed operations personnel on their knowledge of

selected workarounds and the associated compensatory actions. In addition, the

inspectors discussed with engineering and operations management the planned

corrective actions for restoration of some of the degraded systems.

24 b. Assessment and Observations No findings of significance were identified. None of the identified issues, individually or in the aggregate, appear to have a negative impact on the ability of the operators to

complete action in procedures, or to significantly affect the timeliness of those actions.

.5 Annual Sample: Review of

NMP [[]]

NS Response to Generic Letter 2007-01 (One Sample)

a. Inspection Scope The inspectors selected CRs 2007-0895 and 2007-1977 as a problem identification and

resolution (PI&R) sample for a detailed follow-up review. CR 2007-0895 documented the

applicability and response to Generic Letter (GL) 2007-01, "Inaccessible or Underground

Power Cable Failures that Disable Accident Mitigation Systems or Cause Plant

Transients." CR 2007-1977 documented water leaking into both the control and reactor

buildings from a Unit 2 Division 3 electrical raceway. The Unit 2 Division 3 electrical raceway supports the power cables from the Division 3 EDG in the control building to the

high pressure core spray (HPCS) pump in the reactor building. The inspectors reviewed

relevant CRs to ensure that issues associated with potentially submerged cables were

fully identified, appropriately evaluated, and corrective actions were specified and

prioritized to prevent recurrence. The inspectors discussed the issue with engineering

personnel and reviewed work orders, maintenance procedures, drawings and completed

surveillance and test procedures on the potential submerged cables.

b. Findings The inspectors inspected

NMP 's evaluation of the

GL and corrective actions taken to

resolve the potential adverse condition documented in CR 2007-1977. Specifically, on

April 1, 2007, a few months after receiving

GL 2007-01,

NMPNS identified a condition

where water was leaking into both the control and reactor buildings indicating that the

HPCS power cables were submerged in water. Then on May 7, 2007,

NMPNS provided

the requested information in

GL 2007-01 to the

NRC. GL 2007-01 informed licensees of an increase in inaccessible or underground cable

failure in the industry due to moisture-induced degradation. The GL discussed that

periodic draining may decrease the rate of cable insulation degradation, but would not

prevent cable failures. In addition, GL 2007-01 discussed that some licensees have

detected cable degradation prior to failures through techniques for measuring and

trending the condition of cable insulation. Although

NMP [[]]

NS inspected and pumped down manholes every six months and tested the

insulation resistance to ground (megger) of some inaccessible/underground power cables

as part of the associated

HP [[]]
CS motor's routine maintenance, the inspectors noted that
NMPNS did not evaluate the potential impact of moisture-induced failure on the
HPCS power cables. In addition, the inspectors were informed that
NMP [[]]
NS did not consider the
GL recommendations because they believed the

HPCS power cables were qualified for

submergence and have had no failures of underground cables at the site.

25The

NRC reviewed
NMPNS 's
HPCS power cable documentation to determine the
HPCS power cable's qualification for submerged conditions. The
NRC identified that the

HPCS

power cables are very similar, if not identical to other power cables recently reviewed.

Based on the information provided by

NMPNS , it was not clear that the

HPCS power

cables are qualified to be submerged for the life of the plant. As a result, the submergence qualification of the

HP [[]]

CS power cables was a potential

performance deficiency, in that

10 CFR 50, Appendix B, Criterion

III requires that measures shall be established to ensure that applicable regulatory requirements and the

design basis are correctly translated into specifications, drawings, procedures, and instructions. This issue is an unresolved item pending

NMP [[]]

NS providing documentation

that the

HPCS cables were purchased, tested and evaluated to be qualified for submergence for the life of the plant and
NRC review of these documents. (URI 05000410/2008005-02, Qualification of
HPCS Power Cables for Submergence) 4

OA3 Followup of Events and Notices of Enforcement Discretion (71153 - One sample)

