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{{#Wiki_filter:August 5, 2008  
{{#Wiki_filter:UNITED STATES
  EA-08-190  
                                NUC LE AR RE G UL AT O RY C O M M I S S I O N
                                                    R E GI ON I V
Mr. Adam C. Heflin, Senior Vice   President and Chief Nuclear Officer Union Electric Company P.O. Box 620 Fulton, MO 65251  
                                        612 EAST LAMAR BLVD , SU I TE 400
                                        AR LI N GTON , TEXAS 76011-4125
                                                  August 5, 2008
EA-08-190
Mr. Adam C. Heflin, Senior Vice
  President and Chief Nuclear Officer
Union Electric Company
P.O. Box 620
Fulton, MO 65251
SUBJECT: CALLAWAY PLANT - NRC INTEGRATED INSPECTION
              REPORT AND NOTICE OF VIOLATION 05000483/2008003
Dear Mr. Heflin:
On June 24, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated
inspection at your Callaway Plant. The enclosed report documents the inspection results, which
were discussed on June 24, 2008, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
Based on the results of this inspection, one violation is cited in the enclosed Notice of
Violation (Notice) and the circumstances surrounding this violation are described in detail in the
enclosed report. The violation involved failure to implement corrective actions to preclude the
repetition of void formation in the emergency core cooling piping (EA-08-190). Although
determined to be of very low safety significance (Green), this violation is being cited because
one of the criteria specified in Section VI.A.1 of the NRC Enforcement Policy for a noncited
violation was satisfied. Specifically, AmerenUE failed to restore compliance within a reasonable
time after the violation was last identified in NRC Inspection Report 05000483/2006002-012.
Please note that you are required to respond to this letter and should follow the instructions
specified in the enclosed Notice when preparing your response. The NRC will use your
response, in part, to determine whether further enforcement action is necessary to ensure
compliance with regulatory requirements.
This report also documents four NRC-identified and self-revealing findings of very low safety
significance (Green). These findings were determined to involve violations of NRC
requirements. Additionally, two licensee-identified violations which were determined to be of
very low safety significance are listed in this report. However, because of the very low safety
significance and because they were entered into your corrective action program, the NRC is
treating these findings as NCVs consistent with Section VI.A of the NRC Enforcement Policy. If
you contest these NCVs, you should provide a response within 30 days of the date of this
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,


SUBJECT: CALLAWAY PLANT - NRC INTEGRATED INSPECTION        REPORT AND NOTICE OF VIOLATION 05000483/2008003 Dear Mr. Heflin: On June 24, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Callaway Plant. The enclosed report documents the inspection results, which were discussed on June 24 , 2008 , with you and other members of your staff.  
Union Electric Company                    -2-
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. 
ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional
Administrator, U.S. Nuclear Regulatory Commission Region IV, 612 East Lamar Drive,
Suite 400, Arlington, Texas 76011-4125; the Director, Office of Enforcement, U.S. Nuclear
Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at the
Callaway Plant.
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its
enclosures will be made available electronically for public inspection in the NRC Public
Document Room or from the Publicly Available Records component of NRCs document system
(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the
Public Electronic Reading Room).
                                            Sincerely,
                                                    /RA/
                                            Vincent G. Gaddy, Chief,
                                            Projects Branch B
                                            Division of Reactor Projects
Docket: 50-483
License: NPF-30
Enclosures: Notice of Violation and
NRC Inspection Report 05000483/2008003
  w/attachment: Supplemental Information
cc w/enclosure:                                      Rick A. Muench, President and
John ONeill, Esq.                                    Chief Executive Officer
Pillsbury Winthrop Shaw Pittman LLP                  Wolf Creek Nuclear Operating Corporation
2300 N. Street, N.W.                                P.O. Box 411
Washington, DC 20037                                Burlington, KS 66839
Scott A. Maglio, Assistant Manager                  Kathleen Smith, Executive Director and
  Regulatory Affairs                                Kay Drey, Representative Board of
AmerenUE                                            Directors
P.O. Box 620                                        Missouri Coalition for the Environment
Fulton, MO 65251                                    6267 Delmar Boulevard, Suite 2E
                                                    St. Louis City, MO 63130
Missouri Public Service Commission
Governors Office Building                          Lee Fritz, Presiding Commissioner
200 Madison Street                                  Callaway County Courthouse
P.O. Box 360                                        10 East Fifth Street
Jefferson City, MO 65102-0360                        Fulton, MO 65251
H. Floyd Gilzow                                      Les H. Kanuckel, Manager
Deputy Director for Policy                          Quality Assurance
Missouri Department of Natural Resources            AmerenUE
P. O. Box 176                                        P.O. Box 620
Jefferson City, MO 65102-0176                        Fulton, MO 65251


Based on the results of this inspection, one violation is cited in the enclosed Notice of Violation (Notice) and the circumstances surrounding this violation are described in detail in the enclosed report.  The violation involved failure to implement corrective actions to preclude the repetition of void formation in the emergency core cooling piping (EA-08-190).  Although
Union Electric Company                  -3-
determined to be of very low safety significance (Green), this violation is being cited because one of the criteria specified in Section VI.A.1 of the NRC Enforcement Policy for a noncited violation was satisfied. Specifically, AmerenUE failed to restore compliance within a reasonable time after the violation was last identified in NRC Inspection Report 05000483/2006002-012. Please note that you are required to respond to this letter and should follow the instructions
Director, Missouri State Emergency          Certrec Corporation
specified in the enclosed Notice when preparing your response. The NRC will use your response, in part, to determine whether further enforcement action is necessary to ensure compliance with regulatory requirements.
  Management Agency                          4200 South Hulen, Suite 422
This report also documents four NRC-identified and self-revealing findings of very low safety significance (Green).  These findings were determined to involve violations of NRC requirements. Additionally, two licensee-identified violations which were determined to be of
P.O. Box 116                                Fort Worth, TX 76109
very low safety significance are listed in this report.  However, because of the very low safety significance and because they were entered into your corrective action program, the NRC is treating these findings as NCVs consistent with Section VI.A of the NRC Enforcement Policy.  If you contest these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, UNITED STATESNUCLEAR REGULATORY COMMISSIONREGION IV612 EAST LAMAR BLVD, SUITE 400ARLINGTON, TEXAS 76011-4125
Jefferson City, MO 65102-0116
Union Electric Company - 2 -
                                            Keith G. Henke, Planner III
  ATTN:  Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission Region IV, 612 East Lamar Drive, Suite 400, Arlington, Texas  76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at the Callaway Plant.
Scott Clardy, Director                      Division of Community and Public Health
Section for Environmental Public Health    Office of Emergency Coordination
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosures will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Missouri Department of Health and          Missouri Department of Health and
Senior Services                            Senior Services
P.O. Box 570                                930 Wildwood,
Jefferson City, MO 65102-0570              P.O. Box 570
                                            Jefferson City, MO 65102
Luke H. Graessle, Manager
  Regulatory Affairs                        Technical Services Branch Chief
AmerenUE                                    FEMA Region VII
P.O. Box 620                                2323 Grand Boulevard, Suite 900
Fulton, MO 65251                            Kansas City, MO 64108-2670
Thomas B. Elwood, Supervising Engineer      Ronald L. McCabe, Chief
  Regulatory Affairs and Licensing          Technological Hazards Branch
AmerenUE                                    National Preparedness Division
P.O. Box 620                                DHS/FEMA
Fulton, MO 65251                            9221 Ward Parkway, Suite 300
                                            Kansas City, MO 64114-3372


Sincerely,   /RA/  Vincent G. Gaddy, Chief,  Projects Branch B
Union Electric Company                      -4-
Division of Reactor Projects
Electronic distribution by RIV:
  Docket50-483  License: NPF-30 
Regional Administrator (Elmo.Collins@nrc.gov)
   
DRP Director (Dwight.Chamberlain@nrc.gov)
Enclosures: Notice of Violation and NRC Inspection Report 05000483/2008003  w/attachment:  Supplemental Information
DRS Director (Roy.Caniano@nrc.gov)
  cc w/enclosure:  
DRS Deputy Director (Troy.Pruett@nrc.gov)
John O'Neill, Esq. Pillsbury Winthrop Shaw Pittman LLP 2300 N. Street, N.W. Washington, DC 20037
Senior Resident Inspector (David.Dumbacher@nrc.gov)
   
Branch Chief, DRP/B (Vincent.Gaddy@nrc.gov)
Scott A. Maglio, Assistant Manager  Regulatory Affairs AmerenUE P.O. Box 620 Fulton, MO  65251
Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)
Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)
Only inspection reports to the following:
DRS STA (Dale.Powers@nrc.gov)
M. Cox, OEDO RIV Coordinator (Mark.Cox@nrc.gov)
OEMail.Resource@nrc.gov
Enforcement Officer (Michael.Vasquez@nrc.gov)
Chief Allegation Coordination/Enforcement Staff (William.Jones@nrc.gov)
Office of Enforcement (Alexander.Sapountizis@nrc.gov)
ROPreports
CWY Site Secretary (Dawn.Yancey@nrc.gov)
SUNSI Review Completed: VGG ADAMS: ; Yes No                      Initials: __VGG__
;Publicly Available        Non-Publicly Available Sensitive  ;Non-Sensitive
R:\_Reactors\_CW\2008\CW 2008003RP-DED.doc                              ML 082180851
  RIV:SRI:DRP/B          C:DRS/OB        C:DRS/PSB1      C:DRS/EB2              C:DRS/EB1
  DDumbacher            RELantz        MPShannon      NFO'Keefe              RLBywater
  /RA/ VGGaddy for      /RA/            /RA/            /RA/ MFRunyan for      /RA/
07/29/2008            07/9/2008      07/14/2008      07/15/2008            07/11/2008
  C:DRS/PSB2            DRS/SRA        ACES            C:DRP/B                D:DRP
  GEWerner              DPLoveless      GMVasquez      VGGaddy                DDChamberlain
  /RA/                  /RA/            /RA/            /RA/                  /RA/
07/17/2008            07/15/2008      07/24/2008      08/5/2008              07/28/2008
OFFICIAL RECORD COPY                                  T=Telephone        E=E-mail      F=Fax


Missouri Public Service Commission Governor's Office Building 200 Madison Street P.O. Box 360 Jefferson City, MO  65102-0360
                                        NOTICE OF VIOLATION
AmerenUE                                                                Docket 50-483
H. Floyd Gilzow Deputy Director for Policy Missouri Department of Natural Resources P. O. Box 176 Jefferson City, MO  65102-0176
Callaway Plant                                                          License NPF-30
                                                                        EA-08-190
During an NRC inspection conducted March 24 through June 24, 2008, a violation of NRC
requirements was identified. In accordance with the NRC Enforcement Policy, the violation is
listed below:
        10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that
        measures shall be established to ensure that, for significant conditions adverse to
        quality, the cause of the condition is determined and corrective action taken to preclude
        repetition.
        Contrary to this, from December 26, 2006, through May 21, 2008, the licensee failed to
        take corrective actions to preclude repetition of safety-related emergency core cooling
        system pipe voiding, and the licensee determined that this condition was a significant
        condition adverse to quality.
This violation is associated with a Green Significance Determination Process finding.
Pursuant to the provisions of 10 CFR 2.201, AmerenUE is hereby required to submit a written
statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document
Control Desk, Washington, DC 20555 with a copy to the Regional Administrator, Region IV,
and a copy to the NRC Senior Resident Inspector at the facility that is the subject of this Notice
of Violation (Notice), within 30 days of the date of the letter transmitting this Notice. This reply
should be clearly marked as a "Reply to Notice of Violation EA-08-190," and should include:
(1) the reason for the violation, or, if contested, the basis for disputing the violation or severity
level, (2) the corrective steps that have been taken and the results achieved, (3) the corrective
steps that will be taken to avoid further violations, and (4) the date when full compliance will be
achieved. Your response may reference or include previous docketed correspondence, if the
correspondence adequately addresses the required response. If an adequate reply is not
received within the time specified in this Notice, an order or a Demand for Information may be
issued as to why the license should not be modified, suspended, or revoked, or why such other
action as may be proper should not be taken. Where good cause is shown, consideration will
be given to extending the response time.
If you contest this enforcement action, you should also provide a copy of your response, with
the basis for your denial, to the Director, Office of Enforcement, United States Nuclear
Regulatory Commission, Washington, DC 20555-0001.
Because your response will be made available electronically for public inspection in the NRC
Public Document Room or from the NRCs document system (ADAMS), accessible from the
NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not
include any personal privacy, proprietary, or safeguards information so that it can be made
available to the public without redaction. If personal privacy or proprietary information is
necessary to provide an acceptable response, then please provide a bracketed copy of your
response that identifies the information that should be protected and a redacted copy of your
response that deletes such information. If you request withholding of such material, you must
specifically identify the portions of your response that you seek to have withheld and provide in
                                              -1-                                         Enclosure 1


Rick A. Muench, President and    Chief Executive Officer Wolf Creek Nuclear Operating Corporation P.O. Box 411 Burlington, KS  66839
detail the bases for your claim of withholding (e.g., explain why the disclosure of information will
create an unwarranted invasion of personal privacy or provide the information required by
Kathleen Smith, Executive Director and  Kay Drey, Representative Board of Directors Missouri Coalition for the Environment 6267 Delmar Boulevard, Suite 2E
10 CFR 2.390(b) to support a request for withholding confidential commercial or financial
St. Louis City, MO  63130
information). If safeguards information is necessary to provide an acceptable response, please
Lee Fritz, Presiding Commissioner Callaway County Courthouse 10 East Fifth Street Fulton, MO 65251
provide the level of protection described in 10 CFR 73.21.
Dated this  5th    day of July 2008
Les H. Kanuckel, Manager Quality Assurance AmerenUE P.O. Box 620 Fulton, MO  65251
                                            -2-                                        Enclosure 1


 
                  U.S. NUCLEAR REGULATORY COMMISSION
Union Electric Company - 3 -
                                    REGION IV
  Director, Missouri State Emergency   Management Agency P.O. Box 116 Jefferson City, MO 65102-0116
Docket:      50-483
  Scott Clardy, Director
License:    NPF-30
Section for Environmental Public Health Missouri Department of Health and    Senior Services P.O. Box 570 Jefferson City, MO 65102-0570
Report:      05000483/2008003
Licensee:    Union Electric Company
Facility:    Callaway Plant
Location:   Junction Highway CC and Highway O
            Fulton, MO
Dates:      March 25 - June 24, 2008
Inspectors: D. Dumbacher, Senior Resident Inspector
            J. Groom, Resident Inspector
            J. Drake, Senior Reactor Inspector, Plant Support, Branch 2
            G. Guerra, CHP, Health Physicist, Plant Support Branch 1
Approved By: V. Gaddy, Chief, Project Branch B
            Division of Reactor Projects
                                    -1-                                 Enclosure 2


Luke H. Graessle, Manager  Regulatory Affairs AmerenUE P.O. Box 620 Fulton, MO  65251
                                      SUMMARY OF FINDINGS
IR 05000483/2008003: 3/25 - 6/24/2008; Callaway Plant, Operability Evaluations,
Thomas B. Elwood, Supervising Engineer  Regulatory Affairs and Licensing AmerenUE P.O. Box 620 Fulton, MO  65251
Postmaintenance Testing, Surveillance Testing, and Identification and Resolution of Problems.
This report covered a 3-month period of inspection by resident inspectors. The significance of
most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual
Chapter 0609, "Significance Determination Process." Findings for which the Significance
Determination Process does not apply may be Green or assigned a severity level after NRC
management review. The NRCs program for overseeing the safe operation of commercial
nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,
dated December 2006.
A.      NRC-Identified and Self-Revealing Findings
        Cornerstone: Mitigating Systems
        *      Green. The inspectors identified a noncited violation of Technical
              Specification 3.5.2, "Emergency Core Cooling Systems," after an inadequate
              surveillance procedure resulted in the licensee failing to maintain the emergency
              core cooling system full of water as required per Technical Specification 3.5.2.
              On May 21, 2008, Callaway Plant engineering discovered that a section of the
              cold leg recirculation piping, specifically the discharge of the residual heat
              removal pumps to the safety injection pumps, contained 6.6 cubic feet of air.
              Callaway monthly surveillance Procedure OSP-SA-00003, "Emergency Core
              Cooling Flow Path Verification and Venting," had a purpose to: "Verify the ECCS
              is full of water," in accordance with Technical Specification Surveillance
              Requirement 3.5.2.3. The monthly verification and vent procedure was not
              comprehensive enough to ensure all the emergency core cooling system was full
              of water.
              This finding was more than minor because it was similar to Example 3e of NRC
              Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues," and
              met the Not Minor If, criteria because the failure to meet the licensees
              administrative requirement for allowable void fraction impacted the ability of the
              Train A safety injection system to function upon initiation of high-pressure
              recirculation. This finding affected the mitigating systems cornerstone procedure
              quality attribute. Using the Manual Chapter 0609.04, Phase 1 - Initial Screening
              and Characterization of Findings, the inspectors determined that this finding
              should be evaluated using the Phase 2 process described in Manual
              Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection
              Findings for At-Power Situations. As described in Section III, of Appendix A,
              given that the presolved table did not contain a suitable target or surrogate for
              this finding, the senior reactor analyst used the risk-informed notebook to
              evaluate the significance of this finding affecting only high-pressure recirculation
              as very low risk significance (Green). This finding has a crosscutting aspect in
              the area of human performance associated with the decision making component
              because the licensee failed to use conservative assumptions in decision making
              and did not adopt a requirement to demonstrate that a single vent valve was
              sufficient to vent the affected line rather than assuming that an additional
                                            -2-                                        Enclosure 2


Certrec Corporation 4200 South Hulen, Suite 422 Fort Worth, TX  76109
  installed valve was not necessary to completely fill, vent, and test the line [H.1(b)]
Keith G. Henke, Planner III Division of Community and Public Health
  (Section 1R15).
Office of Emergency Coordination Missouri Department of Health and  Senior Services 930 Wildwood, P.O. Box 570
* Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B,
Jefferson City, MO  65102
  Criterion XVI, "Corrective Action," was identified after the licensee failed to
Technical Services Branch Chief FEMA Region VII 2323 Grand Boulevard, Suite 900 Kansas City, MO 64108-2670
  promptly correct leakage from diesel generator jacket water o-rings. On
  February 20, 2008, during a normal surveillance run of Emergency Diesel
Ronald L. McCabe, Chief Technological Hazards Branch National Preparedness Division DHS/FEMA 9221 Ward Parkway, Suite 300
  Generator B, Callaway operations personnel identified an approximately
Kansas City,  MO  64114-3372 
  80 drop-per-minute jacket water leak caused by premature failure of Nitrile type
Union Electric Company - 4 -
  o-rings. Following restoration of Emergency Diesel Generator B, the licensee
Electronic distribution by RIV: Regional Administrator (Elmo.Collins@nrc.gov) DRP Director (Dwight.Chamberlain@nrc.gov) DRS Director (Roy.Caniano@nrc.gov) DRS Deputy Director (Troy.Pruett@nrc.gov) Senior Resident Inspector (David.Dumbacher@nrc.gov)
  re-evaluated the preventative maintenance frequency for jacket water o-ring
Branch Chief, DRP/B (Vincent.Gaddy@nrc.gov) Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov) Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov) RITS Coordinator (Marisa.Herrera@nrc.gov)
  replacement and reduced the replacement frequency from once every 3 years to
   once every refueling cycle. Then, on May 28, 2008, during a routine surveillance
Only inspection reports to the following: DRS STA (Dale.Powers@nrc.gov) M. Cox, OEDO RIV Coordinator (Mark.Cox@nrc.gov) OEMail.Resource@nrc.gov
   run of Emergency Diesel Generator A, Callaway operations personnel identified
Enforcement Officer (Michael.Vasquez@nrc.gov) Chief Allegation Coordination/Enforcement Staff (William.Jones@nrc.gov) Office of Enforcement (Alexander.Sapountizis@nrc.gov) 
  that Emergency Diesel Generator A had a 200 drop-per-minute jacket water leak.
ROPreports CWY Site Secretary (Dawn.Yancey@nrc.gov)
  Similar to the condition observed on Emergency Diesel Generator B on
 
  February 20, 2008, the source of the leakage was from Nitrile type o-rings within
   
  the jacket water system. The o-rings responsible for jacket water leakage were
   
  found to be of similar age to those that failed during the February 20, 2008,
   SUNSI Review Completed:    VGG  ADAMS:    Yes      No          Initials: __VGG__
  surveillance but had not been replaced despite the change to the licensee's
Publicly Available  Non-Publicly Available  Sensitive Non-Sensitive R:\_Reactors\_CW\2008\CW 2008003RP-DED.doc    ML 082180851 RIV:SRI:DRP/B C:DRS/OB C:DRS/PSB1 C:DRS/EB2 C:DRS/EB1 DDumbacher RELantz MPShannon NFO'Keefe RLBywater /RA/ VGGaddy for /RA/ /RA/ /RA/ MFRunyan for  /RA/ 07/29/2008 07/9/2008 07/14/2008 07/15/2008 07/11/2008 C:DRS/PSB2 DRS/SRA ACES C:DRP/B D:DRP GEWerner DPLoveless GMVasquez VGGaddy DDChamberlain /RA/ /RA/ /RA/ /RA/ /RA/ 07/17/2008 07/15/2008 07/24/2008 08/5/2008 07/28/2008 OFFICIAL RECORD COPY  T=Telephone          E=E-mail        F=Fax 
  preventive maintenance frequency.
   - 1 - Enclosure 1 NOTICE OF VIOLATION
  This finding, failure to implement adequate corrective actions for degraded Nitrile
AmerenUE        Docket 50-483 Callaway Plant      License NPF-30            EA-08-190
  type o-rings in Emergency Diesel Generator A after previously identifying the
  adverse condition on Emergency Diesel Generator B, was more than minor
During an NRC inspection conducted March 24 through June 24, 2008, a violation of NRC requirements was identified. In accordance with the NRC Enforcement Policy, the violation is listed below: 
  because, if left uncorrected, degraded diesel generator jacket water o-rings could
10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that
  become a more significant safety concern. This finding affected the mitigating
"measures shall be established to ensure that, for significant conditions adverse to quality, the cause of the condition is determined and corrective action taken to preclude repetition."
  systems cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial
Contrary to this, from December 26, 2006, through May 21, 2008, the licensee failed to take corrective actions to preclude repetition of safety-related emergency core cooling system pipe voiding, and the licensee determined that this condition was a significant
  Screening and Characterization of Findings, this finding was determined to be of
condition adverse to quality. 
  very low safety significance because it was a design deficiency confirmed not to
This violation is associated with a Green Significance Determination Process finding.
  result in loss of operability. This finding has a crosscutting aspect in the area of
Pursuant to the provisions of 10 CFR 2.201, AmerenUE is hereby required to submit a written
  human performance associated with the work controls component because the
statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN:  Document Control Desk, Washington, DC  20555 with a copy to the Regional Administrator, Region IV, and a copy to the NRC Senior Resident Inspector at the facility that is the subject of this Notice of Violation (Notice), within 30 days of the date of the letter transmitting this Notice. This reply should be clearly marked as a "Reply to Notice of Violation EA-08-190," and should include:  (1) the reason for the violation, or, if contested, the basis for disputing the violation or severity level, (2) the corrective steps that have been taken and the results achieved, (3) the corrective steps that will be taken to avoid further violations, and (4) the date when full compliance will be achieved.  Your response may reference or include previous docketed correspondence, if the correspondence adequately addresses the required response.  If an adequate reply is not
  licensee failed to plan work activities to support long-term equipment reliability by
received within the time specified in this Notice, an order or a Demand for Information may be issued as to why the license should not be modified, suspended, or revoked, or why such other action as may be proper should not be taken. Where good cause is shown, consideration will be given to extending the response time.  
  addressing known degraded conditions in a more reactive than preventative
  manner [H.3(b)] (Section 1R19).
If you contest this enforcement action, you should also provide a copy of your response, with the basis for your denial, to the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC  20555-0001. 
* Green. The inspectors identified a violation of 10 CFR Part 50, Appendix B,
Because your response will be made available electronically for public inspection in the NRC Public Document Room or from the NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not include any personal privacy, proprietary, or safeguards information so that it can be made available to the public without redaction. If personal privacy or proprietary information is necessary to provide an acceptable response, then please provide a bracketed copy of your response that identifies the information that should be protected and a redacted copy of your response that deletes such information.  If you request withholding of such material, you must
  Criterion XVI, "Corrective Action," because the licensee failed to take corrective
specifically identify the portions of your response that you seek to have withheld and provide in 
  actions to preclude repetition of void formation in emergency core cooling system
   - 2 - Enclosure 1 detail the bases for your claim of withholding (e.g., explain why the disclosure of information will create an unwarranted invasion of personal privacy or provide the information required by 10 CFR 2.390(b) to support a request for withholding confidential commercial or financial information). If safeguards information is necessary to provide an acceptable response, please provide the level of protection described in 10 CFR 73.21. 
  piping, a significant condition adverse to quality. After experiencing void
  formations in 2005 and 2006, the NRC identified violations of Criterion XVI.
Dated this    5th    day of July 2008    
  However, licensee corrective actions did not preclude repetition of void
   - 1 - Enclosure 2 U.S. NUCLEAR REGULATORY COMMISSION REGION IV Docket: 50-483
  formations that were discovered on May 21, 2008. On that date, Callaway Plant
License: NPF-30 Report: 05000483/2008003
  engineering performed ultrasonic inspection of the safety injection system
Licensee: Union Electric Company
   common suction piping Line EM023-HCB - 6" and discovered a 6.6 cubic foot
Facility: Callaway Plant
  voided area. This exceeded the allowable void fraction of 2.1 cubic feet required
Location: Junction Highway CC and Highway O  Fulton, MO  Dates: March 25 - June 24, 2008
  for operability. This voided piping, determined to have existed for over a year,
Inspectors: D. Dumbacher, Senior Resident Inspector  J. Groom, Resident Inspector  J. Drake, Senior Reactor Inspector, Plant Support, Branch 2  G. Guerra, CHP, Health Physicist, Plant Support Branch 1 Approved By: V. Gaddy, Chief, Project Branch B  Division of Reactor Projects 
  was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The
  - 2 - Enclosure 2 SUMMARY OF FINDINGS
   maintenance restoration failed to perform an adequate fill and vent to ensure the
  IR 05000483/2008003: 3/25 - 6/24/2008; Callaway Plant, Operability Evaluations, Postmaintenance Testing, Surveillance Testing, and Identification and Resolution of Problems.  This report covered a 3-month period of inspection by resident inspectors.  The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination Process."  Findings for which the Significance Determination Process does not apply may be Green or assigned a severity level after NRC management review.  The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4,
   suction pipe was full of water. The inspectors identified several related examples
dated December 2006.
  where the licensee had performed either inadequate operating experience
A. NRC-Identified and Self-Revealing Findings 
                                -3-                                       Enclosure 2
Cornerstone:  Mitigating Systems
* Green.  The inspectors identified a noncited violation of Technical Specification 3.5.2, "Emergency Core Cooling Systems," after an inadequate surveillance procedure resulted in the licensee failing to maintain the emergency core cooling system full of water as required per Technical Specification 3.5.2.  On May 21, 2008, Callaway Plant engineering discovered that a section of the cold leg recirculation piping, specifically the discharge of the residual heat removal pumps to the safety injection pumps, contained 6.6 cubic feet of air. 
Callaway monthly surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow Path Verification and Venting," had a purpose to:  "Verify the ECCS is full of water," in accordance with Technical Specification Surveillance Requirement 3.5.2.3.  The monthly verification and vent procedure was not comprehensive enough to ensure all the emergency core cooling system was full of water.  This finding was more than minor because it was similar to Example 3e of NRC Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues," and
met the "Not Minor If," criteria because the failure to meet the licensee's administrative requirement for allowable void fraction impacted the ability of the Train A safety injection system to function upon initiation of high-pressure recirculation.  This finding affected the mitigating systems cornerstone procedure quality attribute.  Using the Manual Chapter 0609.04, "Phase 1 - Initial Screening
and Characterization of Findings," the inspectors determined that this finding should be evaluated using the Phase 2 process described in Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations."  As described in Section III, of Appendix A, given that the presolved table did not contain a suitable target or surrogate for
this finding, the senior reactor analyst used the risk-informed notebook to evaluate the significance of this finding affecting only high-pressure recirculation as very low risk significance (Green).  This finding has a crosscutting aspect in the area of human performance associated with the decision making component because the licensee failed to use conservative assumptions in decision making and did not adopt a requirement to demonstrate that a single vent valve was sufficient to vent the affected line rather than assuming that an additional 
  - 3 - Enclosure 2 installed valve was not necessary to completely fill, vent, and test the line [H.1(b)] (Section 1R15). 
* Green.  A self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," was identified after the licensee failed to promptly correct leakage from diesel generator jacket water o-rings.  On February 20, 2008, during a normal surveillance run of Emergency Diesel Generator B, Callaway operations personnel identified an approximately 80 drop-per-minute jacket water leak caused by premature failure of Nitrile type o-rings.  Following restoration of Emergency Diesel Generator B, the licensee re-evaluated the preventative maintenance frequency for jacket water o-ring replacement and reduced the replacement frequency from once every 3 years to
once every refueling cycle.  Then, on May 28, 2008, during a routine surveillance run of Emergency Diesel Generator A, Callaway operations personnel identified that Emergency Diesel Generator A had a 200 drop-per-minute jacket water leak.  Similar to the condition observed on Emergency Diesel Generator B on February 20, 2008, the source of the leakage was from Nitrile type o-rings within
the jacket water system.  The o-rings responsible for jacket water leakage were found to be of similar age to those that failed during the February 20, 2008, surveillance but had not been replaced despite the change to the licensee's preventive maintenance frequency. This finding, failure to implement adequate corrective actions for degraded Nitrile type o-rings in Emergency Diesel Generator A after previously identifying the
adverse condition on Emergency Diesel Generator B, was more than minor because, if left uncorrected, degraded diesel generator jacket water o-rings could become a more significant safety concern.  This finding affected the mitigating systems cornerstone.  Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," this finding was determined to be of very low safety significance because it was a design deficiency confirmed not to result in loss of operability.  This finding has a crosscutting aspect in the area of
human performance associated with the work controls component because the licensee failed to plan work activities to support long-term equipment reliability by addressing known degraded conditions in a more reactive than preventative manner [H.3(b)] (Section 1R19).
* Green.  The inspectors identified a violation of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," because the licensee failed to take corrective actions to preclude repetition of void formation in emergency core cooling system piping, a significant condition adverse to quality.  After experiencing void
formations in 2005 and 2006, the NRC identified violations of Criterion XVI.  However, licensee corrective actions did not preclude repetition of void formations that were discovered on May 21, 2008.  On that date, Callaway Plant engineering performed ultrasonic inspection of the safety injection system common suction piping Line EM023-HCB - 6" and discovered a 6.6 cubic foot
voided area.  This exceeded the allowable void fraction of 2.1 cubic feet required for operability.  This voided piping, determined to have existed for over a year, was caused by relief valve maintenance on Valve EM8858A (May 7, 2007).  The maintenance restoration failed to perform an adequate fill and vent to ensure the suction pipe was full of water.  The inspectors identified several related examples where the licensee had performed either inadequate operating experience 
  - 4 - Enclosure 2 evaluations, inadequate extent of condition reviews, or inadequate procedure corrections.  The violation is being cited in a Notice of Violation because the licensee failed to restore compliance with a reasonable time after a violation was last identified in 2006. This finding, failure to restore compliance to prevent recurrence of emergency core cooling system voids, was more than minor because it is similar to Example 3e of NRC Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues," criteria because the failure impacted the ability of the emergency core cooling system to function upon initiation of high-pressure recirculation. 
Using the Manual Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," the inspectors determined that this finding should be evaluated using the Phase 2 process described in Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations."  As described in Section III, of Appendix A, given that the
presolved table did not contain a suitable target or surrogate for this finding, the senior reactor analyst used the risk-informed notebook to evaluate the significance of this finding as very low risk significance (Green).  This finding has a crosscutting aspect in the area of problem identification and resolution associated with the corrective action program component because AmerenUE
failed to thoroughly evaluate voiding problems such that the resolutions addressed causes and extent of condition, as necessary [P.1(c)] (Section 4OA2). Cornerstone:  Barrier Integrity
* Green.  A self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," was identified after determining that the licensee had not adequately selected and reviewed the suitability of the design of the
containment air cooler control circuitry.  On March 26, 2008, Containment Air Cooler A fan shut down when shifted from fast to slow speed.  Troubleshooting by the licensee determined that voltage was lost to the control power circuitry when the fast speed thermal overload tripped.  Since the overload contacts were wired in series, Containment Air Cooler A experienced a complete loss of control
power rendering it inoperable.  The licensee determined the trip to be caused by operation of containment air coolers in fast speed, during a period of higher than normal containment pressure.  The licensee analyzed the potential impact of the newly discovered adverse containment cooler design vulnerability against design basis accident scenarios.  The licensee determined that a hot zero power main
steam line break results in a delayed safety injection signal allowing the fan motor overloads to trip prior to being shed by the load sequencer.  The containment air coolers would then experience a complete loss of control power and would not be capable of automatically restarting in slow speed.  The analysis revealed that the peak containment pressure limit of 48.1 psig would be
preserved.  The licensee submitted a licensee event report as required by 10 CFR 50.73 since the inadequate containment air cooler control circuitry resulted in a condition prohibited by the plant's Technical Specifications.  This finding, failure to ensure the design of the containment air cooler control circuitry was suitable for all plant conditions, was more than minor because it was associated with the barrier integrity cornerstone attribute of design control and affects the associated cornerstone objective to provide reasonable assurance 
  - 5 - Enclosure 2 that physical design barriers protect the public from radio nuclide releases caused by accidents or releases.  Using Manual Chapter 0609, Appendix H, "Containment Integrity Significance Determination Process," this finding was determined to be a Type B finding since it was related to a degraded condition that has potentially important implications for the integrity of the containment, without affecting the likelihood of core damage.  This finding was found to be of
very low safety significance because containment coolers are structures, systems or components that are not significant contributors to the large early release frequency.  The inspectors determined that this finding does not have a crosscutting aspect associated with it since the performance deficiency was not indicative of current licensee performance (Section 1R15). 
* Green.  The inspectors identified a noncited violation of Technical Specification 5.4.1.a, "Procedures," after Callaway control room operators improperly entered a wrong Technical Specification action statement due to the failure to maintain the Technical Specification Bases current.  On June 17, 2008, during surveillance testing, Valve EMHV8823 failed to indicate fully closed. 
Since EMHV8823 is an isolation valve for containment Penetration 49, the licensee entered Technical Specification 3.6.3, "Containment Isolation Valves," Condition C, with an action to restore the valve to an operable status or isolate the penetration within 72 hours.  Approximately 8 hours after Valve EMHV8823 had been declared inoperable, Callaway licensing personnel contacted the
control room and informed them of an approved Technical Specification Bases change that did not allow Technical Specification 3.6.3, Condition C, to be applicable to containment Penetration 49.  The Technical Specification Bases change was effective May 1, 2008, but had not been issued to the control room.  The licensee determined that the more restrictive Technical Specification 3.6.3,
Condition A, should have been entered with an action to isolate the affected penetration within 4 hours.  The licensee performed a containment entry following discovery of entry into Technical Specification 3.6.3, Condition A, and found that Valve EMHV8823 failed its surveillance due to out of adjustment position indicator limit switches.  The valve was verified closed and isolated
allowing exit from Technical Specification 3.6.3, Condition A. This finding, failure to ensure the Technical Specification Bases were maintained current and available to the Callaway control room staff, was more than minor
because if left uncorrected, the failure to maintain the Technical Specification Bases current could become a more significant safety concern.  This finding was determined to affect the barrier integrity cornerstone.  Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," this finding is determined to be of very low safety significance since this finding
did not represent an actual open pathway in the physical integrity of reactor containment and did not involve an actual reduction in function of hydrogen ignitors in the reactor containment.  This finding has a crosscutting aspect in the area of human performance associated with the decision making component because the licensee failed to communicate, in a timely manner, decisions to
personnel who have a need to know the information in order to perform work safely [H.1(c)] (Section 1R22).
 
  - 6 - Enclosure 2 B. Licensee-Identified Violations
Two violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors.  Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program.  These violations and corrective action tracking numbers are listed in Section 4OA7. 
  - 7 - Enclosure 2 REPORT DETAILS Summary of Plant Status
  AmerenUE operated the Callaway Plant at near 100 percent for the entire quarter. 1. REACTOR SAFETY
Cornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity and Emergency Preparedness 1R01 Adverse Weather Protection (71111.01)
.1 Readiness of Offsite and Alternate AC Power System
      a. Inspection Scope
The inspectors reviewed the licensee's plant features, training lesson plans, and procedures for operation and continued availability of offsite and alternate AC power systems to verify they were appropriate.  The review included communication protocols and agreement procedures between the transmission system operator and the nuclear power plant to verify that appropriate information is exchanged when issues arise that
could impact the offsite power system.  Specifically, the procedures were verified to ensure they specified:
* Required actions needed when notified by the transmission system operator that posttrip voltage of the offsite power system would not be acceptable to assure the continued operation of safety related loads without transferring to the onsite power supply.
* Compensatory actions needed when it is not possible to predict the posttrip voltage at the nuclear power plant for current grid conditions.
* Required assessment of plant risk based on maintenance activities which could affect grid reliability, or the ability of the transmission system to provide the offsite power system.
* Required communications between the nuclear power plant and the transmission system operator when changes at the nuclear power plant could impact the transmission system, or when the capability of the transmission system to provide adequate offsite system power is challenged.  On May 16, 2008, the inspectors evaluated the licensee staff's preparations for summer readiness of offsite and AC power systems against the site's procedures and determined that the staff's actions were adequate.  Documents reviewed are listed in the
attachment.
These activities constituted one readiness of offsite power inspection sample as defined by Inspection Procedure 71111.01.
 
