ML17272A759
ML17272A759 | |
Person / Time | |
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Site: | Susquehanna, Columbia |
Issue date: | 11/30/1979 |
From: | WASHINGTON PUBLIC POWER SUPPLY SYSTEM |
To: | |
Shared Package | |
ML17272A757 | List: |
References | |
NUDOCS 7912280651 | |
Download: ML17272A759 (2) | |
Similar Documents at Susquehanna, Columbia | |
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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML17292B5341999-01-15015 January 1999
[Table view]Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20198E0631998-01-0707 January 1998 Part 21 Rept Re Shipment by Dubose National Energy Svcs,Inc, of 40 Pieces of 4 inch,90 Degree Elbows Which Did Not Meet ASME Section II SA-234 Requirements ML20140A9661997-05-29029 May 1997 Part 21 Rept Re Ksv Emergency Diesel Generator Power Piston Failure.Caused by Jacket Water in Combustion Chamber. Recommends That Users Verify That Crown Thickness at Valve Cutout Be 100 Minimum ML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20137G6261997-03-25025 March 1997 Svcs Part 21 Rept Re Emergency Generators Installed at Zion Station Which Developed Significant Drop in Crankcase Lube Oil Level.Caused by Crack in Liner Wall,Allowing Jacket Water to Enter Chamber ML20117G4641996-05-14014 May 1996 Part 21 Rept Re Cooper Bessemer Reciprocating Products,Div of Cooper Cameron Corp,Issued Ltr to Define Utils/Plants Containing Similar Equipment as Supplied on Cooper Bessemer Ksv & Enterprise Dsr EDGs ML17292A2141996-05-0808 May 1996 Part 21 Rept Re Capscrews Supplied to Wppss by Now Defunct Cardinal Industrial Products,Lp (CIP) Having Nonconforming Hardness.Failed Lots & Any Remaining Product Found to Have Been Heat Treated by CIP Scrapped & Removed from Premises ML20094M6251995-11-21021 November 1995 Final Part 21 Rept of Investigation & Analysis of Suspect Fasteners Event 29257.B&G-Cardinal Discontinued Using Heat Treatment Equipment at Cardinal Facility Until Such Time That Satisfactory Mods Made to Hardware & Procedures ML17291A2571994-07-22022 July 1994 Part 21 Rept Re Westinghouse Containment Penetration Modules Scotchcast Strain Relief & Varglas Insulated Conductors. Replaced Six of 12 RPIS Scotchcast/Varglas Modules & Three Scotchcast/Okonite Modules During Refueling Outage (R-9) ML17291A2351994-07-15015 July 1994 Deficiency Rept Re Material Defects in Facility Containment Penetration Modules.Initially Reported on 940715.Modules Were Replaced ML17290B2001994-05-26026 May 1994 Part 21 Rept Re Automatic Switch Co Replacement Solenoid Pilot Valve Diaphragms Supplied by GE Nuclear Energy.Unusual Combination of Scram Soleniod Pilot Valve Pressure & Exhaust Diaphragm Degradation Caused Failure of Rod to Scram ML20044G5311993-05-26026 May 1993 Suppl to 921207 Part 21 Rept Re Declutch Sys Anomaly in Certain Types of Valve Actuators Supplied by Limitorque Corp.Limitorque Designed New Declutch Lever Which Will Be Available in First Quarter 1993 ML20044G5011993-05-26026 May 1993 Part 21 Rept Re Buffer Amplifier Modules Mfg by Bailey Controls Co Containing Suspect Negative Ref Power Supply Having Safety Implications.Caused by Design Error in Circuitry.Modules Would Not Result in Miscalibration ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126D7211992-12-16016 December 1992 Potential Part 21 Rept Re Actual Performance of Rosemount Supplied Bailey Bq Differential Pressure Transmitters Differing from Rosemount Original Spec.Bailey Controls Encl.Evaluation Not Yet Performed ML18017A0421992-12-14014 