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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
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!+ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM REGULATOR INFORMATION DISTRlBUTION pTEM (RIDS)ACCESSION NBR:9203110291 DOC.DATE: 92/03/04 NOTARIZED:
NO DOCKET¹FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH.NAME AUTHOR AFFILIATION BACKUSiW.H.
Rochester Gas&Electric Corp.MECREDY,R.C.
Rochester Gas&Electric Corp.RECIP.NAME RECiPIENT AFFILIATION
SUBJECT:
LER 92-002-00:on 920203,reactor trip occurred w/reactor at approx 23%full power just subsequent to turbine trip while at 47%power.Caused by lo lo level in SG A due to design perturbations.New setting calculated.W/920304 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
R D/05000244 A RECIPIENT ID CODE/NAME PDl-3 LA JOHNSON,A COPIES LTTR ENCL 1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD COPIES LTTR ENCL 1 1 D D INTERNAL: ACNW AEOD/DSP/TPAB NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DREP/PRPBll NRR/DST/SICB8H3 NRR/DST/SRXB 8E RES/DSIR/EIB EXTERNAL'G&G BRYCE i J~H NRC PDR NSIC POOREiW.AEOD/DOA AEOD/ROAB/DSP NRR/DLPQ/LHFB10" NRR/DOEA/OEAB NRR/DST/SELB 8D gNR~D-.LB8Dl-G~02 RGN1 FILE 01 3 3 L ST LOBBY WARD 1 1 1 1 NSIC MURPHYgG.A 1 1 1.1 NUDOCS FULL TXT 1 1 2 2 1 1 1 1 2 2 1 1 1 1 1 1 1 1 2 2 1~1'1 1 1 1 1 1 1 1 1 1 1 1 D NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!A D D S FULL'TEXT CONVERSION REQUIRED TOTAL NUMB R OF COPIES REQUIRED: LTTR 30 ENCL 30 I
rr f~'I~zotrr.sT4 M ROCHESTER GAS AND ELECTRIC CORPORATION 4 89 EAST AVENUE, ROCHESTER N.K-74649-0001 ROBER't (, hlECRjtpY Vrr<Vresidenl Crnna No<lcm Prodursrorr TELE&>0'ME ARErr COM 716 546'2700 March 4, 1992 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER 92-002, Feedwater Transient, Due To Loss Of Excitation Induced Turbine/Generator Trip, Causes Lo Lo Steam Gen'erator Level Reactor Trip-R.E.Ginna Nuclear Power Plant Docket No.50-244In accordance with 10CFR50.73, Licensee.Event Report System, item (a)(2)(iv), which requires a report of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)", the attached Event Report LER 92-002 is hereby submitted.
This event has in no way affected the public's health and safety.Very truly yours, Robert C.Mecredy.xco U.S.Nuclear Regulatory Commission Re'gion I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector f)~g(4~(q'l 92031i0291
'720304 PDR ADOCK 05000244 5 PDR I t'l
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'" Feedwater Transient, Due to Loss of Excitation n uced Tur z.ne Generator Trip, Causes Lo Lo Steam Generator Level Reactor Trip I VINS OATS III LtR NueettA III AIMRT OATI III OTHIA eACILITISI INVOLVIO Nl VO<<TH OAY YIA1 YIAR 0 2 3 9 2 9 2~save<<ewe<<vee~IA 0 0 2 Ae v orcee Irueee~A 0 IION TH 0 3 OAY 0 4 YIAR 9 2 eACIUTY<<Aeeee OOCAIT<<uee~SAISI 0 6 0 0 O 0 6 0 0 0 Oel1*TINO eeOOI Itl~Oeel1 LlvlL 0 2 3 THIS 1leOAT N SuteeITTIO euAWANT I$Lea$4I SO.NQ Nl ll I II Sa.calle III I III St.e le I II I I RI$OAOllel ll I l<<l SO.OOS lelll llel St.cell el~OMW III~OMWQI~O.T SN I QI I I~O.T tie I Q I I II IO.TSNIQIIVO
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OATII AJSTA*cT ILeevl 4 Ieco eeeer.I A, eeereee<<e>>re AY>>ee ree>>eeeee eeoer<>e<<eev lltl ttetCTSO LVINISSION OA'll ll~I eeONTH CAY YIAR On February 3, 1992 with the reactor at approximately 23%full power, just subsequent to a turbine trip while at 474 reactor power, a reactor trip occurred due to Lo Lo Level (</=17%)in the"A" Steam Generator (S/G).The Control Room operators immediately performed the appropriate actions of Emergency Operating Procedures E-0 (Reactor Trip or Safety Injection) and ES-0.1 (Reactor Trip Response).
