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{{#Wiki_filter:ACCELERATED DIS RIBUTION DEMONST TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9011060419
{{#Wiki_filter:ACCELERATED DIS RIBUTION DEMONST                                       TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
.DOC.DATE: 90/10/26 NOTARIZED:
ACCESSION NBR:9011060419             . DOC.DATE: 90/10/26         NOTARIZED: NO             DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester                     G   05000244 AUTH. NAME           .AUTHOR AFFILIATION BACKUS,W.H.           Rochester Gas 6 Electric Corp.
NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH.NAME.AUTHOR AFFILIATION BACKUS,W.H.
MECREDY,R.C.         Rochester Gas       & Electric   Corp.
Rochester Gas 6 Electric Corp.MECREDY,R.C.
RECIP.NAME         . RECIPIENT AFFILIATION
Rochester Gas&Electric Corp.RECIP.NAME
.RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 90-012-00:on 900926,turbine trip relay actuation due to dropped flashlight in relay rack.DISTRIBUTION CODE: 1E22T COPIES RECEIVED:LTR ENCL 0 SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
LER   90-012-00:on 900926,turbine dropped   flashlight in relay rack.
D 05000244 A RECIPIENT ID CODE/NAME PD1-3 LA JOHNSON,A INTERNAL: ACNW AEOD/DSP/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFB11 NRR/DREP/PRPB11 NRR/DST/SICB 7E NRR/DST/SRXB 8E'ES/DSIR/EIB EXTERNAL: EGS(G BRYCE,J.H NRC PDR NSIC MURPHY G.A Lid>P>'f8]'/fig 7 COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1'2 2 1 1 1 1 1 1 3 3 1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD AEOD/DOA AEOD/ROAB/DSP NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DST/SELB 8D N T-.~LB8D1 EG FIL~02 G FILE 01 L ST LOBBY WARD NSIC MAYS,G NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1~1 1 1 1 1 1 1 1 D D D NOTE TO ALL"RIDS" RECIPIENTS:
trip    relay actuation  due  to D
D D PLEASE HELP US TO REDUCE WASTETH CONTACT THE DOCUMENT CONTROL DESK ROOM P 1-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 30 ENCL 30 ROCHESTER GAS AND ELECTRIC CORPORATION ROBERT C MECREOY Vice President Clnna Nuclear Production
DISTRIBUTION CODE: 1E22T COPIES RECEIVED:LTR TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
\slee t/t Tears i.~fr sta'st~89 EAST AVENUE, ROCHESTER N.Y.14649-0001 TELEPHONE AAEACODEVte 546 2700 October 26, 1990 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555  
ENCL  0  SIZE:
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).                           05000244 A
RECIPIENT               COPIES            RECIPIENT            COPIES ID CODE/NAME             LTTR ENCL        ID CODE/NAME        LTTR ENCL              D PD1-3 LA                     1      1    PD1-3 PD                  1    1 JOHNSON,A                     1      1                                                    D INTERNAL: ACNW                         2      2    AEOD/DOA                  1    1 AEOD/DSP/TPAB                 1      1    AEOD/ROAB/DSP              2    2 NRR/DET/ECMB 9H               1    '
1    NRR/DET/EMEB 7E            1    1 NRR/DLPQ/LHFB11               1            NRR/DLPQ/LPEB10            1    1 NRR/DREP/PRPB11               2      2    NRR/DST/SELB 8D            1    1
                                                                  ~LB8D1 NRR/DST/SICB 7E NRR/DST/SRXB 8E
          'ES/DSIR/EIB 1
1 1
1 1
1 N
EG G
T-.
FIL   ~
FILE 02 01     ~
1 1
1 1
1 1
EXTERNAL:  EGS(G  BRYCE,J.H              3      3    L ST LOBBY      WARD      1   1 NRC PDR                      1     1     NSIC MAYS,G                1   1 NSIC MURPHY      G.A        1     1     NUDOCS FULL TXT            1   1 Lid>
P>'f8]'/fig 7 D
D D
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTETH CONTACT THE DOCUMENT CONTROL DESK ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR               30   ENCL     30
 
slee t /     t   Tears i.~fr     sta'st ROCHESTER GAS AND ELECTRIC CORPORATION            ~ 89 EAST AVENUE, ROCHESTER N. Y. 14649-0001 ROBERT    C  MECREOY                                                              TELEPHONE Vice President AAEACODEVte 546 2700 Clnna Nuclear Production
                          \
October 26, 1990 U.S. Nuclear Regulatory Commission Document             Control Desk Washington,               DC 20555


==Subject:==
==Subject:==
LER 90-012, Turbine Trip Relay Actuation Due to Dropped Flashlight in Relay Rack (Personnel Error), Causes a Reactor Trip R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires a report of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF)including the Reactor Protec-tion System (RPS)", the attached Licensee Event Report LER 90-012 is hereby submitted.
LER   90-012, Turbine Trip Relay Actuation Due to Dropped Flashlight in Relay Rack         (Personnel Error),
Ve trul y rs, This event has in no way affected the public's health and safety.Robert C.Me redy XC~U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406.Ginna USNRC Senior Resident Inspector 90 f]0!~04 i 9 90$02I PDR ATiOCV 0" t.l00264 PDC NAC tsss NS HAS I LICENSEE EVENT REPORT (LER)IAS.SAJCLSAA ASOULATOA>
Causes a Reactor Trip R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System,             item (a)(2)(iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF) including the Reactor Protec-tion System (RPS)", the attached Licensee Event Report LER 90-012 is hereby submitted.
CSNNS~AttAOVSOOIIS aO.SIN.OIOv SASIASS~4/SII~S IAOILITY NAsss Ill R.E.Ginna Nuclear Power Plant oocAAT NUasssA ol 0 d 0 0 0 24 4 I Of',"~'" Turbine Trip Relay Actuation Due to Dropped F1ashlight in Relay Rack (Personnel Error Causes a Reactor Tri~VSIST OATS ISI LSA NULHSA Hl AStoAT CArs<II 0THAA taclLITlss lssvoLvso HI SSONTH OAY YSA1 YCAA 0926 9090 SSOVSVfSAL
This event has in no way affected the public's health and safety.
+VSS~SA 012~~NONTH 010 OAY 2 6 Y IAA 0~AOUTY NASSSS OOCAST NUssSSAISI 0 S 0 O 0 5 0 0 0 Ota 1 Ar INC~soOS all~Ossl 1 LsvsL 0 9 7",~")pkg+%$+~Y s%SS sSSIal SOAN4IIIII
Ve    trul    y rs, Robert C. Me redy XC ~             U.S. Nuclear Regulatory Commission Region I 475     Allendale Road King of Prussia, PA 19406.
~N.ASS Is I II I II I SS.ANNI II NNI NInIAH SIAN 4l Il I lsl Sa.saalsl N JINI ll I NMWOI, N.T S41 O I I'.TSNIOIISI NTSNIOIIHI N.T SNI O loss N.r SW Ollsl NPSWOIIsal NPSW OIIsHI W N.TSNIOIHHIHI N.T SW Ollal 0 THE AICUIAsHCNrs ot I set 1$: Icasss<<v ss ssNs tI Hs svssssasl III THIS ASIOAT H SUSSSITTSO tUASUANT T lklllal I ATINI OTHSA ISsssAV as Aasvsss~SSHS SSS SS TssL NAC tash ASSAI LICSNSSS CONTACT tOA THH LS1 IISI NAIIS TSLStHONS NUTSO Wesley H.Backus AIISA COOS Technical Assistant to the ations Man 31552-4446~LSTS ONS LINS to1 SACH COaVCNSNT tAILUAS OSSCAISSO IN THH AStOAT II%CAUSS SYSTSII SSANUt AC TUAIA SIOATASLS TO NtAOS SYSTSII COQIONSNT asANU I AC TUN SA StOATAS TO IHAOS 4?Svs&.s ss SUttLSISSNTAL AltOAT S&#xc3;tSCTSO IISI Y SS III tss.sssHNN SAASCTIO SUSasOSICUI OATSI assTAAcr IIJvvs%lsoI NssN.IA, sAAsssssvNst INNse~vssvAHs ltrreettHs Aseat llsl SXtSCTSO~Us as I NI01 OATS Illl NONTH CAY YSAA On September 26, 1990, at 1100 EDST with the reactor at approximately 974 full power, a reactor trip occurred from an opening of the"A" Reactor Trip Breaker, followed in approximately seven (7)seconds by'low pressurizer pressure reactor trip signal and the opening of the"B" Reactor Trip Breaker.The'" Reactor Trip Breaker opening was caused by the inadvertent dropping of a flashlight on two of three turbine autostop trip relays.The low pressurizer pressure reactor trip was caused by the reactor coolant system cooldown due to the reactor being tripped with the turbine still on the line.F Immediate corrective action was to stabilize the plant in hot shutdown.Corrective action to prevent recurrence will be based upon the recommendations of a Human Performance Enhancement System (HPES)evaluation of the dropped flashlight event.Corrective action for subsequent hardware malfunctions will also be taken.
Ginna     USNRC Senior Resident Inspector 90 f ] 0!~04 i 9 90$   02I PDR       ATiOCV 0" t.l00264 PDC
UCENSEE EVENT REPORT{LER)TEXT CONTINUATION UA.NUCLNAh RIOULATOhT C~l&KW AttlKWED OUO HO.31iO&IOI 0 htlh N4."i/all&
 
