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| {{#Wiki_filter:As Indian Point Energy Center Status Report June 6, 2006 Operational Status IP2 is currently at 100% reactor power; the unit has been on line for 19 days and Unit 3 is operating at 100% reactor power and has been on-line for 247 days.Groundwater Investigation | | {{#Wiki_filter:As Indian Point Energy Center Status Report June 6, 2006 Operational Status IP2 is currently at 100% reactor power; the unit has been on line for 19 days and Unit 3 is operating at 100% reactor power and has been on-line for 247 days. |
| -MW-42 Well Entergy released updated/corrected sample results today from a series of samples obtained from MW- "MW-42 9 42, which is located adjacent to the Unit I spent fuel pool. The results show isotopes characteristic of North curtain drain water. (See diagram showing updated sample results). | | Groundwater Investigation - MW-42 Well Entergy released updated/corrected sample results today from a series of samples obtained from MW- "MW-42 9 42, which is located adjacent to the Unit I spent fuel pool. The results show isotopes characteristic of North curtain drain water. (See diagram showing updatedsample results). Hydrologists are investigating the possibility that the well intercepted a section of the North curtain drains at Unit 1. The updated sample results do not affect the bounding dose calculations. Results for tritium are lower than previously reported although the Cesium numbers are higher. An additional sample taken on April 7 showed results consistent with the 1020001 corrected data from March 23/24. 1 MW-42 @ 49' Sampled 19 49' April 7, 2006 L.IL..J d Results in pCi/L r H-3 3980 Sr-90 74.6 Cs-137 5310 Co-60 67.2 Entergy has initiated actions to reduce the I: |
| Hydrologists are investigating the possibility that the well intercepted a section of the North curtain drains at Unit 1. The updated sample results do not affect the bounding dose calculations. | | concentration of Sr-90 in the Unit 1 spent fuel1" pool. Deminieralizers connected to the pool will ,: J, help reduce the amount of Sr-90 in the pool and thus the amount which is captured by the curtain drains. Entergy is evaluating additional processing Samples taken 3/23-24/2006 in the curtain drains to further reduce the Sr-90 Correctedresults are in green. |
| Results for tritium are lower than previously reported although the Cesium numbers are higher. An additional sample taken on April 7 showed results consistent with the 1020001 corrected data from March 23/24. 1 MW-42 @ 49' Sampled 19 49'April 7, 2006 L.IL..J d Results in pCi/L r H-3 3980 Sr-90 74.6 Cs-137 5310 Co-60 67.2 Entergy has initiated actions to reduce the I: concentration of Sr-90 in the Unit 1 spent fuel1" pool. Deminieralizers connected to the pool will ,: J, help reduce the amount of Sr-90 in the pool and thus the amount which is captured by the curtain drains. Entergy is evaluating additional processing Samples taken 3/23-24/2006 in the curtain drains to further reduce the Sr-90 Corrected results are in green.concentration. | | concentration. These actions are being taken in advance Previously reportedtritium value of any overall site remediation plan and will enhance the was 261,000pCi/L and the Cs-137 effectiveness of which ever strategy maybe employed, number was 10,200pCi/L.All results in pCi/L |
| These actions are being taken in advance Previously reported tritium value of any overall site remediation plan and will enhance the was 261,000pCi/L and the Cs-137 effectiveness of which ever strategy maybe employed, number was 10,200pCi/L. | | / |
| All results in pCi/L/(if) | | (if) |
| | |
| ~Enler~gy Tracer tests, mentioned above, will help evaluate the effectiveness of the Sr-90 processing. | | ~Enler~gy Tracer tests, mentioned above, will help evaluate the effectiveness of the Sr-90 processing. |
| No radioactivity has been detected in any off-site monitoring location.Educational Outreach Entergy Nuclear Northeast provides customized outreach education programs for schools, youth groups, and civic organizations. | | No radioactivity has been detected in any off-site monitoring location. |