  - 8 - Enclosure 2      b. Findings
No findings of significance were identified. .2 Readiness for Impending Adverse Weather Conditions
      a. Inspection Scope
On May 2, 2008, the inspectors completed a review of the licensee's readiness for impending adverse weather involving severe thunderstorms.  The inspectors:  (1) reviewed plant procedures, the Final Safety Analysis Report (FSAR), and Technical Specifications to ensure that operator actions defined in adverse weather procedures maintained the readiness of essential systems; (2) walked down portions of the
emergency diesel generators and offsite power systems to ensure that adverse weather protection features were sufficient to support operability; (3) reviewed maintenance records to determine that applicable surveillance requirements were current before the anticipated severe thunderstorms developed; and (4) reviewed plant modifications, procedure revisions, and operator work arounds to determine if recent facility changes
challenged plant operation.  Documents reviewed by the inspectors are listed in the attachment. 
These activities constituted one readiness for impending adverse weather inspection sample as defined by Inspection Procedure 71111.01.


       b. Findings
       evaluations, inadequate extent of condition reviews, or inadequate procedure
No findings of significance were identified.
       corrections. The violation is being cited in a Notice of Violation because the
1R04 Equipment Alignments (71111.04)
      licensee failed to restore compliance with a reasonable time after a violation was
.1 Quarterly Partial System Walkdowns
      last identified in 2006.
       a. Inspection Scope
      This finding, failure to restore compliance to prevent recurrence of emergency
The inspectors performed partial system walkdowns of the following risk-significant systems:  * June 3, 2008, Train A auxiliary feedwater system while the Train B motor-driven auxiliary feedwater pump was out of service for planned maintenance.  
      core cooling system voids, was more than minor because it is similar to
* June 10, 2008, Train A 480 volt NG Class 1E switchgear while the Train B emergency diesel generator was out of service for planned and emergent maintenance issues.  The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected.  The inspectors attempted to identify discrepancies that could impact the function of the system, and, therefore, potentially increase risk.  The inspectors reviewed applicable operating procedures, system diagrams, FSAR, Technical Specification requirements, outstanding work orders, corrective action documents, and the impact of ongoing work activities on redundant
      Example 3e of NRC Inspection Manual Chapter 0612, Appendix E, "Examples of
trains of equipment in order to identify conditions that could have rendered the systems 
      Minor Issues," criteria because the failure impacted the ability of the emergency
  - 9 - Enclosure 2 incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify components and support equipment were aligned correctly and were operable.  The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies.  The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events
      core cooling system to function upon initiation of high-pressure recirculation.
or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization.  Documents reviewed are listed in the attachment.
      Using the Manual Chapter 0609.04, Phase 1 - Initial Screening and
These activities constituted two partial system walkdown samples as defined by
      Characterization of Findings, the inspectors determined that this finding should
Inspection Procedure 71111.04.
      be evaluated using the Phase 2 process described in Manual Chapter 0609,
       b. Findings
      Appendix A, Determining the Significance of Reactor Inspection Findings for
No findings of significance were identified. .2 Complete System Walkdown (71111.04S)
       At-Power Situations. As described in Section III, of Appendix A, given that the
       a. Inspection Scope
       presolved table did not contain a suitable target or surrogate for this finding, the
On April 17, 2008, the inspectors performed a complete system alignment inspection of Train B of the residual heat removal system to verify the functional capability of the system.  The inspectors selected this system because it was considered both safety-significant and risk-significant in the licensee's probabilistic risk assessment. The inspectors walked down the system to review mechanical and electrical equipment line ups, electrical power availability, system pressure and temperature indications, as
      senior reactor analyst used the risk-informed notebook to evaluate the
appropriate, component labeling, component lubrication, component and equipment cooling, hangers and supports, operability of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation.  The inspectors reviewed a sample of past and outstanding work orders to determine whether any deficiencies significantly affected the system function.  In addition, the inspectors
      significance of this finding as very low risk significance (Green). This finding has
reviewed the corrective action program database to ensure that system equipment alignment problems were being identified and appropriately resolved.  The documents used for the walkdown and issue review are listed in the attachment.
      a crosscutting aspect in the area of problem identification and resolution
These activities constituted one complete system walkdown sample as defined by
      associated with the corrective action program component because AmerenUE
Inspection Procedure 71111.04.
      failed to thoroughly evaluate voiding problems such that the resolutions
       b. Findings
       addressed causes and extent of condition, as necessary [P.1(c)] (Section 4OA2).
No findings of significance were identified.  
Cornerstone: Barrier Integrity
 
*     Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B,
  - 10 - Enclosure 2 1R05 Fire Protection (71111.05)
      Criterion III, Design Control, was identified after determining that the licensee
.1 Quarterly Fire Inspector Tours (71111.05Q)
      had not adequately selected and reviewed the suitability of the design of the
      a. Inspection Scope
       containment air cooler control circuitry. On March 26, 2008, Containment Air
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant
      Cooler A fan shut down when shifted from fast to slow speed. Troubleshooting
plant areas:  
      by the licensee determined that voltage was lost to the control power circuitry
* March 27, 2008, Fire Area C-21, Lower Cable Spreading Room
      when the fast speed thermal overload tripped. Since the overload contacts were
* April 16, 2008, Fire Area A-17, Electrical Penetration Room (South)
      wired in series, Containment Air Cooler A experienced a complete loss of control
* April 25, 2008, Condensate Storage Tank
       power rendering it inoperable. The licensee determined the trip to be caused by
* April 29, 2008, Fire Area A-23, Main Steam and Feedwater Isolation Valve Enclosure
      operation of containment air coolers in fast speed, during a period of higher than
* April 30, 2008, Reactor Building
      normal containment pressure. The licensee analyzed the potential impact of the
* June 18, 2008, Fire Area A-1, North Pipe Chase The inspectors reviewed areas to assess if the licensee implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire
       newly discovered adverse containment cooler design vulnerability against design
protection features in good material condition, and implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensee's fire plan.  The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events with later additional insights, their
       basis accident scenarios. The licensee determined that a hot zero power main
potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event.  The inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration
      steam line break results in a delayed safety injection signal allowing the fan
seals appeared to be in satisfactory condition.  Documents reviewed are listed in the attachment. 
      motor overloads to trip prior to being shed by the load sequencer. The
These activities constituted six
      containment air coolers would then experience a complete loss of control power
quarterly fire protection inspection samples as defined by Inspection Procedure 71111.05.      b. Findings
      and would not be capable of automatically restarting in slow speed. The analysis
No findings of significance were identified. .2 Annual Fire Protection Drill Observation (71111.05A)
       revealed that the peak containment pressure limit of 48.1 psig would be
       a. Inspection Scope
      preserved. The licensee submitted a licensee event report as required by
On March 27, 2008 , the inspectors observed a fire brigade activation due to a report of smoke in the laundry decontamination area
       10 CFR 50.73 since the inadequate containment air cooler control circuitry
. The observation evaluated the readiness of 
      resulted in a condition prohibited by the plants Technical Specifications.
  - 11 - Enclosure 2 the plant fire brigade to fight fires.  The inspectors verified that the licensee staff identified deficiencies; openly discussed them in a self-critical manner at the drill debrief, and took appropriate corrective actions.  Specific attributes evaluated were:  (1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper use and layout of fire hoses; (3) employment of appropriate fire fighting techniques; (4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade leader
      This finding, failure to ensure the design of the containment air cooler control
communications, command, and control; (6) search for victims and propagation of the fire into other plant areas; (7) smoke removal operations; (8) utilization of preplanned strategies; (9) adherence to the preplanned drill scenario; and (10) drill objectives. Documents reviewed are listed in the attachment. These activities constituted one annual fire protection inspection sample as defined by Inspection Procedure 71111.05.      b. Findings
      circuitry was suitable for all plant conditions, was more than minor because it was
No findings of significance were identified. 1R06 Flood Protection Measures (71111.06)
      associated with the barrier integrity cornerstone attribute of design control and
Internal Flooding
      affects the associated cornerstone objective to provide reasonable assurance
       a. Inspection Scope
                                    -4-                                      Enclosure 2
The inspectors reviewed selected risk-significant plant design features and licensee procedures intended to protect the plant and its safety related equipment from internal
flooding events.  The inspectors reviewed flood analyses and design documents, including the FSAR, engineering calculations, and abnormal operating procedures for licensee commitments.  The inspectors reviewed licensee drawings to identify areas and equipment that may be affected by internal flooding caused by the failure or misalignment of nearby sources of water. The inspectors also reviewed the licensee's
corrective actions for previously identified flood-related items.  The inspectors performed a walkdown of the following plant area to assess the adequacy of any watertight doors and verify drains and sumps were clear of debris and operable, and that the licensee complied with its flooding related commitments:
* June 23, 2008, Control Building West Corridor
The document reviewed during this inspection is listed as follows:
* Callaway Action Request 200805189
This inspection constituted one internal flooding sample as defined in Inspection Procedure 71111.06.
       b. Findings
No findings of significance were identified.
 
  - 12 - Enclosure 2 1R11 Licensed Operator Requalification Program (71111.11)
       a. Inspection Scope
On June 2, 2008, the inspectors observed a crew of licensed operators perform a Cycle 08-3 as found scenario in the plant's simulator to verify that operator performance was adequate, evaluators were identifying and documenting crew performance
problems, and that training was being conducted in accordance with licensee procedures.  The scenario involved an operating design basis earthquake with a lockout on essential 4 kV Bus NB01.  The inspectors evaluated the crew in the following areas:
* Licensed operator performance
* Crew clarity and formality of communications
* Ability to take timely actions in the conservative direction
* Prioritization, interpretation, and verification of annunciator alarms
* Correct use and implementation of abnormal and emergency procedures
* Control board manipulations
* Oversight and direction from supervisors
* Ability to identify and implement appropriate Technical Specification actions and Emergency Plan actions and notifications
The crew's performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements.  Documents reviewed are listed in the attachment. 
This inspection constituted one quarterly licensed operator requalification program
sample as defined in Inspection Procedure 71111.11.  
       b. Findings
  No findings of significance were identified.  
1R12 Maintenance Effectiveness (71111.12)
       a. Inspection Scope
The inspectors evaluated degraded performance issues involving the following risk-significant systems:
* May 15, 2008, Callaway Action Request (CAR) 200801644, an additional anode was found in the north end of the Train A emergency diesel generator intercooler
* May 15, 2008, CAR 200802854, KKJ01A (Train A emergency diesel generator) engine oil sump high 
  - 13 - Enclosure 2 The inspectors reviewed events such as where ineffective equipment maintenance has resulted in valid or invalid automatic actuations of risk-important systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
* Implementing appropriate work practices
* Identifying and addressing common cause failures
* Scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule
* Characterizing system reliability issues for performance
* Charging unavailability time
* Trending key parameters for condition monitoring
* Ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or reclassification
* Verifying appropriate performance criteria for structures, systems, and components/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1)
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system.  The inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization.  Documents reviewed are listed in the attachment. 


This inspection constituted two quarterly maintenance effectiveness samples as defined in Inspection Procedure 71111.12Q.
   that physical design barriers protect the public from radio nuclide releases
      b. Findings
  caused by accidents or releases. Using Manual Chapter 0609, Appendix H,
  No findings of significance were identified.
  Containment Integrity Significance Determination Process," this finding was
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
  determined to be a Type B finding since it was related to a degraded condition
      a. Inspection Scope
  that has potentially important implications for the integrity of the containment,
The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:
  without affecting the likelihood of core damage. This finding was found to be of
* April 3, 2008, Routine - Work on turbine-driven auxiliary feedwater Valve KAPCV-0102
  very low safety significance because containment coolers are structures,
* April 21, 2008, Emergency Diesel Generator A lube oil trouble shooting
  systems or components that are not significant contributors to the large early
* April 28, 2008, Routine - associated with Loose Creek-Callaway 345 kV line outage 
  release frequency. The inspectors determined that this finding does not have a
  - 14 - Enclosure 2
  crosscutting aspect associated with it since the performance deficiency was not
* June 10, 2008, Risk management actions associated with Emergency Diesel Generator B jacket water o-ring replacement outage These activities were selected based on their potential risk significance relative to the reactor safety cornerstones.  As applicable for each activity, the inspectors verified that
  indicative of current licensee performance (Section 1R15).
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete.  When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed.  The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment.  The inspectors also reviewed Technical Specification requirements and walked down portions of redundant safety systems,
* Green. The inspectors identified a noncited violation of Technical
when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.  Documents reviewed are listed in the attachment.
  Specification 5.4.1.a, Procedures, after Callaway control room operators
These activities constituted four samples as defined by Inspection Procedure 71111.13.
  improperly entered a wrong Technical Specification action statement due to the
      b. Findings
  failure to maintain the Technical Specification Bases current. On June 17, 2008,
No findings of significance were identified.
  during surveillance testing, Valve EMHV8823 failed to indicate fully closed.
1R15 Operability Evaluations (71111.15)
  Since EMHV8823 is an isolation valve for containment Penetration 49, the
      a. Inspection Scope
  licensee entered Technical Specification 3.6.3, Containment Isolation Valves,
The inspectors reviewed the following issues: 
  Condition C, with an action to restore the valve to an operable status or isolate
* March 26, 2008, CARs 200802348, 200802365, and 200802264, Containment coolers inoperable in fast speed
  the penetration within 72 hours. Approximately 8 hours after Valve EMHV8823
* April 4, 2008, CARs 200800461 and 200802625, Containment recirculation sump operability determination, Revisions 3 and 4
  had been declared inoperable, Callaway licensing personnel contacted the
* April 9, 2008, Source Range Channel N32 inoperable due to a failed surveillance
  control room and informed them of an approved Technical Specification Bases
* April 23, 2008, Component cooling water system following Valve EGHV0069 failing inservice test stroke time surveillance
  change that did not allow Technical Specification 3.6.3, Condition C, to be
* April 30, 2008, CAR 200803465, Emergency diesel generator Garlock flexible expansion joints
  applicable to containment Penetration 49. The Technical Specification Bases
* May 6, 2008, CAR 200803462, Voiding identified in containment spray pump piping from sump
  change was effective May 1, 2008, but had not been issued to the control room.
* May 22, 2008, CAR 200904000, Line EM-023 allowable void fraction exceeded The inspectors selected potential operability issues based on the risk significance of the associated components and systems.  The inspectors evaluated the technical adequacy of the evaluations to ensure that Technical Specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred.  The inspectors compared the operability and design criteria in the appropriate sections of the Technical Specifications and FSAR to the licensee's 
  The licensee determined that the more restrictive Technical Specification 3.6.3,
  - 15 - Enclosure 2 evaluations to determine whether the components or systems were operable.  Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled.  The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.  Additionally, the inspectors reviewed a sample of corrective action documents to verify that the licensee was
  Condition A, should have been entered with an action to isolate the affected
identifying and correcting deficiencies associated with operability evaluations.  Documents reviewed are listed in the attachment.
  penetration within 4 hours. The licensee performed a containment entry
This inspection constituted seven samples as defined in Inspection Procedure 71111.15.
  following discovery of entry into Technical Specification 3.6.3, Condition A, and
      b. Findings
  found that Valve EMHV8823 failed its surveillance due to out of adjustment
   .1 Introduction.  A self-revealing Green noncited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," was identified after determining that the
  position indicator limit switches. The valve was verified closed and isolated
licensee had not adequately selected and reviewed the suitability of the design of the containment air cooler control circuitry.
   allowing exit from Technical Specification 3.6.3, Condition A.
Description.  On March 26, 2008, Containment Air Cooler A fan shut down when shifted from fast to slow speed.  Troubleshooting by the licensee determined that voltage was
  This finding, failure to ensure the Technical Specification Bases were maintained
lost to the control power circuitry when the fast speed thermal overload tripped.  Since the overload contacts were wired in series, Containment Air Cooler A experienced a complete loss of control power rendering it inoperable.  AmerenUE personnel noted that Precaution 3.6 of Procedure OTN-GN-00001, "Containment Cooling and CRDM Cooling," Revision 14, cautioned that high pressure and cool temperatures across
  current and available to the Callaway control room staff, was more than minor
containment coolers will cause the coolers to operate close to the setpoint of the thermal overloads. However, the licensee's operability determination dismissed the 1987 precaution as not having a technical basis believing it was implemented to address discrepancies in motor overload setpoints.  Later, the licensee determined that operation of containment air coolers in fast speed, during a period of higher than normal
  because if left uncorrected, the failure to maintain the Technical Specification
containment pressure, challenged the fast speed thermal overload setpoint and resulted in the trip of Containment Air Cooler A on March 26, 2008.  As an interim measure to prevent a trip from fast speed, the licensee imposed a standing order to maintain the containment coolers in slow speed.
  Bases current could become a more significant safety concern. This finding was
The licensee analyzed the potential impact of the newly discovered adverse containment cooler design vulnerability against design basis accident scenarios.  The licensee determined that a hot zero power main steam line break results in a delayed safety injection signal allowing the fan motor overloads to trip prior to being shed by the load sequencer.  The containment air coolers would then experience a complete loss of control power and would not be capable of automatically restarting in slow speed.  The analysis revealed that in this scenario, utilizing assumed accident conditions, the peak
  determined to affect the barrier integrity cornerstone. Using Manual
containment pressure would exceed the 48.1 psig limit described in the FSAR.  However, analysis using actual plant conditions determined that the peak containment pressure limit of 48.1 psig would be preserved.  The licensee submitted a licensee event report (LER) as required by 10 CFR 50.73 since the inadequate containment air cooler control circuitry resulted in a condition prohibited by the plant's Technical Specifications. 
  Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,
The inspector's review of the licensee's LER is described in Section 4OA3 of this report.
  this finding is determined to be of very low safety significance since this finding
To address the design deficiency associated with the containment air cooler control circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit 
  did not represent an actual open pathway in the physical integrity of reactor
  - 16 - Enclosure 2 such that tripping of the fast speed overloads would not impact the safety-related slow speed function of the containment air coolers.
  containment and did not involve an actual reduction in function of hydrogen
Analysis.  The performance deficiency associated with this finding involved the licensee's failure to ensure the design of the containment air cooler control circuitry was suitable for all plant conditions.  This finding was greater than minor because it was
   ignitors in the reactor containment. This finding has a crosscutting aspect in the
associated with the barrier integrity cornerstone attribute of design control and affects the associated cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radio nuclide releases caused by accidents or releases. Using Manual Chapter 0609, Appendix H, "Containment Integrity Significance Determination Process," this finding was determined to be a Type B finding since it was  
  area of human performance associated with the decision making component
related to a degraded condition that has potentially important implications for the integrity of the containment, without affecting the likelihood of core damage. This finding was found to be of very low safety significance since containment coolers are structures, systems, and components that have no impact on large early release frequency. The inspectors determined that this finding does not have a crosscutting aspect associated with it since the performance deficiency is not indicative of current licensee performance.  
  because the licensee failed to communicate, in a timely manner, decisions to
  personnel who have a need to know the information in order to perform work
Enforcement. 10 CFR Part 50, Appendix B, Criterion III, "Design Control," requires, in part, that measures be established for the selection and review for suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of structures, systems, and components. Contrary to the above, prior to April 2, 2008, the licensee failed to ensure that the containment air coolers would
  safely [H.1(c)] (Section 1R22).
be able to perform their safety-related function in all accident scenarios due to a design deficiency associated with the overload contacts in the containment air cooler control circuitry.  Because this finding is of very low safety significance and has been entered into the corrective action program as CAR 200702264, this violation is being treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy: 
                                -5-                                       Enclosure 2
NCV 05000483/2008003-01, Failure to Ensure the Suitability of the Design of the Containment Air Cooler Control Circuitry.
.2 Introduction.  The inspectors identified a Green NCV of Technical Specification 3.5.2, "Emergency Core Cooling Systems," after an inadequate surveillance procedure
resulted in the licensee failing to maintain the emergency core cooling system (ECCS) full of water as required per Technical Specification 3.5.2.  
Description.  On May 21, 2008, Callaway Plant engineering discovered that a section of the cold leg recirculation piping, specifically the discharge of the residual heat removal
pumps to the safety injection pumps, contained 6.6 cubic feet of air. This exceeded the allowable void fraction of 2.1 cubic feet required for operability.  Callaway monthly surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow Path Verification and Venting," had a purpose to:  "Verify the ECCS is full of water," in accordance with Technical Specification Surveillance Requirement 3.5.2.3.  This monthly surveillance was reviewed as part of significant condition adverse to quality (SCAQ) CAR 200501092 corrective actions.  Callaway engineering had determined that
residual heat removal pump discharge vent Valve EJV0193 to the safety injection system was the high point vent for these lines and was thus sufficient to vent Line EM-023-HCB - 6" to the safety injection pumps. However, this vent valve was not adequate due to the pipe sloping issues and normally closed Valves EMHIS8807A/B.  Venting through Valve EMV0179 was necessary to completely fill, vent, and test the line. 
The monthly verification and vent procedure was inadequate to identify and remove air 
   - 17 - Enclosure 2 introduced by relief valve maintenance on May 7, 2007, and thus ensure the ECCS was full of water.  See Violation (VIO) 05000483/2008003-05 in Section 4OA2. 
Analysis.  Failure to adequately verify ECCS piping was full of water as required by Technical Specification 3.5.2 is a performance deficiency. This finding affected the mitigating system cornerstone procedure quality attribute.  This finding is more than  
minor because it was similar to Example 3e of NRC Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues," and met the "Not Minor If," criteria because the failure to meet the licensee's administrative requirement for allowable void fraction impacted the ability of the Train A safety injection system to function upon initiation of high-pressure recirculation. Using Manual Chapter 0609.04, "Phase 1 - Initial Screening  
and Characterization of Findings," the inspectors determined that this finding should be evaluated using the Phase 2 process described in Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations."
As described in Section III of Appendix A, given that the presolved table did not contain a suitable target or surrogate for this finding, the senior reactor analyst used the risk-informed notebook to evaluate the significance of this finding.  Table 2 provides the
definitions for acronyms and initialisms used in the risk-informed notebook and discussed in this inspection report.
TABLE 2 Acronyms and Initialisms used in Phase 2 Notebook Initialism Initiating Event or Mitigating Function TPCS Transient with Loss of the Power Conversion System SLOCA Small-Break Loss of Coolant Accident MLOCA Medium-Break Loss of Coolant Accident LLOCA Large-Break Loss of Coolant Accident LOOP Loss of Offsite Power MSLB Main Steam Line Break LBDC Loss of Vital Direct-Current Bus AFW Auxiliary Feedwater PCS Power Conversion System (Steam and Feed) HPR High Pressure Recirculation DEPR Depressurization of the Reactor Coolant System EAC Emergency Power (Alternating Current) TDAFW Turbine-Driven Auxiliary Feedwater Pump Train SEAL Reactor Coolant Pump Seal Integrity STIN Operators Stop High-Pressure Injection MDAFW Motor-Driven Auxiliary Feedwater Pump Train
The analyst performed a Phase 2 estimation in accordance with Inspection Manual
Chapter 0609, Appendix A, Attachment 2, "Site Specific Risk-Informed Inspection Notebook Usage Rules."  Given that the performance deficiency was known to have existed for 378 days (May 7, 2007, until May 21, 2008) the analyst used 1 year as the exposure period.  In accordance with Table 2 of the risk-informed notebook, the analyst evaluated all worksheets except LLOCA.  All worksheets were evaluated using the
nominal 1-year initiating event frequency.  Because this finding only affected system functionality during recirculation, nominal mitigation credit was given for all functions with the exception of HPR.  For HPR, the analyst made the bounding assumption that either 
   - 18 - Enclosure 2 both centrifugal charging pumps or both safety injection pumps would be affected.  This assumption was supported by licensee evaluation.  The analyst solved each applicable worksheet and the dominant sequences are documented in Table 1.
TABLE 1 Phase 2 Dominant Sequences Initiating Event Sequence Number Mitigating Functions Results Transients 1 AFW-PCS-HPR
9 TPCS 1 AFW-HPR 8 SLOCA 2 DEPR-HPR 8 MLOCA 2 DEPR-HPR 9 1 AFW-HPR 9 5 EAC-TDAFW-HPR 9 LOOP 9 EAC-SEAL-HPR 9 MSLB 8 STIN-HPR 8 LBDC 8 TDAFW-MDAFW-HPR
8  Using Inspection Manual Chapter 0609, Appendix A, Attachment 1, Table 5, "Counting Rule Worksheet," the analyst determined that the risk contribution of this finding from internal initiating events was of very low risk significance.  In accordance with Appendix A, Attachment 1, Steps 2.2.5 and 2.2.6, the analyst and determined that the risk contribution of this finding from external initiating events or the contribution from
large-early release frequency were very low. Therefore, this finding was of very low risk significance (Green).  This finding has a crosscutting aspect in the area of human performance associated with the decision making component because the licensee failed to use conservative assumptions in decision making and did not adopt a requirement to demonstrate that the single vent Valve EJV0193 was sufficient to vent
the Line EM-023-HCB - 6" rather than assuming that installed Valve EMV0179 was not necessary to completely fill, vent, and test the line [H.1(b)].  
Enforcement.  Technical Specification 3.5.2 "Emergency Core Cooling Systems," Surveillance Requirement 3.5.2.3, required that the licensee verify that ECCS piping is
full of water every 31 days.  Contrary to the above, from June 2007 through April 2008, AmerenUE surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow Path Verification and Venting," was inadequate to meet Technical Specification Surveillance Requirement 3.5.2.3.  Because this finding is of very low safety significance and was entered into the licensee's corrective action program as CAR 200804000, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:  NCV 05000483/2008003-02, Inadequate Surveillance Procedure
Resulted in an Inoperable ECCS.
 
  - 19 - Enclosure 2 1R18 Plant Modifications (71111.18)
      a. Inspection Scope
The inspectors reviewed the design adequacy of the listed modifications.  This included verifying that the modification preparation did not impair the following:  (a) in-plant emergency/abnormal operating procedure actions, (b) key safety functions, and 
(c) operator response to loss of key safety functions.
The inspectors verified that postmodification testing maintained the plant in a safe configuration during testing and that the postmodification testing established operability by:  (a) verifying that unintended system interactions did not occur; (b) verifying that
performance characteristics, which could have been affected by the modification, met the design bases; (c) validating the appropriateness of modification design assumptions; and (d) demonstrating that the modification test acceptance criteria had been met.
* April 18, 2008, Modification M-08-0013 to separate fast and slow speed overload contacts for containment air coolers
* June 1, 2008, Temporary Modification TM 08-0003 for the instrument air system to provide an additional diesel-driven air compressor to improve system reliability while the system was in degraded reliability
Documents reviewed are listed in the attachment. 
These activities constituted two samples as defined by Inspection Procedure 71111.18.


      b. Findings
B. Licensee-Identified Violations
No findings of significance were identified
  Two violations of very low safety significance, which were identified by the licensee,
1R19 Postmaintenance Testing (71111.19)
  have been reviewed by the inspectors. Corrective actions taken or planned by the
      a. Inspection Scope
  licensee have been entered into the licensees corrective action program. These
The inspectors reviewed the following postmaintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
  violations and corrective action tracking numbers are listed in Section 4OA7.
* April 10, 2008, Job 08002765.900, Source Range N32 postmaintenance test
                                        -6-                                       Enclosure 2
* April 17, 2008, Postmaintenance test containment Cooler D, Modification 0800267/950(951)(952)
* May 7, 2008, Job 06524419.940, Emergency Diesel Generator B
* May 28, 2008, Job 08003910, Postmaintence test of Emergency Diesel Generator A following repair of jacket water leaks
* May 30, 2008, Job 08001080, Postmaintenance local leakrate test of containment personnel hatch door 
  - 20 - Enclosure 2 These activities were selected based upon the structure, system, and component's ability to impact risk.  The inspectors evaluated these activities to verify (as applicable):  the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was
returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test documentation was properly evaluated.  The inspectors evaluated the activities against Technical Specifications, the FSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately
ensured that the equipment met the licensing basis and design requirements.  In addition, the inspectors reviewed corrective action documents associated with postmaintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the attachment.
This inspection constitutes five samples as defined in Inspection Procedure 71111.19.      b. Findings
Introduction.  A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," was identified after the licensee failed to promptly correct leakage from diesel generator jacket water o-rings.
Description.  On February 20, 2008, during performance of Procedure OSP-NE-0001B, "Standby Diesel Generator 'B' Periodic Tests," Callaway operations personnel identified that the Emergency Diesel Generator B had an approximately 80 drop-per-minute jacket water leak.  Analysis by the licensee determined the cause of the leakage to be from premature failure of Nitrile type o-rings in the jacket water supply and return headers. 
Operational history at Callaway revealed o-ring failures prior to reaching 3 years of service life.  The o-rings responsible for the February 20, 2008, leakage had been in service since Refueling Outage 14 in October 2005.  Following restoration of Emergency Diesel Generator B, the licensee re-evaluated the preventative maintenance frequency for jacket water o-ring replacement.  Based on a review of prior o-ring failures, the replacement schedule for diesel generator jacket water o-rings was reduced from once every 3 years to once every refueling cycle. 
On May 28, 2008, during performance of Procedure OSP-NE-0001A, "Standby Diesel Generator 'A' Periodic Tests," Callaway operations personnel identified that Emergency Diesel Generator A had a 200 drop-per-minute jacket water leak.  Based on the quantity of the leakage, operations personnel declared Emergency Diesel Generator A
inoperable.  Similar to the condition observed on Emergency Diesel Generator B on February 20, 2008, the source of the leakage was from Nitrile type o-rings within the jacket water system.  While the licensee replaced the o-rings responsible for jacket water leakage following the February 20, 2008, surveillance, several Nitrile type o-rings installed during Refueling Outage 14 in October 2005 remained in service in both
Emergency Diesel Generators Trains A and B including those that failed during the May 28, 2008, surveillance.
 
  - 21 - Enclosure 2 Subsequent analysis by the licensee determined that the required mission time of the Emergency Diesel Generator A was preserved since adequate inventory in the jacket water expansion tank existed such that the leakage observed on May 28, 2008, would not have impacted the net positive suction head analysis for the jacket water cooling pump. 
Analysis.  The performance deficiency associated with this finding involved the licensee's failure to implement adequate corrective actions for an adverse condition.  Specifically, the licensee failed to correct degraded Nitrile type o-rings in Emergency Diesel Generator A after previously identifying the adverse condition on Emergency Diesel Generator B.  This finding was greater than minor because, if left uncorrected,
degraded diesel generator jacket water o-rings could become a more significant safety concern.  This finding affected the mitigating systems cornerstone.  Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," this finding was determined be of very low safety significance because it was a design deficiency confirmed not to result in loss of operability.  This finding had a crosscutting aspect in the area of human performance associated with the work control component because the licensee failed to plan work activities to support long-term equipment
reliability by addressing known degraded conditions in a more reactive than preventative manner [H.3(b)].
Enforcement.  10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that measures be established to assure conditions adverse to quality are
promptly identified and corrected.  Contrary to the above, the licensee failed to implement adequate corrective actions for the identified adverse condition that Nitrile type o-rings would prematurely fail prior to the completion of the regularly scheduled 3-year replacement interval.  Because this violation is of very low safety significance and has been entered into the licensee's corrective action program as CAR 200804164, this
violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:  NCV 05000483/2008003-03, Failure to Correct a Condition Adverse to Quality for Diesel Generator Jacket Water O-Rings.
1R22 Surveillance Testing (71111.22)
      a. Inspection Scope
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural
and Technical Specification requirements:
* April 2, 2008, Job 07513515.500, Routine surveillance auxiliary building Train A negative pressure test 
* April 4, 2008, Job 08501501, Routine surveillance Slave Relay K645 test of essential service water component lineup
* April 18, 2008, Job 08501499, Routine surveillance Slave Relay K615 test
* April 29, 2008, Job 08501254.500, Residual heat removal Pump A inservice test 
  - 22 - Enclosure 2
* May 5, 2008, Jobs 08502271 and 08503327, Routine surveillance containment base strong motion accelerometer seismic monitor calibration
* May 14, 2008, Job 07505653, Residual heat removal Train B valve inservice test
* June 11, 2008, Job 08504820, Routine surveillance diesel generator Train B 1-hour run
* June 17, 2008, Job 08503115, Safety injection system Train A valve inservice
test * June 18, 2008, Job 08505155, Routine surveillance ECCS flow path verification and venting
* June 23, 2008, Job 08506247, Reactor coolant system leakage surveillance, reactor coolant system inventory balance, plant status The inspectors observed in-plant activities and reviewed procedures and associated records to determine whether:  any preconditioning occurred; effects of the testing were
adequately addressed by control room personnel or engineers prior to the commencement of the testing; acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented; as left setpoints were within required ranges; the calibration frequency was in accordance with Technical
Specifications, the FSAR, procedures, and applicable commitments; measuring and test equipment calibration was current; test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied; test frequencies met Technical Specification requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other
applicable procedures; jumpers and lifted leads were controlled and restored where used; test data and results were accurate, complete, within limits, and valid; test equipment was removed after testing; where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable; where applicable for safety-related
instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure; equipment was returned to a position or status required to support the performance of the safety functions; and all problems identified during the testing were appropriately documented and dispositioned in the corrective action program.  Documents reviewed are listed in the attachment. 
The inspectors completed six routine, three inservice test, and one reactor coolant
system leakage samples.  
      b. Findings
Introduction.  A self-revealing Green NCV of Technical Specification 5.4.1.a, "Procedures," was identified after Callaway control room operators improperly entered the wrong Technical Specification action statement due to the failure to maintain the
Technical Specification Bases current.
 
  - 23 - Enclosure 2 Description.  On June 17, 2008, during surveillance testing, Valve EMHV8823 failed to indicate fully closed.  Since EMHV8823 is an isolation valve for containment Penetration 49, the licensee entered Technical Specification 3.6.3, "Containment Isolation Valves," Condition C, with an action to restore the valve to an operable status or isolate the penetration within 72 hours.  The control room staff believed the appropriate action statement was entered since Condition C is described in the  
Technical Specification Bases as applicable to flow paths that meet the requirements of a closed system per the Callaway FSAR.  Chapter 6.2.6.3 of the Callaway FSAR described Containment Penetration 49 as a closed engineered safety feature containment penetration.
Approximately 8 hours after Valve EMHV8823 had been declared inoperable, Callaway licensing personnel contacted the control room and informed them of an approved Technical Specification Bases change that did not allow the classification of containment Penetration 49 as a closed system.  Procedure APA-ZZ-00108, "Primary Licensing Document; Change/Revision Process," required that the change be implemented within 45 days following approval.  The Technical Specification Bases change was effective May 1, 2008, but had not been issued to the control room.  The change resulted in
Condition C of Technical Specification 3.6.3 applying specifically to penetrations for which a single containment isolation valve is credited per flow path.  Since containment Penetration 49 relies on multiple valves for flow path isolation, the licensee determined that Condition C of Technical Specification 3.6.3 was not applicable for Penetration 49, and the wrong Technical Specification action statement had been entered following the
failed surveillance on Valve EMHV8823.  The licensee determined that the more restrictive Technical Specification 3.6.3, Condition A, should have been entered with an action to isolate the affected penetration within 4 hours. 
The licensee performed a containment entry following discovery of entry into Technical
Specification 3.6.3, Condition A, and found that Valve EMHV8823 had failed its surveillance due to out-of-adjustment position indicator limit switches.  The valve was verified closed with power removed allowing exit from Technical Specification 3.6.3, Condition A.
Analysis.  The performance deficiency associated with this finding involved the licensee's failure to ensure the Technical Specification Bases were maintained current and available to the Callaway control room staff.  This finding was greater than minor because, if left uncorrected, the failure to maintain the Technical Specification Bases current could become a more significant safety concern.  This finding was determined to
affect the barrier integrity cornerstone.  Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," this finding is determined to be of very low safety significance since this finding did not represent an actual open pathway in the physical integrity of reactor containment and did not involve an actual reduction in function of hydrogen ignitors in the reactor containment.  This finding had a crosscutting aspect in the area of human performance associated with the decision making component because the licensee failed to communicate, in a timely manner, decisions to
personnel who have a need to know the information in order to perform work safely [H.1(c)].
Enforcement.  Technical Specification 5.4.1.a, "Procedures," required that written procedures be established and implemented covering activities specified in Appendix A,
"Typical Procedures for Pressurized Water Reactors," of Regulatory Guide 1.33, "Quality 
  - 24 - Enclosure 2 Assurance Program Requirements (Operation)," February 1978.  Regulatory Guide 1.33, Appendix A, Section 1, required administrative procedures for procedure review and approval.  Procedure APA-ZZ-00108 provides a process for implementing Technical Specification Bases change notices.  Contrary to the above, on May 1, 2008, Procedure APA-ZZ-00108 was not adequate to ensure changes to the Technical Specification Bases were implemented in a timely manner.  Because of the very low
safety significance and AmerenUE's action to place this issue in their corrective action program as CAR 200805283, this violation is being treated as an NCV in accordance with Section VI.A.1 of the Enforcement Policy:  NCV 05000483/2008003-04, Failure to Maintain an Adequate Technical Specification Bases Change Process.  
2. RADIATION SAFETY
Cornerstone:  Occupational Radiation Safety 2OS1 Access Control to Radiologically Significant Areas (71121.01)
      a. Inspection Scope
This area was inspected to assess the licensee's performance in implementing physical and administrative controls for airborne radioactivity areas, radiation areas, high radiation areas, and worker adherence to these controls.  The inspectors used the requirements in 10 CFR Part 20, the Technical Specifications, and the licensee's
procedures required by Technical Specifications as criteria for determining compliance.  During the inspection, the inspectors interviewed the radiation protection manager, radiation protection supervisors, and radiation workers.  The inspectors performed independent radiation dose rate measurements and reviewed the following items:
* Performance indicator events and associated documentation packages reported by the licensee in the occupational radiation safety cornerstone 
* Controls (surveys, posting, and barricades) of radiation, high radiation, or airborne radioactivity areas 
* Radiation work permits, procedures, engineering controls, and air sampler locations 
* Physical and programmatic controls for highly activated or contaminated materials (non-fuel) stored within spent fuel and other storage pools 
* Self-assessments, audits, LERs, and special reports related to the access control program since the last inspection 
* Changes in licensee procedural controls of high dose rate - high radiation areas and very high radiation areas 
* Controls for special areas that have the potential to become very high radiation areas during certain plant operations 
* Posting and locking of entrances to accessible high dose rate - high radiation areas and very high radiation areas 
  - 25 - Enclosure 2 Documents reviewed are listed in the attachment. 
  The inspectors completed 8 of the required 21 samples. 
      b. Findings
  No findings of significance were identified.  
2OS2 ALARA Planning and Controls (71121.02)
      a. Inspection Scope
  The inspectors assessed licensee performance with respect to maintaining individual and collective radiation exposures as low as is reasonably achievable (ALARA).  The
inspectors used the requirements in 10 CFR Part 20 and the licensee's procedures required by technical specifications as criteria for determining compliance.  The inspectors interviewed licensee personnel and reviewed:
* Current 3-year rolling average collective exposure 
* Site-specific trends in collective exposures, plant historical data, and source-term measurements 
* Site-specific ALARA procedures
* Work activities of highest exposure significance during the inspection 
* Integration of ALARA requirements into work procedure and radiation work permit documents
* Post-job (work activity) reviews 
* Workers' use of the low dose waiting areas 
* First-line job supervisors' contribution to ensuring work activities are conducted in a dose efficient manner 
* Records detailing the historical trends and current status of tracked plant source terms and contingency plans for expected changes in the source term due to changes in plant fuel performance issues or changes in plant primary chemistry 
* Source-term control strategy or justifications for not pursuing such exposure reduction initiatives 
* Specific sources identified by the licensee for exposure reduction actions,  priorities established for these actions, and results achieved since the last refueling cycle 
* Radiation worker and radiation protection technician performance during work activities in radiation areas, airborne radioactivity areas, or high radiation areas 
  - 26 - Enclosure 2  
* Declared pregnant workers during the current assessment period, monitoring controls, and the exposure results 
* Self-assessments, audits, and special reports related to the ALARA program since the last inspection 
* Resolution through the corrective action process of problems identified through post-job reviews and post-outage ALARA report critiques 
* Corrective action documents related to the ALARA program and follow-up activities, such as initial problem identification, characterization, and tracking
* Effectiveness of self-assessment activities with respect to identifying and addressing repetitive deficiencies or significant individual deficiencies  Documents reviewed are listed in the attachment. 
The inspectors completed 9 of the required 15 samples and 8 of the optional samples. 
      b. Findings
  No findings of significance were identified.
4. OTHER ACTIVITIES 4OA1 Performance Indicator Verification (71151)
  .1 Data Submission Issue
      a. Inspection Scope
The inspectors performed a review of the data submitted by the licensee for the first Quarter 2008 performance indicators for any obvious inconsistencies prior to its public release in accordance with IMC 0608, "Performance Indicator Program."


