ML18153A314

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Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610
ML18153A314
Person / Time
Site: Surry  Dominion icon.png
Issue date: 05/31/1998
From: Christian D, Mason D, Pincus J
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
98-363, NUDOCS 9806190063
Download: ML18153A314 (17)


Text

  • e VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 June 10,1998 United States Nuclear Regulatory Commission Attention:

Document Control Desk Washington, D.C. 20555 Gentlemen:

VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Serial No.98-363 SPS Lic/BCB RO Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 The Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of May 1998, is provided in the attachment. . If you have any questions or require additional information, please contact us. Very truly yours, D. A. Christian, Site Vice President Surry Power Station Attachment Commitments made by this letter: None cc: U.S. Nuclear Regulatory Commission Region II Atlanta Federal Center 61 Forsyth Street, S. W. Suite 23T85 Atlanta, Georgia 30303 Mr. R. A. Musser NRC Senior Resident Inspector Surry Power Station * ( 9806190063 980531 i PDR ADOCK 05000280 , R PDR

.-"*** ,.-* 1

  • VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT No. 98-05 Approved:

~*JcL.10-"li?*

Site Vice President Date TABLE OF CONTENTS Section -Surry Monthly Operating Report No. 98-05 Page 2 of 16 Page Operating Data Report -Unit No. 1 ******************************************************************:*********************************************************3 Operating Data Report -Unit No. 2 ............................................................................................................................

4 Unit Shutdowns and Power Reductions

-Unit No. 1 ..................................................................................................

5 Unit Shutdowns and Power Reductions

-Unit No. 2 ..................................................................................................

6 Average Daily Unit Power Level -Unit No. 1 ..............................................................................................................

7 Average Daily Unit Power Level -Unit No. 2 ..............................................................................................................

8 Summary of Operating Experience

-Unit Nos. 1 and 2 .............................................................................................

9 Facility Changes That Did Not Require NRG Approval ............................................................................................

10 Procedure or Method of Operation Changes That Did Not Require NRG Approval .................................................

11 Tests and Experiments That Did Not Require NRG Approval.

.................................................................................

12 Chemistry Report .....................................................................................................................................................

13 Fuel Handling -Unit Nos. 1 and 2 ............................................................................................................................

14 Description of Periodic Test(s) Which Were Not Completed Within the Time Limits Specified in Technical Specifications

.......................................................................................................................

16

. . Surry Monthly Operating Report OPERATING DATA REPORT Docket No.: 50-280

  • Date: . 06/01/98
  • No. 98-05 . Page 3 of 16 Completed By: D. K. Mason Telephone:

(757) 365-2459 1. . ** Unit Name: ........................................................... . 2. Reporting Period: ................................................. . 3. Licensed Thermal Power (MWt): ......................... . 4. Nameplate Rating (Gross MWe): ...... : .................. . 5. Design Electrical Rating (Net MWe): ................... . 6. Maximum Dependable Capacity (Gross MWe): ... . 7. Maximum Dependable Capacity (Net MWe): ....... . Surry Unit 1 May, 1998 2546 847.5 788 840 801 *

  • 8. If Changes Occur in Capacity Ratings *(Items Number 3 Through 7) Since Last Report, Give Reasons: 9. Power Level To Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any: This Month Year-To-Date Cumulative
11. Hours in Reporting Period 744.0 3623.0 223007.0 .
  • 12. Hours Reactor Was Critical 374.3 2952.6 156978.4 13. Reactor Reserve Shutdown Hours 0.0 0.0 3774.5 14. Hours Generator On-Line 361.3 2919.8 154519.3 15. Unit Reserve Shutdown Hours 0.0 0.0 3736.2 16. Gross Thermal Energy Generated (MWH) 910694.0 7390353.7.

363635369.3

17. Gross Electrical Energy Generated (MWH) 299707.0 2470739.0 119286493.

0 18. Net Electrical Energy Generated (MWH) 289639.0 2388990.0 113623211.0

19. Unit Service Factor 48.6% 80.6% 69.3% 20. Unit Availability Factor 48.6% 80.6% 71.0% 21 .. Unit Capacity Factor (Using MDC Net) 48.6% 82.3 % 65.4% 22. Unit Capacity Factor (Using DER Net) 49.4% 83.7% 64.7% 23. Unit Forced Outage Rate 51.4% 13.1% 14.7% , 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each): Refueling, October 19, 1998, 35 Days 25: If Shut Down at End of Report Period, Estimated Date of Start-up:
26. Unit In Test Status (Prior to Commercial Operation):

INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION FORECAST ACHIEVED

. .). i .. I. I ,.' ... :,

  • OPERATING DATA REPORT e .. Surry Monthly Operating Report No. 98-05 Page 4 of 16 Docket No.: 50-281 Date: 06/02/98 Completed By: D. K. Mason Telephone:

(757) 365-2459 1. Unit Name: ........................................................... . 2. Reporting Period: ................................................. . 3. Licensed Thermal Power (MWt): ......................... . 4. Nameplate Rating (Gross MWe): ......................... . 5. Design Electrical Rating (Net MWe): ................... . 6. Maximum Dependable Capacity (Gross MWe): ... . . 7. Maximum Dependable Capacity (Net MWe): ....... . Surry Unit 2 May, 1998 2546 847.5 788 840 801 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: 9. Power Level To Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any: This Month Year-To-Date

11. Hours in Reporting Period 744.0 3623.0 12. Hours Reactor Was Critical 744.0 3623.0 13. Reactor Reserve Shutdown Hours 0.0 0.0 14. Hours Generator On-Line 744.0 3623.0 15. Unit Reserve Shutdown Hours 0.0 0.0 16. Gross Thermal Energy Generated (MWH) 1894101.8 9220308.5
17. Gross Electrical Energy Generated (MWH) 631500.0 3085960.0
18. Net Electrical Energy Generated (MWH) 609791.0 2985183.0
19. Unit Service Factor 100.0% 100.0% 20 .. Unit Availability Factor 100.0% 100.0% 21. Unit Capacity Factor (Using MDC Net) 102.3% 102.9% 22. Unit Capacity Factor (Using DER Net) 104.0% 104.6% 23. Unit Forced Outage Rate 0.0% 0.0% 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each): None 25. If Shut Down at End of Report Period, Estimated Date of Start-up:
26. Unit In Test Status (Prior to Commercial Operation):

INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION FORECAST ACHIEVED Cumulative 219888.0 154773.3 328.1 152756.5 0.0 360753875.8 118211568.0 112628334.0 69.5% 69.5% 65.5% 65.0% 11.7%

... ~. ,:: ,,,. *.,: ... *. (1) ' . .. Date Type '05/10/98 F (1) F: Forced S: Scheduled (4) * (2) UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%) REPORT MONTH: May, 1998 (3) (4) Method e . Surry Monthly Operating Report , No. 98-05 Page 5 of 16 Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 06/03/98 Completed by: J. R. Pincus Telephone:

(757) 365-2863 (5) Duration of LER No. System Component Cause & Corrective Action Hours 382.7 Reason A (2) REASON: Shutting Down Rx 1 50/280-009-00 A -Equipment Failure (Explain)

B Maintenance or Test C Refueling D Regulatory Restriction Code AB E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)

Code to Prevent Recurrence PSP Non-isolable weld leak on "C" reactor coolant pump seal injection line. Affected piping was replaced.

(3) METHOD: 1 -Manual 2 . Manual Scram 3 -Automatic Scram 4 Other (Explain)

(5) Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG 0161) Exhibit 1 -Same Source (1) Date Type (1) F: Forced S:

  • Scheduled

' (4) * (2) e Surry Monthly Operating Report No. 98-05 Page 6 of 16 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%) REPORT MONTH: May, 1998 (3) (4) Method Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 06/03/98 Completed by: J. R. Pincus Telephone:

(757) 365~2863 (5) Duration of LER No. System Component Cause & Corrective Action Hours Reason Shutting Code Down Rx None During the Reporting Period (2) REASON: A Equipment Failure (Explain)

B -Maintenance or Test C Refueling D Regulatory Restriction E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)

Code to Prevent Recurrence . (3) METHOD: 1 Manual 2 -Manual Scram 3 Automatic Scram 4 -other (Explain)

(5) ' Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG 0161) Exhibit 1 -Same Source MONTH: May, 1998 Day 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 INSTRUCTIONS .e e Surry Monthly Operating Report No. 98-05 Page 7 of 16 AVERAGE DAILY UNIT POWER LEVEL Average Daily Power Level (MWe-Net) Day 825 17 824 18 824 19 825 20 825 21 824 22 823 23 823 24 734 25 9 26 0 27 0 28 0 29 0 30 0 31 0 Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 06/03/98 Completed by: Barry C. Bryant Telephone:

(757) 365-2834 Average Daily Power Level (MWe -Net) 0 0 0 0 0 0 0 0 0 646 819 818 819 817 816 On this format, list the average daily unit power level in MWe -Net for each day in the reporting month. Compute to the nearest whole megawatt.