tACILITY Nets I I I COCKET~lh QI eTA1 Llh MLSlh IO QiQMCNTIAL
NAC tsss NS HAS I                                                                                                                                                     IAS. SAJCLSAA ASOULATOA>CSNNS~
)(p OIOII 1 tAOC Iil R.E.Ginna Nuclear Power Plant TlXT Idssae Nece 4 lese'ee eeeweeel AOC tete~'tl IITI o 5 o o o2 449 0 0 12 00 0 20F I~PRE=-P CONDITIONS The reactor was at approximately 974 steady state full power with no ma)or activities in progress.Electrical Control Configuration Drawing (ECCD)-personnel were performing electrical wire verifications in the RAl Relay Protection Rack.DESCRIPTION OF EVENT A.Dates and approximate times of major occurrences:
AttAOVSOOIIS aO.SIN.OIOv LICENSEE EVENT REPORT (LER)                                                                        SASIASS   ~ 4/SII ~ S IAOILITYNAsss        Ill                                                                                                                       oocAAT NUasssA        ol R.E. Ginna Nuclear Power Plant                                                                                                               0     d     0     0     0     24       4     I Of
.'I o September 26, 1990, 1100 EDST: Event date and time.0 September 26, 1990, 1100 EDST: Discovery date and time.0 0 September 26, 1990, 1100 EDST: Control Room operators verify both reactor tiip breakers open and all control and shutdown rods inserted.September 26, 1990, 1105 EDST: Control Room operators closed both Main Steam Isolation Valves (MSIVs)to terminate plant cooldown.September 26, 1990, 1115 EDST: Plant stabilized at hot, shutdown.B.EVENT: On September 26, 1990,:at 1100 EDST, with the reactor at approximately 974 full power, the Control Room received several annunciator alarms., Most notable of these alarms was the red first out annunciator alarm, K-2 (Rx Trip Breakers Open).%1C t01M teeA l145 I SACILITY NAIIE III UCEN8EE EVENT REPORT ILER)TEXT CONTINUATION DOCKET NLNNEh IEI M$.hUCLEAh hEOULATOhT C~IKIOH ASSAOVED OISE HO.31ED&IOE EKSIKEE: EIBIIEE R.E.Ginna Nuclear gower.Plant TEXT I/mar~e nakeC~~IIIIC Ssrw~WJ IITI 0 5 0-0 0 2 4 YEAA 9 0 LEh WANIh IN EEOUENTIAL 1 0 1 2 SION 1 0 0~AOE (N 03 o~1 1 The Control Room operators immediately checked the reactor trip breaker position indicators and observed-that the>>A>>Reactor Trip Breaker was open and the>>B>>Reactor Trip Breaker.was, still closed.The Reactor Trip Annunciator Panel was also checked at this time for the cause of the trip.There were no annunciators The Control Room operators immediately began verifying the immediate actions of procedure E-0 (Reactor Trip or Safety Injection) from memory as follows: o At least one train of reactor trip breakers open;-The>>A>>Reactor Trip Breaker was open.I o Neutron Flux decreasing o MRPI indicates all control and shutdown rods on the bottom At.this time (i.e.approximately seven (7)seconds into the'event), the Reactor Protection System received a reactor trip signal from low pressurizer pressure.The>>B>>Reactor Trip Breaker opened and the turbine was verified to be tripped.It should be noted here that for the approximately seven (7)seconds, between the>>A>>Reactor Trip Breaker opening until the low pressurizer pressure reactor trip, the turbine was still online at approximately 80%power.This was due to the Turbine Emergency Trip (ET)solenoid valve not functioning
  ',"~'" Turbine Trip Relay Actuation Due                                                     to           Dropped F1ashlight                       in     Relay Rack (Personnel Error                             Causes       a Reactor                     Tri
:.properly when the ET relay received a trip signal.from the>>A>>Reactor Tr'ip Breaker>>open>>contact.The-'low pressurizer pressure reactor trip and the opening of the>>B>>Reactor Trip Breaker subsecpxently tripped the turbine.
      ~ VSIST OATS ISI SSONTH        OAY        YSA1    YCAA LSA NULHSA Hl SSOVSVfSAL
0'hhC terM~041 I OCENSEE EVENT REPORT{LER)TEXT CONTINUATlON UA.NUCLEAh hEOULATOhY COMEOENOH AtttKIV EO OME HO, g I EO~I OE ElltlhEE;E/SIIEE I'ACI LITT NAME I I I DOCKET~Eh tlI LEh NVMEEh IEI~AOE IS R.E.'Ginna Nuclear Power Plant TEKT IS~~M?tE??Eth ow ttEEAMtllthC Pena~'el IITI o so o o2 44 TEAK g, 9 0-~EQVENTIAL M??012 1IOM M 1.0 0 ov 11 With the turbine operating at approximately 804 power and the reactor shutdown (i.e.all shutdown and control rods inserted), a Reactor Coolant System (RCS)cooldown occurred, due to the heat removal imbalance.
                                                      +VSS ~ SA
The level of both steam generators decreased below 164 narrow range level indication for, a short period of time.Level recovery was achieved through the operation of the turbine-driven and motor-driven auxiliary feedwater pumps.The RCS cooldown from the seven (7)second heat imbalance caused RCS temperature to decrease to approximately 535 F, which is about 10 F less than the temperature at stable hot shutdown conditions.
                                                                      ~~       NONTH AStoAT CArs <II OAY             Y IAA 0THAA taclLITlss lssvoLvso HI
The operators, believing a cooldown was still in progress five (5)minutes after the reactor shutdown, followed optional;procedural guidance, and closed both Steam Generator MSIVs.The closed'SIVs, coupled with the turbine trip, mitigated any remaining mechanisms for RCS cooldown, and the plant was stabilized in hot shutdown.This cooldown was also partially due to cooler water being fed to the steam generators by the Auxiliary Feedwater System.Other equipment problems that occurred during the event were: 0 0 The"A" Steam Generator MSIV failed to fully close after receipt of an actuation signal.The valve external indicator'revealed approximately one-quarter of an inch lack of travel from being fully closed.'he valve subsequently closed approximately five minutes after signal receipt.The Intermediate Range Nuclear Instrumentation, Channel N-35, after tracking-identical to Channel N-36, down to approximately 10 amps had its indication rapidly drop below 10 1~amps.The N-35 channel returned to normal approximately ten hours following the trip.The Control Room operators notified higher supervision and'he Nuclear Regulatory Commission (NRC)of the event.MAC fOAM EEEA lE 431 NNC versa~IS4$)FACILITY NANO III\LICENSEE EVENT REPORT ILERI TEXT CONTINUATION OOCIIKT NUMCKII ISI UW NUCLSAII lllOULATOIIY COMMNNON Aft AOVSO OMS NO 3150W104 r S)ttllISS SISI/SS LSII NUiNSN ISI SSOUSNTIAL
                                                                                                                                    ~ AOUTY NASSSS                       OOCAST NUssSSAISI 0     S   0     O 0926 9090                                        012                      010            2 6                  0                                                         0    5   0     0   0 Ota 1 ArINC THIS ASIOAT H SUSSSITTSO tUASUANT T 0 THE AICUIAsHCNrs ot                        I set 1 $: Icasss  <<v ss  ssNs tI Hs  svssssasl    III
'.>ASVNION N M II"~N M~AOS ISIR.E.Ginna Nuclear Power Plant TEXT IS tllNO~N~~OJ45asV NIIC AnM~SI I Ill o 5 o o o 2 4 4 0-0 1 2 000 5 OF C~INOPERABLE STRUCTURES
        ~ soOS all SS  sSSIal                                Sa.saalsl                                      N.T SNI O loss                                  lklllal
~COMPONENTS
    ~ Ossl 1                         SOAN4IIIII~                                NJINI llI                                      N.rSW Ollsl                                    IATINI LsvsL          0     9 7         N.ASS Is I II I III                        NMWOI,                                          NPSWOIIsal                                      OTHSA ISsssAV as Aasvsss
/OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None D.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: None E~METHOD OF DISCOVERY:
                                                                                                                                                                                  ~SSHS SSS SS TssL NAC tash SS.ANNI II NNI                             N.T S41 O II                                    NPSW OIIsHIW                                    ASSAI NInIAH                                          '.TSNIOIISI N.TSNIOIHHIHI
The event was immediately apparent due to alarms and indications in the Control Room.F.OPERATOR ACTION: After the reactor trip, the Control Room operators performed the actions of Emergency Operating Procedures E-O, (Reactor Trip or Saf ety Zng ection)and ES-O.l, (Reactor Trip Response)and stabilized the plant.The MSZVs were closed approximately five (5)minutes'after the trip to prevent further plant cooldown.G.SAFETY SYSTEM RESPONSE: None IIZ.CAUSE OF EVENT A.IMMEDIATE CAUSE: The'eactor trip occurred due to the"A" Reactor Trip Breaker opening.B.INTERMEDIATE CAUSE: The"A" Reactor Trip Breaker opening was due to the bumping, of two turbine autostop trip (AST)relays in the RAl Relay Rack.This bumping occurred from a smail flashlight (powered by"AA" batteries) that was 1 NAC AOAM SSSA I$4$l NRC eerro 9$9A (9491\~US.NUCLEAR REOULATORY COMMIEEION LICENSEE EVENT REPORT ILERI TEXT CONTINUATION
      ", ~" )pkg+%$+~Y s%
'eehovEo oME'No.$1$C~ICI EX91RE$"9191/9$eACILITY NAME I'l OOCKET NUMOER QI LER NINER IEI H.E.Ginna Nuclear Power Plant" o s o o o 2 4 4 TExT II1 more RMoe o terhreerE oee Iroerenor Hrrlc Fdic@99EAOI I ITI YEAR 9 0-I 9 QU 9 N'Fl A L 4 M O 1 2 OEVrorOH 4 M-00 06 OF being used by an ECCD person..While performing electrical wire verifications, the flashlight was accidently dropped and fell onto the relays.A normal actuation of the two relays would result in , actuation of both trains of logic'(i.e.opening of both reactor trip breakers and subsequent turbine trip)as each relay has an"A" and"B" train contact.The postulated cause for actuation of only one.train of logic, ("A" Train Reactor Trip Breaker)is that the bumping effect was such that localized chatter of only the"A" train contacts occurred.The logic for., reactor trip is the actuation of at least two out of the three AST relays.Later testing confirmed that,:-if normally actuated, the"B" train trip signal AST.circuit would operate properly.C.ROOT CAUSE: The accidental dropping of the flashlight that bumped the relays was a personnel error.IV ANALYSIS OF EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires reporting of"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)," in that the"A" Reactor Trip Breaker opening and subsequent Low Pressurizer Pressure Reactor-Trip was an automatic actuation of the RPS.An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
SIAN 4l IlI lsl                            NTSNIOIIHI                                      N.T SW Ollal LICSNSSS CONTACT tOA THH LS1                IISI NAIIS                                                                                                                                                                    TSLStHONS NUTSO Wesley H. Backus                                                                                                                               AIISA COOS Technical Assistant to the                                               ations                   Man                                           31552                               -4446
o When initiated by an input signal, the two reactor trip breakers opened as required.41C eORM$$OA r94$1 eQ p'wH 0 NRC Pens 999A 043)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION Ug.NUCLfAR Rf4ULATORY COMMCSION APPROYfO OM9 NO.3194M10e f RPIRf 9: 9l9 I I99 I'ACILITY NAMf 111 OOCKf T NUM9 f R Ill Lfh NUMhfh IQ II QUA NTIAL N YNIOS H N PA4f 191 R.E.Ginna Nuclear.Power Plant~(SsNN NNee N Nfsleh eM eAWosel WIC Pens~'II 11Tl o s o o o 244 90 1 2 00 07 o~1 1 o All control and shutdown rods inserted to shut the.reactor down as designed.o The plant was quickly stabilized in hot shutdown.This transient was compared to'ncrease in decay heat removal transients in the Ginna Updated Final Safety Analysis(UFSAR).None of the assumptions of the UFSAR were violated during the event.The resultant cooldown from the reactor trip-and the turbine remaining on line caused pressurizer pressure to decrease rapidly.The rate sensitive low pressurizer pressure trip caused'reactor trip, opening the"B" Reactor Trip Breaker.The opening-: of the"B" Reactor Trip Breaker caused the turbine to trip.The following factors led to the cooldown, as compared with the cooldown expected following a normal reactor trip: o Failure of the 20 ET solenoid to trip the turbine when the"A" Reactor Trip Breaker opened.Reactor trip without turbine trip caused the RCS to cooldown to approximately 535 F.o.Lo Lo level on both steam generators caused the turbine driven auxiliary feedwater pump to start.Steam extracted from the header by the turbine driven auxiliary feedwater pump contributed to the cooldown.o Total auxiliary feedwater flow of greater than 470 gallons per minute per steam generator-also contributed to the cooldown.Due to the above circumstances, the cooldown of the RCS to approximately 535 F is not unexpected.
                                                  ~LSTS         ONS LINS to1 SACH COaVCNSNT tAILUAS OSSCAISSO IN THH AStOAT                       II%
This cooldown is bounded by plant accident analysis and does not exceed the technical specification limit of 100oF per hour.Additional protection is provided by closure of the MSZVs.Based on the above, it can be concluded that the public health and safety was assured at all times.nsc PQRM 9ee*19491  
CAUSS       SYSTSII                         SSANUt AC           SIOATASLS SYSTSII     COQIONSNT           asANU ACI              StOATAS TUAIA            TO NtAOS                                                                              TUN SA               TO IHAOS 4?Svs&. s ss SUttLSISSNTAL AltOAT S&#xc3;tSCTSO IISI                                                                                                 NONTH      CAY    YSAA SXtSCTSO
~~~y~I I I I I I~i i i i i i~~~i~~~~~II~~~~II 0~~~~~~~~~~II~~~~II~~0~~~~~~~I~~~~~~~~~~~~0~~ll~II~~~11~~11~II~~~~0 0~~~~4 II~0 II~Il~~I~~4~~I~
                                                                                                                                                            ~ Us as I NI01 OATS    Illl Y SS   III tss. sssHNN SAASCTIO SUSasOSICUI OATSI assTAAcr IIJvvs       % lsoI NssN. IA, sAAsssssvNst     INNse ~ vssvAHs ltrreettHs Aseat llsl On         September                         26, 1990, at 1100 EDST with the reactor at approximately 974 full power, a reactor trip occurred from an opening of the "A" Reactor                                               Trip Breaker, followed in approximately seven (7) seconds by '                                                   low pressurizer pressure reactor trip signal and the opening of the "B" Reactor Trip Breaker.
MAC tSNS SSSA NSS)L'ICENSEE EVENT REPORT (LERI TEXT CONTINUATION US.NUCLtAA AlOULATOAY COSSSIISSION AttAOVSD OSIS NO JISOWIOS tlItIASS: SQI ISS tACILITY AASSS Ill OOCKST IIU~SA ITI LtA IIUSSSSA Itl~SOVSNTIAL N V II VISION V N~Aot ISI R.E.Ginna Nuclear%?ower Plant TECT II'INSIS DISCS~ISSVSSA SSS SASSSASI lYAC ANN~'Sl IITI 0 5 0 0 0 2 4 4 9 0.0 1 2-0009 OF 0 valve shaft due'o the valve packing.Both MSZV's were stroked several times to ensure aperability and adequate closure capability.
The         '"       Reactor Trip Breaker opening was caused by the inadvertent dropping of a flashlight on two of three turbine autostop trip relays. The low pressurizer pressure reactor trip was caused by the reactor coolant system cooldown due to the reactor being tripped with the turbine                                               still                   on the line.
Results of these tests, support the conclusian that failure of the"A"-MSZV to fully seat during the plant trip was not due to internal valve distortion and bending, but was the result of a lack of flow across the valve disc.Failure to close is attributed to.the closure operation occurring in a quiescent environment.
F Immediate corrective action was to stabilize the plant in hot shutdown.                       Corrective action to prevent recurrence will be based upon the recommendations of a Human Performance Enhancement System (HPES) evaluation of the dropped flashlight event.                                                                                                                 Corrective action for subsequent hardware malfunctions will also be taken.
Valve closure was dependent solely upon two factors: the moment developed by the weight of the valve disc, and the spring pravided to,-assist in, valve closure.Without the additional assistance of steam flow across the valve disc;the valve was not capable af completing its closing operation.
 
Based upon valve seat area, a one (1)psi differential across the valve seat would develop a moment oi approximately 450 ft-lbs.This moment is comparable to the moment developed by the weight of'he valve disc in its closed position.For all design basis accidents where MSIV closure is required, the accident transient would develop a large enough differen-tial pressure to obtain complete valve closure.We are evaluating various packing materials which have a low friction coefficient and can perform the sealing function.As the Intermediate Range NZS Channel N-35 tracked NIS Channel N-36 for its normal operating range and returned to normal'pproximately ten (10)hours after the trip, no.immediate.action was deemed necessary.
UA. NUCLNAh RIOULATOhT C~l&KW UCENSEE EVENT REPORT {LER) TEXT CONTINUATION                                AttlKWEDOUO      HO. 31iO&IOI 0 htlh N4."i/all&
Specific logarithmic amplifier idle current adjustments internal to the PC card are being considered to correct NIS Channel N-35 response below 10 10 amps.Westing-house personnel were contacted, and they confirmed potential impact af the amplifier idle'current on channel autput, and that this output does not affect the safety function of the Intermediate NAC SOAIS SSSA 19491  
tACILITYNets I I I                                           COCKET ~lh   QI               Llh MLSlh IO                       tAOC Iil eTA1    QiQMCNTIAL )(p       OIOII 1
~~I I I I~I'I I I I~~~~~~11~~~0~~~~~0~~0~~0~~~0~I II I~II~~~~~~~~~~~II II~~~II 4~~~~0~~~~~0~~~~~~~~'~~~~I~~~~~~~~11~~~~~  
R.E. Ginna Nuclear Power Plant                             o  5  o o  o2 449      0    0    12            00      0    20F TlXT Idssae Nece 4 lese'ee eeeweeel AOC tete ~'tl IITI I ~          PRE=                 -P         CONDITIONS The       reactor was at approximately 974 steady state full power         with no ma)or activities in progress.                               Electrical Control Configuration Drawing (ECCD) - personnel were performing electrical wire verifications in the RAl Relay Protection Rack.
~~~~~~~~~~~I I I I~~I I~II~~~0~~~~~~~~II~~~II~~~e~~t~~0 I 0 0}}
DESCRIPTION OF EVENT A.         Dates and approximate times                 of major occurrences:
                                                                                                                                        .'I o         September       26, 1990,       1100 EDST:         Event date and time.
0         September       26, 1990,       1100 EDST:         Discovery date and     time.
0         September       26,     1990,   1100   EDST:         Control             Room operators verify both reactor and     all control       and shutdown tiip breakers rods inserted.
open September       26,     1990,   1105 EDST:             Control Room operators         closed       both Main Steam Isolation Valves (MSIVs) to terminate plant cooldown.
0        September 26, 1990, 1115 EDST: Plant stabilized at     hot, shutdown.
B.         EVENT:
On     September 26, 1990,:at 1100 EDST, with the reactor at approximately               974   full   power, the Control Room received several annunciator alarms., Most notable of these alarms was the               red first out       annunciator alarm, K-2 (Rx Trip Breakers Open).
%1C   t01M teeA l145 I
 