Both Main Steam Isolation Valves (MSIVs)were subsequently closed to limit a Reactor Coolant System (RCS)cooldown and the plant was stabil-ized at hot shutdown.The underlying cause of the event was the inability to control the"A" S/G level above the reactor trip setpoint due to design and transient induced perturbations.(This event is NUREG-1022 (x)Cause Code).Corrective action taken or planned are discussed in Section V of the text.<<AC e<<r<>AOVlO 0+1 4O IIQI~IQA l)et<All II)I'lS SACILITY IIAIAl III" OOCIIKZ IIVIACCA Ill%lA A LlA IIIAAI~II Ill S~QMA4TIAL'V U A ACVOIOH V IA~AOl IlI R.E.Ginna Nuclear Power Plant tlXTOr~aeOee~.
~~~AAC~~'sIIlll o s o o o24 4 92 002 00020F].PRE-L?V1?NT PLANT CONDITIONS The plant was at approximately 47%reactor power due to a load reduction earlier in the day.Part of this load.reduction (i.e.to approximately 60%reactor power)was requested by the Rochester Gas and Electric Corporation (RG&E)Power Control Dispatcher to remove a major trans-mission line from service (circuit 908)for repair.The remainder of this load reduction (from 60%to 47%reactor power)was made to reduce reactor power below permissive P-9 (i.e.Reactor Trip From Turbine Trip Blocked)to perform condenser water box maintenance and turbine on-line trip testing and valve testing.The main generator voltage control was in the manual mode due to voltage oscillations experienced earlier in tQe day.The reactor control rods were also in the manual mode to maintain the core axial flux within its operating band.Turbine on-line trip testing and'alve testing was in progress with the last test's initial conditions being verified prior to performance of the test.II DESCRIPTION OF EVENT A.DATES AND APPROXIMATE TIMES OP MAZOR OCCUEGU9iCES:
o February 3, 1992, 2220 EST: due to loss of excitation.
Main Generator.
Trip 0 February 3, 1992, 2220 EST: Main Turbine trip due=to main generator trip.0 February,3, 1992, 2224 EST: Event date and time.0 February 3, 1992, 2224 EST: Discovery date and time.0 February 3,'992, 2224 EST: Control Room operators verify both reactor trip breakers open, and all control and shutdown rods inserted.VAC~QALI lAAA Il 4$I
IIAC Svv~(041 I LICENSEE EVENT REPORT ILERI TEXT CONTINUATION U l, vUCLSAA Al<<ULATOA Y<<OvvlllIOAI S ArrrovlO Ovl vO IISO~IOs l)erirf5 llII%$C SACILITY VAVl Ill CO<<II CT IIUVClr l1I LlA lsUVCSA lll$I 4 v S r 7 I A I.r v ASVISIOH V 1~AOl Ill R.E.Ginna Nuclear Power Plant o s o o o 2 4 4 TlxT III~vSSS r rrsrvr.vv SrrrrAv Ivrc svrl~'ll I ITI 92-0 0 2-0 0 0 30>1 2 o February 3, 1992, 2229 EST: Control Room operators close both Main Steam Isolation Valves (MSIVs)to limit a Reactor Coolant System (RCS)cooldown.o February 3, 1992, 2307 EST: Plant stabilized at hot shutdown condition.