This review was performed as part of the inspectors' normal plant status activities and, as such, did not constitute a separate inspection sample.
                                          REPORT DETAILS
       b. Findings
Summary of Plant Status
No findings of significance were identified.  
AmerenUE operated the Callaway Plant at near 100 percent for the entire quarter.
.2 Safety System Functional Failures
1.    REACTOR SAFETY
  Cornerstone:  Mitigating Systems
      Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity and
    a. Inspection Scope
       Emergency Preparedness
The inspectors sampled licensee submittals for the safety system functional failures performance indicator for the period March 2007 until March 2008.  To determine the accuracy of the performance indicator data reported during this period, performance indicator definitions and guidance contained in the Nuclear Energy Institute (NEI) 
1R01 Adverse Weather Protection (71111.01)
  - 27 - Enclosure 2 Document 99-02, Revision 5, "Regulatory Assessment Performance Indicator Guideline," and NUREG-1022, "Event Reporting Guidelines 10 CFR 50.72 and 50.73," definitions and guidance were used. The inspectors reviewed the licensee's operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC integrated inspection reports for the period of  2nd Quarter 2007, through 1st Quarter 2008 to validate the accuracy of the  
.1    Readiness of Offsite and Alternate AC Power System
submittals.  The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the attachment.
  a. Inspection Scope
      The inspectors reviewed the licensees plant features, training lesson plans, and
This inspection constitutes one safety system functional failures sample as defined by Inspection Procedure 71151.  
      procedures for operation and continued availability of offsite and alternate AC power
       b. Findings
      systems to verify they were appropriate. The review included communication protocols
No findings of significance were identified.
      and agreement procedures between the transmission system operator and the nuclear
.3 Mitigating Systems Performance Index - High Pressure Injection Systems
      power plant to verify that appropriate information is exchanged when issues arise that
  Cornerstone:  Mitigating Systems
      could impact the offsite power system. Specifically, the procedures were verified to
     a. Inspection Scope
      ensure they specified:
The inspectors sampled licensee submittals for the mitigating systems performance index - high pressure injection systems performance indicator for the period from March 2007 until March 2008.  To determine the accuracy of the performance indicator data reported during this period, performance indicator definitions and guidance
      *      Required actions needed when notified by the transmission system operator that
contained in the NEI Document 99-02, 5, "Regulatory Assessment Performance Indicator Guideline," Revision 5, were used.  The inspectors reviewed the licensee's operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports for the period of 2nd Quarter 2007 through 1st Quarter 2008 to validate the accuracy of the submittals. 
              posttrip voltage of the offsite power system would not be acceptable to assure
The inspectors reviewed the mitigating systems performance index component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance.  The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the attachment.  
              the continued operation of safety related loads without transferring to the onsite
              power supply.
      *      Compensatory actions needed when it is not possible to predict the posttrip
              voltage at the nuclear power plant for current grid conditions.
       *      Required assessment of plant risk based on maintenance activities which could
              affect grid reliability, or the ability of the transmission system to provide the offsite
              power system.
      *     Required communications between the nuclear power plant and the transmission
              system operator when changes at the nuclear power plant could impact the
              transmission system, or when the capability of the transmission system to
              provide adequate offsite system power is challenged.
      On May 16, 2008, the inspectors evaluated the licensee staffs preparations for summer
      readiness of offsite and AC power systems against the sites procedures and determined
      that the staffs actions were adequate. Documents reviewed are listed in the
      attachment.
      These activities constituted one readiness of offsite power inspection sample as defined
      by Inspection Procedure 71111.01.
                                              -7-                                        Enclosure 2


This inspection constitutes one mitigating systems performance index high pressure injection systems sample as defined by Inspection Procedure 71151.
  b. Findings
      b. Findings
      No findings of significance were identified.
No findings of significance were identified.  
.2   Readiness for Impending Adverse Weather Conditions
 
  a. Inspection Scope
  - 28 - Enclosure 2 .4 Occupational Exposure Control Effectiveness
      On May 2, 2008, the inspectors completed a review of the licensee's readiness for
  Cornerstone:  Occupational Radiation Safety
      impending adverse weather involving severe thunderstorms. The inspectors:
    a. Inspection Scope
      (1) reviewed plant procedures, the Final Safety Analysis Report (FSAR), and Technical
The inspectors reviewed licensee documents from October 1, 2007, through March 31, 2008.  The review included corrective action documentation that identified occurrences in locked high radiation areas (as defined in the licensee's Technical Specifications),  
      Specifications to ensure that operator actions defined in adverse weather procedures
very high radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel exposures (as defined in NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 5).  Additional records reviewed included ALARA records and whole body counts of selected individual exposures.  The inspectors interviewed licensee personnel that were accountable for collecting and evaluating the performance indicator data.  In
      maintained the readiness of essential systems; (2) walked down portions of the
addition, the inspectors toured plant areas to verify that high radiation, locked high radiation, and very high radiation areas were properly controlled. Performance indicator definitions and guidance contained in NEI 99-02, Revision 5, were used to verify the basis in reporting for each data element.
      emergency diesel generators and offsite power systems to ensure that adverse weather
The inspectors completed the required sample (1) in this cornerstone.  
      protection features were sufficient to support operability; (3) reviewed maintenance
      b. Findings
      records to determine that applicable surveillance requirements were current before the
No findings of significance were identified.  
      anticipated severe thunderstorms developed; and (4) reviewed plant modifications,
.5 Radiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences
      procedure revisions, and operator work arounds to determine if recent facility changes
   Cornerstone:  Public Radiation Safety
      challenged plant operation. Documents reviewed by the inspectors are listed in the
    a. Inspection Scope
      attachment.
The inspectors reviewed licensee documents from October 1, 2007, through March 31, 2008.  Licensee records reviewed included corrective action documentation that identified occurrences for liquid or gaseous effluent releases that exceeded performance indicator thresholds and those reported to the NRC.  The inspectors interviewed licensee
      These activities constituted one readiness for impending adverse weather inspection
personnel that were accountable for collecting and evaluating the performance indicator data. Performance indicator definitions and guidance contained in NEI 99-02, Revision 5, were used to verify the basis in reporting for each data element.
      sample as defined by Inspection Procedure 71111.01.
  The inspectors completed the required sample (1) in this cornerstone.
  b. Findings
       b. Findings
      No findings of significance were identified.
No findings of significance were identified.  
1R04 Equipment Alignments (71111.04)
  4OA2 Identification and Resolution of Problems (71152)
.1   Quarterly Partial System Walkdowns
Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
  a. Inspection Scope
 
      The inspectors performed partial system walkdowns of the following risk-significant
  - 29 - Enclosure 2 .1 Routine Review of Items Entered into the Corrective Action Program
      systems:
      a. Inspection Scope
      *      June 3, 2008, Train A auxiliary feedwater system while the Train B motor-driven
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities to verify that they were being entered into the licensee's corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed.  The attributes reviewed included:  the complete and accurate identification of the problem; that timeliness was
              auxiliary feedwater pump was out of service for planned maintenance.
commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrence reviews were proper and adequate; and that the classification, prioritization, focus, and timeliness of corrective actions were commensurate with safety and sufficient to prevent recurrence of the issue. 
      *      June 10, 2008, Train A 480 volt NG Class 1E switchgear while the Train B
              emergency diesel generator was out of service for planned and emergent
              maintenance issues.
      The inspectors selected these systems based on their risk significance relative to the
       reactor safety cornerstones at the time they were inspected. The inspectors attempted
      to identify discrepancies that could impact the function of the system, and, therefore,
      potentially increase risk. The inspectors reviewed applicable operating procedures,
      system diagrams, FSAR, Technical Specification requirements, outstanding work orders,
      corrective action documents, and the impact of ongoing work activities on redundant
      trains of equipment in order to identify conditions that could have rendered the systems
                                          -8-                                      Enclosure 2


These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples.  
      incapable of performing their intended functions. The inspectors also walked down
       b. Findings
       accessible portions of the systems to verify components and support equipment were
No findings of significance were identified.
       aligned correctly and were operable. The inspectors examined the material condition of
.2 Daily Corrective Action Program Reviews
      the components and observed operating parameters of equipment to verify that there
       a. Inspection Scope
      were no obvious deficiencies. The inspectors also verified that the licensee had properly
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's corrective action program. This review was
      identified and resolved equipment alignment problems that could cause initiating events
accomplished through inspection of the station's daily condition report packages.  
      or impact the capability of mitigating systems or barriers and entered them into the
These daily reviews were performed, by procedure, as part of the inspectors' daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.     
      corrective action program with the appropriate significance characterization. Documents
      b. Findings
      reviewed are listed in the attachment.
  No findings of significance were identified.  
      These activities constituted two partial system walkdown samples as defined by
.3 Selected Issue Follow-up Inspection
      Inspection Procedure 71111.04.
      a. Inspection Scope
   b. Findings
The inspectors selected the below listed issues for a more in-depth review.  The inspectors considered the following during the review of AmerenUE's actions: (1) complete and accurate identification of the problem in a timely manner; (2) evaluation and disposition of operability/reportability issues; (3) consideration of extent of condition,  
      No findings of significance were identified.
generic implications, common cause, and previous occurrences; (4) classification and prioritization of the resolution of the problem; (5) identification of root and contributing causes of the problem; (6) identification of corrective actions; and (7) completion of corrective actions in a timely manner.  
.2    Complete System Walkdown (71111.04S)
  - 30 - Enclosure 2
  a. Inspection Scope
* Voiding discovered in the common residual heat removal discharge piping for high pressure recirculation.
      On April 17, 2008, the inspectors performed a complete system alignment inspection of
* FSAR changes/updates Documents reviewed are listed in the attachment.  
      Train B of the residual heat removal system to verify the functional capability of the
This inspection constituted two in-depth problem identification and resolution samples.  
      system. The inspectors selected this system because it was considered both
      b. Findings
      safety-significant and risk-significant in the licensees probabilistic risk assessment. The
Introduction. The inspectors identified a Green violation of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," because the licensee failed to take corrective actions to preclude repetition of void formations in the ECCS, a significant condition adverse to quality (SCAQ).  Contributors to the violation included:  (1) the failure of corrective actions from inspection report findings NCV 05000483/2005002-01, 05000483/2006012-04 and CAR 200501092 to ensure adequate fill and vent of 
      inspectors walked down the system to review mechanical and electrical equipment line
systems following maintenance to replace safety injection system relief valves, and (2) inadequate extent of condition reviews in responding to internal and external operating experience associated with pipe sloping issues in the safety injection system. 
      ups, electrical power availability, system pressure and temperature indications, as
Description.  On May 21, 2008, the Callaway Plant staff initiated CAR 200804000, a SCAQ corrective action document, indicating that some piping in Train A safety injection system suction lines had incorrect sloping and were susceptible to voiding due to high
      appropriate, component labeling, component lubrication, component and equipment
points.  Callaway Plant engineering performed ultrasonic inspection of the safety injection system common suction piping Line EM023-HCB - 6" and discovered a 6.6 cubic foot voided area.  This exceeded the allowable void fraction of 2.1 cubic feet required for operability.  This voided piping, determined to have existed for over a year, was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The  
      cooling, hangers and supports, operability of support systems, and to ensure that
maintenance restoration failed to perform an adequate fill and vent to ensure the suction pipe was full of water. 
      ancillary equipment or debris did not interfere with equipment operation. The inspectors
In 2005 and 2006 the NRC issued NCVs regarding ineffective corrective actions related to safety injection system voids in discharge piping (05000483/2005002-01 dated May 6,  
      reviewed a sample of past and outstanding work orders to determine whether any
2005, and 05000483/2006012-04 dated December 26, 2006). These were each 10 CFR Part 50, Appendix B, Criterion XVI, NCVs, each for SCAQ. The Callaway Plant staff issued CAR 200501092 as a SCAQ corrective action document. The CAR determined that the causes of the voids (2004, 2005, and 2006) were related to incorrect pipe sloping (allowing high points where voids could not be swept away by normal online
      deficiencies significantly affected the system function. In addition, the inspectors
pump surveillances) and inadequate postmaintenance fill and vent operations (following discharge piping relief Valve EM8853A replacement) to ensure the piping was full of water.    Inadequate Operating Experience and Extent of Condition Corrections:  The inspectors identified several related examples where the licensee had performed either
      reviewed the corrective action program database to ensure that system equipment
inadequate operating experience evaluations, inadequate extent of condition reviews, or inadequate procedure corrections.
      alignment problems were being identified and appropriately resolved. The documents
Callaway CAR 200501092 referenced industry operating experience at Beaver Valley Unit 2 in 2002:  "The void was located in the piping used following a loss of coolant 
      used for the walkdown and issue review are listed in the attachment.
   - 31 - Enclosure 2 accident after the transfer to containment sump recirculation. The piping containing the void led to a common suction header for both trains of high head pumps."  This was the same location as the voiding discovered at Callaway Plant on May 21, 2008.   
      These activities constituted one complete system walkdown sample as defined by
NRC Information Notice 2006-21, "Operating Experience Regarding Entrainment of Air into Emergency Core Cooling and Containment Spray Systems," dated September 21,
      Inspection Procedure 71111.04.
2006, discussed mechanisms that could result in air entrainment on the suction sides of emergency core cooling pumps. The notice emphasized the importance of ensuring that entrained air will not enter suction supply lines and impair the ability of the ECCS and containment spray pumps to perform their safety function.  
  b. Findings
The licensee's evaluation of NRC Information Notice 2006-21 was documented in CAR 200608956.  It stated that the information notice was applicable to Callaway and that past review of these operating experiences and Callaway procedures and practices were adequate. The CAR was closed December 5, 2006.
      No findings of significance were identified.
Callaway CAR 200501092 had Action 7 assigned to address the previous NRC violations discussed above.  The action required that system specific fill and vent
                                            -9-                                        Enclosure 2
restoration guidance be developed to address maintenance on ECCS safety-related systems.  Initially, operating department Standing Order 05-002 dated June 8, 2005, stated that the CAR 200501092 common cause analysis supported the need for formalized restoration instructions.  Until the system specific restoration instructions were developed, the standing order required reactor operators to perform reviews to
 
ensure dynamic filling and venting occurred to reduce the susceptibility of voiding. Also nuclear engineering department staff were to provide concurrence on such restoration plans.  Night Order ODP-ZZ-00310, "System Fill and Vent," issued February 13, 2006, reiterated that reactor operator reviews and engineering concurrence were required when these risk-significant systems were drained.  However, on May 7, 2007,  
1R05 Fire Protection (71111.05)
Procedure OTN-EM-00001, "Safety Injection System," (developed to address filling and venting evaluations) had Line EM-023-HCB - 6" isolated by Valve EMHIS8807B being closed. The procedure did not include use of the available installed vent Valve EM179 for this line.
.1    Quarterly Fire Inspector Tours (71111.05Q)
Callaway monthly Surveillance OSP-SA-00003, "Emergency Core Cooling Flow Path Verification and Venting," had a purpose to:  "Verify the ECCS is full of water in accordance with Technical Specification Surveillance Requirement 3.5.2.3."  This monthly surveillance was reviewed as part of CAR 200501092 corrective actions. Callaway engineering had determined that residual heat removal pump discharge vent
  a. Inspection Scope
Valve EJV0193 to the safety injection suction line was the high point vent for these lines and was thus sufficient to vent supply Line EM-023-HCB - 6"  to the safety injection pumps.  However, this vent valve was not adequate due to the pipe sloping issues and normally closed Valves EMHIS8807A/B.  The monthly verification and vent procedure was inadequate to remove the air entrained by the May 7, 2007, relief valve maintenance.  See Section 1R15, NCV 05000483/2008003-02. 
      The inspectors conducted fire protection walkdowns which were focused on availability,
      accessibility, and the condition of firefighting equipment in the following risk-significant
Callaway CARs 200800226 and 200800246, initiated in January 2008, discussed operating experience at Wolf Creek Nuclear Operating Corporation describing gas voiding in the residual heat removal piggyback Line EM-022-HCB - 6" to the suction of centrifugal charging pumps and safety injection pumps.  The CARs stated that Callaway had taken a proactive approach and had immediately performed ultrasonic testing to  
      plant areas:
demonstrate that the associated piping was water solid.  However, the adjacent 
      *      March 27, 2008, Fire Area C-21, Lower Cable Spreading Room
  - 32 - Enclosure 2 connecting Line EM-023-HCB - 6" had not been vented nor had ultrasonic testing occurred since the May 7, 2007, relief Valve EM8858A maintenance.
      *      April 16, 2008, Fire Area A-17, Electrical Penetration Room (South)
NRC Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems," was issued January 11, 2008. The Callaway Plant staff initiated CAR 200800298 to respond to the generic letterThe
      *      April 25, 2008, Condensate Storage Tank
generic letter identified that a licensing basis concern existed for some plants, such as Callaway, that Technical Specifications require verifying that ECCS discharge piping is full of water but may not include verification of the suction piping despite the realistic concern that gas accumulation in suction piping may be more serious than gas accumulation in discharge piping.  The void found in Line EM-023-HCB - 6" was the
      *      April 29, 2008, Fire Area A-23, Main Steam and Feedwater Isolation Valve
discharge of the residual heat removal pumps providing suction to the Train A safety injection pump. The Callaway monthly Surveillance OSP-SA-00003, "Emergency Core Cooling Flow Path Verification and Venting," did not test for or vent the discharge line from residual heat removal to safety injection pump suction piping.
              Enclosure
Analysis. The inspectors determined that the failure to restore compliance within a reasonable time by establishing measures to prevent void formation in ECCS suction
      *      April 30, 2008, Reactor Building
piping for the Train A safety injection system was a performance deficiency.  This finding is more than minor because it was similar to Example 3e of NRC Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues," and met the "Not Minor If," criteria because the failure to meet the licensee's administrative requirement for allowable void fraction impacted the ability of the Train A safety injection system to  
      *      June 18, 2008, Fire Area A-1, North Pipe Chase
function upon initiation of high-pressure recirculation. Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," the inspectors determined that this finding should be evaluated using the Phase 2 process described in Manual Chapter 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations."
      The inspectors reviewed areas to assess if the licensee implemented a fire protection
The senior reactor analyst determined that the risk of this finding was bounded by that analyzed for NCV 05000423/2008003-02 (See Section 1R15.b.2).  Therefore, this finding was of very low risk significance (Green). 
      program that adequately controlled combustibles and ignition sources within the plant,
      effectively maintained fire detection and suppression capability, maintained passive fire
This finding has a crosscutting aspect in the area of problem identification and resolution associated with the corrective action component because AmerenUE failed to thoroughly evaluate voiding problems such that the resolutions addressed causes and extent of condition, as necessary.  This also includes, for significant problems, conducting effectiveness reviews of corrective actions to ensure that the problems are resolved
      protection features in good material condition, and implemented adequate compensatory
[P.1(c)].
      measures for out of service, degraded or inoperable fire protection equipment, systems,
Enforcement.  10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires the licensee to, in the case of SCAQ, establish measures to assure that the cause of the condition is determined and corrective action is taken to preclude repetition.  Contrary to the above, from December 26, 2006, to May 21, 2008, the licensee did not implement corrective action to preclude repetition of void formation in the safety injection piping
      or features in accordance with the licensees fire plan. The inspectors selected fire
which the licensee categorized as an SCAQ. Specifically, void formation recurred after performing maintenance on relief valve.  Valve EM8858A, on May 7, 2007.  Previously discovered voiding of the safety injection system was last documented as an SCAQ in NCV 05000483/2006012-04 dated December 26, 2006.  For each instance of the previously discovered voids, the causes were determined to be related to inadequate fill  
      areas based on their overall contribution to internal fire risk as documented in the plants
and vent of the system piping following relief valve replacements and design deficiencies
      Individual Plant Examination of External Events with later additional insights, their
  - 33 - Enclosure 2 associated with inadequate sloping of the piping. It was a reasonable assumption that maintenance that drained either the suction or discharge piping could create significant void areas.  
      potential to impact equipment which could initiate or mitigate a plant transient, or their
Although this violation is of very low safety significance, the violation is being cited in a Notice of Violation consistent with Section VI.A.1 of the NRC Enforcement  
      impact on the plants ability to respond to a security event. The inspectors verified that
Policy because the licensee did not restore compliance within a reasonable time after a previous violation NCV 05000483/2006012-04 was identified: VIO 05000483/2008003-05, Failure to Prevent Recurrence of Voids in ECCS Cold Leg Recirculation Piping. This finding has been entered into the licensee's corrective action program as a SCAQ in CAR 200804000.  
      fire hoses and extinguishers were in their designated locations and available for
.4 Semiannual Trend Review
      immediate use; that fire detectors and sprinklers were unobstructed, that transient
The inspectors assessed trends that might indicate the existence of a more significant safety issue. These issues included trends that might not rise to the level of an inspection finding.  
      material loading was within the analyzed limits; and fire doors, dampers, and penetration
      seals appeared to be in satisfactory condition. Documents reviewed are listed in the
      attachment.
      These activities constituted six quarterly fire protection inspection samples as defined by
      Inspection Procedure 71111.05.
  b. Findings
      No findings of significance were identified.
.2    Annual Fire Protection Drill Observation (71111.05A)
  a. Inspection Scope
      On March 27, 2008, the inspectors observed a fire brigade activation due to a report of
      smoke in the laundry decontamination area. The observation evaluated the readiness of
                                          - 10 -                                      Enclosure 2
 
    the plant fire brigade to fight fires. The inspectors verified that the licensee staff
    identified deficiencies; openly discussed them in a self-critical manner at the drill debrief,
    and took appropriate corrective actions. Specific attributes evaluated were: (1) proper
    wearing of turnout gear and self-contained breathing apparatus; (2) proper use and
    layout of fire hoses; (3) employment of appropriate fire fighting techniques; (4) sufficient
    firefighting equipment brought to the scene; (5) effectiveness of fire brigade leader
    communications, command, and control; (6) search for victims and propagation of the
    fire into other plant areas; (7) smoke removal operations; (8) utilization of preplanned
    strategies; (9) adherence to the preplanned drill scenario; and (10) drill objectives.
    Documents reviewed are listed in the attachment.
    These activities constituted one annual fire protection inspection sample as defined by
    Inspection Procedure 71111.05.
   b. Findings
    No findings of significance were identified.
1R06 Flood Protection Measures (71111.06)
    Internal Flooding
   a. Inspection Scope
    The inspectors reviewed selected risk-significant plant design features and licensee
    procedures intended to protect the plant and its safety related equipment from internal
    flooding events. The inspectors reviewed flood analyses and design documents,
    including the FSAR, engineering calculations, and abnormal operating procedures for
    licensee commitments. The inspectors reviewed licensee drawings to identify areas and
    equipment that may be affected by internal flooding caused by the failure or
    misalignment of nearby sources of water. The inspectors also reviewed the licensees
    corrective actions for previously identified flood-related items. The inspectors performed
    a walkdown of the following plant area to assess the adequacy of any watertight doors
    and verify drains and sumps were clear of debris and operable, and that the licensee
    complied with its flooding related commitments:
    *        June 23, 2008, Control Building West Corridor
    The document reviewed during this inspection is listed as follows:
      *      Callaway Action Request 200805189
    This inspection constituted one internal flooding sample as defined in Inspection
    Procedure 71111.06.
  b. Findings
    No findings of significance were identified.
                                            - 11 -                                     Enclosure 2
 
1R11 Licensed Operator Requalification Program (71111.11)
  a. Inspection Scope
    On June 2, 2008, the inspectors observed a crew of licensed operators perform a
    Cycle 08-3 as found scenario in the plants simulator to verify that operator performance
    was adequate, evaluators were identifying and documenting crew performance
    problems, and that training was being conducted in accordance with licensee
    procedures. The scenario involved an operating design basis earthquake with a lockout
    on essential 4 kV Bus NB01. The inspectors evaluated the crew in the following areas:
    *        Licensed operator performance
    *        Crew clarity and formality of communications
    *        Ability to take timely actions in the conservative direction
    *        Prioritization, interpretation, and verification of annunciator alarms
    *        Correct use and implementation of abnormal and emergency procedures
    *        Control board manipulations
    *        Oversight and direction from supervisors
    *        Ability to identify and implement appropriate Technical Specification actions and
              Emergency Plan actions and notifications
    The crews performance in these areas was compared to pre-established operator action
    expectations and successful critical task completion requirements. Documents reviewed
    are listed in the attachment.
    This inspection constituted one quarterly licensed operator requalification program
    sample as defined in Inspection Procedure 71111.11.
  b. Findings
    No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12)
  a. Inspection Scope
    The inspectors evaluated degraded performance issues involving the following
    risk-significant systems:
    *        May 15, 2008, Callaway Action Request (CAR) 200801644, an additional anode
              was found in the north end of the Train A emergency diesel generator intercooler
    *        May 15, 2008, CAR 200802854, KKJ01A (Train A emergency diesel generator)
              engine oil sump high
                                            - 12 -                                   Enclosure 2
 
      The inspectors reviewed events such as where ineffective equipment maintenance has
      resulted in valid or invalid automatic actuations of risk-important systems and
      independently verified the licensee's actions to address system performance or condition
      problems in terms of the following:
      *        Implementing appropriate work practices
      *        Identifying and addressing common cause failures
      *        Scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule
      *        Characterizing system reliability issues for performance
      *        Charging unavailability time
      *        Trending key parameters for condition monitoring
      *        Ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or reclassification
      *        Verifying appropriate performance criteria for structures, systems, and
              components/functions classified as (a)(2) or appropriate and adequate goals and
              corrective actions for systems classified as (a)(1)
      The inspectors assessed performance issues with respect to the reliability, availability,
      and condition monitoring of the system. The inspectors verified maintenance
      effectiveness issues were entered into the corrective action program with the appropriate
      significance characterization. Documents reviewed are listed in the attachment.
      This inspection constituted two quarterly maintenance effectiveness samples as defined
      in Inspection Procedure 71111.12Q.
  bFindings
      No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
  a.  Inspection Scope
      The inspectors reviewed the licensee's evaluation and management of plant risk for the
      maintenance and emergent work activities affecting risk-significant and safety-related
      equipment listed below to verify that the appropriate risk assessments were performed
      prior to removing equipment for work:
      *      April 3, 2008, Routine - Work on turbine-driven auxiliary feedwater
              Valve KAPCV-0102
      *      April 21, 2008, Emergency Diesel Generator A lube oil trouble shooting
    *        April 28, 2008, Routine - associated with Loose Creek-Callaway 345 kV line
              outage
                                          - 13 -                                    Enclosure 2
 
    *      June 10, 2008, Risk management actions associated with Emergency Diesel
            Generator B jacket water o-ring replacement outage
    These activities were selected based on their potential risk significance relative to the
    reactor safety cornerstones. As applicable for each activity, the inspectors verified that
    risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
    and complete. When emergent work was performed, the inspectors verified that the
    plant risk was promptly reassessed and managed. The inspectors reviewed the scope
    of maintenance work, discussed the results of the assessment with the licensee's
    probabilistic risk analyst or shift technical advisor, and verified plant conditions were
    consistent with the risk assessment. The inspectors also reviewed Technical
    Specification requirements and walked down portions of redundant safety systems,
    when applicable, to verify risk analysis assumptions were valid and applicable
    requirements were met. Documents reviewed are listed in the attachment.
    These activities constituted four samples as defined by Inspection Procedure 71111.13.
  b. Findings
    No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
  a. Inspection Scope
    The inspectors reviewed the following issues:
    *      March 26, 2008, CARs 200802348, 200802365, and 200802264, Containment
            coolers inoperable in fast speed
    *      April 4, 2008, CARs 200800461 and 200802625, Containment recirculation sump
            operability determination, Revisions 3 and 4
    *      April 9, 2008, Source Range Channel N32 inoperable due to a failed surveillance
    *      April 23, 2008, Component cooling water system following Valve EGHV0069
            failing inservice test stroke time surveillance
    *      April 30, 2008, CAR 200803465, Emergency diesel generator Garlock flexible
            expansion joints
    *      May 6, 2008, CAR 200803462, Voiding identified in containment spray pump
            piping from sump
    *      May 22, 2008, CAR 200904000, Line EM-023 allowable void fraction exceeded
    The inspectors selected potential operability issues based on the risk significance of the
    associated components and systems. The inspectors evaluated the technical adequacy
    of the evaluations to ensure that Technical Specification operability was properly justified
    and the subject component or system remained available such that no unrecognized
    increase in risk occurred. The inspectors compared the operability and design criteria in
    the appropriate sections of the Technical Specifications and FSAR to the licensees
                                          - 14 -                                      Enclosure 2
 
      evaluations to determine whether the components or systems were operable. Where
      compensatory measures were required to maintain operability, the inspectors
      determined whether the measures in place would function as intended and were
      properly controlled. The inspectors determined, where appropriate, compliance with
      bounding limitations associated with the evaluations. Additionally, the inspectors
      reviewed a sample of corrective action documents to verify that the licensee was
      identifying and correcting deficiencies associated with operability evaluations.
      Documents reviewed are listed in the attachment.
      This inspection constituted seven samples as defined in Inspection Procedure 71111.15.
  b. Findings
.1    Introduction. A self-revealing Green noncited violation (NCV) of 10 CFR Part 50,
      Appendix B, Criterion III, Design Control, was identified after determining that the
      licensee had not adequately selected and reviewed the suitability of the design of the
      containment air cooler control circuitry.
      Description. On March 26, 2008, Containment Air Cooler A fan shut down when shifted
      from fast to slow speed. Troubleshooting by the licensee determined that voltage was
      lost to the control power circuitry when the fast speed thermal overload tripped. Since
      the overload contacts were wired in series, Containment Air Cooler A experienced a
      complete loss of control power rendering it inoperable. AmerenUE personnel noted that
      Precaution 3.6 of Procedure OTN-GN-00001, Containment Cooling and CRDM
      Cooling, Revision 14, cautioned that high pressure and cool temperatures across
      containment coolers will cause the coolers to operate close to the setpoint of the thermal
      overloads. However, the licensees operability determination dismissed the 1987
      precaution as not having a technical basis believing it was implemented to address
      discrepancies in motor overload setpoints. Later, the licensee determined that operation
      of containment air coolers in fast speed, during a period of higher than normal
      containment pressure, challenged the fast speed thermal overload setpoint and resulted
      in the trip of Containment Air Cooler A on March 26, 2008. As an interim measure to
      prevent a trip from fast speed, the licensee imposed a standing order to maintain the
      containment coolers in slow speed.
      The licensee analyzed the potential impact of the newly discovered adverse containment
      cooler design vulnerability against design basis accident scenarios. The licensee
      determined that a hot zero power main steam line break results in a delayed safety
      injection signal allowing the fan motor overloads to trip prior to being shed by the load
      sequencer. The containment air coolers would then experience a complete loss of
      control power and would not be capable of automatically restarting in slow speed. The
      analysis revealed that in this scenario, utilizing assumed accident conditions, the peak
      containment pressure would exceed the 48.1 psig limit described in the FSAR.
      However, analysis using actual plant conditions determined that the peak containment
      pressure limit of 48.1 psig would be preserved. The licensee submitted a licensee event
      report (LER) as required by 10 CFR 50.73 since the inadequate containment air cooler
      control circuitry resulted in a condition prohibited by the plants Technical Specifications.
      The inspectors review of the licensees LER is described in Section 4OA3 of this report.
      To address the design deficiency associated with the containment air cooler control
      circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit
                                          - 15 -                                    Enclosure 2
 
  such that tripping of the fast speed overloads would not impact the safety-related slow
  speed function of the containment air coolers.
  Analysis. The performance deficiency associated with this finding involved the
  licensees failure to ensure the design of the containment air cooler control circuitry was
  suitable for all plant conditions. This finding was greater than minor because it was
  associated with the barrier integrity cornerstone attribute of design control and affects
  the associated cornerstone objective to provide reasonable assurance that physical
  design barriers protect the public from radio nuclide releases caused by accidents or
  releases. Using Manual Chapter 0609, Appendix H, Containment Integrity Significance
  Determination Process," this finding was determined to be a Type B finding since it was
  related to a degraded condition that has potentially important implications for the integrity
  of the containment, without affecting the likelihood of core damage. This finding was
  found to be of very low safety significance since containment coolers are structures,
  systems, and components that have no impact on large early release frequency. The
  inspectors determined that this finding does not have a crosscutting aspect associated
  with it since the performance deficiency is not indicative of current licensee performance.
  Enforcement. 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in
  part, that measures be established for the selection and review for suitability of
  application of materials, parts, equipment, and processes that are essential to the
  safety-related functions of structures, systems, and components. Contrary to the above,
  prior to April 2, 2008, the licensee failed to ensure that the containment air coolers would
  be able to perform their safety-related function in all accident scenarios due to a design
  deficiency associated with the overload contacts in the containment air cooler control
  circuitry. Because this finding is of very low safety significance and has been entered
  into the corrective action program as CAR 200702264, this violation is being treated as
  an NCV consistent with Section VI.A of the NRC Enforcement Policy:
  NCV 05000483/2008003-01, Failure to Ensure the Suitability of the Design of the
  Containment Air Cooler Control Circuitry.
.2 Introduction. The inspectors identified a Green NCV of Technical Specification 3.5.2,
  "Emergency Core Cooling Systems," after an inadequate surveillance procedure
  resulted in the licensee failing to maintain the emergency core cooling system (ECCS)
  full of water as required per Technical Specification 3.5.2.
  Description. On May 21, 2008, Callaway Plant engineering discovered that a section of
  the cold leg recirculation piping, specifically the discharge of the residual heat removal
  pumps to the safety injection pumps, contained 6.6 cubic feet of air. This exceeded the
  allowable void fraction of 2.1 cubic feet required for operability. Callaway monthly
  surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow Path
  Verification and Venting," had a purpose to: "Verify the ECCS is full of water," in
  accordance with Technical Specification Surveillance Requirement 3.5.2.3. This
  monthly surveillance was reviewed as part of significant condition adverse to quality
  (SCAQ) CAR 200501092 corrective actions. Callaway engineering had determined that
  residual heat removal pump discharge vent Valve EJV0193 to the safety injection
  system was the high point vent for these lines and was thus sufficient to vent
  Line EM-023-HCB - 6" to the safety injection pumps. However, this vent valve was not
  adequate due to the pipe sloping issues and normally closed Valves EMHIS8807A/B.
  Venting through Valve EMV0179 was necessary to completely fill, vent, and test the line.
  The monthly verification and vent procedure was inadequate to identify and remove air
                                        - 16 -                                      Enclosure 2
 
introduced by relief valve maintenance on May 7, 2007, and thus ensure the ECCS was
full of water. See Violation (VIO) 05000483/2008003-05 in Section 4OA2.
Analysis. Failure to adequately verify ECCS piping was full of water as required by
Technical Specification 3.5.2 is a performance deficiency. This finding affected the
mitigating system cornerstone procedure quality attribute. This finding is more than
minor because it was similar to Example 3e of NRC Inspection Manual Chapter 0612,
Appendix E, "Examples of Minor Issues," and met the Not Minor If, criteria because the
failure to meet the licensees administrative requirement for allowable void fraction
impacted the ability of the Train A safety injection system to function upon initiation of
high-pressure recirculation. Using Manual Chapter 0609.04, Phase 1 - Initial Screening
and Characterization of Findings, the inspectors determined that this finding should be
evaluated using the Phase 2 process described in Manual Chapter 0609, Appendix A,
Determining the Significance of Reactor Inspection Findings for At-Power Situations.
As described in Section III of Appendix A, given that the presolved table did not contain
a suitable target or surrogate for this finding, the senior reactor analyst used the
risk-informed notebook to evaluate the significance of this finding. Table 2 provides the
definitions for acronyms and initialisms used in the risk-informed notebook and
discussed in this inspection report.
                                          TABLE 2
                  Acronyms and Initialisms used in Phase 2 Notebook
          Initialism Initiating Event or Mitigating Function
          TPCS        Transient with Loss of the Power Conversion System
          SLOCA        Small-Break Loss of Coolant Accident
          MLOCA        Medium-Break Loss of Coolant Accident
          LLOCA        Large-Break Loss of Coolant Accident
          LOOP        Loss of Offsite Power
          MSLB        Main Steam Line Break
          LBDC        Loss of Vital Direct-Current Bus
          AFW          Auxiliary Feedwater
          PCS          Power Conversion System (Steam and Feed)
          HPR          High Pressure Recirculation
          DEPR        Depressurization of the Reactor Coolant System
          EAC          Emergency Power (Alternating Current)
          TDAFW        Turbine-Driven Auxiliary Feedwater Pump Train
          SEAL        Reactor Coolant Pump Seal Integrity
          STIN        Operators Stop High-Pressure Injection
          MDAFW        Motor-Driven Auxiliary Feedwater Pump Train
The analyst performed a Phase 2 estimation in accordance with Inspection Manual
Chapter 0609, Appendix A, Attachment 2, Site Specific Risk-Informed Inspection
Notebook Usage Rules. Given that the performance deficiency was known to have
existed for 378 days (May 7, 2007, until May 21, 2008) the analyst used 1 year as the
exposure period. In accordance with Table 2 of the risk-informed notebook, the analyst
evaluated all worksheets except LLOCA. All worksheets were evaluated using the
nominal 1-year initiating event frequency. Because this finding only affected system
functionality during recirculation, nominal mitigation credit was given for all functions with
the exception of HPR. For HPR, the analyst made the bounding assumption that either
                                    - 17 -                                      Enclosure 2
 
both centrifugal charging pumps or both safety injection pumps would be affected. This
assumption was supported by licensee evaluation. The analyst solved each applicable
worksheet and the dominant sequences are documented in Table 1.
                                            TABLE 1
                                Phase 2 Dominant Sequences
      Initiating Event        Sequence        Mitigating Functions              Results
                              Number
      Transients                    1        AFW-PCS-HPR                          9
      TPCS                          1        AFW-HPR                              8
      SLOCA                          2        DEPR-HPR                              8
      MLOCA                          2        DEPR-HPR                              9
                                    1        AFW-HPR                              9
      LOOP                          5        EAC-TDAFW-HPR                        9
                                    9        EAC-SEAL-HPR                          9
      MSLB                          8        STIN-HPR                              8
      LBDC                          8        TDAFW-MDAFW-HPR                      8
Using Inspection Manual Chapter 0609, Appendix A, Attachment 1, Table 5, Counting
Rule Worksheet, the analyst determined that the risk contribution of this finding from
internal initiating events was of very low risk significance. In accordance with
Appendix A, Attachment 1, Steps 2.2.5 and 2.2.6, the analyst and determined that the
risk contribution of this finding from external initiating events or the contribution from
large-early release frequency were very low. Therefore, this finding was of very low risk
significance (Green). This finding has a crosscutting aspect in the area of human
performance associated with the decision making component because the licensee
failed to use conservative assumptions in decision making and did not adopt a
requirement to demonstrate that the single vent Valve EJV0193 was sufficient to vent
the Line EM-023-HCB - 6" rather than assuming that installed Valve EMV0179 was not
necessary to completely fill, vent, and test the line [H.1(b)].
Enforcement. Technical Specification 3.5.2 "Emergency Core Cooling Systems,"
Surveillance Requirement 3.5.2.3, required that the licensee verify that ECCS piping is
full of water every 31 days. Contrary to the above, from June 2007 through April 2008,
AmerenUE surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow
Path Verification and Venting," was inadequate to meet Technical Specification
Surveillance Requirement 3.5.2.3. Because this finding is of very low safety significance
and was entered into the licensee's corrective action program as CAR 200804000, this
violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC
Enforcement Policy: NCV 05000483/2008003-02, Inadequate Surveillance Procedure
Resulted in an Inoperable ECCS.
                                      - 18 -                                      Enclosure 2
 