.1 Manual Scram due to EPR Failure a. Inspection Scope On October 23 at about 9:00 p.m., Unit 1 operators began to observe small oscillations in

reactor pressure. They attempted to transfer pressure control from the electronic

pressure regulator (EPR) to the mechanical pressure regulator (MPR) in accordance with

N1-SOP-31.2, "Pressure Regulator Malfunctions;" however, the EPR would not

disengage. At 9:26 p.m., when the pressure oscillations had turned into a decreasing

trend in pressure, operators manually scrammed the reactor. Following the scram, reactor vessel water level shrank to 36 inches (an expected

response to a scram) and operators entered

EOP -2, "

RPV Control." The high pressure

coolant injection system initiated to restore normal water level. Following the main turbine

trip, all of the turbine bypass valves (TBVs) opened and remained open due to the

EPR failure. To regain pressure control, the operators closed the
MS [[]]

IVs at 9:28 p.m. Several

minutes later, the

EPR disengaged and pressure control transferred to the
MPR. The
TBV s closed, allowing operators to reopen the

MSIVs. A normal plant cooldown to cold

shutdown was then commenced using the TBVs. Cold shutdown conditions were

achieved on October 24 at 9:32 a.m. The inspectors responded to the control room and observed operators' responses to the

event. The inspectors verified that operators responded in accordance with the applicable

procedures. The inspectors confirmed that no emergency plan emergency action level

thresholds had been exceeded and that the event was appropriately reported to the NRC. The inspectors reviewed the circumstances surrounding the event. The inspectors

monitored troubleshooting activities and corrective actions through attendance of outage

update meetings, discussions with plant personnel, and review of records, including the

post-scram review.

26b. Findings No findings of significance were identified. 4OA5 Other Activities .1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with

NMP [[]]

NS's

security procedures and regulatory requirements relating to nuclear plant security. These

observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors' normal plant status review and inspection activities.

b. Findings No findings of significance were identified.

.2 Temporary Instruction (TI) 2515/176 - Emergency Diesel Generator TS Surveillance Requirements Regarding Endurance and Margin Testing

a. Inspection Scope The objective of

TI 2515/176, "

EDG TS Surveillance Requirements Regarding Endurance

and Margin Testing," is to gather information to assess the adequacy of nuclear power

plant

EDG endurance and margin testing as prescribed in plant-specific

TS. The

inspectors reviewed EDG ratings, design basis event load calculations, surveillance

testing requirements and EDG vendor specifications, and gathered information in

accordance with TI 2515/176.

The inspectors' assessment and information gathered while completing this TI was

discussed with licensee personnel. This information was forwarded to the Office of

Nuclear Reactor Regulation for further review and evaluation.

b. Findings

No findings of significance were identified. 4OA6 Meetings, including Exit Exit Meeting Summary

27 The inspectors presented the inspection results to Mr. Keith Polson and other members of

NMPNS management on January 23, 2009.

NMPNS acknowledged that no proprietary

information was involved.

ATTACH [[]]
MENT [[:]]
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION A-1
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION [[]]
KEY [[]]
POINTS [[]]
OF [[]]

CONTACT Licensee Personnel

K. Polson, Vice President

P. Bartolini, Supervisor, Mechanical Engineering

S. Belcher, Plant Manager

W. Byrne, Manager, Nuclear Security

R. Dean, Director, Quality and Performance Assessment
C. Fisher, Senior Engineer (

MSPI Coordinator)

J. Kaminski, Manager, Emergency Preparedness

J. Krakuszeski, Manager, Operations

J. Laughlin, Manager, Engineering Services

C. Nielsen, Supervisor, Engineering

T. Shortell, Manager, Training

S. Sova, Manager, Radiation Protection

H. Strahley, Unit 2 General Supervisor Operations

T. Syrell, Director, Licensing

J. Torbitt, Assistant Operations Manager P. Walsh, Shift Manager (Operator Workaround Coordinator)
LIST [[]]
OF [[]]
ITEMS [[]]
OPENED ,
CLOSED ,
AND [[]]
DISCUS [[]]