December 1992 Suppl to 921127 Part 21 Rept Re High Air Concentration in Reactor Bldg Making Area Uninhabitable for Retrieving Air Filters,Per NUREG-0737,Item II.F.1.Util Current Position Re Fuel Pool Cooling Issues Contrary to Reg Guide 1.3 ML18026A2481992-11-27027 November 1992 Part 21 Rept Re Substantial Safety Hazard in Design of Facility for Loss of Normal Spent Fuel Pool Cooling ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML17289A8241992-08-14014 August 1992 Part 21 Rept Re Undersized Yoke Clamps on Three HPCS motor- Operated Valves Supplied by Anchor/Darling Valve Co.Nde Will Be Performed on All Clamps to Determine If Condition Affects Valve Operability.Clamps to Be Replaced by 921031 ML17289A8061992-08-14014 August 1992 Part 21 Rept Re Undersized Yoke Clamps in Three Anchor Darling HPCS motor-operated Valves.Clamps Located on Return Lines to Condensate Storage Tanks & Suppression Pool.Clamps Will Be Replaced by Util by 921031 ML17289A7991992-08-13013 August 1992 Part 21 Rept Re Limitorque Failure to Use Grade 5 Housing Cap to motor-operator Housing,Per Generic Ltr 89-10. Initially Reported on 920730.Seven GL 89-10 Category Valves Could Have Failed Due to Condition ML17289A7721992-08-0606 August 1992 Interim Part 21 Rept Re Discrepancy in Procedure Used by Siemens Nuclear Power Corp to Analyze Feedwater Controller Failure Event w/COTRANSA2 Computer Code.Initially Reported on 920709.Analysis for Cycle 8 Revised & Incorporated ML17289A7851992-07-30030 July 1992 Part 21 Rept 23965:on 920730,determined That Limitorque motor-operators Had Upper Housing Cover Cap Screws Set at 100% of Mfg Rated Thrust Which Could Fail in Svc.Caused by Installation of Grade 1 or 2 Instead of Grade 5 or 7 Screws ML17289A7521992-07-0909 July 1992 Part 21 Rept Re Discrepancy in Procedure Used to Analyze Feedwater Controller Failure Event Using COTRANSA2 Code. Initially Reported by Siemens Nuclear Power Corp on 920617. Caused by Transient Analysis Error ML17289A8591992-07-0808 July 1992 Part 21 Rept Re Delta CPR Transient Analysis Error for Feedwater Controller Failure Event Performed by Siemens Nuclear Power Corp.Feedwater Transient Actually Occurred on 911119.Fuel Cladding Failure Not Possible ML17289A6971992-06-26026 June 1992 Amend 1 to Part 21 Rept 158 Re gear-wear Induced Failures in engine-driven Jacket Water Pump in DSRV-16-4 Standby DG Sys. Initially Reported on 911029.Grand Gulf Station Observed Wear Characteristics in as Little as 500 Operating Hours ML17286B2501991-11-14014 November 1991 Part 21 Rept Re Potential Deficiency W/Asl Dry Type Transformers.Initially Reported on 910610.Recommends Issue Be Pursued W/Abb Since Westinghouse Did Not Have Necessary Technical Info or Expertise to Identify Cause or Solution ML20079B8591991-06-10010 June 1991 Interim Deviation/Noncompliance Rept 067 Re dry-type Insulator Cracking in Transformer Supplied by Westinghouse.Initially Reported on 910513.Util Notified Vendor on 910430 That Problem Affects Class 1E Transformer ML19325C9521989-09-29029 September 1989 Part 21 Rept Re Potential Common Failure of SMB-000 & SMB-00 Cam Type Torque Switches Supplied Prior to 1981 & 1976. Vendor Recommends That Switch W/Fiber Spacer Be Replaced ML20248E0121989-09-13013 September 1989 Supplemental Part 21 Rept Re Potential Problem W/Six Specific Engine Control Devices in Air Start,Lube Oil, Jacket Water & Crankcase Sys.Initially Reported on 890429. California Controls Co Will Redesign Valve Seating GO2-89-144, Part 21 Rept Re Defect in Fault Tripping