1R18 Plant Modifications (71111.18)
  a. Inspection Scope
    The inspectors reviewed the design adequacy of the listed modifications. This included
    verifying that the modification preparation did not impair the following: (a) in-plant
    emergency/abnormal operating procedure actions, (b) key safety functions, and
    (c) operator response to loss of key safety functions.
    The inspectors verified that postmodification testing maintained the plant in a safe
    configuration during testing and that the postmodification testing established operability
    by: (a) verifying that unintended system interactions did not occur; (b) verifying that
    performance characteristics, which could have been affected by the modification, met
    the design bases; (c) validating the appropriateness of modification design assumptions;
    and (d) demonstrating that the modification test acceptance criteria had been met.
      *      April 18, 2008, Modification M-08-0013 to separate fast and slow speed overload
            contacts for containment air coolers
    *      June 1, 2008, Temporary Modification TM 08-0003 for the instrument air system
            to provide an additional diesel-driven air compressor to improve system reliability
            while the system was in degraded reliability
    Documents reviewed are listed in the attachment.
    These activities constituted two samples as defined by Inspection Procedure 71111.18.
  b. Findings
    No findings of significance were identified
1R19 Postmaintenance Testing (71111.19)
  a. Inspection Scope
    The inspectors reviewed the following postmaintenance activities to verify that
    procedures and test activities were adequate to ensure system operability and functional
    capability:
    *      April 10, 2008, Job 08002765.900, Source Range N32 postmaintenance test
      *      April 17, 2008, Postmaintenance test containment Cooler D,
            Modification 0800267/950(951)(952)
      *      May 7, 2008, Job 06524419.940, Emergency Diesel Generator B
      *      May 28, 2008, Job 08003910, Postmaintence test of Emergency Diesel
            Generator A following repair of jacket water leaks
      *      May 30, 2008, Job 08001080, Postmaintenance local leakrate test of
            containment personnel hatch door
                                        - 19 -                                      Enclosure 2
 
  These activities were selected based upon the structure, system, and component's
  ability to impact risk. The inspectors evaluated these activities to verify (as applicable):
  the effect of testing on the plant had been adequately addressed; testing was adequate
  for the maintenance performed; acceptance criteria were clear and demonstrated
  operational readiness; test instrumentation was appropriate; tests were performed as
  written in accordance with properly reviewed and approved procedures; equipment was
  returned to its operational status following testing (temporary modifications or jumpers
  required for test performance were properly removed after test completion); and test
  documentation was properly evaluated. The inspectors evaluated the activities against
  Technical Specifications, the FSAR, 10 CFR Part 50 requirements, licensee procedures,
  and various NRC generic communications to ensure that the test results adequately
  ensured that the equipment met the licensing basis and design requirements. In
  addition, the inspectors reviewed corrective action documents associated with
  postmaintenance tests to determine whether the licensee was identifying problems and
  entering them in the corrective action program and that the problems were being
  corrected commensurate with their importance to safety. Documents reviewed are listed
  in the attachment.
  This inspection constitutes five samples as defined in Inspection Procedure 71111.19.
b. Findings
  Introduction. A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion XVI,
  "Corrective Action," was identified after the licensee failed to promptly correct leakage
  from diesel generator jacket water o-rings.
  Description. On February 20, 2008, during performance of Procedure OSP-NE-0001B,
  Standby Diesel Generator B Periodic Tests, Callaway operations personnel identified
  that the Emergency Diesel Generator B had an approximately 80 drop-per-minute jacket
  water leak. Analysis by the licensee determined the cause of the leakage to be from
  premature failure of Nitrile type o-rings in the jacket water supply and return headers.
  Operational history at Callaway revealed o-ring failures prior to reaching 3 years of
  service life. The o-rings responsible for the February 20, 2008, leakage had been in
  service since Refueling Outage 14 in October 2005. Following restoration of Emergency
  Diesel Generator B, the licensee re-evaluated the preventative maintenance frequency
  for jacket water o-ring replacement. Based on a review of prior o-ring failures, the
  replacement schedule for diesel generator jacket water o-rings was reduced from once
  every 3 years to once every refueling cycle.
  On May 28, 2008, during performance of Procedure OSP-NE-0001A, Standby Diesel
  Generator A Periodic Tests, Callaway operations personnel identified that Emergency
  Diesel Generator A had a 200 drop-per-minute jacket water leak. Based on the quantity
  of the leakage, operations personnel declared Emergency Diesel Generator A
  inoperable. Similar to the condition observed on Emergency Diesel Generator B on
  February 20, 2008, the source of the leakage was from Nitrile type o-rings within the
  jacket water system. While the licensee replaced the o-rings responsible for jacket
  water leakage following the February 20, 2008, surveillance, several Nitrile type o-rings
  installed during Refueling Outage 14 in October 2005 remained in service in both
  Emergency Diesel Generators Trains A and B including those that failed during the
  May 28, 2008, surveillance.
                                        - 20 -                                      Enclosure 2
 
    Subsequent analysis by the licensee determined that the required mission time of the
    Emergency Diesel Generator A was preserved since adequate inventory in the jacket
    water expansion tank existed such that the leakage observed on May 28, 2008, would
    not have impacted the net positive suction head analysis for the jacket water cooling
    pump.
    Analysis. The performance deficiency associated with this finding involved the
    licensees failure to implement adequate corrective actions for an adverse condition.
    Specifically, the licensee failed to correct degraded Nitrile type o-rings in Emergency
    Diesel Generator A after previously identifying the adverse condition on Emergency
    Diesel Generator B. This finding was greater than minor because, if left uncorrected,
    degraded diesel generator jacket water o-rings could become a more significant safety
    concern. This finding affected the mitigating systems cornerstone. Using Manual
    Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, this
    finding was determined be of very low safety significance because it was a design
    deficiency confirmed not to result in loss of operability. This finding had a crosscutting
    aspect in the area of human performance associated with the work control component
    because the licensee failed to plan work activities to support long-term equipment
    reliability by addressing known degraded conditions in a more reactive than preventative
    manner [H.3(b)].
    Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires,
    in part, that measures be established to assure conditions adverse to quality are
    promptly identified and corrected. Contrary to the above, the licensee failed to
    implement adequate corrective actions for the identified adverse condition that Nitrile
    type o-rings would prematurely fail prior to the completion of the regularly scheduled
    3-year replacement interval. Because this violation is of very low safety significance and
    has been entered into the licensee's corrective action program as CAR 200804164, this
    violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC
    Enforcement Policy: NCV 05000483/2008003-03, Failure to Correct a Condition
    Adverse to Quality for Diesel Generator Jacket Water O-Rings.
1R22 Surveillance Testing (71111.22)
  a. Inspection Scope
    The inspectors reviewed the test results for the following activities to determine whether
    risk-significant systems and equipment were capable of performing their intended safety
    function and to verify testing was conducted in accordance with applicable procedural
    and Technical Specification requirements:
    *        April 2, 2008, Job 07513515.500, Routine surveillance auxiliary building Train A
              negative pressure test
    *        April 4, 2008, Job 08501501, Routine surveillance Slave Relay K645 test of
              essential service water component lineup
    *        April 18, 2008, Job 08501499, Routine surveillance Slave Relay K615 test
    *        April 29, 2008, Job 08501254.500, Residual heat removal Pump A inservice test
                                          - 21 -                                    Enclosure 2
 
  *      May 5, 2008, Jobs 08502271 and 08503327, Routine surveillance containment
          base strong motion accelerometer seismic monitor calibration
  *      May 14, 2008, Job 07505653, Residual heat removal Train B valve inservice test
  *      June 11, 2008, Job 08504820, Routine surveillance diesel generator Train B
          1-hour run
  *      June 17, 2008, Job 08503115, Safety injection system Train A valve inservice
          test
  *      June 18, 2008, Job 08505155, Routine surveillance ECCS flow path verification
          and venting
  *      June 23, 2008, Job 08506247, Reactor coolant system leakage surveillance,
          reactor coolant system inventory balance, plant status
  The inspectors observed in-plant activities and reviewed procedures and associated
  records to determine whether: any preconditioning occurred; effects of the testing were
  adequately addressed by control room personnel or engineers prior to the
  commencement of the testing; acceptance criteria were clearly stated, demonstrated
  operational readiness, and were consistent with the system design basis; plant
  equipment calibration was correct, accurate, and properly documented; as left setpoints
  were within required ranges; the calibration frequency was in accordance with Technical
  Specifications, the FSAR, procedures, and applicable commitments; measuring and test
  equipment calibration was current; test equipment was used within the required range
  and accuracy; applicable prerequisites described in the test procedures were satisfied;
  test frequencies met Technical Specification requirements to demonstrate operability
  and reliability; tests were performed in accordance with the test procedures and other
  applicable procedures; jumpers and lifted leads were controlled and restored where
  used; test data and results were accurate, complete, within limits, and valid; test
  equipment was removed after testing; where applicable, test results not meeting
  acceptance criteria were addressed with an adequate operability evaluation or the
  system or component was declared inoperable; where applicable for safety-related
  instrument control surveillance tests, reference setting data were accurately incorporated
  in the test procedure; equipment was returned to a position or status required to support
  the performance of the safety functions; and all problems identified during the testing
  were appropriately documented and dispositioned in the corrective action program.
  Documents reviewed are listed in the attachment.
  The inspectors completed six routine, three inservice test, and one reactor coolant
  system leakage samples.
b. Findings
  Introduction. A self-revealing Green NCV of Technical Specification 5.4.1.a,
  Procedures, was identified after Callaway control room operators improperly entered
  the wrong Technical Specification action statement due to the failure to maintain the
  Technical Specification Bases current.
                                      - 22 -                                    Enclosure 2
 
Description. On June 17, 2008, during surveillance testing, Valve EMHV8823 failed to
indicate fully closed. Since EMHV8823 is an isolation valve for containment
Penetration 49, the licensee entered Technical Specification 3.6.3, Containment
Isolation Valves," Condition C, with an action to restore the valve to an operable status
or isolate the penetration within 72 hours. The control room staff believed the
appropriate action statement was entered since Condition C is described in the
Technical Specification Bases as applicable to flow paths that meet the requirements of
a closed system per the Callaway FSAR. Chapter 6.2.6.3 of the Callaway FSAR
described Containment Penetration 49 as a closed engineered safety feature
containment penetration.
Approximately 8 hours after Valve EMHV8823 had been declared inoperable, Callaway
licensing personnel contacted the control room and informed them of an approved
Technical Specification Bases change that did not allow the classification of containment
Penetration 49 as a closed system. Procedure APA-ZZ-00108, Primary Licensing
Document; Change/Revision Process," required that the change be implemented within
45 days following approval. The Technical Specification Bases change was effective
May 1, 2008, but had not been issued to the control room. The change resulted in
Condition C of Technical Specification 3.6.3 applying specifically to penetrations for
which a single containment isolation valve is credited per flow path. Since containment
Penetration 49 relies on multiple valves for flow path isolation, the licensee determined
that Condition C of Technical Specification 3.6.3 was not applicable for Penetration 49,
and the wrong Technical Specification action statement had been entered following the
failed surveillance on Valve EMHV8823. The licensee determined that the more
restrictive Technical Specification 3.6.3, Condition A, should have been entered with an
action to isolate the affected penetration within 4 hours.
The licensee performed a containment entry following discovery of entry into Technical
Specification 3.6.3, Condition A, and found that Valve EMHV8823 had failed its
surveillance due to out-of-adjustment position indicator limit switches. The valve was
verified closed with power removed allowing exit from Technical Specification 3.6.3,
Condition A.
Analysis. The performance deficiency associated with this finding involved the
licensees failure to ensure the Technical Specification Bases were maintained current
and available to the Callaway control room staff. This finding was greater than minor
because, if left uncorrected, the failure to maintain the Technical Specification Bases
current could become a more significant safety concern. This finding was determined to
affect the barrier integrity cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial
Screening and Characterization of Findings," this finding is determined to be of very low
safety significance since this finding did not represent an actual open pathway in the
physical integrity of reactor containment and did not involve an actual reduction in
function of hydrogen ignitors in the reactor containment. This finding had a crosscutting
aspect in the area of human performance associated with the decision making
component because the licensee failed to communicate, in a timely manner, decisions to
personnel who have a need to know the information in order to perform work safely
[H.1(c)].
Enforcement. Technical Specification 5.4.1.a, Procedures, required that written
procedures be established and implemented covering activities specified in Appendix A,
Typical Procedures for Pressurized Water Reactors, of Regulatory Guide 1.33, Quality
                                    - 23 -                                    Enclosure 2
 
      Assurance Program Requirements (Operation), February 1978. Regulatory Guide 1.33,
      Appendix A, Section 1, required administrative procedures for procedure review and
      approval. Procedure APA-ZZ-00108 provides a process for implementing Technical
      Specification Bases change notices. Contrary to the above, on May 1, 2008,
      Procedure APA-ZZ-00108 was not adequate to ensure changes to the Technical
      Specification Bases were implemented in a timely manner. Because of the very low
      safety significance and AmerenUEs action to place this issue in their corrective action
      program as CAR 200805283, this violation is being treated as an NCV in accordance
      with Section VI.A.1 of the Enforcement Policy: NCV 05000483/2008003-04, Failure to
      Maintain an Adequate Technical Specification Bases Change Process.
2.    RADIATION SAFETY
      Cornerstone: Occupational Radiation Safety
2OS1 Access Control to Radiologically Significant Areas (71121.01)
  a. Inspection Scope
      This area was inspected to assess the licensees performance in implementing physical
      and administrative controls for airborne radioactivity areas, radiation areas, high
      radiation areas, and worker adherence to these controls. The inspectors used the
      requirements in 10 CFR Part 20, the Technical Specifications, and the licensees
      procedures required by Technical Specifications as criteria for determining compliance.
      During the inspection, the inspectors interviewed the radiation protection manager,
      radiation protection supervisors, and radiation workers. The inspectors performed
      independent radiation dose rate measurements and reviewed the following items:
      *      Performance indicator events and associated documentation packages reported
              by the licensee in the occupational radiation safety cornerstone
      *      Controls (surveys, posting, and barricades) of radiation, high radiation, or
              airborne radioactivity areas
      *      Radiation work permits, procedures, engineering controls, and air sampler
              locations
      *      Physical and programmatic controls for highly activated or contaminated
              materials (non-fuel) stored within spent fuel and other storage pools
      *      Self-assessments, audits, LERs, and special reports related to the access control
              program since the last inspection
      *      Changes in licensee procedural controls of high dose rate - high radiation areas
              and very high radiation areas
      *      Controls for special areas that have the potential to become very high radiation
              areas during certain plant operations
      *      Posting and locking of entrances to accessible high dose rate - high radiation
              areas and very high radiation areas
                                          - 24 -                                      Enclosure 2
 
    Documents reviewed are listed in the attachment.
    The inspectors completed 8 of the required 21 samples.
  b. Findings
    No findings of significance were identified.
2OS2 ALARA Planning and Controls (71121.02)
  a. Inspection Scope
    The inspectors assessed licensee performance with respect to maintaining individual
    and collective radiation exposures as low as is reasonably achievable (ALARA). The
    inspectors used the requirements in 10 CFR Part 20 and the licensees procedures
    required by technical specifications as criteria for determining compliance. The
    inspectors interviewed licensee personnel and reviewed:
    *      Current 3-year rolling average collective exposure
    *      Site-specific trends in collective exposures, plant historical data, and source-term
            measurements
    *      Site-specific ALARA procedures
    *      Work activities of highest exposure significance during the inspection
    *      Integration of ALARA requirements into work procedure and radiation work
            permit documents
    *      Post-job (work activity) reviews
    *      Workers use of the low dose waiting areas
    *      First-line job supervisors contribution to ensuring work activities are conducted in
            a dose efficient manner
    *      Records detailing the historical trends and current status of tracked plant source
            terms and contingency plans for expected changes in the source term due to
            changes in plant fuel performance issues or changes in plant primary chemistry
    *      Source-term control strategy or justifications for not pursuing such exposure
            reduction initiatives
    *      Specific sources identified by the licensee for exposure reduction actions,
            priorities established for these actions, and results achieved since the last
            refueling cycle
    *      Radiation worker and radiation protection technician performance during work
            activities in radiation areas, airborne radioactivity areas, or high radiation areas
                                          - 25 -                                      Enclosure 2
 
      *      Declared pregnant workers during the current assessment period, monitoring
              controls, and the exposure results
      *      Self-assessments, audits, and special reports related to the ALARA program
              since the last inspection
      *      Resolution through the corrective action process of problems identified through
              post-job reviews and post-outage ALARA report critiques
      *      Corrective action documents related to the ALARA program and follow-up
              activities, such as initial problem identification, characterization, and tracking
      *      Effectiveness of self-assessment activities with respect to identifying and
              addressing repetitive deficiencies or significant individual deficiencies
      Documents reviewed are listed in the attachment.
      The inspectors completed 9 of the required 15 samples and 8 of the optional samples.
  b. Findings
      No findings of significance were identified.
4.    OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
.1    Data Submission Issue
  a. Inspection Scope
      The inspectors performed a review of the data submitted by the licensee for the first
      Quarter 2008 performance indicators for any obvious inconsistencies prior to its public
      release in accordance with IMC 0608, Performance Indicator Program.
      This review was performed as part of the inspectors normal plant status activities and,
      as such, did not constitute a separate inspection sample.
  b. Findings
      No findings of significance were identified.
.2    Safety System Functional Failures
      Cornerstone: Mitigating Systems
  a. Inspection Scope
      The inspectors sampled licensee submittals for the safety system functional failures
      performance indicator for the period March 2007 until March 2008. To determine the
      accuracy of the performance indicator data reported during this period, performance
      indicator definitions and guidance contained in the Nuclear Energy Institute (NEI)
                                            - 26 -                                      Enclosure 2
 
      Document 99-02, Revision 5, Regulatory Assessment Performance Indicator
      Guideline, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73,"
      definitions and guidance were used. The inspectors reviewed the licensees operator
      narrative logs, operability assessments, maintenance rule records, maintenance work
      orders, issue reports, event reports and NRC integrated inspection reports for the period
      of 2nd Quarter 2007, through 1st Quarter 2008 to validate the accuracy of the
      submittals. The inspectors also reviewed the licensees issue report database to
      determine if any problems had been identified with the performance indicator data
      collected or transmitted for this indicator and none were identified. Documents reviewed
      are listed in the attachment.
      This inspection constitutes one safety system functional failures sample as defined by
      Inspection Procedure 71151.
  b. Findings
      No findings of significance were identified.
.3    Mitigating Systems Performance Index - High Pressure Injection Systems
      Cornerstone: Mitigating Systems
  a. Inspection Scope
      The inspectors sampled licensee submittals for the mitigating systems performance
      index - high pressure injection systems performance indicator for the period from
      March 2007 until March 2008. To determine the accuracy of the performance indicator
      data reported during this period, performance indicator definitions and guidance
      contained in the NEI Document 99-02, 5, Regulatory Assessment Performance
      Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees
      operator narrative logs, issue reports, mitigating systems performance index derivation
      reports, event reports, and NRC integrated inspection reports for the period of
      2nd Quarter 2007 through 1st Quarter 2008 to validate the accuracy of the submittals.
      The inspectors reviewed the mitigating systems performance index component risk
      coefficient to determine if it had changed by more than 25 percent in value since the
      previous inspection, and if so, that the change was in accordance with applicable NEI
      guidance. The inspectors also reviewed the licensees issue report database to
      determine if any problems had been identified with the performance indicator data
      collected or transmitted for this indicator and none were identified. Documents reviewed
      are listed in the attachment.
      This inspection constitutes one mitigating systems performance index high pressure
      injection systems sample as defined by Inspection Procedure 71151.
  b. Findings
      No findings of significance were identified.
                                          - 27 -                                  Enclosure 2
 
.4    Occupational Exposure Control Effectiveness
      Cornerstone: Occupational Radiation Safety
  a. Inspection Scope
      The inspectors reviewed licensee documents from October 1, 2007, through March 31,
      2008. The review included corrective action documentation that identified occurrences
      in locked high radiation areas (as defined in the licensees Technical Specifications),
      very high radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel
      exposures (as defined in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
      Revision 5). Additional records reviewed included ALARA records and whole body
      counts of selected individual exposures. The inspectors interviewed licensee personnel
      that were accountable for collecting and evaluating the performance indicator data. In
      addition, the inspectors toured plant areas to verify that high radiation, locked high
      radiation, and very high radiation areas were properly controlled. Performance indicator
      definitions and guidance contained in NEI 99-02, Revision 5, were used to verify the
      basis in reporting for each data element.
      The inspectors completed the required sample (1) in this cornerstone.
  b. Findings
      No findings of significance were identified.
.5    Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
      Radiological Effluent Occurrences
      Cornerstone: Public Radiation Safety
  a. Inspection Scope
      The inspectors reviewed licensee documents from October 1, 2007, through March 31,
      2008. Licensee records reviewed included corrective action documentation that
      identified occurrences for liquid or gaseous effluent releases that exceeded performance
      indicator thresholds and those reported to the NRC. The inspectors interviewed licensee
      personnel that were accountable for collecting and evaluating the performance indicator
      data. Performance indicator definitions and guidance contained in NEI 99-02,
      Revision 5, were used to verify the basis in reporting for each data element.
      The inspectors completed the required sample (1) in this cornerstone.
  b. Findings
      No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152)
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical
      Protection
                                          - 28 -                                    Enclosure 2
 
.1    Routine Review of Items Entered into the Corrective Action Program
  a. Inspection Scope
      As part of the various baseline inspection procedures discussed in previous sections of
      this report, the inspectors routinely reviewed issues during baseline inspection activities
      to verify that they were being entered into the licensees corrective action program at an
      appropriate threshold, that adequate attention was being given to timely corrective
      actions, and that adverse trends were identified and addressed. The attributes reviewed
      included: the complete and accurate identification of the problem; that timeliness was
      commensurate with the safety significance; that evaluation and disposition of
      performance issues, generic implications, common causes, contributing factors, root
      causes, extent of condition reviews, and previous occurrence reviews were proper and
      adequate; and that the classification, prioritization, focus, and timeliness of corrective
      actions were commensurate with safety and sufficient to prevent recurrence of the issue.
      These routine reviews for the identification and resolution of problems did not constitute
      any additional inspection samples.
  b. Findings
      No findings of significance were identified.
.2    Daily Corrective Action Program Reviews
  a. Inspection Scope
      In order to assist with the identification of repetitive equipment failures and specific
      human performance issues for follow-up, the inspectors performed a daily screening of
      items entered into the licensees corrective action program. This review was
      accomplished through inspection of the stations daily condition report packages.
      These daily reviews were performed, by procedure, as part of the inspectors daily plant
      status monitoring activities and, as such, did not constitute any separate inspection
      samples.
  b. Findings
      No findings of significance were identified.
.3    Selected Issue Follow-up Inspection
  a. Inspection Scope
      The inspectors selected the below listed issues for a more in-depth review. The
      inspectors considered the following during the review of AmerenUE's actions:
      (1) complete and accurate identification of the problem in a timely manner; (2) evaluation
      and disposition of operability/reportability issues; (3) consideration of extent of condition,
      generic implications, common cause, and previous occurrences; (4) classification and
      prioritization of the resolution of the problem; (5) identification of root and contributing
      causes of the problem; (6) identification of corrective actions; and (7) completion of
      corrective actions in a timely manner.
                                            - 29 -                                      Enclosure 2
 
      *      Voiding discovered in the common residual heat removal discharge piping for
              high pressure recirculation.
      *      FSAR changes/updates
  Documents reviewed are listed in the attachment.
  This inspection constituted two in-depth problem identification and resolution samples.
b. Findings
  Introduction. The inspectors identified a Green violation of 10 CFR Part 50, Appendix B,
  Criterion XVI, "Corrective Action," because the licensee failed to take corrective actions
  to preclude repetition of void formations in the ECCS, a significant condition adverse to
  quality (SCAQ). Contributors to the violation included: (1) the failure of corrective
  actions from inspection report findings NCV 05000483/2005002-01,
  05000483/2006012-04 and CAR 200501092 to ensure adequate fill and vent of
  systems following maintenance to replace safety injection system relief valves, and
  (2) inadequate extent of condition reviews in responding to internal and external
  operating experience associated with pipe sloping issues in the safety injection system.
  Description. On May 21, 2008, the Callaway Plant staff initiated CAR 200804000, a
  SCAQ corrective action document, indicating that some piping in Train A safety injection
  system suction lines had incorrect sloping and were susceptible to voiding due to high
  points. Callaway Plant engineering performed ultrasonic inspection of the safety
  injection system common suction piping Line EM023-HCB - 6" and discovered a
  6.6 cubic foot voided area. This exceeded the allowable void fraction of 2.1 cubic feet
  required for operability. This voided piping, determined to have existed for over a year,
  was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The
  maintenance restoration failed to perform an adequate fill and vent to ensure the suction
  pipe was full of water.
  In 2005 and 2006 the NRC issued NCVs regarding ineffective corrective actions related
  to safety injection system voids in discharge piping (05000483/2005002-01 dated May 6,
  2005, and 05000483/2006012-04 dated December 26, 2006). These were each 10 CFR
  Part 50, Appendix B, Criterion XVI, NCVs, each for SCAQ. The Callaway Plant staff
  issued CAR 200501092 as a SCAQ corrective action document. The CAR determined
  that the causes of the voids (2004, 2005, and 2006) were related to incorrect pipe
  sloping (allowing high points where voids could not be swept away by normal online
  pump surveillances) and inadequate postmaintenance fill and vent operations (following
  discharge piping relief Valve EM8853A replacement) to ensure the piping was full of
  water.
  Inadequate Operating Experience and Extent of Condition Corrections: The
  inspectors identified several related examples where the licensee had performed either
  inadequate operating experience evaluations, inadequate extent of condition reviews, or
  inadequate procedure corrections.
  Callaway CAR 200501092 referenced industry operating experience at Beaver Valley
  Unit 2 in 2002: "The void was located in the piping used following a loss of coolant
                                      - 30 -                                    Enclosure 2
 
accident after the transfer to containment sump recirculation. The piping containing the
void led to a common suction header for both trains of high head pumps." This was the
same location as the voiding discovered at Callaway Plant on May 21, 2008.
NRC Information Notice 2006-21, "Operating Experience Regarding Entrainment of Air
into Emergency Core Cooling and Containment Spray Systems," dated September 21,
2006, discussed mechanisms that could result in air entrainment on the suction sides of
emergency core cooling pumps. The notice emphasized the importance of ensuring that
entrained air will not enter suction supply lines and impair the ability of the ECCS and
containment spray pumps to perform their safety function.
The licensee's evaluation of NRC Information Notice 2006-21 was documented in
CAR 200608956. It stated that the information notice was applicable to Callaway and
that past review of these operating experiences and Callaway procedures and practices
were adequate. The CAR was closed December 5, 2006.
Callaway CAR 200501092 had Action 7 assigned to address the previous NRC
violations discussed above. The action required that system specific fill and vent
restoration guidance be developed to address maintenance on ECCS safety-related
systems. Initially, operating department Standing Order 05-002 dated June 8, 2005,
stated that the CAR 200501092 common cause analysis supported the need for
formalized restoration instructions. Until the system specific restoration instructions
were developed, the standing order required reactor operators to perform reviews to
ensure dynamic filling and venting occurred to reduce the susceptibility of voiding. Also
nuclear engineering department staff were to provide concurrence on such restoration
plans. Night Order ODP-ZZ-00310, "System Fill and Vent," issued February 13, 2006,
reiterated that reactor operator reviews and engineering concurrence were required
when these risk-significant systems were drained. However, on May 7, 2007,
Procedure OTN-EM-00001, "Safety Injection System," (developed to address filling and
venting evaluations) had Line EM-023-HCB - 6" isolated by Valve EMHIS8807B being
closed. The procedure did not include use of the available installed vent Valve EM179
for this line.
Callaway monthly Surveillance OSP-SA-00003, "Emergency Core Cooling Flow Path
Verification and Venting," had a purpose to: "Verify the ECCS is full of water in
accordance with Technical Specification Surveillance Requirement 3.5.2.3." This
monthly surveillance was reviewed as part of CAR 200501092 corrective actions.
Callaway engineering had determined that residual heat removal pump discharge vent
Valve EJV0193 to the safety injection suction line was the high point vent for these lines
and was thus sufficient to vent supply Line EM-023-HCB - 6" to the safety injection
pumps. However, this vent valve was not adequate due to the pipe sloping issues and
normally closed Valves EMHIS8807A/B. The monthly verification and vent procedure
was inadequate to remove the air entrained by the May 7, 2007, relief valve
maintenance. See Section 1R15, NCV 05000483/2008003-02.
Callaway CARs 200800226 and 200800246, initiated in January 2008, discussed
operating experience at Wolf Creek Nuclear Operating Corporation describing gas
voiding in the residual heat removal piggyback Line EM-022-HCB - 6" to the suction of
centrifugal charging pumps and safety injection pumps. The CARs stated that Callaway
had taken a proactive approach and had immediately performed ultrasonic testing to
demonstrate that the associated piping was water solid. However, the adjacent
                                    - 31 -                                      Enclosure 2
 
connecting Line EM-023-HCB - 6" had not been vented nor had ultrasonic testing
occurred since the May 7, 2007, relief Valve EM8858A maintenance.
NRC Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling,
Decay Heat Removal, and Containment Spray Systems," was issued January 11, 2008.
The Callaway Plant staff initiated CAR 200800298 to respond to the generic letter. The
generic letter identified that a licensing basis concern existed for some plants, such as
Callaway, that Technical Specifications require verifying that ECCS discharge piping is
full of water but may not include verification of the suction piping despite the realistic
concern that gas accumulation in suction piping may be more serious than gas
accumulation in discharge piping. The void found in Line EM-023-HCB - 6" was the
discharge of the residual heat removal pumps providing suction to the Train A safety
injection pump. The Callaway monthly Surveillance OSP-SA-00003, "Emergency Core
Cooling Flow Path Verification and Venting," did not test for or vent the discharge line
from residual heat removal to safety injection pump suction piping.
Analysis. The inspectors determined that the failure to restore compliance within a
reasonable time by establishing measures to prevent void formation in ECCS suction
piping for the Train A safety injection system was a performance deficiency. This finding
is more than minor because it was similar to Example 3e of NRC Inspection Manual
Chapter 0612, Appendix E, "Examples of Minor Issues," and met the Not Minor If,
criteria because the failure to meet the licensees administrative requirement for
allowable void fraction impacted the ability of the Train A safety injection system to
function upon initiation of high-pressure recirculation. Using Manual Chapter 0609.04,
Phase 1 - Initial Screening and Characterization of Findings, the inspectors determined
that this finding should be evaluated using the Phase 2 process described in Manual
Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection Findings
for At-Power Situations.
The senior reactor analyst determined that the risk of this finding was bounded by that
analyzed for NCV 05000423/2008003-02 (See Section 1R15.b.2). Therefore, this
finding was of very low risk significance (Green).
This finding has a crosscutting aspect in the area of problem identification and resolution
associated with the corrective action component because AmerenUE failed to thoroughly
evaluate voiding problems such that the resolutions addressed causes and extent of
condition, as necessary. This also includes, for significant problems, conducting
effectiveness reviews of corrective actions to ensure that the problems are resolved
[P.1(c)].
Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires
the licensee to, in the case of SCAQ, establish measures to assure that the cause of the
condition is determined and corrective action is taken to preclude repetition. Contrary to
the above, from December 26, 2006, to May 21, 2008, the licensee did not implement
corrective action to preclude repetition of void formation in the safety injection piping
which the licensee categorized as an SCAQ. Specifically, void formation recurred after
performing maintenance on relief valve. Valve EM8858A, on May 7, 2007. Previously
discovered voiding of the safety injection system was last documented as an SCAQ in
NCV 05000483/2006012-04 dated December 26, 2006. For each instance of the
previously discovered voids, the causes were determined to be related to inadequate fill
and vent of the system piping following relief valve replacements and design deficiencies
                                      - 32 -                                     Enclosure 2
 
  associated with inadequate sloping of the piping. It was a reasonable assumption that
  maintenance that drained either the suction or discharge piping could create significant
  void areas.
  Although this violation is of very low safety significance, the violation is being
  cited in a Notice of Violation consistent with Section VI.A.1 of the NRC Enforcement
  Policy because the licensee did not restore compliance within a reasonable
  time after a previous violation NCV 05000483/2006012-04 was identified:
  VIO 05000483/2008003-05, Failure to Prevent Recurrence of Voids in ECCS Cold Leg
  Recirculation Piping. This finding has been entered into the licensee's corrective action
  program as a SCAQ in CAR 200804000.
.4 Semiannual Trend Review
  The inspectors assessed trends that might indicate the existence of a more significant
  safety issue. These issues included trends that might not rise to the level of an
  inspection finding.
   NRC-Identified Trends
   NRC-Identified Trends
   The NRC identified emergency diesel generator material condition and design control issues degrading diesel reliability:  
   The NRC identified emergency diesel generator material condition and design control
  issues degrading diesel reliability:
  *      CAR 200801270: 80 Drops per minute jacket water leak identified on Diesel
          Generator B
  *      CAR 200801644: Additional sacrificial anode found in Emergency Diesel
          Generator A intercooler heat exchanger
  *      CAR 200802019: Emergency Diesel Generator B declared inoperable due to
          fuel oil leaks
  *      CAR 200802177: Cracked fuel oil return line fitting identified on Emergency
            Diesel Generator A
  *      CAR 200804164: Emergency Diesel Generator A declared inoperable due to a
          200 drops per minute jacket water leak
  Licensee-Identified Trends
  The licensee identified a continued trend in plant status control and configuration control
  with a key causal factor being procedure adherence.
  *      CAR 200706832: This trend CAR from Third Quarter 2007 identified the cause
          of plant status control issues to be a "Failure to follow written instructions."
  *      CAR 200801457: A gauge was installed on an incorrect component during Test
            Procedure OSP-EN-P001A.
  *      CAR 200800580: A trend of critical steps not being included in work packages
            was identified.
                                        - 33 -                                        Enclosure 2
 
      *      CAR 200802603: Component cooling water pump autostarted due to an
              interlock with the centrifugal charging pumps. The operator failed to wait the
              procedure prerequisite 30 minutes prior to securing the component cooling water
              pump.
      *      CAR 200802818: Source range Channel N31 was not restored to "block" as
              required by procedure in Mode 1.
      *      CAR 200800328: Not following procedures resulted in gaseous Radiation
              Monitor RM-11 trip setpoint not being capable of isolating the waste gas decay
              tank release.
      *      CAR 200803351: Steam generator blowdown tripped due to an incorrect
              demineralizer valve lineup.
    *        CAR 200804483: Train B motor-driven auxiliary feedwater pump made
              inoperable when its room cooler was taken to "stop" vice "auto." This was
              performed outside the out of service restoration process.
    This inspection constituted one semiannual trend review sample.
4OA3 Event Follow-up (71153)
    (Closed) LER 05000483/2008-001-00, Containment Cooler Inoperability
    On March 26, 2008, Containment Air Cooler A fan shut down when shifted from fast to
    slow speed. The licensee determined that operation of containment air coolers in fast
    speed, during a period of higher than normal containment pressure, would challenge the
    fast speed thermal overload setpoint. Additionally, since the overload contacts are wired
    in series, containment air coolers were determined to experience a complete loss of
    control power following a trip from fast speed. The licensee analyzed the potential
    impact of the containment cooler design vulnerability against design basis accident
    scenarios. The licensee determined that a hot zero power main steam line break results
    in a delayed safety injection signal allowing the fan motor overloads to trip prior to being
    shed from the load sequencer. In this scenario, utilizing actual plant conditions, the peak
    containment pressure would not exceed the 48.1 psig limit described in the FSAR. To
    address the design deficiency associated with the containment air cooler control
    circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit
    such that tripping of the fast speed overloads would not impact the safety-related slow
    speed function of the containment air coolers. This finding is of very low safety
    significance because the containment coolers are structures, systems, and components
    that are not significant contributors to the large early release frequency. Licensee
    corrective actions were recorded in CAR 200802264. The inspectors reviewed the LER
    and identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design
    Control, for the licensees failure to adequately review the suitability of the design of the
    containment air cooler control circuitry (Section 1R15). This LER is closed.
    This inspection constituted one sample of follow-up of events.
                                          - 34 -                                      Enclosure 2
 