SED Opened

05000410/2008005-02

URI Qualification of

HPCS Power Cables for

Submergence (Section 4OA2)

Opened and Closed 05000410/2008005-01

NCV Untimely Corrective Action for Degraded Service Water Pumps (Section 13)
LIST [[]]
OF [[]]
DOCUME [[]]
NTS [[]]
REVIEW [[]]
ED Section 1R01: Adverse Weather Protection
EPIP -

EPP-26, "Natural Hazard Preparation and Recovery," Revision 01

N1-OP-64, "Meteorological Monitoring," Revision 01

A-2N2-OP-102, "Meteorological Monitoring," Revision

04 NAI -
PSH -11, "Seasonal Readiness Program," Revision 04
NRC [[]]

IE Bulletin No. 79-24, "Frozen Lines"

NRC Information Notice 96-36, "Degradation of Cooling Water Systems Due to Icing"
NRC Information Notice 98-02, "Nuclear Power Plant Cold Weather Problems and Protective Measures" Section 1R04: Equipment Alignment N1-

OP-14, "Containment Spray System," Revision 04301

C-18012, "Reactor Containment Spray Raw Water System P&I Diagram," Revision 25

N2-OP-100A, Standby Diesel Generators," Revision 09

N2-VLU-01, "Walkdown Order Valve Lineup and Valve Operations," Revision 00, Attachment 100A, "N2-OP-100A Walkdown Valve Lineup" N2-OP-35, "Reactor Core Isolation Cooling," Revision 07

N2-VLU-01, "Walkdown Order Valve Lineup and Valve Operations," Revision 00, Attachment 35, "N2-OP-35 Walkdown Valve Lineup" Section 1R05: Fire Protection Unit

1 UFS [[]]

AR, Appendix 10A, "Fire Hazards Analysis"

Unit

2 UFS [[]]
AR , Appendix 9A, "Degree of Compliance with Branch Technical Position
CM [[]]

EB 9.5-1"

Unit

2 UFS [[]]

AR, Appendix 9B, "Safe Shutdown Evaluation"

N2-FPI-PFP-0201, "Unit 2 Pre-Fire Plans," Revision 0

Section 1R11: Licensed Operator Requalification Program Quarterly Review N1-SOP-1.4, "Stuck Open ERV," Revision 01

N1-SOP-1, "Reactor Scram," Revision 01900

N1-EOP-2, "RPV Control," Revision 01400

N1-EOP-4, "Primary Containment Control," Revision 01400

N2-SOP-23, "EHC Pressure Regulator Failure," Revision 05

N2-SOP-08, "Unplanned Power Changes," Revision 05

N2-SOP-13, "Loss or Degraded CCP System," Revision 02

N2-SOP-101C, "Reactor Scram," Revision 03

N2-SOP-34, "Stuck Open Safety Relief Valve," Revision 04

N2-EOP-RPV, "RPV Control," Revision 01200

N2-EOP-PC, "Primary Containment Control," Revision 12

N2-EOP-C2, "RPV Blowdown," Revision 11

Biennial Review

NMP -

TR-1.01-22, "License Operator Requalification Exam Writers Guide," Revision 00401

S102-CY0807OE Cycle 0807 Selected Operating Experience

Feedback Notebook -

CY 0807
NMP -

TR-1.01-40, Attachment 4, "Evaluation Failure Action Plan," Revision 03

A-3NMP-TR-1.01-40, "Implementation Phase Activities," Revision

04 CNG -

TR-1.01-1005, "Implementation Phase Activities," Revision 02

N2-215003-RBO-03 - Power Range Neutron Monitoring System & Rod Block Monitor

N2-242001-RBO-02 - Auxiliary Steam System

2102-CY0807C01E,

2TME -

PIC122 Controller Training

S-SAF-16, "Schedule, Perform, Process, and Transmit Results for Physical Examinations on Licensed Reactor Operator and License Candidate," Revision 06 CR 2007-2380

