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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:August 5, 2008  
                                NUC LE AR RE G UL AT O RY C O M M I S S I O N
                                                    R E GI ON I V
                                        612 EAST LAMAR BLVD , SU I TE 400
EA-08-190  
                                        AR LI N GTON , TEXAS 76011-4125
                                                  August 5, 2008
Mr. Adam C. Heflin, Senior Vice
EA-08-190
   President and Chief Nuclear Officer  
Mr. Adam C. Heflin, Senior Vice
Union Electric Company  
   President and Chief Nuclear Officer
P.O. Box 620  
Union Electric Company
Fulton, MO 65251  
P.O. Box 620
Fulton, MO 65251
SUBJECT: CALLAWAY PLANT - NRC INTEGRATED INSPECTION  
SUBJECT: CALLAWAY PLANT - NRC INTEGRATED INSPECTION
        REPORT AND NOTICE OF VIOLATION 05000483/2008003  
              REPORT AND NOTICE OF VIOLATION 05000483/2008003
Dear Mr. Heflin:  
Dear Mr. Heflin:
On June 24, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated  
On June 24, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated
inspection at your Callaway Plant. The enclosed report documents the inspection results, which  
inspection at your Callaway Plant. The enclosed report documents the inspection results, which
were discussed on June 24, 2008, with you and other members of your staff.  
were discussed on June 24, 2008, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
The inspection examined activities conducted under your license as they relate to safety and  
compliance with the Commissions rules and regulations and with the conditions of your license.
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
The inspectors reviewed selected procedures and records, observed activities, and interviewed  
personnel.
personnel.  
Based on the results of this inspection, one violation is cited in the enclosed Notice of
Violation (Notice) and the circumstances surrounding this violation are described in detail in the
Based on the results of this inspection, one violation is cited in the enclosed Notice of  
enclosed report. The violation involved failure to implement corrective actions to preclude the
Violation (Notice) and the circumstances surrounding this violation are described in detail in the  
repetition of void formation in the emergency core cooling piping (EA-08-190). Although
enclosed report. The violation involved failure to implement corrective actions to preclude the  
determined to be of very low safety significance (Green), this violation is being cited because
repetition of void formation in the emergency core cooling piping (EA-08-190). Although  
one of the criteria specified in Section VI.A.1 of the NRC Enforcement Policy for a noncited
determined to be of very low safety significance (Green), this violation is being cited because  
violation was satisfied. Specifically, AmerenUE failed to restore compliance within a reasonable
one of the criteria specified in Section VI.A.1 of the NRC Enforcement Policy for a noncited  
time after the violation was last identified in NRC Inspection Report 05000483/2006002-012.
violation was satisfied. Specifically, AmerenUE failed to restore compliance within a reasonable  
Please note that you are required to respond to this letter and should follow the instructions
time after the violation was last identified in NRC Inspection Report 05000483/2006002-012.
specified in the enclosed Notice when preparing your response. The NRC will use your
Please note that you are required to respond to this letter and should follow the instructions  
response, in part, to determine whether further enforcement action is necessary to ensure
specified in the enclosed Notice when preparing your response. The NRC will use your  
compliance with regulatory requirements.
response, in part, to determine whether further enforcement action is necessary to ensure  
This report also documents four NRC-identified and self-revealing findings of very low safety
compliance with regulatory requirements.  
significance (Green). These findings were determined to involve violations of NRC
requirements. Additionally, two licensee-identified violations which were determined to be of
This report also documents four NRC-identified and self-revealing findings of very low safety  
very low safety significance are listed in this report. However, because of the very low safety
significance (Green). These findings were determined to involve violations of NRC  
significance and because they were entered into your corrective action program, the NRC is
requirements. Additionally, two licensee-identified violations which were determined to be of  
treating these findings as NCVs consistent with Section VI.A of the NRC Enforcement Policy. If
very low safety significance are listed in this report. However, because of the very low safety  
you contest these NCVs, you should provide a response within 30 days of the date of this
significance and because they were entered into your corrective action program, the NRC is  
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
treating these findings as NCVs consistent with Section VI.A of the NRC Enforcement Policy. If  
you contest these NCVs, you should provide a response within 30 days of the date of this  
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,  
UNITED STATES
NUCLEAR REGULATORY COMMISSION
R E GI ON  I V
612 EAST LAMAR BLVD, SUITE 400
ARLINGTON, TEXAS 76011-4125


Union Electric Company                   -2-
Union Electric Company  
ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional
- 2 -  
Administrator, U.S. Nuclear Regulatory Commission Region IV, 612 East Lamar Drive,
Suite 400, Arlington, Texas 76011-4125; the Director, Office of Enforcement, U.S. Nuclear
Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at the
ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional  
Callaway Plant.
Administrator, U.S. Nuclear Regulatory Commission Region IV, 612 East Lamar Drive,  
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its
Suite 400, Arlington, Texas 76011-4125; the Director, Office of Enforcement, U.S. Nuclear  
enclosures will be made available electronically for public inspection in the NRC Public
Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at the  
Document Room or from the Publicly Available Records component of NRCs document system
Callaway Plant.  
(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the
Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its  
                                            Sincerely,
enclosures will be made available electronically for public inspection in the NRC Public  
                                                    /RA/
Document Room or from the Publicly Available Records component of NRCs document system  
                                            Vincent G. Gaddy, Chief,
(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the  
                                            Projects Branch B
Public Electronic Reading Room).  
                                            Division of Reactor Projects
Docket: 50-483
Sincerely,  
License: NPF-30
Enclosures: Notice of Violation and
NRC Inspection Report 05000483/2008003
/RA/  
   w/attachment: Supplemental Information
cc w/enclosure:                                     Rick A. Muench, President and
Vincent G. Gaddy, Chief,
John ONeill, Esq.                                   Chief Executive Officer
Projects Branch B  
Pillsbury Winthrop Shaw Pittman LLP                 Wolf Creek Nuclear Operating Corporation
Division of Reactor Projects  
2300 N. Street, N.W.                                 P.O. Box 411
Washington, DC 20037                                 Burlington, KS 66839
Docket: 50-483  
Scott A. Maglio, Assistant Manager                   Kathleen Smith, Executive Director and
License: NPF-30  
   Regulatory Affairs                                 Kay Drey, Representative Board of
AmerenUE                                             Directors
Enclosures: Notice of Violation and
P.O. Box 620                                         Missouri Coalition for the Environment
NRC Inspection Report 05000483/2008003  
Fulton, MO 65251                                     6267 Delmar Boulevard, Suite 2E
   w/attachment: Supplemental Information  
                                                    St. Louis City, MO 63130
Missouri Public Service Commission
cc w/enclosure:  
Governors Office Building                           Lee Fritz, Presiding Commissioner
John ONeill, Esq.  
200 Madison Street                                   Callaway County Courthouse
Pillsbury Winthrop Shaw Pittman LLP  
P.O. Box 360                                         10 East Fifth Street
2300 N. Street, N.W.  
Jefferson City, MO 65102-0360                       Fulton, MO 65251
Washington, DC 20037  
H. Floyd Gilzow                                     Les H. Kanuckel, Manager
Deputy Director for Policy                           Quality Assurance
Scott A. Maglio, Assistant Manager  
Missouri Department of Natural Resources             AmerenUE
   Regulatory Affairs  
P. O. Box 176                                       P.O. Box 620
AmerenUE  
Jefferson City, MO 65102-0176                        Fulton, MO 65251
P.O. Box 620  
Fulton, MO 65251  
Missouri Public Service Commission  
Governors Office Building  
200 Madison Street  
P.O. Box 360  
Jefferson City, MO 65102-0360  
H. Floyd Gilzow  
Deputy Director for Policy  
Missouri Department of Natural Resources  
P. O. Box 176  
Jefferson City, MO  65102-0176
Rick A. Muench, President and 
  Chief Executive Officer
Wolf Creek Nuclear Operating Corporation
P.O. Box 411
Burlington, KS  66839
Kathleen Smith, Executive Director and 
Kay Drey, Representative Board of
Directors
Missouri Coalition for the Environment
6267 Delmar Boulevard, Suite 2E
St. Louis City, MO 63130
Lee Fritz, Presiding Commissioner
Callaway County Courthouse
10 East Fifth Street
Fulton, MO 65251
Les H. Kanuckel, Manager
Quality Assurance
AmerenUE
P.O. Box 620
Fulton, MO 65251  


Union Electric Company                 -3-
Union Electric Company  
Director, Missouri State Emergency         Certrec Corporation
- 3 -  
Management Agency                         4200 South Hulen, Suite 422
P.O. Box 116                               Fort Worth, TX 76109
Jefferson City, MO 65102-0116
Director, Missouri State Emergency
                                            Keith G. Henke, Planner III
  Management Agency  
Scott Clardy, Director                     Division of Community and Public Health
P.O. Box 116  
Section for Environmental Public Health     Office of Emergency Coordination
Jefferson City, MO 65102-0116  
Missouri Department of Health and           Missouri Department of Health and
Senior Services                            Senior Services
Scott Clardy, Director  
P.O. Box 570                               930 Wildwood,
Section for Environmental Public Health  
Jefferson City, MO 65102-0570               P.O. Box 570
Missouri Department of Health and
                                            Jefferson City, MO 65102
  Senior Services  
Luke H. Graessle, Manager
P.O. Box 570  
Regulatory Affairs                        Technical Services Branch Chief
Jefferson City, MO 65102-0570  
AmerenUE                                    FEMA Region VII
P.O. Box 620                                2323 Grand Boulevard, Suite 900
Luke H. Graessle, Manager
Fulton, MO 65251                            Kansas City, MO 64108-2670
  Regulatory Affairs
Thomas B. Elwood, Supervising Engineer      Ronald L. McCabe, Chief
AmerenUE
Regulatory Affairs and Licensing          Technological Hazards Branch
P.O. Box 620
AmerenUE                                    National Preparedness Division
Fulton, MO  65251
P.O. Box 620                                DHS/FEMA
Fulton, MO 65251                            9221 Ward Parkway, Suite 300
Thomas B. Elwood, Supervising Engineer
                                            Kansas City, MO 64114-3372
  Regulatory Affairs and Licensing
AmerenUE
P.O. Box 620
Fulton, MO  65251
Certrec Corporation
4200 South Hulen, Suite 422
Fort Worth, TX  76109
Keith G. Henke, Planner III
Division of Community and Public Health
Office of Emergency Coordination
Missouri Department of Health and
  Senior Services
930 Wildwood,
P.O. Box 570  
Jefferson City, MO 65102  
Technical Services Branch Chief  
FEMA Region VII  
2323 Grand Boulevard, Suite 900  
Kansas City, MO 64108-2670  
Ronald L. McCabe, Chief  
Technological Hazards Branch  
National Preparedness Division  
DHS/FEMA  
9221 Ward Parkway, Suite 300  
Kansas City, MO 64114-3372  


Union Electric Company                     -4-
Union Electric Company  
Electronic distribution by RIV:
- 4 -  
Regional Administrator (Elmo.Collins@nrc.gov)
DRP Director (Dwight.Chamberlain@nrc.gov)
Electronic distribution by RIV:  
DRS Director (Roy.Caniano@nrc.gov)
Regional Administrator (Elmo.Collins@nrc.gov)  
DRS Deputy Director (Troy.Pruett@nrc.gov)
DRP Director (Dwight.Chamberlain@nrc.gov)  
Senior Resident Inspector (David.Dumbacher@nrc.gov)
DRS Director (Roy.Caniano@nrc.gov)  
Branch Chief, DRP/B (Vincent.Gaddy@nrc.gov)
DRS Deputy Director (Troy.Pruett@nrc.gov)  
Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)
Senior Resident Inspector (David.Dumbacher@nrc.gov)  
Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)
Branch Chief, DRP/B (Vincent.Gaddy@nrc.gov)  
RITS Coordinator (Marisa.Herrera@nrc.gov)
Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)  
Only inspection reports to the following:
Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)  
DRS STA (Dale.Powers@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)  
M. Cox, OEDO RIV Coordinator (Mark.Cox@nrc.gov)
OEMail.Resource@nrc.gov
Only inspection reports to the following:  
Enforcement Officer (Michael.Vasquez@nrc.gov)
DRS STA (Dale.Powers@nrc.gov)  
Chief Allegation Coordination/Enforcement Staff (William.Jones@nrc.gov)
M. Cox, OEDO RIV Coordinator (Mark.Cox@nrc.gov)  
Office of Enforcement (Alexander.Sapountizis@nrc.gov)
OEMail.Resource@nrc.gov  
ROPreports
Enforcement Officer (Michael.Vasquez@nrc.gov)  
CWY Site Secretary (Dawn.Yancey@nrc.gov)
Chief Allegation Coordination/Enforcement Staff (William.Jones@nrc.gov)  
SUNSI Review Completed: VGG ADAMS: ; Yes No                       Initials: __VGG__
Office of Enforcement (Alexander.Sapountizis@nrc.gov)
;Publicly Available         Non-Publicly Available  Sensitive   ;Non-Sensitive
ROPreports  
R:\_Reactors\_CW\2008\CW 2008003RP-DED.doc                               ML 082180851
CWY Site Secretary (Dawn.Yancey@nrc.gov)  
RIV:SRI:DRP/B         C:DRS/OB       C:DRS/PSB1     C:DRS/EB2             C:DRS/EB1
DDumbacher             RELantz         MPShannon       NFO'Keefe             RLBywater
/RA/ VGGaddy for       /RA/           /RA/           /RA/ MFRunyan for     /RA/
07/29/2008             07/9/2008       07/14/2008       07/15/2008             07/11/2008
C:DRS/PSB2             DRS/SRA         ACES           C:DRP/B               D:DRP
GEWerner               DPLoveless     GMVasquez       VGGaddy               DDChamberlain
/RA/                   /RA/           /RA/           /RA/                   /RA/
07/17/2008             07/15/2008     07/24/2008       08/5/2008             07/28/2008
OFFICIAL RECORD COPY                                   T=Telephone         E=E-mail     F=Fax
SUNSI Review Completed:     VGG   ADAMS: ;   Yes       No         Initials: __VGG__  
;Publicly Available  
Non-Publicly Available  Sensitive  
;Non-Sensitive  
R:\\_Reactors\\_CW\\2008\\CW 2008003RP-DED.doc
ML 082180851  
RIV:SRI:DRP/B  
C:DRS/OB  
C:DRS/PSB1  
C:DRS/EB2  
C:DRS/EB1  
DDumbacher  
RELantz  
MPShannon  
NFO'Keefe  
RLBywater  
/RA/ VGGaddy for /RA/  
/RA/  
/RA/ MFRunyan for /RA/  
07/29/2008  
07/9/2008  
07/14/2008  
07/15/2008  
07/11/2008  
C:DRS/PSB2  
DRS/SRA  
ACES  
C:DRP/B  
D:DRP  
GEWerner  
DPLoveless  
GMVasquez  
VGGaddy  
DDChamberlain  
/RA/  
/RA/  
/RA/  
/RA/  
/RA/  
07/17/2008  
07/15/2008  
07/24/2008  
08/5/2008  
07/28/2008  
OFFICIAL RECORD COPY
T=Telephone           E=E-mail       F=Fax  


                                        NOTICE OF VIOLATION
AmerenUE                                                                 Docket 50-483
Callaway Plant                                                           License NPF-30
- 1 -
                                                                        EA-08-190
Enclosure 1
During an NRC inspection conducted March 24 through June 24, 2008, a violation of NRC
NOTICE OF VIOLATION  
requirements was identified. In accordance with the NRC Enforcement Policy, the violation is
listed below:
AmerenUE  
        10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that
        measures shall be established to ensure that, for significant conditions adverse to
        quality, the cause of the condition is determined and corrective action taken to preclude
        repetition.
        Contrary to this, from December 26, 2006, through May 21, 2008, the licensee failed to
        take corrective actions to preclude repetition of safety-related emergency core cooling
        system pipe voiding, and the licensee determined that this condition was a significant
        condition adverse to quality.
Docket 50-483  
This violation is associated with a Green Significance Determination Process finding.
Callaway Plant  
Pursuant to the provisions of 10 CFR 2.201, AmerenUE is hereby required to submit a written
statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document
Control Desk, Washington, DC 20555 with a copy to the Regional Administrator, Region IV,
and a copy to the NRC Senior Resident Inspector at the facility that is the subject of this Notice
of Violation (Notice), within 30 days of the date of the letter transmitting this Notice. This reply
should be clearly marked as a "Reply to Notice of Violation EA-08-190," and should include:
(1) the reason for the violation, or, if contested, the basis for disputing the violation or severity
License NPF-30  
level, (2) the corrective steps that have been taken and the results achieved, (3) the corrective
steps that will be taken to avoid further violations, and (4) the date when full compliance will be
achieved. Your response may reference or include previous docketed correspondence, if the
correspondence adequately addresses the required response. If an adequate reply is not
received within the time specified in this Notice, an order or a Demand for Information may be
issued as to why the license should not be modified, suspended, or revoked, or why such other
action as may be proper should not be taken. Where good cause is shown, consideration will
be given to extending the response time.
If you contest this enforcement action, you should also provide a copy of your response, with
the basis for your denial, to the Director, Office of Enforcement, United States Nuclear
EA-08-190  
Regulatory Commission, Washington, DC 20555-0001.
Because your response will be made available electronically for public inspection in the NRC
During an NRC inspection conducted March 24 through June 24, 2008, a violation of NRC  
Public Document Room or from the NRCs document system (ADAMS), accessible from the
requirements was identified. In accordance with the NRC Enforcement Policy, the violation is  
NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not
listed below:
include any personal privacy, proprietary, or safeguards information so that it can be made
available to the public without redaction. If personal privacy or proprietary information is
10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that  
necessary to provide an acceptable response, then please provide a bracketed copy of your
measures shall be established to ensure that, for significant conditions adverse to  
response that identifies the information that should be protected and a redacted copy of your
quality, the cause of the condition is determined and corrective action taken to preclude  
response that deletes such information. If you request withholding of such material, you must
repetition.  
specifically identify the portions of your response that you seek to have withheld and provide in
                                              -1-                                          Enclosure 1
Contrary to this, from December 26, 2006, through May 21, 2008, the licensee failed to  
take corrective actions to preclude repetition of safety-related emergency core cooling  
system pipe voiding, and the licensee determined that this condition was a significant  
condition adverse to quality.
This violation is associated with a Green Significance Determination Process finding.  
Pursuant to the provisions of 10 CFR 2.201, AmerenUE is hereby required to submit a written  
statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document  
Control Desk, Washington, DC 20555 with a copy to the Regional Administrator, Region IV,  
and a copy to the NRC Senior Resident Inspector at the facility that is the subject of this Notice  
of Violation (Notice), within 30 days of the date of the letter transmitting this Notice. This reply  
should be clearly marked as a "Reply to Notice of Violation EA-08-190," and should include:
(1) the reason for the violation, or, if contested, the basis for disputing the violation or severity  
level, (2) the corrective steps that have been taken and the results achieved, (3) the corrective  
steps that will be taken to avoid further violations, and (4) the date when full compliance will be  
achieved. Your response may reference or include previous docketed correspondence, if the  
correspondence adequately addresses the required response. If an adequate reply is not  
received within the time specified in this Notice, an order or a Demand for Information may be  
issued as to why the license should not be modified, suspended, or revoked, or why such other  
action as may be proper should not be taken. Where good cause is shown, consideration will  
be given to extending the response time.  
If you contest this enforcement action, you should also provide a copy of your response, with  
the basis for your denial, to the Director, Office of Enforcement, United States Nuclear  
Regulatory Commission, Washington, DC 20555-0001.
Because your response will be made available electronically for public inspection in the NRC  
Public Document Room or from the NRCs document system (ADAMS), accessible from the  
NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not  
include any personal privacy, proprietary, or safeguards information so that it can be made  
available to the public without redaction. If personal privacy or proprietary information is  
necessary to provide an acceptable response, then please provide a bracketed copy of your  
response that identifies the information that should be protected and a redacted copy of your  
response that deletes such information. If you request withholding of such material, you must  
specifically identify the portions of your response that you seek to have withheld and provide in  


detail the bases for your claim of withholding (e.g., explain why the disclosure of information will
create an unwarranted invasion of personal privacy or provide the information required by
10 CFR 2.390(b) to support a request for withholding confidential commercial or financial
- 2 -
information). If safeguards information is necessary to provide an acceptable response, please
Enclosure 1
provide the level of protection described in 10 CFR 73.21.
detail the bases for your claim of withholding (e.g., explain why the disclosure of information will  
Dated this   5th   day of July 2008
create an unwarranted invasion of personal privacy or provide the information required by  
                                            -2-                                        Enclosure 1
10 CFR 2.390(b) to support a request for withholding confidential commercial or financial  
information). If safeguards information is necessary to provide an acceptable response, please  
provide the level of protection described in 10 CFR 73.21.  
Dated this   5th     day of July 2008


                  U.S. NUCLEAR REGULATORY COMMISSION
                                    REGION IV
Docket:     50-483
- 1 -
License:     NPF-30
Enclosure 2
Report:     05000483/2008003
U.S. NUCLEAR REGULATORY COMMISSION  
Licensee:   Union Electric Company
REGION IV  
Facility:   Callaway Plant
Docket:  
Location:   Junction Highway CC and Highway O
50-483  
            Fulton, MO
License:  
Dates:       March 25 - June 24, 2008
NPF-30  
Inspectors: D. Dumbacher, Senior Resident Inspector
Report:  
            J. Groom, Resident Inspector
05000483/2008003  
            J. Drake, Senior Reactor Inspector, Plant Support, Branch 2
Licensee:  
            G. Guerra, CHP, Health Physicist, Plant Support Branch 1
Union Electric Company  
Approved By: V. Gaddy, Chief, Project Branch B
Facility:  
            Division of Reactor Projects
Callaway Plant  
                                    -1-                                  Enclosure 2
Location:  
Junction Highway CC and Highway O  
Fulton, MO
Dates:  
March 25 - June 24, 2008  
Inspectors:  
D. Dumbacher, Senior Resident Inspector  
J. Groom, Resident Inspector  
J. Drake, Senior Reactor Inspector, Plant Support, Branch 2  
G. Guerra, CHP, Health Physicist, Plant Support Branch 1  
Approved By:  
V. Gaddy, Chief, Project Branch B  
Division of Reactor Projects  


                                      SUMMARY OF FINDINGS
IR 05000483/2008003: 3/25 - 6/24/2008; Callaway Plant, Operability Evaluations,
Postmaintenance Testing, Surveillance Testing, and Identification and Resolution of Problems.
- 2 -
This report covered a 3-month period of inspection by resident inspectors. The significance of
Enclosure 2
most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual
SUMMARY OF FINDINGS  
Chapter 0609, "Significance Determination Process." Findings for which the Significance
Determination Process does not apply may be Green or assigned a severity level after NRC
management review. The NRCs program for overseeing the safe operation of commercial
IR 05000483/2008003: 3/25 - 6/24/2008; Callaway Plant, Operability Evaluations,  
nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,
Postmaintenance Testing, Surveillance Testing, and Identification and Resolution of Problems.  
dated December 2006.
This report covered a 3-month period of inspection by resident inspectors. The significance of  
A.     NRC-Identified and Self-Revealing Findings
most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual  
        Cornerstone: Mitigating Systems
Chapter 0609, "Significance Determination Process." Findings for which the Significance  
        *     Green. The inspectors identified a noncited violation of Technical
Determination Process does not apply may be Green or assigned a severity level after NRC  
              Specification 3.5.2, "Emergency Core Cooling Systems," after an inadequate
management review. The NRCs program for overseeing the safe operation of commercial  
              surveillance procedure resulted in the licensee failing to maintain the emergency
nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,  
              core cooling system full of water as required per Technical Specification 3.5.2.
dated December 2006.  
              On May 21, 2008, Callaway Plant engineering discovered that a section of the
              cold leg recirculation piping, specifically the discharge of the residual heat
A.  
              removal pumps to the safety injection pumps, contained 6.6 cubic feet of air.
NRC-Identified and Self-Revealing Findings  
              Callaway monthly surveillance Procedure OSP-SA-00003, "Emergency Core
Cornerstone: Mitigating Systems  
              Cooling Flow Path Verification and Venting," had a purpose to: "Verify the ECCS
*  
              is full of water," in accordance with Technical Specification Surveillance
Green. The inspectors identified a noncited violation of Technical  
              Requirement 3.5.2.3. The monthly verification and vent procedure was not
Specification 3.5.2, "Emergency Core Cooling Systems," after an inadequate  
              comprehensive enough to ensure all the emergency core cooling system was full
surveillance procedure resulted in the licensee failing to maintain the emergency  
              of water.
core cooling system full of water as required per Technical Specification 3.5.2.
              This finding was more than minor because it was similar to Example 3e of NRC
On May 21, 2008, Callaway Plant engineering discovered that a section of the  
              Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues," and
cold leg recirculation piping, specifically the discharge of the residual heat  
              met the Not Minor If, criteria because the failure to meet the licensees
removal pumps to the safety injection pumps, contained 6.6 cubic feet of air.
              administrative requirement for allowable void fraction impacted the ability of the
Callaway monthly surveillance Procedure OSP-SA-00003, "Emergency Core  
              Train A safety injection system to function upon initiation of high-pressure
Cooling Flow Path Verification and Venting," had a purpose to: "Verify the ECCS  
              recirculation. This finding affected the mitigating systems cornerstone procedure
is full of water," in accordance with Technical Specification Surveillance  
              quality attribute. Using the Manual Chapter 0609.04, Phase 1 - Initial Screening
Requirement 3.5.2.3. The monthly verification and vent procedure was not  
              and Characterization of Findings, the inspectors determined that this finding
comprehensive enough to ensure all the emergency core cooling system was full  
              should be evaluated using the Phase 2 process described in Manual
of water.  
              Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection
This finding was more than minor because it was similar to Example 3e of NRC  
              Findings for At-Power Situations. As described in Section III, of Appendix A,
Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues," and  
              given that the presolved table did not contain a suitable target or surrogate for
met the Not Minor If, criteria because the failure to meet the licensees  
              this finding, the senior reactor analyst used the risk-informed notebook to
administrative requirement for allowable void fraction impacted the ability of the  
              evaluate the significance of this finding affecting only high-pressure recirculation
Train A safety injection system to function upon initiation of high-pressure  
              as very low risk significance (Green). This finding has a crosscutting aspect in
recirculation. This finding affected the mitigating systems cornerstone procedure  
              the area of human performance associated with the decision making component
quality attribute. Using the Manual Chapter 0609.04, Phase 1 - Initial Screening  
              because the licensee failed to use conservative assumptions in decision making
and Characterization of Findings, the inspectors determined that this finding  
              and did not adopt a requirement to demonstrate that a single vent valve was
should be evaluated using the Phase 2 process described in Manual  
              sufficient to vent the affected line rather than assuming that an additional
Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection  
                                            -2-                                        Enclosure 2
Findings for At-Power Situations. As described in Section III, of Appendix A,  
given that the presolved table did not contain a suitable target or surrogate for  
this finding, the senior reactor analyst used the risk-informed notebook to  
evaluate the significance of this finding affecting only high-pressure recirculation  
as very low risk significance (Green). This finding has a crosscutting aspect in  
the area of human performance associated with the decision making component  
because the licensee failed to use conservative assumptions in decision making  
and did not adopt a requirement to demonstrate that a single vent valve was  
sufficient to vent the affected line rather than assuming that an additional  