| The topics we cover include Emergency Planning, Understanding Radiation, Nuclear Fuel and a general overview of the operations of Indian Point Energy Center. If you would like a brochure or are interested in scheduling a program, contact IPEC Communications at 914-271-7441. | | Educational Outreach Entergy Nuclear Northeast provides customized outreach education programs for schools, youth groups, and civic organizations. The topics we cover include Emergency Planning, Understanding Radiation, Nuclear Fuel and a general overview of the operations of Indian Point Energy Center. If you would like a brochure or are interested in scheduling a program, contact IPEC Communications at 914-271-7441. |
| If you have any questions or need clarification of the information provided, please contact Kathy McMullin, manager of communications, Indian Point Energy Center, at 914-271-7132.}} | | If you have any questions or need clarification of the information provided, please contact Kathy McMullin, manager of communications, Indian Point Energy Center, at 914-271-7132.}} |
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Category:Status Report
MONTHYEARML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status L-24-007, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations – Holtec Decommissioning International, LLC (HDI)2024-03-29029 March 2024 Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations – Holtec Decommissioning International, LLC (HDI) L-22-022, and Indian Point Nuclear Generating Stations 1, 2, & 3 - Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations - Holtec.2022-03-25025 March 2022 and Indian Point Nuclear Generating Stations 1, 2, & 3 - Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations - Holtec. L-21-134, and Indian Point Nuclear Generating Stations 1, 2, & 3 - Report on Status of Decommissioning Funding for Independent Spent Fuel Storage Installations2021-12-17017 December 2021 and Indian Point Nuclear Generating Stations 1, 2, & 3 - Report on Status of Decommissioning Funding for Independent Spent Fuel Storage Installations ML21084A7892021-03-25025 March 2021 Entergy Nuclear Operations, Inc. Status of Funding for Managing Irradiated Fuel for Year Ending December 31, 2020 - 10 CFR 50.82(a)(8)(vii) CNRO-2019-00006, Stations - Status of Funding for Managing Irradiated Fuel for Year Ending December 31, 2018 - 10 CFR 50.82(a)(8)(vii) - Entergy Nuclear Operations, Inc2019-03-28028 March 2019 Stations - Status of Funding for Managing Irradiated Fuel for Year Ending December 31, 2018 - 10 CFR 50.82(a)(8)(vii) - Entergy Nuclear Operations, Inc CNRO-2019-00005, Stations - Decommissioning Funding Status Report Per 10 CFR 50.75(f)(1) and 10 CFR 50.82(a)(8)(v) - Entergy Nuclear Operations, Inc2019-03-28028 March 2019 Stations - Decommissioning Funding Status Report Per 10 CFR 50.75(f)(1) and 10 CFR 50.82(a)(8)(v) - Entergy Nuclear Operations, Inc ML18088B2462018-03-29029 March 2018 Status of Funding for Managing Irradiated Fuel for Year Ending December 31, 2017, Per 10 CFR 50.82(a)(8)(vii) CNRO-2017-00009, Entergy Nuclear Operations, Inc. - Decommissioning Funding Status Report Per 10 CFR 50.75(f)(1) and 10 CFR 50.82(a)(8)(v)2017-03-31031 March 2017 Entergy Nuclear Operations, Inc. - Decommissioning Funding Status Report Per 10 CFR 50.75(f)(1) and 10 CFR 50.82(a)(8)(v) ENOC-17-00006, Status of Funding for Managing Irradiated Fuel for Year Ending December 31, 2016 - 10 CFR 50.82(a)(8)(vii)2017-03-30030 March 2017 Status of Funding for Managing Irradiated Fuel for Year Ending December 31, 2016 - 10 CFR 50.82(a)(8)(vii) NL-16-024, Center'S Sixth Six-Month Status Report for the Implementation of Order EA-12-049 Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events2016-02-29029 February 2016 Center'S Sixth Six-Month Status Report for the Implementation of Order EA-12-049 Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events NL-15-111, Implementation of Order EA-12-051 Modifying Licenses with Regard to Requirements for to Reliable Spent Fuel Pool Instrumentation2015-08-28028 August 2015 Implementation of Order EA-12-051 Modifying Licenses with Regard to Requirements for to Reliable Spent Fuel Pool Instrumentation NL-15-112, Fifth Six-Month Status Report for the Implementation of Order EA-12-049 Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events2015-08-28028 August 2015 Fifth Six-Month Status Report for the Implementation of Order EA-12-049 Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events NL-15-026, Fourth Six-Month Status Report for the Implementation of Order EA-12-051 Modifying