M$. hUCLEAh hEOULATOhT C~IKIOH UCEN8EE EVENT REPORT ILER) TEXT CONTINUATION                             ASSAOVED OISE HO. 31ED&IOE EKSIKEE: EIBIIEE SACILITY NAIIE III                                      DOCKET NLNNEh IEI LEh WANIh IN                  ~ AOE (N YEAA    EEOUENTIAL      SION 1            1 TEXT I/mar      e nakeC ~ ~
R.E. Ginna Nuclear gower. Plant
          ~                IIIICSsrw ~WJ IITI 0   5   0-0   0 2   4 9 0       0 1   2   0 0       03     o~1   1 The     Control Room operators immediately checked the reactor         trip breaker position indicators and observed-that the >>A>> Reactor Trip Breaker was open and the >>B>>
Reactor Trip Breaker .was, still closed.                           The Reactor Trip Annunciator Panel was also checked at this time for the cause of the trip. There were no annunciators The     Control Room operators immediately began verifying the immediate actions of procedure E-0 (Reactor Trip or Safety Injection) from memory as follows:
o       At least one train of reactor trip breakers open;
                                          - The >>A>> Reactor Trip Breaker was open.
I o       Neutron Flux decreasing o       MRPI     indicates       all control       and shutdown rods on the bottom At. this time (i.e. approximately seven (7) seconds into the 'event), the Reactor Protection System received a reactor trip signal from low pressurizer pressure.           The >>B>> Reactor Trip Breaker opened and the turbine was verified to be tripped.
It     should be noted here that for the approximately seven         (7) seconds, between the >>A>> Reactor Trip Breaker opening until the low pressurizer pressure reactor approximately trip, 80%
the power.
turbine     was       still This was due to the Turbine online            at Emergency Trip (ET) solenoid valve not functioning
:.properly when the ET relay received a trip signal
                            . from the >>A>> Reactor Tr'ip Breaker >>open>> contact.                                     The
                            - 'low pressurizer pressure reactor trip and the opening of the >>B>> Reactor Trip Breaker subsecpxently tripped the turbine.
 