4OA5 Other Activities
.1    Quarterly Resident Inspector Observations of Security Personnel and Activities
  a.  During the inspection period, the inspectors performed the following observations of
      security force personnel and activities to ensure that the activities were consistent with
      licensees security procedures and regulatory requirements relating to nuclear plant
      security. These observations took place during both normal and off-normal plant
      working hours.
      These quarterly resident inspector observation of security force personnel and activities
      did not constitute any additional inspection samples. Rather, they were considered an
      integral part of the inspectors normal plant status review and inspection activities.
  b.  Findings
      No findings of significance were identified.
.2    (Closed) NRC Temporary Instruction 2515/166: Pressurized Water Reactor
      Containment Sump Blockage
  a. Inspection Scope
      From March 17-19, 2008, the inspectors reviewed the licensees implementation of plant
      modifications and design modification packages associated with their response to
      Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency
      Recirculation During Design Basis Accidents at Pressurized Water Reactors. The
      inspectors reviewed various aspects of the on-going procedural changes. Those
      changes that have been completed were verified to be properly documented in
      accordance with the requirements of 10 CFR 50.59. At the completion of this inspection,
      the licensee had completed the installation stage of the new sump strainers; many of the
      procedural changes associated with the modifications had not been completed.
      The inspectors compared and evaluated the recirculation sump modifications to the
      original design basis using Temporary Instruction 2515/166 and referred to Regulatory
      Guide 1.82, Revision 0, Water Sources for Long-Term Recirculation Cooling Following
      a Loss-of-Coolant Accident.
      Status of the implementation of the plant modifications and procedure changes
      committed to by the licensee in their Generic Letter 2004-02 response is:
      1.      Containment walkdown to provide current assessment of Callaway's containment
              coatings and latent debris.
              The licensee completed a containment walkdown and latent debris assessment
              during Refueling Outage 14. The resident inspectors completed a walkdown of
              the containment prior to reactor startup following the outage. The licensee
              report, Containment Building Latent Debris Assessment Refuel 14 Fall 2005,
              was reviewed by the inspectors.
                                          - 35 -                                    Enclosure 2


* CAR 200801270: 80 Drops per minute jacket water leak identified on Diesel Generator B
2. The following corrective action activities will be completed:
* CAR 200801644:  Additional sacrificial anode found in Emergency Diesel Generator A intercooler heat exchanger
  a.      Replacement sump strainer structural analysis.
* CAR 200802019:  Emergency Diesel Generator B declared inoperable due to fuel oil leaks
          The strainers were not built in accordance with the design. As a result,
* CAR 200802177:  Cracked fuel oil return line fitting identified on Emergency Diesel Generator A
          calculations needed to be revised due to the deviations of the as built
* CAR 200804164:  Emergency Diesel Generator A declared inoperable due to a 200 drops per minute jacket water leak  Licensee-Identified Trends    The licensee identified a continued trend in plant status control and configuration control with a key causal factor being procedure adherence.
          condition from design and errors in temperature correction values used in
* CAR 200706832:  This trend CAR from Third Quarter 2007 identified the cause of plant status control issues to be a "Failure to follow written instructions." 
          the initial calculations. Completion date: June 30, 2008
* CAR 200801457:  A gauge was installed on an incorrect component during Test Procedure OSP-EN-P001A. 
  b.     Downstream effects evaluation
* CAR 200800580:  A trend of critical steps not being included in work packages was identified. 
          Completion date: June 30, 2008
  - 34 - Enclosure 2
  c.     Upstream effects evaluation
* CAR 200802603:  Component cooling water pump autostarted due to an interlock with the centrifugal charging pumps. The operator failed to wait the procedure prerequisite 30 minutes prior to securing the component cooling water
          Completion date: June 30, 2008
pump. * CAR 200802818: Source range Channel N31 was not restored to "block" as required by procedure in Mode 1.
  d.     Resolution of debris generation calculation unverified assumption of 5D
* CAR 200800328:  Not following procedures resulted in gaseous Radiation Monitor RM-11 trip setpoint not being capable of isolating the waste gas decay tank release.
          ZOI for qualified coatings (via coatings testing)
* CAR 200803351: Steam generator blowdown tripped due to an incorrect demineralizer valve lineup.
          Completion date: June 30, 2008
* CAR 200804483:  Train B motor-driven auxiliary feedwater pump made inoperable when its room cooler was taken to "stop" vice "auto."  This was performed outside the out of service restoration process.  This inspection constituted one semiannual trend review sample.
  e.      Replacement sump screen head loss testing
4OA3 Event Follow-up (71153)
          Completion date: June 30, 2008
(Closed) LER 05000483/2008-001-00, Containment Cooler Inoperability
3. Provide an update of the information contained in Section 2(c) regarding analysis
  On March 26, 2008, Containment Air Cooler A fan shut down when shifted from fast to slow speed. The licensee determined that operation of containment air coolers in fast speed, during a period of higher than normal containment pressure, would challenge the fast speed thermal overload setpoint. Additionally, since the overload contacts are wired in series, containment air coolers were determined to experience a complete loss of control power following a trip from fast speed. The licensee analyzed the potential
  methodology.
impact of the containment cooler design vulnerability against design basis accident scenarios.  The licensee determined that a hot zero power main steam line break results in a delayed safety injection signal allowing the fan motor overloads to trip prior to being shed from the load sequencer. In this scenario, utilizing actual plant conditions, the peak containment pressure would not exceed the 48.1 psig limit described in the FSAR.  To
  Completion date: June 30, 2008
address the design deficiency associated with the containment air cooler control circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit such that tripping of the fast speed overloads would not impact the safety-related slow speed function of the containment air coolers. This finding is of very low safety significance because the containment coolers are structures, systems, and components that are not significant contributors to the large early release frequency.  Licensee corrective actions were recorded in CAR 200802264.  The inspectors reviewed the LER and identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the licensee's failure to adequately review the suitability of the design of the containment air cooler control circuitry (Section 1R15).  This LER is closed.
4. The following evaluations and testing will be completed.
  a.     Industry chemical effects testing
          Completion date: June 30, 2008
  b.     Nuclear Energy Institute 04-07 debris generation calculation
          Completion date: June 30, 2008
  c.      Evaluation of chemical effects impact on sump-strainer head loss
          Completion date: June 30, 2008
  d.     Confirmation that the replacement sump strainer design provides for
          available Net Positive Suction Head (NPSH) to be in excess of required
          NPSH
          Completion date: June 30, 2008
                                - 36 -                                  Enclosure 2


This inspection constituted one sample of follow-up of events.
   e.     Completion of the final site acceptance review of the Westinghouse team
 
          analysis summary report
  - 35 - Enclosure 2 4OA5 Other Activities
          Completion date: June 30, 2008
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities
5. Callaway Plant will complete the following items during Refueling Outage15:
      a. During the inspection period, the inspectors performed the following observations of security force personnel and activities to ensure that the activities were consistent with licensee's security procedures and regulatory requirements relating to nuclear plant security.  These observations took place during both normal and off-normal plant working hours.
  a.     Replacement of containment recirculation sump strainers
          Completed. As noted in the previous Temporary Instruction 166 report,
These quarterly resident inspector observation of security force personnel and activities did not constitute any additional inspection samples.  Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities.
          the resident inspectors had observed the installation of sump strainers
      b. Findings
          and debris barriers during their containment walkdown; however, the
   No findings of significance were identified.
          strainers were not built in accordance with the design. The licensee has
.2 (Closed) NRC Temporary Instruction 2515/166:  Pressurized Water Reactor Containment Sump Blockage
          completed their initial determination of operability and was finalizing their
      a. Inspection Scope
          acceptance calculations.
  From March 17-19, 2008, the inspectors reviewed the licensee's implementation of plant modifications and design modification packages associated with their response to
  b.     Modification of containment debris barriers and interceptors as required
Generic Letter 2004-02, "Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized Water Reactors."  The inspectors reviewed various aspects of the on-going procedural changes.  Those changes that have been completed were verified to be properly documented in accordance with the requirements of 10 CFR 50.59.  At the completion of this inspection,
          Completed. As noted in the previous Temporary Instruction 166 report,
the licensee had completed the installation stage of the new sump strainers; many of the procedural changes associated with the modifications had not been completed. 
          the resident inspectors had observed the installation of sump strainers
The inspectors compared and evaluated the recirculation sump modifications to the original design basis using Temporary Instruction 2515/166 and referred to Regulatory Guide 1.82, Revision 0, "Water Sources for Long-Term Recirculation Cooling Following a Loss-of-Coolant Accident." 
          and debris barriers during their containment walkdown.
Status of the implementation of the plant modifications and procedure changes committed to by the licensee in their Generic Letter 2004-02 response is:
  c.     Evaluation and implementation of potential modification to the safety
1. Containment walkdown to provide current assessment of Callaway's containment coatings and latent debris. The licensee completed a containment walkdown and latent debris assessment during Refueling Outage 14.  The resident inspectors completed a walkdown of the containment prior to reactor startup following the outage.  The licensee report, "Containment Building Latent Debris Assessment Refuel 14 Fall 2005," was reviewed by the inspectors. 
          injection system to address downstream effects
 
          Completion date: June 30, 2008
  - 36 - Enclosure 2 2.  The following corrective action activities will be completed: a. Replacement sump strainer structural analysis. The strainers were not built in accordance with the design.  As a result, calculations needed to be revised due to the deviations of the as built condition from design and errors in temperature correction values used in
6. Callaway Plant will complete removal of containment spray system pump cyclone
the initial calculations.  Completion date:  June 30, 2008
  separators, if required, based on the results of the downstream effects
b. Downstream effects evaluation  Completion date:  June 30, 2008
  evaluation.
c. Upstream effects evaluation  Completion date:  June 30, 2008
  Completion date: June 30, 2008
d.  Resolution of debris generation calculation unverified assumption of 5D ZOI for qualified coatings (via coatings testing)  Completion date:  June 30, 2008
7. The following programs and controls will be implemented at Callaway Plant to
e. Replacement sump screen head loss testing  Completion date:  June 30, 2008
  control debris sources:
3. Provide an update of the information contained in Section 2(c) regarding analysis methodology.  Completion date:  June 30, 2008
  a.     Changes to design change process procedures to ensure that necessary
          engineering evaluations will be performed for plant design that either
4.  The following evaluations and testing will be completed. a. Industry chemical effects testing  Completion date:  June 30, 2008
          directly or indirectly affects containment, ECCS, or CSS.
          Changes are being processed.
b.  Nuclear Energy Institute 04-07 debris generation calculation  Completion date:  June 30, 2008
  b.     Changes to containment entry and material control procedure
c.  Evaluation of chemical effects impact on sump-strainer head loss  Completion date:  June 30, 2008
          requirements for control of materials during work activities conducted in
d.  Confirmation that the replacement sump strainer design provides for available Net Positive Suction Head (NPSH) to be in excess of required
          the containment
NPSH  Completion date:  June 30, 2008
  c.     The following procedures were reviewed and completed as of
 
          December 2007:
  - 37 - Enclosure 2 e.  Completion of the final site acceptance review of the Westinghouse team analysis summary report Completion date: June 30, 2008  
          APA-ZZ-01004, Radiological Work Standards, Revision 9
5. Callaway Plant will complete the following items during Refueling Outage15: a. Replacement of containment recirculation sump strainers Completed. As noted in the previous Temporary Instruction 166 report, the resident inspectors had observed the installation of sump strainers and debris barriers during their containment walkdown; however, the strainers were not built in accordance with the design. The licensee has completed their initial determination of operability and was finalizing their  
          HDP-ZZ-06100, Reactor Building Access, Revision 7
acceptance calculations.  
                                - 37 -                                   Enclosure 2
b. Modification of containment debris barriers and interceptors as required Completed. As noted in the previous Temporary Instruction 166 report, the resident inspectors had observed the installation of sump strainers and debris barriers during their containment walkdown.  
c. Evaluation and implementation of potential modification to the safety injection system to address downstream effects Completion date: June 30, 2008  
6. Callaway Plant will complete removal of containment spray system pump cyclone separators, if required, based on the results of the downstream effects evaluation. Completion date: June 30, 2008  
7. The following programs and controls will be implemented at Callaway Plant to control debris sources: a. Changes to design change process procedures to ensure that necessary engineering evaluations will be performed for plant design that either directly or indirectly affects containment, ECCS, or CSS. Changes are being processed.
b. Changes to containment entry and material control procedure requirements for control of materials during work activities conducted in the containment c. The following procedures were reviewed and completed as of December 2007: APA-ZZ-01004, Radiological Work Standards, Revision 9 HDP-ZZ-06100, Reactor Building Access, Revision 7 
  - 38 - Enclosure 2 MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22 OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6
OSP-SA-00004, Visual Inspection of Containment for Loose Debris, Revision 19 OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices, Revision 2 d.  Changes to programs and procedures that have the potential to add tags and labels inside containment  Completed:  December 2007  
The following documents were reviewed:  
APA-ZZ-01004, Radiological Work Standards, Revision 9 HDP-ZZ-06100, Reactor Building Access, Revision 7  
MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22 
OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6 OSP-SA-00004, Visual Inspection of Containment for Loose Debris, Revision 19 OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices, Revision 2 e.  Implementation of a containment coatings assessment program Licensee reported as complete.  The inspectors reviewed SWE07848, "Containment Coating Condition Assessment."  A preventative
maintenance item has been scheduled to perform containment coating assessments with a periodicity of each refueling cycle. 
f. Implementation of a containment latent debris assessment program Licensee reported as complete.  The inspectors reviewed report, "Containment Building Latent Debris Assessment Refuel 14 Fall 2005,"
and Procedure OSP-SA-00004, "Visual Inspection of Containment for Loose Debris," Revision 019.  A preventative maintenance item has been scheduled for a visual inspection of containment for loose debris with a periodicity of each refueling cycle.
g. Implementation of changes to the inspection processes for the installed sump strainers Licensee reported as complete.  Reviewed Procedure OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6 
 
  - 39 - Enclosure 2 8. A final response will be submitted to the NRC to provide a final status of actions requested by Generic Letter 2004-02. Completion date:  June 30, 2008 
The Office of Nuclear Reactor Regulation will determine the adequacy of the sump modifications with respect to Generic Safety Issue 191.  This temporary instruction is closed.  Documents reviewed by the inspectors are listed in the attachment. 
      b. Findings
No findings of significance were identified.
4OA6 Management Meetings
  Exit Meeting Summary
On April 25, 2008, the health physics inspector presented the occupational radiation safety inspection results to Mr. T. Herrmann and other members of his staff who acknowledged the findings.  The inspector confirmed that proprietary information was not provided or examined during the inspection.


On June 18, 2008, the Temporary Instruction 2515/166 inspector presented the inspection results to Mr. S. Maglio and other members of his staff who acknowledged the findings. The inspector confirmed that proprietary information provided or examined during the inspection had been returned.  
  MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22
  OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6
  OSP-SA-00004, Visual Inspection of Containment for Loose Debris,
  Revision 19
  OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices,
  Revision 2
d. Changes to programs and procedures that have the potential to add tags
  and labels inside containment
  Completed: December 2007
  The following documents were reviewed:
  APA-ZZ-01004, Radiological Work Standards, Revision 9
  HDP-ZZ-06100, Reactor Building Access, Revision 7
  MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22
  OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6
  OSP-SA-00004, Visual Inspection of Containment for Loose Debris,
  Revision 19
  OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices,
  Revision 2
e. Implementation of a containment coatings assessment program
  Licensee reported as complete. The inspectors reviewed SWE07848,
  Containment Coating Condition Assessment. A preventative
  maintenance item has been scheduled to perform containment coating
  assessments with a periodicity of each refueling cycle.
f. Implementation of a containment latent debris assessment program
  Licensee reported as complete. The inspectors reviewed report,
  Containment Building Latent Debris Assessment Refuel 14 Fall 2005,
  and Procedure OSP-SA-00004, Visual Inspection of Containment for
  Loose Debris, Revision 019. A preventative maintenance item has been
  scheduled for a visual inspection of containment for loose debris with a
  periodicity of each refueling cycle.
g. Implementation of changes to the inspection processes for the installed
  sump strainers
  Licensee reported as complete. Reviewed Procedure OSP-EJ-00003,
  Containment Recirculation Sump Inspection, Revision 6
                        - 38 -                                  Enclosure 2


On June 24, 2008, the resident inspectors presented the inspection results to Mr. C. Naslund, Senior Vice President and Chief Nuclear Officer, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors understood and acknowledged that proprietary information reviewed would not be
    8.      A final response will be submitted to the NRC to provide a final status of actions
retained following report issuance.
            requested by Generic Letter 2004-02.
4OA7 Licensee-Identified Violations
            Completion date: June 30, 2008
The following violations of very low safety significance (Green) were identified by the licensee and were violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.  
    The Office of Nuclear Reactor Regulation will determine the adequacy of the sump
* 10 CFR Part 50, Appendix B, Criterion III, "Design Control," requires, in part, that applicable regulatory requirements and the design basis are correctly translated into specifications, drawings, procedures, and instructions. 
    modifications with respect to Generic Safety Issue 191. This temporary instruction is
Contrary to the above, on March 5, 2008, the licensee identified that a 4-foot section of suction piping within containment spray system, Train A was approximately 50 percent voided. Voiding within the containment spray system was due to a design deficiency that did not allow for a proper fill and vent of the system.  This was entered in the licensee's corrective action
    closed.
program as CAR 200803462. This finding is greater than minor because it is similar to the Example 3j in Manual Chapter 0612, Appendix E, "Examples of 
    Documents reviewed by the inspectors are listed in the attachment.
  - 40 - Enclosure 2 Minor Issues," in that the presence of air within the containment spray system suction header resulted in a condition where there was reasonable doubt on the operability of the system. This finding is of very low safety significance because it was a design or qualification deficiency confirmed not to result in loss of operability.  
  b. Findings
* 10 CFR Part 50, Appendix B, Criterion III, requires measures be established to assure that applicable regulatory requirements and design basis be correctly translated into specifications, drawings, procedures, and instructions.  Technical Specifications 3.5.2 and 3.6.6 require that residual heat removal and containment spray system components remain operable.  Contrary to this, measures were not adequate to assure installed center tube
    No findings of significance were identified.
diameters for the containment recirculation sump modification were correctly accounted for by an accurate net positive suction head calculation.   The vendor supplying AmerenUE the containment recirculation sump strainer identified that associated Vendor Calculation TDI-6002-05 for clean strainer head loss did not account for the installed orifices located in the strainer support plate. The size of the orifice beneath each strainer was smaller than
4OA6 Management Meetings
assumed in head loss calculations and was not large enough to prevent head loss in excess of the net positive suction head required as defined in the purchase specification supplied to the strainer vendor. The additional head loss due to the calculation translation error was 2.28 feet.  This resulted in required net positive suction head being less than available.  AmerenUE
    Exit Meeting Summary
performed three separate operability determination reviews to demonstrate that the head loss margin could be recovered. The initial operability determination on January 22, 2008, addressed the smaller support plate orifice holes by using a separate vendor's flow analysis of the residual heat removal and containment spray piping systems to demonstrate lower flow and head losses than described in the FSAR. This operability determination resulted in the limiting case flow path being the hot leg recirculation flow path.
    On April 25, 2008, the health physics inspector presented the occupational radiation
Another operability review on March 12, 2008, addressed a nonconservative temperature correction through the orifices. Subsequent to this, the licensee informed the NRC that the additional nonconservative inputs were used in the January 22, 2008, flow re-analysis of the residual heat removal system. Additional analyses were performed to regain margin. This resulted in the  
    safety inspection results to Mr. T. Herrmann and other members of his staff who
limiting case flow path changing from hot leg recirculation to cold leg recirculation.  
    acknowledged the findings. The inspector confirmed that proprietary information was
This example of inadequate design control was captured in the licensee's corrective action program as CARs 200800461 and 200802618. These  
    not provided or examined during the inspection.
corrective action reviews documented three causes related to the following design error:  
    On June 18, 2008, the Temporary Instruction 2515/166 inspector presented the
* Time pressure to address Generic Letter 2004-02
    inspection results to Mr. S. Maglio and other members of his staff who acknowledged the
* A complex design with parallel sequencing of different parts of the design * AmerenUE not independently verifying the vendor's design due to perceived expertise and an approved 10 CFR Part 50, Appendix B,
    findings. The inspector confirmed that proprietary information provided or examined
  - 41 - Enclosure 2 Quality Assurance program. AmerenUE did not perform a review of the design, nor did they contract to have a third party engineering review of the design.   This finding is greater than minor because it is similar to the Example 3j in Manual Chapter 0612, Appendix E, Examples of Minor Issues, in that the contractor error translating the design to the calculations resulted in a condition where there was reasonable doubt on the operability of the ECCS. This finding is of very low safety significance because it was a design or qualification deficiency confirmed not to result in loss of operability. This  
    during the inspection had been returned.
licensee-identified violation closes out Unresolved Item 05000483/2008002-01.  
    On June 24, 2008, the resident inspectors presented the inspection results to
  ATTACHMENT: SUPPLEMENTAL INFORMATION  
    Mr. C. Naslund, Senior Vice President and Chief Nuclear Officer, and other members of
  A-1 Attachment SUPPLEMENTAL INFORMATION
    the licensee staff. The licensee acknowledged the issues presented. The inspectors
KEY POINTS OF CONTACT  
    understood and acknowledged that proprietary information reviewed would not be
Licensee Personnel   B. Barton, Training Manager M. Brandes, Consulting Engineer, Nuclear Engineering - Major Modifications K. Bruckerhoff, Supervisor, Emergency Preparedness  
    retained following report issuance.
F. Diya, Plant Director T. Elwood, Supervising Engineer, Licensing R. Farnam, Manager, Radiation Protection K. Gilliam, Supervisor, Radiation Protection L. Graessle, Manager, Regulatory Affairs  
4OA7 Licensee-Identified Violations
A. Heflin, Vice President, Nuclear T. Herrmann, Vice President, Engineering B. Holderness, Senior Health Physicist, Environmental Services L. Kanuckel, Manager, Quality Assurance D. Lantz, Superintendent of Operations Training S. Maglio, Assistant Manager, Regulatory Affairs R. Myatt, Supervisor, Engineering  
    The following violations of very low safety significance (Green) were identified by the
K. Mills, Manager, Engineering D. Neterer, Manager, Nuclear Operations T. Parker, Trainer, Radiation Protection S. Petzel, Engineer, Regulatory Affairs J. Pitts, Component Engineer  
    licensee and were violations of NRC requirements which meet the criteria of Section VI
V. Rider, ALARA Specialist, Radiation Protection  
    of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.
LIST OF ITEMS OPENED AND CLOSED Opened 05000483/2008003-05 VIO Failure to Prevent Recurrence of Voids in ECCS Cold Leg Recirculation Piping (Section 4OA2)  
        *      10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part,
Opened and Closed
                that applicable regulatory requirements and the design basis are correctly
  05000483/2008003-01 NCV Failure to Ensure the Suitability of the Design of the Containment Air Cooler Control Circuitry (Section 1R15) 05000483/2008003-02 NCV Inadequate Surveillance Procedure Resulted in an Inoperable ECCS (Section 1R15) 05000483/2008003-03 NCV Failure to Correct a Condition Adverse to Quality for Diesel Generator Jacket Water O-Rings (Section 1R19) 05000483/2008003-04 NCV Failure to Maintain an Adequate Technical Specification Bases Change Process (Section 1R22)  
                translated into specifications, drawings, procedures, and instructions.
Closed 05000483/2008001-00 LER Containment Cooler Inoperability (Section 4OA3) 05000483/2008002-01 URI Containment Recirculation Sump Operability (Section 4OA7)
                Contrary to the above, on March 5, 2008, the licensee identified that a 4-foot
  A-2 Attachment LIST OF DOCUMENTS REVIEWED The following is a partial list of documents reviewed during the inspection. Inclusion on this list does not imply that the NRC inspector reviewed the documents in their entirety, but rather that selected sections or portions of the documents were evaluated as part of the overall inspection effort.  Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.  
                section of suction piping within containment spray system, Train A was
                approximately 50 percent voided. Voiding within the containment spray
Section 1R01: Adverse Weather Protection
                system was due to a design deficiency that did not allow for a proper fill and
Procedures
                vent of the system. This was entered in the licensees corrective action
ODP-ZZ-00001, Operations Department - Code of Conduct, Revision 41  
                program as CAR 200803462. This finding is greater than minor because it is
OSP-NB-00001, Class 1E Electrical Source Verification, Revision 032  
                similar to the Example 3j in Manual Chapter 0612, Appendix E, "Examples of
OTN-NB-0001A, 4.16 KV Vital (Class 1E) Electrical System - A Train, Revision 12  
                                          - 39 -                                    Enclosure 2
OTN-NB-0001A, Addendum 5, NB01 Loss of Power Recovery, Revision 0  
 
OTO-ZZ-00012, Severe Weather, Revision 10  
  Minor Issues," in that the presence of air within the containment spray system
  suction header resulted in a condition where there was reasonable doubt on
  the operability of the system. This finding is of very low safety significance
  because it was a design or qualification deficiency confirmed not to result in
  loss of operability.
* 10 CFR Part 50, Appendix B, Criterion III, requires measures be established
  to assure that applicable regulatory requirements and design basis be
  correctly translated into specifications, drawings, procedures, and
   instructions. Technical Specifications 3.5.2 and 3.6.6 require that residual
  heat removal and containment spray system components remain operable.
  Contrary to this, measures were not adequate to assure installed center tube
  diameters for the containment recirculation sump modification were correctly
  accounted for by an accurate net positive suction head calculation.
  The vendor supplying AmerenUE the containment recirculation sump strainer
  identified that associated Vendor Calculation TDI-6002-05 for clean strainer
  head loss did not account for the installed orifices located in the strainer
  support plate. The size of the orifice beneath each strainer was smaller than
  assumed in head loss calculations and was not large enough to prevent head
  loss in excess of the net positive suction head required as defined in the
  purchase specification supplied to the strainer vendor. The additional head
  loss due to the calculation translation error was 2.28 feet. This resulted in
  required net positive suction head being less than available. AmerenUE
  performed three separate operability determination reviews to demonstrate
  that the head loss margin could be recovered. The initial operability
  determination on January 22, 2008, addressed the smaller support plate
  orifice holes by using a separate vendor's flow analysis of the residual heat
  removal and containment spray piping systems to demonstrate lower flow
  and head losses than described in the FSAR. This operability determination
  resulted in the limiting case flow path being the hot leg recirculation flow path.
  Another operability review on March 12, 2008, addressed a nonconservative
  temperature correction through the orifices. Subsequent to this, the licensee
  informed the NRC that the additional nonconservative inputs were used in
  the January 22, 2008, flow re-analysis of the residual heat removal system.
  Additional analyses were performed to regain margin. This resulted in the
  limiting case flow path changing from hot leg recirculation to cold leg
  recirculation.
  This example of inadequate design control was captured in the licensees
  corrective action program as CARs 200800461 and 200802618. These
  corrective action reviews documented three causes related to the following
  design error:
    *     Time pressure to address Generic Letter 2004-02
    *     A complex design with parallel sequencing of different parts of the
          design
    *     AmerenUE not independently verifying the vendor's design due to
          perceived expertise and an approved 10 CFR Part 50, Appendix B,
                            - 40 -                                     Enclosure 2
 
                    Quality Assurance program. AmerenUE did not perform a review of
                    the design, nor did they contract to have a third party engineering
                    review of the design.
            This finding is greater than minor because it is similar to the Example 3j in
            Manual Chapter 0612, Appendix E, Examples of Minor Issues, in that the
            contractor error translating the design to the calculations resulted in a
            condition where there was reasonable doubt on the operability of the ECCS.
            This finding is of very low safety significance because it was a design or
            qualification deficiency confirmed not to result in loss of operability. This
            licensee-identified violation closes out Unresolved
            Item 05000483/2008002-01.
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                      - 41 -                                     Enclosure 2
 
                              SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Licensee Personnel
B. Barton, Training Manager
M. Brandes, Consulting Engineer, Nuclear Engineering - Major Modifications
K. Bruckerhoff, Supervisor, Emergency Preparedness
F. Diya, Plant Director
T. Elwood, Supervising Engineer, Licensing
R. Farnam, Manager, Radiation Protection
K. Gilliam, Supervisor, Radiation Protection
L. Graessle, Manager, Regulatory Affairs
A. Heflin, Vice President, Nuclear
T. Herrmann, Vice President, Engineering
B. Holderness, Senior Health Physicist, Environmental Services
L. Kanuckel, Manager, Quality Assurance
D. Lantz, Superintendent of Operations Training
S. Maglio, Assistant Manager, Regulatory Affairs
R. Myatt, Supervisor, Engineering
K. Mills, Manager, Engineering
D. Neterer, Manager, Nuclear Operations
T. Parker, Trainer, Radiation Protection
S. Petzel, Engineer, Regulatory Affairs
J. Pitts, Component Engineer
V. Rider, ALARA Specialist, Radiation Protection
                            LIST OF ITEMS OPENED AND CLOSED
Opened
05000483/2008003-05         VIO     Failure to Prevent Recurrence of Voids in ECCS Cold Leg
                                    Recirculation Piping (Section 4OA2)
Opened and Closed
  05000483/2008003-01         NCV     Failure to Ensure the Suitability of the Design of the
                                    Containment Air Cooler Control Circuitry (Section 1R15)
05000483/2008003-02         NCV     Inadequate Surveillance Procedure Resulted in an
                                    Inoperable ECCS (Section 1R15)
05000483/2008003-03         NCV     Failure to Correct a Condition Adverse to Quality for
                                    Diesel Generator Jacket Water O-Rings (Section 1R19)
05000483/2008003-04         NCV     Failure to Maintain an Adequate Technical Specification
                                    Bases Change Process (Section 1R22)
Closed
05000483/2008001-00         LER     Containment Cooler Inoperability (Section 4OA3)
05000483/2008002-01         URI     Containment Recirculation Sump Operability
                                    (Section 4OA7)
                                            A-1                                Attachment
 
                                  LIST OF DOCUMENTS REVIEWED
The following is a partial list of documents reviewed during the inspection. Inclusion on this list
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that
selected sections or portions of the documents were evaluated as part of the overall inspection
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
any part of it, unless this is stated in the body of the inspection report.
Section 1R01: Adverse Weather Protection
Procedures
ODP-ZZ-00001, Operations Department - Code of Conduct, Revision 41
OSP-NB-00001, Class 1E Electrical Source Verification, Revision 032
OTN-NB-0001A, 4.16 KV Vital (Class 1E) Electrical System - A Train, Revision 12
OTN-NB-0001A, Addendum 5, NB01 Loss of Power Recovery, Revision 0
OTO-ZZ-00012, Severe Weather, Revision 10
Miscellaneous
Miscellaneous
AmerenUE Response to Generic Letter 2006-02, Grid Reliability and the Impact on Plant Risk and the Operability of Offsite Power Training Lesson Plan LP-01, Systems, Switchyard MD  
AmerenUE Response to Generic Letter 2006-02, Grid Reliability and the Impact on Plant Risk
Training Lesson Plan T61.0110.6, Systems, Switchyard MD Section 1RO4: Equipment Alignment
and the Operability of Offsite Power
Drawings M-22AL01A, Piping and Instrumentation Diagram Auxiliary Feedwater System, Revision 33  
Training Lesson Plan LP-01, Systems, Switchyard MD
M-22BB01(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 30  
Training Lesson Plan T61.0110.6, Systems, Switchyard MD
M-22BB03A(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9  
Section 1RO4: Equipment Alignment
M-22BB03B(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9  
Drawings
M-22BB03C(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7 M-22BB03D(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7 M-22BG01(Q), Piping and Instrumentation Diagram Chemical and Volume Control System, Revision 28 M-22BG03(Q), Piping and Instrumentation Diagram Chemical and Volume Control System, Revision 52
M-22AL01A, Piping and Instrumentation Diagram Auxiliary Feedwater System, Revision 33
  A-3 Attachment M-22EJ01(Q), Piping and Instrumentation Diagram Residual Heat Removal System, Revision 57 M-22EM01(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System, Revision 33 M-22EM02(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System, Revision 19 M-22EP01(Q), Piping and Instrumentation Diagram Accumulator and Safety Injection, Revision 16 Section 1RO5: Fire Protection  
M-22BB01(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 30
Miscellaneous
M-22BB03A(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9
Drill Number 08-01, Evaluate Fire Brigade Response in a Radiation Area, dated March 27, 2008  
M-22BB03B(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9
Drill Critique Number 08-01, Unannounced Fire Drill, dated March 27, 2008  
M-22BB03C(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7
FSAR, Appendix 9.5B, Fire Hazard Analysis Section 1R11: Licensed Operator Requalification Program  
M-22BB03D(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7
Procedures
M-22BG01(Q), Piping and Instrumentation Diagram Chemical and Volume Control System,
OTA-RK-00024, Addendum 98D, Seismic Event, Revision 0 OTO-SG-0001, Design Basis Earthquake, Revision 13  
Revision 28
M-22BG03(Q), Piping and Instrumentation Diagram Chemical and Volume Control System,
Section 1R12: Maintenance Effectiveness
Revision 52
Procedures
                                              A-2                            Attachment
EDP-ZZ-01128, Maintenance Rule Program, Revision 8  
 
NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3  
M-22EJ01(Q), Piping and Instrumentation Diagram Residual Heat Removal System,
Callaway Action Requests
Revision 57
200706892 200801644 200802854
M-22EM01(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System,
Section 1R13:  Maintenance Risk Assessment and Emergent Work Controls
Revision 33
Procedure EDP-ZZ-01129, Callaway Plant Risk Assessment, Revision 14
M-22EM02(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System,
Section 1R15:  Operability Evaluations
Revision 19
Calculations
M-22EP01(Q), Piping and Instrumentation Diagram Accumulator and Safety Injection,
ARC-687, AFT Fathom 6.0 Output, Revision 0 
Revision 16
  A-4 Attachment
Section 1RO5: Fire Protection
M-FL-18, LOCA and MSLB Containment Flood Level, Revision 1
Miscellaneous
WES-009-CALC-001, Wolf Creek/Callaway Post-LOCA Containment Water Level Calculation, Revision 0
Drill Number 08-01, Evaluate Fire Brigade Response in a Radiation Area, dated March 27, 2008
Drill Critique Number 08-01, Unannounced Fire Drill, dated March 27, 2008
FSAR, Appendix 9.5B, Fire Hazard Analysis
Section 1R11: Licensed Operator Requalification Program
Procedures
OTA-RK-00024, Addendum 98D, Seismic Event, Revision 0
OTO-SG-0001, Design Basis Earthquake, Revision 13
Section 1R12: Maintenance Effectiveness
Procedures
EDP-ZZ-01128, Maintenance Rule Program, Revision 8
NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear
Power Plants, Revision 3
Callaway Action Requests
Callaway Action Requests
200800461
200706892                        200801644                        200802854
200802231
Section 1R13: Maintenance Risk Assessment and Emergent Work Controls
Procedure
EDP-ZZ-01129, Callaway Plant Risk Assessment, Revision 14
Section 1R15: Operability Evaluations
Calculations
ARC-687, AFT Fathom 6.0 Output, Revision 0
                                          A-3                              Attachment


200802264  
M-FL-18, LOCA and MSLB Containment Flood Level, Revision 1
200802348  
WES-009-CALC-001, Wolf Creek/Callaway Post-LOCA Containment Water Level Calculation,
200802352
Revision 0
200802365
Callaway Action Requests
200800461                      200802352                        200803462
200802231                      200802365                        200804000
200802264                       200802618
200802348                       200803252
Drawings
E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19
E-018-00273, Motor Control Center Ambient Compensated Overload Relay Heater Chart,
Revision 3
E-018-00847, Overload Relay Time Current Characteristics, Revision 4
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5
E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12
E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,
Revision 2
J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,
Revision 1
M-018-00943, 206 Ez-Flo Expansion Joint, Revision 0
M-22BG03, Piping and Instrumentation Diagram Chemical and Volume Control System,
Revision 52
M-22EM01, Piping and Instrumentation Diagram High Pressure Coolant Injection System,
Revision 33
M-23BG02, Piping Isometric CVCS-Max Charging Flow A and B Train Auxiliary Building,
Revision 12
                                        A-4                              Attachment