Licenses with Regard to Requirements for Reliable Spent Fuel Pool Instrumentation2015-02-27027 February 2015 Fourth Six-Month Status Report for the Implementation of Order EA-12-051 Modifying Licenses with Regard to Requirements for Reliable Spent Fuel Pool Instrumentation NL-14-059, Status of Planned Resolutions of the Unapproved III.G.2 Operator Manual Actions2014-04-29029 April 2014 Status of Planned Resolutions of the Unapproved III.G.2 Operator Manual Actions ENOC-14-00009, Decommissioning Funding Status Report Per 10 CFR Section 50.75(f)(1) and 10 CFR 50.82(a)(8)(v) - Entergy Nuclear Operations, Inc2014-03-28028 March 2014 Decommissioning Funding Status Report Per 10 CFR Section 50.75(f)(1) and 10 CFR 50.82(a)(8)(v) - Entergy Nuclear Operations, Inc NL-14-031, Center'S Second Six-Month Status Report for the Implementation of Order EA-12-049 Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events2014-02-27027 February 2014 Center'S Second Six-Month Status Report for the Implementation of Order EA-12-049 Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events NL-14-029, Second Six-Month Status Report for the Implementation of Order EA-12-051, Modifying Licenses with Regard to Requirements for Reliable Spent Fuel Pool Instrumentation2014-02-27027 February 2014 Second Six-Month Status Report for the Implementation of Order EA-12-051, Modifying Licenses with Regard to Requirements for Reliable Spent Fuel Pool Instrumentation NL-13-109, First Six-Month Status Report for the Implementation of Order EA-12-051 Modifying Licenses with Regard to Requirements for to Reliable Spent Fuel Pool Instrumentation2013-08-27027 August 2013 First Six-Month Status Report for the Implementation of Order EA-12-051 Modifying Licenses with Regard to Requirements for to Reliable Spent Fuel Pool Instrumentation NL-13-110, First Six-Month Status Report for the Implementation of Order EA-12-049 Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events2013-08-27027 August 2013 First Six-Month Status Report for the Implementation of Order EA-12-049 Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events NL-13-072, Status of Planned Resolutions of the Unapproved III.G.2 Operator Manual Actions2013-05-0202 May 2013 Status of Planned Resolutions of the Unapproved III.G.2 Operator Manual Actions ENOC-13-00007, Decommissioning Funding Status Report Per 10 CFR Section 50.75(f)(1) and 10 CFR 50.82(a)(8)(v) - Entergy Nuclear Operations, Inc2013-03-29029 March 2013 Decommissioning Funding Status Report Per 10 CFR Section 50.75(f)(1) and 10 CFR 50.82(a)(8)(v) - Entergy Nuclear Operations, Inc ENOC-13-00011, Status of Funding for Managing Irradiated Fuel for Year Ending December 31, 2012 - 10 CFR 50.82(a)(8)(vii)2013-03-29029 March 2013 Status of Funding for Managing Irradiated Fuel for Year Ending December 31, 2012 - 10 CFR 50.82(a)(8)(vii) ML12137A1362012-05-29029 May 2012 Decommissioning Funding Status Report ML12137A1052012-05-29029 May 2012 Decommissioning Funding Status Report ML12137A0902012-05-29029 May 2012 Decommissioning Funding Status Report ML12122A0712012-05-14014 May 2012 Enclosure 1: April 2012 Report on the Status of Public Petitions Under Title 10 of the Code of Federal Regulations, Section 2.206 ENOC-11-00005, Status of Decommissioning Funding for Plants Operated by Entergy Nuclear Operations, Inc., for Year Ending December 31, 2010 - 10 CFR 50.75(f)(1)2011-03-31031 March 2011 Status of Decommissioning Funding for Plants Operated by Entergy Nuclear Operations, Inc., for Year Ending December 31, 2010 - 10 CFR 50.75(f)(1) ML1029403622010-11-12012 November 2010 October 2010 10 CFR 2.206 Monthly Status Report: Enclosures ENOC-10-00010, Entergy Nuclear Operations, Inc. - Status of Decommissioning Funding for Year Ending December 31, 20092010-03-31031 March 2010 Entergy Nuclear Operations, Inc. - Status of Decommissioning Funding for Year Ending December 31, 2009 ML1100404362009-09-16016 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 09/16/2009 ML0830800812008-11-20020 November 2008 October 2008 Report on the Status of Public Petitions Under Title 10 of the Code of Federal Regulations (10 CFR) Section 2.206- Enclosures ML0905708302008-11-0505 November 2008 Entergy Center Status Report NL-08-131, Siren Project Status Update2008-08-12012 August 2008 Siren Project Status Update NL-08-121, Siren Project Milestone Schedule - Status