B.EVENT: On February 3, 1992 at approximately 2220 EST, with the reactor at approximately 47%stable reactor power, the Control Room received turbine trip first out annunciator alarm K-26 (Generator Lockout Relay).As reactor power was less than 50%full power with the main condenser available, (i.e.less than permis-sive P-9), reactor trip from turbine trip was automatically blocked.The Control Room operators immediately entered-Abnormal Procedure AP-TURB.'1 (Turbine Trip Without Reactor Trip Required)and performed its applicable actions.The responses of the Steam Generator (S/G)Feedwater Regulating Valves (FRVs)for different control configurations are noted here for clarity of subsequent events: o When all FRVs (Main and Bypass)are in the automatic mode, they will go full open on a turbine trip with RCS average temperature (Tavg)greater than 554 F.When temperature goes below 554 F, these valves will go full closed.0 All FRVs, both main and bypass, will fully close upon receiving a HI S/G Level ()/=674)or safety injection signal regardless of their auto/manual status (feedwater isolation).
'When the Main FRVs are placed in the, manual mode from the above configuration, they will assume the position abased on the current controller manual demand signal and stay there until adjusted by the responsible operator.Assuming that the bypass FRVs are left in auto, the bypass FRVs will continue to respond to the automatic feedwater control demand.VAC sOAv SCCA<l4$I tl HISC Term~IMMI e LICENSEE EVENT REPORT ILERI TEXT CONTINUATION U.S.HUclcAA itoUUAToir cossssls$loi/ASSAOV CO OH$HO$1$OWIOS$Ilr<A$5 IISI'$$AACIUI'TY HAMI I 1 I OOCIICT HUMOIA 111 Cli HUMOti I~I SSOU~HTIAI, ASvlQIOr M r SA0$1$1 R.E.Ginna Nuclear Power Plant RAT lr mar MSrs r Hssrsr.~sr srrrsAM Hrc Ilsrr~$1 11TI o s o o o 2 4 4 9 2--0.'2"-0'0 4 os l 2 Prior to the turbine trip all FRVs were in the automatic control mode with the bypass FRVs full open and the main FRVs controlling S/G level in some midposition.
Subsequent to the turbine trip, the ma'in FRVs went full open per design (the bypass FRVs were already full open)and the Control Room operator transferred the main FRVs to manual control and adjusted them to control S/G levels.The bypass FRVs were left in the automatic control mode.The narrow range S/G levels were at approximately 534 and rapidly increasing when the main FRVs were shifted to the manual mode.The Control Room operator closed'own the main FRVs to approximately 10-134 open to control S/G levels.During this time the"A" S/G FRV isolated on HI Level (i.e.)/=67%narrow range level).During approximately this same time the full open bypass FRVs rapidly clo".ed because their automatic controlling setpoint was now 394 S/G level.The Control Room operator'continued to make adjustments to the main FRVs to compensate for the transient perturbations, but was unsuccessful.
At 2224 EST, February 3, 1992, with the reactor at approximately 234 full power a reactor trip occurred due to Lo Lo Level ((/=174)in the"A" S/G.The Control Room operators performed the immediate actions of Emergency Operating Procedure E-0 (Reactor Trip Or Safety Injection) and transitioned to Emergency Operating Procedure ES-O.l (Reactor Trip Response)when it was verified that both reactor trip breakers were open, all control and shutdown rods were inserted, and safety injection was not actuated or required.Both MSIVs were subsequently closed at 2229 EST to limit the RCS cooldown.The closing of the MSIVs subsequently mitigated the RCS cooldown and the plant was stabilized in hot shutdown at 2307 EST.MAC sorv sAAA I$441 I
IIAC Soew%CA I%45>LICENSEE EVENT REPORT{LER)TEXT CONTINUATION y,l, IIUCLSAA AlOULATOA V COSSMISCIOII
/ASSAOV lO Oul IO TISO&104 l~>All SINAI 1$SACILITV IIASSt III OOCKtt IIUI&lA ITI vSAA Llll IIUSSCIA ISI S~4USatiAL U 1 SAOl ISI R.E.Ginna Nuclear Power Plant TlXT IIT~~e~.We eerCeW+AC Arm WS S I UTI osooo244 9 2 0 2 0 0 0 50vl 2 Equipment problems that occurred during the event were as follows: 0'he"ALT Steam Generator MSIV Main Control Board indication showed the valve to be not fully closed.An auxiliary operator was immediately sent out to check and reported the valve closed based on viewing the valve external indicator.