Design for Class 1E safety-related 480 Volt Divs 1 & 2 Ac Power Distribution Sys for Motor Control Ctrs.Caused by Improperly Designed Volt Electrical Distribution Sys.Circuit Breakers Replaced1989-08-21021 August 1989 Part 21 Rept Re Defect in Fault Tripping Design for Class 1E safety-related 480 Volt Divs 1 & 2 Ac Power Distribution Sys for Motor Control Ctrs.Caused by Improperly Designed Volt Electrical Distribution Sys.Circuit Breakers Replaced ML17285A5001989-06-0202 June 1989 Part 21 Rept Re Defect Discovered in Valve Motor Operator of RCIC Inboard Containment Isolation Valve RCIC-V-63.Upper Housing Cover Will Be Machined to Remove Excess Matl to Provide Required Recess ML17285A4771989-05-19019 May 1989 Part 21 Rept Re Defects in Target Rock Actuator Kits (Part 300562-1).Initially Reported on 890516.Defects Noted in Cold Solder Condition,Insufficient Solder Joints & Failed Solder Joints.Defective Kits Returned to Mfg for Repair ML17285A4321989-04-26026 April 1989 Part 21 Rept Re Defect in Limitorque Valve Motor Operator Model SMB-2 W/Soft Worm Shaft Clutch Gear Assembly.Caused by Failure to Install Split Spacer of Worm Shaft Clutch Gear assembly.Safety-related Valves Manually Operated ML20205F3211988-10-10010 October 1988 Part 21 Rept Re Potential Deviation from Tech Spec Concerning Ry Indicators Due to Operating Temp Effect on Analog Meter Movement.Initially Reported on 881006.Customers Verbally Notified on 881006-07 ML20154J4101988-05-12012 May 1988 Addendum 1 to Supplemental Part 21 Rept 145 Re Potential Problem w/F-573-156 Pressure Sensor/Lube Oil Trip.Initially Reported on 880429.Addl 1-1/8-inch Diameter W/Deep Counterbone in Pressure Head Added to Activate Valve ML20153B6191988-04-29029 April 1988 Part 21 Rept Re Potential Defect in Component of Dsr or Dsrv Standby Diesel Generators Supplied to Utils.Recommends Return of Subj Components in Onsite Warehouse Storage & Suggests Surveillance of Devices Already Installed ML20211P7211987-02-23023 February 1987 Part 21 Rept Re Rockbestos Coaxial Cable Used in Sorrento Electronics Digital & Analog high-range Radiation Monitor. Insulation Resistance at High Temp Not High Enough for Ion Chamber & Associated Electronics to Operate Properly ML20212E5631986-12-19019 December 1986 Part 21 Rept Re Valve Problem.Houghto 620 Lubricant Attacks & Degrades Aluminum in Valves.Valves Have Been or Being Rebuilt ML20212A5601986-12-17017 December 1986 Part 21 Rept Re Amplified Response Spectra.Applicable Floor & Wall Mounted safety-related Equipment Reviewed & as-built Geometry & Mass of Seismic Category I Structures Compared to Original Use in Generating Amplified Response Spectra ML20215G5351986-10-10010 October 1986 Part 21 Rept Re Vendor Tests of air-operated Diaphragm Valves Revealing Natural Frequencies Less than Required Values of 33 Hz.Initially Reported on 841227.No Adverse Effects Noted During Testing ML20215G6801986-10-10010 October 1986 Part 21 Rept Re Vendor Tests of air-operated Diaphragm Valves Revealing Natural Frequencies Less than Required Values of 33 Hz.Initially Reported on 841227.No Adverse Effects Noted During Testing ML20215B9681986-09-26026 September 1986 Part 21 & Deficiency Rept Re Synchro-Start Type Essb Speed Switches.Initially Reported on 860822.Speed Switches Currently in Svc or Designated for Svc Will Be Tested for Relay Contact Closure & Relay Contact Condition ML20210F4741986-09-16016 September 1986 Part 21 Rept Re Possible Sticking in Closed or Partially Open Position on Dresser 3050 Diaphragm Valves.Initially