CR 2006-545

CR 2007-5266

CR 2006-5646

Simulator Testing:

2007 Annual

AN [[]]

SI Testing Real Time Test

Operating Limits Exceeded Test

Normal Operating Tests Steady State Tests

Transient Tests (10)

Reactivity Manipulation Certification

Scenario Based Testing: Control Rod Drive System

Reactor Recirculation System

Shutdown Cooling System

Plant Shutdown and Cooldown from Power Operations

Main Power Scenario

Emergency Cooling System

Emergency AC Distribution Scenario

N1-SOP-1 Reactor Scram

N1-SOP-31.1 Turbine Trip

NRC Scenario 1, 2/27/07

NRC Scenario 2, 2/27/07

NRC Scenario 3, 9/19/06

NRC Scenario 4, 2/27/07

Section 1R12: Maintenance Effectiveness S-MRM-REL-0101, "Maintenance Rule," Revision 18

S-MRM-REL-0104, "Maintenance Rule Scope," Revision 01

S-MRM-REL-0105, "Maintenance Rule Performance Criteria," Revision 01

Maintenance Rule Expert Panel Meeting Record, March 14, 2008

Unit

2 RCIC System Report, 4th Quarter 2008 Unit 2

RCIC Maintenance Rule Scoping Document

A-4Section 1R13: Maintenance Risk Assessments and Emergent Work Control

GAP -
OPS -117, "Integrated Risk Management," Revision 14
GAP -
PSH -03, "Control of On-line Work Activities," Revision 15
NAI -

PSH-03, "On-line Work Management Process," Revision 11

Section 1R15: Operability Evaluations

CNG -

OP-1.01-1002, "Conduct of Operability Determinations / Functionality Assessments,"

Revision 00

N1-SOP-29.1, "EOP Key Parameter - Alternate Instrumentation," Revision 01

Section 1R18: Plant Modifications N2-08-059, "Instrument Air Header Hot Tap Blow Down Valve," Revision 00

Section 1R19: Post Maintenance Testing

GAP -

SAT-02, "Pre/Post Maintenance Test Requirements," Revision 26

Section 1R20: Refueling and Other Outage Activities N1-OP-43C, "Plant Shutdown," Revision 02

N1-OP-4, "Shutdown Cooling System," Revision 02701

NMP Unit 1 Post Scram Review for scram 08-01 on October 23, 2008

N2-OP-101C, Plant Shutdown, Revision 18

N2-OP-31, Residual Heat Removal System, Revision 18

Shutdown Safety Review Report for Unit 2 Outage 2P801

NIP -

OUT-01, "Shutdown Safety," Revision 02400

Section 1R22: Surveillance Testing

CNG -
HU -1.01, "Human Performance Program," Revision 01
CNG -
HU -1.01-1000, "Human Performance," Revision 02
CNG -
HU -1.01-1001, "Human Performance Tools and Verification Practices," Revision 02
CNG -
HU -1.01-1002, "Pre-Job Briefings and Post-Job Critiques," Revision 02
GAP -
SAT -01, "ST Program," Revision 16
GAP -

OPS-117, "Integrated Risk Management," Revision 14

Section

2OS 1: Access Control to Radiologically Significant Areas

QPA Quarterly Reports: First Quarter 2008; Second Quarter 2008; Third Quarter 2008

QPA Assessment Reports: Radiation Protection Practices; Unit 2 Radiologically Controlled Area Egress; Radiography of the Unit 2 Stator Cooling Water System; Radiation

Protection Technician Training Program Effectiveness Quarterly Performance Review Report - Radiation Protection: March 2008; June 2008;