  installed valve was not necessary to completely fill, vent, and test the line [H.1(b)]
  (Section 1R15).
* Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B,
- 3 -
  Criterion XVI, "Corrective Action," was identified after the licensee failed to
Enclosure 2
  promptly correct leakage from diesel generator jacket water o-rings. On
installed valve was not necessary to completely fill, vent, and test the line [H.1(b)]  
  February 20, 2008, during a normal surveillance run of Emergency Diesel
(Section 1R15).  
  Generator B, Callaway operations personnel identified an approximately
*  
  80 drop-per-minute jacket water leak caused by premature failure of Nitrile type
Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B,  
  o-rings. Following restoration of Emergency Diesel Generator B, the licensee
Criterion XVI, "Corrective Action," was identified after the licensee failed to  
  re-evaluated the preventative maintenance frequency for jacket water o-ring
promptly correct leakage from diesel generator jacket water o-rings. On  
  replacement and reduced the replacement frequency from once every 3 years to
February 20, 2008, during a normal surveillance run of Emergency Diesel  
  once every refueling cycle. Then, on May 28, 2008, during a routine surveillance
Generator B, Callaway operations personnel identified an approximately  
  run of Emergency Diesel Generator A, Callaway operations personnel identified
80 drop-per-minute jacket water leak caused by premature failure of Nitrile type  
  that Emergency Diesel Generator A had a 200 drop-per-minute jacket water leak.
o-rings. Following restoration of Emergency Diesel Generator B, the licensee  
  Similar to the condition observed on Emergency Diesel Generator B on
re-evaluated the preventative maintenance frequency for jacket water o-ring  
  February 20, 2008, the source of the leakage was from Nitrile type o-rings within
replacement and reduced the replacement frequency from once every 3 years to  
  the jacket water system. The o-rings responsible for jacket water leakage were
once every refueling cycle. Then, on May 28, 2008, during a routine surveillance  
  found to be of similar age to those that failed during the February 20, 2008,
run of Emergency Diesel Generator A, Callaway operations personnel identified  
  surveillance but had not been replaced despite the change to the licensee's
that Emergency Diesel Generator A had a 200 drop-per-minute jacket water leak.
  preventive maintenance frequency.
Similar to the condition observed on Emergency Diesel Generator B on  
  This finding, failure to implement adequate corrective actions for degraded Nitrile
February 20, 2008, the source of the leakage was from Nitrile type o-rings within  
  type o-rings in Emergency Diesel Generator A after previously identifying the
the jacket water system. The o-rings responsible for jacket water leakage were  
  adverse condition on Emergency Diesel Generator B, was more than minor
found to be of similar age to those that failed during the February 20, 2008,  
  because, if left uncorrected, degraded diesel generator jacket water o-rings could
surveillance but had not been replaced despite the change to the licensee's  
  become a more significant safety concern. This finding affected the mitigating
preventive maintenance frequency.  
  systems cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial
This finding, failure to implement adequate corrective actions for degraded Nitrile  
  Screening and Characterization of Findings, this finding was determined to be of
type o-rings in Emergency Diesel Generator A after previously identifying the  
  very low safety significance because it was a design deficiency confirmed not to
adverse condition on Emergency Diesel Generator B, was more than minor  
  result in loss of operability. This finding has a crosscutting aspect in the area of
because, if left uncorrected, degraded diesel generator jacket water o-rings could  
  human performance associated with the work controls component because the
become a more significant safety concern. This finding affected the mitigating  
  licensee failed to plan work activities to support long-term equipment reliability by
systems cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial  
  addressing known degraded conditions in a more reactive than preventative
Screening and Characterization of Findings, this finding was determined to be of  
  manner [H.3(b)] (Section 1R19).
very low safety significance because it was a design deficiency confirmed not to  
* Green. The inspectors identified a violation of 10 CFR Part 50, Appendix B,
result in loss of operability. This finding has a crosscutting aspect in the area of  
  Criterion XVI, "Corrective Action," because the licensee failed to take corrective
human performance associated with the work controls component because the  
  actions to preclude repetition of void formation in emergency core cooling system
licensee failed to plan work activities to support long-term equipment reliability by  
  piping, a significant condition adverse to quality. After experiencing void
addressing known degraded conditions in a more reactive than preventative  
  formations in 2005 and 2006, the NRC identified violations of Criterion XVI.
manner [H.3(b)] (Section 1R19).  
  However, licensee corrective actions did not preclude repetition of void
*  
  formations that were discovered on May 21, 2008. On that date, Callaway Plant
Green. The inspectors identified a violation of 10 CFR Part 50, Appendix B,  
  engineering performed ultrasonic inspection of the safety injection system
Criterion XVI, "Corrective Action," because the licensee failed to take corrective  
  common suction piping Line EM023-HCB - 6" and discovered a 6.6 cubic foot
actions to preclude repetition of void formation in emergency core cooling system  
  voided area. This exceeded the allowable void fraction of 2.1 cubic feet required
piping, a significant condition adverse to quality. After experiencing void  
  for operability. This voided piping, determined to have existed for over a year,
formations in 2005 and 2006, the NRC identified violations of Criterion XVI.
  was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The
However, licensee corrective actions did not preclude repetition of void  
  maintenance restoration failed to perform an adequate fill and vent to ensure the
formations that were discovered on May 21, 2008. On that date, Callaway Plant  
  suction pipe was full of water. The inspectors identified several related examples
engineering performed ultrasonic inspection of the safety injection system  
  where the licensee had performed either inadequate operating experience
common suction piping Line EM023-HCB - 6" and discovered a 6.6 cubic foot  
                                -3-                                      Enclosure 2
voided area. This exceeded the allowable void fraction of 2.1 cubic feet required  
for operability. This voided piping, determined to have existed for over a year,  
was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The  
maintenance restoration failed to perform an adequate fill and vent to ensure the  
suction pipe was full of water. The inspectors identified several related examples  
where the licensee had performed either inadequate operating experience  


      evaluations, inadequate extent of condition reviews, or inadequate procedure
      corrections. The violation is being cited in a Notice of Violation because the
      licensee failed to restore compliance with a reasonable time after a violation was
- 4 -
      last identified in 2006.
Enclosure 2
      This finding, failure to restore compliance to prevent recurrence of emergency
evaluations, inadequate extent of condition reviews, or inadequate procedure  
      core cooling system voids, was more than minor because it is similar to
corrections. The violation is being cited in a Notice of Violation because the  
      Example 3e of NRC Inspection Manual Chapter 0612, Appendix E, "Examples of
licensee failed to restore compliance with a reasonable time after a violation was  
      Minor Issues," criteria because the failure impacted the ability of the emergency
last identified in 2006.  
      core cooling system to function upon initiation of high-pressure recirculation.
This finding, failure to restore compliance to prevent recurrence of emergency  
      Using the Manual Chapter 0609.04, Phase 1 - Initial Screening and
core cooling system voids, was more than minor because it is similar to  
      Characterization of Findings, the inspectors determined that this finding should
Example 3e of NRC Inspection Manual Chapter 0612, Appendix E, "Examples of  
      be evaluated using the Phase 2 process described in Manual Chapter 0609,
Minor Issues," criteria because the failure impacted the ability of the emergency  
      Appendix A, Determining the Significance of Reactor Inspection Findings for
core cooling system to function upon initiation of high-pressure recirculation.
      At-Power Situations. As described in Section III, of Appendix A, given that the
Using the Manual Chapter 0609.04, Phase 1 - Initial Screening and  
      presolved table did not contain a suitable target or surrogate for this finding, the
Characterization of Findings, the inspectors determined that this finding should  
      senior reactor analyst used the risk-informed notebook to evaluate the
be evaluated using the Phase 2 process described in Manual Chapter 0609,  
      significance of this finding as very low risk significance (Green). This finding has
Appendix A, Determining the Significance of Reactor Inspection Findings for  
      a crosscutting aspect in the area of problem identification and resolution
At-Power Situations. As described in Section III, of Appendix A, given that the  
      associated with the corrective action program component because AmerenUE
presolved table did not contain a suitable target or surrogate for this finding, the  
      failed to thoroughly evaluate voiding problems such that the resolutions
senior reactor analyst used the risk-informed notebook to evaluate the  
      addressed causes and extent of condition, as necessary [P.1(c)] (Section 4OA2).
significance of this finding as very low risk significance (Green). This finding has  
Cornerstone: Barrier Integrity
a crosscutting aspect in the area of problem identification and resolution  
*     Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B,
associated with the corrective action program component because AmerenUE  
      Criterion III, Design Control, was identified after determining that the licensee
failed to thoroughly evaluate voiding problems such that the resolutions  
      had not adequately selected and reviewed the suitability of the design of the
addressed causes and extent of condition, as necessary [P.1(c)] (Section 4OA2).  
      containment air cooler control circuitry. On March 26, 2008, Containment Air
Cornerstone: Barrier Integrity  
      Cooler A fan shut down when shifted from fast to slow speed. Troubleshooting
*  
      by the licensee determined that voltage was lost to the control power circuitry
Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B,  
      when the fast speed thermal overload tripped. Since the overload contacts were
Criterion III, Design Control, was identified after determining that the licensee  
      wired in series, Containment Air Cooler A experienced a complete loss of control
had not adequately selected and reviewed the suitability of the design of the  
      power rendering it inoperable. The licensee determined the trip to be caused by
containment air cooler control circuitry. On March 26, 2008, Containment Air  
      operation of containment air coolers in fast speed, during a period of higher than
Cooler A fan shut down when shifted from fast to slow speed. Troubleshooting  
      normal containment pressure. The licensee analyzed the potential impact of the
by the licensee determined that voltage was lost to the control power circuitry  
      newly discovered adverse containment cooler design vulnerability against design
when the fast speed thermal overload tripped. Since the overload contacts were  
      basis accident scenarios. The licensee determined that a hot zero power main
wired in series, Containment Air Cooler A experienced a complete loss of control  
      steam line break results in a delayed safety injection signal allowing the fan
power rendering it inoperable. The licensee determined the trip to be caused by  
      motor overloads to trip prior to being shed by the load sequencer. The
operation of containment air coolers in fast speed, during a period of higher than  
      containment air coolers would then experience a complete loss of control power
normal containment pressure. The licensee analyzed the potential impact of the  
      and would not be capable of automatically restarting in slow speed. The analysis
newly discovered adverse containment cooler design vulnerability against design  
      revealed that the peak containment pressure limit of 48.1 psig would be
basis accident scenarios. The licensee determined that a hot zero power main  
      preserved. The licensee submitted a licensee event report as required by
steam line break results in a delayed safety injection signal allowing the fan  
      10 CFR 50.73 since the inadequate containment air cooler control circuitry
motor overloads to trip prior to being shed by the load sequencer. The  
      resulted in a condition prohibited by the plants Technical Specifications.
containment air coolers would then experience a complete loss of control power  
      This finding, failure to ensure the design of the containment air cooler control
and would not be capable of automatically restarting in slow speed. The analysis  
      circuitry was suitable for all plant conditions, was more than minor because it was
revealed that the peak containment pressure limit of 48.1 psig would be  
      associated with the barrier integrity cornerstone attribute of design control and
preserved. The licensee submitted a licensee event report as required by  
      affects the associated cornerstone objective to provide reasonable assurance
10 CFR 50.73 since the inadequate containment air cooler control circuitry  
                                    -4-                                      Enclosure 2
resulted in a condition prohibited by the plants Technical Specifications.
This finding, failure to ensure the design of the containment air cooler control  
circuitry was suitable for all plant conditions, was more than minor because it was  
associated with the barrier integrity cornerstone attribute of design control and  
affects the associated cornerstone objective to provide reasonable assurance  


  that physical design barriers protect the public from radio nuclide releases
  caused by accidents or releases. Using Manual Chapter 0609, Appendix H,
  Containment Integrity Significance Determination Process," this finding was
- 5 -
  determined to be a Type B finding since it was related to a degraded condition
Enclosure 2
  that has potentially important implications for the integrity of the containment,
that physical design barriers protect the public from radio nuclide releases  
  without affecting the likelihood of core damage. This finding was found to be of
caused by accidents or releases. Using Manual Chapter 0609, Appendix H,  
  very low safety significance because containment coolers are structures,
Containment Integrity Significance Determination Process," this finding was  
  systems or components that are not significant contributors to the large early
determined to be a Type B finding since it was related to a degraded condition  
  release frequency. The inspectors determined that this finding does not have a
that has potentially important implications for the integrity of the containment,  
  crosscutting aspect associated with it since the performance deficiency was not
without affecting the likelihood of core damage. This finding was found to be of  
  indicative of current licensee performance (Section 1R15).
very low safety significance because containment coolers are structures,  
* Green. The inspectors identified a noncited violation of Technical
systems or components that are not significant contributors to the large early  
  Specification 5.4.1.a, Procedures, after Callaway control room operators
release frequency. The inspectors determined that this finding does not have a  
  improperly entered a wrong Technical Specification action statement due to the
crosscutting aspect associated with it since the performance deficiency was not  
  failure to maintain the Technical Specification Bases current. On June 17, 2008,
indicative of current licensee performance (Section 1R15).  
  during surveillance testing, Valve EMHV8823 failed to indicate fully closed.
*  
  Since EMHV8823 is an isolation valve for containment Penetration 49, the
Green. The inspectors identified a noncited violation of Technical  
  licensee entered Technical Specification 3.6.3, Containment Isolation Valves,
Specification 5.4.1.a, Procedures, after Callaway control room operators  
  Condition C, with an action to restore the valve to an operable status or isolate
improperly entered a wrong Technical Specification action statement due to the  
  the penetration within 72 hours. Approximately 8 hours after Valve EMHV8823
failure to maintain the Technical Specification Bases current. On June 17, 2008,  
  had been declared inoperable, Callaway licensing personnel contacted the
during surveillance testing, Valve EMHV8823 failed to indicate fully closed.
  control room and informed them of an approved Technical Specification Bases
Since EMHV8823 is an isolation valve for containment Penetration 49, the  
  change that did not allow Technical Specification 3.6.3, Condition C, to be
licensee entered Technical Specification 3.6.3, Containment Isolation Valves,  
  applicable to containment Penetration 49. The Technical Specification Bases
Condition C, with an action to restore the valve to an operable status or isolate  
  change was effective May 1, 2008, but had not been issued to the control room.
the penetration within 72 hours. Approximately 8 hours after Valve EMHV8823  
  The licensee determined that the more restrictive Technical Specification 3.6.3,
had been declared inoperable, Callaway licensing personnel contacted the  
  Condition A, should have been entered with an action to isolate the affected
control room and informed them of an approved Technical Specification Bases  
  penetration within 4 hours. The licensee performed a containment entry
change that did not allow Technical Specification 3.6.3, Condition C, to be  
  following discovery of entry into Technical Specification 3.6.3, Condition A, and
applicable to containment Penetration 49. The Technical Specification Bases  
  found that Valve EMHV8823 failed its surveillance due to out of adjustment
change was effective May 1, 2008, but had not been issued to the control room.
  position indicator limit switches. The valve was verified closed and isolated
The licensee determined that the more restrictive Technical Specification 3.6.3,  
  allowing exit from Technical Specification 3.6.3, Condition A.
Condition A, should have been entered with an action to isolate the affected  
  This finding, failure to ensure the Technical Specification Bases were maintained
penetration within 4 hours. The licensee performed a containment entry  
  current and available to the Callaway control room staff, was more than minor
following discovery of entry into Technical Specification 3.6.3, Condition A, and  
  because if left uncorrected, the failure to maintain the Technical Specification
found that Valve EMHV8823 failed its surveillance due to out of adjustment  
  Bases current could become a more significant safety concern. This finding was
position indicator limit switches. The valve was verified closed and isolated  
  determined to affect the barrier integrity cornerstone. Using Manual
allowing exit from Technical Specification 3.6.3, Condition A.  
  Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,
This finding, failure to ensure the Technical Specification Bases were maintained  
  this finding is determined to be of very low safety significance since this finding
current and available to the Callaway control room staff, was more than minor  
  did not represent an actual open pathway in the physical integrity of reactor
because if left uncorrected, the failure to maintain the Technical Specification  
  containment and did not involve an actual reduction in function of hydrogen
Bases current could become a more significant safety concern. This finding was  
  ignitors in the reactor containment. This finding has a crosscutting aspect in the
determined to affect the barrier integrity cornerstone. Using Manual  
  area of human performance associated with the decision making component
Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,  
  because the licensee failed to communicate, in a timely manner, decisions to
this finding is determined to be of very low safety significance since this finding  
  personnel who have a need to know the information in order to perform work
did not represent an actual open pathway in the physical integrity of reactor  
  safely [H.1(c)] (Section 1R22).
containment and did not involve an actual reduction in function of hydrogen  
                                -5-                                        Enclosure 2
ignitors in the reactor containment. This finding has a crosscutting aspect in the  
area of human performance associated with the decision making component  
because the licensee failed to communicate, in a timely manner, decisions to  
personnel who have a need to know the information in order to perform work  
safely [H.1(c)] (Section 1R22).  


B. Licensee-Identified Violations
  Two violations of very low safety significance, which were identified by the licensee,
  have been reviewed by the inspectors. Corrective actions taken or planned by the
- 6 -
  licensee have been entered into the licensees corrective action program. These
Enclosure 2
  violations and corrective action tracking numbers are listed in Section 4OA7.
B.  
                                        -6-                                        Enclosure 2
Licensee-Identified Violations  
Two violations of very low safety significance, which were identified by the licensee,  
have been reviewed by the inspectors. Corrective actions taken or planned by the  
licensee have been entered into the licensees corrective action program. These  
violations and corrective action tracking numbers are listed in Section 4OA7.


                                          REPORT DETAILS
Summary of Plant Status
AmerenUE operated the Callaway Plant at near 100 percent for the entire quarter.
- 7 -
1.   REACTOR SAFETY
Enclosure 2
      Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity and
REPORT DETAILS  
      Emergency Preparedness
Summary of Plant Status
1R01 Adverse Weather Protection (71111.01)
AmerenUE operated the Callaway Plant at near 100 percent for the entire quarter.  
.1   Readiness of Offsite and Alternate AC Power System
1.  
  a. Inspection Scope
REACTOR SAFETY  
      The inspectors reviewed the licensees plant features, training lesson plans, and
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity and  
      procedures for operation and continued availability of offsite and alternate AC power
Emergency Preparedness  
      systems to verify they were appropriate. The review included communication protocols
1R01 Adverse Weather Protection (71111.01)  
      and agreement procedures between the transmission system operator and the nuclear
.1  
      power plant to verify that appropriate information is exchanged when issues arise that
Readiness of Offsite and Alternate AC Power System  
      could impact the offsite power system. Specifically, the procedures were verified to
    a. Inspection Scope  
      ensure they specified:
The inspectors reviewed the licensees plant features, training lesson plans, and  
      *       Required actions needed when notified by the transmission system operator that
procedures for operation and continued availability of offsite and alternate AC power  
              posttrip voltage of the offsite power system would not be acceptable to assure
systems to verify they were appropriate. The review included communication protocols  
              the continued operation of safety related loads without transferring to the onsite
and agreement procedures between the transmission system operator and the nuclear  
              power supply.
power plant to verify that appropriate information is exchanged when issues arise that  
      *       Compensatory actions needed when it is not possible to predict the posttrip
could impact the offsite power system. Specifically, the procedures were verified to  
              voltage at the nuclear power plant for current grid conditions.
ensure they specified:  
      *       Required assessment of plant risk based on maintenance activities which could
              affect grid reliability, or the ability of the transmission system to provide the offsite
*  
              power system.
Required actions needed when notified by the transmission system operator that  
      *     Required communications between the nuclear power plant and the transmission
posttrip voltage of the offsite power system would not be acceptable to assure  
              system operator when changes at the nuclear power plant could impact the
the continued operation of safety related loads without transferring to the onsite  
              transmission system, or when the capability of the transmission system to
power supply.  
              provide adequate offsite system power is challenged.
*  
      On May 16, 2008, the inspectors evaluated the licensee staffs preparations for summer
Compensatory actions needed when it is not possible to predict the posttrip  
      readiness of offsite and AC power systems against the sites procedures and determined
voltage at the nuclear power plant for current grid conditions.  
      that the staffs actions were adequate. Documents reviewed are listed in the
*  
      attachment.
Required assessment of plant risk based on maintenance activities which could  
      These activities constituted one readiness of offsite power inspection sample as defined
affect grid reliability, or the ability of the transmission system to provide the offsite  
      by Inspection Procedure 71111.01.
power system.  
                                              -7-                                        Enclosure 2
*  
Required communications between the nuclear power plant and the transmission  
system operator when changes at the nuclear power plant could impact the  
transmission system, or when the capability of the transmission system to  
provide adequate offsite system power is challenged.  
On May 16, 2008, the inspectors evaluated the licensee staffs preparations for summer  
readiness of offsite and AC power systems against the sites procedures and determined  
that the staffs actions were adequate. Documents reviewed are listed in the  
attachment.  
These activities constituted one readiness of offsite power inspection sample as defined  
by Inspection Procedure 71111.01.  


  b. Findings
      No findings of significance were identified.
.2   Readiness for Impending Adverse Weather Conditions
- 8 -
  a. Inspection Scope
Enclosure 2
      On May 2, 2008, the inspectors completed a review of the licensee's readiness for
    b. Findings  
      impending adverse weather involving severe thunderstorms. The inspectors:
No findings of significance were identified.  
      (1) reviewed plant procedures, the Final Safety Analysis Report (FSAR), and Technical
.2  
      Specifications to ensure that operator actions defined in adverse weather procedures
Readiness for Impending Adverse Weather Conditions  
      maintained the readiness of essential systems; (2) walked down portions of the
    a. Inspection Scope  
      emergency diesel generators and offsite power systems to ensure that adverse weather
On May 2, 2008, the inspectors completed a review of the licensee's readiness for  
      protection features were sufficient to support operability; (3) reviewed maintenance
impending adverse weather involving severe thunderstorms. The inspectors:
      records to determine that applicable surveillance requirements were current before the
(1) reviewed plant procedures, the Final Safety Analysis Report (FSAR), and Technical  
      anticipated severe thunderstorms developed; and (4) reviewed plant modifications,
Specifications to ensure that operator actions defined in adverse weather procedures  
      procedure revisions, and operator work arounds to determine if recent facility changes
maintained the readiness of essential systems; (2) walked down portions of the  
      challenged plant operation. Documents reviewed by the inspectors are listed in the
emergency diesel generators and offsite power systems to ensure that adverse weather  
      attachment.
protection features were sufficient to support operability; (3) reviewed maintenance  
      These activities constituted one readiness for impending adverse weather inspection
records to determine that applicable surveillance requirements were current before the  
      sample as defined by Inspection Procedure 71111.01.
anticipated severe thunderstorms developed; and (4) reviewed plant modifications,  
  b. Findings
procedure revisions, and operator work arounds to determine if recent facility changes  
      No findings of significance were identified.
challenged plant operation. Documents reviewed by the inspectors are listed in the  
1R04 Equipment Alignments (71111.04)
attachment.
.1   Quarterly Partial System Walkdowns
  a. Inspection Scope
These activities constituted one readiness for impending adverse weather inspection  
      The inspectors performed partial system walkdowns of the following risk-significant
sample as defined by Inspection Procedure 71111.01.  
      systems:
      *       June 3, 2008, Train A auxiliary feedwater system while the Train B motor-driven
    b. Findings  
              auxiliary feedwater pump was out of service for planned maintenance.
No findings of significance were identified.  
      *       June 10, 2008, Train A 480 volt NG Class 1E switchgear while the Train B
              emergency diesel generator was out of service for planned and emergent
1R04 Equipment Alignments (71111.04)  
              maintenance issues.
.1  
      The inspectors selected these systems based on their risk significance relative to the
Quarterly Partial System Walkdowns  
      reactor safety cornerstones at the time they were inspected. The inspectors attempted
    a. Inspection Scope  
      to identify discrepancies that could impact the function of the system, and, therefore,
The inspectors performed partial system walkdowns of the following risk-significant  
      potentially increase risk. The inspectors reviewed applicable operating procedures,
systems:  
      system diagrams, FSAR, Technical Specification requirements, outstanding work orders,
      corrective action documents, and the impact of ongoing work activities on redundant
*  
      trains of equipment in order to identify conditions that could have rendered the systems
June 3, 2008, Train A auxiliary feedwater system while the Train B motor-driven  
                                          -8-                                      Enclosure 2
auxiliary feedwater pump was out of service for planned maintenance.  
*  
June 10, 2008, Train A 480 volt NG Class 1E switchgear while the Train B  
emergency diesel generator was out of service for planned and emergent  
maintenance issues.
The inspectors selected these systems based on their risk significance relative to the  
reactor safety cornerstones at the time they were inspected. The inspectors attempted  
to identify discrepancies that could impact the function of the system, and, therefore,  
potentially increase risk. The inspectors reviewed applicable operating procedures,  
system diagrams, FSAR, Technical Specification requirements, outstanding work orders,  
corrective action documents, and the impact of ongoing work activities on redundant  
trains of equipment in order to identify conditions that could have rendered the systems  


      incapable of performing their intended functions. The inspectors also walked down
      accessible portions of the systems to verify components and support equipment were
      aligned correctly and were operable. The inspectors examined the material condition of
- 9 -
      the components and observed operating parameters of equipment to verify that there
Enclosure 2
      were no obvious deficiencies. The inspectors also verified that the licensee had properly
incapable of performing their intended functions. The inspectors also walked down  
      identified and resolved equipment alignment problems that could cause initiating events
accessible portions of the systems to verify components and support equipment were  
      or impact the capability of mitigating systems or barriers and entered them into the
aligned correctly and were operable. The inspectors examined the material condition of  
      corrective action program with the appropriate significance characterization. Documents
the components and observed operating parameters of equipment to verify that there  
      reviewed are listed in the attachment.
were no obvious deficiencies. The inspectors also verified that the licensee had properly  
      These activities constituted two partial system walkdown samples as defined by
identified and resolved equipment alignment problems that could cause initiating events  
      Inspection Procedure 71111.04.
or impact the capability of mitigating systems or barriers and entered them into the  
  b. Findings
corrective action program with the appropriate significance characterization. Documents  
      No findings of significance were identified.
reviewed are listed in the attachment.  
.2   Complete System Walkdown (71111.04S)
  a. Inspection Scope
These activities constituted two partial system walkdown samples as defined by  
      On April 17, 2008, the inspectors performed a complete system alignment inspection of
Inspection Procedure 71111.04.  
      Train B of the residual heat removal system to verify the functional capability of the
      system. The inspectors selected this system because it was considered both
    b. Findings  
      safety-significant and risk-significant in the licensees probabilistic risk assessment. The
No findings of significance were identified.  
      inspectors walked down the system to review mechanical and electrical equipment line
.2  
      ups, electrical power availability, system pressure and temperature indications, as
Complete System Walkdown (71111.04S)  
      appropriate, component labeling, component lubrication, component and equipment
    a. Inspection Scope  
      cooling, hangers and supports, operability of support systems, and to ensure that
On April 17, 2008, the inspectors performed a complete system alignment inspection of  
      ancillary equipment or debris did not interfere with equipment operation. The inspectors
Train B of the residual heat removal system to verify the functional capability of the  
      reviewed a sample of past and outstanding work orders to determine whether any
system. The inspectors selected this system because it was considered both  
      deficiencies significantly affected the system function. In addition, the inspectors
safety-significant and risk-significant in the licensees probabilistic risk assessment. The  
      reviewed the corrective action program database to ensure that system equipment
inspectors walked down the system to review mechanical and electrical equipment line  
      alignment problems were being identified and appropriately resolved. The documents
ups, electrical power availability, system pressure and temperature indications, as  
      used for the walkdown and issue review are listed in the attachment.
appropriate, component labeling, component lubrication, component and equipment  
      These activities constituted one complete system walkdown sample as defined by
cooling, hangers and supports, operability of support systems, and to ensure that  
      Inspection Procedure 71111.04.
ancillary equipment or debris did not interfere with equipment operation. The inspectors  
  b. Findings
reviewed a sample of past and outstanding work orders to determine whether any  
      No findings of significance were identified.
deficiencies significantly affected the system function. In addition, the inspectors  
                                            -9-                                        Enclosure 2
reviewed the corrective action program database to ensure that system equipment  
alignment problems were being identified and appropriately resolved. The documents  
used for the walkdown and issue review are listed in the attachment.  
These activities constituted one complete system walkdown sample as defined by  
Inspection Procedure 71111.04.  
    b. Findings  
No findings of significance were identified.  


