ML18139A633

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LER 80-044/03L-0:on 800707,during Periodic Test 22.2, Circuit Breaker for 1-EE-P-1F Found Open.Caused by Personnel Error.Breaker Reclosed
ML18139A633
Person / Time
Site: Surry Dominion icon.png
Issue date: 08/06/1980
From: WILSON J L
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139A631 List:
References
LER-80-044-03L-01, LER-80-44-3L-1, NUDOCS 8008080373
Download: ML18139A633 (2)


Text

CONT~"OL BLOCK: !-! __. _ __.__..._......i.._l..._...J*, 0 -* I o I o I o Io 1-Io Io 1014 !PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION!

1e111 l1101 I 10 L *v I A I s I P I 5 I 1 101 o Io I 8 9 LICENSEE CODI: 14 15 LICENSE NUMBER 25 26 LICENSE. TYPE. ;JO 57 CAT SS "T e

~I 01 s Io Io 10 I 21 s I o 101 o j 7 Io 17 I s1 o 101 ° 1 8 1° 1 6 I 8 I O JG) 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE BO EVENT DESCRIPTION AND PROBABLE CONSEQUENCES

@ L While performing Perio'di-c Tes-t 22 **2 , which is designed *to prove the operability of the 2 3 L diesel fuel oil transfer pumps, it was found that the circuit breaker for 1-EE-P-lF was [3J L open. This is contrary to Technical Specification 3 .16 .A. 5 and is reportable as per }] L Technical Specification 6.6.2.b(2)The alternate flow path through 1-EE-P-lC was operable.

The health and safety of the public were not affected.

]] B 9 SYSTEM CAUSE CAUSE CODE CODE SUBCDDE }] I El El@ ~@ w@ le 6 9 10 11 12 13 SEQUENTIAL

@ LER,RO LVENTVEAR . REPORTNO.

REPORT j 8 I o j l==.J Io 14 I 4! NUMBER 21 22 23 24 26 ACTION FUTURE EFFECT SHUTDOWN TAKEN ACTION ON PLANT METHOD COMPONENT CODE I Kl TI BIR I K 1@ 18 OCCURRENCE CODE 1,1 I O I 31 27 28 29 COMP. SUBCODE ~@) 19 REPORT TYPE LI 30 VALVE SUBCODE ~@ 20 REVISION NO. l=:J LQJ 31 32 NPRD-4 FORM!:iUB.

PRIME COMP. SUPPLIER COMPONENT MANUFACTURER BO W@LlJ@ ~@ ~ I 0 33 34 3~ 36 37 {22) ATTAl.:HMENT HOURS Rr" SUBMITTED I O I O I I Lil@ W@) I.Ll@ IC 11 I 11 0 I CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS @ 40 41 4:2 43 44 47 l The breaker was inadvertently opened by personnel working in the vicinity o.f the MCC. The JJ I breaker was reclosed and i?eri~dic-Test 22.*i complet:ed*

satisfactorly.

}] . ....._ ________________________________

~-------'

TI TI B 9 FACILITY STATUS BO '3a' METHOD OF % POWER OTHER STATUS \:/ DISCOVERY DISCOVERY DESCRIPTION

\:31 I O I O I ~@1-I __ N_A ____ .-..J W@.._l __....;:O~p;.;;:e=-r=-at;::.;o;..;;r~o.;;;.b;;:_se.;;.;.:rv;..;...;...a...;.t.;;;.io;...n~-----.----

........ B 9 10 12 1"3 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY w (§) LI@)l.____NA

______ _. B 9 10 11 44 *s PERSONNEL EXPOSURES . NUMBER TYPE DESCRIPTION@

?J -1 a I o Io 10~@ 8 9 11 12 1._3--------------------------------------.--JBO SD LOCATION OF RELEASE @ NA 80 NA PERSONNEL INJURIES I:";\ NUMBER DESCRIPTION~

~] I o Io Io I@ 8 9 11 ~1:1:--------------------------------------.-----B...lO NA LOSS OF OR DAMAGE TO FACILITY '4J' TYPE OESCRIPTIOIII . NA 8 9 10 BO PUBLICITY ISSUED~ DESCRIPTION~

NRC USE ONLY ., D U!.16~--=-=:-=---------N-A

_________

__J I I I I I I I I I I I I I ! 8 9 8 0 0 8°0 8 0 3 7'3 68 69 NAME OF PRE PARER-_...;J;...:..

  • ...;L~. _W:.;.1::.*

1_s_o_n,;__

_________

_ PHONE: (804) 3 57-3184 80 -;; 0 II. 0

.t.. ATTACHMENT 1 SURRY POWER STATION, UNI~ DOCKET NO: ~0-230 REPORT NO: 80-044/031-0 EVENT DATE: 07-07-80 TITLE OF EVENT: TRANSFER PUMP BREAKER INADVERTANTLY OPENED 1. Description of Event: While performing Periodic Test 22.2, which is. des.igned to prove the operability of the diesel fuel oil transfer pumps., it was. found that the circuit breaker for 1-EE-P-lF was open. This is contrary to Technical Specification 3.16.AiS and_is Reportable

flow path through 1-EE-P-lC was operable and capable of supplying fuel oil to #3 emergency diesel day tank. The health and safety of the public were not affected.

3. Cause: The breaker was inadvertently opened by personnel working in the vicinity of the motor control center. 4. Irmnediate Corrective Action: Reclosed the circuit breaker and tested the pump as per Periodic Test 22.2. 5. Subsequent Corrective Action: _None Required 6. Action Taken to Prevent Recurrence:

None Required 7. Generic Implications None