Update, Letter Dated 07/25/082008-07-25025 July 2008 Siren Project Milestone Schedule - Status Update, Letter Dated 07/25/08 ENOC-08-00028, J.A. FitzPatrick, Palisades, and Big Rock Point, Decommissioning Fund Status Report2008-05-0808 May 2008 J.A. FitzPatrick, Palisades, and Big Rock Point, Decommissioning Fund Status Report ML0729506172007-09-13013 September 2007 E-mail from K. Mcmullin, Entergy to J. Boska, NRR Et Al on IPEC Status Report, September 13, 2007 ML0729705242007-08-0707 August 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for Aug 7 2007 ML0729705222007-08-0606 August 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for Aug 6 2007 ML0729705042007-07-31031 July 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for July 31 2007 ML0729704422007-07-27027 July 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for July 27, 2007 ML0729704332007-07-26026 July 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for July 26 ML0729703852007-07-18018 July 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for July 18 2007 ML0729506092007-06-11011 June 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for June 11, 2007 ML0729506082007-06-0707 June 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for June 7, 2007 ML0729506032007-06-0505 June 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding Indian Point Energy Center Status Report, June 5, 2007 ML0729506002007-06-0101 June 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for June 1, 2007 ML0729505982007-05-31031 May 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for May 31, 2007 ML0729505922007-05-30030 May 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for May 30, 2007 ML0729505912007-05-29029 May 2007 E-mail from K. Mcmullin of Entergy to Various, Regarding IPEC Status Report for May 29, 2007 2024-09-18
[Table view] |
Text
As Indian Point Energy Center Status Report June 6, 2006 Operational Status IP2 is currently at 100% reactor power; the unit has been on line for 19 days and Unit 3 is operating at 100% reactor power and has been on-line for 247 days.
Groundwater Investigation - MW-42 Well Entergy released updated/corrected sample results today from a series of samples obtained from MW- "MW-42 9 42, which is located adjacent to the Unit I spent fuel pool. The results show isotopes characteristic of North curtain drain water. (See diagram showing updatedsample results). Hydrologists are investigating the possibility that the well intercepted a section of the North curtain drains at Unit 1. The updated sample results do not affect the bounding dose calculations. Results for tritium are lower than previously reported although the Cesium numbers are higher. An additional sample taken on April 7 showed results consistent with the 1020001 corrected data from March 23/24. 1 MW-42 @ 49' Sampled 19 49' April 7, 2006 L.IL..J d Results in pCi/L r H-3 3980 Sr-90 74.6 Cs-137 5310 Co-60 67.2 Entergy has initiated actions to reduce the I:
concentration of Sr-90 in the Unit 1 spent fuel1" pool. Deminieralizers connected to the pool will ,: J, help reduce the amount of Sr-90 in the pool and thus the amount which is captured by the curtain drains. Entergy is evaluating additional processing Samples taken 3/23-24/2006 in the curtain drains to further reduce the Sr-90 Correctedresults are in green.
concentration. These actions are being taken in advance Previously reportedtritium value of any overall site remediation plan and will enhance the was 261,000pCi/L and the Cs-137 effectiveness of which ever strategy maybe employed, number was 10,200pCi/L.All results in pCi/L
/
(if)
~Enler~gy Tracer tests, mentioned above, will help evaluate the effectiveness of the Sr-90 processing.
No radioactivity has been detected in any off-site monitoring location.
Educational Outreach Entergy Nuclear Northeast provides customized outreach education programs for schools, youth groups, and civic organizations. The topics we cover include Emergency Planning, Understanding Radiation, Nuclear Fuel and a general overview of the operations of Indian Point Energy Center. If you would like a brochure or are interested in scheduling a program, contact IPEC Communications at 914-271-7441.
If you have any questions or need clarification of the information provided, please contact Kathy McMullin, manager of communications, Indian Point Energy Center, at 914-271-7132.