1R05 Fire Protection (71111.05)
.1   Quarterly Fire Inspector Tours (71111.05Q)
  a. Inspection Scope
- 10 -
      The inspectors conducted fire protection walkdowns which were focused on availability,
Enclosure 2
      accessibility, and the condition of firefighting equipment in the following risk-significant
1R05 Fire Protection (71111.05)  
      plant areas:
.1  
      *       March 27, 2008, Fire Area C-21, Lower Cable Spreading Room
Quarterly Fire Inspector Tours (71111.05Q)  
      *       April 16, 2008, Fire Area A-17, Electrical Penetration Room (South)
    a. Inspection Scope  
      *       April 25, 2008, Condensate Storage Tank
The inspectors conducted fire protection walkdowns which were focused on availability,  
      *       April 29, 2008, Fire Area A-23, Main Steam and Feedwater Isolation Valve
accessibility, and the condition of firefighting equipment in the following risk-significant  
              Enclosure
plant areas:  
      *       April 30, 2008, Reactor Building
      *       June 18, 2008, Fire Area A-1, North Pipe Chase
*  
      The inspectors reviewed areas to assess if the licensee implemented a fire protection
March 27, 2008, Fire Area C-21, Lower Cable Spreading Room  
      program that adequately controlled combustibles and ignition sources within the plant,
*  
      effectively maintained fire detection and suppression capability, maintained passive fire
April 16, 2008, Fire Area A-17, Electrical Penetration Room (South)  
      protection features in good material condition, and implemented adequate compensatory
*  
      measures for out of service, degraded or inoperable fire protection equipment, systems,
April 25, 2008, Condensate Storage Tank  
      or features in accordance with the licensees fire plan. The inspectors selected fire
*  
      areas based on their overall contribution to internal fire risk as documented in the plants
April 29, 2008, Fire Area A-23, Main Steam and Feedwater Isolation Valve  
      Individual Plant Examination of External Events with later additional insights, their
Enclosure  
      potential to impact equipment which could initiate or mitigate a plant transient, or their
*  
      impact on the plants ability to respond to a security event. The inspectors verified that
April 30, 2008, Reactor Building  
      fire hoses and extinguishers were in their designated locations and available for
*  
      immediate use; that fire detectors and sprinklers were unobstructed, that transient
June 18, 2008, Fire Area A-1, North Pipe Chase  
      material loading was within the analyzed limits; and fire doors, dampers, and penetration
The inspectors reviewed areas to assess if the licensee implemented a fire protection  
      seals appeared to be in satisfactory condition. Documents reviewed are listed in the
program that adequately controlled combustibles and ignition sources within the plant,  
      attachment.
effectively maintained fire detection and suppression capability, maintained passive fire  
      These activities constituted six quarterly fire protection inspection samples as defined by
protection features in good material condition, and implemented adequate compensatory  
      Inspection Procedure 71111.05.
measures for out of service, degraded or inoperable fire protection equipment, systems,  
  b. Findings
or features in accordance with the licensees fire plan. The inspectors selected fire  
      No findings of significance were identified.
areas based on their overall contribution to internal fire risk as documented in the plants  
.2   Annual Fire Protection Drill Observation (71111.05A)
Individual Plant Examination of External Events with later additional insights, their  
  a. Inspection Scope
potential to impact equipment which could initiate or mitigate a plant transient, or their  
      On March 27, 2008, the inspectors observed a fire brigade activation due to a report of
impact on the plants ability to respond to a security event. The inspectors verified that  
      smoke in the laundry decontamination area. The observation evaluated the readiness of
fire hoses and extinguishers were in their designated locations and available for  
                                          - 10 -                                      Enclosure 2
immediate use; that fire detectors and sprinklers were unobstructed, that transient  
material loading was within the analyzed limits; and fire doors, dampers, and penetration  
seals appeared to be in satisfactory condition. Documents reviewed are listed in the  
attachment.  
These activities constituted six quarterly fire protection inspection samples as defined by  
Inspection Procedure 71111.05.  
    b. Findings  
No findings of significance were identified.  
.2  
Annual Fire Protection Drill Observation (71111.05A)  
    a. Inspection Scope  
On March 27, 2008, the inspectors observed a fire brigade activation due to a report of  
smoke in the laundry decontamination area. The observation evaluated the readiness of  


    the plant fire brigade to fight fires. The inspectors verified that the licensee staff
    identified deficiencies; openly discussed them in a self-critical manner at the drill debrief,
    and took appropriate corrective actions. Specific attributes evaluated were: (1) proper
- 11 -
    wearing of turnout gear and self-contained breathing apparatus; (2) proper use and
Enclosure 2
    layout of fire hoses; (3) employment of appropriate fire fighting techniques; (4) sufficient
the plant fire brigade to fight fires. The inspectors verified that the licensee staff  
    firefighting equipment brought to the scene; (5) effectiveness of fire brigade leader
identified deficiencies; openly discussed them in a self-critical manner at the drill debrief,  
    communications, command, and control; (6) search for victims and propagation of the
and took appropriate corrective actions. Specific attributes evaluated were: (1) proper  
    fire into other plant areas; (7) smoke removal operations; (8) utilization of preplanned
wearing of turnout gear and self-contained breathing apparatus; (2) proper use and  
    strategies; (9) adherence to the preplanned drill scenario; and (10) drill objectives.
layout of fire hoses; (3) employment of appropriate fire fighting techniques; (4) sufficient  
    Documents reviewed are listed in the attachment.
firefighting equipment brought to the scene; (5) effectiveness of fire brigade leader  
    These activities constituted one annual fire protection inspection sample as defined by
communications, command, and control; (6) search for victims and propagation of the  
    Inspection Procedure 71111.05.
fire into other plant areas; (7) smoke removal operations; (8) utilization of preplanned  
  b. Findings
strategies; (9) adherence to the preplanned drill scenario; and (10) drill objectives.
    No findings of significance were identified.
Documents reviewed are listed in the attachment.  
1R06 Flood Protection Measures (71111.06)
These activities constituted one annual fire protection inspection sample as defined by  
    Internal Flooding
Inspection Procedure 71111.05.  
  a. Inspection Scope
    b. Findings  
    The inspectors reviewed selected risk-significant plant design features and licensee
No findings of significance were identified.  
    procedures intended to protect the plant and its safety related equipment from internal
1R06 Flood Protection Measures (71111.06)  
    flooding events. The inspectors reviewed flood analyses and design documents,
Internal Flooding  
    including the FSAR, engineering calculations, and abnormal operating procedures for
    a. Inspection Scope  
    licensee commitments. The inspectors reviewed licensee drawings to identify areas and
The inspectors reviewed selected risk-significant plant design features and licensee  
    equipment that may be affected by internal flooding caused by the failure or
procedures intended to protect the plant and its safety related equipment from internal  
    misalignment of nearby sources of water. The inspectors also reviewed the licensees
flooding events. The inspectors reviewed flood analyses and design documents,  
    corrective actions for previously identified flood-related items. The inspectors performed
including the FSAR, engineering calculations, and abnormal operating procedures for  
    a walkdown of the following plant area to assess the adequacy of any watertight doors
licensee commitments. The inspectors reviewed licensee drawings to identify areas and  
    and verify drains and sumps were clear of debris and operable, and that the licensee
equipment that may be affected by internal flooding caused by the failure or  
    complied with its flooding related commitments:
misalignment of nearby sources of water. The inspectors also reviewed the licensees  
    *       June 23, 2008, Control Building West Corridor
corrective actions for previously identified flood-related items. The inspectors performed  
    The document reviewed during this inspection is listed as follows:
a walkdown of the following plant area to assess the adequacy of any watertight doors  
      *       Callaway Action Request 200805189
and verify drains and sumps were clear of debris and operable, and that the licensee  
    This inspection constituted one internal flooding sample as defined in Inspection
complied with its flooding related commitments:  
    Procedure 71111.06.
  b. Findings
*  
    No findings of significance were identified.
June 23, 2008, Control Building West Corridor  
                                            - 11 -                                    Enclosure 2
The document reviewed during this inspection is listed as follows:  
*  
Callaway Action Request 200805189  
This inspection constituted one internal flooding sample as defined in Inspection  
Procedure 71111.06.  
    b. Findings  
No findings of significance were identified.  


1R11 Licensed Operator Requalification Program (71111.11)
  a. Inspection Scope
    On June 2, 2008, the inspectors observed a crew of licensed operators perform a
- 12 -
    Cycle 08-3 as found scenario in the plants simulator to verify that operator performance
Enclosure 2
    was adequate, evaluators were identifying and documenting crew performance
1R11 Licensed Operator Requalification Program (71111.11)  
    problems, and that training was being conducted in accordance with licensee
    a. Inspection Scope  
    procedures. The scenario involved an operating design basis earthquake with a lockout
On June 2, 2008, the inspectors observed a crew of licensed operators perform a  
    on essential 4 kV Bus NB01. The inspectors evaluated the crew in the following areas:
Cycle 08-3 as found scenario in the plants simulator to verify that operator performance  
    *       Licensed operator performance
was adequate, evaluators were identifying and documenting crew performance  
    *       Crew clarity and formality of communications
problems, and that training was being conducted in accordance with licensee  
    *       Ability to take timely actions in the conservative direction
procedures. The scenario involved an operating design basis earthquake with a lockout  
    *       Prioritization, interpretation, and verification of annunciator alarms
on essential 4 kV Bus NB01. The inspectors evaluated the crew in the following areas:  
    *       Correct use and implementation of abnormal and emergency procedures
    *       Control board manipulations
*  
    *       Oversight and direction from supervisors
Licensed operator performance  
    *       Ability to identify and implement appropriate Technical Specification actions and
              Emergency Plan actions and notifications
*  
    The crews performance in these areas was compared to pre-established operator action
Crew clarity and formality of communications  
    expectations and successful critical task completion requirements. Documents reviewed
    are listed in the attachment.
*  
    This inspection constituted one quarterly licensed operator requalification program
Ability to take timely actions in the conservative direction  
    sample as defined in Inspection Procedure 71111.11.
  b. Findings
*  
    No findings of significance were identified.
Prioritization, interpretation, and verification of annunciator alarms  
1R12 Maintenance Effectiveness (71111.12)
  a. Inspection Scope
*  
    The inspectors evaluated degraded performance issues involving the following
Correct use and implementation of abnormal and emergency procedures  
    risk-significant systems:
    *       May 15, 2008, Callaway Action Request (CAR) 200801644, an additional anode
*  
              was found in the north end of the Train A emergency diesel generator intercooler
Control board manipulations  
    *       May 15, 2008, CAR 200802854, KKJ01A (Train A emergency diesel generator)
              engine oil sump high
*  
                                            - 12 -                                  Enclosure 2
Oversight and direction from supervisors  
*  
Ability to identify and implement appropriate Technical Specification actions and  
Emergency Plan actions and notifications  
The crews performance in these areas was compared to pre-established operator action  
expectations and successful critical task completion requirements. Documents reviewed  
are listed in the attachment.  
This inspection constituted one quarterly licensed operator requalification program  
sample as defined in Inspection Procedure 71111.11.  
    b. Findings
No findings of significance were identified.  
1R12 Maintenance Effectiveness (71111.12)  
    a. Inspection Scope  
The inspectors evaluated degraded performance issues involving the following  
risk-significant systems:  
*  
May 15, 2008, Callaway Action Request (CAR) 200801644, an additional anode  
was found in the north end of the Train A emergency diesel generator intercooler  
*  
May 15, 2008, CAR 200802854, KKJ01A (Train A emergency diesel generator)  
engine oil sump high  


      The inspectors reviewed events such as where ineffective equipment maintenance has
      resulted in valid or invalid automatic actuations of risk-important systems and
      independently verified the licensee's actions to address system performance or condition
- 13 -
      problems in terms of the following:
Enclosure 2
      *       Implementing appropriate work practices
The inspectors reviewed events such as where ineffective equipment maintenance has  
      *       Identifying and addressing common cause failures
resulted in valid or invalid automatic actuations of risk-important systems and  
      *       Scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule
independently verified the licensee's actions to address system performance or condition  
      *       Characterizing system reliability issues for performance
problems in terms of the following:  
      *       Charging unavailability time
      *       Trending key parameters for condition monitoring
*  
      *       Ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or reclassification
Implementing appropriate work practices  
      *       Verifying appropriate performance criteria for structures, systems, and
              components/functions classified as (a)(2) or appropriate and adequate goals and
*  
              corrective actions for systems classified as (a)(1)
Identifying and addressing common cause failures  
      The inspectors assessed performance issues with respect to the reliability, availability,
      and condition monitoring of the system. The inspectors verified maintenance
*  
      effectiveness issues were entered into the corrective action program with the appropriate
Scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule  
      significance characterization. Documents reviewed are listed in the attachment.
      This inspection constituted two quarterly maintenance effectiveness samples as defined
*  
      in Inspection Procedure 71111.12Q.
Characterizing system reliability issues for performance  
  b.  Findings
      No findings of significance were identified.
*  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
Charging unavailability time  
  a. Inspection Scope
      The inspectors reviewed the licensee's evaluation and management of plant risk for the
*  
      maintenance and emergent work activities affecting risk-significant and safety-related
Trending key parameters for condition monitoring  
      equipment listed below to verify that the appropriate risk assessments were performed
      prior to removing equipment for work:
*  
      *       April 3, 2008, Routine - Work on turbine-driven auxiliary feedwater
Ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or reclassification  
              Valve KAPCV-0102
      *       April 21, 2008, Emergency Diesel Generator A lube oil trouble shooting
*  
    *       April 28, 2008, Routine - associated with Loose Creek-Callaway 345 kV line
Verifying appropriate performance criteria for structures, systems, and  
              outage
components/functions classified as (a)(2) or appropriate and adequate goals and  
                                          - 13 -                                    Enclosure 2
corrective actions for systems classified as (a)(1)  
The inspectors assessed performance issues with respect to the reliability, availability,  
and condition monitoring of the system. The inspectors verified maintenance  
effectiveness issues were entered into the corrective action program with the appropriate  
significance characterization. Documents reviewed are listed in the attachment.  
This inspection constituted two quarterly maintenance effectiveness samples as defined  
in Inspection Procedure 71111.12Q.  
    b. Findings  
No findings of significance were identified.  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
    a. Inspection Scope  
The inspectors reviewed the licensee's evaluation and management of plant risk for the  
maintenance and emergent work activities affecting risk-significant and safety-related  
equipment listed below to verify that the appropriate risk assessments were performed  
prior to removing equipment for work:  
*  
April 3, 2008, Routine - Work on turbine-driven auxiliary feedwater  
Valve KAPCV-0102  
*  
April 21, 2008, Emergency Diesel Generator A lube oil trouble shooting  
*  
April 28, 2008, Routine - associated with Loose Creek-Callaway 345 kV line  
outage  


    *       June 10, 2008, Risk management actions associated with Emergency Diesel
            Generator B jacket water o-ring replacement outage
    These activities were selected based on their potential risk significance relative to the
- 14 -
    reactor safety cornerstones. As applicable for each activity, the inspectors verified that
Enclosure 2
    risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
*  
    and complete. When emergent work was performed, the inspectors verified that the
June 10, 2008, Risk management actions associated with Emergency Diesel  
    plant risk was promptly reassessed and managed. The inspectors reviewed the scope
Generator B jacket water o-ring replacement outage  
    of maintenance work, discussed the results of the assessment with the licensee's
These activities were selected based on their potential risk significance relative to the  
    probabilistic risk analyst or shift technical advisor, and verified plant conditions were
reactor safety cornerstones. As applicable for each activity, the inspectors verified that  
    consistent with the risk assessment. The inspectors also reviewed Technical
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate  
    Specification requirements and walked down portions of redundant safety systems,
and complete. When emergent work was performed, the inspectors verified that the  
    when applicable, to verify risk analysis assumptions were valid and applicable
plant risk was promptly reassessed and managed. The inspectors reviewed the scope  
    requirements were met. Documents reviewed are listed in the attachment.
of maintenance work, discussed the results of the assessment with the licensee's  
    These activities constituted four samples as defined by Inspection Procedure 71111.13.
probabilistic risk analyst or shift technical advisor, and verified plant conditions were  
  b. Findings
consistent with the risk assessment. The inspectors also reviewed Technical  
    No findings of significance were identified.
Specification requirements and walked down portions of redundant safety systems,  
1R15 Operability Evaluations (71111.15)
when applicable, to verify risk analysis assumptions were valid and applicable  
  a. Inspection Scope
requirements were met. Documents reviewed are listed in the attachment.  
    The inspectors reviewed the following issues:
    *       March 26, 2008, CARs 200802348, 200802365, and 200802264, Containment
These activities constituted four samples as defined by Inspection Procedure 71111.13.  
            coolers inoperable in fast speed
    *       April 4, 2008, CARs 200800461 and 200802625, Containment recirculation sump
    b. Findings  
            operability determination, Revisions 3 and 4
No findings of significance were identified.  
    *       April 9, 2008, Source Range Channel N32 inoperable due to a failed surveillance
    *       April 23, 2008, Component cooling water system following Valve EGHV0069
1R15 Operability Evaluations (71111.15)  
            failing inservice test stroke time surveillance
    a. Inspection Scope  
    *       April 30, 2008, CAR 200803465, Emergency diesel generator Garlock flexible
The inspectors reviewed the following issues:  
            expansion joints
    *       May 6, 2008, CAR 200803462, Voiding identified in containment spray pump
*  
            piping from sump
March 26, 2008, CARs 200802348, 200802365, and 200802264, Containment  
    *       May 22, 2008, CAR 200904000, Line EM-023 allowable void fraction exceeded
coolers inoperable in fast speed  
    The inspectors selected potential operability issues based on the risk significance of the
*  
    associated components and systems. The inspectors evaluated the technical adequacy
April 4, 2008, CARs 200800461 and 200802625, Containment recirculation sump  
    of the evaluations to ensure that Technical Specification operability was properly justified
operability determination, Revisions 3 and 4  
    and the subject component or system remained available such that no unrecognized
*  
    increase in risk occurred. The inspectors compared the operability and design criteria in
April 9, 2008, Source Range Channel N32 inoperable due to a failed surveillance  
    the appropriate sections of the Technical Specifications and FSAR to the licensees
*  
                                          - 14 -                                      Enclosure 2
April 23, 2008, Component cooling water system following Valve EGHV0069  
failing inservice test stroke time surveillance  
*  
April 30, 2008, CAR 200803465, Emergency diesel generator Garlock flexible  
expansion joints  
*  
May 6, 2008, CAR 200803462, Voiding identified in containment spray pump  
piping from sump  
*  
May 22, 2008, CAR 200904000, Line EM-023 allowable void fraction exceeded  
The inspectors selected potential operability issues based on the risk significance of the  
associated components and systems. The inspectors evaluated the technical adequacy  
of the evaluations to ensure that Technical Specification operability was properly justified  
and the subject component or system remained available such that no unrecognized  
increase in risk occurred. The inspectors compared the operability and design criteria in  
the appropriate sections of the Technical Specifications and FSAR to the licensees  


      evaluations to determine whether the components or systems were operable. Where
      compensatory measures were required to maintain operability, the inspectors
      determined whether the measures in place would function as intended and were
- 15 -
      properly controlled. The inspectors determined, where appropriate, compliance with
Enclosure 2
      bounding limitations associated with the evaluations. Additionally, the inspectors
evaluations to determine whether the components or systems were operable. Where  
      reviewed a sample of corrective action documents to verify that the licensee was
compensatory measures were required to maintain operability, the inspectors  
      identifying and correcting deficiencies associated with operability evaluations.
determined whether the measures in place would function as intended and were  
      Documents reviewed are listed in the attachment.
properly controlled. The inspectors determined, where appropriate, compliance with  
      This inspection constituted seven samples as defined in Inspection Procedure 71111.15.
bounding limitations associated with the evaluations. Additionally, the inspectors  
  b. Findings
reviewed a sample of corrective action documents to verify that the licensee was  
.1   Introduction. A self-revealing Green noncited violation (NCV) of 10 CFR Part 50,
identifying and correcting deficiencies associated with operability evaluations.
      Appendix B, Criterion III, Design Control, was identified after determining that the
Documents reviewed are listed in the attachment.  
      licensee had not adequately selected and reviewed the suitability of the design of the
      containment air cooler control circuitry.
This inspection constituted seven samples as defined in Inspection Procedure 71111.15.  
      Description. On March 26, 2008, Containment Air Cooler A fan shut down when shifted
      from fast to slow speed. Troubleshooting by the licensee determined that voltage was
    b. Findings
      lost to the control power circuitry when the fast speed thermal overload tripped. Since
.1  
      the overload contacts were wired in series, Containment Air Cooler A experienced a
Introduction. A self-revealing Green noncited violation (NCV) of 10 CFR Part 50,  
      complete loss of control power rendering it inoperable. AmerenUE personnel noted that
Appendix B, Criterion III, Design Control, was identified after determining that the  
      Precaution 3.6 of Procedure OTN-GN-00001, Containment Cooling and CRDM
licensee had not adequately selected and reviewed the suitability of the design of the  
      Cooling, Revision 14, cautioned that high pressure and cool temperatures across
containment air cooler control circuitry.  
      containment coolers will cause the coolers to operate close to the setpoint of the thermal
      overloads. However, the licensees operability determination dismissed the 1987
Description. On March 26, 2008, Containment Air Cooler A fan shut down when shifted  
      precaution as not having a technical basis believing it was implemented to address
from fast to slow speed. Troubleshooting by the licensee determined that voltage was  
      discrepancies in motor overload setpoints. Later, the licensee determined that operation
lost to the control power circuitry when the fast speed thermal overload tripped. Since  
      of containment air coolers in fast speed, during a period of higher than normal
the overload contacts were wired in series, Containment Air Cooler A experienced a  
      containment pressure, challenged the fast speed thermal overload setpoint and resulted
complete loss of control power rendering it inoperable. AmerenUE personnel noted that  
      in the trip of Containment Air Cooler A on March 26, 2008. As an interim measure to
Precaution 3.6 of Procedure OTN-GN-00001, Containment Cooling and CRDM  
      prevent a trip from fast speed, the licensee imposed a standing order to maintain the
Cooling, Revision 14, cautioned that high pressure and cool temperatures across  
      containment coolers in slow speed.
containment coolers will cause the coolers to operate close to the setpoint of the thermal  
      The licensee analyzed the potential impact of the newly discovered adverse containment
overloads. However, the licensees operability determination dismissed the 1987  
      cooler design vulnerability against design basis accident scenarios. The licensee
precaution as not having a technical basis believing it was implemented to address  
      determined that a hot zero power main steam line break results in a delayed safety
discrepancies in motor overload setpoints. Later, the licensee determined that operation  
      injection signal allowing the fan motor overloads to trip prior to being shed by the load
of containment air coolers in fast speed, during a period of higher than normal  
      sequencer. The containment air coolers would then experience a complete loss of
containment pressure, challenged the fast speed thermal overload setpoint and resulted  
      control power and would not be capable of automatically restarting in slow speed. The
in the trip of Containment Air Cooler A on March 26, 2008. As an interim measure to  
      analysis revealed that in this scenario, utilizing assumed accident conditions, the peak
prevent a trip from fast speed, the licensee imposed a standing order to maintain the  
      containment pressure would exceed the 48.1 psig limit described in the FSAR.
containment coolers in slow speed.  
      However, analysis using actual plant conditions determined that the peak containment
      pressure limit of 48.1 psig would be preserved. The licensee submitted a licensee event
The licensee analyzed the potential impact of the newly discovered adverse containment  
      report (LER) as required by 10 CFR 50.73 since the inadequate containment air cooler
cooler design vulnerability against design basis accident scenarios. The licensee  
      control circuitry resulted in a condition prohibited by the plants Technical Specifications.
determined that a hot zero power main steam line break results in a delayed safety  
      The inspectors review of the licensees LER is described in Section 4OA3 of this report.
injection signal allowing the fan motor overloads to trip prior to being shed by the load  
      To address the design deficiency associated with the containment air cooler control
sequencer. The containment air coolers would then experience a complete loss of  
      circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit
control power and would not be capable of automatically restarting in slow speed. The  
                                          - 15 -                                    Enclosure 2
analysis revealed that in this scenario, utilizing assumed accident conditions, the peak  
containment pressure would exceed the 48.1 psig limit described in the FSAR.
However, analysis using actual plant conditions determined that the peak containment  
pressure limit of 48.1 psig would be preserved. The licensee submitted a licensee event  
report (LER) as required by 10 CFR 50.73 since the inadequate containment air cooler  
control circuitry resulted in a condition prohibited by the plants Technical Specifications.
The inspectors review of the licensees LER is described in Section 4OA3 of this report.  
To address the design deficiency associated with the containment air cooler control  
circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit  