                                                                                                                                '
0 hhC terM 041 I
                ~                OCENSEE EVENT REPORT {LER) TEXT CONTINUATlON UA. NUCLEAh hEOULATOhY COMEOENOH AtttKIVEO  OME HO, g I EO~I OE ElltlhEE; E/SIIEE I'ACI LITT NAME I I I                                   DOCKET ~Eh tlI             LEh NVMEEh IEI                     ~ AOE IS TEAK g, ~ EQVENTIAL M  ??
1IOM M 1 R.E.'Ginna Nuclear Power Plant TEKT       ~
IS~ M?tE??Eth ow ttEEAMtllthCPena ~'el IITI o so o o2       44 9 0012                .0 0               ov   11 With the turbine operating at approximately 804 power and the reactor shutdown (i.e. all shutdown and control rods inserted), a Reactor Coolant System (RCS) cooldown occurred,               due to the heat removal imbalance.           The level of both steam generators decreased below 164 narrow range level indication for, a short period of time.             Level recovery was achieved through the operation of the turbine-driven and motor-driven auxiliary feedwater pumps.                                 The RCS cooldown from the seven (7) second heat imbalance caused RCS temperature to decrease to approximately 535 F, which is about 10 F less than the temperature at stable hot shutdown conditions.                       The operators, believing a cooldown was still in progress five (5) minutes after the reactor shutdown, followed optional; procedural guidance, and closed both Steam Generator MSIVs.         The closed'SIVs, coupled with the turbine trip, mitigated any remaining mechanisms for RCS cooldown, and the plant was stabilized in hot shutdown.         This cooldown was also partially due to cooler water being fed to the steam generators by the Auxiliary Feedwater           System.
Other equipment problems that occurred during the event were:
0       The "A" Steam Generator MSIV failed to fully close after receipt of an actuation signal. The valve external indicator 'revealed approximately one-quarter of an inch lack of travel from being fully closed. 'he valve subsequently closed approximately five minutes after signal receipt.
0        The Intermediate Range Nuclear Instrumentation, Channel     N-35, after tracking -identical to Channel N-36, down to approximately 10                                 amps had its indication rapidly drop below 10 1~
amps.       The N-35 channel returned to normal approximately ten hours following the trip.
The Control Room operators notified higher supervision and 'he Nuclear Regulatory Commission (NRC) of the event.
MAC fOAM EEEA lE 431
 