Subsequently, the Main Control Board indicated the valve fully closed approximately 23 minutes after signal receipt.0 0 Following the start of the Turbine ,Driven Auxiliary Feedwater (TDAFW)pump on Lo Lo S/G Levels, it exhibited some oscillations in flow, however total flow remained above the required 400 gallons per minute (GPM)as recorded on the Plant Process Computer System (PPCS).The Intermediate Range Nuclear Instrumentation, Channel N-35, after tracking consistant with Channel N-36 down'to approximately 10 E-10 amps, had its indication continue to drop below 10 E-11 amps.The N-35-channel returned to normal (10 E-11 amps)approximately ten hours following the trip.C.INOPERABLE STRUCTURES g COMPONENTS l OR SYSTEMS THAT CONTRIBUTED TO THE KG9iT: D.None.OWNER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:~None.E.METHOD OF DISCOVERY:
The event was immediately apparent due to alarms and indications in the Control Room.hAC SOAIS SASA ISASI 0~~1 HAC Sore M I$4$I LICENSEE EVENT REPORT ILERI TEXT CONTINUATION v t.IIUCLEA+AtOULATCAY coooorlttrorr AssAOYEO Ovt HO$I$0aIOo-t)eOIAES trtI 1$SACILITY HAltt Ill OOCKET IIUoottA Itl Lt1 HUOSOEA III$$4v~rrYIOL M o otveOI<o~AOE IEI R.E.Ginna Nuclear Power Plant TEXT lrs rrreo HIOoo~rotreoS.re oroorror HPC AHe~$I IITI o so oo244 9 2-0 0 2-0 60F 1 2 OPERATOR ACTION: After the reactor trip, the Control Room operators performed the actions of Emergency Operating Procedures E-O, (Reactor Trip Or Safety Injection) and ES-0.1, (Reactor Trip Response).
The MSIVs were manually actuated closed approximately four (4)minutes after the trip to prevent further plant cooldown.The plant was subsequently stabilized at hot shutdown..Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Com-mission per 10 CFR 50.72, non-emergency, 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> notification.
G.SAFETX SXSTEM RESPONSES:
The"A" S/G FRVs closed automatically from a feedwatdr isolation signal.III.CAUSE OF KGDFZ A.IMMEDIATE CAUSE: The reactor trip was due to"Att S/G Lo Lo Level (</=>>4)B.ROOT CAUSE: The underlying cause of she"A" S/G Lo Lo Level~(</=174)was determined to be the Control Room operator's inability to control the"A" S/G level above its reactor trip setpoint due to the following contributing factors: The transient perturbations that were occurring due to design (i.e.the design of the FRVs to go full open, when in automatic mode, following a turbine trip, and the design of having the bypass FRVs open at the higher power levels).0 The shrink and swell phenomenon of the S/G water levels due to the above design induced perturba-tions and the transient induced perturbations.