September 2008

A-5Snapshot Assessments High Radiation Area Barricades and Controls

Gaps to Excellence for High Radiation Control

Radiography Controls

RFO-11 Personnel Contamination Events

Documentation of the Radiation Protection Vertical Slice Presentation Section

2OS 2:
ALARA Planning and Controls
QPA Assessment Reports: Source Term Reduction; Source Term Reduction Meetings Snapshot Assessment -
ALARA Self-Assessment Effectiveness Review Section
2OS 3: Radiation Monitoring Instrumentation and Protective Equipment

QPA Assessment Report - Calibration of Unit 2 Main Control Room Ventilation Radiation Monitors

Self-Assessment FSA-2008-0036-07, Respiratory Protection, Calibration and Surveillances,

and Control of Radioactive Material, Sources, and Contaminations

Snapshot Assessments: Knowledge Transfer and Retention for Dosimetry; Documentation of

Air Sample Analysis during mid cycle outage 2F702 Section

2PS 2: Radioactive Material Processing and Transportation Unit 2 Radwaste

PCP, Revision 7, 6/26/08 Unit 1 Radwaste PCP, Revision 8, 4/11/07

Focused Self Assessment 2007-26, "Radioactive Materials Shipping"

Mid-Cycle Focused Self-Assessment Report, August 20-24, 2007

QPA ; 08-123]]
GET -
IFRWT -R1-C0, "Industry and Fleet Radiation Worker Training," Revision 1, Change 0
RPT -004, "Movement/Storage of Radioactive Material (

NS202RPT004Q01)," Revision 0

S202-CT0703C06, "2007 Cycle 3 Toolbox Training"

S202-CT0802C05, "Movement and Storage of RAM Refresher"

S202-CT0803C03, "Guidance for Loading Radioactive Equipment into Containers for Transport Offsite"

S000-49CFRS-QPA, "Function Specific Training for QPA"

Areva

NP , Inc. 10

CFR Part 50/61 Analysis Reports: 2006 Unit 2 Plant Smears; 2007 Unit 2 Plant Smears; 2006 Unit 2 Condenser Resins; 2007 Unit 2 Condenser Resins; 2006

Unit 1 Filter Sludge; 2007 Unit 1 Iron Prefilter; 2007 Unit 1 Cleanup Resin; 2007 Unit 1

Carbon; 2006 Unit

1 SS [[]]

CV; 2006 Unit 1 Condenser Resin; 2007 Unit 1 Condenser

Resin; 2006 Unit 1 Plant Smears; 2007 Unit 1 Plant Smears Radioactive Material Shipping Records: 08-1074; 08-1090; 08-1145; 08-2011; 08-2038 Section

4OA 1: Performance Indicator Verification 2007/2008
MSPI Submittal Data for Units 1 and 2 2008 System Health Reports for Unit
1 EDG ,
HPCI ,
IC ,
RHR , and
SC [[]]
WS 2008 System Health Reports for Unit
2 EDG ,
HPCS ,
RCIC ,

RHR, and

SW A-6CNG-NL-1.01-1010, "NRC and
INPO Performance Indicator Reporting," Revision 00201
MSPI -1, "Nine Mile Point Unit
1 MS [[]]
PI Basis Document," Revision 01
MSPI -2, "Nine Mile Point Unit 2

MSPI Basis Document," Revision 01

N2-OP-13, "Reactor Building Closed Loop Cooling System," Revision 07

NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5
NRC [[]]
MSPI Report for Nine Mile Point Units 1 and 2 Section
4OA 2: Identification and Resolution of Problems Operator Workarounds 10

CFR 50.59 Screening Form for N1-OP-4, "Shutdown Cooling System"

CR 2004-3921

N1-OP-04, "Shutdown Cooling System," Revision 26

NAI -
REL -02 Second Quarter 2008 Review, dated July 17, 2008
NAI -

REL-02, "Control of Operator Workarounds, Burdens, and Interests," Revision 07

Nine Mile Point Performance Indicators for Operator Workaround Backlog, Control Room Deficiency Backlog, and Operations Compensatory Measure Backlog Unit 1 Control Room Deficiency and Defeated Annunciator Logs

