ML18139B387

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LER 81-031/03L-0:on 810508,amp Reading for Heat Tracing Panel 11,circuit 1B,found Below Acceptance Criteria.Caused by Mechanical Damage to Tape.Heat Tracing Replaced & Tested. Design Change Initiated
ML18139B387
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/05/1981
From: WILSON J L
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139B384 List:
References
LER-81-031-03L-02, LER-81-31-3L-2, NUDOCS 8106090548
Download: ML18139B387 (2)


Text

EVENT REPORT U.S. NUCL.EAR REGUL.ATORV COMMISSION r,. 7i'll .*

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"-!.I I V I A I s I p I s I 2 101 0 I O I S 9 L.ICSNSEE CODE 14 ~S -10101010101-10101@1411111111101 l I© LICENSE NUMBER 25 . 26 LICENSE 'iYPE JO 57 CAT SS CON'i [ITIJ ; 6 LI© I o J s l o l o I o I 21 s 1 1 101 o I s I o I s l s I 1 I© Io ! 6 I o I s I s 11 I© 60 61 COCKE'T NUMBER 6S 69 EVENT DATE 74 75 REPORT OAi'c BO EVENT DESCRIPTION AND PROSABL.E CONSEQUENCES@

l With Unit No. 2 at 100% power, PT-27C revealed that amp reading for heat tracing . Panel 11, circuit lB was below the acceptance criteria stipulated in the PT. IIm This everit is contrary to T. S. 3 ,3 .A. 4 and is reportable per-T, S. 6. 6. 2. b (2). 'T'he _l]J]J [§]]:] __ [ill] redundant.heat tracing circuit was operable, therefore, the health and safety of the L-...;;P.;;u;,;;;b.;;l;,;;;i:.;;c;....;.w;.;;e;,:r;.;;e;_;,n:.:o;.;;t:.....:a:.:f;.;f;.;e::.:c;;.;t;;.;e::.:d::..:...*


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  • 44 * '. ' 47 Personnel had been working in the near b'y area, !he defective heat tracing was replaced and test-[I]]] .ed. A design change has been initiated to change the manner by which these borated liries are heat traced. o:m 7 8 9 FACILITY /jo'I STATUS % "0WER . OTHER STATUS '.;::;:; iI1TI .LI@ __ I 1 l O I O l .... I _!_i/_A~---

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ATTACHMENT SURRY POWER DOCKET NO: REPORT NO: EVENT DATE:

  • STATION, UNIT NO. 2 50-281 8l-031/03L-O 05-08-81 TITLE OF EVENT: HEAT TRACING FAILURE 1. DESCRIPTION OF EVENT:
2. PROBABLE CONSEQUENCES and STATUS of REDUNDANT EQUIPMENT:

The heat tracing circuits are intended to maintain a fluid temperature above that needed for flow. The redundant heat tracing circuit was operable, fore, the health and safety of the public were not affected.

3. CAUSE: The loss of heat tracing was du~to mechanical

~amage to the tape. Personnel from various crafts had been working .in the nearby area. 4. IMMEDIATE CORRECT I VE ACT I ON: The immediate corrective action was to verify that the redundant circuit was opera9le.

5. SUBSEQUEST CORRECTIVE ACTION: The defective heat tracing tape was replaced and tested within the time span specified by Technical Specifications.
6. ACTION TAKEN to PREVENT RECURRENCE:

No additional actions:were deemed necessary.

7. GENERIC IMPLICATIONS:

A task force has reviewed the total spectrum of the Heat Tracing *system and a Design Change is being prepared as a result of the Task Force's study. Long lead ttems are being procured.