NNC versa IS4$ )
                ~            \                                                                 UW NUCLSAII lllOULATOIIYCOMMNNON LICENSEE EVENT REPORT ILERI TEXT CONTINUATION                             AftAOVSO OMS rNO    3150W104 S)ttllISS SISI/SS FACILITYNANO III                                OOCIIKT NUMCKII ISI LSII NUiNSN ISI                      ~ AOS ISI SSOUSNTIAL   '. >
                                                                                                      "~      ASVNION N M   II           N M TEXT IS tllNO ~ ~~
R.E. Ginna Nuclear Power Plant N   OJ45asV NIIC AnM ~SI I Ill o   5   o o   o 2   4 4   0 0     1 2               000       5 OF C~         INOPERABLE STRUCTURES ~ COMPONENTS /                   OR     SYSTEMS               THAT CONTRIBUTED TO THE EVENT:
None D.         OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None E~         METHOD OF DISCOVERY:
The event was immediately apparent                   due     to alarms                 and indications in the Control               Room.
F.         OPERATOR ACTION:
After the reactor trip, the Control Room operators performed the actions of Emergency Operating Procedures E-O, (Reactor Trip or Saf ety Zng ection) and ES-O. l, (Reactor Trip Response) and stabilized the plant.
The MSZVs were closed approximately five (5) minutes
                                  'after the trip to prevent further plant cooldown.
G.         SAFETY SYSTEM RESPONSE:
None IIZ. CAUSE OF EVENT A.         IMMEDIATE CAUSE:
The'eactor     trip   occurred due to the "A" Reactor Trip Breaker opening.
B.         INTERMEDIATE CAUSE:
The "A" Reactor       Trip Breaker opening was due to the bumping, of two turbine autostop trip (AST) relays in the RAl Relay Rack.                   This bumping occurred from a smail flashlight (powered by "AA" batteries) that was                   1 NAC AOAM SSSA I$ 4$ l
 
NRC eerro 9$ 9A                         \~                                                                             US. NUCLEAR REOULATORY COMMIEEION (9491 LICENSEE EVENT REPORT ILERI TEXT CONTINUATION                           'eehovEo               oME'No. $ 1$ C~ICI EX91RE$ "9191/9$
eACILITY NAME I'l                                                           OOCKET NUMOER QI LER NINER IEI YEAR  I9 QU 9 N'Fl A L 4 M O OEVrorOH 4 M H.E. Ginna Nuclear Power Plant TExT II1 more RMoe o terhreerE
                                                                              "
o   s   o o   o 2 4 4 9  0        1 2        00 06                OF oee Iroerenor Hrrlc Fdic@ 99EAOI I ITI being used                 by an       ECCD     person.. While performing electrical wire verifications, the flashlight was accidently dropped and fell onto the relays.                                                         A normal actuation of the two relays would result in
                                                ,
actuation of both trains of logic '(i.e. opening of both reactor trip breakers and subsequent turbine trip) as each relay has an "A" and "B" train contact.
The postulated cause for actuation of only one .train of logic, ("A" Train Reactor Trip Breaker) is that the bumping effect was such that localized chatter of only the "A" train contacts occurred. The logic for.,
reactor trip is the actuation of at least two out of the three AST relays. Later testing confirmed that,:-
if normally actuated, the "B" train trip signal AST.
circuit               would operate properly.
C.         ROOT CAUSE:
The         accidental dropping of the flashlight that                                   bumped the relays was a personnel error.
IV             ANALYSIS OF EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires reporting of "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)," in that the "A" Reactor Trip Breaker opening and subsequent Low Pressurizer Pressure Reactor -Trip was an automatic actuation of the RPS.
An assessment                         was performed         considering both the safety consequences                         and   implications of this event with the following results                       and conclusions:
o             When           initiated         by an input signal,             the two reactor trip         breakers opened as required.
41C eORM     $ $ OA r94$ 1
 