MONTH: May, 1998 Day 1 2 3 4. 5 6 7 8 9 10 11 12 13 14 15 16 INSTRUCTIONS

  • e Surry Monthly Operating Report No. 98-05 Page 8 of 16 AVERAGE DAILY UNIT POWER LEVEL Average Daily Power Level (MWe-Net) Day 822 17 823 18 822 19 821 20 821 21 : 820 22 821 23 822 24 823 25 822 26 825 27 825 28 826 29
  • 826 30 825 31 . 824 Docket No.: 50-281 Unit Name: Surry Unit 2 Date: . 06/03/98 Completed by: Barry C. Bryant Telephone:

(757) 365-2837 Average Daily Power Level (MWe-Net) 824 822 822 821 821 820 819 813 809 817 819 818 801 805 811 On this format, list the average daily unit power level in MWe -Net for each day in the reporting month. Compute to

  • the nearest whole megawatt.

',-* r , .... **. e

SUMMARY

OF OPERATING EXPERIENCE MONTHNEAR:

May, 1998 * *

  • Surry Monthly Operating Report No. 98-05 Page 9 of 16 . . . The following chronological sequence by unit is a summary of operating experiences for this month which req.uired . load reductions or resulted in significant non-load related incidents.

UNIT ONE: 05/01/98 05/09/98 05/09/98 05/09/98 05/10/98 05/10/98 05/25/98 05/26/98 05/26/98 05/31/98 UNITTwo: 05/01/98 05/31/98*.

0000 1720 2112 2304 0151 0223 1206 0032 1330 2400 0000 2400 Unit operating at 100% power, 855 MWe. Began power reduction to reduce dose rate to facilitate an investigation of a noted increase in reactor coolant leakage. Stopped power reduction at 50%, 400 MWe. Began power reduction to place unit at Cold Shutdown as required by Technical Specification 3.1.C.4 due to a non-isolable weld leak on the "C" reactor coolant pump seal injection line. Generator off-line.

Reactor manually tripped. Reactor critical.

Generator on-line. Began power increase.

Stopped power increase at 100%, 850 MWe. Unit operating at 100% power, 850 MWe. I Unit operating at 100% power, 855 MWe. Unit operating at 100% power, 845 MWe.

  • DCP 92-22 TM S2-98-02
  • TM S1-98-12 SE 98-060 TM S1-98-13 * * *** Surry Monthly Operating Report . No. 98-05
  • Page 10 of 16 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR:

May, 1998 Design Change Package 05/07/98 . . Design Change Package 92-22 replaced various older model Unit 1 and Unit 2 operated valves (SOV) with newer models. The modification did not affect the original design function or operation of the SOVs. Temporary Modification (Safety Evaluation 98-056) 05/12/98 Temporary Modification S2-98-02 replaced the failed manual actuator for service water system isolation valve, 2-SW-478, with a valve handwheel.

Temporary Modification (Safety Evaluation 98-057) 05/14/98 Temporary Modification (TM) S1-98-12 installed a cap to isolate the failed capillary tubing on the discharge of the Unit 1 turbine bearing lift pump. Installation of the TM also isolated the pump discharge pressure gauge. Safety Evaluation 05/21/98 Safety Evaluation 98-060 was performed to assess the installation of a freeze seal to facilitate the replacement of Unit 1 reactor coolant system valve, 1-RC-6. The evaluation concluded that the installation of the freeze seal in accordance with Mechanical Corrective Maintenance procedure O-MCM-1918-03, "Freeze Seal of Piping," was acceptable.

Temporary Modification (Safety Evaluation 98-061) 05/24/98 Temporary Modification S1-98-13 installed a recorder on the acoustic monitors used to monitor the performance of the Unit 1 pressurizer safety valves;*

FS 98-16 FS 98-10 1-0P-RC-011 GMP-011 * *

  • PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID Nor REQUIRE NRC APPROVAL
  • MONTHNEAR:

May, 1998 UFSAR Change (Safety Evaluation 98-052) Surry Monthly Operating Report No. 98-05 Page 11 of 16 05/04/98 . UFSAR Section 17.2, "Operational Quality Assurance Program Topical Report," was revised to reflect the replacement of the Instruction Manual for Architect/Engineers with a General

  • Nuclear Standard which describes the interface between the company and its contractors.
uFSAR Change 05/07/98 . (Safety Evaluation 98-053) UFSAR Section 7.2.3.2.7, "Anticipated Transient Without SCRAM (ATWS) Mitigation System Actuation Circuitry (AMSAC)," was revised to clarify the licensing basis associated with the AMSAC C-20 interlock setpoint.

