ML19253B609

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LER 79-085/03L-0:on 790915,while in Mode 1,control Rod Partially Dropped.Cause Unknown.Rod Withdrawn to Group Average Position.No Further Corrective Action Deemed Necessary
ML19253B609
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 10/08/1979
From: Cooper J
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19253B608 List:
References
LER-79-085-03L, LER-79-85-3L, NUDOCS 7910160488
Download: ML19253B609 (2)


Text

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I g ,$r 1620 in Mode 1, it was reported that control rod 07-07 partially drooped This created an event contrary to Technig

,, ,from 41*. withdrawn to 18% withdrawn.

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, o (The cause of this event is unknown. Reactor power was reduced to 60%. Rod 07-07 was pulled from 10% to 25% and position was verified-by zone reference at 25%.i L'_E.J l

, , g Rod 07-07 was withdrawn to its group average position. No further corrective actt-ion deemed necessary. l

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SUPPLEMENTARY INFORMATION Report No.: 50-302/79-085/03L-0 Facility: Crystal River Unit #3 Report Date: 8 October 1979 Occurrence Date: 15 September 1979 Identification of Occurrence:

Control rod 07-07 greater than 6.5% (indicated position) away from group average position.

Conditions Prior to Occurrence:

Mode 1 power operation (72%)

Description of 0 warra.ce:

At 1620 it was reported that rod 07-07 had dropped from 41%

withdrawn to 18% withdrawn. This event resulted in a step drop in reactor power of 3%. Reactor power was reduced to 60%. Rod 07-07 was transferred to the auxiliary power supply and withdrawn to 25% by absolute position indication. Rod 07-07 position was verified at 25% on zone reference lamps.

The rod was withdrawn to its average group position and power was returned to its normal supply.

Designation of Apparent Cause:

The cause of this event is unknown. Troubleshooting of the control rod power supply revealed no immediate cause of this event.

Analysis of Occurrence:

No effect upon the plant or general public.

Corrective Action:

No corrective action deemed necessary.

Failure Data:

This is the fifth occurrence of this type reported. Reference LER's 77-34, 43, 47, and 135.

/rc 1!S4 555