eQ p'wH 0
NRC Pens 999A                                                                                   Ug. NUCLfAR Rf4ULATORY COMMCSION 043)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                       APPROYfO OM9 NO. 3194M10e f RPIRf 9: 9l9 I I99 I'ACILITYNAMf 111                                         OOCKfT NUM9 fR Ill         Lfh NUMhfh IQ                       PA4f 191 IIQUANNTIAL        YNIOS H N Ginna Nuclear .Power Plant                                       244 90
    ~ R.E.(SsNN NNee N Nfsleh eM eAWosel WIC Pens ~'II11Tl o s   o o   o                 1 2         00 07             o~ 1 1 o         All control       and shutdown rods inserted to shut the.
reactor down as designed.
o         The plant was quickly stabilized in hot shutdown.
This transient was compared to 'ncrease in decay heat removal transients in the Ginna Updated Final Safety Analysis (UFSAR). None of the assumptions of the UFSAR were violated during the event.                       The resultant cooldown from the reactor trip -and the turbine remaining on line caused pressurizer pressure to decrease rapidly. The rate sensitive low pressurizer pressure trip caused'                                     reactor trip, opening             the "B" Reactor Trip Breaker. The opening-:
of the "B" Reactor Trip Breaker caused the turbine to trip.
The following factors led to the cooldown, as compared with the cooldown expected following a normal reactor trip:
o         Failure of the 20 ET solenoid to trip the turbine when the "A" Reactor Trip Breaker opened.                                 Reactor trip without turbine trip caused the RCS to cooldown to approximately 535 F.
o   . Lo Lo level on both steam generators                           caused the turbine driven auxiliary feedwater pump to start.
Steam extracted from the header by the turbine driven auxiliary feedwater pump contributed to the cooldown.
o         Total auxiliary feedwater flow of greater than 470 gallons per minute per steam generator-also contributed to the cooldown.
Due to the above circumstances, the cooldown of the RCS to approximately 535 F is not unexpected.                       This cooldown is bounded by plant accident analysis and does not exceed the technical specification limit of 100oF per hour. Additional protection is provided by closure of the MSZVs.
Based on the above, it can be concluded that the public health and safety was assured at all times.
nsc   PQRM 9ee*
19491
 
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MAC tSNS SSSA                                                                                             US. NUCLtAA AlOULATOAYCOSSSIISSION NSS)
L'ICENSEE EVENT REPORT (LERI TEXT CONTINUATION                           AttAOVSD OSIS NO JISOWIOS tlItIASS: SQI ISS tACILITYAASSS      Ill                                           OOCKST IIU~SA ITI           LtA IIUSSSSA Itl                   ~ Aot ISI
                                                                                                    ~ SOVSNTIAL           VISION N V   II           V   N R.E. Ginna Nuclear%?ower Plant TECT II'INSIS DISCS ~ ISSVSSA     SASSSASI lYAC ANN ~'Sl IITI 0   5   0 0   0 2 4 4 9 0. 0 1       2 0009                   OF SSS valve shaft due         'o   the valve packing.
MSZV's were stroked several times to ensure Both aperability and adequate closure capability.
Results of these tests, support the conclusian that failure of the "A" -MSZV to fully seat during the plant trip was not due to internal valve distortion and bending, but was the result of a lack of flow across the valve disc.
Failure to close is attributed to .the closure operation occurring in a quiescent environment.
Valve closure was dependent solely upon two factors: the moment developed by the weight of the valve disc, and the spring pravided to,-
assist in,valve closure. Without the additional assistance of steam flow across the valve disc; the valve was not capable af completing its closing operation. Based upon valve seat area, a one (1) psi differential across the valve seat would develop a moment oi approximately 450 ft-lbs. This moment is comparable to the moment developed by the weight of'he valve disc in its closed position. For all design basis accidents where MSIV closure is required, the accident transient would                   a large enough differen-tial pressure todevelop  obtain complete valve closure.
We are   evaluating various packing materials which have a low friction coefficient and can perform the sealing function.
0        As the Intermediate Range NZS Channel N-35 tracked NIS Channel N-36 for its normal operating range and returned to normal'pproximately ten (10) hours after the trip, no .immediate .action was deemed       necessary.         Specific logarithmic amplifier idle current adjustments internal to the PC card are being considered to correct NIS Channel N-35 response below 10 10 amps. Westing-house personnel were contacted, and they confirmed potential impact af the amplifier idle 'current on channel autput, and that this output does not affect the safety function of the Intermediate NAC SOAIS SSSA 19491
 
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Revision as of 17:44, 29 October 2019

LER 90-012-00:on 900926,turbine Trip Relay Actuation Due to Dropped Flashlight in Relay rack.W/901026 Ltr
ML17262A217
Person / Time
Site: Ginna Constellation icon.png
Issue date: 10/26/1990
From: Backus W, Mecredy R
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-90-012, LER-90-12, NUDOCS 9011060419
Download: ML17262A217 (13)


Text

ACCELERATED DIS RIBUTION DEMONST TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9011060419 . DOC.DATE: 90/10/26 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME .AUTHOR AFFILIATION BACKUS,W.H. Rochester Gas 6 Electric Corp.

MECREDY,R.C. Rochester Gas & Electric Corp.

RECIP.NAME . RECIPIENT AFFILIATION

SUBJECT:

LER 90-012-00:on 900926,turbine dropped flashlight in relay rack.

trip relay actuation due to D

DISTRIBUTION CODE: 1E22T COPIES RECEIVED:LTR TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

ENCL 0 SIZE:

NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 A

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL D PD1-3 LA 1 1 PD1-3 PD 1 1 JOHNSON,A 1 1 D INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DET/ECMB 9H 1 '

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NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTETH CONTACT THE DOCUMENT CONTROL DESK ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 30 ENCL 30

slee t / t Tears i.~fr sta'st ROCHESTER GAS AND ELECTRIC CORPORATION ~ 89 EAST AVENUE, ROCHESTER N. Y. 14649-0001 ROBERT C MECREOY TELEPHONE Vice President AAEACODEVte 546 2700 Clnna Nuclear Production

\

October 26, 1990 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Subject:

LER 90-012, Turbine Trip Relay Actuation Due to Dropped Flashlight in Relay Rack (Personnel Error),

Causes a Reactor Trip R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF) including the Reactor Protec-tion System (RPS)", the attached Licensee Event Report LER 90-012 is hereby submitted.

This event has in no way affected the public's health and safety.

Ve trul y rs, Robert C. Me redy XC ~ U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406.

Ginna USNRC Senior Resident Inspector 90 f ] 0!~04 i 9 90$ 02I PDR ATiOCV 0" t.l00264 PDC

NAC tsss NS HAS I IAS. SAJCLSAA ASOULATOA>CSNNS~

AttAOVSOOIIS aO.SIN.OIOv LICENSEE EVENT REPORT (LER) SASIASS ~ 4/SII ~ S IAOILITYNAsss Ill oocAAT NUasssA ol R.E. Ginna Nuclear Power Plant 0 d 0 0 0 24 4 I Of

',"~'" Turbine Trip Relay Actuation Due to Dropped F1ashlight in Relay Rack (Personnel Error Causes a Reactor Tri

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SIAN 4l IlI lsl NTSNIOIIHI N.T SW Ollal LICSNSSS CONTACT tOA THH LS1 IISI NAIIS TSLStHONS NUTSO Wesley H. Backus AIISA COOS Technical Assistant to the ations Man 31552 -4446

~LSTS ONS LINS to1 SACH COaVCNSNT tAILUAS OSSCAISSO IN THH AStOAT II%

CAUSS SYSTSII SSANUt AC SIOATASLS SYSTSII COQIONSNT asANU ACI StOATAS TUAIA TO NtAOS TUN SA TO IHAOS 4?Svs&. s ss SUttLSISSNTAL AltOAT SÃtSCTSO IISI NONTH CAY YSAA SXtSCTSO

~ Us as I NI01 OATS Illl Y SS III tss. sssHNN SAASCTIO SUSasOSICUI OATSI assTAAcr IIJvvs  % lsoI NssN. IA, sAAsssssvNst INNse ~ vssvAHs ltrreettHs Aseat llsl On September 26, 1990, at 1100 EDST with the reactor at approximately 974 full power, a reactor trip occurred from an opening of the "A" Reactor Trip Breaker, followed in approximately seven (7) seconds by ' low pressurizer pressure reactor trip signal and the opening of the "B" Reactor Trip Breaker.

