ML18139B388

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LER 81-022/03L-0:on 810514,amp Reading for Heat Tracing Panel 9,circuit 20C,found Below Acceptance Criteria.Caused by Excessive Heat.Tracing Replaced & Tested.Design Change Initiated
ML18139B388
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/05/1981
From: WILSON J L
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139B384 List:
References
LER-81-022-03L-01, LER-81-22-3L-1, NUDOCS 8106090559
Download: ML18139B388 (3)


Text

  • NRC FORM 366 .LICENSEE EVENT REPORT U.S. NUCLEAR REGULA. TORY COMMISSION li-7') ** CONTROL BLOCK: ' I',\ (PLEASE P~INT OR TYPE ALL REOUIREC INFORMATION) l--..... _ ...............

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I With Unit No. 2 at 100% power, PT-27C revealed*

that amn readino for heat tracing .III!]. J Panel 9, circuit 20C, was below the acceptance criteria stipulated in the PT. This ([II] I event is contrary to T.S. 3.2.B.5 and is reportable per T.s: 6.6.2.b(2)

.. ~he [TI]] _I redundant.

heat tracing circuit was operable, therefore, the health* and safety of the J .. [£I[] I public were not affected, IITil L.....------------------------------------___..

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TAKEN ACTION ON PLANT METHOD . HOURS SUBMITTED FORMliUB.

SUPPI.IER MANUl'ACTURER

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  • CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS @ D:I]J j The loss of heat tracing was aue to excessive heat. The defective heat trac;n2 was o:::IIJ replaced and tested. A design change has been initiated tq change tbe manner by !III! which these borated lines are heat traced. I 1-., _____________

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  • ATTACHMENT 1 SURRY POWER STATION, UNIT No. 2 DOCKET NO: 50-281 REPORT NO: 81-022/03L-0 EVENT DATE: 05-14-81 TITLE OF EVENT: HEAT TRACING FAILURE 1. DESCRIPTION OF EVENT:
2. PROBABLE CONSEQUENCES and STATUS of REDUNDANT EQUIPMENT:

The heat tracing circuits are intended to maintain a fluid temperature above that needed for flow. The redundant heat tracing.circuit was operable, therefore, the health and safety of the public were not affected.

3. CAUSE: The loss o:1; heat tracing was due to excessive heat. 4. U1MEDIATK CORRECTIVE ACTION: The irrnnediate corrective action was to verify that the redundant circuit was operable.
5. SUBSEQUENT CORRECTIVE ACTION: The defective heat tracing tape-was** replaced and tested within the time span specified by Technical Specifications.
6. ACTION TAKEN TO PREVENT RECURRENCE:

No additional actions were deemed necessary.

7. GENERIC IMPLICATIONS:

A task force has reviewed the total spectrum of the Heat Tracing system and a Design Change is being prepared as a result of the Task Force's study. Long lead items are being procured.

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  • 38. Personnel exposure type 42. Type damage/loss L