Unit 1 Open Operability Determination Log

Unit 1 Operator Workaround / Burden / Items of Interest List

Unit 2 Control Room Deficiency Log

Unit 2 Open Operability Determination Log

Unit 2 Operator Workaround / Burden / Items of Interest List

Trend Review Second Quarter Performance Reviews for Work Management, Radiation Protection, Operations, Maintenance, Chemistry, and Training Third Quarter Performance Reviews for Chemistry, Engineering, Maintenance, and Radiation Protection

NAI -

ECA-24, "Performance Improvement Process," Revision 01

Condition Reports 2007-0962 2007-5322

2007-7659

2007-7660

2007-7661

2007-7739

2008-2021

2008-2683

2008-4651

2008-8875

2008-8832

2008-8813

2008-8810

2008-8786 2008-8660 2008-8623

2008-7910

2008-7850

2008-7839

2008-7377

2008-7149

2008-7124

2008-6645

2008-6491

2008-6286

2008-5931

2008-5869

2008-5731 2008-5350 2008-4562

2008-4118

2008-6983

2008-3949

2008-3738

2008-3592

2008-3531

2008-3439

2008-3237

2008-2945

2008-2672

2008-2428

2008-2297

A-72008-2121 2008-2027

2008-1996

2008-1891

2008-1812

2008-1696

2008-1604

2008-1142

2008-1114

2008-0913

2008-0734

2008-0310

2008-9024

2008-4466

2008-4999

2008-0086

2008-0470

2008-1011 2008-1591 2008-1697

2008-1907

2008-2354

2008-2842

2008-3173

2008-3251

2008-3984

2008-4003

2008-4219

2008-4515

2008-4516

2008-5720

2008-6246

2008-6934

2008-7022

2008-8509

2008-5382 2008-6368 2008-8985

2008-8231

2008-8680

2008-8851

2008-8753

2008-8492

2008-8547

2008-7842

2008-7891

2008-7893

2008-7550

2008-8016

2008-8270

2008-5398

Section

4OA 5: Other Activities Calculations 4.16

KVACDGES, "Diesel Generator Loading (Unit 1)," Revision 06

E-32, "Diesel Generator Loading," Revision 12

Procedures N1-TTP-DGE-R01, "Diesel Generator Load Testing," Revision 02

N1-OP-45, "Emergency Diesel Generators," Revision 26

N1-ST-M4A, "Emergency Diesel Generator 102 and PB 102 Operability Test," Revision 02

N1-ST-M4B, "Emergency Diesel Generator 103 and PB 103 Operability Test," Revision 02

N1-ST-R2, "LOCA and EDG Simulated Auto Initiation Test," Revision 27

N1-SOP-33A.1, "Loss of 115KV," Revision 01

N2-OP-100A, "High Pressure Core Spray (HPCS) Diesel Generator," Revision 08

N2-OP-100B, "Standby Diesel Generators," Revision 09

N-2-OSP-EGS-R002, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division I and

II ," Revision 04 N-2-

OSP-EGS-R006, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division III," Revision 05

Completed Surveillances N1-TTP-DGE-R01, "Diesel Generator (102) Load Testing," Revision 02, dated 03/29/03

N1-TTP-DGE-R01, "Diesel Generator (102) Load Testing," Revision 02, dated 04/09/05

N1-TTP-DGE-R01, "Diesel Generator (102) Load Testing," Revision 02, dated 03/25/07

N1-TTP-DGE-R01, "Diesel Generator (103) Load Testing," Revision 01, dated 03/23/03

N1-TTP-DGE-R01, "Diesel Generator (103) Load Testing," Revision 02, dated 04/02/05