The '" Reactor Trip Breaker opening was caused by the inadvertent dropping of a flashlight on two of three turbine autostop trip relays. The low pressurizer pressure reactor trip was caused by the reactor coolant system cooldown due to the reactor being tripped with the turbine still on the line.

F Immediate corrective action was to stabilize the plant in hot shutdown. Corrective action to prevent recurrence will be based upon the recommendations of a Human Performance Enhancement System (HPES) evaluation of the dropped flashlight event. Corrective action for subsequent hardware malfunctions will also be taken.

UA. NUCLNAh RIOULATOhT C~l&KW UCENSEE EVENT REPORT {LER) TEXT CONTINUATION AttlKWEDOUO HO. 31iO&IOI 0 htlh N4."i/all&

tACILITYNets I I I COCKET ~lh QI Llh MLSlh IO tAOC Iil eTA1 QiQMCNTIAL )(p OIOII 1

R.E. Ginna Nuclear Power Plant o 5 o o o2 449 0 0 12 00 0 20F TlXT Idssae Nece 4 lese'ee eeeweeel AOC tete ~'tl IITI I ~ PRE= -P CONDITIONS The reactor was at approximately 974 steady state full power with no ma)or activities in progress. Electrical Control Configuration Drawing (ECCD) - personnel were performing electrical wire verifications in the RAl Relay Protection Rack.

DESCRIPTION OF EVENT A. Dates and approximate times of major occurrences:

.'I o September 26, 1990, 1100 EDST: Event date and time.

0 September 26, 1990, 1100 EDST: Discovery date and time.

0 September 26, 1990, 1100 EDST: Control Room operators verify both reactor and all control and shutdown tiip breakers rods inserted.

open September 26, 1990, 1105 EDST: Control Room operators closed both Main Steam Isolation Valves (MSIVs) to terminate plant cooldown.

0 September 26, 1990, 1115 EDST: Plant stabilized at hot, shutdown.

B. EVENT:

On September 26, 1990,:at 1100 EDST, with the reactor at approximately 974 full power, the Control Room received several annunciator alarms., Most notable of these alarms was the red first out annunciator alarm, K-2 (Rx Trip Breakers Open).

%1C t01M teeA l145 I

M$. hUCLEAh hEOULATOhT C~IKIOH UCEN8EE EVENT REPORT ILER) TEXT CONTINUATION ASSAOVED OISE HO. 31ED&IOE EKSIKEE: EIBIIEE SACILITY NAIIE III DOCKET NLNNEh IEI LEh WANIh IN ~ AOE (N YEAA EEOUENTIAL SION 1 1 TEXT I/mar e nakeC ~ ~

R.E. Ginna Nuclear gower. Plant

~ IIIICSsrw ~WJ IITI 0 5 0-0 0 2 4 9 0 0 1 2 0 0 03 o~1 1 The Control Room operators immediately checked the reactor trip breaker position indicators and observed-that the >>A>> Reactor Trip Breaker was open and the >>B>>

Reactor Trip Breaker .was, still closed. The Reactor Trip Annunciator Panel was also checked at this time for the cause of the trip. There were no annunciators The Control Room operators immediately began verifying the immediate actions of procedure E-0 (Reactor Trip or Safety Injection) from memory as follows:

o At least one train of reactor trip breakers open;

- The >>A>> Reactor Trip Breaker was open.

I o Neutron Flux decreasing o MRPI indicates all control and shutdown rods on the bottom At. this time (i.e. approximately seven (7) seconds into the 'event), the Reactor Protection System received a reactor trip signal from low pressurizer pressure. The >>B>> Reactor Trip Breaker opened and the turbine was verified to be tripped.

It should be noted here that for the approximately seven (7) seconds, between the >>A>> Reactor Trip Breaker opening until the low pressurizer pressure reactor approximately trip, 80%

the power.

turbine was still This was due to the Turbine online at Emergency Trip (ET) solenoid valve not functioning

.properly when the ET relay received a trip signal

. from the >>A>> Reactor Tr'ip Breaker >>open>> contact. The

- 'low pressurizer pressure reactor trip and the opening of the >>B>> Reactor Trip Breaker subsecpxently tripped the turbine.

'

0 hhC terM 041 I

~ OCENSEE EVENT REPORT {LER) TEXT CONTINUATlON UA. NUCLEAh hEOULATOhY COMEOENOH AtttKIVEO OME HO, g I EO~I OE ElltlhEE; E/SIIEE I'ACI LITT NAME I I I DOCKET ~Eh tlI LEh NVMEEh IEI ~ AOE IS TEAK g, ~ EQVENTIAL M  ??

1IOM M 1 R.E.'Ginna Nuclear Power Plant TEKT ~

IS~ M?tE??Eth ow ttEEAMtllthCPena ~'el IITI o so o o2 44 9 0012 .0 0 ov 11 With the turbine operating at approximately 804 power and the reactor shutdown (i.e. all shutdown and control rods inserted), a Reactor Coolant System (RCS) cooldown occurred, due to the heat removal imbalance. The level of both steam generators decreased below 164 narrow range level indication for, a short period of time. Level recovery was achieved through the operation of the turbine-driven and motor-driven auxiliary feedwater pumps. The RCS cooldown from the seven (7) second heat imbalance caused RCS temperature to decrease to approximately 535 F, which is about 10 F less than the temperature at stable hot shutdown conditions. The operators, believing a cooldown was still in progress five (5) minutes after the reactor shutdown, followed optional; procedural guidance, and closed both Steam Generator MSIVs. The closed'SIVs, coupled with the turbine trip, mitigated any remaining mechanisms for RCS cooldown, and the plant was stabilized in hot shutdown. This cooldown was also partially due to cooler water being fed to the steam generators by the Auxiliary Feedwater System.

Other equipment problems that occurred during the event were:

0 The "A" Steam Generator MSIV failed to fully close after receipt of an actuation signal. The valve external indicator 'revealed approximately one-quarter of an inch lack of travel from being fully closed. 'he valve subsequently closed approximately five minutes after signal receipt.

0 The Intermediate Range Nuclear Instrumentation, Channel N-35, after tracking -identical to Channel N-36, down to approximately 10 amps had its indication rapidly drop below 10 1~

amps. The N-35 channel returned to normal approximately ten hours following the trip.

The Control Room operators notified higher supervision and 'he Nuclear Regulatory Commission (NRC) of the event.