  such that tripping of the fast speed overloads would not impact the safety-related slow
  speed function of the containment air coolers.
  Analysis. The performance deficiency associated with this finding involved the
- 16 -
  licensees failure to ensure the design of the containment air cooler control circuitry was
Enclosure 2
  suitable for all plant conditions. This finding was greater than minor because it was
such that tripping of the fast speed overloads would not impact the safety-related slow  
  associated with the barrier integrity cornerstone attribute of design control and affects
speed function of the containment air coolers.  
  the associated cornerstone objective to provide reasonable assurance that physical
  design barriers protect the public from radio nuclide releases caused by accidents or
Analysis. The performance deficiency associated with this finding involved the  
  releases. Using Manual Chapter 0609, Appendix H, Containment Integrity Significance
licensees failure to ensure the design of the containment air cooler control circuitry was  
  Determination Process," this finding was determined to be a Type B finding since it was
suitable for all plant conditions. This finding was greater than minor because it was  
  related to a degraded condition that has potentially important implications for the integrity
associated with the barrier integrity cornerstone attribute of design control and affects  
  of the containment, without affecting the likelihood of core damage. This finding was
the associated cornerstone objective to provide reasonable assurance that physical  
  found to be of very low safety significance since containment coolers are structures,
design barriers protect the public from radio nuclide releases caused by accidents or  
  systems, and components that have no impact on large early release frequency. The
releases. Using Manual Chapter 0609, Appendix H, Containment Integrity Significance  
  inspectors determined that this finding does not have a crosscutting aspect associated
Determination Process," this finding was determined to be a Type B finding since it was  
  with it since the performance deficiency is not indicative of current licensee performance.
related to a degraded condition that has potentially important implications for the integrity  
  Enforcement. 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in
of the containment, without affecting the likelihood of core damage. This finding was  
  part, that measures be established for the selection and review for suitability of
found to be of very low safety significance since containment coolers are structures,  
  application of materials, parts, equipment, and processes that are essential to the
systems, and components that have no impact on large early release frequency. The  
  safety-related functions of structures, systems, and components. Contrary to the above,
inspectors determined that this finding does not have a crosscutting aspect associated  
  prior to April 2, 2008, the licensee failed to ensure that the containment air coolers would
with it since the performance deficiency is not indicative of current licensee performance.  
  be able to perform their safety-related function in all accident scenarios due to a design
  deficiency associated with the overload contacts in the containment air cooler control
Enforcement. 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in  
  circuitry. Because this finding is of very low safety significance and has been entered
part, that measures be established for the selection and review for suitability of  
  into the corrective action program as CAR 200702264, this violation is being treated as
application of materials, parts, equipment, and processes that are essential to the  
  an NCV consistent with Section VI.A of the NRC Enforcement Policy:
safety-related functions of structures, systems, and components. Contrary to the above,  
  NCV 05000483/2008003-01, Failure to Ensure the Suitability of the Design of the
prior to April 2, 2008, the licensee failed to ensure that the containment air coolers would  
  Containment Air Cooler Control Circuitry.
be able to perform their safety-related function in all accident scenarios due to a design  
.2 Introduction. The inspectors identified a Green NCV of Technical Specification 3.5.2,
deficiency associated with the overload contacts in the containment air cooler control  
  "Emergency Core Cooling Systems," after an inadequate surveillance procedure
circuitry. Because this finding is of very low safety significance and has been entered  
  resulted in the licensee failing to maintain the emergency core cooling system (ECCS)
into the corrective action program as CAR 200702264, this violation is being treated as  
  full of water as required per Technical Specification 3.5.2.
an NCV consistent with Section VI.A of the NRC Enforcement Policy:
  Description. On May 21, 2008, Callaway Plant engineering discovered that a section of
NCV 05000483/2008003-01, Failure to Ensure the Suitability of the Design of the  
  the cold leg recirculation piping, specifically the discharge of the residual heat removal
Containment Air Cooler Control Circuitry.  
  pumps to the safety injection pumps, contained 6.6 cubic feet of air. This exceeded the
  allowable void fraction of 2.1 cubic feet required for operability. Callaway monthly
.2  
  surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow Path
Introduction. The inspectors identified a Green NCV of Technical Specification 3.5.2,  
  Verification and Venting," had a purpose to: "Verify the ECCS is full of water," in
"Emergency Core Cooling Systems," after an inadequate surveillance procedure  
  accordance with Technical Specification Surveillance Requirement 3.5.2.3. This
resulted in the licensee failing to maintain the emergency core cooling system (ECCS)  
  monthly surveillance was reviewed as part of significant condition adverse to quality
full of water as required per Technical Specification 3.5.2.  
  (SCAQ) CAR 200501092 corrective actions. Callaway engineering had determined that
  residual heat removal pump discharge vent Valve EJV0193 to the safety injection
Description. On May 21, 2008, Callaway Plant engineering discovered that a section of  
  system was the high point vent for these lines and was thus sufficient to vent
the cold leg recirculation piping, specifically the discharge of the residual heat removal  
  Line EM-023-HCB - 6" to the safety injection pumps. However, this vent valve was not
pumps to the safety injection pumps, contained 6.6 cubic feet of air. This exceeded the  
  adequate due to the pipe sloping issues and normally closed Valves EMHIS8807A/B.
allowable void fraction of 2.1 cubic feet required for operability. Callaway monthly  
  Venting through Valve EMV0179 was necessary to completely fill, vent, and test the line.
surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow Path  
  The monthly verification and vent procedure was inadequate to identify and remove air
Verification and Venting," had a purpose to: "Verify the ECCS is full of water," in  
                                        - 16 -                                      Enclosure 2
accordance with Technical Specification Surveillance Requirement 3.5.2.3. This  
monthly surveillance was reviewed as part of significant condition adverse to quality  
(SCAQ) CAR 200501092 corrective actions. Callaway engineering had determined that  
residual heat removal pump discharge vent Valve EJV0193 to the safety injection  
system was the high point vent for these lines and was thus sufficient to vent  
Line EM-023-HCB - 6" to the safety injection pumps. However, this vent valve was not  
adequate due to the pipe sloping issues and normally closed Valves EMHIS8807A/B.
Venting through Valve EMV0179 was necessary to completely fill, vent, and test the line.
The monthly verification and vent procedure was inadequate to identify and remove air  


introduced by relief valve maintenance on May 7, 2007, and thus ensure the ECCS was
full of water. See Violation (VIO) 05000483/2008003-05 in Section 4OA2.
Analysis. Failure to adequately verify ECCS piping was full of water as required by
- 17 -
Technical Specification 3.5.2 is a performance deficiency. This finding affected the
Enclosure 2
mitigating system cornerstone procedure quality attribute. This finding is more than
introduced by relief valve maintenance on May 7, 2007, and thus ensure the ECCS was  
minor because it was similar to Example 3e of NRC Inspection Manual Chapter 0612,
full of water. See Violation (VIO) 05000483/2008003-05 in Section 4OA2.  
Appendix E, "Examples of Minor Issues," and met the Not Minor If, criteria because the
failure to meet the licensees administrative requirement for allowable void fraction
Analysis. Failure to adequately verify ECCS piping was full of water as required by  
impacted the ability of the Train A safety injection system to function upon initiation of
Technical Specification 3.5.2 is a performance deficiency. This finding affected the  
high-pressure recirculation. Using Manual Chapter 0609.04, Phase 1 - Initial Screening
mitigating system cornerstone procedure quality attribute. This finding is more than  
and Characterization of Findings, the inspectors determined that this finding should be
minor because it was similar to Example 3e of NRC Inspection Manual Chapter 0612,  
evaluated using the Phase 2 process described in Manual Chapter 0609, Appendix A,
Appendix E, "Examples of Minor Issues," and met the Not Minor If, criteria because the  
Determining the Significance of Reactor Inspection Findings for At-Power Situations.
failure to meet the licensees administrative requirement for allowable void fraction  
As described in Section III of Appendix A, given that the presolved table did not contain
impacted the ability of the Train A safety injection system to function upon initiation of  
a suitable target or surrogate for this finding, the senior reactor analyst used the
high-pressure recirculation. Using Manual Chapter 0609.04, Phase 1 - Initial Screening  
risk-informed notebook to evaluate the significance of this finding. Table 2 provides the
and Characterization of Findings, the inspectors determined that this finding should be  
definitions for acronyms and initialisms used in the risk-informed notebook and
evaluated using the Phase 2 process described in Manual Chapter 0609, Appendix A,  
discussed in this inspection report.
Determining the Significance of Reactor Inspection Findings for At-Power Situations.  
                                          TABLE 2
                  Acronyms and Initialisms used in Phase 2 Notebook
As described in Section III of Appendix A, given that the presolved table did not contain  
          Initialism Initiating Event or Mitigating Function
a suitable target or surrogate for this finding, the senior reactor analyst used the  
          TPCS         Transient with Loss of the Power Conversion System
risk-informed notebook to evaluate the significance of this finding. Table 2 provides the  
          SLOCA       Small-Break Loss of Coolant Accident
definitions for acronyms and initialisms used in the risk-informed notebook and  
          MLOCA       Medium-Break Loss of Coolant Accident
discussed in this inspection report.  
          LLOCA       Large-Break Loss of Coolant Accident
          LOOP         Loss of Offsite Power
TABLE 2  
          MSLB         Main Steam Line Break
Acronyms and Initialisms used in Phase 2 Notebook  
          LBDC         Loss of Vital Direct-Current Bus
Initialism  
          AFW         Auxiliary Feedwater
Initiating Event or Mitigating Function  
          PCS         Power Conversion System (Steam and Feed)
TPCS  
          HPR         High Pressure Recirculation
Transient with Loss of the Power Conversion System  
          DEPR         Depressurization of the Reactor Coolant System
SLOCA  
          EAC         Emergency Power (Alternating Current)
Small-Break Loss of Coolant Accident  
          TDAFW       Turbine-Driven Auxiliary Feedwater Pump Train
MLOCA  
          SEAL         Reactor Coolant Pump Seal Integrity
Medium-Break Loss of Coolant Accident  
          STIN         Operators Stop High-Pressure Injection
LLOCA  
          MDAFW       Motor-Driven Auxiliary Feedwater Pump Train
Large-Break Loss of Coolant Accident  
The analyst performed a Phase 2 estimation in accordance with Inspection Manual
LOOP  
Chapter 0609, Appendix A, Attachment 2, Site Specific Risk-Informed Inspection
Loss of Offsite Power  
Notebook Usage Rules. Given that the performance deficiency was known to have
MSLB  
existed for 378 days (May 7, 2007, until May 21, 2008) the analyst used 1 year as the
Main Steam Line Break  
exposure period. In accordance with Table 2 of the risk-informed notebook, the analyst
LBDC  
evaluated all worksheets except LLOCA. All worksheets were evaluated using the
Loss of Vital Direct-Current Bus  
nominal 1-year initiating event frequency. Because this finding only affected system
AFW  
functionality during recirculation, nominal mitigation credit was given for all functions with
Auxiliary Feedwater  
the exception of HPR. For HPR, the analyst made the bounding assumption that either
PCS  
                                    - 17 -                                      Enclosure 2
Power Conversion System (Steam and Feed)  
HPR  
High Pressure Recirculation  
DEPR  
Depressurization of the Reactor Coolant System  
EAC  
Emergency Power (Alternating Current)  
TDAFW  
Turbine-Driven Auxiliary Feedwater Pump Train  
SEAL  
Reactor Coolant Pump Seal Integrity  
STIN  
Operators Stop High-Pressure Injection  
MDAFW  
Motor-Driven Auxiliary Feedwater Pump Train  
The analyst performed a Phase 2 estimation in accordance with Inspection Manual  
Chapter 0609, Appendix A, Attachment 2, Site Specific Risk-Informed Inspection  
Notebook Usage Rules. Given that the performance deficiency was known to have  
existed for 378 days (May 7, 2007, until May 21, 2008) the analyst used 1 year as the  
exposure period. In accordance with Table 2 of the risk-informed notebook, the analyst  
evaluated all worksheets except LLOCA. All worksheets were evaluated using the  
nominal 1-year initiating event frequency. Because this finding only affected system  
functionality during recirculation, nominal mitigation credit was given for all functions with  
the exception of HPR. For HPR, the analyst made the bounding assumption that either  


both centrifugal charging pumps or both safety injection pumps would be affected. This
assumption was supported by licensee evaluation. The analyst solved each applicable
worksheet and the dominant sequences are documented in Table 1.
- 18 -
                                            TABLE 1
Enclosure 2
                                Phase 2 Dominant Sequences
both centrifugal charging pumps or both safety injection pumps would be affected. This  
      Initiating Event         Sequence       Mitigating Functions             Results
assumption was supported by licensee evaluation. The analyst solved each applicable  
                              Number
worksheet and the dominant sequences are documented in Table 1.  
      Transients                    1         AFW-PCS-HPR                           9
      TPCS                           1         AFW-HPR                               8
TABLE 1  
      SLOCA                         2         DEPR-HPR                             8
Phase 2 Dominant Sequences  
      MLOCA                         2         DEPR-HPR                             9
Initiating Event  
                                    1         AFW-HPR                               9
Sequence  
      LOOP                          5         EAC-TDAFW-HPR                         9
Number
                                    9         EAC-SEAL-HPR                         9
Mitigating Functions  
      MSLB                           8         STIN-HPR                             8
Results  
      LBDC                           8         TDAFW-MDAFW-HPR                       8
Transients
Using Inspection Manual Chapter 0609, Appendix A, Attachment 1, Table 5, Counting
1  
Rule Worksheet, the analyst determined that the risk contribution of this finding from
AFW-PCS-HPR  
internal initiating events was of very low risk significance. In accordance with
9  
Appendix A, Attachment 1, Steps 2.2.5 and 2.2.6, the analyst and determined that the
TPCS  
risk contribution of this finding from external initiating events or the contribution from
1  
large-early release frequency were very low. Therefore, this finding was of very low risk
AFW-HPR  
significance (Green). This finding has a crosscutting aspect in the area of human
8  
performance associated with the decision making component because the licensee
SLOCA  
failed to use conservative assumptions in decision making and did not adopt a
2  
requirement to demonstrate that the single vent Valve EJV0193 was sufficient to vent
DEPR-HPR  
the Line EM-023-HCB - 6" rather than assuming that installed Valve EMV0179 was not
8  
necessary to completely fill, vent, and test the line [H.1(b)].
MLOCA  
Enforcement. Technical Specification 3.5.2 "Emergency Core Cooling Systems,"
2  
Surveillance Requirement 3.5.2.3, required that the licensee verify that ECCS piping is
DEPR-HPR  
full of water every 31 days. Contrary to the above, from June 2007 through April 2008,
9  
AmerenUE surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow
1  
Path Verification and Venting," was inadequate to meet Technical Specification
AFW-HPR  
Surveillance Requirement 3.5.2.3. Because this finding is of very low safety significance
9  
and was entered into the licensee's corrective action program as CAR 200804000, this
5  
violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC
EAC-TDAFW-HPR  
Enforcement Policy: NCV 05000483/2008003-02, Inadequate Surveillance Procedure
9  
Resulted in an Inoperable ECCS.
LOOP
                                      - 18 -                                      Enclosure 2
9  
EAC-SEAL-HPR  
9  
MSLB  
8  
STIN-HPR  
8  
LBDC  
8  
TDAFW-MDAFW-HPR  
8  
Using Inspection Manual Chapter 0609, Appendix A, Attachment 1, Table 5, Counting  
Rule Worksheet, the analyst determined that the risk contribution of this finding from  
internal initiating events was of very low risk significance. In accordance with  
Appendix A, Attachment 1, Steps 2.2.5 and 2.2.6, the analyst and determined that the  
risk contribution of this finding from external initiating events or the contribution from  
large-early release frequency were very low. Therefore, this finding was of very low risk  
significance (Green). This finding has a crosscutting aspect in the area of human  
performance associated with the decision making component because the licensee  
failed to use conservative assumptions in decision making and did not adopt a  
requirement to demonstrate that the single vent Valve EJV0193 was sufficient to vent  
the Line EM-023-HCB - 6" rather than assuming that installed Valve EMV0179 was not  
necessary to completely fill, vent, and test the line [H.1(b)].  
Enforcement. Technical Specification 3.5.2 "Emergency Core Cooling Systems,"  
Surveillance Requirement 3.5.2.3, required that the licensee verify that ECCS piping is  
full of water every 31 days. Contrary to the above, from June 2007 through April 2008,  
AmerenUE surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow  
Path Verification and Venting," was inadequate to meet Technical Specification  
Surveillance Requirement 3.5.2.3. Because this finding is of very low safety significance  
and was entered into the licensee's corrective action program as CAR 200804000, this  
violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC  
Enforcement Policy: NCV 05000483/2008003-02, Inadequate Surveillance Procedure  
Resulted in an Inoperable ECCS.  


1R18 Plant Modifications (71111.18)
  a. Inspection Scope
    The inspectors reviewed the design adequacy of the listed modifications. This included
- 19 -
    verifying that the modification preparation did not impair the following: (a) in-plant
Enclosure 2
    emergency/abnormal operating procedure actions, (b) key safety functions, and
1R18 Plant Modifications (71111.18)  
    (c) operator response to loss of key safety functions.
    a. Inspection Scope  
    The inspectors verified that postmodification testing maintained the plant in a safe
The inspectors reviewed the design adequacy of the listed modifications. This included  
    configuration during testing and that the postmodification testing established operability
verifying that the modification preparation did not impair the following: (a) in-plant  
    by: (a) verifying that unintended system interactions did not occur; (b) verifying that
emergency/abnormal operating procedure actions, (b) key safety functions, and
    performance characteristics, which could have been affected by the modification, met
(c) operator response to loss of key safety functions.  
    the design bases; (c) validating the appropriateness of modification design assumptions;
    and (d) demonstrating that the modification test acceptance criteria had been met.
The inspectors verified that postmodification testing maintained the plant in a safe  
      *     April 18, 2008, Modification M-08-0013 to separate fast and slow speed overload
configuration during testing and that the postmodification testing established operability  
            contacts for containment air coolers
by: (a) verifying that unintended system interactions did not occur; (b) verifying that  
    *       June 1, 2008, Temporary Modification TM 08-0003 for the instrument air system
performance characteristics, which could have been affected by the modification, met  
            to provide an additional diesel-driven air compressor to improve system reliability
the design bases; (c) validating the appropriateness of modification design assumptions;  
            while the system was in degraded reliability
and (d) demonstrating that the modification test acceptance criteria had been met.  
    Documents reviewed are listed in the attachment.
    These activities constituted two samples as defined by Inspection Procedure 71111.18.
*  
  b. Findings
April 18, 2008, Modification M-08-0013 to separate fast and slow speed overload  
    No findings of significance were identified
contacts for containment air coolers  
1R19 Postmaintenance Testing (71111.19)
  a. Inspection Scope
*  
    The inspectors reviewed the following postmaintenance activities to verify that
June 1, 2008, Temporary Modification TM 08-0003 for the instrument air system  
    procedures and test activities were adequate to ensure system operability and functional
to provide an additional diesel-driven air compressor to improve system reliability  
    capability:
while the system was in degraded reliability  
    *       April 10, 2008, Job 08002765.900, Source Range N32 postmaintenance test
      *     April 17, 2008, Postmaintenance test containment Cooler D,
Documents reviewed are listed in the attachment.
            Modification 0800267/950(951)(952)
      *     May 7, 2008, Job 06524419.940, Emergency Diesel Generator B
These activities constituted two samples as defined by Inspection Procedure 71111.18.  
      *     May 28, 2008, Job 08003910, Postmaintence test of Emergency Diesel
            Generator A following repair of jacket water leaks
    b. Findings  
      *     May 30, 2008, Job 08001080, Postmaintenance local leakrate test of
No findings of significance were identified  
            containment personnel hatch door
                                        - 19 -                                      Enclosure 2
1R19 Postmaintenance Testing (71111.19)  
    a. Inspection Scope  
The inspectors reviewed the following postmaintenance activities to verify that  
procedures and test activities were adequate to ensure system operability and functional  
capability:  
*  
April 10, 2008, Job 08002765.900, Source Range N32 postmaintenance test  
*  
April 17, 2008, Postmaintenance test containment Cooler D,  
Modification 0800267/950(951)(952)  
*  
May 7, 2008, Job 06524419.940, Emergency Diesel Generator B
*  
May 28, 2008, Job 08003910, Postmaintence test of Emergency Diesel  
Generator A following repair of jacket water leaks  
*  
May 30, 2008, Job 08001080, Postmaintenance local leakrate test of  
containment personnel hatch door  


  These activities were selected based upon the structure, system, and component's
  ability to impact risk. The inspectors evaluated these activities to verify (as applicable):
  the effect of testing on the plant had been adequately addressed; testing was adequate
- 20 -
  for the maintenance performed; acceptance criteria were clear and demonstrated
Enclosure 2
  operational readiness; test instrumentation was appropriate; tests were performed as
These activities were selected based upon the structure, system, and component's  
  written in accordance with properly reviewed and approved procedures; equipment was
ability to impact risk. The inspectors evaluated these activities to verify (as applicable):
  returned to its operational status following testing (temporary modifications or jumpers
the effect of testing on the plant had been adequately addressed; testing was adequate  
  required for test performance were properly removed after test completion); and test
for the maintenance performed; acceptance criteria were clear and demonstrated  
  documentation was properly evaluated. The inspectors evaluated the activities against
operational readiness; test instrumentation was appropriate; tests were performed as  
  Technical Specifications, the FSAR, 10 CFR Part 50 requirements, licensee procedures,
written in accordance with properly reviewed and approved procedures; equipment was  
  and various NRC generic communications to ensure that the test results adequately
returned to its operational status following testing (temporary modifications or jumpers  
  ensured that the equipment met the licensing basis and design requirements. In
required for test performance were properly removed after test completion); and test  
  addition, the inspectors reviewed corrective action documents associated with
documentation was properly evaluated. The inspectors evaluated the activities against  
  postmaintenance tests to determine whether the licensee was identifying problems and
Technical Specifications, the FSAR, 10 CFR Part 50 requirements, licensee procedures,  
  entering them in the corrective action program and that the problems were being
and various NRC generic communications to ensure that the test results adequately  
  corrected commensurate with their importance to safety. Documents reviewed are listed
ensured that the equipment met the licensing basis and design requirements. In  
  in the attachment.
addition, the inspectors reviewed corrective action documents associated with  
  This inspection constitutes five samples as defined in Inspection Procedure 71111.19.
postmaintenance tests to determine whether the licensee was identifying problems and  
b. Findings
entering them in the corrective action program and that the problems were being  
  Introduction. A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion XVI,
corrected commensurate with their importance to safety. Documents reviewed are listed  
  "Corrective Action," was identified after the licensee failed to promptly correct leakage
in the attachment.  
  from diesel generator jacket water o-rings.
  Description. On February 20, 2008, during performance of Procedure OSP-NE-0001B,
This inspection constitutes five samples as defined in Inspection Procedure 71111.19.
  Standby Diesel Generator B Periodic Tests, Callaway operations personnel identified
    b. Findings  
  that the Emergency Diesel Generator B had an approximately 80 drop-per-minute jacket
Introduction. A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion XVI,  
  water leak. Analysis by the licensee determined the cause of the leakage to be from
"Corrective Action," was identified after the licensee failed to promptly correct leakage  
  premature failure of Nitrile type o-rings in the jacket water supply and return headers.
from diesel generator jacket water o-rings.  
  Operational history at Callaway revealed o-ring failures prior to reaching 3 years of
  service life. The o-rings responsible for the February 20, 2008, leakage had been in
Description. On February 20, 2008, during performance of Procedure OSP-NE-0001B,  
  service since Refueling Outage 14 in October 2005. Following restoration of Emergency
Standby Diesel Generator B Periodic Tests, Callaway operations personnel identified  
  Diesel Generator B, the licensee re-evaluated the preventative maintenance frequency
that the Emergency Diesel Generator B had an approximately 80 drop-per-minute jacket  
  for jacket water o-ring replacement. Based on a review of prior o-ring failures, the
water leak. Analysis by the licensee determined the cause of the leakage to be from  
  replacement schedule for diesel generator jacket water o-rings was reduced from once
premature failure of Nitrile type o-rings in the jacket water supply and return headers.
  every 3 years to once every refueling cycle.
Operational history at Callaway revealed o-ring failures prior to reaching 3 years of  
  On May 28, 2008, during performance of Procedure OSP-NE-0001A, Standby Diesel
service life. The o-rings responsible for the February 20, 2008, leakage had been in  
  Generator A Periodic Tests, Callaway operations personnel identified that Emergency
service since Refueling Outage 14 in October 2005. Following restoration of Emergency  
  Diesel Generator A had a 200 drop-per-minute jacket water leak. Based on the quantity
Diesel Generator B, the licensee re-evaluated the preventative maintenance frequency  
  of the leakage, operations personnel declared Emergency Diesel Generator A
for jacket water o-ring replacement. Based on a review of prior o-ring failures, the  
  inoperable. Similar to the condition observed on Emergency Diesel Generator B on
replacement schedule for diesel generator jacket water o-rings was reduced from once  
  February 20, 2008, the source of the leakage was from Nitrile type o-rings within the
every 3 years to once every refueling cycle.  
  jacket water system. While the licensee replaced the o-rings responsible for jacket
  water leakage following the February 20, 2008, surveillance, several Nitrile type o-rings
On May 28, 2008, during performance of Procedure OSP-NE-0001A, Standby Diesel  
  installed during Refueling Outage 14 in October 2005 remained in service in both
Generator A Periodic Tests, Callaway operations personnel identified that Emergency  
  Emergency Diesel Generators Trains A and B including those that failed during the
Diesel Generator A had a 200 drop-per-minute jacket water leak. Based on the quantity  
  May 28, 2008, surveillance.
of the leakage, operations personnel declared Emergency Diesel Generator A  
                                        - 20 -                                      Enclosure 2
inoperable. Similar to the condition observed on Emergency Diesel Generator B on  
February 20, 2008, the source of the leakage was from Nitrile type o-rings within the  
jacket water system. While the licensee replaced the o-rings responsible for jacket  
water leakage following the February 20, 2008, surveillance, several Nitrile type o-rings  
installed during Refueling Outage 14 in October 2005 remained in service in both  
Emergency Diesel Generators Trains A and B including those that failed during the  
May 28, 2008, surveillance.  