Reported on 850118.Disc Caps,Including Chamfers on Outside Diameter,Will Be Modified ML20203F6471986-07-23023 July 1986 Part 21 Rept Re Morrison-Knudsen Undersized Welds at Plant. Initially Reported on 860630.Study Concluded That Welds Not Cause for Failure of Plant.Welds Will Be Repaired by Vendor ML20206S0841986-06-30030 June 1986 Part 21 Rept Re Possible Cut Wires in Wire Harness of Bbc Brown Boveri K600/K800 Circuit Breakers.Initially Reported on 860509.Safety Implications Listed.Gear Guard Designed to Prevent Cut Wires ML20195E4881986-05-23023 May 1986 Part 21 Rept Re Potential Failure of Ite/Gould Disconnect Switch,Type 7860 Ds Series.Instructions for Verification of Proper Operation of Switches Included in Notification to Plants.New Switches Available by 860901 1999-01-15 Category:TEXT-SAFETY REPORT MONTHYEARML17284A9001999-10-31031 October 1999
[Table view]Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17146B1741999-08-0303 August 1999 GL 96-06 Risk Assessment for Sses. ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML20206D3331999-04-27027 April 1999 SER of Individual Plant Examination of External Events Submittal on Susquehanna Steam Electric Station,Units 1 & 2. Staff Notes That Licensee IPEEE Complete with Regard to Info Requested by Suppl 4 to GL 88-20 ML20195B2381999-03-31031 March 1999 Redacted Version for 10CFR2.790 Request for Decommissioning Status Rept for Sses,Units 1 & 2 ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17164A8451998-10-31031 October 1998 SSES Unit 1 Tenth Refueling & Insp Outage ISI Outage Summary Rept. ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML20217Q4891998-04-21021 April 1998 Rev 1 to Draft LDCN 2482, FSAR Chapter 13.4 & FSAR Chapter 17.2 Changes to Support ITS Implementation ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D 1999-09-30 |
Text
Attachment REPORTABLE DEFICIENCY AND CORRECTIVE ACTION
, ECCS PUMP ROOM FLOODING DUE TO .
FUEL POOL BOIL-OFF Descri tion of the Deficienc During a LOCA or after a safe shutdown earthquake (SSE) the spent fuel pool cooling system is assumed to fail because it is not designed to Seismic Category I standards, nor is it Class 1E. Eventually, the fuel pool will begin to boil, with the vapor condensing on walls and floors.
This condensate (maximum of 18 gpm) will end up in the floor drain system. All the sumps in the Reactor Building floor drain system are located in the Emergency Core Cooling System (ECCS) pump rooms. Because the Reactor Building sump pump system is not Seismic Category I nor Class 1E, it cannot be counted on to pump out the ECCS pump rooms. Even though Class lE instrumentation is available within each ECCS pump room to tell the operator that the room is flooding, there is no way to stop the source of flooding (fuel pool boiling), to isolate the ECCS pump rooms from the condensate, and pump out the ECCS pump rooms post-LOCA Eventually, the ECCS pump rooms will flood, shorting out ECCS oi'ost-SSE.
pumps.
Safet Im lications Loss of any ECCS pump, post-LOCA, due to flooding from fuel pool boiloff could reduce the number of core cooling pumps below the minimum required to keep the core covered and to keep the suppression pool cool.
Corrective Action Taken The Fuel Pool Cooling System wil be upgraded through reanalysis and redesign to improve reliability. The system will be analyzed to Seismic Category I cri teria and modifi cations will include the addition of a safety grade heat sink and emergency power supply.
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