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{{#Wiki_filter:. _ _ , . . . _ _ . . . . _ . . . _ _ _ _ _ . . . . _ . . _ _ _ _ _ _ _ ._ | {{#Wiki_filter:. _ _ , . . . _ _ . . . . _ . . . _ _ _ _ _ . . . . _ . . _ _ _ _ _ _ _ ._ | ||
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9- | 9- | ||
: 1. Abnormal Occurrence Report No. 50-313/74-8A 4 | : 1. Abnormal Occurrence Report No. 50-313/74-8A 4 | ||
: 2. Report Date: July 16,'1975 3. Occurrence Date: October 3, 1974 | : 2. Report Date: July 16,'1975 3. Occurrence Date: October 3, 1974 | ||
; 4 Facility: Arkansas Nuclear One-Unit 1 i Russellville, Arkansas | ; 4 Facility: Arkansas Nuclear One-Unit 1 i Russellville, Arkansas | ||
, t | , t | ||
; 5. Identification of Occurrence: | ; 5. Identification of Occurrence: | ||
) | ) | ||
i See Abnormal Occurrence Report No. 50-313/74-8 dated 10/9/74. | i See Abnormal Occurrence Report No. 50-313/74-8 dated 10/9/74. | ||
I i | I i | ||
}. | }. | ||
: 6. Conditions Prior to Occurrence: | : 6. Conditions Prior to Occurrence: | ||
Steady-State Power Reactor Power SIWth I | Steady-State Power Reactor Power SIWth I | ||
!!ot Standby Not Output SINC Cold Shutdown Percent of Full Power "6 Refueling Shutdown Load Changes .During Routine | !!ot Standby Not Output SINC Cold Shutdown Percent of Full Power "6 Refueling Shutdown Load Changes .During Routine | ||
. Power Operation l Routine Startup - | . Power Operation l Routine Startup - | ||
4 | 4 Operation Routrie Shutdown Operation j- Other (specify) ' | ||
Operation | |||
Routrie Shutdown Operation | |||
j- Other (specify) ' | |||
l See Abnormal Occurrence Report No. 50-313/74-8 dated 10/9/74. | l See Abnormal Occurrence Report No. 50-313/74-8 dated 10/9/74. | ||
? i 1 | ? i 1 | ||
', 1 | ', 1 | ||
: 7. Description of Occurrence: ~: | : 7. Description of Occurrence: ~: | ||
See Abnormal Occurrence Report No. 50-313/74-8. | See Abnormal Occurrence Report No. 50-313/74-8. | ||
i | i i | ||
i | |||
[ | [ | ||
l | l 800415074g t! arch 4, 1975 NSP-10, Rev. 2 Page 2 of 4 | ||
800415074g t! arch 4, 1975 NSP-10, Rev. 2 Page 2 of 4 | |||
_ ~_ _ . . . _ . _ _ . _ . _ . _ . _ . _ . _ _ . . . . _ _ . __. _ _ _ _ __.. .. . . _ . . _ _ . | _ ~_ _ . . . _ . _ _ . _ . _ . _ . _ . _ . _ _ . . . . _ _ . __. _ _ _ _ __.. .. . . _ . . _ _ . | ||
'1 , | '1 , | ||
Abnormal Occurrence Report No. 50-313/74-8A | Abnormal Occurrence Report No. 50-313/74-8A | ||
: 8. Designation of Apparent Cause of Occurrence: | : 8. Designation of Apparent Cause of Occurrence: | ||
Design X Frocedure Ahnufacture . Unusual Service Condition ~ | Design X Frocedure Ahnufacture . Unusual Service Condition ~ | ||
including Environmental Installation / | including Environmental Installation / | ||
Crestruction Componen: Fellure | Crestruction Componen: Fellure Cy rstor Other (specify) _ | ||
Initial investigation as reported in AOR 50-313/74-8 revealed that loss i of the core flood tank reference leg was a result of evaporation as no j leakage was found. Investigation per corrective action of AOR 50-313/74-8 revealed evidence of leakage on the reference legs of each tank. | |||
Cy rstor | i l | ||
1 l-I i * | |||
Other (specify) _ | |||
Initial investigation as reported in AOR 50-313/74-8 revealed that loss i of the core flood tank reference leg was a result of evaporation as no j leakage was found. Investigation per corrective action of AOR 50-313/74-8 | |||
revealed evidence of leakage on the reference legs of each tank. | |||
i | |||