    Subsequent analysis by the licensee determined that the required mission time of the
    Emergency Diesel Generator A was preserved since adequate inventory in the jacket
    water expansion tank existed such that the leakage observed on May 28, 2008, would
- 21 -
    not have impacted the net positive suction head analysis for the jacket water cooling
Enclosure 2
    pump.
Subsequent analysis by the licensee determined that the required mission time of the  
    Analysis. The performance deficiency associated with this finding involved the
Emergency Diesel Generator A was preserved since adequate inventory in the jacket  
    licensees failure to implement adequate corrective actions for an adverse condition.
water expansion tank existed such that the leakage observed on May 28, 2008, would  
    Specifically, the licensee failed to correct degraded Nitrile type o-rings in Emergency
not have impacted the net positive suction head analysis for the jacket water cooling  
    Diesel Generator A after previously identifying the adverse condition on Emergency
pump.  
    Diesel Generator B. This finding was greater than minor because, if left uncorrected,
    degraded diesel generator jacket water o-rings could become a more significant safety
Analysis. The performance deficiency associated with this finding involved the  
    concern. This finding affected the mitigating systems cornerstone. Using Manual
licensees failure to implement adequate corrective actions for an adverse condition.
    Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, this
Specifically, the licensee failed to correct degraded Nitrile type o-rings in Emergency  
    finding was determined be of very low safety significance because it was a design
Diesel Generator A after previously identifying the adverse condition on Emergency  
    deficiency confirmed not to result in loss of operability. This finding had a crosscutting
Diesel Generator B. This finding was greater than minor because, if left uncorrected,  
    aspect in the area of human performance associated with the work control component
degraded diesel generator jacket water o-rings could become a more significant safety  
    because the licensee failed to plan work activities to support long-term equipment
concern. This finding affected the mitigating systems cornerstone. Using Manual  
    reliability by addressing known degraded conditions in a more reactive than preventative
Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, this  
    manner [H.3(b)].
finding was determined be of very low safety significance because it was a design  
    Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires,
deficiency confirmed not to result in loss of operability. This finding had a crosscutting  
    in part, that measures be established to assure conditions adverse to quality are
aspect in the area of human performance associated with the work control component  
    promptly identified and corrected. Contrary to the above, the licensee failed to
because the licensee failed to plan work activities to support long-term equipment  
    implement adequate corrective actions for the identified adverse condition that Nitrile
reliability by addressing known degraded conditions in a more reactive than preventative  
    type o-rings would prematurely fail prior to the completion of the regularly scheduled
manner [H.3(b)].  
    3-year replacement interval. Because this violation is of very low safety significance and
    has been entered into the licensee's corrective action program as CAR 200804164, this
Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires,  
    violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC
in part, that measures be established to assure conditions adverse to quality are  
    Enforcement Policy: NCV 05000483/2008003-03, Failure to Correct a Condition
promptly identified and corrected. Contrary to the above, the licensee failed to  
    Adverse to Quality for Diesel Generator Jacket Water O-Rings.
implement adequate corrective actions for the identified adverse condition that Nitrile  
1R22 Surveillance Testing (71111.22)
type o-rings would prematurely fail prior to the completion of the regularly scheduled  
  a. Inspection Scope
3-year replacement interval. Because this violation is of very low safety significance and  
    The inspectors reviewed the test results for the following activities to determine whether
has been entered into the licensee's corrective action program as CAR 200804164, this  
    risk-significant systems and equipment were capable of performing their intended safety
violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC  
    function and to verify testing was conducted in accordance with applicable procedural
Enforcement Policy: NCV 05000483/2008003-03, Failure to Correct a Condition  
    and Technical Specification requirements:
Adverse to Quality for Diesel Generator Jacket Water O-Rings.  
    *       April 2, 2008, Job 07513515.500, Routine surveillance auxiliary building Train A
              negative pressure test
1R22 Surveillance Testing (71111.22)  
    *       April 4, 2008, Job 08501501, Routine surveillance Slave Relay K645 test of
    a. Inspection Scope  
              essential service water component lineup
The inspectors reviewed the test results for the following activities to determine whether  
    *       April 18, 2008, Job 08501499, Routine surveillance Slave Relay K615 test
risk-significant systems and equipment were capable of performing their intended safety  
    *       April 29, 2008, Job 08501254.500, Residual heat removal Pump A inservice test
function and to verify testing was conducted in accordance with applicable procedural  
                                          - 21 -                                    Enclosure 2
and Technical Specification requirements:  
*  
April 2, 2008, Job 07513515.500, Routine surveillance auxiliary building Train A  
negative pressure test
*  
April 4, 2008, Job 08501501, Routine surveillance Slave Relay K645 test of  
essential service water component lineup  
*  
April 18, 2008, Job 08501499, Routine surveillance Slave Relay K615 test  
*  
April 29, 2008, Job 08501254.500, Residual heat removal Pump A inservice test  


  *       May 5, 2008, Jobs 08502271 and 08503327, Routine surveillance containment
          base strong motion accelerometer seismic monitor calibration
  *       May 14, 2008, Job 07505653, Residual heat removal Train B valve inservice test
- 22 -
  *       June 11, 2008, Job 08504820, Routine surveillance diesel generator Train B
Enclosure 2
          1-hour run
*  
  *       June 17, 2008, Job 08503115, Safety injection system Train A valve inservice
May 5, 2008, Jobs 08502271 and 08503327, Routine surveillance containment  
          test
base strong motion accelerometer seismic monitor calibration  
  *       June 18, 2008, Job 08505155, Routine surveillance ECCS flow path verification
*  
          and venting
May 14, 2008, Job 07505653, Residual heat removal Train B valve inservice test  
  *       June 23, 2008, Job 08506247, Reactor coolant system leakage surveillance,
*  
          reactor coolant system inventory balance, plant status
June 11, 2008, Job 08504820, Routine surveillance diesel generator Train B  
  The inspectors observed in-plant activities and reviewed procedures and associated
1-hour run  
  records to determine whether: any preconditioning occurred; effects of the testing were
*  
  adequately addressed by control room personnel or engineers prior to the
June 17, 2008, Job 08503115, Safety injection system Train A valve inservice  
  commencement of the testing; acceptance criteria were clearly stated, demonstrated
test  
  operational readiness, and were consistent with the system design basis; plant
*  
  equipment calibration was correct, accurate, and properly documented; as left setpoints
June 18, 2008, Job 08505155, Routine surveillance ECCS flow path verification  
  were within required ranges; the calibration frequency was in accordance with Technical
and venting  
  Specifications, the FSAR, procedures, and applicable commitments; measuring and test
*  
  equipment calibration was current; test equipment was used within the required range
June 23, 2008, Job 08506247, Reactor coolant system leakage surveillance,  
  and accuracy; applicable prerequisites described in the test procedures were satisfied;
reactor coolant system inventory balance, plant status  
  test frequencies met Technical Specification requirements to demonstrate operability
The inspectors observed in-plant activities and reviewed procedures and associated  
  and reliability; tests were performed in accordance with the test procedures and other
records to determine whether: any preconditioning occurred; effects of the testing were  
  applicable procedures; jumpers and lifted leads were controlled and restored where
adequately addressed by control room personnel or engineers prior to the  
  used; test data and results were accurate, complete, within limits, and valid; test
commencement of the testing; acceptance criteria were clearly stated, demonstrated  
  equipment was removed after testing; where applicable, test results not meeting
operational readiness, and were consistent with the system design basis; plant  
  acceptance criteria were addressed with an adequate operability evaluation or the
equipment calibration was correct, accurate, and properly documented; as left setpoints  
  system or component was declared inoperable; where applicable for safety-related
were within required ranges; the calibration frequency was in accordance with Technical  
  instrument control surveillance tests, reference setting data were accurately incorporated
Specifications, the FSAR, procedures, and applicable commitments; measuring and test  
  in the test procedure; equipment was returned to a position or status required to support
equipment calibration was current; test equipment was used within the required range  
  the performance of the safety functions; and all problems identified during the testing
and accuracy; applicable prerequisites described in the test procedures were satisfied;  
  were appropriately documented and dispositioned in the corrective action program.
test frequencies met Technical Specification requirements to demonstrate operability  
  Documents reviewed are listed in the attachment.
and reliability; tests were performed in accordance with the test procedures and other  
  The inspectors completed six routine, three inservice test, and one reactor coolant
applicable procedures; jumpers and lifted leads were controlled and restored where  
  system leakage samples.
used; test data and results were accurate, complete, within limits, and valid; test  
b. Findings
equipment was removed after testing; where applicable, test results not meeting  
  Introduction. A self-revealing Green NCV of Technical Specification 5.4.1.a,
acceptance criteria were addressed with an adequate operability evaluation or the  
  Procedures, was identified after Callaway control room operators improperly entered
system or component was declared inoperable; where applicable for safety-related  
  the wrong Technical Specification action statement due to the failure to maintain the
instrument control surveillance tests, reference setting data were accurately incorporated  
  Technical Specification Bases current.
in the test procedure; equipment was returned to a position or status required to support  
                                      - 22 -                                    Enclosure 2
the performance of the safety functions; and all problems identified during the testing  
were appropriately documented and dispositioned in the corrective action program.
Documents reviewed are listed in the attachment.  
The inspectors completed six routine, three inservice test, and one reactor coolant  
system leakage samples.  
    b. Findings  
Introduction. A self-revealing Green NCV of Technical Specification 5.4.1.a,  
Procedures, was identified after Callaway control room operators improperly entered  
the wrong Technical Specification action statement due to the failure to maintain the  
Technical Specification Bases current.  


Description. On June 17, 2008, during surveillance testing, Valve EMHV8823 failed to
indicate fully closed. Since EMHV8823 is an isolation valve for containment
Penetration 49, the licensee entered Technical Specification 3.6.3, Containment
- 23 -
Isolation Valves," Condition C, with an action to restore the valve to an operable status
Enclosure 2
or isolate the penetration within 72 hours. The control room staff believed the
Description. On June 17, 2008, during surveillance testing, Valve EMHV8823 failed to  
appropriate action statement was entered since Condition C is described in the
indicate fully closed. Since EMHV8823 is an isolation valve for containment  
Technical Specification Bases as applicable to flow paths that meet the requirements of
Penetration 49, the licensee entered Technical Specification 3.6.3, Containment  
a closed system per the Callaway FSAR. Chapter 6.2.6.3 of the Callaway FSAR
Isolation Valves," Condition C, with an action to restore the valve to an operable status  
described Containment Penetration 49 as a closed engineered safety feature
or isolate the penetration within 72 hours. The control room staff believed the  
containment penetration.
appropriate action statement was entered since Condition C is described in the  
Approximately 8 hours after Valve EMHV8823 had been declared inoperable, Callaway
Technical Specification Bases as applicable to flow paths that meet the requirements of  
licensing personnel contacted the control room and informed them of an approved
a closed system per the Callaway FSAR. Chapter 6.2.6.3 of the Callaway FSAR  
Technical Specification Bases change that did not allow the classification of containment
described Containment Penetration 49 as a closed engineered safety feature  
Penetration 49 as a closed system. Procedure APA-ZZ-00108, Primary Licensing
containment penetration.  
Document; Change/Revision Process," required that the change be implemented within
45 days following approval. The Technical Specification Bases change was effective
Approximately 8 hours after Valve EMHV8823 had been declared inoperable, Callaway  
May 1, 2008, but had not been issued to the control room. The change resulted in
licensing personnel contacted the control room and informed them of an approved  
Condition C of Technical Specification 3.6.3 applying specifically to penetrations for
Technical Specification Bases change that did not allow the classification of containment  
which a single containment isolation valve is credited per flow path. Since containment
Penetration 49 as a closed system. Procedure APA-ZZ-00108, Primary Licensing  
Penetration 49 relies on multiple valves for flow path isolation, the licensee determined
Document; Change/Revision Process," required that the change be implemented within  
that Condition C of Technical Specification 3.6.3 was not applicable for Penetration 49,
45 days following approval. The Technical Specification Bases change was effective  
and the wrong Technical Specification action statement had been entered following the
May 1, 2008, but had not been issued to the control room. The change resulted in  
failed surveillance on Valve EMHV8823. The licensee determined that the more
Condition C of Technical Specification 3.6.3 applying specifically to penetrations for  
restrictive Technical Specification 3.6.3, Condition A, should have been entered with an
which a single containment isolation valve is credited per flow path. Since containment  
action to isolate the affected penetration within 4 hours.
Penetration 49 relies on multiple valves for flow path isolation, the licensee determined  
The licensee performed a containment entry following discovery of entry into Technical
that Condition C of Technical Specification 3.6.3 was not applicable for Penetration 49,  
Specification 3.6.3, Condition A, and found that Valve EMHV8823 had failed its
and the wrong Technical Specification action statement had been entered following the  
surveillance due to out-of-adjustment position indicator limit switches. The valve was
failed surveillance on Valve EMHV8823. The licensee determined that the more  
verified closed with power removed allowing exit from Technical Specification 3.6.3,
restrictive Technical Specification 3.6.3, Condition A, should have been entered with an  
Condition A.
action to isolate the affected penetration within 4 hours.  
Analysis. The performance deficiency associated with this finding involved the
licensees failure to ensure the Technical Specification Bases were maintained current
The licensee performed a containment entry following discovery of entry into Technical  
and available to the Callaway control room staff. This finding was greater than minor
Specification 3.6.3, Condition A, and found that Valve EMHV8823 had failed its  
because, if left uncorrected, the failure to maintain the Technical Specification Bases
surveillance due to out-of-adjustment position indicator limit switches. The valve was  
current could become a more significant safety concern. This finding was determined to
verified closed with power removed allowing exit from Technical Specification 3.6.3,  
affect the barrier integrity cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial
Condition A.  
Screening and Characterization of Findings," this finding is determined to be of very low
safety significance since this finding did not represent an actual open pathway in the
Analysis. The performance deficiency associated with this finding involved the  
physical integrity of reactor containment and did not involve an actual reduction in
licensees failure to ensure the Technical Specification Bases were maintained current  
function of hydrogen ignitors in the reactor containment. This finding had a crosscutting
and available to the Callaway control room staff. This finding was greater than minor  
aspect in the area of human performance associated with the decision making
because, if left uncorrected, the failure to maintain the Technical Specification Bases  
component because the licensee failed to communicate, in a timely manner, decisions to
current could become a more significant safety concern. This finding was determined to  
personnel who have a need to know the information in order to perform work safely
affect the barrier integrity cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial  
[H.1(c)].
Screening and Characterization of Findings," this finding is determined to be of very low  
Enforcement. Technical Specification 5.4.1.a, Procedures, required that written
safety significance since this finding did not represent an actual open pathway in the  
procedures be established and implemented covering activities specified in Appendix A,
physical integrity of reactor containment and did not involve an actual reduction in  
Typical Procedures for Pressurized Water Reactors, of Regulatory Guide 1.33, Quality
function of hydrogen ignitors in the reactor containment. This finding had a crosscutting  
                                    - 23 -                                    Enclosure 2
aspect in the area of human performance associated with the decision making  
component because the licensee failed to communicate, in a timely manner, decisions to  
personnel who have a need to know the information in order to perform work safely  
[H.1(c)].  
Enforcement. Technical Specification 5.4.1.a, Procedures, required that written  
procedures be established and implemented covering activities specified in Appendix A,  
Typical Procedures for Pressurized Water Reactors, of Regulatory Guide 1.33, Quality  


      Assurance Program Requirements (Operation), February 1978. Regulatory Guide 1.33,
      Appendix A, Section 1, required administrative procedures for procedure review and
      approval. Procedure APA-ZZ-00108 provides a process for implementing Technical
- 24 -
      Specification Bases change notices. Contrary to the above, on May 1, 2008,
Enclosure 2
      Procedure APA-ZZ-00108 was not adequate to ensure changes to the Technical
Assurance Program Requirements (Operation), February 1978. Regulatory Guide 1.33,  
      Specification Bases were implemented in a timely manner. Because of the very low
Appendix A, Section 1, required administrative procedures for procedure review and  
      safety significance and AmerenUEs action to place this issue in their corrective action
approval. Procedure APA-ZZ-00108 provides a process for implementing Technical  
      program as CAR 200805283, this violation is being treated as an NCV in accordance
Specification Bases change notices. Contrary to the above, on May 1, 2008,  
      with Section VI.A.1 of the Enforcement Policy: NCV 05000483/2008003-04, Failure to
Procedure APA-ZZ-00108 was not adequate to ensure changes to the Technical  
      Maintain an Adequate Technical Specification Bases Change Process.
Specification Bases were implemented in a timely manner. Because of the very low  
2.   RADIATION SAFETY
safety significance and AmerenUEs action to place this issue in their corrective action  
      Cornerstone: Occupational Radiation Safety
program as CAR 200805283, this violation is being treated as an NCV in accordance  
2OS1 Access Control to Radiologically Significant Areas (71121.01)
with Section VI.A.1 of the Enforcement Policy: NCV 05000483/2008003-04, Failure to  
  a. Inspection Scope
Maintain an Adequate Technical Specification Bases Change Process.  
      This area was inspected to assess the licensees performance in implementing physical
      and administrative controls for airborne radioactivity areas, radiation areas, high
2.  
      radiation areas, and worker adherence to these controls. The inspectors used the
RADIATION SAFETY  
      requirements in 10 CFR Part 20, the Technical Specifications, and the licensees
      procedures required by Technical Specifications as criteria for determining compliance.
Cornerstone: Occupational Radiation Safety  
      During the inspection, the inspectors interviewed the radiation protection manager,
2OS1 Access Control to Radiologically Significant Areas (71121.01)  
      radiation protection supervisors, and radiation workers. The inspectors performed
    a. Inspection Scope  
      independent radiation dose rate measurements and reviewed the following items:
This area was inspected to assess the licensees performance in implementing physical  
      *       Performance indicator events and associated documentation packages reported
and administrative controls for airborne radioactivity areas, radiation areas, high  
              by the licensee in the occupational radiation safety cornerstone
radiation areas, and worker adherence to these controls. The inspectors used the  
      *       Controls (surveys, posting, and barricades) of radiation, high radiation, or
requirements in 10 CFR Part 20, the Technical Specifications, and the licensees  
              airborne radioactivity areas
procedures required by Technical Specifications as criteria for determining compliance.
      *       Radiation work permits, procedures, engineering controls, and air sampler
During the inspection, the inspectors interviewed the radiation protection manager,  
              locations
radiation protection supervisors, and radiation workers. The inspectors performed  
      *       Physical and programmatic controls for highly activated or contaminated
independent radiation dose rate measurements and reviewed the following items:  
              materials (non-fuel) stored within spent fuel and other storage pools
      *       Self-assessments, audits, LERs, and special reports related to the access control
*  
              program since the last inspection
Performance indicator events and associated documentation packages reported  
      *       Changes in licensee procedural controls of high dose rate - high radiation areas
by the licensee in the occupational radiation safety cornerstone
              and very high radiation areas
*  
      *       Controls for special areas that have the potential to become very high radiation
Controls (surveys, posting, and barricades) of radiation, high radiation, or  
              areas during certain plant operations
airborne radioactivity areas
      *       Posting and locking of entrances to accessible high dose rate - high radiation
*  
              areas and very high radiation areas
Radiation work permits, procedures, engineering controls, and air sampler  
                                          - 24 -                                      Enclosure 2
locations
*  
Physical and programmatic controls for highly activated or contaminated  
materials (non-fuel) stored within spent fuel and other storage pools  
*  
Self-assessments, audits, LERs, and special reports related to the access control  
program since the last inspection
*  
Changes in licensee procedural controls of high dose rate - high radiation areas  
and very high radiation areas
*  
Controls for special areas that have the potential to become very high radiation  
areas during certain plant operations
*  
Posting and locking of entrances to accessible high dose rate - high radiation  
areas and very high radiation areas


    Documents reviewed are listed in the attachment.
    The inspectors completed 8 of the required 21 samples.
  b. Findings
- 25 -
    No findings of significance were identified.
Enclosure 2
2OS2 ALARA Planning and Controls (71121.02)
Documents reviewed are listed in the attachment.  
  a. Inspection Scope
    The inspectors assessed licensee performance with respect to maintaining individual
    and collective radiation exposures as low as is reasonably achievable (ALARA). The
The inspectors completed 8 of the required 21 samples.  
    inspectors used the requirements in 10 CFR Part 20 and the licensees procedures
    required by technical specifications as criteria for determining compliance. The
    b. Findings  
    inspectors interviewed licensee personnel and reviewed:
    *     Current 3-year rolling average collective exposure
No findings of significance were identified.  
    *     Site-specific trends in collective exposures, plant historical data, and source-term
            measurements
2OS2 ALARA Planning and Controls (71121.02)  
    *     Site-specific ALARA procedures
    a. Inspection Scope  
    *     Work activities of highest exposure significance during the inspection
    *     Integration of ALARA requirements into work procedure and radiation work
The inspectors assessed licensee performance with respect to maintaining individual  
            permit documents
and collective radiation exposures as low as is reasonably achievable (ALARA). The  
    *     Post-job (work activity) reviews
inspectors used the requirements in 10 CFR Part 20 and the licensees procedures  
    *     Workers use of the low dose waiting areas
required by technical specifications as criteria for determining compliance. The  
    *     First-line job supervisors contribution to ensuring work activities are conducted in
inspectors interviewed licensee personnel and reviewed:  
            a dose efficient manner
    *     Records detailing the historical trends and current status of tracked plant source
*  
            terms and contingency plans for expected changes in the source term due to
Current 3-year rolling average collective exposure
            changes in plant fuel performance issues or changes in plant primary chemistry
*  
    *     Source-term control strategy or justifications for not pursuing such exposure
Site-specific trends in collective exposures, plant historical data, and source-term  
            reduction initiatives
measurements
    *     Specific sources identified by the licensee for exposure reduction actions,
*  
            priorities established for these actions, and results achieved since the last
Site-specific ALARA procedures  
            refueling cycle
*  
    *     Radiation worker and radiation protection technician performance during work
Work activities of highest exposure significance during the inspection
            activities in radiation areas, airborne radioactivity areas, or high radiation areas
*  
                                          - 25 -                                      Enclosure 2
Integration of ALARA requirements into work procedure and radiation work  
permit documents  
*  
Post-job (work activity) reviews
*  
Workers use of the low dose waiting areas
*  
First-line job supervisors contribution to ensuring work activities are conducted in  
a dose efficient manner
*  
Records detailing the historical trends and current status of tracked plant source  
terms and contingency plans for expected changes in the source term due to  
changes in plant fuel performance issues or changes in plant primary chemistry
*  
Source-term control strategy or justifications for not pursuing such exposure  
reduction initiatives
*  
Specific sources identified by the licensee for exposure reduction actions,
priorities established for these actions, and results achieved since the last  
refueling cycle
*  
Radiation worker and radiation protection technician performance during work  
activities in radiation areas, airborne radioactivity areas, or high radiation areas  


      *       Declared pregnant workers during the current assessment period, monitoring
              controls, and the exposure results
      *       Self-assessments, audits, and special reports related to the ALARA program
- 26 -
              since the last inspection
Enclosure 2
      *       Resolution through the corrective action process of problems identified through
*  
              post-job reviews and post-outage ALARA report critiques
Declared pregnant workers during the current assessment period, monitoring  
      *       Corrective action documents related to the ALARA program and follow-up
controls, and the exposure results
              activities, such as initial problem identification, characterization, and tracking
*  
      *       Effectiveness of self-assessment activities with respect to identifying and
Self-assessments, audits, and special reports related to the ALARA program  
              addressing repetitive deficiencies or significant individual deficiencies
since the last inspection
      Documents reviewed are listed in the attachment.
*  
      The inspectors completed 9 of the required 15 samples and 8 of the optional samples.
Resolution through the corrective action process of problems identified through  
  b. Findings
post-job reviews and post-outage ALARA report critiques
      No findings of significance were identified.
*  
4.   OTHER ACTIVITIES
Corrective action documents related to the ALARA program and follow-up  
4OA1 Performance Indicator Verification (71151)
activities, such as initial problem identification, characterization, and tracking  
.1   Data Submission Issue
*  
  a. Inspection Scope
Effectiveness of self-assessment activities with respect to identifying and  
      The inspectors performed a review of the data submitted by the licensee for the first
addressing repetitive deficiencies or significant individual deficiencies
      Quarter 2008 performance indicators for any obvious inconsistencies prior to its public
Documents reviewed are listed in the attachment.  
      release in accordance with IMC 0608, Performance Indicator Program.
      This review was performed as part of the inspectors normal plant status activities and,
The inspectors completed 9 of the required 15 samples and 8 of the optional samples.
      as such, did not constitute a separate inspection sample.
  b. Findings
    b. Findings  
      No findings of significance were identified.
.2   Safety System Functional Failures
No findings of significance were identified.  
      Cornerstone: Mitigating Systems
  a. Inspection Scope
4.  
      The inspectors sampled licensee submittals for the safety system functional failures
OTHER ACTIVITIES  
      performance indicator for the period March 2007 until March 2008. To determine the
4OA1 Performance Indicator Verification (71151)  
      accuracy of the performance indicator data reported during this period, performance
.1  
      indicator definitions and guidance contained in the Nuclear Energy Institute (NEI)
Data Submission Issue  
                                            - 26 -                                      Enclosure 2
    a. Inspection Scope  
The inspectors performed a review of the data submitted by the licensee for the first  
Quarter 2008 performance indicators for any obvious inconsistencies prior to its public  
release in accordance with IMC 0608, Performance Indicator Program.  
This review was performed as part of the inspectors normal plant status activities and,  
as such, did not constitute a separate inspection sample.  
    b. Findings  
No findings of significance were identified.  
.2  
Safety System Functional Failures  
Cornerstone: Mitigating Systems  
    a. Inspection Scope  
The inspectors sampled licensee submittals for the safety system functional failures  
performance indicator for the period March 2007 until March 2008. To determine the  
accuracy of the performance indicator data reported during this period, performance  
indicator definitions and guidance contained in the Nuclear Energy Institute (NEI)  


      Document 99-02, Revision 5, Regulatory Assessment Performance Indicator
      Guideline, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73,"
      definitions and guidance were used. The inspectors reviewed the licensees operator
- 27 -
      narrative logs, operability assessments, maintenance rule records, maintenance work
Enclosure 2
      orders, issue reports, event reports and NRC integrated inspection reports for the period
Document 99-02, Revision 5, Regulatory Assessment Performance Indicator  
      of 2nd Quarter 2007, through 1st Quarter 2008 to validate the accuracy of the
Guideline, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73,"  
      submittals. The inspectors also reviewed the licensees issue report database to
definitions and guidance were used. The inspectors reviewed the licensees operator  
      determine if any problems had been identified with the performance indicator data
narrative logs, operability assessments, maintenance rule records, maintenance work  
      collected or transmitted for this indicator and none were identified. Documents reviewed
orders, issue reports, event reports and NRC integrated inspection reports for the period  
      are listed in the attachment.
of 2nd Quarter 2007, through 1st Quarter 2008 to validate the accuracy of the  
      This inspection constitutes one safety system functional failures sample as defined by
submittals. The inspectors also reviewed the licensees issue report database to  
      Inspection Procedure 71151.
determine if any problems had been identified with the performance indicator data  
  b. Findings
collected or transmitted for this indicator and none were identified. Documents reviewed  
      No findings of significance were identified.
are listed in the attachment.  
.3   Mitigating Systems Performance Index - High Pressure Injection Systems
      Cornerstone: Mitigating Systems
This inspection constitutes one safety system functional failures sample as defined by  
  a. Inspection Scope
Inspection Procedure 71151.  
      The inspectors sampled licensee submittals for the mitigating systems performance
      index - high pressure injection systems performance indicator for the period from
    b. Findings  
      March 2007 until March 2008. To determine the accuracy of the performance indicator
No findings of significance were identified.  
      data reported during this period, performance indicator definitions and guidance
      contained in the NEI Document 99-02, 5, Regulatory Assessment Performance
.3  
      Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees
Mitigating Systems Performance Index - High Pressure Injection Systems  
      operator narrative logs, issue reports, mitigating systems performance index derivation
      reports, event reports, and NRC integrated inspection reports for the period of
Cornerstone: Mitigating Systems  
      2nd Quarter 2007 through 1st Quarter 2008 to validate the accuracy of the submittals.
    a. Inspection Scope  
      The inspectors reviewed the mitigating systems performance index component risk
The inspectors sampled licensee submittals for the mitigating systems performance  
      coefficient to determine if it had changed by more than 25 percent in value since the
index - high pressure injection systems performance indicator for the period from  
      previous inspection, and if so, that the change was in accordance with applicable NEI
March 2007 until March 2008. To determine the accuracy of the performance indicator  
      guidance. The inspectors also reviewed the licensees issue report database to
data reported during this period, performance indicator definitions and guidance  
      determine if any problems had been identified with the performance indicator data
contained in the NEI Document 99-02, 5, Regulatory Assessment Performance  
      collected or transmitted for this indicator and none were identified. Documents reviewed
Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees  
      are listed in the attachment.
operator narrative logs, issue reports, mitigating systems performance index derivation  
      This inspection constitutes one mitigating systems performance index high pressure
reports, event reports, and NRC integrated inspection reports for the period of  
      injection systems sample as defined by Inspection Procedure 71151.
2nd Quarter 2007 through 1st Quarter 2008 to validate the accuracy of the submittals.
  b. Findings
The inspectors reviewed the mitigating systems performance index component risk  
      No findings of significance were identified.
coefficient to determine if it had changed by more than 25 percent in value since the  
                                          - 27 -                                  Enclosure 2
previous inspection, and if so, that the change was in accordance with applicable NEI  
guidance. The inspectors also reviewed the licensees issue report database to  
determine if any problems had been identified with the performance indicator data  
collected or transmitted for this indicator and none were identified. Documents reviewed  
are listed in the attachment.  
This inspection constitutes one mitigating systems performance index high pressure  
injection systems sample as defined by Inspection Procedure 71151.  
    b. Findings  
No findings of significance were identified.  