MAC fOAM EEEA lE 431

NNC versa IS4$ )

~ \ UW NUCLSAII lllOULATOIIYCOMMNNON LICENSEE EVENT REPORT ILERI TEXT CONTINUATION AftAOVSO OMS rNO 3150W104 S)ttllISS SISI/SS FACILITYNANO III OOCIIKT NUMCKII ISI LSII NUiNSN ISI ~ AOS ISI SSOUSNTIAL '. >

"~ ASVNION N M II N M TEXT IS tllNO ~ ~~

R.E. Ginna Nuclear Power Plant N OJ45asV NIIC AnM ~SI I Ill o 5 o o o 2 4 4 0 0 1 2 000 5 OF C~ INOPERABLE STRUCTURES ~ COMPONENTS / OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:

None D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:

None E~ METHOD OF DISCOVERY:

The event was immediately apparent due to alarms and indications in the Control Room.

F. OPERATOR ACTION:

After the reactor trip, the Control Room operators performed the actions of Emergency Operating Procedures E-O, (Reactor Trip or Saf ety Zng ection) and ES-O. l, (Reactor Trip Response) and stabilized the plant.

The MSZVs were closed approximately five (5) minutes

'after the trip to prevent further plant cooldown.

G. SAFETY SYSTEM RESPONSE:

None IIZ. CAUSE OF EVENT A. IMMEDIATE CAUSE:

The'eactor trip occurred due to the "A" Reactor Trip Breaker opening.

B. INTERMEDIATE CAUSE:

The "A" Reactor Trip Breaker opening was due to the bumping, of two turbine autostop trip (AST) relays in the RAl Relay Rack. This bumping occurred from a smail flashlight (powered by "AA" batteries) that was 1 NAC AOAM SSSA I$ 4$ l

NRC eerro 9$ 9A \~ US. NUCLEAR REOULATORY COMMIEEION (9491 LICENSEE EVENT REPORT ILERI TEXT CONTINUATION 'eehovEo oME'No. $ 1$ C~ICI EX91RE$ "9191/9$

eACILITY NAME I'l OOCKET NUMOER QI LER NINER IEI YEAR I9 QU 9 N'Fl A L 4 M O OEVrorOH 4 M H.E. Ginna Nuclear Power Plant TExT II1 more RMoe o terhreerE

"

o s o o o 2 4 4 9 0 1 2 00 06 OF oee Iroerenor Hrrlc Fdic@ 99EAOI I ITI being used by an ECCD person.. While performing electrical wire verifications, the flashlight was accidently dropped and fell onto the relays. A normal actuation of the two relays would result in

,

actuation of both trains of logic '(i.e. opening of both reactor trip breakers and subsequent turbine trip) as each relay has an "A" and "B" train contact.

The postulated cause for actuation of only one .train of logic, ("A" Train Reactor Trip Breaker) is that the bumping effect was such that localized chatter of only the "A" train contacts occurred. The logic for.,

reactor trip is the actuation of at least two out of the three AST relays. Later testing confirmed that,:-

if normally actuated, the "B" train trip signal AST.

circuit would operate properly.

C. ROOT CAUSE:

The accidental dropping of the flashlight that bumped the relays was a personnel error.

IV ANALYSIS OF EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires reporting of "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)," in that the "A" Reactor Trip Breaker opening and subsequent Low Pressurizer Pressure Reactor -Trip was an automatic actuation of the RPS.

An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:

o When initiated by an input signal, the two reactor trip breakers opened as required.

41C eORM $ $ OA r94$ 1

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NRC Pens 999A Ug. NUCLfAR Rf4ULATORY COMMCSION 043)

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROYfO OM9 NO. 3194M10e f RPIRf 9: 9l9 I I99 I'ACILITYNAMf 111 OOCKfT NUM9 fR Ill Lfh NUMhfh IQ PA4f 191 IIQUANNTIAL YNIOS H N Ginna Nuclear .Power Plant 244 90

~ R.E.(SsNN NNee N Nfsleh eM eAWosel WIC Pens ~'II11Tl o s o o o 1 2 00 07 o~ 1 1 o All control and shutdown rods inserted to shut the.

reactor down as designed.

o The plant was quickly stabilized in hot shutdown.

This transient was compared to 'ncrease in decay heat removal transients in the Ginna Updated Final Safety Analysis (UFSAR). None of the assumptions of the UFSAR were violated during the event. The resultant cooldown from the reactor trip -and the turbine remaining on line caused pressurizer pressure to decrease rapidly. The rate sensitive low pressurizer pressure trip caused' reactor trip, opening the "B" Reactor Trip Breaker. The opening-:

of the "B" Reactor Trip Breaker caused the turbine to trip.

The following factors led to the cooldown, as compared with the cooldown expected following a normal reactor trip:

o Failure of the 20 ET solenoid to trip the turbine when the "A" Reactor Trip Breaker opened. Reactor trip without turbine trip caused the RCS to cooldown to approximately 535 F.

o . Lo Lo level on both steam generators caused the turbine driven auxiliary feedwater pump to start.

Steam extracted from the header by the turbine driven auxiliary feedwater pump contributed to the cooldown.

o Total auxiliary feedwater flow of greater than 470 gallons per minute per steam generator-also contributed to the cooldown.

Due to the above circumstances, the cooldown of the RCS to approximately 535 F is not unexpected. This cooldown is bounded by plant accident analysis and does not exceed the technical specification limit of 100oF per hour. Additional protection is provided by closure of the MSZVs.

Based on the above, it can be concluded that the public health and safety was assured at all times.

nsc PQRM 9ee*

19491

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L'ICENSEE EVENT REPORT (LERI TEXT CONTINUATION AttAOVSD OSIS NO JISOWIOS tlItIASS: SQI ISS tACILITYAASSS Ill OOCKST IIU~SA ITI LtA IIUSSSSA Itl ~ Aot ISI

~ SOVSNTIAL VISION N V II V N R.E. Ginna Nuclear%?ower Plant TECT II'INSIS DISCS ~ ISSVSSA SASSSASI lYAC ANN ~'Sl IITI 0 5 0 0 0 2 4 4 9 0. 0 1 2 0009 OF SSS valve shaft due 'o the valve packing.

MSZV's were stroked several times to ensure Both aperability and adequate closure capability.

Results of these tests, support the conclusian that failure of the "A" -MSZV to fully seat during the plant trip was not due to internal valve distortion and bending, but was the result of a lack of flow across the valve disc.

Failure to close is attributed to .the closure operation occurring in a quiescent environment.

Valve closure was dependent solely upon two factors: the moment developed by the weight of the valve disc, and the spring pravided to,-

assist in,valve closure. Without the additional assistance of steam flow across the valve disc; the valve was not capable af completing its closing operation. Based upon valve seat area, a one (1) psi differential across the valve seat would develop a moment oi approximately 450 ft-lbs. This moment is comparable to the moment developed by the weight of'he valve disc in its closed position. For all design basis accidents where MSIV closure is required, the accident transient would a large enough differen-tial pressure todevelop obtain complete valve closure.

We are evaluating various packing materials which have a low friction coefficient and can perform the sealing function.

0 As the Intermediate Range NZS Channel N-35 tracked NIS Channel N-36 for its normal operating range and returned to normal'pproximately ten (10) hours after the trip, no .immediate .action was deemed necessary. Specific logarithmic amplifier idle current adjustments internal to the PC card are being considered to correct NIS Channel N-35 response below 10 10 amps. Westing-house personnel were contacted, and they confirmed potential impact af the amplifier idle 'current on channel autput, and that this output does not affect the safety function of the Intermediate NAC SOAIS SSSA 19491

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