HAC Soaks ttAA rtttl 4 4 IINC Notes~I$4$I 0 LICENSEE EVENT REPORT ILER)TEXT CONTINUATION V l.1VCLlAA 1$OVLATO1Y COMMI$$IO1 N ANNAOVlO OVNAO$I$O~ION lNNI1$$$I$I 1$NACILITY IIANlt Ill OOCIIlZ IIVINCCA Ill Ll1 IIINNC$1 I~I slavlseviAL M alv+IOAOl I$I R.E.Ginna Nuclear Power Plant TEXT IN'1INNN 1~.vNN OeeeaW IYNC/erat~$I I ITI 0 5IO 0 0 2 4 4 9 2-00 2-0 0 0 70'2 , ANALYSIS OF EV19iT This event is reportable in accordance with 10CFR50.73, Licensee Event Report system, item (a)(2)(iv), which requires reporting of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF)including the Reactor'rotection System (RPS)".The"A" S/G Lo Lo Level reactor trip was an automatic actuation of the RPS.An assessment was performed considering both the safety consequences.
and implications of this event with the following results and conclusions:
There were no safety consequences or implications attributed to the reactor trip because: o The two reactor trip breakers opened as required.o All control and shutdown rods inserted as designed.o The plant was stabilized at hot shutdown.The Ginna Updated Final Safety Analysis Report (UFSAR)Chapter 15.2.2,"Loss of External Electrical Load", was reviewed and compared to the plant response for this event.The plant is designed to accept a 50%loss of electrical load while operating at full power or a complete loss of electrical load while operating below 50%, without initiating a reactor trip.Although plant design can accept a 50%loss of load, past experience has'hown a vulnerability to S/G shrink and swell.Since the S/G main FRVs are placed in manual, actual plant response will be dependent upon operator response to indicated S/G level.Ginna UFSAR Chapter 15.2.2 evaluates the plant behavior for a complete loss of load from full power without a direct reactor trip, primarily to show the adequacy of the pressure-relieving devices and also to show that no core damage occurs.Complete loss of load analysis shows that DNBR does not drop below 2.0 and pressurizer pressure does not exceed 2500 psia.Only a small pressure spike (approxi-mately 30 psig)and a small temperature spike (2.5 F)was encountered during this transient.
wAC NOAIN$NAA I$44I
ISAC Tens 444A I4431 LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U.S.HUCLSAA ASOULATOAY CO>>>>ISSIOSI ASSAOYSO OU4'SO)ISO~IOs 4)ctiA 4$41SI SS FACILITY IIA>>4 Ill OOCIIST HUIS44A ISI T~AA LSA KUSA44A ISI SSQUSNT<AL U A ASYhlOR U SA SAO4 ISI R.E.Ginna Nuclear Power Plant TSXT/IT~>>S>>h>>SUse4.v>>>>h>>On>>hfISC A>>>>~'S1 1171 I 0 5 0 0 0 2 4 9 2 0 0 2-0 OF 1 2 Following the reactor trip, pressurizer'level decreased to approximately 54 level as a result of the cooldown.This is an expected observed'ransient.
The S/G levels both decreased to the narrow range taps.This is an expected transient based upon the encountered shrink in the S/Gs.A slow cooldown resulted during the post trip recovery period.This cooldown is bounded by the plant accident'nalysis and does not exceed the Technical Specification limit of 100 F per hour.Additional protection was provided by closure of the MSIVs.Based on the above and a review of post trip data and past plant transients, it can be concluded that the plant has operated as designed and that there'as no unreviewed safety questions and that the public's health and safety was assured at all times.CORRECTIVE ACTION A.ACTION TAKEN TO RRKZJBN AFFECTED SYSTEMS TO PRE-&TENT NORMAL STATUS: 0 The S/G levels were returned to their normal operating levels by addition of Auxiliary Feedwater, subsequent to the reactor trip.0 The"A" MSIV, manufactured by Atwood and Morrill, is a 30 inch air operated swing check valve, installed in the reverse direction to use S/G steam flow to ensure proper closure.As with any swing check valve, the closing moment must be large enough to overcome the friction on the valve shaft due to the valve packing-..Complete closure is accomplished by the force of the fluid flow on the valve disc.The"A" MSIV was subsequently stroked several times successfully to ensure operability and adequate closure capability.