.4   Occupational Exposure Control Effectiveness
      Cornerstone: Occupational Radiation Safety
  a. Inspection Scope
- 28 -
      The inspectors reviewed licensee documents from October 1, 2007, through March 31,
Enclosure 2
      2008. The review included corrective action documentation that identified occurrences
.4  
      in locked high radiation areas (as defined in the licensees Technical Specifications),
Occupational Exposure Control Effectiveness  
      very high radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel
      exposures (as defined in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
Cornerstone: Occupational Radiation Safety  
      Revision 5). Additional records reviewed included ALARA records and whole body
    a. Inspection Scope  
      counts of selected individual exposures. The inspectors interviewed licensee personnel
The inspectors reviewed licensee documents from October 1, 2007, through March 31,  
      that were accountable for collecting and evaluating the performance indicator data. In
2008. The review included corrective action documentation that identified occurrences  
      addition, the inspectors toured plant areas to verify that high radiation, locked high
in locked high radiation areas (as defined in the licensees Technical Specifications),  
      radiation, and very high radiation areas were properly controlled. Performance indicator
very high radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel  
      definitions and guidance contained in NEI 99-02, Revision 5, were used to verify the
exposures (as defined in NEI 99-02, "Regulatory Assessment Indicator Guideline,"  
      basis in reporting for each data element.
Revision 5). Additional records reviewed included ALARA records and whole body  
      The inspectors completed the required sample (1) in this cornerstone.
counts of selected individual exposures. The inspectors interviewed licensee personnel  
  b. Findings
that were accountable for collecting and evaluating the performance indicator data. In  
      No findings of significance were identified.
addition, the inspectors toured plant areas to verify that high radiation, locked high  
.5   Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
radiation, and very high radiation areas were properly controlled. Performance indicator  
      Radiological Effluent Occurrences
definitions and guidance contained in NEI 99-02, Revision 5, were used to verify the  
      Cornerstone: Public Radiation Safety
basis in reporting for each data element.  
  a. Inspection Scope
      The inspectors reviewed licensee documents from October 1, 2007, through March 31,
The inspectors completed the required sample (1) in this cornerstone.  
      2008. Licensee records reviewed included corrective action documentation that
      identified occurrences for liquid or gaseous effluent releases that exceeded performance
    b. Findings  
      indicator thresholds and those reported to the NRC. The inspectors interviewed licensee
No findings of significance were identified.  
      personnel that were accountable for collecting and evaluating the performance indicator
      data. Performance indicator definitions and guidance contained in NEI 99-02,
.5  
      Revision 5, were used to verify the basis in reporting for each data element.
Radiological Effluent Technical Specification/Offsite Dose Calculation Manual  
      The inspectors completed the required sample (1) in this cornerstone.
Radiological Effluent Occurrences
  b. Findings
      No findings of significance were identified.
Cornerstone: Public Radiation Safety  
4OA2 Identification and Resolution of Problems (71152)
    a. Inspection Scope  
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
The inspectors reviewed licensee documents from October 1, 2007, through March 31,  
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical
2008. Licensee records reviewed included corrective action documentation that  
      Protection
identified occurrences for liquid or gaseous effluent releases that exceeded performance  
                                          - 28 -                                    Enclosure 2
indicator thresholds and those reported to the NRC. The inspectors interviewed licensee  
personnel that were accountable for collecting and evaluating the performance indicator  
data. Performance indicator definitions and guidance contained in NEI 99-02,  
Revision 5, were used to verify the basis in reporting for each data element.  
The inspectors completed the required sample (1) in this cornerstone.  
    b. Findings  
No findings of significance were identified.  
4OA2 Identification and Resolution of Problems (71152)  
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency  
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical  
Protection  


.1   Routine Review of Items Entered into the Corrective Action Program
  a. Inspection Scope
      As part of the various baseline inspection procedures discussed in previous sections of
- 29 -
      this report, the inspectors routinely reviewed issues during baseline inspection activities
Enclosure 2
      to verify that they were being entered into the licensees corrective action program at an
.1  
      appropriate threshold, that adequate attention was being given to timely corrective
Routine Review of Items Entered into the Corrective Action Program  
      actions, and that adverse trends were identified and addressed. The attributes reviewed
      included: the complete and accurate identification of the problem; that timeliness was
    a. Inspection Scope  
      commensurate with the safety significance; that evaluation and disposition of
As part of the various baseline inspection procedures discussed in previous sections of  
      performance issues, generic implications, common causes, contributing factors, root
this report, the inspectors routinely reviewed issues during baseline inspection activities  
      causes, extent of condition reviews, and previous occurrence reviews were proper and
to verify that they were being entered into the licensees corrective action program at an  
      adequate; and that the classification, prioritization, focus, and timeliness of corrective
appropriate threshold, that adequate attention was being given to timely corrective  
      actions were commensurate with safety and sufficient to prevent recurrence of the issue.
actions, and that adverse trends were identified and addressed. The attributes reviewed  
      These routine reviews for the identification and resolution of problems did not constitute
included: the complete and accurate identification of the problem; that timeliness was  
      any additional inspection samples.
commensurate with the safety significance; that evaluation and disposition of  
  b. Findings
performance issues, generic implications, common causes, contributing factors, root  
      No findings of significance were identified.
causes, extent of condition reviews, and previous occurrence reviews were proper and  
.2   Daily Corrective Action Program Reviews
adequate; and that the classification, prioritization, focus, and timeliness of corrective  
  a. Inspection Scope
actions were commensurate with safety and sufficient to prevent recurrence of the issue.  
      In order to assist with the identification of repetitive equipment failures and specific
      human performance issues for follow-up, the inspectors performed a daily screening of
These routine reviews for the identification and resolution of problems did not constitute  
      items entered into the licensees corrective action program. This review was
any additional inspection samples.  
      accomplished through inspection of the stations daily condition report packages.
      These daily reviews were performed, by procedure, as part of the inspectors daily plant
    b. Findings  
      status monitoring activities and, as such, did not constitute any separate inspection
No findings of significance were identified.  
      samples.
  b. Findings
.2  
      No findings of significance were identified.
Daily Corrective Action Program Reviews  
.3   Selected Issue Follow-up Inspection
    a. Inspection Scope  
  a. Inspection Scope
In order to assist with the identification of repetitive equipment failures and specific  
      The inspectors selected the below listed issues for a more in-depth review. The
human performance issues for follow-up, the inspectors performed a daily screening of  
      inspectors considered the following during the review of AmerenUE's actions:
items entered into the licensees corrective action program. This review was  
      (1) complete and accurate identification of the problem in a timely manner; (2) evaluation
accomplished through inspection of the stations daily condition report packages.  
      and disposition of operability/reportability issues; (3) consideration of extent of condition,
      generic implications, common cause, and previous occurrences; (4) classification and
These daily reviews were performed, by procedure, as part of the inspectors daily plant  
      prioritization of the resolution of the problem; (5) identification of root and contributing
status monitoring activities and, as such, did not constitute any separate inspection  
      causes of the problem; (6) identification of corrective actions; and (7) completion of
samples.  
      corrective actions in a timely manner.
                                            - 29 -                                      Enclosure 2
    b. Findings
No findings of significance were identified.  
.3  
Selected Issue Follow-up Inspection  
    a. Inspection Scope  
The inspectors selected the below listed issues for a more in-depth review. The  
inspectors considered the following during the review of AmerenUE's actions:  
(1) complete and accurate identification of the problem in a timely manner; (2) evaluation  
and disposition of operability/reportability issues; (3) consideration of extent of condition,  
generic implications, common cause, and previous occurrences; (4) classification and  
prioritization of the resolution of the problem; (5) identification of root and contributing  
causes of the problem; (6) identification of corrective actions; and (7) completion of  
corrective actions in a timely manner.


      *       Voiding discovered in the common residual heat removal discharge piping for
              high pressure recirculation.
      *       FSAR changes/updates
- 30 -
  Documents reviewed are listed in the attachment.
Enclosure 2
  This inspection constituted two in-depth problem identification and resolution samples.
b. Findings
*  
  Introduction. The inspectors identified a Green violation of 10 CFR Part 50, Appendix B,
Voiding discovered in the common residual heat removal discharge piping for  
  Criterion XVI, "Corrective Action," because the licensee failed to take corrective actions
high pressure recirculation.  
  to preclude repetition of void formations in the ECCS, a significant condition adverse to
*  
  quality (SCAQ). Contributors to the violation included: (1) the failure of corrective
FSAR changes/updates  
  actions from inspection report findings NCV 05000483/2005002-01,
Documents reviewed are listed in the attachment.  
  05000483/2006012-04 and CAR 200501092 to ensure adequate fill and vent of
  systems following maintenance to replace safety injection system relief valves, and
This inspection constituted two in-depth problem identification and resolution samples.  
  (2) inadequate extent of condition reviews in responding to internal and external
  operating experience associated with pipe sloping issues in the safety injection system.
    b. Findings  
  Description. On May 21, 2008, the Callaway Plant staff initiated CAR 200804000, a
Introduction. The inspectors identified a Green violation of 10 CFR Part 50, Appendix B,  
  SCAQ corrective action document, indicating that some piping in Train A safety injection
Criterion XVI, "Corrective Action," because the licensee failed to take corrective actions  
  system suction lines had incorrect sloping and were susceptible to voiding due to high
to preclude repetition of void formations in the ECCS, a significant condition adverse to  
  points. Callaway Plant engineering performed ultrasonic inspection of the safety
quality (SCAQ). Contributors to the violation included: (1) the failure of corrective  
  injection system common suction piping Line EM023-HCB - 6" and discovered a
actions from inspection report findings NCV 05000483/2005002-01,  
  6.6 cubic foot voided area. This exceeded the allowable void fraction of 2.1 cubic feet
05000483/2006012-04 and CAR 200501092 to ensure adequate fill and vent of
  required for operability. This voided piping, determined to have existed for over a year,
systems following maintenance to replace safety injection system relief valves, and  
  was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The
(2) inadequate extent of condition reviews in responding to internal and external  
  maintenance restoration failed to perform an adequate fill and vent to ensure the suction
operating experience associated with pipe sloping issues in the safety injection system.  
  pipe was full of water.
  In 2005 and 2006 the NRC issued NCVs regarding ineffective corrective actions related
Description. On May 21, 2008, the Callaway Plant staff initiated CAR 200804000, a  
  to safety injection system voids in discharge piping (05000483/2005002-01 dated May 6,
SCAQ corrective action document, indicating that some piping in Train A safety injection  
  2005, and 05000483/2006012-04 dated December 26, 2006). These were each 10 CFR
system suction lines had incorrect sloping and were susceptible to voiding due to high  
  Part 50, Appendix B, Criterion XVI, NCVs, each for SCAQ. The Callaway Plant staff
points. Callaway Plant engineering performed ultrasonic inspection of the safety  
  issued CAR 200501092 as a SCAQ corrective action document. The CAR determined
injection system common suction piping Line EM023-HCB - 6" and discovered a  
  that the causes of the voids (2004, 2005, and 2006) were related to incorrect pipe
6.6 cubic foot voided area. This exceeded the allowable void fraction of 2.1 cubic feet  
  sloping (allowing high points where voids could not be swept away by normal online
required for operability. This voided piping, determined to have existed for over a year,  
  pump surveillances) and inadequate postmaintenance fill and vent operations (following
was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The  
  discharge piping relief Valve EM8853A replacement) to ensure the piping was full of
maintenance restoration failed to perform an adequate fill and vent to ensure the suction  
  water.
pipe was full of water.
  Inadequate Operating Experience and Extent of Condition Corrections: The
  inspectors identified several related examples where the licensee had performed either
In 2005 and 2006 the NRC issued NCVs regarding ineffective corrective actions related  
  inadequate operating experience evaluations, inadequate extent of condition reviews, or
to safety injection system voids in discharge piping (05000483/2005002-01 dated May 6,  
  inadequate procedure corrections.
2005, and 05000483/2006012-04 dated December 26, 2006). These were each 10 CFR  
  Callaway CAR 200501092 referenced industry operating experience at Beaver Valley
Part 50, Appendix B, Criterion XVI, NCVs, each for SCAQ. The Callaway Plant staff  
  Unit 2 in 2002: "The void was located in the piping used following a loss of coolant
issued CAR 200501092 as a SCAQ corrective action document. The CAR determined  
                                      - 30 -                                    Enclosure 2
that the causes of the voids (2004, 2005, and 2006) were related to incorrect pipe  
sloping (allowing high points where voids could not be swept away by normal online  
pump surveillances) and inadequate postmaintenance fill and vent operations (following  
discharge piping relief Valve EM8853A replacement) to ensure the piping was full of  
water.  
Inadequate Operating Experience and Extent of Condition Corrections: The  
inspectors identified several related examples where the licensee had performed either  
inadequate operating experience evaluations, inadequate extent of condition reviews, or  
inadequate procedure corrections.
Callaway CAR 200501092 referenced industry operating experience at Beaver Valley  
Unit 2 in 2002: "The void was located in the piping used following a loss of coolant  


accident after the transfer to containment sump recirculation. The piping containing the
void led to a common suction header for both trains of high head pumps." This was the
same location as the voiding discovered at Callaway Plant on May 21, 2008.
- 31 -
NRC Information Notice 2006-21, "Operating Experience Regarding Entrainment of Air
Enclosure 2
into Emergency Core Cooling and Containment Spray Systems," dated September 21,
accident after the transfer to containment sump recirculation. The piping containing the  
2006, discussed mechanisms that could result in air entrainment on the suction sides of
void led to a common suction header for both trains of high head pumps." This was the  
emergency core cooling pumps. The notice emphasized the importance of ensuring that
same location as the voiding discovered at Callaway Plant on May 21, 2008.  
entrained air will not enter suction supply lines and impair the ability of the ECCS and
containment spray pumps to perform their safety function.
NRC Information Notice 2006-21, "Operating Experience Regarding Entrainment of Air  
The licensee's evaluation of NRC Information Notice 2006-21 was documented in
into Emergency Core Cooling and Containment Spray Systems," dated September 21,  
CAR 200608956. It stated that the information notice was applicable to Callaway and
2006, discussed mechanisms that could result in air entrainment on the suction sides of  
that past review of these operating experiences and Callaway procedures and practices
emergency core cooling pumps. The notice emphasized the importance of ensuring that  
were adequate. The CAR was closed December 5, 2006.
entrained air will not enter suction supply lines and impair the ability of the ECCS and  
Callaway CAR 200501092 had Action 7 assigned to address the previous NRC
containment spray pumps to perform their safety function.  
violations discussed above. The action required that system specific fill and vent
restoration guidance be developed to address maintenance on ECCS safety-related
The licensee's evaluation of NRC Information Notice 2006-21 was documented in  
systems. Initially, operating department Standing Order 05-002 dated June 8, 2005,
CAR 200608956. It stated that the information notice was applicable to Callaway and  
stated that the CAR 200501092 common cause analysis supported the need for
that past review of these operating experiences and Callaway procedures and practices  
formalized restoration instructions. Until the system specific restoration instructions
were adequate. The CAR was closed December 5, 2006.
were developed, the standing order required reactor operators to perform reviews to
ensure dynamic filling and venting occurred to reduce the susceptibility of voiding. Also
Callaway CAR 200501092 had Action 7 assigned to address the previous NRC  
nuclear engineering department staff were to provide concurrence on such restoration
violations discussed above. The action required that system specific fill and vent  
plans. Night Order ODP-ZZ-00310, "System Fill and Vent," issued February 13, 2006,
restoration guidance be developed to address maintenance on ECCS safety-related  
reiterated that reactor operator reviews and engineering concurrence were required
systems. Initially, operating department Standing Order 05-002 dated June 8, 2005,  
when these risk-significant systems were drained. However, on May 7, 2007,
stated that the CAR 200501092 common cause analysis supported the need for  
Procedure OTN-EM-00001, "Safety Injection System," (developed to address filling and
formalized restoration instructions. Until the system specific restoration instructions  
venting evaluations) had Line EM-023-HCB - 6" isolated by Valve EMHIS8807B being
were developed, the standing order required reactor operators to perform reviews to  
closed. The procedure did not include use of the available installed vent Valve EM179
ensure dynamic filling and venting occurred to reduce the susceptibility of voiding. Also  
for this line.
nuclear engineering department staff were to provide concurrence on such restoration  
Callaway monthly Surveillance OSP-SA-00003, "Emergency Core Cooling Flow Path
plans. Night Order ODP-ZZ-00310, "System Fill and Vent," issued February 13, 2006,  
Verification and Venting," had a purpose to: "Verify the ECCS is full of water in
reiterated that reactor operator reviews and engineering concurrence were required  
accordance with Technical Specification Surveillance Requirement 3.5.2.3." This
when these risk-significant systems were drained. However, on May 7, 2007,  
monthly surveillance was reviewed as part of CAR 200501092 corrective actions.
Procedure OTN-EM-00001, "Safety Injection System," (developed to address filling and  
Callaway engineering had determined that residual heat removal pump discharge vent
venting evaluations) had Line EM-023-HCB - 6" isolated by Valve EMHIS8807B being  
Valve EJV0193 to the safety injection suction line was the high point vent for these lines
closed. The procedure did not include use of the available installed vent Valve EM179  
and was thus sufficient to vent supply Line EM-023-HCB - 6" to the safety injection
for this line.  
pumps. However, this vent valve was not adequate due to the pipe sloping issues and
normally closed Valves EMHIS8807A/B. The monthly verification and vent procedure
Callaway monthly Surveillance OSP-SA-00003, "Emergency Core Cooling Flow Path  
was inadequate to remove the air entrained by the May 7, 2007, relief valve
Verification and Venting," had a purpose to: "Verify the ECCS is full of water in  
maintenance. See Section 1R15, NCV 05000483/2008003-02.
accordance with Technical Specification Surveillance Requirement 3.5.2.3." This  
Callaway CARs 200800226 and 200800246, initiated in January 2008, discussed
monthly surveillance was reviewed as part of CAR 200501092 corrective actions.
operating experience at Wolf Creek Nuclear Operating Corporation describing gas
Callaway engineering had determined that residual heat removal pump discharge vent  
voiding in the residual heat removal piggyback Line EM-022-HCB - 6" to the suction of
Valve EJV0193 to the safety injection suction line was the high point vent for these lines  
centrifugal charging pumps and safety injection pumps. The CARs stated that Callaway
and was thus sufficient to vent supply Line EM-023-HCB - 6" to the safety injection  
had taken a proactive approach and had immediately performed ultrasonic testing to
pumps. However, this vent valve was not adequate due to the pipe sloping issues and  
demonstrate that the associated piping was water solid. However, the adjacent
normally closed Valves EMHIS8807A/B. The monthly verification and vent procedure  
                                    - 31 -                                      Enclosure 2
was inadequate to remove the air entrained by the May 7, 2007, relief valve  
maintenance. See Section 1R15, NCV 05000483/2008003-02.
Callaway CARs 200800226 and 200800246, initiated in January 2008, discussed  
operating experience at Wolf Creek Nuclear Operating Corporation describing gas  
voiding in the residual heat removal piggyback Line EM-022-HCB - 6" to the suction of  
centrifugal charging pumps and safety injection pumps. The CARs stated that Callaway  
had taken a proactive approach and had immediately performed ultrasonic testing to  
demonstrate that the associated piping was water solid. However, the adjacent  


connecting Line EM-023-HCB - 6" had not been vented nor had ultrasonic testing
occurred since the May 7, 2007, relief Valve EM8858A maintenance.
NRC Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling,
- 32 -
Decay Heat Removal, and Containment Spray Systems," was issued January 11, 2008.
Enclosure 2
The Callaway Plant staff initiated CAR 200800298 to respond to the generic letter. The
connecting Line EM-023-HCB - 6" had not been vented nor had ultrasonic testing  
generic letter identified that a licensing basis concern existed for some plants, such as
occurred since the May 7, 2007, relief Valve EM8858A maintenance.  
Callaway, that Technical Specifications require verifying that ECCS discharge piping is
full of water but may not include verification of the suction piping despite the realistic
NRC Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling,  
concern that gas accumulation in suction piping may be more serious than gas
Decay Heat Removal, and Containment Spray Systems," was issued January 11, 2008.
accumulation in discharge piping. The void found in Line EM-023-HCB - 6" was the
The Callaway Plant staff initiated CAR 200800298 to respond to the generic letter. The  
discharge of the residual heat removal pumps providing suction to the Train A safety
generic letter identified that a licensing basis concern existed for some plants, such as  
injection pump. The Callaway monthly Surveillance OSP-SA-00003, "Emergency Core
Callaway, that Technical Specifications require verifying that ECCS discharge piping is  
Cooling Flow Path Verification and Venting," did not test for or vent the discharge line
full of water but may not include verification of the suction piping despite the realistic  
from residual heat removal to safety injection pump suction piping.
concern that gas accumulation in suction piping may be more serious than gas  
Analysis. The inspectors determined that the failure to restore compliance within a
accumulation in discharge piping. The void found in Line EM-023-HCB - 6" was the  
reasonable time by establishing measures to prevent void formation in ECCS suction
discharge of the residual heat removal pumps providing suction to the Train A safety  
piping for the Train A safety injection system was a performance deficiency. This finding
injection pump. The Callaway monthly Surveillance OSP-SA-00003, "Emergency Core  
is more than minor because it was similar to Example 3e of NRC Inspection Manual
Cooling Flow Path Verification and Venting," did not test for or vent the discharge line  
Chapter 0612, Appendix E, "Examples of Minor Issues," and met the Not Minor If,
from residual heat removal to safety injection pump suction piping.  
criteria because the failure to meet the licensees administrative requirement for
allowable void fraction impacted the ability of the Train A safety injection system to
Analysis. The inspectors determined that the failure to restore compliance within a  
function upon initiation of high-pressure recirculation. Using Manual Chapter 0609.04,
reasonable time by establishing measures to prevent void formation in ECCS suction  
Phase 1 - Initial Screening and Characterization of Findings, the inspectors determined
piping for the Train A safety injection system was a performance deficiency. This finding  
that this finding should be evaluated using the Phase 2 process described in Manual
is more than minor because it was similar to Example 3e of NRC Inspection Manual  
Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection Findings
Chapter 0612, Appendix E, "Examples of Minor Issues," and met the Not Minor If,  
for At-Power Situations.
criteria because the failure to meet the licensees administrative requirement for  
The senior reactor analyst determined that the risk of this finding was bounded by that
allowable void fraction impacted the ability of the Train A safety injection system to  
analyzed for NCV 05000423/2008003-02 (See Section 1R15.b.2). Therefore, this
function upon initiation of high-pressure recirculation. Using Manual Chapter 0609.04,  
finding was of very low risk significance (Green).
Phase 1 - Initial Screening and Characterization of Findings, the inspectors determined  
This finding has a crosscutting aspect in the area of problem identification and resolution
that this finding should be evaluated using the Phase 2 process described in Manual  
associated with the corrective action component because AmerenUE failed to thoroughly
Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection Findings  
evaluate voiding problems such that the resolutions addressed causes and extent of
for At-Power Situations.  
condition, as necessary. This also includes, for significant problems, conducting
effectiveness reviews of corrective actions to ensure that the problems are resolved
The senior reactor analyst determined that the risk of this finding was bounded by that  
[P.1(c)].
analyzed for NCV 05000423/2008003-02 (See Section 1R15.b.2). Therefore, this  
Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires
finding was of very low risk significance (Green).  
the licensee to, in the case of SCAQ, establish measures to assure that the cause of the
condition is determined and corrective action is taken to preclude repetition. Contrary to
This finding has a crosscutting aspect in the area of problem identification and resolution  
the above, from December 26, 2006, to May 21, 2008, the licensee did not implement
associated with the corrective action component because AmerenUE failed to thoroughly  
corrective action to preclude repetition of void formation in the safety injection piping
evaluate voiding problems such that the resolutions addressed causes and extent of  
which the licensee categorized as an SCAQ. Specifically, void formation recurred after
condition, as necessary. This also includes, for significant problems, conducting  
performing maintenance on relief valve. Valve EM8858A, on May 7, 2007. Previously
effectiveness reviews of corrective actions to ensure that the problems are resolved  
discovered voiding of the safety injection system was last documented as an SCAQ in
[P.1(c)].  
NCV 05000483/2006012-04 dated December 26, 2006. For each instance of the
previously discovered voids, the causes were determined to be related to inadequate fill
Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires  
and vent of the system piping following relief valve replacements and design deficiencies
the licensee to, in the case of SCAQ, establish measures to assure that the cause of the  
                                      - 32 -                                    Enclosure 2
condition is determined and corrective action is taken to preclude repetition. Contrary to  
the above, from December 26, 2006, to May 21, 2008, the licensee did not implement  
corrective action to preclude repetition of void formation in the safety injection piping  
which the licensee categorized as an SCAQ. Specifically, void formation recurred after  
performing maintenance on relief valve. Valve EM8858A, on May 7, 2007. Previously  
discovered voiding of the safety injection system was last documented as an SCAQ in  
NCV 05000483/2006012-04 dated December 26, 2006. For each instance of the  
previously discovered voids, the causes were determined to be related to inadequate fill  
and vent of the system piping following relief valve replacements and design deficiencies  


  associated with inadequate sloping of the piping. It was a reasonable assumption that
  maintenance that drained either the suction or discharge piping could create significant
  void areas.
- 33 -
  Although this violation is of very low safety significance, the violation is being
Enclosure 2
  cited in a Notice of Violation consistent with Section VI.A.1 of the NRC Enforcement
associated with inadequate sloping of the piping. It was a reasonable assumption that  
  Policy because the licensee did not restore compliance within a reasonable
maintenance that drained either the suction or discharge piping could create significant  
  time after a previous violation NCV 05000483/2006012-04 was identified:
void areas.  
  VIO 05000483/2008003-05, Failure to Prevent Recurrence of Voids in ECCS Cold Leg
  Recirculation Piping. This finding has been entered into the licensee's corrective action
Although this violation is of very low safety significance, the violation is being
  program as a SCAQ in CAR 200804000.
cited in a Notice of Violation consistent with Section VI.A.1 of the NRC Enforcement  
.4 Semiannual Trend Review
Policy because the licensee did not restore compliance within a reasonable
  The inspectors assessed trends that might indicate the existence of a more significant
time after a previous violation NCV 05000483/2006012-04 was identified:
  safety issue. These issues included trends that might not rise to the level of an
VIO 05000483/2008003-05, Failure to Prevent Recurrence of Voids in ECCS Cold Leg  
  inspection finding.
Recirculation Piping. This finding has been entered into the licensee's corrective action  
  NRC-Identified Trends
program as a SCAQ in CAR 200804000.  
  The NRC identified emergency diesel generator material condition and design control
  issues degrading diesel reliability:
.4  
  *       CAR 200801270: 80 Drops per minute jacket water leak identified on Diesel
Semiannual Trend Review  
          Generator B
The inspectors assessed trends that might indicate the existence of a more significant  
  *       CAR 200801644: Additional sacrificial anode found in Emergency Diesel
safety issue. These issues included trends that might not rise to the level of an  
          Generator A intercooler heat exchanger
inspection finding.  
  *       CAR 200802019: Emergency Diesel Generator B declared inoperable due to
 
          fuel oil leaks
  *       CAR 200802177: Cracked fuel oil return line fitting identified on Emergency
NRC-Identified Trends  
            Diesel Generator A
The NRC identified emergency diesel generator material condition and design control  
  *       CAR 200804164: Emergency Diesel Generator A declared inoperable due to a
issues degrading diesel reliability:  
          200 drops per minute jacket water leak
  Licensee-Identified Trends
*  
  The licensee identified a continued trend in plant status control and configuration control
CAR 200801270: 80 Drops per minute jacket water leak identified on Diesel  
  with a key causal factor being procedure adherence.
Generator B  
  *       CAR 200706832: This trend CAR from Third Quarter 2007 identified the cause
*  
          of plant status control issues to be a "Failure to follow written instructions."
CAR 200801644: Additional sacrificial anode found in Emergency Diesel  
  *       CAR 200801457: A gauge was installed on an incorrect component during Test
Generator A intercooler heat exchanger  
            Procedure OSP-EN-P001A.
*  
  *       CAR 200800580: A trend of critical steps not being included in work packages
CAR 200802019: Emergency Diesel Generator B declared inoperable due to  
            was identified.
fuel oil leaks  
                                        - 33 -                                        Enclosure 2
*  
CAR 200802177: Cracked fuel oil return line fitting identified on Emergency  
Diesel Generator A  
*  
CAR 200804164: Emergency Diesel Generator A declared inoperable due to a  
200 drops per minute jacket water leak  
Licensee-Identified Trends    
The licensee identified a continued trend in plant status control and configuration control  
with a key causal factor being procedure adherence.  
*  
CAR 200706832: This trend CAR from Third Quarter 2007 identified the cause  
of plant status control issues to be a "Failure to follow written instructions."
*  
CAR 200801457: A gauge was installed on an incorrect component during Test  
Procedure OSP-EN-P001A.
*  
CAR 200800580: A trend of critical steps not being included in work packages  
was identified.  


