ML18139B389

From kanterella
Jump to navigation Jump to search
LER 81-033/03L-0:on 810518,amp Reading for Heat Tracing Panel 8,circuit 6A,found Below Acceptance Criteria.Caused by Excessive Heat.Tracing Replaced & Tested.Design Change Initiated
ML18139B389
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/05/1981
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139B384 List:
References
LER-81-033-03L-02, LER-81-33-3L-2, NUDOCS 8106090568
Download: ML18139B389 (2)


Text

es,

~

NRC FORM 266 CONTROL BLOCK:

IV I A I s l pl s I 2 101


6 J l 0

"LICENSEE EVENT REPORT

! 0 I -j

!f';"\

O

\.!)

I Pl 01 01 01 -!

- N.UCL.i:.AR REGULATORY COMMISSION

!PLEASE PRINT OR TYPE ALL. REOUIREO INFORMATION)

O! 0 IG)l 4 11 111111101 I I©

~ S 9 L.IC:ENS!:E COO: 14 15 LIC:ENSE NUMBEFi . 25 . 26 LIC:ENSE 'iYPE ;JO 57 C:.I.T 5S CON'i

[IT:Q

s

~;~~~~ LI© j O!

SO 61 5 I OI O! 0 I 2 DOCKET NUMBER

! B! l GI 0 js EVENT 6S 69 11 \s CATE Is 11 741©1° 75 16 1° !5 IB 11 80IG)

REPORT CATE EVENT DESCRIPTION AND PROBABI..E CONSEQUENCES@

J With Unit No. 2 at 100~~ power, PT-27C revealed* that amn readin2 for beat tracing

[llJ ..l Panel 8, circuit 6A was below the acceptance criteria stipulated in the PT. This

((ill I event is contrary to T.S, 3.3.A.4 and is reportable per T.s.6--:6.2.b(2). The J___ ..

..[I))] .I redundant heat tracing circuit was operable, therefore,* the health and safetv of the l_

IillJ Public were not affected*.* 1 i.....,:....;..,_ _ _ _..;.,,__ _ _ . . ; ; ; , . ; . . ; . . ~ - - - - - - - - - - - - - - - - - - - - - ~ - - - - *

[IT]

.. [))))

7 8 9 60 SYSTEM CAUSE CAUSE COMP. VAL.VE COCE cooe .SUBCOOE COMPONENT CODE SUBCOOE SUBCCCE

[ill] .. IS !H.I@ Lu@ L!..J@) !H!EIAITiE!R!E) 9 . 10 .

W W 20 .

' .8 11 12 T3 18 19 SEQUENTIAL.. OCCURRENCE REPORT REVISION C-;\ LERtRo* Lv* ENT.YEAR REPORT NO. cooE TYP.E NO.

~ :s~~~~ I s *1-1 I __ I I I o *1 3 ! 326I I ......-1 Io I 3 29I . L1..J l=:J L.oJ 21 . 22 :3. 24 .27 2S 30 31 :i:.:

. ACTION FUT\.IRE EFFECT * ._

  • SHUTt>OWN ~ ATTACHMENT NPRQ.4 PRIME COMP, COMPONENT TAKEN ACTION *, ';-:.: -
  • ON PLANT .. METHOD HOURS ; ~ SUBMITTED FORM ::iUB. SUPPLIEFI MANUFACTURER I33:GJ@)W@ .. ~. , ,

W@).

3S ,

  • W.

36 l*O l*OJ ,~_:I 37(.;:;\

  • er:!

. 40 L!J@-

41 L..!J W@ :J TI 1 Is I s*J@

42 43 .. 44 47 ,*

CA.USE DESCRIPTION AND ~ORRECTIVE ACTIONS ~

[I))] I The loss of heat tracing was due to excessive heat. The defective heat tracine; IWS DJJ] I replaced and tested. A design change has been initiated to change the manner by which these borated lines are heat traced, o:::u::]'IL------------------------~------------------~-----------------..----------

o:rn

.*o:::m 7 B 9 BC FACILITY STAT\JS 'If, POWER OTHER STATUS

'JO'

',:::;:)

METHOC OF CISCOVERY . OISCO_VERY CESCRIPTION t,:;::\

'5 tITIJ L!l@__ 11 I O I O l@.... I _N__/_A_ _ __ W@i..l_R_o_u_t_1_*n.;..;;e;...;;T..e-s_t~i.;..;;n.a.g_ _ _ _ _ _ _ _ _ ____.l_." __ ...