Results of these tests support the conclusion that failure of the"A" MSIV to fully seat during the reactor trip was not due to internal valve distortion and bending, but was the result of a lack of flow across the valve disc.Failure to close is attributed to the closure operation occurring in a quiescent environment.
'eAC AOASI 444A iSWI Lh 0 IIAC tovv%CA 104ll UCENSEE EVENT REPORT{LER)TEXT CONTINUATION V l.IIVCLtAA AlCULATCAY CISALIIQQCII
/AitAOVEO OVI W)ISOWIOC E)ctiACS~ITI%S S*CILITY IIANI III DOCKCT IIVINIA ITI L41 IILNNI1 III vTAA SICVINTiAL VIVOS<V 1 V~ACE Iel R.E.Ginna Nuclear P'ower Plant 0 s 0 0 o 2 4 4 9 2-p p 2 p p ftXT W~~1~vm eeeaaeV IIAC AVVI~'ll IITl 0 90~1 2 Valve closure is dependent upon two factors: The moment, developed by the weight of the valve disc and the spring provided to assist in valve.closure, plus sufficient steam flow across the valve disc, without which the valve was not capable of completing its clc g operation.
When the demand signal for MSI~=o close was ger.ated d/p across the A MSIV was lower than th-.d/p across the B MSIV.The d/p across the B=.IV was enough to fully seat the valve while the d/p across the A MSIV did not provide enough force to overcome shaft packing frictional forces.Approximately 23 minutes later, the d/p across the A MSIV increased approximately 2 psid which resulted in complete closure of the valve.For all design basis accidents, where MSIV closure is required, the=-accident transients would develop a large enough differential pressure to obtain complete valve closure.RG&E is continuing to evaluate various packing materials which have a low friction coefficient and can perform the required sealing function.o The TDAFW pump was subsequently tested to determine the cause of the flow oscillations, but the test had to be aborted due to a steam leak on the governor valve.The governor valve was disassembled, inspected and placed back in service.The steam leak was the result of gasket leak (probably caused due to excessive travel of the governor valve).The gasket was replaced with a qualified spare.The cause of the flow oscillations was due to the"hunting" of the governor valve.The hunting of the governor valve was caused by a feedback nut being out of proper position., The position of the feedback nut was corrected and the TDAFW pump was subsequently tested successfully and returned to service.11C PCAIv~IIABI
IIAC t<<<<~IS45 I LICENSEE EVENT REPORT ILER)TEXT CONTINUATION M 5,~IICLSAA AlauLASOA V CO<<AIISSIOII Alt1OVSO OUI NO SISO~IO4 5)cttII55 SISI'SS FACILITY HAAIS I'l OOCIIS7 HUIAllA ISI Llll NIIIASSII I~I SSQMSle TILL~U 8'IYCIOR<<SA AAOl ISI R.E.Ginna Nuclear Power Plant o s o o o 2 4 4 9 2 p 2 p p raXt W~eeae e~.v<<~+AC A<<~'iI Im 1 poi:1 2 0 0 As the Intermediate Range" NIS Channel N-35 tracked NIS Channel N-36 for, its normal operating range.and returned to normal approximately ten (10)hours after the trip, no immediate action was deemed necessary.
This abnormality has been observed and researched extensively in the past in cooperation with the NSSS vendor, Westinghouse.
No technical basis has been identified as to why the 10 E-11 idle current does not maintain indication at 10 E-11 amps;RG&E and Westinghouse concurred that the channel was operable and capable of performing all intended functions.
Further evaluations of the response characteris-tics of NIS channel N-35 will be performed during the 1992 Annual Refueling and Maintenance Outage.This event was initiated by a main generator trip due to loss of excitation.
Extensive examination, evaluation and testing was performed on the main generator voltage control system, with the following results and conclusions:
The automatic and manual voltage control units were extensively tested and found to operate satisfactorily.