      *       CAR 200802603: Component cooling water pump autostarted due to an
              interlock with the centrifugal charging pumps. The operator failed to wait the
              procedure prerequisite 30 minutes prior to securing the component cooling water
- 34 -
              pump.
Enclosure 2
      *       CAR 200802818: Source range Channel N31 was not restored to "block" as
*  
              required by procedure in Mode 1.
CAR 200802603: Component cooling water pump autostarted due to an  
      *       CAR 200800328: Not following procedures resulted in gaseous Radiation
interlock with the centrifugal charging pumps. The operator failed to wait the  
              Monitor RM-11 trip setpoint not being capable of isolating the waste gas decay
procedure prerequisite 30 minutes prior to securing the component cooling water  
              tank release.
pump.  
      *       CAR 200803351: Steam generator blowdown tripped due to an incorrect
*  
              demineralizer valve lineup.
CAR 200802818: Source range Channel N31 was not restored to "block" as  
    *       CAR 200804483: Train B motor-driven auxiliary feedwater pump made
required by procedure in Mode 1.  
              inoperable when its room cooler was taken to "stop" vice "auto." This was
*  
              performed outside the out of service restoration process.
CAR 200800328: Not following procedures resulted in gaseous Radiation  
    This inspection constituted one semiannual trend review sample.
Monitor RM-11 trip setpoint not being capable of isolating the waste gas decay  
4OA3 Event Follow-up (71153)
tank release.
    (Closed) LER 05000483/2008-001-00, Containment Cooler Inoperability
*  
    On March 26, 2008, Containment Air Cooler A fan shut down when shifted from fast to
CAR 200803351: Steam generator blowdown tripped due to an incorrect  
    slow speed. The licensee determined that operation of containment air coolers in fast
demineralizer valve lineup.  
    speed, during a period of higher than normal containment pressure, would challenge the
*  
    fast speed thermal overload setpoint. Additionally, since the overload contacts are wired
CAR 200804483: Train B motor-driven auxiliary feedwater pump made  
    in series, containment air coolers were determined to experience a complete loss of
inoperable when its room cooler was taken to "stop" vice "auto." This was  
    control power following a trip from fast speed. The licensee analyzed the potential
performed outside the out of service restoration process.  
    impact of the containment cooler design vulnerability against design basis accident
This inspection constituted one semiannual trend review sample.  
    scenarios. The licensee determined that a hot zero power main steam line break results
    in a delayed safety injection signal allowing the fan motor overloads to trip prior to being
4OA3 Event Follow-up (71153)  
    shed from the load sequencer. In this scenario, utilizing actual plant conditions, the peak
(Closed) LER 05000483/2008-001-00, Containment Cooler Inoperability
    containment pressure would not exceed the 48.1 psig limit described in the FSAR. To
On March 26, 2008, Containment Air Cooler A fan shut down when shifted from fast to  
    address the design deficiency associated with the containment air cooler control
slow speed. The licensee determined that operation of containment air coolers in fast  
    circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit
speed, during a period of higher than normal containment pressure, would challenge the  
    such that tripping of the fast speed overloads would not impact the safety-related slow
fast speed thermal overload setpoint. Additionally, since the overload contacts are wired  
    speed function of the containment air coolers. This finding is of very low safety
in series, containment air coolers were determined to experience a complete loss of  
    significance because the containment coolers are structures, systems, and components
control power following a trip from fast speed. The licensee analyzed the potential  
    that are not significant contributors to the large early release frequency. Licensee
impact of the containment cooler design vulnerability against design basis accident  
    corrective actions were recorded in CAR 200802264. The inspectors reviewed the LER
scenarios. The licensee determined that a hot zero power main steam line break results  
    and identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design
in a delayed safety injection signal allowing the fan motor overloads to trip prior to being  
    Control, for the licensees failure to adequately review the suitability of the design of the
shed from the load sequencer. In this scenario, utilizing actual plant conditions, the peak  
    containment air cooler control circuitry (Section 1R15). This LER is closed.
containment pressure would not exceed the 48.1 psig limit described in the FSAR. To  
    This inspection constituted one sample of follow-up of events.
address the design deficiency associated with the containment air cooler control  
                                          - 34 -                                      Enclosure 2
circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit  
such that tripping of the fast speed overloads would not impact the safety-related slow  
speed function of the containment air coolers. This finding is of very low safety  
significance because the containment coolers are structures, systems, and components  
that are not significant contributors to the large early release frequency. Licensee  
corrective actions were recorded in CAR 200802264. The inspectors reviewed the LER  
and identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design  
Control, for the licensees failure to adequately review the suitability of the design of the  
containment air cooler control circuitry (Section 1R15). This LER is closed.  
This inspection constituted one sample of follow-up of events.  


4OA5 Other Activities
.1   Quarterly Resident Inspector Observations of Security Personnel and Activities
  a. During the inspection period, the inspectors performed the following observations of
- 35 -
      security force personnel and activities to ensure that the activities were consistent with
Enclosure 2
      licensees security procedures and regulatory requirements relating to nuclear plant
4OA5 Other Activities  
      security. These observations took place during both normal and off-normal plant
.1  
      working hours.
Quarterly Resident Inspector Observations of Security Personnel and Activities  
      These quarterly resident inspector observation of security force personnel and activities
      did not constitute any additional inspection samples. Rather, they were considered an
    a.  
      integral part of the inspectors normal plant status review and inspection activities.
During the inspection period, the inspectors performed the following observations of  
  b.  Findings
security force personnel and activities to ensure that the activities were consistent with  
      No findings of significance were identified.
licensees security procedures and regulatory requirements relating to nuclear plant  
.2   (Closed) NRC Temporary Instruction 2515/166: Pressurized Water Reactor
security. These observations took place during both normal and off-normal plant  
      Containment Sump Blockage
working hours.  
  a. Inspection Scope
      From March 17-19, 2008, the inspectors reviewed the licensees implementation of plant
      modifications and design modification packages associated with their response to
These quarterly resident inspector observation of security force personnel and activities  
      Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency
did not constitute any additional inspection samples. Rather, they were considered an  
      Recirculation During Design Basis Accidents at Pressurized Water Reactors. The
integral part of the inspectors normal plant status review and inspection activities.  
      inspectors reviewed various aspects of the on-going procedural changes. Those
      changes that have been completed were verified to be properly documented in
    b.  
      accordance with the requirements of 10 CFR 50.59. At the completion of this inspection,
Findings
      the licensee had completed the installation stage of the new sump strainers; many of the
      procedural changes associated with the modifications had not been completed.
   
      The inspectors compared and evaluated the recirculation sump modifications to the
No findings of significance were identified.  
      original design basis using Temporary Instruction 2515/166 and referred to Regulatory
      Guide 1.82, Revision 0, Water Sources for Long-Term Recirculation Cooling Following
.2  
      a Loss-of-Coolant Accident.
(Closed) NRC Temporary Instruction 2515/166: Pressurized Water Reactor  
      Status of the implementation of the plant modifications and procedure changes
Containment Sump Blockage
      committed to by the licensee in their Generic Letter 2004-02 response is:
      1.     Containment walkdown to provide current assessment of Callaway's containment
    a. Inspection Scope  
              coatings and latent debris.
              The licensee completed a containment walkdown and latent debris assessment
From March 17-19, 2008, the inspectors reviewed the licensees implementation of plant  
              during Refueling Outage 14. The resident inspectors completed a walkdown of
modifications and design modification packages associated with their response to  
              the containment prior to reactor startup following the outage. The licensee
Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency  
              report, Containment Building Latent Debris Assessment Refuel 14 Fall 2005,
Recirculation During Design Basis Accidents at Pressurized Water Reactors. The  
              was reviewed by the inspectors.
inspectors reviewed various aspects of the on-going procedural changes. Those  
                                          - 35 -                                    Enclosure 2
changes that have been completed were verified to be properly documented in  
accordance with the requirements of 10 CFR 50.59. At the completion of this inspection,  
the licensee had completed the installation stage of the new sump strainers; many of the  
procedural changes associated with the modifications had not been completed.
The inspectors compared and evaluated the recirculation sump modifications to the  
original design basis using Temporary Instruction 2515/166 and referred to Regulatory  
Guide 1.82, Revision 0, Water Sources for Long-Term Recirculation Cooling Following  
a Loss-of-Coolant Accident.
Status of the implementation of the plant modifications and procedure changes  
committed to by the licensee in their Generic Letter 2004-02 response is:  
1.  
Containment walkdown to provide current assessment of Callaway's containment  
coatings and latent debris.  
The licensee completed a containment walkdown and latent debris assessment  
during Refueling Outage 14. The resident inspectors completed a walkdown of  
the containment prior to reactor startup following the outage. The licensee  
report, Containment Building Latent Debris Assessment Refuel 14 Fall 2005,  
was reviewed by the inspectors.  


2. The following corrective action activities will be completed:
  a.     Replacement sump strainer structural analysis.
          The strainers were not built in accordance with the design. As a result,
- 36 -
          calculations needed to be revised due to the deviations of the as built
Enclosure 2
          condition from design and errors in temperature correction values used in
2.
          the initial calculations. Completion date: June 30, 2008
The following corrective action activities will be completed:  
  b.     Downstream effects evaluation
a.  
          Completion date: June 30, 2008
Replacement sump strainer structural analysis.  
  c.     Upstream effects evaluation
The strainers were not built in accordance with the design. As a result,  
          Completion date: June 30, 2008
calculations needed to be revised due to the deviations of the as built  
  d.     Resolution of debris generation calculation unverified assumption of 5D
condition from design and errors in temperature correction values used in  
          ZOI for qualified coatings (via coatings testing)
the initial calculations. Completion date: June 30, 2008  
          Completion date: June 30, 2008
  e.     Replacement sump screen head loss testing
b.  
          Completion date: June 30, 2008
Downstream effects evaluation  
3. Provide an update of the information contained in Section 2(c) regarding analysis
  methodology.
Completion date: June 30, 2008  
  Completion date: June 30, 2008
4. The following evaluations and testing will be completed.
c.  
  a.     Industry chemical effects testing
Upstream effects evaluation  
          Completion date: June 30, 2008
  b.     Nuclear Energy Institute 04-07 debris generation calculation
Completion date: June 30, 2008  
          Completion date: June 30, 2008
  c.     Evaluation of chemical effects impact on sump-strainer head loss
d.
          Completion date: June 30, 2008
Resolution of debris generation calculation unverified assumption of 5D  
  d.     Confirmation that the replacement sump strainer design provides for
ZOI for qualified coatings (via coatings testing)  
          available Net Positive Suction Head (NPSH) to be in excess of required
          NPSH
Completion date: June 30, 2008  
          Completion date: June 30, 2008
                                - 36 -                                  Enclosure 2
e.
Replacement sump screen head loss testing  
Completion date: June 30, 2008  
3.  
Provide an update of the information contained in Section 2(c) regarding analysis  
methodology.  
Completion date: June 30, 2008  
4.
The following evaluations and testing will be completed.  
a.  
Industry chemical effects testing  
Completion date: June 30, 2008  
b.
Nuclear Energy Institute 04-07 debris generation calculation  
Completion date: June 30, 2008  
c.
Evaluation of chemical effects impact on sump-strainer head loss  
Completion date: June 30, 2008  
d.
Confirmation that the replacement sump strainer design provides for  
available Net Positive Suction Head (NPSH) to be in excess of required  
NPSH  
Completion date: June 30, 2008  


  e.     Completion of the final site acceptance review of the Westinghouse team
          analysis summary report
          Completion date: June 30, 2008
- 37 -
5. Callaway Plant will complete the following items during Refueling Outage15:
Enclosure 2
  a.     Replacement of containment recirculation sump strainers
e.
          Completed. As noted in the previous Temporary Instruction 166 report,
Completion of the final site acceptance review of the Westinghouse team  
          the resident inspectors had observed the installation of sump strainers
analysis summary report  
          and debris barriers during their containment walkdown; however, the
          strainers were not built in accordance with the design. The licensee has
Completion date: June 30, 2008  
          completed their initial determination of operability and was finalizing their
          acceptance calculations.
5.
  b.     Modification of containment debris barriers and interceptors as required
Callaway Plant will complete the following items during Refueling Outage15:  
          Completed. As noted in the previous Temporary Instruction 166 report,
a.  
          the resident inspectors had observed the installation of sump strainers
Replacement of containment recirculation sump strainers  
          and debris barriers during their containment walkdown.
Completed. As noted in the previous Temporary Instruction 166 report,  
  c.     Evaluation and implementation of potential modification to the safety
the resident inspectors had observed the installation of sump strainers  
          injection system to address downstream effects
and debris barriers during their containment walkdown; however, the  
          Completion date: June 30, 2008
strainers were not built in accordance with the design. The licensee has  
6. Callaway Plant will complete removal of containment spray system pump cyclone
completed their initial determination of operability and was finalizing their  
  separators, if required, based on the results of the downstream effects
acceptance calculations.  
  evaluation.
  Completion date: June 30, 2008
b.
7. The following programs and controls will be implemented at Callaway Plant to
Modification of containment debris barriers and interceptors as required  
  control debris sources:
Completed. As noted in the previous Temporary Instruction 166 report,  
  a.     Changes to design change process procedures to ensure that necessary
the resident inspectors had observed the installation of sump strainers  
          engineering evaluations will be performed for plant design that either
and debris barriers during their containment walkdown.  
          directly or indirectly affects containment, ECCS, or CSS.
          Changes are being processed.
c.
  b.     Changes to containment entry and material control procedure
Evaluation and implementation of potential modification to the safety  
          requirements for control of materials during work activities conducted in
injection system to address downstream effects  
          the containment
  c.     The following procedures were reviewed and completed as of
Completion date: June 30, 2008  
          December 2007:
          APA-ZZ-01004, Radiological Work Standards, Revision 9
6.
          HDP-ZZ-06100, Reactor Building Access, Revision 7
Callaway Plant will complete removal of containment spray system pump cyclone  
                                - 37 -                                    Enclosure 2
separators, if required, based on the results of the downstream effects  
evaluation.  
Completion date: June 30, 2008  
7.
The following programs and controls will be implemented at Callaway Plant to  
control debris sources:  
a.  
Changes to design change process procedures to ensure that necessary  
engineering evaluations will be performed for plant design that either  
directly or indirectly affects containment, ECCS, or CSS.  
Changes are being processed.
b.  
Changes to containment entry and material control procedure  
requirements for control of materials during work activities conducted in  
the containment  
c.  
The following procedures were reviewed and completed as of  
December 2007:  
APA-ZZ-01004, Radiological Work Standards, Revision 9  
HDP-ZZ-06100, Reactor Building Access, Revision 7  


  MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22
  OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6
  OSP-SA-00004, Visual Inspection of Containment for Loose Debris,
- 38 -
  Revision 19
Enclosure 2
  OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices,
MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22  
  Revision 2
OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6  
d. Changes to programs and procedures that have the potential to add tags
OSP-SA-00004, Visual Inspection of Containment for Loose Debris,  
  and labels inside containment
Revision 19  
  Completed: December 2007
OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices,  
  The following documents were reviewed:
Revision 2  
  APA-ZZ-01004, Radiological Work Standards, Revision 9
d.
  HDP-ZZ-06100, Reactor Building Access, Revision 7
Changes to programs and procedures that have the potential to add tags  
  MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22
and labels inside containment  
  OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6
  OSP-SA-00004, Visual Inspection of Containment for Loose Debris,
Completed: December 2007  
  Revision 19
  OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices,
The following documents were reviewed:  
  Revision 2
e. Implementation of a containment coatings assessment program
APA-ZZ-01004, Radiological Work Standards, Revision 9  
  Licensee reported as complete. The inspectors reviewed SWE07848,
HDP-ZZ-06100, Reactor Building Access, Revision 7  
  Containment Coating Condition Assessment. A preventative
MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22
  maintenance item has been scheduled to perform containment coating
OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6  
  assessments with a periodicity of each refueling cycle.
OSP-SA-00004, Visual Inspection of Containment for Loose Debris,  
f. Implementation of a containment latent debris assessment program
Revision 19  
  Licensee reported as complete. The inspectors reviewed report,
OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices,  
  Containment Building Latent Debris Assessment Refuel 14 Fall 2005,
Revision 2  
  and Procedure OSP-SA-00004, Visual Inspection of Containment for
e.
  Loose Debris, Revision 019. A preventative maintenance item has been
Implementation of a containment coatings assessment program  
  scheduled for a visual inspection of containment for loose debris with a
Licensee reported as complete. The inspectors reviewed SWE07848,  
  periodicity of each refueling cycle.
Containment Coating Condition Assessment. A preventative  
g. Implementation of changes to the inspection processes for the installed
maintenance item has been scheduled to perform containment coating  
  sump strainers
assessments with a periodicity of each refueling cycle.
  Licensee reported as complete. Reviewed Procedure OSP-EJ-00003,
  Containment Recirculation Sump Inspection, Revision 6
f.  
                        - 38 -                                  Enclosure 2
Implementation of a containment latent debris assessment program  
Licensee reported as complete. The inspectors reviewed report,  
Containment Building Latent Debris Assessment Refuel 14 Fall 2005,  
and Procedure OSP-SA-00004, Visual Inspection of Containment for  
Loose Debris, Revision 019. A preventative maintenance item has been  
scheduled for a visual inspection of containment for loose debris with a  
periodicity of each refueling cycle.  
g.  
Implementation of changes to the inspection processes for the installed  
sump strainers  
Licensee reported as complete. Reviewed Procedure OSP-EJ-00003,  
Containment Recirculation Sump Inspection, Revision 6


    8.     A final response will be submitted to the NRC to provide a final status of actions
            requested by Generic Letter 2004-02.
            Completion date: June 30, 2008
- 39 -
    The Office of Nuclear Reactor Regulation will determine the adequacy of the sump
Enclosure 2
    modifications with respect to Generic Safety Issue 191. This temporary instruction is
8.  
    closed.
A final response will be submitted to the NRC to provide a final status of actions  
    Documents reviewed by the inspectors are listed in the attachment.
requested by Generic Letter 2004-02.  
  b. Findings
Completion date: June 30, 2008
    No findings of significance were identified.
4OA6 Management Meetings
The Office of Nuclear Reactor Regulation will determine the adequacy of the sump  
    Exit Meeting Summary
modifications with respect to Generic Safety Issue 191. This temporary instruction is  
    On April 25, 2008, the health physics inspector presented the occupational radiation
closed.  
    safety inspection results to Mr. T. Herrmann and other members of his staff who
    acknowledged the findings. The inspector confirmed that proprietary information was
Documents reviewed by the inspectors are listed in the attachment.
    not provided or examined during the inspection.
    On June 18, 2008, the Temporary Instruction 2515/166 inspector presented the
    b. Findings  
    inspection results to Mr. S. Maglio and other members of his staff who acknowledged the
No findings of significance were identified.  
    findings. The inspector confirmed that proprietary information provided or examined
    during the inspection had been returned.
4OA6 Management Meetings  
    On June 24, 2008, the resident inspectors presented the inspection results to
    Mr. C. Naslund, Senior Vice President and Chief Nuclear Officer, and other members of
Exit Meeting Summary  
    the licensee staff. The licensee acknowledged the issues presented. The inspectors
On April 25, 2008, the health physics inspector presented the occupational radiation  
    understood and acknowledged that proprietary information reviewed would not be
safety inspection results to Mr. T. Herrmann and other members of his staff who  
    retained following report issuance.
acknowledged the findings. The inspector confirmed that proprietary information was  
4OA7 Licensee-Identified Violations
not provided or examined during the inspection.  
    The following violations of very low safety significance (Green) were identified by the
    licensee and were violations of NRC requirements which meet the criteria of Section VI
On June 18, 2008, the Temporary Instruction 2515/166 inspector presented the  
    of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.
inspection results to Mr. S. Maglio and other members of his staff who acknowledged the  
        *       10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part,
findings. The inspector confirmed that proprietary information provided or examined  
                that applicable regulatory requirements and the design basis are correctly
during the inspection had been returned.  
                translated into specifications, drawings, procedures, and instructions.
                Contrary to the above, on March 5, 2008, the licensee identified that a 4-foot
On June 24, 2008, the resident inspectors presented the inspection results to  
                section of suction piping within containment spray system, Train A was
Mr. C. Naslund, Senior Vice President and Chief Nuclear Officer, and other members of  
                approximately 50 percent voided. Voiding within the containment spray
the licensee staff. The licensee acknowledged the issues presented. The inspectors  
                system was due to a design deficiency that did not allow for a proper fill and
understood and acknowledged that proprietary information reviewed would not be  
                vent of the system. This was entered in the licensees corrective action
retained following report issuance.  
                program as CAR 200803462. This finding is greater than minor because it is
                similar to the Example 3j in Manual Chapter 0612, Appendix E, "Examples of
4OA7 Licensee-Identified Violations  
                                          - 39 -                                    Enclosure 2
The following violations of very low safety significance (Green) were identified by the  
licensee and were violations of NRC requirements which meet the criteria of Section VI  
of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.  
*  
10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part,  
that applicable regulatory requirements and the design basis are correctly  
translated into specifications, drawings, procedures, and instructions.
Contrary to the above, on March 5, 2008, the licensee identified that a 4-foot  
section of suction piping within containment spray system, Train A was  
approximately 50 percent voided. Voiding within the containment spray  
system was due to a design deficiency that did not allow for a proper fill and  
vent of the system. This was entered in the licensees corrective action  
program as CAR 200803462. This finding is greater than minor because it is  
similar to the Example 3j in Manual Chapter 0612, Appendix E, "Examples of  


  Minor Issues," in that the presence of air within the containment spray system
  suction header resulted in a condition where there was reasonable doubt on
  the operability of the system. This finding is of very low safety significance
- 40 -
  because it was a design or qualification deficiency confirmed not to result in
Enclosure 2
  loss of operability.
Minor Issues," in that the presence of air within the containment spray system  
* 10 CFR Part 50, Appendix B, Criterion III, requires measures be established
suction header resulted in a condition where there was reasonable doubt on  
  to assure that applicable regulatory requirements and design basis be
the operability of the system. This finding is of very low safety significance  
  correctly translated into specifications, drawings, procedures, and
because it was a design or qualification deficiency confirmed not to result in  
  instructions. Technical Specifications 3.5.2 and 3.6.6 require that residual
loss of operability.  
  heat removal and containment spray system components remain operable.
*  
  Contrary to this, measures were not adequate to assure installed center tube
10 CFR Part 50, Appendix B, Criterion III, requires measures be established  
  diameters for the containment recirculation sump modification were correctly
to assure that applicable regulatory requirements and design basis be  
  accounted for by an accurate net positive suction head calculation.
correctly translated into specifications, drawings, procedures, and  
  The vendor supplying AmerenUE the containment recirculation sump strainer
instructions. Technical Specifications 3.5.2 and 3.6.6 require that residual  
  identified that associated Vendor Calculation TDI-6002-05 for clean strainer
heat removal and containment spray system components remain operable.
  head loss did not account for the installed orifices located in the strainer
Contrary to this, measures were not adequate to assure installed center tube  
  support plate. The size of the orifice beneath each strainer was smaller than
diameters for the containment recirculation sump modification were correctly  
  assumed in head loss calculations and was not large enough to prevent head
accounted for by an accurate net positive suction head calculation.  
  loss in excess of the net positive suction head required as defined in the
The vendor supplying AmerenUE the containment recirculation sump strainer  
  purchase specification supplied to the strainer vendor. The additional head
identified that associated Vendor Calculation TDI-6002-05 for clean strainer  
  loss due to the calculation translation error was 2.28 feet. This resulted in
head loss did not account for the installed orifices located in the strainer  
  required net positive suction head being less than available. AmerenUE
support plate. The size of the orifice beneath each strainer was smaller than  
  performed three separate operability determination reviews to demonstrate
assumed in head loss calculations and was not large enough to prevent head  
  that the head loss margin could be recovered. The initial operability
loss in excess of the net positive suction head required as defined in the  
  determination on January 22, 2008, addressed the smaller support plate
purchase specification supplied to the strainer vendor. The additional head  
  orifice holes by using a separate vendor's flow analysis of the residual heat
loss due to the calculation translation error was 2.28 feet. This resulted in  
  removal and containment spray piping systems to demonstrate lower flow
required net positive suction head being less than available. AmerenUE  
  and head losses than described in the FSAR. This operability determination
performed three separate operability determination reviews to demonstrate  
  resulted in the limiting case flow path being the hot leg recirculation flow path.
that the head loss margin could be recovered. The initial operability  
  Another operability review on March 12, 2008, addressed a nonconservative
determination on January 22, 2008, addressed the smaller support plate  
  temperature correction through the orifices. Subsequent to this, the licensee
orifice holes by using a separate vendor's flow analysis of the residual heat  
  informed the NRC that the additional nonconservative inputs were used in
removal and containment spray piping systems to demonstrate lower flow  
  the January 22, 2008, flow re-analysis of the residual heat removal system.
and head losses than described in the FSAR. This operability determination  
  Additional analyses were performed to regain margin. This resulted in the
resulted in the limiting case flow path being the hot leg recirculation flow path.
  limiting case flow path changing from hot leg recirculation to cold leg
Another operability review on March 12, 2008, addressed a nonconservative  
  recirculation.
temperature correction through the orifices. Subsequent to this, the licensee  
  This example of inadequate design control was captured in the licensees
informed the NRC that the additional nonconservative inputs were used in  
  corrective action program as CARs 200800461 and 200802618. These
the January 22, 2008, flow re-analysis of the residual heat removal system.
  corrective action reviews documented three causes related to the following
Additional analyses were performed to regain margin. This resulted in the  
  design error:
limiting case flow path changing from hot leg recirculation to cold leg  
    *     Time pressure to address Generic Letter 2004-02
recirculation.  
    *     A complex design with parallel sequencing of different parts of the
          design
This example of inadequate design control was captured in the licensees  
    *     AmerenUE not independently verifying the vendor's design due to
corrective action program as CARs 200800461 and 200802618. These  
          perceived expertise and an approved 10 CFR Part 50, Appendix B,
corrective action reviews documented three causes related to the following  
                            - 40 -                                      Enclosure 2
design error:  
*  
Time pressure to address Generic Letter 2004-02
*  
A complex design with parallel sequencing of different parts of the  
design  
*  
AmerenUE not independently verifying the vendor's design due to  
perceived expertise and an approved 10 CFR Part 50, Appendix B,  


                    Quality Assurance program. AmerenUE did not perform a review of
                    the design, nor did they contract to have a third party engineering
                    review of the design.
- 41 -
            This finding is greater than minor because it is similar to the Example 3j in
Enclosure 2
            Manual Chapter 0612, Appendix E, Examples of Minor Issues, in that the
Quality Assurance program. AmerenUE did not perform a review of  
            contractor error translating the design to the calculations resulted in a
the design, nor did they contract to have a third party engineering  
            condition where there was reasonable doubt on the operability of the ECCS.
review of the design.  
            This finding is of very low safety significance because it was a design or
This finding is greater than minor because it is similar to the Example 3j in  
            qualification deficiency confirmed not to result in loss of operability. This
Manual Chapter 0612, Appendix E, Examples of Minor Issues, in that the  
            licensee-identified violation closes out Unresolved
contractor error translating the design to the calculations resulted in a  
            Item 05000483/2008002-01.
condition where there was reasonable doubt on the operability of the ECCS.
ATTACHMENT: SUPPLEMENTAL INFORMATION
This finding is of very low safety significance because it was a design or  
                                      - 41 -                                      Enclosure 2
qualification deficiency confirmed not to result in loss of operability. This  
licensee-identified violation closes out Unresolved  
Item 05000483/2008002-01.  
ATTACHMENT: SUPPLEMENTAL INFORMATION