200802618
Procedures
200803252
ECA-0.1, Loss of All AC Power Recover Without Safety Injection Required, Revision 8
200803462
ECA-1.1, Loss of Emergency Coolant Recirculation, Revision 8
200804000
EDP-ZZ-04021, Review of Supplier Documents, Revision 5
Drawings E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19
ISF-SE-00N32, FCTNAL-NUC INSTM SOURCE RANGE N32, Revision 20
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19
OSP-EJ-PV04A, Train A RHR and RCS Check Valve Inservice Test -IPTE, Revision 0
E-018-00273, Motor Control Center Ambient Compensated Overload Relay Heater Chart, Revision 3 E-018-00847, Overload Relay Time Current Characteristics, Revision 4
OSP-EJ-PV04B, Train B RHR and RCS Check Valve Inservice Test -IPTE, Revision 1
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11
OTN-EN-00001, Containment Spray System, Revision 14
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12
OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 1
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5 E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12 E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C, Revision 2 J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D, Revision 1 M-018-00943, 206 Ez-Flo Expansion Joint, Revision 0
M-22BG03, Piping and Instrumentation Diagram Chemical and Volume Control System, Revision 52 M-22EM01, Piping and Instrumentation Diagram High Pressure Coolant Injection System, Revision 33 M-23BG02, Piping Isometric CVCS-Max Charging Flow A and B Train Auxiliary Building, Revision 12 
  A-5 Attachment Procedures
  ECA-0.1, Loss of All AC Power Recover Without Safety Injection Required, Revision 8  
ECA-1.1, Loss of Emergency Coolant Recirculation, Revision 8  
EDP-ZZ-04021, Review of Supplier Documents, Revision 5  
ISF-SE-00N32, FCTNAL-NUC INSTM SOURCE RANGE N32, Revision 20  
OSP-EJ-PV04A, Train A RHR and RCS Check Valve Inservice Test -IPTE, Revision 0  
OSP-EJ-PV04B, Train B RHR and RCS Check Valve Inservice Test -IPTE, Revision 1 OTN-EN-00001, Containment Spray System, Revision 14 OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 1  
Miscellaneous
Miscellaneous
Job 07513275 for SEN0032  
Job 07513275 for SEN0032
Letter ULNRC-04884, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co., Facility Operating License NPF-30, Response to NRC Bulletin 2003-01, Potential Impact of Debris Blockage on Emergency Sump Recirculation at Pressurized Water Reactor, dated August 3, 2003 Letter ULNRC-05481, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co., Facility Operating License NPF-30 Response to Request for Additional Information, Response to NRC Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency  
Letter ULNRC-04884, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co.,
Recirculation During Design Basis Accidents at Pressurized Water Reactors, dated February 29, 2008 Garlock Sealing Technologies Customer Requested Test 206 Ez-Flo Expansion Test, dated November 15, 2006 Section 1R18: Plant Modifications
Facility Operating License NPF-30, Response to NRC Bulletin 2003-01, Potential Impact of
Procedure OTN-KA-00001, Compressed Air System, Revision 18 Drawings E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19  
Debris Blockage on Emergency Sump Recirculation at Pressurized Water Reactor, dated
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19  
August 3, 2003
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11  
Letter ULNRC-05481, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co.,
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12  
Facility Operating License NPF-30 Response to Request for Additional Information, Response
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5
to NRC Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency
  A-6 Attachment E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12 E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13
Recirculation During Design Basis Accidents at Pressurized Water Reactors, dated
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C, Revision 2 J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D, Revision 1 M-22KA01, Piping and Instrumentation Diagram Compressed Air System, Revision 016A
February 29, 2008
M-22KA06, Piping and Instrumentation Diagram Instrument Air Filter/Dryer Turbine, Building, Revision 30A Miscellaneous
Garlock Sealing Technologies Customer Requested Test 206 Ez-Flo Expansion Test, dated
Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change, Revision 0
November 15, 2006
Job 08003842 Section 1R19:  Postmaintenance Testing
Section 1R18: Plant Modifications
Procedures
Procedure
APA-ZZ-00330, Preventative Maintenance Program, Revision 29
OTN-KA-00001, Compressed Air System, Revision 18
Drawings
OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 14
E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19
Callaway Action Requests
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19
200801270          200802810      200804164
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11
Jobs 06524419 07006905 08001080 08002676 08002765 08003910 
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12
Drawings E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19 E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12 E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11
                                          A-5                             Attachment
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5
  A-7 Attachment E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12 E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C, Revision 2 J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D, Revision 1 Miscellaneous
Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change, Revision 0
Simple Surveillance SP08-017, Containment Cooler Control Circuit Changes, dated April 16, 2008 
Section 1R22:  Surveillance Testing
Procedures
EDP-ZZ-04107, HVAC Pressure Boundary Control, Revision 19
FDP-ZZ-00101, Technical Specification Bases Control Program, Revision 6
OSP-GL-0001A, Auxiliary Building Train A Negative Pressure Test, Revision 6
OSP-EJ-P001A, RHR Train A inservice Test - Group A, Revision 44 
OSP-EJ-V001B, Residual heat removal Train B valve inservice test, Revision 21
OSP-NE-0001B, Standby Diesel Generator B Periodic Tests, Revision 29
OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting, Revision 30 Section 2OS1:  Access Controls to Radiologically Significant Areas and
Section 2OS2:  ALARA Planning and Controls
Callaway Action Requests
200703726
200703956
200710799


200711181
E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12
200711846
E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13
200711875
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,
200711880
Revision 2
200711881
J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,
200711883
Revision 1
200800219
M-22KA01, Piping and Instrumentation Diagram Compressed Air System, Revision 016A
M-22KA06, Piping and Instrumentation Diagram Instrument Air Filter/Dryer Turbine, Building,
Revision 30A
Miscellaneous
Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change,
Revision 0
Job
08003842
Section 1R19: Postmaintenance Testing
Procedures
APA-ZZ-00330, Preventative Maintenance Program, Revision 29
OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 14
Callaway Action Requests
200801270                      200802810                          200804164
Jobs
06524419                        08001080                          08002765
07006905                        08002676                          08003910
Drawings
E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5
                                        A-6                                Attachment


200800438
E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12
200800631  
E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13
200800632  
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,
200800633  
Revision 2
J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,
Revision 1
Miscellaneous
Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change,
Revision 0
Simple Surveillance SP08-017, Containment Cooler Control Circuit Changes, dated April 16,
2008
Section 1R22: Surveillance Testing
Procedures
EDP-ZZ-04107, HVAC Pressure Boundary Control, Revision 19
FDP-ZZ-00101, Technical Specification Bases Control Program, Revision 6
OSP-GL-0001A, Auxiliary Building Train A Negative Pressure Test, Revision 6
OSP-EJ-P001A, RHR Train A inservice Test - Group A, Revision 44
OSP-EJ-V001B, Residual heat removal Train B valve inservice test, Revision 21
OSP-NE-0001B, Standby Diesel Generator B Periodic Tests, Revision 29
OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting,
Revision 30
Section 2OS1: Access Controls to Radiologically Significant Areas and
Section 2OS2: ALARA Planning and Controls
Callaway Action Requests
200703726                      200800631                         200800991
200703956                      200800632                         200801135
200710799                      200800633                         200801390
200711181                      200800727                        200801430
200711846                      200800838                        200802003
200711875                      200800887                        200802280
200711880                      200800888                        200803141
200711881                      200800891                        200803204
200711883                      200800957                        200803205
200800219                      200800973                        200803208
200800438                      200800988
                                        A-7                              Attachment


200800727
Audits and Self-Assessments
200800838
Quality Assurance Audit of Radiation Protection AP08-001, February 28, 2008
200800887
Quality Assurance Supplemental Audit of Radwaste AP07-012, October 30, 2007
200800888
Simple Self-assessment Report SA07-RP-S06, January 9, 2008
200800891
Radiation Work Permits/ALARA Reviews
200800957
RWP 803321RESIN, Transfer Spent Resin from Primary Tank to Liner
200800973
ALARA Package 07-03120, Reinstall Bladders into the Recycle Hold Up Tanks
Other/Meetings/Training/Work Review
ALARA Simulator Class
Callaway Plant Long Range Dose and Source Term Reduction Plan, Revision 2
Hot Spot and Shielding Log
Job 08000834 Transfer Spent Resin from Primary Tank to Liner
Plant ALARA Review Committee Meeting
Procedures
APA-ZZ-00405, Special Nuclear Material Control and Accounting, Revision 20
APA-ZZ-01000, Callaway Plant Radiation Protection Program, Revision 26
APA-ZZ-01001, Callaway Plant ALARA Program, Revision 11
APA-ZZ-01106, Lock and Key Control, Revision 16
HDP-ZZ-01100, ALARA Planning and Review, Revision 6
HDP-ZZ-01200, Radiation Work Permits, Revision 9
HTP-ZZ-01203, Radiological Area Access Control, Revision 36
HTP-ZZ-06001, High Radiation/Very High Radiation Area Access, Revision 31
HTP-ZZ-06028, Radiological Controls for Pools that Contain or Store Spent Fuel, Revision 5
RTS-HC-00350, Primary Spent Resin Storage Tank Transfer to Bulk Waste Disposal Station,
Revision 3
Section 4OA1: Performance Indicator Verification
Procedure
NOD-QP-40, NRC Performance Indicator Program, Revision 2
Miscellaneous
Various Callaway Control Room Logs, dated March 2007 through March 2008
Callaway Integrated Inspection Report 05000483/2007002
                                          A-8                              Attachment


200800988
Callaway Integrated Inspection Report 05000483/2007003
200800991
Callaway Integrated Inspection Report 05000483/2007004
200801135
Callaway Integrated Inspection Report 05000483/2008002
200801390
Section 4OA2: Identification and Resolution of Problems
Inspection Findings
NCV 05000483/2005002-01
NCV 05000483/2006012-04
Callaway Action Requests
200501192                        200800355                        200804000
200709819                        200800522                        200804164
200711496                        200801270                        200805049
200800246                        200801529                        200805122
200800298                        200801830                        200808956
Generic Communications
NRC Information Notice 2006-21, OE Regarding Entrainment of Air into Emergency Core
Cooling and Containment Spray Systems, September 21, 2006
Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat
Removal , and Containment Spray Systems, January 11, 2009
Procedures
OTN-EM0001, Safety Injection System, Revision 27
OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting,
Revision 27
Section 4OA5: Other
Procedures
APA-ZZ-01004, Radiological Work Standards, Revision 9
HDP-ZZ-06100, Reactor Building Access, Revision 7
MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22
OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6
OSP-SA-00004, Visual Inspection of Containment for Loose Debris, Revision 19
OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices, Revision 2
Calculations
Calculation BG-75, Impact of MP 06-0003, Replacement Containment Recirculation Sump
Strainers, and MP 06-0027, TSP Basket Relocation, Revision 0
Calculation BN-21, Impact of MP 06-0003, Replacement Containment Recirculation Sump
Strainer on BN21, Revision 0
                                        A-9                              Attachment


200801430
Calculation BN-22, Impact of MP 06-0003, Replacement Containment Recirculation Sump
200802003
Strainer on BN22, Revision 0
200802280
Calculation EJ-29, NPSH Margin for RHR Pumps at Transition to Recirculation When NPSH
200803141
Margin is at its Minimum Value, Revision 1
200803204
Calculation TDI-6002-05/TDI-6003-05, Clean Head Loss - Wolf Creek/Callaway, Revision 0
200803205
200803208 
  A-8 Attachment
Audits and Self-Assessments
Quality Assurance Audit of Radiation Protection AP08-001, February 28, 2008 Quality Assurance Supplemental Audit of Radwaste AP07-012, October 30, 2007 Simple Self-assessment Report SA07-RP-S06, January 9, 2008
Radiation Work Permits/ALARA Reviews
RWP 803321RESIN, Transfer Spent Resin from Primary Tank to Liner ALARA Package 07-03120, Reinstall Bladders into the Recycle Hold Up Tanks
Other/Meetings/Training/Work Review
ALARA Simulator Class Callaway Plant Long Range Dose and Source Term Reduction Plan, Revision 2 Hot Spot and Shielding Log Job 08000834 Transfer Spent Resin from Primary Tank to Liner Plant ALARA Review Committee Meeting
Procedures
APA-ZZ-00405, Special Nuclear Material Control and Accounting, Revision 20
APA-ZZ-01000, Callaway Plant Radiation Protection Program, Revision 26
APA-ZZ-01001, Callaway Plant ALARA Program, Revision 11
APA-ZZ-01106, Lock and Key Control, Revision 16
HDP-ZZ-01100, ALARA Planning and Review, Revision 6
HDP-ZZ-01200, Radiation Work Permits, Revision 9
HTP-ZZ-01203, Radiological Area Access Control, Revision 36 HTP-ZZ-06001, High Radiation/Very High Radiation Area Access, Revision 31 HTP-ZZ-06028, Radiological Controls for Pools that Contain or Store Spent Fuel, Revision 5 RTS-HC-00350, Primary Spent Resin Storage Tank Transfer to Bulk Waste Disposal Station, Revision 3 Section 4OA1: Performance Indicator Verification
Procedure NOD-QP-40, NRC Performance Indicator Program, Revision 2
Miscellaneous
Various Callaway Control Room Logs, dated March 2007 through March 2008 Callaway Integrated Inspection Report 05000483/2007002 
  A-9 Attachment Callaway Integrated Inspection Report 05000483/2007003 Callaway Integrated Inspection Report 05000483/2007004 Callaway Integrated Inspection Report 05000483/2008002
Section 4OA2:  Identification and Resolution of Problems
Inspection Findings
NCV 05000483/2005002-01 NCV 05000483/2006012-04
Callaway Action Requests
200501192
200709819
200711496
200800246
200800298
200800355
200800522
200801270
200801529
200801830
200804000
200804164
200805049
200805122
200808956
Generic Communications
NRC Information Notice 2006-21, OE Regarding Entrainment  of Air into Emergency Core Cooling and Containment Spray Systems, September 21, 2006 Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal , and Containment Spray Systems, January 11, 2009 Procedures
OTN-EM0001, Safety Injection System, Revision 27
OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting, Revision 27
Section 4OA5:  Other
Procedures
APA-ZZ-01004, Radiological Work Standards, Revision 9 HDP-ZZ-06100, Reactor Building Access, Revision 7 MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22 OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6 OSP-SA-00004, Visual Inspection of Containment for Loose Debris, Revision 19 OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices, Revision 2
Calculations
Calculation BG-75, Impact of MP 06-0003, Replacement Containment Recirculation Sump Strainers, and MP 06-0027, TSP Basket Relocation, Revision 0 Calculation BN-21, Impact of MP 06-0003, Replacement Containment Recirculation Sump Strainer on BN21, Revision 0 
  A-10 Attachment Calculation BN-22, Impact of MP 06-0003, Replacement Containment Recirculation Sump Strainer on BN22, Revision 0 Calculation EJ-29, NPSH Margin for RHR Pumps at Transition to Recirculation When NPSH Margin is at its Minimum Value, Revision 1 Calculation TDI-6002-05/TDI-6003-05, Clean Head Loss - Wolf Creek/Callaway, Revision 0  
Callaway Action Request
Callaway Action Request
200800461, Prompt Operability Determination for Containment Spray and Residual Heat Removal Systems, Revision 0 Miscellaneous
200800461, Prompt Operability Determination for Containment Spray and Residual Heat
Ameren/UE comments on ECI-PCI-WC-CAL-6002-6003-1001  
Removal Systems, Revision 0
Callaway Plant Containment Building Latent Debris Assessment Report Refuel 14 Fall 2005  
Miscellaneous
EC-PCI-WC/CAL-6002/6003-1001, AES Calculation No. PCI-5304-S01 Structural Evaluation of the Containment Sump Strainers, Revision 1 MP 06-0003-EC-PCI-WC-CAL-6002-6003- (000) AES Document No. PCI-5304-S01 Structural Evaluation of the Containment Sump Strainers, Revision 1 NUREG/CR-6914, Vol. 4, Integrated Chemical Effects Test, Revision 0  
Ameren/UE comments on ECI-PCI-WC-CAL-6002-6003-1001
SWE07848, Containment Coating Condition Assessment  
Callaway Plant Containment Building Latent Debris Assessment Report Refuel 14 Fall 2005
TDI-6002/TDI-6003, Sure-Flow Suction Strainer Qualification Report and Addendums, Wolf Creek/Callaway ULNRC-05124, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility Operating License NPF-30 Response To Generic Letter 2004-02, Potential Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors. ULNRC-05194, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility Operating License NPF-30 September 1, 2005, Response To Generic Letter 2004-02, Potential Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors. ULNRC-05295, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility Operating License NPF-30 Response Update To Generic Letter 2004-02, Potential Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors. ULNRC-05408, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility Operating License NPF-30 Update For Response To Generic Letter 2004-02, Potential Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.
EC-PCI-WC/CAL-6002/6003-1001, AES Calculation No. PCI-5304-S01 Structural Evaluation of
  A-11 Attachment ULNRC-05461, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility Operating License NPF-30 Request for Extension Of Completion Date For Corrective Actions Associated with NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors. ULNRC-05465, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility Operating License NPF-30 Supplement to Request for Extension of Corrective Actions Completion Date For NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors. WCAP-16568-P, Jet Impingement Testing to Determine the Zone of Influence (ZOI) for  BAQualified/Acceptable Coatings (Proprietary) Wolf Creek/Callaway Comments on Calculation PCI-5304-S01, Structural Evaluation of the Containment Sump Strainers. Section 4OA7:  Licensee-Identified Violations
the Containment Sump Strainers, Revision 1
Callaway Action Requests
MP 06-0003-EC-PCI-WC-CAL-6002-6003- (000) AES Document No. PCI-5304-S01 Structural
200802618 200803462 200800461
Evaluation of the Containment Sump Strainers, Revision 1
Generic Communication
NUREG/CR-6914, Vol. 4, Integrated Chemical Effects Test, Revision 0
Generic Letter 2004-02, "Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized Water Reactors," dated September 13, 2004
SWE07848, Containment Coating Condition Assessment
TDI-6002/TDI-6003, Sure-Flow Suction Strainer Qualification Report and Addendums, Wolf
Creek/Callaway
ULNRC-05124, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
Operating License NPF-30 Response To Generic Letter 2004-02, Potential Impact of Debris
Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water
Reactors.
ULNRC-05194, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
Operating License NPF-30 September 1, 2005, Response To Generic Letter 2004-02, Potential
Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At
Pressurized-Water Reactors.
ULNRC-05295, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
Operating License NPF-30 Response Update To Generic Letter 2004-02, Potential Impact of
Debris Blockage On Emergency Recirculation During Design Basis Accidents At
Pressurized-Water Reactors.
ULNRC-05408, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
Operating License NPF-30 Update For Response To Generic Letter 2004-02, Potential Impact
of Debris Blockage On Emergency Recirculation During Design Basis Accidents At
Pressurized-Water Reactors.
                                          A-10                            Attachment


Calculation
ULNRC-05461, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
TDI-6002-05  
Operating License NPF-30 Request for Extension Of Completion Date For Corrective Actions
Correspondence
Associated with NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On
Amendment 180 to Facility Operating License NPF-30 from Mr. J. Donohew, Senior Project Manager, Office of Nuclear Reactor Regulation to Mr. C. Naslund, AmerenUE  
Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.
Procedure APA-ZZ-00408, Professional Service Agreements and Nuclear Fuel Contracts, Revision 12 AmerenUE Callaway Plant Nuclear Plant Operating Quality Assurance Manual, Section 3, Revision 25  
ULNRC-05465, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
Audits Quality Assurance Audit of Design Control AP08-003  
Operating License NPF-30 Supplement to Request for Extension of Corrective Actions
Independent Technical Review Report, SEGR 08-012, Temperature Correction Factor for Strainer Stack Orifice Head Losses
Completion Date For NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On
Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.
WCAP-16568-P, Jet Impingement Testing to Determine the Zone of Influence (ZOI) for
BAQualified/Acceptable Coatings (Proprietary)
Wolf Creek/Callaway Comments on Calculation PCI-5304-S01, Structural Evaluation of the
Containment Sump Strainers.
Section 4OA7: Licensee-Identified Violations
Callaway Action Requests
200802618                          200803462                      200800461
Generic Communication
Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation
During Design Basis Accidents at Pressurized Water Reactors, dated September 13, 2004
Calculation
TDI-6002-05
Correspondence
Amendment 180 to Facility Operating License NPF-30 from Mr. J. Donohew, Senior Project
Manager, Office of Nuclear Reactor Regulation to Mr. C. Naslund, AmerenUE
Procedure
APA-ZZ-00408, Professional Service Agreements and Nuclear Fuel Contracts, Revision 12
AmerenUE Callaway Plant Nuclear Plant Operating Quality Assurance Manual, Section 3,
Revision 25
Audits
Quality Assurance Audit of Design Control AP08-003
Independent Technical Review Report, SEGR 08-012, Temperature Correction Factor for
Strainer Stack Orifice Head Losses
                                          A-11                            Attachment
}}
}}

Revision as of 14:19, 14 November 2019

IR 05000483-08-003, on 3/25 - 6/24/08, Callaway Plant, Operability Evaluations, Postmaintenance Testing, Surveillance Testing, and Identification and Resolution of Problems
ML082180851
Person / Time
Site: Callaway Ameren icon.png
Issue date: 08/05/2008
From: Vincent Gaddy
NRC/RGN-IV/DRP/RPB-B
To: Heflin A
Union Electric Co
References
EA-08-190 IR-08-003
Download: ML082180851 (58)


See also: IR 05000483/2008003

Text

UNITED STATES

NUC LE AR RE G UL AT O RY C O M M I S S I O N

R E GI ON I V

612 EAST LAMAR BLVD , SU I TE 400

AR LI N GTON , TEXAS 76011-4125

August 5, 2008

EA-08-190

Mr. Adam C. Heflin, Senior Vice

President and Chief Nuclear Officer

Union Electric Company

P.O. Box 620

Fulton, MO 65251

SUBJECT: CALLAWAY PLANT - NRC INTEGRATED INSPECTION

REPORT AND NOTICE OF VIOLATION 05000483/2008003

Dear Mr. Heflin:

On June 24, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Callaway Plant. The enclosed report documents the inspection results, which

were discussed on June 24, 2008, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, one violation is cited in the enclosed Notice of

Violation (Notice) and the circumstances surrounding this violation are described in detail in the

enclosed report. The violation involved failure to implement corrective actions to preclude the

repetition of void formation in the emergency core cooling piping (EA-08-190). Although

determined to be of very low safety significance (Green), this violation is being cited because

one of the criteria specified in Section VI.A.1 of the NRC Enforcement Policy for a noncited

violation was satisfied. Specifically, AmerenUE failed to restore compliance within a reasonable

time after the violation was last identified in NRC Inspection Report 05000483/2006002-012.

Please note that you are required to respond to this letter and should follow the instructions

specified in the enclosed Notice when preparing your response. The NRC will use your

response, in part, to determine whether further enforcement action is necessary to ensure

compliance with regulatory requirements.

This report also documents four NRC-identified and self-revealing findings of very low safety

significance (Green). These findings were determined to involve violations of NRC

requirements. Additionally, two licensee-identified violations which were determined to be of

very low safety significance are listed in this report. However, because of the very low safety

significance and because they were entered into your corrective action program, the NRC is

treating these findings as NCVs consistent with Section VI.A of the NRC Enforcement Policy. If

you contest these NCVs, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

Union Electric Company -2-

ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional

Administrator, U.S. Nuclear Regulatory Commission Region IV, 612 East Lamar Drive,

Suite 400, Arlington, Texas 76011-4125; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at the

Callaway Plant.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its

enclosures will be made available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records component of NRCs document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA/

Vincent G. Gaddy, Chief,

Projects Branch B

Division of Reactor Projects

Docket: 50-483

License: NPF-30

Enclosures: Notice of Violation and

NRC Inspection Report 05000483/2008003

w/attachment: Supplemental Information

cc w/enclosure: Rick A. Muench, President and

John ONeill, Esq. Chief Executive Officer

Pillsbury Winthrop Shaw Pittman LLP Wolf Creek Nuclear Operating Corporation

2300 N. Street, N.W. P.O. Box 411

Washington, DC 20037 Burlington, KS 66839

Scott A. Maglio, Assistant Manager Kathleen Smith, Executive Director and

Regulatory Affairs Kay Drey, Representative Board of

AmerenUE Directors

P.O. Box 620 Missouri Coalition for the Environment

Fulton, MO 65251 6267 Delmar Boulevard, Suite 2E

St. Louis City, MO 63130

Missouri Public Service Commission

Governors Office Building Lee Fritz, Presiding Commissioner

200 Madison Street Callaway County Courthouse

P.O. Box 360 10 East Fifth Street

Jefferson City, MO 65102-0360 Fulton, MO 65251

H. Floyd Gilzow Les H. Kanuckel, Manager

Deputy Director for Policy Quality Assurance

Missouri Department of Natural Resources AmerenUE

P. O. Box 176 P.O. Box 620

Jefferson City, MO 65102-0176 Fulton, MO 65251

Union Electric Company -3-

Director, Missouri State Emergency Certrec Corporation

Management Agency 4200 South Hulen, Suite 422

P.O. Box 116 Fort Worth, TX 76109

Jefferson City, MO 65102-0116

Keith G. Henke, Planner III

Scott Clardy, Director Division of Community and Public Health

Section for Environmental Public Health Office of Emergency Coordination

Missouri Department of Health and Missouri Department of Health and

Senior Services Senior Services

P.O. Box 570 930 Wildwood,

Jefferson City, MO 65102-0570 P.O. Box 570

Jefferson City, MO 65102

Luke H. Graessle, Manager

Regulatory Affairs Technical Services Branch Chief

AmerenUE FEMA Region VII

P.O. Box 620 2323 Grand Boulevard, Suite 900

Fulton, MO 65251 Kansas City, MO 64108-2670

Thomas B. Elwood, Supervising Engineer Ronald L. McCabe, Chief

Regulatory Affairs and Licensing Technological Hazards Branch

AmerenUE National Preparedness Division

P.O. Box 620 DHS/FEMA

Fulton, MO 65251 9221 Ward Parkway, Suite 300

Kansas City, MO 64114-3372

Union Electric Company -4-

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

DRP Director (Dwight.Chamberlain@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

DRS Deputy Director (Troy.Pruett@nrc.gov)

Senior Resident Inspector (David.Dumbacher@nrc.gov)

Branch Chief, DRP/B (Vincent.Gaddy@nrc.gov)

Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)

Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Only inspection reports to the following:

DRS STA (Dale.Powers@nrc.gov)

M. Cox, OEDO RIV Coordinator (Mark.Cox@nrc.gov)

OEMail.Resource@nrc.gov

Enforcement Officer (Michael.Vasquez@nrc.gov)

Chief Allegation Coordination/Enforcement Staff (William.Jones@nrc.gov)

Office of Enforcement (Alexander.Sapountizis@nrc.gov)

ROPreports

CWY Site Secretary (Dawn.Yancey@nrc.gov)

SUNSI Review Completed: VGG ADAMS: ; Yes No Initials: __VGG__

Publicly Available Non-Publicly Available Sensitive ;Non-Sensitive

R:\_Reactors\_CW\2008\CW 2008003RP-DED.doc ML 082180851

RIV:SRI:DRP/B C:DRS/OB C:DRS/PSB1 C:DRS/EB2 C:DRS/EB1

DDumbacher RELantz MPShannon NFO'Keefe RLBywater

/RA/ VGGaddy for /RA/ /RA/ /RA/ MFRunyan for /RA/

07/29/2008 07/9/2008 07/14/2008 07/15/2008 07/11/2008

C:DRS/PSB2 DRS/SRA ACES C:DRP/B D:DRP

GEWerner DPLoveless GMVasquez VGGaddy DDChamberlain

/RA/ /RA/ /RA/ /RA/ /RA/

07/17/2008 07/15/2008 07/24/2008 08/5/2008 07/28/2008

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

NOTICE OF VIOLATION

AmerenUE Docket 50-483

Callaway Plant License NPF-30

EA-08-190

During an NRC inspection conducted March 24 through June 24, 2008, a violation of NRC

requirements was identified. In accordance with the NRC Enforcement Policy, the violation is

listed below:

10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that

measures shall be established to ensure that, for significant conditions adverse to

quality, the cause of the condition is determined and corrective action taken to preclude

repetition.

Contrary to this, from December 26, 2006, through May 21, 2008, the licensee failed to

take corrective actions to preclude repetition of safety-related emergency core cooling

system pipe voiding, and the licensee determined that this condition was a significant

condition adverse to quality.

This violation is associated with a Green Significance Determination Process finding.

Pursuant to the provisions of 10 CFR 2.201, AmerenUE is hereby required to submit a written

statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document

Control Desk, Washington, DC 20555 with a copy to the Regional Administrator, Region IV,

and a copy to the NRC Senior Resident Inspector at the facility that is the subject of this Notice

of Violation (Notice), within 30 days of the date of the letter transmitting this Notice. This reply

should be clearly marked as a "Reply to Notice of Violation EA-08-190," and should include:

(1) the reason for the violation, or, if contested, the basis for disputing the violation or severity

level, (2) the corrective steps that have been taken and the results achieved, (3) the corrective

steps that will be taken to avoid further violations, and (4) the date when full compliance will be

achieved. Your response may reference or include previous docketed correspondence, if the

correspondence adequately addresses the required response. If an adequate reply is not

received within the time specified in this Notice, an order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or why such other

action as may be proper should not be taken. Where good cause is shown, consideration will

be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), accessible from the

NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not

include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. If personal privacy or proprietary information is

necessary to provide an acceptable response, then please provide a bracketed copy of your

response that identifies the information that should be protected and a redacted copy of your

response that deletes such information. If you request withholding of such material, you must

specifically identify the portions of your response that you seek to have withheld and provide in

-1- Enclosure 1

detail the bases for your claim of withholding (e.g., explain why the disclosure of information will

create an unwarranted invasion of personal privacy or provide the information required by

10 CFR 2.390(b) to support a request for withholding confidential commercial or financial

information). If safeguards information is necessary to provide an acceptable response, please

provide the level of protection described in 10 CFR 73.21.

Dated this 5th day of July 2008

-2- Enclosure 1

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-483

License: NPF-30

Report: 05000483/2008003

Licensee: Union Electric Company

Facility: Callaway Plant

Location: Junction Highway CC and Highway O

Fulton, MO

Dates: March 25 - June 24, 2008

Inspectors: D. Dumbacher, Senior Resident Inspector

J. Groom, Resident Inspector

J. Drake, Senior Reactor Inspector, Plant Support, Branch 2

G. Guerra, CHP, Health Physicist, Plant Support Branch 1

Approved By: V. Gaddy, Chief, Project Branch B

Division of Reactor Projects

-1- Enclosure 2

SUMMARY OF FINDINGS

IR 05000483/2008003: 3/25 - 6/24/2008; Callaway Plant, Operability Evaluations,

Postmaintenance Testing, Surveillance Testing, and Identification and Resolution of Problems.

This report covered a 3-month period of inspection by resident inspectors. The significance of

most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual

Chapter 0609, "Significance Determination Process." Findings for which the Significance

Determination Process does not apply may be Green or assigned a severity level after NRC

management review. The NRCs program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,

dated December 2006.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a noncited violation of Technical

Specification 3.5.2, "Emergency Core Cooling Systems," after an inadequate

surveillance procedure resulted in the licensee failing to maintain the emergency

core cooling system full of water as required per Technical Specification 3.5.2.

On May 21, 2008, Callaway Plant engineering discovered that a section of the

cold leg recirculation piping, specifically the discharge of the residual heat

removal pumps to the safety injection pumps, contained 6.6 cubic feet of air.

Callaway monthly surveillance Procedure OSP-SA-00003, "Emergency Core

Cooling Flow Path Verification and Venting," had a purpose to: "Verify the ECCS

is full of water," in accordance with Technical Specification Surveillance

Requirement 3.5.2.3. The monthly verification and vent procedure was not

comprehensive enough to ensure all the emergency core cooling system was full

of water.

This finding was more than minor because it was similar to Example 3e of NRC

Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues," and

met the Not Minor If, criteria because the failure to meet the licensees

administrative requirement for allowable void fraction impacted the ability of the

Train A safety injection system to function upon initiation of high-pressure

recirculation. This finding affected the mitigating systems cornerstone procedure

quality attribute. Using the Manual Chapter 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, the inspectors determined that this finding

should be evaluated using the Phase 2 process described in Manual

Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection

Findings for At-Power Situations. As described in Section III, of Appendix A,

given that the presolved table did not contain a suitable target or surrogate for

this finding, the senior reactor analyst used the risk-informed notebook to

evaluate the significance of this finding affecting only high-pressure recirculation

as very low risk significance (Green). This finding has a crosscutting aspect in

the area of human performance associated with the decision making component

because the licensee failed to use conservative assumptions in decision making

and did not adopt a requirement to demonstrate that a single vent valve was

sufficient to vent the affected line rather than assuming that an additional

-2- Enclosure 2

installed valve was not necessary to completely fill, vent, and test the line H.1(b)

(Section 1R15).

Criterion XVI, "Corrective Action," was identified after the licensee failed to

promptly correct leakage from diesel generator jacket water o-rings. On

February 20, 2008, during a normal surveillance run of Emergency Diesel

Generator B, Callaway operations personnel identified an approximately

80 drop-per-minute jacket water leak caused by premature failure of Nitrile type

o-rings. Following restoration of Emergency Diesel Generator B, the licensee

re-evaluated the preventative maintenance frequency for jacket water o-ring

replacement and reduced the replacement frequency from once every 3 years to

once every refueling cycle. Then, on May 28, 2008, during a routine surveillance

run of Emergency Diesel Generator A, Callaway operations personnel identified

that Emergency Diesel Generator A had a 200 drop-per-minute jacket water leak.

Similar to the condition observed on Emergency Diesel Generator B on

February 20, 2008, the source of the leakage was from Nitrile type o-rings within

the jacket water system. The o-rings responsible for jacket water leakage were

found to be of similar age to those that failed during the February 20, 2008,

surveillance but had not been replaced despite the change to the licensee's

preventive maintenance frequency.

This finding, failure to implement adequate corrective actions for degraded Nitrile

type o-rings in Emergency Diesel Generator A after previously identifying the

adverse condition on Emergency Diesel Generator B, was more than minor

because, if left uncorrected, degraded diesel generator jacket water o-rings could

become a more significant safety concern. This finding affected the mitigating

systems cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial

Screening and Characterization of Findings, this finding was determined to be of

very low safety significance because it was a design deficiency confirmed not to

result in loss of operability. This finding has a crosscutting aspect in the area of

human performance associated with the work controls component because the

licensee failed to plan work activities to support long-term equipment reliability by

addressing known degraded conditions in a more reactive than preventative

manner H.3(b) (Section 1R19).

Criterion XVI, "Corrective Action," because the licensee failed to take corrective

actions to preclude repetition of void formation in emergency core cooling system

piping, a significant condition adverse to quality. After experiencing void

formations in 2005 and 2006, the NRC identified violations of Criterion XVI.

However, licensee corrective actions did not preclude repetition of void

formations that were discovered on May 21, 2008. On that date, Callaway Plant

engineering performed ultrasonic inspection of the safety injection system

common suction piping Line EM023-HCB - 6" and discovered a 6.6 cubic foot

voided area. This exceeded the allowable void fraction of 2.1 cubic feet required

for operability. This voided piping, determined to have existed for over a year,

was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The

maintenance restoration failed to perform an adequate fill and vent to ensure the

suction pipe was full of water. The inspectors identified several related examples

where the licensee had performed either inadequate operating experience

-3- Enclosure 2

evaluations, inadequate extent of condition reviews, or inadequate procedure

corrections. The violation is being cited in a Notice of Violation because the

licensee failed to restore compliance with a reasonable time after a violation was

last identified in 2006.

This finding, failure to restore compliance to prevent recurrence of emergency

core cooling system voids, was more than minor because it is similar to

Example 3e of NRC Inspection Manual Chapter 0612, Appendix E, "Examples of

Minor Issues," criteria because the failure impacted the ability of the emergency

core cooling system to function upon initiation of high-pressure recirculation.

Using the Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, the inspectors determined that this finding should

be evaluated using the Phase 2 process described in Manual Chapter 0609,

Appendix A, Determining the Significance of Reactor Inspection Findings for

At-Power Situations. As described in Section III, of Appendix A, given that the

presolved table did not contain a suitable target or surrogate for this finding, the

senior reactor analyst used the risk-informed notebook to evaluate the

significance of this finding as very low risk significance (Green). This finding has

a crosscutting aspect in the area of problem identification and resolution

associated with the corrective action program component because AmerenUE

failed to thoroughly evaluate voiding problems such that the resolutions

addressed causes and extent of condition, as necessary P.1(c) (Section 4OA2).

Cornerstone: Barrier Integrity

Criterion III, Design Control, was identified after determining that the licensee

had not adequately selected and reviewed the suitability of the design of the

containment air cooler control circuitry. On March 26, 2008, Containment Air

Cooler A fan shut down when shifted from fast to slow speed. Troubleshooting

by the licensee determined that voltage was lost to the control power circuitry

when the fast speed thermal overload tripped. Since the overload contacts were

wired in series, Containment Air Cooler A experienced a complete loss of control

power rendering it inoperable. The licensee determined the trip to be caused by

operation of containment air coolers in fast speed, during a period of higher than

normal containment pressure. The licensee analyzed the potential impact of the

newly discovered adverse containment cooler design vulnerability against design

basis accident scenarios. The licensee determined that a hot zero power main

steam line break results in a delayed safety injection signal allowing the fan

motor overloads to trip prior to being shed by the load sequencer. The

containment air coolers would then experience a complete loss of control power

and would not be capable of automatically restarting in slow speed. The analysis

revealed that the peak containment pressure limit of 48.1 psig would be

preserved. The licensee submitted a licensee event report as required by

10 CFR 50.73 since the inadequate containment air cooler control circuitry

resulted in a condition prohibited by the plants Technical Specifications.

This finding, failure to ensure the design of the containment air cooler control

circuitry was suitable for all plant conditions, was more than minor because it was

associated with the barrier integrity cornerstone attribute of design control and

affects the associated cornerstone objective to provide reasonable assurance

-4- Enclosure 2

that physical design barriers protect the public from radio nuclide releases

caused by accidents or releases. Using Manual Chapter 0609, Appendix H,

Containment Integrity Significance Determination Process," this finding was

determined to be a Type B finding since it was related to a degraded condition

that has potentially important implications for the integrity of the containment,

without affecting the likelihood of core damage. This finding was found to be of

very low safety significance because containment coolers are structures,

systems or components that are not significant contributors to the large early

release frequency. The inspectors determined that this finding does not have a

crosscutting aspect associated with it since the performance deficiency was not

indicative of current licensee performance (Section 1R15).

  • Green. The inspectors identified a noncited violation of Technical

Specification 5.4.1.a, Procedures, after Callaway control room operators

improperly entered a wrong Technical Specification action statement due to the

failure to maintain the Technical Specification Bases current. On June 17, 2008,

during surveillance testing, Valve EMHV8823 failed to indicate fully closed.

Since EMHV8823 is an isolation valve for containment Penetration 49, the

licensee entered Technical Specification 3.6.3, Containment Isolation Valves,

Condition C, with an action to restore the valve to an operable status or isolate

the penetration within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> after Valve EMHV8823

had been declared inoperable, Callaway licensing personnel contacted the

control room and informed them of an approved Technical Specification Bases

change that did not allow Technical Specification 3.6.3, Condition C, to be

applicable to containment Penetration 49. The Technical Specification Bases

change was effective May 1, 2008, but had not been issued to the control room.

The licensee determined that the more restrictive Technical Specification 3.6.3,

Condition A, should have been entered with an action to isolate the affected

penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. The licensee performed a containment entry

following discovery of entry into Technical Specification 3.6.3, Condition A, and

found that Valve EMHV8823 failed its surveillance due to out of adjustment

position indicator limit switches. The valve was verified closed and isolated

allowing exit from Technical Specification 3.6.3, Condition A.

This finding, failure to ensure the Technical Specification Bases were maintained

current and available to the Callaway control room staff, was more than minor

because if left uncorrected, the failure to maintain the Technical Specification

Bases current could become a more significant safety concern. This finding was

determined to affect the barrier integrity cornerstone. Using Manual

Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,

this finding is determined to be of very low safety significance since this finding

did not represent an actual open pathway in the physical integrity of reactor

containment and did not involve an actual reduction in function of hydrogen

ignitors in the reactor containment. This finding has a crosscutting aspect in the

area of human performance associated with the decision making component

because the licensee failed to communicate, in a timely manner, decisions to

personnel who have a need to know the information in order to perform work

safely H.1(c) (Section 1R22).

-5- Enclosure 2

B. Licensee-Identified Violations

Two violations of very low safety significance, which were identified by the licensee,

have been reviewed by the inspectors. Corrective actions taken or planned by the

licensee have been entered into the licensees corrective action program. These

violations and corrective action tracking numbers are listed in Section 4OA7.