Operating Procedure (Safety Evaluation 98-054) 05/11/98 Operating Procedure 1-0P-RC-011, "Pressurizer Relief Tank Operations," was changed to provide instructions for the installation of a mechanical jumper that connects the Unit 1 pressurizer relief tank (PRT) vapor space sample line to the overh.ead gas system. The jumper allows the PRT to be continuously vented to the overhead system without batch releasing to the process vent.

  • General Maintenance Procedure (Safety Evaluation 98-055) 05/12/98 General Maintenance Procedure GMP-011, "Installation and Removal of Stop Logs," was . changed to provide instructions for the installation of an electrical jumper that will enable the circulating water intake level alarms to remain functional in the event that one of the intake
  • bays is stop logged. *
  • e Surry Monthly Operating Report TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:

May, 1998 None During the Reporting Period No. 98-05 Page 12 of 16 Primary Coolant Analysis Gross Radioactivity, µCi/ml Suspended Solids, ppm Gross Tritium, µCi/ml 1131, µCi/ml 113111133 Hydrogen, cc/kg Lithium, ppm Boron -10, ppm* Oxygen, (DO), ppm Chloride, ppm pH at 25 degree. Celsius

None CHEMISTRY REPORT MONTH/YEAR:

May, 1998 Unit No. 1 Max. Min. Avg. 3.93E-1 7.81 E-3 1.62E-1 2.0 ::;;0.010 0.670 1.40E-1 1.37E-1 1.39E-1 1.71 E-1 7.28E-4 2.54E-2 0.27 0.12 0.20 42.1 2.9 15.9 2.34 0.70 1.76 297.1 77.6 200.9 6.0 ::;;0.005 0.410 0.010 0.002 0.004 7.14 6.09 6.56 I 4'urry Monthly Operating Report No. 98-05 Page 13 of 16 Unit No. 2 Max. Min. Avg. 1.88E-1 1.14E-1 1.45E-1 ---9.63E-1 9.30E-1 9.47E-1

  • 6.53E-5 3.73E-5 4.87E-5 0.11 0.06 0.08 41.5 37.5 39.0 2.34 2.08 2.23* 184.8 i 169.5 177.8 ::;;0.005
0.005
0.005 0.005 0.002 0.004 6.76 6.56 6.68 New Fuel Shipment or Date Stored or Cask No. Received Spent Fuel *
  • Cask No. TN 32-07 05/27/98 I * ! '
  • FUEL HANDLING UNITS 1 & 2 MONTHNEAR:

May, 1998 Number of Assemblies Assembly ANSI per Shipment Number Number 32 OP1 LM05Y5 OPS, LM05XF ORB LMOC1R OSB LMOESV 1P2 LM05XG 1P8 LM05X6 1R4 LMOC1W 2C4 LMOBMK 2E2 LMODFS 2PO LM05X9 2P1 LM05XB 2P2 LM05X4 . ' 2P4 LM05XN 2P6 LM05XX 3P1 LM05XP 3P4 LM05YC 4CO LM08N8 4P2 LM05YT 4ilurry Monthly Operating Report No. 98-05 Page 14 of 16 New or Spent Initial Fuel Shipping Enrichment Cask Activity 3.6070 N/A 3.6070 3.5947 3.5955 3.6070 3.6070 3.5986 3.3990 3.5973 3.6070 3.6070 3.6070 3.6070 3.6070 3.6070 3.6070 3.3990 3.6070 New Fuel *

  • Shipment or Date Stored or Cask No. Received . Spent Fuel Cask No. TN 32-07 (Continued)
  • FUEL HANDLING UNITS 1 & 2 MONTHNEAR:

May, 1998 Number of Assemblies Assembly ANSI per Shipment Number Number 4P3 LM05YB 4P4 LM05YM 4P6 LM05YL 5E4 LMODEH 5P2 LM05Y9 5P3 LM05XU 5P4 LM09PH 5P5 LM05XM 5P8 LM05YD 5R2 LMOC2D 5R6 LMOC1Z 5R9 LMOC2B 6P5 LM09PG 6P7 LM05YJ ' -urry Monthly Operating Report No. 98-05 Page 15 of 16 New or Spent Initial Fuel Shipping Enrichment Cask Activity 3.6070 3.6070 3.6070 3.6048 3.6070 3.6070 3.6070 3.6070 3.6070 3.5971 3.5901. 3.5885 3.6070 3.6070

.'i: :..._*,* .. *: -urry Monthly Operating Report* No. 98-05 Page 16 of 16 DESCRIPTION OF PERIODIC TEST(S) WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTHNEAR:

May, 1998 None During the Reporting Period