N1-TTP-DGE-R01, "Diesel Generator (103) Load Testing," Revision 02, dated 03/29/07

N-2-OSP-EGS-R002, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection

A-8Test Division I and

II ," Revision 04, dated 05/07/02 (Division I) N-2-
OSP -EGS-R002, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division I and
II ," Revision 04, dated 05/03/04 (Division I) N-2-
OSP -EGS-R002, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division I and
II ," Revision 04, dated 10/17/06 (Division I) N-2-
OSP -EGS-R002, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division I and
II ," Revision 04, dated 05/15/08 (Division I) N-2-
OSP -EGS-R002, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division I and
II ," Revision 04, dated 10/06/04 (Division
II ) N-2-OSP-EGS-R002, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division I and
II ," Revision 04, dated 12/05/06 (Division
II ) N-2-OSP-EGS-R002, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division I and
II ," Revision 04, dated 01/02/08(Division I) N-2-
OSP -EGS-R006, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division
III ," Revision 05, dated 06/11/04 N-2-
OSP -EGS-R006, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division
III ," Revision 05, dated 10/25/06 N-2-

OSP-EGS-R006, "Operating Cycle Diesel Generator 24 Hr Run and Load Rejection Test Division III," Revision 05, dated 07/24/08

Drawings 3-N2.1-E21.2, "Elementary Wiring Diagram - 4.16 KV Emergency Power Boards & Diesel Generators #102 & #103," Revision 25

Other Documents

SD [[]]

BD-804, "Emergency Diesel Generator System," Revision 04

N10197, Electromotive Division, Maintenance Instructions

N20395, "KSV Diesel Generator Instruction Manual," Revision 43

N20424, "Instruction Manual

HP [[]]

CS Diesel Generator," Volumes 1 through 4, Revision 32

Unit

1 UFS [[]]

AR, Revision 20

Unit 1 & 2 Technical Specifications

Regulatory Guide 1.9, "Application and Testing of Safety-Related Diesel Generators in Nuclear

Power Plants," Revision 4

IE [[]]

EE 387-1984, "Standard Criteria for Diesel-Generator Units Applied as Standby Power Supplies for Nuclear Power Generating Stations"

Attachment

LIST [[]]
OF [[]]
ACRONY [[]]
MS AC alternating current
ADA [[]]
MS Agencywide Documents Access and Management System
ALA [[]]

RA as low as reasonably achievable

CAP corrective action program

CB control building

CFR Code of Federal Regulations

CR condition report

DBD design basis document

DOT Department of Transportation

EDG emergency diesel generator

EOP emergency operating procedure

EPR electronic pressure regulator

F Fahrenheit

GL Generic Letter
HPCS high pressure core spray

IMC inspection manual chapter

JPM job performance measure

kV kilovolt

LDE lens dose equivalent

LER licensee event report
LO [[]]
RT licensed operator requalification training
LP [[]]
CI low pressure coolant injection
LP [[]]

CS low pressure core spray

MPR mechanical pressure regulator

mrem millirem

MS [[]]
IV main steam isolation valve
MS [[]]

PI mitigating system performance indicator

NCV non-cited violation

NEI Nuclear Energy Institute
NMPNS Nine Mile Point Nuclear Station,
LLC NRC Nuclear Regulatory Commission
PA [[]]

RS Publicly Available Records

PCP process control program

PI performance indicator

PI&R problem identification and resolution

PMT post maintenance test

qtr quarter

RC [[]]

IC reactor core isolation cooling

RHR residual heat removal

R/hr rad per hour

RPV reactor pressure vessel

RTP rated thermal power

SDE skin dose equivalent

SDP significance determination process

SOP special operating procedure

Attachment

SW service water
TBV turbine bypass valve
TE [[]]

DE total effective dose equivalent

TI temporary instruction

TS technical specification
UFS [[]]

AR updated final safety analysis report

URI unresolved item

WO work order