The Minimum Excitation Limiter (MEL)data taken during the testing indicated that the setting was too close to normal operating points of the generator.
A new MEL setting was calculated, reviewed by.Westinghouse (the vendor)and implemented.
The revised setting will allow operation to approximately 190 MVAR underexcited at 500 MW.h1C BOA<<SASA il4$I l 4 IIAC IVn XW IS@)I LICENSEE EVENT REPORT (LERI TEXT CONTINUATION V,l.HVCLSAA ASOULATOISY COWHISSIOII J AttrOvlO OUS eO)ISOMI04 SIctirlS SI)I'IS AACILITY HAAIS III OOCIIlt HUUl1 111 Llr IIUMOlr I~I~AOl I)I R.E.Ginna Nuclear Power Plant 0 5 o 0 o 2 4 4 9 tt)IT IIt rrn~r never.vn rrreenr rrC Attn~s I I m S~Ovlrt<AL e v-0 0 2-0 0 110'2 The unit was synchronized to the system with the-voltage regulator in manual and no unusual events were noted.When the voltage regulator was placed in the-automatic mode, the loop within the voltage regulator system was unstable and the voltage regulator was returned to the manual mode.The operation of the voltage regulator damping module was verified and the gain was reduced from maximum setting to the mid point on the potentiometer.
The voltage regulator was returned to the automatic mode and operated satisfactorily.
The plant has now operated at approximately full power and has gone through several normal voltage adjustments such as lowering the voltaqe in the evening and raising the voltage in the morning as required by system load.No abnormalities.
have been encountered.
B.ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
As the underlying cause of the event was determined to be the inability of the Control Room operator to control the"A" S/G leve~above its reactor trip setpoint due to design and transient induced level perturbation, the following actions have been taken or are being planned: 0 Applicable operating procedures have been changed to require that the bypass FRVs be placed in manual closed when increasing above approximately 304 reactor power.0 Applicable operating procedures have been changed to require returning the bypass FRVs to automatic control when decreasing below 304 reactor power.eAC JOAN)SAA il4)1
IIAC Isrse lAAA 104lI LICENSEE EVENT REPORT ILER)TEXT CONTINUATION v l.eevCLlAII AlOULATCAY coseseeClloee
/AASSOvlo Ovl eeo IISOWIOe l>eseAl5~rlI TS I'ACILITY IIAIIl III OOCIIKT eeULQlA 111 LlA IIUAOlA I~I v TAA SloulreveAL SAVes~are v er U~s~Aol IQ R.E.Ginna Nuclear Power.Plant 0 6<<o 2 4 4 TKXT rrr rsrers~r~.vm e seseeeer rrreC Arse~'gr IITI 9 2-0 0 2-1 2o~1 2 o A modification is planned for the 1993 Annual Refueling and Maintenance Outage that would modify the existing feedwater isolation logic for fail-open or fail-closed of the main and bypass FRVs upon turbine trip with main FRVs in automatic control mode.The planned modification will delete the existing fail-open logic and replace the fail-closed logic with actuation upon reactor trip as opposed to turbine trip.As the event was initiated by the Main Generator trip due to loss of excitation, the following actions are planned to prevent recurrence'.
0 0 RG&E is planning to purchase and install a replacement voltage regulator unit.I Routine testing and maintenance will be performed on the existing voltage regulator unit during the 1992 Annual Refueling and Maintenance Outage to attain a high degree of confidence that the unit will operate without incident for the entire fuel cycle.ADDITIONAL INFORMATION A.FAILED COMPONENTS:
The TDAFW pump turbine is a 465 horsepower noncondensing steam turbine, serial number 26635, manufactured by the Worthington Corporation.
B.PREVIOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same underlying cause at Ginna Station could be identified.
C.SPECIAL COMMENTS: None.~eAC SOAee 1AAA rl4lI