l-I | |||
i * | |||
: 9. Analysis of Occurrenec: | : 9. Analysis of Occurrenec: | ||
See AOR 50-313/74-8. | See AOR 50-313/74-8. | ||
1 | 1 | ||
) .. | ) .. | ||
; 2 | ; 2 | ||
! g: | ! g: | ||
^1' t | |||
t 4 | |||
O March 4, 1975 NSP-10, Rev. 2 Page 3 Of 4 F .. | |||
^1' | |||
t | |||
t | |||
NSP-10, Rev. 2 Page 3 Of 4 F . | |||
,m, , . , , - . - , . . . .- ,.,n. , -- - , - - - | ,m, , . , , - . - , . . . .- ,.,n. , -- - , - - - | ||
,.,an,-..n., , . , . , - - - .,,,e ,, a.-.,,,.. ,, , . ,,nn.,, . nnn e n,c.,,.,. , , .nm,,, -, - - - | ,.,an,-..n., , . , . , - - - .,,,e ,, a.-.,,,.. ,, , . ,,nn.,, . nnn e n,c.,,.,. , , .nm,,, -, - - - | ||
j .^ bnormal' Occurrence Report No. 50-313/ 74-8A | j .^ bnormal' Occurrence Report No. 50-313/ 74-8A | ||
: 10. Corrective .?.ction: | : 10. Corrective .?.ction: | ||
Remaking and, in some cases, replacement of fittings were directed 'a y plant personnel with pressure tests follcwing the work. A new surveil-lance program was established on 11/12/74, and readings were taken periodically for two months to discover any trends indicating level changes in reference legs. Console readings and transmitter voltage outputs were read each time showing a deviation over the period of not | Remaking and, in some cases, replacement of fittings were directed 'a y plant personnel with pressure tests follcwing the work. A new surveil-lance program was established on 11/12/74, and readings were taken periodically for two months to discover any trends indicating level changes in reference legs. Console readings and transmitter voltage outputs were read each time showing a deviation over the period of not more than 0.19 feet and 0.28 feet, respectively. | ||
more than 0.19 feet and 0.28 feet, respectively. | |||
Drift has been concluded to have been caused by leakage at the fittings. | Drift has been concluded to have been caused by leakage at the fittings. | ||
This situation has been corrected and better resolution scales have been installed. Procedures will remain in effect that, before the core flood ,, . | This situation has been corrected and better resolution scales have been installed. Procedures will remain in effect that, before the core flood ,, . | ||
tanks are drained, the Instrument and Controls Supervisor will be con- | tanks are drained, the Instrument and Controls Supervisor will be con-suited concerning the need to check the reference legs. | ||
suited concerning the need to check the reference legs. | |||
: 11. Failurc Data: . | : 11. Failurc Data: . | ||
7- s., , See AOR 50-313/74-8. | 7- s., , See AOR 50-313/74-8. | ||
~- | ~- | ||
s s | s s | ||
i -- | i -- | ||
(<~s | (<~s | ||
\s_s/ - | \s_s/ - | ||
March 4, 1975 NSP-10, Rev. 2' Page 4 of 4 | March 4, 1975 NSP-10, Rev. 2' Page 4 of 4 e m -- , , - - , ,---,-- - -n-- , y--m - - - - - ,}} | ||
e m -- , , - - , ,---,-- - -n-- , y--m - - - - - ,}} |
Latest revision as of 17:18, 18 February 2020
ML19326B400 | |
Person / Time | |
---|---|
Site: | Arkansas Nuclear |
Issue date: | 07/16/1975 |
From: | ARKANSAS POWER & LIGHT CO. |
To: | |
Shared Package | |
ML19326B395 | List: |
References | |
NUDOCS 8004150766 | |
Download: ML19326B400 (3) | |
Text
. _ _ , . . . _ _ . . . . _ . . . _ _ _ _ _ . . . . _ . . _ _ _ _ _ _ _ ._
. w t
9-
- 1. Abnormal Occurrence Report No. 50-313/74-8A 4
- 2. Report Date: July 16,'1975 3. Occurrence Date: October 3, 1974
, t
- 5. Identification of Occurrence
)
i See Abnormal Occurrence Report No. 50-313/74-8 dated 10/9/74.