-6- Enclosure 2

REPORT DETAILS

Summary of Plant Status

AmerenUE operated the Callaway Plant at near 100 percent for the entire quarter.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1 Readiness of Offsite and Alternate AC Power System

a. Inspection Scope

The inspectors reviewed the licensees plant features, training lesson plans, and

procedures for operation and continued availability of offsite and alternate AC power

systems to verify they were appropriate. The review included communication protocols

and agreement procedures between the transmission system operator and the nuclear

power plant to verify that appropriate information is exchanged when issues arise that

could impact the offsite power system. Specifically, the procedures were verified to

ensure they specified:

  • Required actions needed when notified by the transmission system operator that

posttrip voltage of the offsite power system would not be acceptable to assure

the continued operation of safety related loads without transferring to the onsite

power supply.

  • Compensatory actions needed when it is not possible to predict the posttrip

voltage at the nuclear power plant for current grid conditions.

  • Required assessment of plant risk based on maintenance activities which could

affect grid reliability, or the ability of the transmission system to provide the offsite

power system.

  • Required communications between the nuclear power plant and the transmission

system operator when changes at the nuclear power plant could impact the

transmission system, or when the capability of the transmission system to

provide adequate offsite system power is challenged.

On May 16, 2008, the inspectors evaluated the licensee staffs preparations for summer

readiness of offsite and AC power systems against the sites procedures and determined

that the staffs actions were adequate. Documents reviewed are listed in the

attachment.

These activities constituted one readiness of offsite power inspection sample as defined

by Inspection Procedure 71111.01.

-7- Enclosure 2

b. Findings

No findings of significance were identified.

.2 Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

On May 2, 2008, the inspectors completed a review of the licensee's readiness for

impending adverse weather involving severe thunderstorms. The inspectors:

(1) reviewed plant procedures, the Final Safety Analysis Report (FSAR), and Technical

Specifications to ensure that operator actions defined in adverse weather procedures

maintained the readiness of essential systems; (2) walked down portions of the

emergency diesel generators and offsite power systems to ensure that adverse weather

protection features were sufficient to support operability; (3) reviewed maintenance

records to determine that applicable surveillance requirements were current before the

anticipated severe thunderstorms developed; and (4) reviewed plant modifications,

procedure revisions, and operator work arounds to determine if recent facility changes

challenged plant operation. Documents reviewed by the inspectors are listed in the

attachment.

These activities constituted one readiness for impending adverse weather inspection

sample as defined by Inspection Procedure 71111.01.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignments (71111.04)

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

auxiliary feedwater pump was out of service for planned maintenance.

  • June 10, 2008, Train A 480 volt NG Class 1E switchgear while the Train B

emergency diesel generator was out of service for planned and emergent

maintenance issues.

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, FSAR, Technical Specification requirements, outstanding work orders,

corrective action documents, and the impact of ongoing work activities on redundant

trains of equipment in order to identify conditions that could have rendered the systems

-8- Enclosure 2

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify components and support equipment were

aligned correctly and were operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the

corrective action program with the appropriate significance characterization. Documents

reviewed are listed in the attachment.

These activities constituted two partial system walkdown samples as defined by

Inspection Procedure 71111.04.

b. Findings

No findings of significance were identified.

.2 Complete System Walkdown (71111.04S)

a. Inspection Scope

On April 17, 2008, the inspectors performed a complete system alignment inspection of

Train B of the residual heat removal system to verify the functional capability of the

system. The inspectors selected this system because it was considered both

safety-significant and risk-significant in the licensees probabilistic risk assessment. The

inspectors walked down the system to review mechanical and electrical equipment line

ups, electrical power availability, system pressure and temperature indications, as

appropriate, component labeling, component lubrication, component and equipment

cooling, hangers and supports, operability of support systems, and to ensure that

ancillary equipment or debris did not interfere with equipment operation. The inspectors

reviewed a sample of past and outstanding work orders to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the corrective action program database to ensure that system equipment

alignment problems were being identified and appropriately resolved. The documents

used for the walkdown and issue review are listed in the attachment.

These activities constituted one complete system walkdown sample as defined by

Inspection Procedure 71111.04.

b. Findings

No findings of significance were identified.

-9- Enclosure 2

1R05 Fire Protection (71111.05)

.1 Quarterly Fire Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • March 27, 2008, Fire Area C-21, Lower Cable Spreading Room
  • April 16, 2008, Fire Area A-17, Electrical Penetration Room (South)
  • April 25, 2008, Condensate Storage Tank

Enclosure

  • April 30, 2008, Reactor Building
  • June 18, 2008, Fire Area A-1, North Pipe Chase

The inspectors reviewed areas to assess if the licensee implemented a fire protection

program that adequately controlled combustibles and ignition sources within the plant,

effectively maintained fire detection and suppression capability, maintained passive fire

protection features in good material condition, and implemented adequate compensatory

measures for out of service, degraded or inoperable fire protection equipment, systems,

or features in accordance with the licensees fire plan. The inspectors selected fire

areas based on their overall contribution to internal fire risk as documented in the plants

Individual Plant Examination of External Events with later additional insights, their

potential to impact equipment which could initiate or mitigate a plant transient, or their

impact on the plants ability to respond to a security event. The inspectors verified that

fire hoses and extinguishers were in their designated locations and available for

immediate use; that fire detectors and sprinklers were unobstructed, that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. Documents reviewed are listed in the

attachment.

These activities constituted six quarterly fire protection inspection samples as defined by

Inspection Procedure 71111.05.

b. Findings

No findings of significance were identified.

.2 Annual Fire Protection Drill Observation (71111.05A)

a. Inspection Scope

On March 27, 2008, the inspectors observed a fire brigade activation due to a report of

smoke in the laundry decontamination area. The observation evaluated the readiness of

- 10 - Enclosure 2

the plant fire brigade to fight fires. The inspectors verified that the licensee staff

identified deficiencies; openly discussed them in a self-critical manner at the drill debrief,

and took appropriate corrective actions. Specific attributes evaluated were: (1) proper

wearing of turnout gear and self-contained breathing apparatus; (2) proper use and

layout of fire hoses; (3) employment of appropriate fire fighting techniques; (4) sufficient

firefighting equipment brought to the scene; (5) effectiveness of fire brigade leader

communications, command, and control; (6) search for victims and propagation of the

fire into other plant areas; (7) smoke removal operations; (8) utilization of preplanned

strategies; (9) adherence to the preplanned drill scenario; and (10) drill objectives.

Documents reviewed are listed in the attachment.

These activities constituted one annual fire protection inspection sample as defined by

Inspection Procedure 71111.05.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures (71111.06)

Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk-significant plant design features and licensee

procedures intended to protect the plant and its safety related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the FSAR, engineering calculations, and abnormal operating procedures for

licensee commitments. The inspectors reviewed licensee drawings to identify areas and

equipment that may be affected by internal flooding caused by the failure or

misalignment of nearby sources of water. The inspectors also reviewed the licensees

corrective actions for previously identified flood-related items. The inspectors performed

a walkdown of the following plant area to assess the adequacy of any watertight doors

and verify drains and sumps were clear of debris and operable, and that the licensee

complied with its flooding related commitments:

  • June 23, 2008, Control Building West Corridor

The document reviewed during this inspection is listed as follows:

  • Callaway Action Request 200805189

This inspection constituted one internal flooding sample as defined in Inspection

Procedure 71111.06.

b. Findings

No findings of significance were identified.

- 11 - Enclosure 2

1R11 Licensed Operator Requalification Program (71111.11)

a. Inspection Scope

On June 2, 2008, the inspectors observed a crew of licensed operators perform a

Cycle 08-3 as found scenario in the plants simulator to verify that operator performance

was adequate, evaluators were identifying and documenting crew performance

problems, and that training was being conducted in accordance with licensee

procedures. The scenario involved an operating design basis earthquake with a lockout

on essential 4 kV Bus NB01. The inspectors evaluated the crew in the following areas:

  • Licensed operator performance
  • Crew clarity and formality of communications
  • Ability to take timely actions in the conservative direction
  • Prioritization, interpretation, and verification of annunciator alarms
  • Correct use and implementation of abnormal and emergency procedures
  • Control board manipulations
  • Oversight and direction from supervisors
  • Ability to identify and implement appropriate Technical Specification actions and

Emergency Plan actions and notifications

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the attachment.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

  • May 15, 2008, Callaway Action Request (CAR) 200801644, an additional anode

was found in the north end of the Train A emergency diesel generator intercooler

engine oil sump high

- 12 - Enclosure 2

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of risk-important systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • Implementing appropriate work practices
  • Identifying and addressing common cause failures
  • Scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule
  • Characterizing system reliability issues for performance
  • Charging unavailability time
  • Trending key parameters for condition monitoring
  • Verifying appropriate performance criteria for structures, systems, and

components/functions classified as (a)(2) or appropriate and adequate goals and

corrective actions for systems classified as (a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. The inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Documents reviewed are listed in the attachment.

This inspection constituted two quarterly maintenance effectiveness samples as defined

in Inspection Procedure 71111.12Q.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

Valve KAPCV-0102

  • April 28, 2008, Routine - associated with Loose Creek-Callaway 345 kV line

outage

- 13 - Enclosure 2

  • June 10, 2008, Risk management actions associated with Emergency Diesel

Generator B jacket water o-ring replacement outage

These activities were selected based on their potential risk significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed Technical

Specification requirements and walked down portions of redundant safety systems,

when applicable, to verify risk analysis assumptions were valid and applicable

requirements were met. Documents reviewed are listed in the attachment.

These activities constituted four samples as defined by Inspection Procedure 71111.13.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

  • March 26, 2008, CARs 200802348, 200802365, and 200802264, Containment

coolers inoperable in fast speed

  • April 4, 2008, CARs 200800461 and 200802625, Containment recirculation sump

operability determination, Revisions 3 and 4

  • April 9, 2008, Source Range Channel N32 inoperable due to a failed surveillance
  • April 23, 2008, Component cooling water system following Valve EGHV0069

failing inservice test stroke time surveillance

expansion joints

piping from sump

  • May 22, 2008, CAR 200904000, Line EM-023 allowable void fraction exceeded

The inspectors selected potential operability issues based on the risk significance of the

associated components and systems. The inspectors evaluated the technical adequacy

of the evaluations to ensure that Technical Specification operability was properly justified

and the subject component or system remained available such that no unrecognized

increase in risk occurred. The inspectors compared the operability and design criteria in

the appropriate sections of the Technical Specifications and FSAR to the licensees

- 14 - Enclosure 2

evaluations to determine whether the components or systems were operable. Where

compensatory measures were required to maintain operability, the inspectors

determined whether the measures in place would function as intended and were

properly controlled. The inspectors determined, where appropriate, compliance with

bounding limitations associated with the evaluations. Additionally, the inspectors

reviewed a sample of corrective action documents to verify that the licensee was

identifying and correcting deficiencies associated with operability evaluations.

Documents reviewed are listed in the attachment.

This inspection constituted seven samples as defined in Inspection Procedure 71111.15.

b. Findings

.1 Introduction. A self-revealing Green noncited violation (NCV) of 10 CFR Part 50,

Appendix B, Criterion III, Design Control, was identified after determining that the

licensee had not adequately selected and reviewed the suitability of the design of the

containment air cooler control circuitry.

Description. On March 26, 2008, Containment Air Cooler A fan shut down when shifted

from fast to slow speed. Troubleshooting by the licensee determined that voltage was

lost to the control power circuitry when the fast speed thermal overload tripped. Since

the overload contacts were wired in series, Containment Air Cooler A experienced a

complete loss of control power rendering it inoperable. AmerenUE personnel noted that

Precaution 3.6 of Procedure OTN-GN-00001, Containment Cooling and CRDM

Cooling, Revision 14, cautioned that high pressure and cool temperatures across

containment coolers will cause the coolers to operate close to the setpoint of the thermal

overloads. However, the licensees operability determination dismissed the 1987

precaution as not having a technical basis believing it was implemented to address

discrepancies in motor overload setpoints. Later, the licensee determined that operation

of containment air coolers in fast speed, during a period of higher than normal

containment pressure, challenged the fast speed thermal overload setpoint and resulted

in the trip of Containment Air Cooler A on March 26, 2008. As an interim measure to

prevent a trip from fast speed, the licensee imposed a standing order to maintain the

containment coolers in slow speed.

The licensee analyzed the potential impact of the newly discovered adverse containment

cooler design vulnerability against design basis accident scenarios. The licensee

determined that a hot zero power main steam line break results in a delayed safety

injection signal allowing the fan motor overloads to trip prior to being shed by the load

sequencer. The containment air coolers would then experience a complete loss of

control power and would not be capable of automatically restarting in slow speed. The

analysis revealed that in this scenario, utilizing assumed accident conditions, the peak

containment pressure would exceed the 48.1 psig limit described in the FSAR.

However, analysis using actual plant conditions determined that the peak containment

pressure limit of 48.1 psig would be preserved. The licensee submitted a licensee event

report (LER) as required by 10 CFR 50.73 since the inadequate containment air cooler

control circuitry resulted in a condition prohibited by the plants Technical Specifications.

The inspectors review of the licensees LER is described in Section 4OA3 of this report.

To address the design deficiency associated with the containment air cooler control

circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit

- 15 - Enclosure 2

such that tripping of the fast speed overloads would not impact the safety-related slow

speed function of the containment air coolers.

Analysis. The performance deficiency associated with this finding involved the

licensees failure to ensure the design of the containment air cooler control circuitry was

suitable for all plant conditions. This finding was greater than minor because it was

associated with the barrier integrity cornerstone attribute of design control and affects

the associated cornerstone objective to provide reasonable assurance that physical

design barriers protect the public from radio nuclide releases caused by accidents or

releases. Using Manual Chapter 0609, Appendix H, Containment Integrity Significance

Determination Process," this finding was determined to be a Type B finding since it was

related to a degraded condition that has potentially important implications for the integrity

of the containment, without affecting the likelihood of core damage. This finding was

found to be of very low safety significance since containment coolers are structures,

systems, and components that have no impact on large early release frequency. The

inspectors determined that this finding does not have a crosscutting aspect associated

with it since the performance deficiency is not indicative of current licensee performance.

Enforcement. 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in

part, that measures be established for the selection and review for suitability of

application of materials, parts, equipment, and processes that are essential to the

safety-related functions of structures, systems, and components. Contrary to the above,

prior to April 2, 2008, the licensee failed to ensure that the containment air coolers would

be able to perform their safety-related function in all accident scenarios due to a design

deficiency associated with the overload contacts in the containment air cooler control

circuitry. Because this finding is of very low safety significance and has been entered

into the corrective action program as CAR 200702264, this violation is being treated as

an NCV consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000483/2008003-01, Failure to Ensure the Suitability of the Design of the

Containment Air Cooler Control Circuitry.

.2 Introduction. The inspectors identified a Green NCV of Technical Specification 3.5.2,

"Emergency Core Cooling Systems," after an inadequate surveillance procedure

resulted in the licensee failing to maintain the emergency core cooling system (ECCS)

full of water as required per Technical Specification 3.5.2.

Description. On May 21, 2008, Callaway Plant engineering discovered that a section of

the cold leg recirculation piping, specifically the discharge of the residual heat removal

pumps to the safety injection pumps, contained 6.6 cubic feet of air. This exceeded the

allowable void fraction of 2.1 cubic feet required for operability. Callaway monthly

surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow Path

Verification and Venting," had a purpose to: "Verify the ECCS is full of water," in

accordance with Technical Specification Surveillance Requirement 3.5.2.3. This

monthly surveillance was reviewed as part of significant condition adverse to quality

(SCAQ) CAR 200501092 corrective actions. Callaway engineering had determined that

residual heat removal pump discharge vent Valve EJV0193 to the safety injection

system was the high point vent for these lines and was thus sufficient to vent

Line EM-023-HCB - 6" to the safety injection pumps. However, this vent valve was not

adequate due to the pipe sloping issues and normally closed Valves EMHIS8807A/B.

Venting through Valve EMV0179 was necessary to completely fill, vent, and test the line.

The monthly verification and vent procedure was inadequate to identify and remove air

- 16 - Enclosure 2

introduced by relief valve maintenance on May 7, 2007, and thus ensure the ECCS was

full of water. See Violation (VIO)05000483/2008003-05 in Section 4OA2.

Analysis. Failure to adequately verify ECCS piping was full of water as required by

Technical Specification 3.5.2 is a performance deficiency. This finding affected the

mitigating system cornerstone procedure quality attribute. This finding is more than

minor because it was similar to Example 3e of NRC Inspection Manual Chapter 0612,

Appendix EProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0612,</br></br>Appendix E" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., "Examples of Minor Issues," and met the Not Minor If, criteria because the

failure to meet the licensees administrative requirement for allowable void fraction

impacted the ability of the Train A safety injection system to function upon initiation of

high-pressure recirculation. Using Manual Chapter 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, the inspectors determined that this finding should be

evaluated using the Phase 2 process described in Manual Chapter 0609, Appendix A,

Determining the Significance of Reactor Inspection Findings for At-Power Situations.

As described in Section III of Appendix A, given that the presolved table did not contain

a suitable target or surrogate for this finding, the senior reactor analyst used the

risk-informed notebook to evaluate the significance of this finding. Table 2 provides the

definitions for acronyms and initialisms used in the risk-informed notebook and

discussed in this inspection report.

TABLE 2

Acronyms and Initialisms used in Phase 2 Notebook

Initialism Initiating Event or Mitigating Function

TPCS Transient with Loss of the Power Conversion System

SLOCA Small-Break Loss of Coolant Accident

MLOCA Medium-Break Loss of Coolant Accident

LLOCA Large-Break Loss of Coolant Accident

LOOP Loss of Offsite Power

MSLB Main Steam Line Break

LBDC Loss of Vital Direct-Current Bus

AFW Auxiliary Feedwater

PCS Power Conversion System (Steam and Feed)

HPR High Pressure Recirculation

DEPR Depressurization of the Reactor Coolant System

EAC Emergency Power (Alternating Current)

TDAFW Turbine-Driven Auxiliary Feedwater Pump Train

SEAL Reactor Coolant Pump Seal Integrity

STIN Operators Stop High-Pressure Injection

MDAFW Motor-Driven Auxiliary Feedwater Pump Train

The analyst performed a Phase 2 estimation in accordance with Inspection Manual

Chapter 0609, Appendix A, Attachment 2, Site Specific Risk-Informed Inspection

Notebook Usage Rules. Given that the performance deficiency was known to have

existed for 378 days (May 7, 2007, until May 21, 2008) the analyst used 1 year as the

exposure period. In accordance with Table 2 of the risk-informed notebook, the analyst

evaluated all worksheets except LLOCA. All worksheets were evaluated using the

nominal 1-year initiating event frequency. Because this finding only affected system

functionality during recirculation, nominal mitigation credit was given for all functions with

the exception of HPR. For HPR, the analyst made the bounding assumption that either

- 17 - Enclosure 2

both centrifugal charging pumps or both safety injection pumps would be affected. This

assumption was supported by licensee evaluation. The analyst solved each applicable

worksheet and the dominant sequences are documented in Table 1.

TABLE 1

Phase 2 Dominant Sequences

Initiating Event Sequence Mitigating Functions Results

Number

Transients 1 AFW-PCS-HPR 9

TPCS 1 AFW-HPR 8

SLOCA 2 DEPR-HPR 8

MLOCA 2 DEPR-HPR 9

1 AFW-HPR 9

LOOP 5 EAC-TDAFW-HPR 9

9 EAC-SEAL-HPR 9

MSLB 8 STIN-HPR 8

LBDC 8 TDAFW-MDAFW-HPR 8

Using Inspection Manual Chapter 0609, Appendix A, Attachment 1, Table 5, Counting

Rule Worksheet, the analyst determined that the risk contribution of this finding from

internal initiating events was of very low risk significance. In accordance with

Appendix A, Attachment 1, Steps 2.2.5 and 2.2.6, the analyst and determined that the

risk contribution of this finding from external initiating events or the contribution from

large-early release frequency were very low. Therefore, this finding was of very low risk

significance (Green). This finding has a crosscutting aspect in the area of human

performance associated with the decision making component because the licensee

failed to use conservative assumptions in decision making and did not adopt a

requirement to demonstrate that the single vent Valve EJV0193 was sufficient to vent

the Line EM-023-HCB - 6" rather than assuming that installed Valve EMV0179 was not

necessary to completely fill, vent, and test the line H.1(b).

Enforcement. Technical Specification 3.5.2 "Emergency Core Cooling Systems,"

Surveillance Requirement 3.5.2.3, required that the licensee verify that ECCS piping is

full of water every 31 days. Contrary to the above, from June 2007 through April 2008,

AmerenUE surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow

Path Verification and Venting," was inadequate to meet Technical Specification

Surveillance Requirement 3.5.2.3. Because this finding is of very low safety significance

and was entered into the licensee's corrective action program as CAR 200804000, this

violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC

Enforcement Policy: NCV 05000483/2008003-02, Inadequate Surveillance Procedure

Resulted in an Inoperable ECCS.

- 18 - Enclosure 2

1R18 Plant Modifications (71111.18)

a. Inspection Scope

The inspectors reviewed the design adequacy of the listed modifications. This included

verifying that the modification preparation did not impair the following: (a) in-plant

emergency/abnormal operating procedure actions, (b) key safety functions, and

(c) operator response to loss of key safety functions.

The inspectors verified that postmodification testing maintained the plant in a safe

configuration during testing and that the postmodification testing established operability

by: (a) verifying that unintended system interactions did not occur; (b) verifying that

performance characteristics, which could have been affected by the modification, met

the design bases; (c) validating the appropriateness of modification design assumptions;

and (d) demonstrating that the modification test acceptance criteria had been met.

  • April 18, 2008, Modification M-08-0013 to separate fast and slow speed overload

contacts for containment air coolers

to provide an additional diesel-driven air compressor to improve system reliability

while the system was in degraded reliability

Documents reviewed are listed in the attachment.

These activities constituted two samples as defined by Inspection Procedure 71111.18.

b. Findings

No findings of significance were identified

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • April 10, 2008, Job 08002765.900, Source Range N32 postmaintenance test
  • April 17, 2008, Postmaintenance test containment Cooler D,

Modification 0800267/950(951)(952)

  • May 28, 2008, Job 08003910, Postmaintence test of Emergency Diesel

Generator A following repair of jacket water leaks

  • May 30, 2008, Job 08001080, Postmaintenance local leakrate test of

containment personnel hatch door

- 19 - Enclosure 2

These activities were selected based upon the structure, system, and component's

ability to impact risk. The inspectors evaluated these activities to verify (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

Technical Specifications, the FSAR, 10 CFR Part 50 requirements, licensee procedures,

and various NRC generic communications to ensure that the test results adequately

ensured that the equipment met the licensing basis and design requirements. In

addition, the inspectors reviewed corrective action documents associated with

postmaintenance tests to determine whether the licensee was identifying problems and

entering them in the corrective action program and that the problems were being

corrected commensurate with their importance to safety. Documents reviewed are listed

in the attachment.

This inspection constitutes five samples as defined in Inspection Procedure 71111.19.

b. Findings

Introduction. A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion XVI,

"Corrective Action," was identified after the licensee failed to promptly correct leakage

from diesel generator jacket water o-rings.

Description. On February 20, 2008, during performance of Procedure OSP-NE-0001B,

Standby Diesel Generator B Periodic Tests, Callaway operations personnel identified

that the Emergency Diesel Generator B had an approximately 80 drop-per-minute jacket

water leak. Analysis by the licensee determined the cause of the leakage to be from

premature failure of Nitrile type o-rings in the jacket water supply and return headers.

Operational history at Callaway revealed o-ring failures prior to reaching 3 years of

service life. The o-rings responsible for the February 20, 2008, leakage had been in

service since Refueling Outage 14 in October 2005. Following restoration of Emergency

Diesel Generator B, the licensee re-evaluated the preventative maintenance frequency

for jacket water o-ring replacement. Based on a review of prior o-ring failures, the

replacement schedule for diesel generator jacket water o-rings was reduced from once

every 3 years to once every refueling cycle.

On May 28, 2008, during performance of Procedure OSP-NE-0001A, Standby Diesel

Generator A Periodic Tests, Callaway operations personnel identified that Emergency

Diesel Generator A had a 200 drop-per-minute jacket water leak. Based on the quantity

of the leakage, operations personnel declared Emergency Diesel Generator A

inoperable. Similar to the condition observed on Emergency Diesel Generator B on

February 20, 2008, the source of the leakage was from Nitrile type o-rings within the

jacket water system. While the licensee replaced the o-rings responsible for jacket

water leakage following the February 20, 2008, surveillance, several Nitrile type o-rings

installed during Refueling Outage 14 in October 2005 remained in service in both

Emergency Diesel Generators Trains A and B including those that failed during the

May 28, 2008, surveillance.

- 20 - Enclosure 2

Subsequent analysis by the licensee determined that the required mission time of the

Emergency Diesel Generator A was preserved since adequate inventory in the jacket

water expansion tank existed such that the leakage observed on May 28, 2008, would

not have impacted the net positive suction head analysis for the jacket water cooling

pump.

Analysis. The performance deficiency associated with this finding involved the

licensees failure to implement adequate corrective actions for an adverse condition.

Specifically, the licensee failed to correct degraded Nitrile type o-rings in Emergency

Diesel Generator A after previously identifying the adverse condition on Emergency

Diesel Generator B. This finding was greater than minor because, if left uncorrected,

degraded diesel generator jacket water o-rings could become a more significant safety

concern. This finding affected the mitigating systems cornerstone. Using Manual

Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, this

finding was determined be of very low safety significance because it was a design

deficiency confirmed not to result in loss of operability. This finding had a crosscutting

aspect in the area of human performance associated with the work control component

because the licensee failed to plan work activities to support long-term equipment

reliability by addressing known degraded conditions in a more reactive than preventative

manner H.3(b).

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires,

in part, that measures be established to assure conditions adverse to quality are

promptly identified and corrected. Contrary to the above, the licensee failed to

implement adequate corrective actions for the identified adverse condition that Nitrile

type o-rings would prematurely fail prior to the completion of the regularly scheduled

3-year replacement interval. Because this violation is of very low safety significance and

has been entered into the licensee's corrective action program as CAR 200804164, this

violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC

Enforcement Policy: NCV 05000483/2008003-03, Failure to Correct a Condition

Adverse to Quality for Diesel Generator Jacket Water O-Rings.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and Technical Specification requirements:

  • April 2, 2008, Job 07513515.500, Routine surveillance auxiliary building Train A

negative pressure test

  • April 4, 2008, Job 08501501, Routine surveillance Slave Relay K645 test of

essential service water component lineup

  • April 18, 2008, Job 08501499, Routine surveillance Slave Relay K615 test

- 21 - Enclosure 2

  • May 5, 2008, Jobs 08502271 and 08503327, Routine surveillance containment

base strong motion accelerometer seismic monitor calibration

  • June 11, 2008, Job 08504820, Routine surveillance diesel generator Train B

1-hour run

  • June 17, 2008, Job 08503115, Safety injection system Train A valve inservice

test

  • June 18, 2008, Job 08505155, Routine surveillance ECCS flow path verification

and venting

reactor coolant system inventory balance, plant status

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine whether: any preconditioning occurred; effects of the testing were

adequately addressed by control room personnel or engineers prior to the

commencement of the testing; acceptance criteria were clearly stated, demonstrated

operational readiness, and were consistent with the system design basis; plant

equipment calibration was correct, accurate, and properly documented; as left setpoints

were within required ranges; the calibration frequency was in accordance with Technical

Specifications, the FSAR, procedures, and applicable commitments; measuring and test

equipment calibration was current; test equipment was used within the required range

and accuracy; applicable prerequisites described in the test procedures were satisfied;

test frequencies met Technical Specification requirements to demonstrate operability

and reliability; tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored where

used; test data and results were accurate, complete, within limits, and valid; test

equipment was removed after testing; where applicable, test results not meeting

acceptance criteria were addressed with an adequate operability evaluation or the

system or component was declared inoperable; where applicable for safety-related

instrument control surveillance tests, reference setting data were accurately incorporated

in the test procedure; equipment was returned to a position or status required to support

the performance of the safety functions; and all problems identified during the testing

were appropriately documented and dispositioned in the corrective action program.

Documents reviewed are listed in the attachment.

The inspectors completed six routine, three inservice test, and one reactor coolant

system leakage samples.

b. Findings

Introduction. A self-revealing Green NCV of Technical Specification 5.4.1.a,

Procedures, was identified after Callaway control room operators improperly entered

the wrong Technical Specification action statement due to the failure to maintain the

Technical Specification Bases current.

- 22 - Enclosure 2

Description. On June 17, 2008, during surveillance testing, Valve EMHV8823 failed to

indicate fully closed. Since EMHV8823 is an isolation valve for containment

Penetration 49, the licensee entered Technical Specification 3.6.3, Containment

Isolation Valves," Condition C, with an action to restore the valve to an operable status

or isolate the penetration within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The control room staff believed the

appropriate action statement was entered since Condition C is described in the

Technical Specification Bases as applicable to flow paths that meet the requirements of

a closed system per the Callaway FSAR. Chapter 6.2.6.3 of the Callaway FSAR

described Containment Penetration 49 as a closed engineered safety feature

containment penetration.

Approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> after Valve EMHV8823 had been declared inoperable, Callaway

licensing personnel contacted the control room and informed them of an approved

Technical Specification Bases change that did not allow the classification of containment

Penetration 49 as a closed system. Procedure APA-ZZ-00108, Primary Licensing

Document; Change/Revision Process," required that the change be implemented within

45 days following approval. The Technical Specification Bases change was effective

May 1, 2008, but had not been issued to the control room. The change resulted in

Condition C of Technical Specification 3.6.3 applying specifically to penetrations for

which a single containment isolation valve is credited per flow path. Since containment

Penetration 49 relies on multiple valves for flow path isolation, the licensee determined

that Condition C of Technical Specification 3.6.3 was not applicable for Penetration 49,

and the wrong Technical Specification action statement had been entered following the

failed surveillance on Valve EMHV8823. The licensee determined that the more

restrictive Technical Specification 3.6.3, Condition A, should have been entered with an

action to isolate the affected penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

The licensee performed a containment entry following discovery of entry into Technical Specification 3.6.3, Condition A, and found that Valve EMHV8823 had failed its

surveillance due to out-of-adjustment position indicator limit switches. The valve was

verified closed with power removed allowing exit from Technical Specification 3.6.3,

Condition A.

Analysis. The performance deficiency associated with this finding involved the

licensees failure to ensure the Technical Specification Bases were maintained current

and available to the Callaway control room staff. This finding was greater than minor

because, if left uncorrected, the failure to maintain the Technical Specification Bases

current could become a more significant safety concern. This finding was determined to

affect the barrier integrity cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial

Screening and Characterization of Findings," this finding is determined to be of very low

safety significance since this finding did not represent an actual open pathway in the

physical integrity of reactor containment and did not involve an actual reduction in

function of hydrogen ignitors in the reactor containment. This finding had a crosscutting

aspect in the area of human performance associated with the decision making

component because the licensee failed to communicate, in a timely manner, decisions to

personnel who have a need to know the information in order to perform work safely

H.1(c).

Enforcement. Technical Specification 5.4.1.a, Procedures, required that written

procedures be established and implemented covering activities specified in Appendix A,

Typical Procedures for Pressurized Water Reactors, of Regulatory Guide 1.33, Quality

- 23 - Enclosure 2

Assurance Program Requirements (Operation), February 1978. Regulatory Guide 1.33,

Appendix A, Section 1, required administrative procedures for procedure review and

approval. Procedure APA-ZZ-00108 provides a process for implementing Technical

Specification Bases change notices. Contrary to the above, on May 1, 2008,

Procedure APA-ZZ-00108 was not adequate to ensure changes to the Technical

Specification Bases were implemented in a timely manner. Because of the very low

safety significance and AmerenUEs action to place this issue in their corrective action

program as CAR 200805283, this violation is being treated as an NCV in accordance

with Section VI.A.1 of the Enforcement Policy: NCV 05000483/2008003-04, Failure to

Maintain an Adequate Technical Specification Bases Change Process.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

a. Inspection Scope

This area was inspected to assess the licensees performance in implementing physical

and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspectors used the

requirements in 10 CFR Part 20, the Technical Specifications, and the licensees

procedures required by Technical Specifications as criteria for determining compliance.

During the inspection, the inspectors interviewed the radiation protection manager,

radiation protection supervisors, and radiation workers. The inspectors performed

independent radiation dose rate measurements and reviewed the following items:

  • Performance indicator events and associated documentation packages reported

by the licensee in the occupational radiation safety cornerstone

  • Controls (surveys, posting, and barricades) of radiation, high radiation, or

airborne radioactivity areas

  • Radiation work permits, procedures, engineering controls, and air sampler

locations

  • Physical and programmatic controls for highly activated or contaminated

materials (non-fuel) stored within spent fuel and other storage pools

  • Self-assessments, audits, LERs, and special reports related to the access control

program since the last inspection

and very high radiation areas

  • Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

  • Posting and locking of entrances to accessible high dose rate - high radiation

areas and very high radiation areas

- 24 - Enclosure 2

Documents reviewed are listed in the attachment.

The inspectors completed 8 of the required 21 samples.

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02)

a. Inspection Scope

The inspectors assessed licensee performance with respect to maintaining individual

and collective radiation exposures as low as is reasonably achievable (ALARA). The

inspectors used the requirements in 10 CFR Part 20 and the licensees procedures

required by technical specifications as criteria for determining compliance. The

inspectors interviewed licensee personnel and reviewed:

  • Current 3-year rolling average collective exposure
  • Site-specific trends in collective exposures, plant historical data, and source-term

measurements

  • Site-specific ALARA procedures
  • Work activities of highest exposure significance during the inspection
  • Integration of ALARA requirements into work procedure and radiation work

permit documents

  • Post-job (work activity) reviews
  • Workers use of the low dose waiting areas
  • First-line job supervisors contribution to ensuring work activities are conducted in

a dose efficient manner

  • Records detailing the historical trends and current status of tracked plant source

terms and contingency plans for expected changes in the source term due to

changes in plant fuel performance issues or changes in plant primary chemistry

  • Source-term control strategy or justifications for not pursuing such exposure

reduction initiatives

  • Specific sources identified by the licensee for exposure reduction actions,

priorities established for these actions, and results achieved since the last

refueling cycle

  • Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

- 25 - Enclosure 2

  • Declared pregnant workers during the current assessment period, monitoring

controls, and the exposure results

  • Self-assessments, audits, and special reports related to the ALARA program

since the last inspection

  • Resolution through the corrective action process of problems identified through

post-job reviews and post-outage ALARA report critiques

  • Corrective action documents related to the ALARA program and follow-up

activities, such as initial problem identification, characterization, and tracking

  • Effectiveness of self-assessment activities with respect to identifying and

addressing repetitive deficiencies or significant individual deficiencies

Documents reviewed are listed in the attachment.

The inspectors completed 9 of the required 15 samples and 8 of the optional samples.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the first

Quarter 2008 performance indicators for any obvious inconsistencies prior to its public

release in accordance with IMC 0608, Performance Indicator Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b. Findings

No findings of significance were identified.

.2 Safety System Functional Failures

Cornerstone: Mitigating Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the safety system functional failures

performance indicator for the period March 2007 until March 2008. To determine the

accuracy of the performance indicator data reported during this period, performance

indicator definitions and guidance contained in the Nuclear Energy Institute (NEI)

- 26 - Enclosure 2

Document 99-02, Revision 5, Regulatory Assessment Performance Indicator

Guideline, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73,"

definitions and guidance were used. The inspectors reviewed the licensees operator

narrative logs, operability assessments, maintenance rule records, maintenance work

orders, issue reports, event reports and NRC integrated inspection reports for the period

of 2nd Quarter 2007, through 1st Quarter 2008 to validate the accuracy of the

submittals. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the performance indicator data

collected or transmitted for this indicator and none were identified. Documents reviewed

are listed in the attachment.

This inspection constitutes one safety system functional failures sample as defined by

Inspection Procedure 71151.

b. Findings

No findings of significance were identified.

.3 Mitigating Systems Performance Index - High Pressure Injection Systems

Cornerstone: Mitigating Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the mitigating systems performance

index - high pressure injection systems performance indicator for the period from

March 2007 until March 2008. To determine the accuracy of the performance indicator

data reported during this period, performance indicator definitions and guidance

contained in the NEI Document 99-02, 5, Regulatory Assessment Performance

Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees

operator narrative logs, issue reports, mitigating systems performance index derivation

reports, event reports, and NRC integrated inspection reports for the period of

2nd Quarter 2007 through 1st Quarter 2008 to validate the accuracy of the submittals.

The inspectors reviewed the mitigating systems performance index component risk

coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable NEI

guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the performance indicator data

collected or transmitted for this indicator and none were identified. Documents reviewed

are listed in the attachment.

This inspection constitutes one mitigating systems performance index high pressure

injection systems sample as defined by Inspection Procedure 71151.

b. Findings

No findings of significance were identified.

- 27 - Enclosure 2

.4 Occupational Exposure Control Effectiveness

Cornerstone: Occupational Radiation Safety

a. Inspection Scope

The inspectors reviewed licensee documents from October 1, 2007, through March 31,

2008. The review included corrective action documentation that identified occurrences

in locked high radiation areas (as defined in the licensees Technical Specifications),

very high radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel

exposures (as defined in NEI 99-02, "Regulatory Assessment Indicator Guideline,"

Revision 5). Additional records reviewed included ALARA records and whole body

counts of selected individual exposures. The inspectors interviewed licensee personnel

that were accountable for collecting and evaluating the performance indicator data. In

addition, the inspectors toured plant areas to verify that high radiation, locked high

radiation, and very high radiation areas were properly controlled. Performance indicator

definitions and guidance contained in NEI 99-02, Revision 5, were used to verify the

basis in reporting for each data element.

The inspectors completed the required sample (1) in this cornerstone.

b. Findings

No findings of significance were identified.

.5 Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

Cornerstone: Public Radiation Safety

a. Inspection Scope

The inspectors reviewed licensee documents from October 1, 2007, through March 31,

2008. Licensee records reviewed included corrective action documentation that

identified occurrences for liquid or gaseous effluent releases that exceeded performance

indicator thresholds and those reported to the NRC. The inspectors interviewed licensee

personnel that were accountable for collecting and evaluating the performance indicator

data. Performance indicator definitions and guidance contained in NEI 99-02,

Revision 5, were used to verify the basis in reporting for each data element.

The inspectors completed the required sample (1) in this cornerstone.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical

Protection

- 28 - Enclosure 2

.1 Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

to verify that they were being entered into the licensees corrective action program at an

appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. The attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent of condition reviews, and previous occurrence reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. This review was

accomplished through inspection of the stations daily condition report packages.

These daily reviews were performed, by procedure, as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings of significance were identified.