7 B 9 10 12 13 44 ~ ~ ~

ACTIVITY CONTENT t.:;\

RELEASED OF RELEASE AMOUNT OF ACTIVITY ~ .LOCA7}0N OF RELEASE@

!IE] Ll.J@ Lll@)I .N/A I L----;;.N/:..;A;....,._________________________ _.1! .

, a a 10 11 " 80 PERSONNEL EXPOSURES .

  • Q NUMBER (.;":;\TYPE~ CESCRl"10N

, a aj O ! 0 ! 0,,l~Ll..J~

8I)

PERSONNEL. INJURIES

. . N/ A

,:r,i..:i--......."'"*_..;.--_.;..-----------------------------e-'c C,'\

Ill UMBER OESCRll"TION~

_Eli]

7 B 9

! 0 I Oj O11l@..__ T:2

______ _ _ ; l . ; . : . . 1 / = A - - - - - - - - - - - - - - - - - - -

80

  • **
  • LOSS OF' OR OAMAGE TO FA(;l 1.ITY '43" TYPE OESCRIPTION \:::;

EITJ .w@......._*___*.....---.,..,.,..~,.....,..N....~ i_A_*_ _.....,,.._ _ _ _ _ _ _ _ _ _ _ _ _ _ ____,_

, a a 10 ** 80 PUB~ICITY 'C\ NRC USE ONLY

~ 0 IIlI] ISSu..EOC OESCRIPTION

~,ei _____. _ _ _ _ _ _N_A_ _ _ _ _ _ _ _ _ _ _ _ ____.

/

I J I I II I I1 I I l I !_

' *s 9 10 68 6S

.~~.o~ o_~

.*~~"'*:_...:: ...., ..~ ':.~+:~.*

Sa"~**

-- -"~----:**-* ~- -*

r *. L ** w.~son
  • --*~*-----~---**-. *. . *-----

(804) 357-3184 ~

ATTACHMENT 1 SURRY POWER STATION, UNIT NO. 2 DOCKET NO: 50-281 REPORT NO: 81-:-033/03L-0 EVENT DATE: 05-18-81 TITLE OF EVENT: HEAT TRACING FAILURE

1. DESCRIPTION OF EVENT:

With Unit No. 2 at 100% power, PT-27C revealed that the amp reading for heat tracing Panel 8, circuit 6A (BIT recirc. return line) was below the acceptance criteria stipulated in the PT. This event is contrary to Technical Specification 3.3.A.4, and is reportable per Technical Specification 6,6,2.b(2).

2. PROBABLE CONSEQUENCES and STATUS of REDUNDANT EQUIPMENT:

The heat tracing circuits are intended to maintain a fluid temperature above that needed for flow. The redundant heat tracing circuit was operable, therefore, the health and safety of the public were not affected,

3. CAUSE:

The loss of heat tracing was due to excessive heat.

4. IMMEDIATE CORRECTIVE ACTION:

The -immediate corre.ctive action was to verify.,thaL, the redundant circuit was operable.

5. SUBSEQUENT CORRECTIVE ACTION:

The defective heat tracing tape was replaced and tested within the time span specified by Technical Specifications.

6. ACTION TAKEN TO PREVENT RECURRENCE:

No additional actions were deemed necessary.

7, GENERIC IMPLICATIONS:

A task force has reviewed the total spectrum of the Heat Tracing system and a Design Change is being prepared as a result of the Task Force's study, Long lead items are being procured.

  • .~~- -c_--;.'::'"':='.~~ .. .---- ,. - ..,.._ ' ..... _,_. _______ - ~ * - . ; : - - ~ - - * - * - - - - - - * - - - - - - - - - - ----- *. -*-----,-. - - . - - ~ - -