I i
}.
- 6. Conditions Prior to Occurrence:
Steady-State Power Reactor Power SIWth I
!!ot Standby Not Output SINC Cold Shutdown Percent of Full Power "6 Refueling Shutdown Load Changes .During Routine
. Power Operation l Routine Startup -
4 Operation Routrie Shutdown Operation j- Other (specify) '
l See Abnormal Occurrence Report No. 50-313/74-8 dated 10/9/74.
? i 1
', 1
- 7. Description of Occurrence: ~:
See Abnormal Occurrence Report No. 50-313/74-8.
i i
[
l 800415074g t! arch 4, 1975 NSP-10, Rev. 2 Page 2 of 4
_ ~_ _ . . . _ . _ _ . _ . _ . _ . _ . _ . _ _ . . . . _ _ . __. _ _ _ _ __.. .. . . _ . . _ _ .
'1 ,
Abnormal Occurrence Report No. 50-313/74-8A
- 8. Designation of Apparent Cause of Occurrence:
Design X Frocedure Ahnufacture . Unusual Service Condition ~
including Environmental Installation /
Crestruction Componen: Fellure Cy rstor Other (specify) _
Initial investigation as reported in AOR 50-313/74-8 revealed that loss i of the core flood tank reference leg was a result of evaporation as no j leakage was found. Investigation per corrective action of AOR 50-313/74-8 revealed evidence of leakage on the reference legs of each tank.
i l
1 l-I i *
- 9. Analysis of Occurrenec:
See AOR 50-313/74-8.
1
) ..
- 2
! g:
^1' t
t 4
O March 4, 1975 NSP-10, Rev. 2 Page 3 Of 4 F ..
,m, , . , , - . - , . . . .- ,.,n. , -- - , - - -
,.,an,-..n., , . , . , - - - .,,,e ,, a.-.,,,.. ,, , . ,,nn.,, . nnn e n,c.,,.,. , , .nm,,, -, - - -
j .^ bnormal' Occurrence Report No. 50-313/ 74-8A
- 10. Corrective .?.ction:
Remaking and, in some cases, replacement of fittings were directed 'a y plant personnel with pressure tests follcwing the work. A new surveil-lance program was established on 11/12/74, and readings were taken periodically for two months to discover any trends indicating level changes in reference legs. Console readings and transmitter voltage outputs were read each time showing a deviation over the period of not more than 0.19 feet and 0.28 feet, respectively.
Drift has been concluded to have been caused by leakage at the fittings.
This situation has been corrected and better resolution scales have been installed. Procedures will remain in effect that, before the core flood ,, .
tanks are drained, the Instrument and Controls Supervisor will be con-suited concerning the need to check the reference legs.
- 11. Failurc Data: .
7- s., , See AOR 50-313/74-8.
~-
s s
i --
(<~s
\s_s/ -
March 4, 1975 NSP-10, Rev. 2' Page 4 of 4 e m -- , , - - , ,---,-- - -n-- , y--m - - - - - ,