.3 Selected Issue Follow-up Inspection

a. Inspection Scope

The inspectors selected the below listed issues for a more in-depth review. The

inspectors considered the following during the review of AmerenUE's actions:

(1) complete and accurate identification of the problem in a timely manner; (2) evaluation

and disposition of operability/reportability issues; (3) consideration of extent of condition,

generic implications, common cause, and previous occurrences; (4) classification and

prioritization of the resolution of the problem; (5) identification of root and contributing

causes of the problem; (6) identification of corrective actions; and (7) completion of

corrective actions in a timely manner.

- 29 - Enclosure 2

high pressure recirculation.

  • FSAR changes/updates

Documents reviewed are listed in the attachment.

This inspection constituted two in-depth problem identification and resolution samples.

b. Findings

Introduction. The inspectors identified a Green violation of 10 CFR Part 50, Appendix B,

Criterion XVI, "Corrective Action," because the licensee failed to take corrective actions

to preclude repetition of void formations in the ECCS, a significant condition adverse to

quality (SCAQ). Contributors to the violation included: (1) the failure of corrective

actions from inspection report findings NCV 05000483/2005002-01,

05000483/2006012-04 and CAR 200501092 to ensure adequate fill and vent of

systems following maintenance to replace safety injection system relief valves, and

(2) inadequate extent of condition reviews in responding to internal and external

operating experience associated with pipe sloping issues in the safety injection system.

Description. On May 21, 2008, the Callaway Plant staff initiated CAR 200804000, a

SCAQ corrective action document, indicating that some piping in Train A safety injection

system suction lines had incorrect sloping and were susceptible to voiding due to high

points. Callaway Plant engineering performed ultrasonic inspection of the safety

injection system common suction piping Line EM023-HCB - 6" and discovered a

6.6 cubic foot voided area. This exceeded the allowable void fraction of 2.1 cubic feet

required for operability. This voided piping, determined to have existed for over a year,

was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The

maintenance restoration failed to perform an adequate fill and vent to ensure the suction

pipe was full of water.

In 2005 and 2006 the NRC issued NCVs regarding ineffective corrective actions related

to safety injection system voids in discharge piping (05000483/2005002-01 dated May 6,

2005, and 05000483/2006012-04 dated December 26, 2006). These were each 10 CFR

Part 50, Appendix B, Criterion XVI, NCVs, each for SCAQ. The Callaway Plant staff

issued CAR 200501092 as a SCAQ corrective action document. The CAR determined

that the causes of the voids (2004, 2005, and 2006) were related to incorrect pipe

sloping (allowing high points where voids could not be swept away by normal online

pump surveillances) and inadequate postmaintenance fill and vent operations (following

discharge piping relief Valve EM8853A replacement) to ensure the piping was full of

water.

Inadequate Operating Experience and Extent of Condition Corrections: The

inspectors identified several related examples where the licensee had performed either

inadequate operating experience evaluations, inadequate extent of condition reviews, or

inadequate procedure corrections.

Callaway CAR 200501092 referenced industry operating experience at Beaver Valley

Unit 2 in 2002: "The void was located in the piping used following a loss of coolant

- 30 - Enclosure 2

accident after the transfer to containment sump recirculation. The piping containing the

void led to a common suction header for both trains of high head pumps." This was the

same location as the voiding discovered at Callaway Plant on May 21, 2008.

NRC Information Notice 2006-21, "Operating Experience Regarding Entrainment of Air

into Emergency Core Cooling and Containment Spray Systems," dated September 21,

2006, discussed mechanisms that could result in air entrainment on the suction sides of

emergency core cooling pumps. The notice emphasized the importance of ensuring that

entrained air will not enter suction supply lines and impair the ability of the ECCS and

containment spray pumps to perform their safety function.

The licensee's evaluation of NRC Information Notice 2006-21 was documented in

CAR 200608956. It stated that the information notice was applicable to Callaway and

that past review of these operating experiences and Callaway procedures and practices

were adequate. The CAR was closed December 5, 2006.

Callaway CAR 200501092 had Action 7 assigned to address the previous NRC

violations discussed above. The action required that system specific fill and vent

restoration guidance be developed to address maintenance on ECCS safety-related

systems. Initially, operating department Standing Order 05-002 dated June 8, 2005,

stated that the CAR 200501092 common cause analysis supported the need for

formalized restoration instructions. Until the system specific restoration instructions

were developed, the standing order required reactor operators to perform reviews to

ensure dynamic filling and venting occurred to reduce the susceptibility of voiding. Also

nuclear engineering department staff were to provide concurrence on such restoration

plans. Night Order ODP-ZZ-00310, "System Fill and Vent," issued February 13, 2006,

reiterated that reactor operator reviews and engineering concurrence were required

when these risk-significant systems were drained. However, on May 7, 2007,

Procedure OTN-EM-00001, "Safety Injection System," (developed to address filling and

venting evaluations) had Line EM-023-HCB - 6" isolated by Valve EMHIS8807B being

closed. The procedure did not include use of the available installed vent Valve EM179

for this line.

Callaway monthly Surveillance OSP-SA-00003, "Emergency Core Cooling Flow Path

Verification and Venting," had a purpose to: "Verify the ECCS is full of water in

accordance with Technical Specification Surveillance Requirement 3.5.2.3." This

monthly surveillance was reviewed as part of CAR 200501092 corrective actions.

Callaway engineering had determined that residual heat removal pump discharge vent

Valve EJV0193 to the safety injection suction line was the high point vent for these lines

and was thus sufficient to vent supply Line EM-023-HCB - 6" to the safety injection

pumps. However, this vent valve was not adequate due to the pipe sloping issues and

normally closed Valves EMHIS8807A/B. The monthly verification and vent procedure

was inadequate to remove the air entrained by the May 7, 2007, relief valve

maintenance. See Section 1R15, NCV 05000483/2008003-02.

Callaway CARs 200800226 and 200800246, initiated in January 2008, discussed

operating experience at Wolf Creek Nuclear Operating Corporation describing gas

voiding in the residual heat removal piggyback Line EM-022-HCB - 6" to the suction of

centrifugal charging pumps and safety injection pumps. The CARs stated that Callaway

had taken a proactive approach and had immediately performed ultrasonic testing to

demonstrate that the associated piping was water solid. However, the adjacent

- 31 - Enclosure 2

connecting Line EM-023-HCB - 6" had not been vented nor had ultrasonic testing

occurred since the May 7, 2007, relief Valve EM8858A maintenance.

NRC Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal, and Containment Spray Systems," was issued January 11, 2008.

The Callaway Plant staff initiated CAR 200800298 to respond to the generic letter. The

generic letter identified that a licensing basis concern existed for some plants, such as

Callaway, that Technical Specifications require verifying that ECCS discharge piping is

full of water but may not include verification of the suction piping despite the realistic

concern that gas accumulation in suction piping may be more serious than gas

accumulation in discharge piping. The void found in Line EM-023-HCB - 6" was the

discharge of the residual heat removal pumps providing suction to the Train A safety

injection pump. The Callaway monthly Surveillance OSP-SA-00003, "Emergency Core

Cooling Flow Path Verification and Venting," did not test for or vent the discharge line

from residual heat removal to safety injection pump suction piping.

Analysis. The inspectors determined that the failure to restore compliance within a

reasonable time by establishing measures to prevent void formation in ECCS suction

piping for the Train A safety injection system was a performance deficiency. This finding

is more than minor because it was similar to Example 3e of NRC Inspection Manual

Chapter 0612, Appendix E, "Examples of Minor Issues," and met the Not Minor If,

criteria because the failure to meet the licensees administrative requirement for

allowable void fraction impacted the ability of the Train A safety injection system to

function upon initiation of high-pressure recirculation. Using Manual Chapter 0609.04,

Phase 1 - Initial Screening and Characterization of Findings, the inspectors determined

that this finding should be evaluated using the Phase 2 process described in Manual

Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection Findings

for At-Power Situations.

The senior reactor analyst determined that the risk of this finding was bounded by that

analyzed for NCV 05000423/2008003-02 (See Section 1R15.b.2). Therefore, this

finding was of very low risk significance (Green).

This finding has a crosscutting aspect in the area of problem identification and resolution

associated with the corrective action component because AmerenUE failed to thoroughly

evaluate voiding problems such that the resolutions addressed causes and extent of

condition, as necessary. This also includes, for significant problems, conducting

effectiveness reviews of corrective actions to ensure that the problems are resolved

P.1(c).

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires

the licensee to, in the case of SCAQ, establish measures to assure that the cause of the

condition is determined and corrective action is taken to preclude repetition. Contrary to

the above, from December 26, 2006, to May 21, 2008, the licensee did not implement

corrective action to preclude repetition of void formation in the safety injection piping

which the licensee categorized as an SCAQ. Specifically, void formation recurred after

performing maintenance on relief valve. Valve EM8858A, on May 7, 2007. Previously

discovered voiding of the safety injection system was last documented as an SCAQ in

NCV 05000483/2006012-04 dated December 26, 2006. For each instance of the

previously discovered voids, the causes were determined to be related to inadequate fill

and vent of the system piping following relief valve replacements and design deficiencies

- 32 - Enclosure 2

associated with inadequate sloping of the piping. It was a reasonable assumption that

maintenance that drained either the suction or discharge piping could create significant

void areas.

Although this violation is of very low safety significance, the violation is being

cited in a Notice of Violation consistent with Section VI.A.1 of the NRC Enforcement

Policy because the licensee did not restore compliance within a reasonable

time after a previous violation NCV 05000483/2006012-04 was identified:

VIO 05000483/2008003-05, Failure to Prevent Recurrence of Voids in ECCS Cold Leg

Recirculation Piping. This finding has been entered into the licensee's corrective action

program as a SCAQ in CAR 200804000.

.4 Semiannual Trend Review

The inspectors assessed trends that might indicate the existence of a more significant

safety issue. These issues included trends that might not rise to the level of an

inspection finding.

NRC-Identified Trends

The NRC identified emergency diesel generator material condition and design control

issues degrading diesel reliability:

  • CAR 200801270: 80 Drops per minute jacket water leak identified on Diesel

Generator B

  • CAR 200801644: Additional sacrificial anode found in Emergency Diesel

Generator A intercooler heat exchanger

fuel oil leaks

  • CAR 200802177: Cracked fuel oil return line fitting identified on Emergency

Diesel Generator A

200 drops per minute jacket water leak

Licensee-Identified Trends

The licensee identified a continued trend in plant status control and configuration control

with a key causal factor being procedure adherence.

  • CAR 200706832: This trend CAR from Third Quarter 2007 identified the cause

of plant status control issues to be a "Failure to follow written instructions."

  • CAR 200801457: A gauge was installed on an incorrect component during Test

Procedure OSP-EN-P001A.

  • CAR 200800580: A trend of critical steps not being included in work packages

was identified.

- 33 - Enclosure 2

  • CAR 200802603: Component cooling water pump autostarted due to an

interlock with the centrifugal charging pumps. The operator failed to wait the

procedure prerequisite 30 minutes prior to securing the component cooling water

pump.

  • CAR 200802818: Source range Channel N31 was not restored to "block" as

required by procedure in Mode 1.

  • CAR 200800328: Not following procedures resulted in gaseous Radiation

Monitor RM-11 trip setpoint not being capable of isolating the waste gas decay

tank release.

demineralizer valve lineup.

inoperable when its room cooler was taken to "stop" vice "auto." This was

performed outside the out of service restoration process.

This inspection constituted one semiannual trend review sample.

4OA3 Event Follow-up (71153)

(Closed) LER 05000483/2008-001-00, Containment Cooler Inoperability

On March 26, 2008, Containment Air Cooler A fan shut down when shifted from fast to

slow speed. The licensee determined that operation of containment air coolers in fast

speed, during a period of higher than normal containment pressure, would challenge the

fast speed thermal overload setpoint. Additionally, since the overload contacts are wired

in series, containment air coolers were determined to experience a complete loss of

control power following a trip from fast speed. The licensee analyzed the potential

impact of the containment cooler design vulnerability against design basis accident

scenarios. The licensee determined that a hot zero power main steam line break results

in a delayed safety injection signal allowing the fan motor overloads to trip prior to being

shed from the load sequencer. In this scenario, utilizing actual plant conditions, the peak

containment pressure would not exceed the 48.1 psig limit described in the FSAR. To

address the design deficiency associated with the containment air cooler control

circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit

such that tripping of the fast speed overloads would not impact the safety-related slow

speed function of the containment air coolers. This finding is of very low safety

significance because the containment coolers are structures, systems, and components

that are not significant contributors to the large early release frequency. Licensee

corrective actions were recorded in CAR 200802264. The inspectors reviewed the LER

and identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design

Control, for the licensees failure to adequately review the suitability of the design of the

containment air cooler control circuitry (Section 1R15). This LER is closed.

This inspection constituted one sample of follow-up of events.

- 34 - Enclosure 2

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. During the inspection period, the inspectors performed the following observations of

security force personnel and activities to ensure that the activities were consistent with

licensees security procedures and regulatory requirements relating to nuclear plant

security. These observations took place during both normal and off-normal plant

working hours.

These quarterly resident inspector observation of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors normal plant status review and inspection activities.

b. Findings

No findings of significance were identified.

.2 (Closed) NRC Temporary Instruction 2515/166: Pressurized Water Reactor

Containment Sump Blockage

a. Inspection Scope

From March 17-19, 2008, the inspectors reviewed the licensees implementation of plant

modifications and design modification packages associated with their response to

Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency

Recirculation During Design Basis Accidents at Pressurized Water Reactors. The

inspectors reviewed various aspects of the on-going procedural changes. Those

changes that have been completed were verified to be properly documented in

accordance with the requirements of 10 CFR 50.59. At the completion of this inspection,

the licensee had completed the installation stage of the new sump strainers; many of the

procedural changes associated with the modifications had not been completed.

The inspectors compared and evaluated the recirculation sump modifications to the

original design basis using Temporary Instruction 2515/166 and referred to Regulatory

Guide 1.82, Revision 0, Water Sources for Long-Term Recirculation Cooling Following

a Loss-of-Coolant Accident.

Status of the implementation of the plant modifications and procedure changes

committed to by the licensee in their Generic Letter 2004-02 response is:

1. Containment walkdown to provide current assessment of Callaway's containment

coatings and latent debris.

The licensee completed a containment walkdown and latent debris assessment

during Refueling Outage 14. The resident inspectors completed a walkdown of

the containment prior to reactor startup following the outage. The licensee

report, Containment Building Latent Debris Assessment Refuel 14 Fall 2005,

was reviewed by the inspectors.

- 35 - Enclosure 2

2. The following corrective action activities will be completed:

a. Replacement sump strainer structural analysis.

The strainers were not built in accordance with the design. As a result,

calculations needed to be revised due to the deviations of the as built

condition from design and errors in temperature correction values used in

the initial calculations. Completion date: June 30, 2008

b. Downstream effects evaluation

Completion date: June 30, 2008

c. Upstream effects evaluation

Completion date: June 30, 2008

d. Resolution of debris generation calculation unverified assumption of 5D

ZOI for qualified coatings (via coatings testing)

Completion date: June 30, 2008

e. Replacement sump screen head loss testing

Completion date: June 30, 2008

3. Provide an update of the information contained in Section 2(c) regarding analysis

methodology.

Completion date: June 30, 2008

4. The following evaluations and testing will be completed.

a. Industry chemical effects testing

Completion date: June 30, 2008

b. Nuclear Energy Institute 04-07 debris generation calculation

Completion date: June 30, 2008

c. Evaluation of chemical effects impact on sump-strainer head loss

Completion date: June 30, 2008

d. Confirmation that the replacement sump strainer design provides for

available Net Positive Suction Head (NPSH) to be in excess of required

NPSH

Completion date: June 30, 2008

- 36 - Enclosure 2

e. Completion of the final site acceptance review of the Westinghouse team

analysis summary report

Completion date: June 30, 2008

5. Callaway Plant will complete the following items during Refueling Outage15:

a. Replacement of containment recirculation sump strainers

Completed. As noted in the previous Temporary Instruction 166 report,

the resident inspectors had observed the installation of sump strainers

and debris barriers during their containment walkdown; however, the

strainers were not built in accordance with the design. The licensee has

completed their initial determination of operability and was finalizing their

acceptance calculations.

b. Modification of containment debris barriers and interceptors as required

Completed. As noted in the previous Temporary Instruction 166 report,

the resident inspectors had observed the installation of sump strainers

and debris barriers during their containment walkdown.

c. Evaluation and implementation of potential modification to the safety

injection system to address downstream effects

Completion date: June 30, 2008

6. Callaway Plant will complete removal of containment spray system pump cyclone

separators, if required, based on the results of the downstream effects

evaluation.

Completion date: June 30, 2008

7. The following programs and controls will be implemented at Callaway Plant to

control debris sources:

a. Changes to design change process procedures to ensure that necessary

engineering evaluations will be performed for plant design that either

directly or indirectly affects containment, ECCS, or CSS.

Changes are being processed.

b. Changes to containment entry and material control procedure

requirements for control of materials during work activities conducted in

the containment

c. The following procedures were reviewed and completed as of

December 2007:

APA-ZZ-01004, Radiological Work Standards, Revision 9

HDP-ZZ-06100, Reactor Building Access, Revision 7

- 37 - Enclosure 2

MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22

OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6

OSP-SA-00004, Visual Inspection of Containment for Loose Debris,

Revision 19

OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices,

Revision 2

d. Changes to programs and procedures that have the potential to add tags

and labels inside containment

Completed: December 2007

The following documents were reviewed:

APA-ZZ-01004, Radiological Work Standards, Revision 9

HDP-ZZ-06100, Reactor Building Access, Revision 7

MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22

OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6

OSP-SA-00004, Visual Inspection of Containment for Loose Debris,

Revision 19

OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices,

Revision 2

e. Implementation of a containment coatings assessment program

Licensee reported as complete. The inspectors reviewed SWE07848,

Containment Coating Condition Assessment. A preventative

maintenance item has been scheduled to perform containment coating

assessments with a periodicity of each refueling cycle.

f. Implementation of a containment latent debris assessment program

Licensee reported as complete. The inspectors reviewed report,

Containment Building Latent Debris Assessment Refuel 14 Fall 2005,

and Procedure OSP-SA-00004, Visual Inspection of Containment for

Loose Debris, Revision 019. A preventative maintenance item has been

scheduled for a visual inspection of containment for loose debris with a

periodicity of each refueling cycle.

g. Implementation of changes to the inspection processes for the installed

sump strainers

Licensee reported as complete. Reviewed Procedure OSP-EJ-00003,

Containment Recirculation Sump Inspection, Revision 6

- 38 - Enclosure 2

8. A final response will be submitted to the NRC to provide a final status of actions

requested by Generic Letter 2004-02.

Completion date: June 30, 2008

The Office of Nuclear Reactor Regulation will determine the adequacy of the sump

modifications with respect to Generic Safety Issue 191. This temporary instruction is

closed.

Documents reviewed by the inspectors are listed in the attachment.

b. Findings

No findings of significance were identified.

4OA6 Management Meetings

Exit Meeting Summary

On April 25, 2008, the health physics inspector presented the occupational radiation

safety inspection results to Mr. T. Herrmann and other members of his staff who

acknowledged the findings. The inspector confirmed that proprietary information was

not provided or examined during the inspection.

On June 18, 2008, the Temporary Instruction 2515/166 inspector presented the

inspection results to Mr. S. Maglio and other members of his staff who acknowledged the

findings. The inspector confirmed that proprietary information provided or examined

during the inspection had been returned.

On June 24, 2008, the resident inspectors presented the inspection results to

Mr. C. Naslund, Senior Vice President and Chief Nuclear Officer, and other members of

the licensee staff. The licensee acknowledged the issues presented. The inspectors

understood and acknowledged that proprietary information reviewed would not be

retained following report issuance.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the

licensee and were violations of NRC requirements which meet the criteria of Section VI

of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.

that applicable regulatory requirements and the design basis are correctly

translated into specifications, drawings, procedures, and instructions.

Contrary to the above, on March 5, 2008, the licensee identified that a 4-foot

section of suction piping within containment spray system, Train A was

approximately 50 percent voided. Voiding within the containment spray

system was due to a design deficiency that did not allow for a proper fill and

vent of the system. This was entered in the licensees corrective action

program as CAR 200803462. This finding is greater than minor because it is

similar to the Example 3j in Manual Chapter 0612, Appendix E, "Examples of

- 39 - Enclosure 2

Minor Issues," in that the presence of air within the containment spray system

suction header resulted in a condition where there was reasonable doubt on

the operability of the system. This finding is of very low safety significance

because it was a design or qualification deficiency confirmed not to result in

loss of operability.

to assure that applicable regulatory requirements and design basis be

correctly translated into specifications, drawings, procedures, and

instructions. Technical Specifications 3.5.2 and 3.6.6 require that residual

heat removal and containment spray system components remain operable.

Contrary to this, measures were not adequate to assure installed center tube

diameters for the containment recirculation sump modification were correctly

accounted for by an accurate net positive suction head calculation.

The vendor supplying AmerenUE the containment recirculation sump strainer

identified that associated Vendor Calculation TDI-6002-05 for clean strainer

head loss did not account for the installed orifices located in the strainer

support plate. The size of the orifice beneath each strainer was smaller than

assumed in head loss calculations and was not large enough to prevent head

loss in excess of the net positive suction head required as defined in the

purchase specification supplied to the strainer vendor. The additional head

loss due to the calculation translation error was 2.28 feet. This resulted in

required net positive suction head being less than available. AmerenUE

performed three separate operability determination reviews to demonstrate

that the head loss margin could be recovered. The initial operability

determination on January 22, 2008, addressed the smaller support plate

orifice holes by using a separate vendor's flow analysis of the residual heat

removal and containment spray piping systems to demonstrate lower flow

and head losses than described in the FSAR. This operability determination

resulted in the limiting case flow path being the hot leg recirculation flow path.

Another operability review on March 12, 2008, addressed a nonconservative

temperature correction through the orifices. Subsequent to this, the licensee

informed the NRC that the additional nonconservative inputs were used in

the January 22, 2008, flow re-analysis of the residual heat removal system.

Additional analyses were performed to regain margin. This resulted in the

limiting case flow path changing from hot leg recirculation to cold leg

recirculation.

This example of inadequate design control was captured in the licensees

corrective action program as CARs 200800461 and 200802618. These

corrective action reviews documented three causes related to the following

design error:

  • A complex design with parallel sequencing of different parts of the

design

  • AmerenUE not independently verifying the vendor's design due to

perceived expertise and an approved 10 CFR Part 50, Appendix B,

- 40 - Enclosure 2

Quality Assurance program. AmerenUE did not perform a review of

the design, nor did they contract to have a third party engineering

review of the design.

This finding is greater than minor because it is similar to the Example 3j in

Manual Chapter 0612, Appendix E, Examples of Minor Issues, in that the

contractor error translating the design to the calculations resulted in a

condition where there was reasonable doubt on the operability of the ECCS.

This finding is of very low safety significance because it was a design or

qualification deficiency confirmed not to result in loss of operability. This

licensee-identified violation closes out Unresolved

Item 05000483/2008002-01.

ATTACHMENT: SUPPLEMENTAL INFORMATION

- 41 - Enclosure 2

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

B. Barton, Training Manager

M. Brandes, Consulting Engineer, Nuclear Engineering - Major Modifications

K. Bruckerhoff, Supervisor, Emergency Preparedness

F. Diya, Plant Director

T. Elwood, Supervising Engineer, Licensing

R. Farnam, Manager, Radiation Protection

K. Gilliam, Supervisor, Radiation Protection

L. Graessle, Manager, Regulatory Affairs

A. Heflin, Vice President, Nuclear

T. Herrmann, Vice President, Engineering

B. Holderness, Senior Health Physicist, Environmental Services

L. Kanuckel, Manager, Quality Assurance

D. Lantz, Superintendent of Operations Training

S. Maglio, Assistant Manager, Regulatory Affairs

R. Myatt, Supervisor, Engineering

K. Mills, Manager, Engineering

D. Neterer, Manager, Nuclear Operations

T. Parker, Trainer, Radiation Protection

S. Petzel, Engineer, Regulatory Affairs

J. Pitts, Component Engineer

V. Rider, ALARA Specialist, Radiation Protection

LIST OF ITEMS OPENED AND CLOSED

Opened

05000483/2008003-05 VIO Failure to Prevent Recurrence of Voids in ECCS Cold Leg

Recirculation Piping (Section 4OA2)

Opened and Closed

05000483/2008003-01 NCV Failure to Ensure the Suitability of the Design of the

Containment Air Cooler Control Circuitry (Section 1R15)05000483/2008003-02 NCV Inadequate Surveillance Procedure Resulted in an

Inoperable ECCS (Section 1R15)05000483/2008003-03 NCV Failure to Correct a Condition Adverse to Quality for

Diesel Generator Jacket Water O-Rings (Section 1R19)05000483/2008003-04 NCV Failure to Maintain an Adequate Technical Specification

Bases Change Process (Section 1R22)

Closed

05000483/2008001-00 LER Containment Cooler Inoperability (Section 4OA3)05000483/2008002-01 URI Containment Recirculation Sump Operability

(Section 4OA7)

A-1 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 1R01: Adverse Weather Protection

Procedures

ODP-ZZ-00001, Operations Department - Code of Conduct, Revision 41

OSP-NB-00001, Class 1E Electrical Source Verification, Revision 032

OTN-NB-0001A, 4.16 KV Vital (Class 1E) Electrical System - A Train, Revision 12

OTN-NB-0001A, Addendum 5, NB01 Loss of Power Recovery, Revision 0

OTO-ZZ-00012, Severe Weather, Revision 10

Miscellaneous

AmerenUE Response to Generic Letter 2006-02, Grid Reliability and the Impact on Plant Risk

and the Operability of Offsite Power

Training Lesson Plan LP-01, Systems, Switchyard MD

Training Lesson Plan T61.0110.6, Systems, Switchyard MD

Section 1RO4: Equipment Alignment

Drawings

M-22AL01A, Piping and Instrumentation Diagram Auxiliary Feedwater System, Revision 33

M-22BB01(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 30

M-22BB03A(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9

M-22BB03B(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9

M-22BB03C(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7

M-22BB03D(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7

M-22BG01(Q), Piping and Instrumentation Diagram Chemical and Volume Control System,

Revision 28

M-22BG03(Q), Piping and Instrumentation Diagram Chemical and Volume Control System,

Revision 52

A-2 Attachment

M-22EJ01(Q), Piping and Instrumentation Diagram Residual Heat Removal System,

Revision 57

M-22EM01(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System,

Revision 33

M-22EM02(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System,

Revision 19

M-22EP01(Q), Piping and Instrumentation Diagram Accumulator and Safety Injection,

Revision 16

Section 1RO5: Fire Protection

Miscellaneous

Drill Number 08-01, Evaluate Fire Brigade Response in a Radiation Area, dated March 27, 2008

Drill Critique Number 08-01, Unannounced Fire Drill, dated March 27, 2008

FSAR, Appendix 9.5B, Fire Hazard Analysis

Section 1R11: Licensed Operator Requalification Program

Procedures

OTA-RK-00024, Addendum 98D, Seismic Event, Revision 0

OTO-SG-0001, Design Basis Earthquake, Revision 13

Section 1R12: Maintenance Effectiveness

Procedures

EDP-ZZ-01128, Maintenance Rule Program, Revision 8

NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear

Power Plants, Revision 3

Callaway Action Requests

200706892 200801644 200802854

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

Procedure

EDP-ZZ-01129, Callaway Plant Risk Assessment, Revision 14

Section 1R15: Operability Evaluations

Calculations

ARC-687, AFT Fathom 6.0 Output, Revision 0

A-3 Attachment

M-FL-18, LOCA and MSLB Containment Flood Level, Revision 1

WES-009-CALC-001, Wolf Creek/Callaway Post-LOCA Containment Water Level Calculation,

Revision 0

Callaway Action Requests

200800461 200802352 200803462

200802231 200802365 200804000

200802264 200802618

200802348 200803252

Drawings

E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19

E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19

E-018-00273, Motor Control Center Ambient Compensated Overload Relay Heater Chart,

Revision 3

E-018-00847, Overload Relay Time Current Characteristics, Revision 4

E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11

E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12

E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5

E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12

E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13

J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,

Revision 2

J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,

Revision 1

M-018-00943, 206 Ez-Flo Expansion Joint, Revision 0

M-22BG03, Piping and Instrumentation Diagram Chemical and Volume Control System,

Revision 52

M-22EM01, Piping and Instrumentation Diagram High Pressure Coolant Injection System,

Revision 33

M-23BG02, Piping Isometric CVCS-Max Charging Flow A and B Train Auxiliary Building,

Revision 12

A-4 Attachment

Procedures

ECA-0.1, Loss of All AC Power Recover Without Safety Injection Required, Revision 8

ECA-1.1, Loss of Emergency Coolant Recirculation, Revision 8

EDP-ZZ-04021, Review of Supplier Documents, Revision 5

ISF-SE-00N32, FCTNAL-NUC INSTM SOURCE RANGE N32, Revision 20

OSP-EJ-PV04A, Train A RHR and RCS Check Valve Inservice Test -IPTE, Revision 0

OSP-EJ-PV04B, Train B RHR and RCS Check Valve Inservice Test -IPTE, Revision 1

OTN-EN-00001, Containment Spray System, Revision 14

OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 1

Miscellaneous

Job 07513275 for SEN0032

Letter ULNRC-04884, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co.,

Facility Operating License NPF-30, Response to NRC Bulletin 2003-01, Potential Impact of

Debris Blockage on Emergency Sump Recirculation at Pressurized Water Reactor, dated

August 3, 2003

Letter ULNRC-05481, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co.,

Facility Operating License NPF-30 Response to Request for Additional Information, Response

to NRC Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency

Recirculation During Design Basis Accidents at Pressurized Water Reactors, dated

February 29, 2008

Garlock Sealing Technologies Customer Requested Test 206 Ez-Flo Expansion Test, dated

November 15, 2006

Section 1R18: Plant Modifications

Procedure

OTN-KA-00001, Compressed Air System, Revision 18

Drawings

E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19

E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19

E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11

E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12

E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5

A-5 Attachment

E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12

E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13

J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,

Revision 2

J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,

Revision 1

M-22KA01, Piping and Instrumentation Diagram Compressed Air System, Revision 016A

M-22KA06, Piping and Instrumentation Diagram Instrument Air Filter/Dryer Turbine, Building,

Revision 30A

Miscellaneous

Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change,

Revision 0

Job

08003842

Section 1R19: Postmaintenance Testing

Procedures

APA-ZZ-00330, Preventative Maintenance Program, Revision 29

OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 14

Callaway Action Requests

200801270 200802810 200804164

Jobs

06524419 08001080 08002765

07006905 08002676 08003910

Drawings

E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19

E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19

E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12

E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11

E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5

A-6 Attachment

E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12

E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13

J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,

Revision 2

J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,

Revision 1

Miscellaneous

Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change,

Revision 0

Simple Surveillance SP08-017, Containment Cooler Control Circuit Changes, dated April 16,

2008

Section 1R22: Surveillance Testing

Procedures

EDP-ZZ-04107, HVAC Pressure Boundary Control, Revision 19

FDP-ZZ-00101, Technical Specification Bases Control Program, Revision 6

OSP-GL-0001A, Auxiliary Building Train A Negative Pressure Test, Revision 6

OSP-EJ-P001A, RHR Train A inservice Test - Group A, Revision 44

OSP-EJ-V001B, Residual heat removal Train B valve inservice test, Revision 21

OSP-NE-0001B, Standby Diesel Generator B Periodic Tests, Revision 29

OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting,

Revision 30

Section 2OS1: Access Controls to Radiologically Significant Areas and

Section 2OS2: ALARA Planning and Controls

Callaway Action Requests

200703726 200800631 200800991

200703956 200800632 200801135

200710799 200800633 200801390

200711181 200800727 200801430

200711846 200800838 200802003

200711875 200800887 200802280

200711880 200800888 200803141

200711881 200800891 200803204

200711883 200800957 200803205

200800219 200800973 200803208

200800438 200800988

A-7 Attachment

Audits and Self-Assessments

Quality Assurance Audit of Radiation Protection AP08-001, February 28, 2008

Quality Assurance Supplemental Audit of Radwaste AP07-012, October 30, 2007

Simple Self-assessment Report SA07-RP-S06, January 9, 2008

Radiation Work Permits/ALARA Reviews

RWP 803321RESIN, Transfer Spent Resin from Primary Tank to Liner

ALARA Package 07-03120, Reinstall Bladders into the Recycle Hold Up Tanks

Other/Meetings/Training/Work Review

ALARA Simulator Class

Callaway Plant Long Range Dose and Source Term Reduction Plan, Revision 2

Hot Spot and Shielding Log

Job 08000834 Transfer Spent Resin from Primary Tank to Liner

Plant ALARA Review Committee Meeting

Procedures

APA-ZZ-00405, Special Nuclear Material Control and Accounting, Revision 20

APA-ZZ-01000, Callaway Plant Radiation Protection Program, Revision 26

APA-ZZ-01001, Callaway Plant ALARA Program, Revision 11

APA-ZZ-01106, Lock and Key Control, Revision 16

HDP-ZZ-01100, ALARA Planning and Review, Revision 6

HDP-ZZ-01200, Radiation Work Permits, Revision 9

HTP-ZZ-01203, Radiological Area Access Control, Revision 36

HTP-ZZ-06001, High Radiation/Very High Radiation Area Access, Revision 31

HTP-ZZ-06028, Radiological Controls for Pools that Contain or Store Spent Fuel, Revision 5

RTS-HC-00350, Primary Spent Resin Storage Tank Transfer to Bulk Waste Disposal Station,

Revision 3

Section 4OA1: Performance Indicator Verification

Procedure

NOD-QP-40, NRC Performance Indicator Program, Revision 2

Miscellaneous

Various Callaway Control Room Logs, dated March 2007 through March 2008

Callaway Integrated Inspection Report 05000483/2007002

A-8 Attachment

Callaway Integrated Inspection Report 05000483/2007003

Callaway Integrated Inspection Report 05000483/2007004

Callaway Integrated Inspection Report 05000483/2008002

Section 4OA2: Identification and Resolution of Problems

Inspection Findings

NCV 05000483/2005002-01

NCV 05000483/2006012-04

Callaway Action Requests

200501192 200800355 200804000

200709819 200800522 200804164

200711496 200801270 200805049

200800246 200801529 200805122

200800298 200801830 200808956

Generic Communications

NRC Information Notice 2006-21, OE Regarding Entrainment of Air into Emergency Core

Cooling and Containment Spray Systems, September 21, 2006

Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat

Removal , and Containment Spray Systems, January 11, 2009

Procedures

OTN-EM0001, Safety Injection System, Revision 27

OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting,

Revision 27

Section 4OA5: Other

Procedures

APA-ZZ-01004, Radiological Work Standards, Revision 9

HDP-ZZ-06100, Reactor Building Access, Revision 7

MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22

OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6

OSP-SA-00004, Visual Inspection of Containment for Loose Debris, Revision 19

OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices, Revision 2

Calculations

Calculation BG-75, Impact of MP 06-0003, Replacement Containment Recirculation Sump

Strainers, and MP 06-0027, TSP Basket Relocation, Revision 0

Calculation BN-21, Impact of MP 06-0003, Replacement Containment Recirculation Sump

Strainer on BN21, Revision 0

A-9 Attachment

Calculation BN-22, Impact of MP 06-0003, Replacement Containment Recirculation Sump

Strainer on BN22, Revision 0

Calculation EJ-29, NPSH Margin for RHR Pumps at Transition to Recirculation When NPSH

Margin is at its Minimum Value, Revision 1

Calculation TDI-6002-05/TDI-6003-05, Clean Head Loss - Wolf Creek/Callaway, Revision 0

Callaway Action Request

200800461, Prompt Operability Determination for Containment Spray and Residual Heat

Removal Systems, Revision 0

Miscellaneous

Ameren/UE comments on ECI-PCI-WC-CAL-6002-6003-1001

Callaway Plant Containment Building Latent Debris Assessment Report Refuel 14 Fall 2005

EC-PCI-WC/CAL-6002/6003-1001, AES Calculation No. PCI-5304-S01 Structural Evaluation of

the Containment Sump Strainers, Revision 1

MP 06-0003-EC-PCI-WC-CAL-6002-6003- (000) AES Document No. PCI-5304-S01 Structural

Evaluation of the Containment Sump Strainers, Revision 1

NUREG/CR-6914, Vol. 4, Integrated Chemical Effects Test, Revision 0

SWE07848, Containment Coating Condition Assessment

TDI-6002/TDI-6003, Sure-Flow Suction Strainer Qualification Report and Addendums, Wolf

Creek/Callaway

ULNRC-05124, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 Response To Generic Letter 2004-02, Potential Impact of Debris

Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water

Reactors.

ULNRC-05194, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 September 1, 2005, Response To Generic Letter 2004-02, Potential

Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At

Pressurized-Water Reactors.

ULNRC-05295, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 Response Update To Generic Letter 2004-02, Potential Impact of

Debris Blockage On Emergency Recirculation During Design Basis Accidents At

Pressurized-Water Reactors.

ULNRC-05408, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 Update For Response To Generic Letter 2004-02, Potential Impact

of Debris Blockage On Emergency Recirculation During Design Basis Accidents At

Pressurized-Water Reactors.

A-10 Attachment

ULNRC-05461, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 Request for Extension Of Completion Date For Corrective Actions

Associated with NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On

Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.

ULNRC-05465, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 Supplement to Request for Extension of Corrective Actions

Completion Date For NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On

Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.

WCAP-16568-P, Jet Impingement Testing to Determine the Zone of Influence (ZOI) for

BAQualified/Acceptable Coatings (Proprietary)

Wolf Creek/Callaway Comments on Calculation PCI-5304-S01, Structural Evaluation of the

Containment Sump Strainers.

Section 4OA7: Licensee-Identified Violations

Callaway Action Requests

200802618 200803462 200800461

Generic Communication

Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation

During Design Basis Accidents at Pressurized Water Reactors, dated September 13, 2004

Calculation

TDI-6002-05

Correspondence

Amendment 180 to Facility Operating License NPF-30 from Mr. J. Donohew, Senior Project

Manager, Office of Nuclear Reactor Regulation to Mr. C. Naslund, AmerenUE

Procedure

APA-ZZ-00408, Professional Service Agreements and Nuclear Fuel Contracts, Revision 12

AmerenUE Callaway Plant Nuclear Plant Operating Quality Assurance Manual, Section 3,

Revision 25

Audits

Quality Assurance Audit of Design Control AP08-003

Independent Technical Review Report, SEGR 08-012, Temperature Correction Factor for

Strainer Stack Orifice Head Losses

A-11 Attachment