                              SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Licensee Personnel
A-1
B. Barton, Training Manager
Attachment
M. Brandes, Consulting Engineer, Nuclear Engineering - Major Modifications
SUPPLEMENTAL INFORMATION  
K. Bruckerhoff, Supervisor, Emergency Preparedness
KEY POINTS OF CONTACT
F. Diya, Plant Director
Licensee Personnel  
T. Elwood, Supervising Engineer, Licensing
B. Barton, Training Manager  
R. Farnam, Manager, Radiation Protection
M. Brandes, Consulting Engineer, Nuclear Engineering - Major Modifications  
K. Gilliam, Supervisor, Radiation Protection
K. Bruckerhoff, Supervisor, Emergency Preparedness  
L. Graessle, Manager, Regulatory Affairs
F. Diya, Plant Director  
A. Heflin, Vice President, Nuclear
T. Elwood, Supervising Engineer, Licensing  
T. Herrmann, Vice President, Engineering
R. Farnam, Manager, Radiation Protection  
B. Holderness, Senior Health Physicist, Environmental Services
K. Gilliam, Supervisor, Radiation Protection  
L. Kanuckel, Manager, Quality Assurance
L. Graessle, Manager, Regulatory Affairs  
D. Lantz, Superintendent of Operations Training
A. Heflin, Vice President, Nuclear  
S. Maglio, Assistant Manager, Regulatory Affairs
T. Herrmann, Vice President, Engineering  
R. Myatt, Supervisor, Engineering
B. Holderness, Senior Health Physicist, Environmental Services  
K. Mills, Manager, Engineering
L. Kanuckel, Manager, Quality Assurance  
D. Neterer, Manager, Nuclear Operations
D. Lantz, Superintendent of Operations Training  
T. Parker, Trainer, Radiation Protection
S. Maglio, Assistant Manager, Regulatory Affairs  
S. Petzel, Engineer, Regulatory Affairs
R. Myatt, Supervisor, Engineering  
J. Pitts, Component Engineer
K. Mills, Manager, Engineering  
V. Rider, ALARA Specialist, Radiation Protection
D. Neterer, Manager, Nuclear Operations  
                            LIST OF ITEMS OPENED AND CLOSED
T. Parker, Trainer, Radiation Protection  
Opened
S. Petzel, Engineer, Regulatory Affairs  
05000483/2008003-05         VIO     Failure to Prevent Recurrence of Voids in ECCS Cold Leg
J. Pitts, Component Engineer  
                                    Recirculation Piping (Section 4OA2)
V. Rider, ALARA Specialist, Radiation Protection  
Opened and Closed
05000483/2008003-01         NCV     Failure to Ensure the Suitability of the Design of the
LIST OF ITEMS OPENED AND CLOSED  
                                    Containment Air Cooler Control Circuitry (Section 1R15)
Opened  
05000483/2008003-02         NCV     Inadequate Surveillance Procedure Resulted in an
05000483/2008003-05  
                                    Inoperable ECCS (Section 1R15)
VIO  
05000483/2008003-03         NCV     Failure to Correct a Condition Adverse to Quality for
Failure to Prevent Recurrence of Voids in ECCS Cold Leg  
                                    Diesel Generator Jacket Water O-Rings (Section 1R19)
Recirculation Piping (Section 4OA2)  
05000483/2008003-04         NCV     Failure to Maintain an Adequate Technical Specification
                                    Bases Change Process (Section 1R22)
Opened and Closed  
Closed
05000483/2008003-01  
05000483/2008001-00         LER     Containment Cooler Inoperability (Section 4OA3)
NCV  
05000483/2008002-01         URI     Containment Recirculation Sump Operability
Failure to Ensure the Suitability of the Design of the  
                                    (Section 4OA7)
Containment Air Cooler Control Circuitry (Section 1R15)  
                                            A-1                                Attachment
05000483/2008003-02  
NCV  
Inadequate Surveillance Procedure Resulted in an  
Inoperable ECCS (Section 1R15)  
05000483/2008003-03  
NCV  
Failure to Correct a Condition Adverse to Quality for  
Diesel Generator Jacket Water O-Rings (Section 1R19)  
05000483/2008003-04  
NCV  
Failure to Maintain an Adequate Technical Specification  
Bases Change Process (Section 1R22)  
Closed  
05000483/2008001-00  
LER  
Containment Cooler Inoperability (Section 4OA3)  
05000483/2008002-01  
URI  
Containment Recirculation Sump Operability  
(Section 4OA7)  


                                  LIST OF DOCUMENTS REVIEWED
The following is a partial list of documents reviewed during the inspection. Inclusion on this list
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that
A-2
selected sections or portions of the documents were evaluated as part of the overall inspection
Attachment
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
LIST OF DOCUMENTS REVIEWED  
any part of it, unless this is stated in the body of the inspection report.
The following is a partial list of documents reviewed during the inspection. Inclusion on this list  
Section 1R01: Adverse Weather Protection
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that  
Procedures
selected sections or portions of the documents were evaluated as part of the overall inspection  
ODP-ZZ-00001, Operations Department - Code of Conduct, Revision 41
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
OSP-NB-00001, Class 1E Electrical Source Verification, Revision 032
any part of it, unless this is stated in the body of the inspection report.  
OTN-NB-0001A, 4.16 KV Vital (Class 1E) Electrical System - A Train, Revision 12
OTN-NB-0001A, Addendum 5, NB01 Loss of Power Recovery, Revision 0
Section 1R01: Adverse Weather Protection  
OTO-ZZ-00012, Severe Weather, Revision 10
Procedures  
Miscellaneous
ODP-ZZ-00001, Operations Department - Code of Conduct, Revision 41  
AmerenUE Response to Generic Letter 2006-02, Grid Reliability and the Impact on Plant Risk
OSP-NB-00001, Class 1E Electrical Source Verification, Revision 032  
and the Operability of Offsite Power
OTN-NB-0001A, 4.16 KV Vital (Class 1E) Electrical System - A Train, Revision 12  
Training Lesson Plan LP-01, Systems, Switchyard MD
OTN-NB-0001A, Addendum 5, NB01 Loss of Power Recovery, Revision 0  
Training Lesson Plan T61.0110.6, Systems, Switchyard MD
OTO-ZZ-00012, Severe Weather, Revision 10  
Section 1RO4: Equipment Alignment
Miscellaneous  
Drawings
AmerenUE Response to Generic Letter 2006-02, Grid Reliability and the Impact on Plant Risk  
M-22AL01A, Piping and Instrumentation Diagram Auxiliary Feedwater System, Revision 33
and the Operability of Offsite Power  
M-22BB01(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 30
Training Lesson Plan LP-01, Systems, Switchyard MD  
M-22BB03A(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9
Training Lesson Plan T61.0110.6, Systems, Switchyard MD  
M-22BB03B(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9
Section 1RO4: Equipment Alignment  
M-22BB03C(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7
Drawings  
M-22BB03D(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7
M-22AL01A, Piping and Instrumentation Diagram Auxiliary Feedwater System, Revision 33  
M-22BG01(Q), Piping and Instrumentation Diagram Chemical and Volume Control System,
M-22BB01(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 30  
Revision 28
M-22BB03A(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9  
M-22BG03(Q), Piping and Instrumentation Diagram Chemical and Volume Control System,
M-22BB03B(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9  
Revision 52
M-22BB03C(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7  
                                              A-2                            Attachment
M-22BB03D(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7  
M-22BG01(Q), Piping and Instrumentation Diagram Chemical and Volume Control System,  
Revision 28  
M-22BG03(Q), Piping and Instrumentation Diagram Chemical and Volume Control System,  
Revision 52  


M-22EJ01(Q), Piping and Instrumentation Diagram Residual Heat Removal System,
Revision 57
M-22EM01(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System,
A-3
Revision 33
Attachment
M-22EM02(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System,
M-22EJ01(Q), Piping and Instrumentation Diagram Residual Heat Removal System,  
Revision 19
Revision 57  
M-22EP01(Q), Piping and Instrumentation Diagram Accumulator and Safety Injection,
M-22EM01(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System,  
Revision 16
Revision 33  
Section 1RO5: Fire Protection
M-22EM02(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System,  
Miscellaneous
Revision 19  
Drill Number 08-01, Evaluate Fire Brigade Response in a Radiation Area, dated March 27, 2008
M-22EP01(Q), Piping and Instrumentation Diagram Accumulator and Safety Injection,  
Drill Critique Number 08-01, Unannounced Fire Drill, dated March 27, 2008
Revision 16  
FSAR, Appendix 9.5B, Fire Hazard Analysis
Section 1RO5: Fire Protection
Section 1R11: Licensed Operator Requalification Program
Miscellaneous  
Procedures
Drill Number 08-01, Evaluate Fire Brigade Response in a Radiation Area, dated March 27, 2008  
OTA-RK-00024, Addendum 98D, Seismic Event, Revision 0
Drill Critique Number 08-01, Unannounced Fire Drill, dated March 27, 2008  
OTO-SG-0001, Design Basis Earthquake, Revision 13
FSAR, Appendix 9.5B, Fire Hazard Analysis  
Section 1R12: Maintenance Effectiveness
Section 1R11: Licensed Operator Requalification Program
Procedures
Procedures  
EDP-ZZ-01128, Maintenance Rule Program, Revision 8
OTA-RK-00024, Addendum 98D, Seismic Event, Revision 0  
NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear
OTO-SG-0001, Design Basis Earthquake, Revision 13  
Power Plants, Revision 3
Callaway Action Requests
Section 1R12: Maintenance Effectiveness  
200706892                         200801644                       200802854
Procedures  
Section 1R13: Maintenance Risk Assessment and Emergent Work Controls
EDP-ZZ-01128, Maintenance Rule Program, Revision 8  
Procedure
NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear  
EDP-ZZ-01129, Callaway Plant Risk Assessment, Revision 14
Power Plants, Revision 3  
Section 1R15: Operability Evaluations
Calculations
Callaway Action Requests  
ARC-687, AFT Fathom 6.0 Output, Revision 0
200706892  
                                          A-3                              Attachment
200801644  
200802854  
Section 1R13: Maintenance Risk Assessment and Emergent Work Controls  
Procedure  
EDP-ZZ-01129, Callaway Plant Risk Assessment, Revision 14  
Section 1R15: Operability Evaluations  
Calculations  
ARC-687, AFT Fathom 6.0 Output, Revision 0  


M-FL-18, LOCA and MSLB Containment Flood Level, Revision 1
WES-009-CALC-001, Wolf Creek/Callaway Post-LOCA Containment Water Level Calculation,
Revision 0
A-4
Callaway Action Requests
Attachment
200800461                       200802352                         200803462
200802231                      200802365                         200804000
M-FL-18, LOCA and MSLB Containment Flood Level, Revision 1  
200802264                      200802618
200802348                      200803252
WES-009-CALC-001, Wolf Creek/Callaway Post-LOCA Containment Water Level Calculation,  
Drawings
Revision 0  
E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19
Callaway Action Requests  
E-018-00273, Motor Control Center Ambient Compensated Overload Relay Heater Chart,
200800461  
Revision 3
200802231
E-018-00847, Overload Relay Time Current Characteristics, Revision 4
200802264
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11
200802348
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12
200802352  
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5
200802365  
E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12
200802618  
E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13
200803252  
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,
200803462
Revision 2
200804000
J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,
Revision 1
Drawings  
M-018-00943, 206 Ez-Flo Expansion Joint, Revision 0
E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19  
M-22BG03, Piping and Instrumentation Diagram Chemical and Volume Control System,
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19  
Revision 52
E-018-00273, Motor Control Center Ambient Compensated Overload Relay Heater Chart,  
M-22EM01, Piping and Instrumentation Diagram High Pressure Coolant Injection System,
Revision 3  
Revision 33
E-018-00847, Overload Relay Time Current Characteristics, Revision 4  
M-23BG02, Piping Isometric CVCS-Max Charging Flow A and B Train Auxiliary Building,
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11  
Revision 12
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12  
                                        A-4                              Attachment
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5  
E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12  
E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13  
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,  
Revision 2  
J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,  
Revision 1  
M-018-00943, 206 Ez-Flo Expansion Joint, Revision 0  
M-22BG03, Piping and Instrumentation Diagram Chemical and Volume Control System,  
Revision 52  
M-22EM01, Piping and Instrumentation Diagram High Pressure Coolant Injection System,  
Revision 33  
M-23BG02, Piping Isometric CVCS-Max Charging Flow A and B Train Auxiliary Building,  
Revision 12  


Procedures
ECA-0.1, Loss of All AC Power Recover Without Safety Injection Required, Revision 8
ECA-1.1, Loss of Emergency Coolant Recirculation, Revision 8
A-5
EDP-ZZ-04021, Review of Supplier Documents, Revision 5
Attachment
ISF-SE-00N32, FCTNAL-NUC INSTM SOURCE RANGE N32, Revision 20
Procedures
OSP-EJ-PV04A, Train A RHR and RCS Check Valve Inservice Test -IPTE, Revision 0
ECA-0.1, Loss of All AC Power Recover Without Safety Injection Required, Revision 8  
OSP-EJ-PV04B, Train B RHR and RCS Check Valve Inservice Test -IPTE, Revision 1
ECA-1.1, Loss of Emergency Coolant Recirculation, Revision 8  
OTN-EN-00001, Containment Spray System, Revision 14
EDP-ZZ-04021, Review of Supplier Documents, Revision 5  
OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 1
ISF-SE-00N32, FCTNAL-NUC INSTM SOURCE RANGE N32, Revision 20  
Miscellaneous
OSP-EJ-PV04A, Train A RHR and RCS Check Valve Inservice Test -IPTE, Revision 0  
Job 07513275 for SEN0032
OSP-EJ-PV04B, Train B RHR and RCS Check Valve Inservice Test -IPTE, Revision 1  
Letter ULNRC-04884, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co.,
OTN-EN-00001, Containment Spray System, Revision 14  
Facility Operating License NPF-30, Response to NRC Bulletin 2003-01, Potential Impact of
OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 1  
Debris Blockage on Emergency Sump Recirculation at Pressurized Water Reactor, dated
Miscellaneous  
August 3, 2003
Job 07513275 for SEN0032  
Letter ULNRC-05481, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co.,
Letter ULNRC-04884, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co.,  
Facility Operating License NPF-30 Response to Request for Additional Information, Response
Facility Operating License NPF-30, Response to NRC Bulletin 2003-01, Potential Impact of  
to NRC Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency
Debris Blockage on Emergency Sump Recirculation at Pressurized Water Reactor, dated  
Recirculation During Design Basis Accidents at Pressurized Water Reactors, dated
August 3, 2003  
February 29, 2008
Letter ULNRC-05481, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co.,  
Garlock Sealing Technologies Customer Requested Test 206 Ez-Flo Expansion Test, dated
Facility Operating License NPF-30 Response to Request for Additional Information, Response  
November 15, 2006
to NRC Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency  
Section 1R18: Plant Modifications
Recirculation During Design Basis Accidents at Pressurized Water Reactors, dated  
Procedure
February 29, 2008  
OTN-KA-00001, Compressed Air System, Revision 18
Garlock Sealing Technologies Customer Requested Test 206 Ez-Flo Expansion Test, dated  
Drawings
November 15, 2006  
E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19
Section 1R18: Plant Modifications  
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19
Procedure  
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11
OTN-KA-00001, Compressed Air System, Revision 18  
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12
Drawings  
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5
E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19  
                                          A-5                              Attachment
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19  
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11  
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12  
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5  


E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12
E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,
A-6
Revision 2
Attachment
J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,
E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12  
Revision 1
E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13  
M-22KA01, Piping and Instrumentation Diagram Compressed Air System, Revision 016A
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,  
M-22KA06, Piping and Instrumentation Diagram Instrument Air Filter/Dryer Turbine, Building,
Revision 2  
Revision 30A
J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,  
Miscellaneous
Revision 1  
Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change,
M-22KA01, Piping and Instrumentation Diagram Compressed Air System, Revision 016A  
Revision 0
M-22KA06, Piping and Instrumentation Diagram Instrument Air Filter/Dryer Turbine, Building,  
Job
Revision 30A  
08003842
Miscellaneous  
Section 1R19: Postmaintenance Testing
Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change,  
Procedures
Revision 0  
APA-ZZ-00330, Preventative Maintenance Program, Revision 29
Job  
OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 14
08003842  
Callaway Action Requests
Section 1R19: Postmaintenance Testing  
200801270                       200802810                         200804164
Procedures  
Jobs
APA-ZZ-00330, Preventative Maintenance Program, Revision 29  
06524419                       08001080                           08002765
07006905                        08002676                          08003910
OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 14  
Drawings
E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19
Callaway Action Requests  
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19
200801270  
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5
        200802810  
                                        A-6                                Attachment
    200804164  
Jobs  
06524419  
07006905
08001080  
08002676
08002765  
08003910  
Drawings  
E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19  
E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19  
E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12  
E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11  
E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5  


E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12
E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,
A-7
Revision 2
Attachment
J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,
E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12  
Revision 1
E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13  
Miscellaneous
J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,  
Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change,
Revision 2  
Revision 0
J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,  
Simple Surveillance SP08-017, Containment Cooler Control Circuit Changes, dated April 16,
Revision 1  
2008
Miscellaneous  
Section 1R22: Surveillance Testing
Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change,  
Procedures
Revision 0  
EDP-ZZ-04107, HVAC Pressure Boundary Control, Revision 19
FDP-ZZ-00101, Technical Specification Bases Control Program, Revision 6
Simple Surveillance SP08-017, Containment Cooler Control Circuit Changes, dated April 16,  
OSP-GL-0001A, Auxiliary Building Train A Negative Pressure Test, Revision 6
2008  
OSP-EJ-P001A, RHR Train A inservice Test - Group A, Revision 44
OSP-EJ-V001B, Residual heat removal Train B valve inservice test, Revision 21
Section 1R22: Surveillance Testing  
OSP-NE-0001B, Standby Diesel Generator B Periodic Tests, Revision 29
Procedures  
OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting,
EDP-ZZ-04107, HVAC Pressure Boundary Control, Revision 19  
Revision 30
FDP-ZZ-00101, Technical Specification Bases Control Program, Revision 6  
Section 2OS1: Access Controls to Radiologically Significant Areas and
OSP-GL-0001A, Auxiliary Building Train A Negative Pressure Test, Revision 6  
Section 2OS2: ALARA Planning and Controls
OSP-EJ-P001A, RHR Train A inservice Test - Group A, Revision 44
Callaway Action Requests
OSP-EJ-V001B, Residual heat removal Train B valve inservice test, Revision 21  
200703726                       200800631                         200800991
OSP-NE-0001B, Standby Diesel Generator B Periodic Tests, Revision 29  
200703956                      200800632                         200801135
OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting,  
200710799                      200800633                         200801390
Revision 30  
200711181                      200800727                         200801430
Section 2OS1: Access Controls to Radiologically Significant Areas and  
200711846                      200800838                         200802003
Section 2OS2: ALARA Planning and Controls  
200711875                      200800887                         200802280
Callaway Action Requests  
200711880                      200800888                         200803141
200703726  
200711881                      200800891                         200803204
200703956
200711883                      200800957                         200803205
200710799
200800219                      200800973                         200803208
200711181
200800438                      200800988
200711846
                                        A-7                              Attachment
200711875
200711880
200711881
200711883
200800219
200800438
200800631  
200800632  
200800633  
200800727  
200800838  
200800887  
200800888  
200800891  
200800957  
200800973  
200800988  
200800991
200801135
200801390
200801430
200802003
200802280
200803141
200803204
200803205
200803208


Audits and Self-Assessments
Quality Assurance Audit of Radiation Protection AP08-001, February 28, 2008
Quality Assurance Supplemental Audit of Radwaste AP07-012, October 30, 2007
A-8
Simple Self-assessment Report SA07-RP-S06, January 9, 2008
Attachment
Radiation Work Permits/ALARA Reviews
RWP 803321RESIN, Transfer Spent Resin from Primary Tank to Liner
Audits and Self-Assessments  
ALARA Package 07-03120, Reinstall Bladders into the Recycle Hold Up Tanks
Quality Assurance Audit of Radiation Protection AP08-001, February 28, 2008  
Other/Meetings/Training/Work Review
Quality Assurance Supplemental Audit of Radwaste AP07-012, October 30, 2007  
ALARA Simulator Class
Simple Self-assessment Report SA07-RP-S06, January 9, 2008  
Callaway Plant Long Range Dose and Source Term Reduction Plan, Revision 2
Hot Spot and Shielding Log
Radiation Work Permits/ALARA Reviews  
Job 08000834 Transfer Spent Resin from Primary Tank to Liner
RWP 803321RESIN, Transfer Spent Resin from Primary Tank to Liner  
Plant ALARA Review Committee Meeting
ALARA Package 07-03120, Reinstall Bladders into the Recycle Hold Up Tanks  
Procedures
APA-ZZ-00405, Special Nuclear Material Control and Accounting, Revision 20
Other/Meetings/Training/Work Review  
APA-ZZ-01000, Callaway Plant Radiation Protection Program, Revision 26
ALARA Simulator Class  
APA-ZZ-01001, Callaway Plant ALARA Program, Revision 11
Callaway Plant Long Range Dose and Source Term Reduction Plan, Revision 2  
APA-ZZ-01106, Lock and Key Control, Revision 16
Hot Spot and Shielding Log  
HDP-ZZ-01100, ALARA Planning and Review, Revision 6
Job 08000834 Transfer Spent Resin from Primary Tank to Liner  
HDP-ZZ-01200, Radiation Work Permits, Revision 9
Plant ALARA Review Committee Meeting  
HTP-ZZ-01203, Radiological Area Access Control, Revision 36
HTP-ZZ-06001, High Radiation/Very High Radiation Area Access, Revision 31
Procedures  
HTP-ZZ-06028, Radiological Controls for Pools that Contain or Store Spent Fuel, Revision 5
APA-ZZ-00405, Special Nuclear Material Control and Accounting, Revision 20  
RTS-HC-00350, Primary Spent Resin Storage Tank Transfer to Bulk Waste Disposal Station,
APA-ZZ-01000, Callaway Plant Radiation Protection Program, Revision 26  
Revision 3
APA-ZZ-01001, Callaway Plant ALARA Program, Revision 11  
Section 4OA1: Performance Indicator Verification
APA-ZZ-01106, Lock and Key Control, Revision 16  
Procedure
HDP-ZZ-01100, ALARA Planning and Review, Revision 6  
NOD-QP-40, NRC Performance Indicator Program, Revision 2
HDP-ZZ-01200, Radiation Work Permits, Revision 9  
Miscellaneous
HTP-ZZ-01203, Radiological Area Access Control, Revision 36  
Various Callaway Control Room Logs, dated March 2007 through March 2008
HTP-ZZ-06001, High Radiation/Very High Radiation Area Access, Revision 31  
Callaway Integrated Inspection Report 05000483/2007002
HTP-ZZ-06028, Radiological Controls for Pools that Contain or Store Spent Fuel, Revision 5  
                                          A-8                              Attachment
RTS-HC-00350, Primary Spent Resin Storage Tank Transfer to Bulk Waste Disposal Station,  
Revision 3  
Section 4OA1: Performance Indicator Verification  
Procedure  
NOD-QP-40, NRC Performance Indicator Program, Revision 2  
Miscellaneous  
Various Callaway Control Room Logs, dated March 2007 through March 2008  
Callaway Integrated Inspection Report 05000483/2007002  


Callaway Integrated Inspection Report 05000483/2007003
Callaway Integrated Inspection Report 05000483/2007004
Callaway Integrated Inspection Report 05000483/2008002
A-9
Section 4OA2: Identification and Resolution of Problems
Attachment
Inspection Findings
Callaway Integrated Inspection Report 05000483/2007003  
NCV 05000483/2005002-01
Callaway Integrated Inspection Report 05000483/2007004  
NCV 05000483/2006012-04
Callaway Integrated Inspection Report 05000483/2008002  
Callaway Action Requests
200501192                       200800355                         200804000
Section 4OA2: Identification and Resolution of Problems  
200709819                        200800522                        200804164
Inspection Findings  
200711496                        200801270                        200805049
NCV 05000483/2005002-01  
200800246                        200801529                        200805122
NCV 05000483/2006012-04  
200800298                        200801830                        200808956
Generic Communications
Callaway Action Requests  
NRC Information Notice 2006-21, OE Regarding Entrainment of Air into Emergency Core
200501192  
Cooling and Containment Spray Systems, September 21, 2006
200709819
Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat
200711496
Removal , and Containment Spray Systems, January 11, 2009
200800246
Procedures
200800298
OTN-EM0001, Safety Injection System, Revision 27
200800355  
OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting,
200800522
Revision 27
200801270
Section 4OA5: Other
200801529
Procedures
200801830
APA-ZZ-01004, Radiological Work Standards, Revision 9
200804000  
HDP-ZZ-06100, Reactor Building Access, Revision 7
200804164  
MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22
200805049  
OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6
200805122  
OSP-SA-00004, Visual Inspection of Containment for Loose Debris, Revision 19
200808956  
OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices, Revision 2
Calculations
Generic Communications  
Calculation BG-75, Impact of MP 06-0003, Replacement Containment Recirculation Sump
NRC Information Notice 2006-21, OE Regarding Entrainment of Air into Emergency Core  
Strainers, and MP 06-0027, TSP Basket Relocation, Revision 0
Cooling and Containment Spray Systems, September 21, 2006  
Calculation BN-21, Impact of MP 06-0003, Replacement Containment Recirculation Sump
Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat  
Strainer on BN21, Revision 0
Removal , and Containment Spray Systems, January 11, 2009  
                                        A-9                              Attachment
Procedures  
OTN-EM0001, Safety Injection System, Revision 27  
OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting,  
Revision 27  
Section 4OA5: Other  
Procedures  
APA-ZZ-01004, Radiological Work Standards, Revision 9  
HDP-ZZ-06100, Reactor Building Access, Revision 7  
MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22  
OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6  
OSP-SA-00004, Visual Inspection of Containment for Loose Debris, Revision 19  
OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices, Revision 2  
Calculations  
Calculation BG-75, Impact of MP 06-0003, Replacement Containment Recirculation Sump  
Strainers, and MP 06-0027, TSP Basket Relocation, Revision 0  
Calculation BN-21, Impact of MP 06-0003, Replacement Containment Recirculation Sump  
Strainer on BN21, Revision 0  


Calculation BN-22, Impact of MP 06-0003, Replacement Containment Recirculation Sump
Strainer on BN22, Revision 0
Calculation EJ-29, NPSH Margin for RHR Pumps at Transition to Recirculation When NPSH
A-10
Margin is at its Minimum Value, Revision 1
Attachment
Calculation TDI-6002-05/TDI-6003-05, Clean Head Loss - Wolf Creek/Callaway, Revision 0
Calculation BN-22, Impact of MP 06-0003, Replacement Containment Recirculation Sump  
Callaway Action Request
Strainer on BN22, Revision 0  
200800461, Prompt Operability Determination for Containment Spray and Residual Heat
Calculation EJ-29, NPSH Margin for RHR Pumps at Transition to Recirculation When NPSH  
Removal Systems, Revision 0
Margin is at its Minimum Value, Revision 1  
Miscellaneous
Calculation TDI-6002-05/TDI-6003-05, Clean Head Loss - Wolf Creek/Callaway, Revision 0  
Ameren/UE comments on ECI-PCI-WC-CAL-6002-6003-1001
Callaway Action Request  
Callaway Plant Containment Building Latent Debris Assessment Report Refuel 14 Fall 2005
200800461, Prompt Operability Determination for Containment Spray and Residual Heat  
EC-PCI-WC/CAL-6002/6003-1001, AES Calculation No. PCI-5304-S01 Structural Evaluation of
Removal Systems, Revision 0  
the Containment Sump Strainers, Revision 1
Miscellaneous  
MP 06-0003-EC-PCI-WC-CAL-6002-6003- (000) AES Document No. PCI-5304-S01 Structural
Ameren/UE comments on ECI-PCI-WC-CAL-6002-6003-1001  
Evaluation of the Containment Sump Strainers, Revision 1
Callaway Plant Containment Building Latent Debris Assessment Report Refuel 14 Fall 2005  
NUREG/CR-6914, Vol. 4, Integrated Chemical Effects Test, Revision 0
EC-PCI-WC/CAL-6002/6003-1001, AES Calculation No. PCI-5304-S01 Structural Evaluation of  
SWE07848, Containment Coating Condition Assessment
the Containment Sump Strainers, Revision 1  
TDI-6002/TDI-6003, Sure-Flow Suction Strainer Qualification Report and Addendums, Wolf
MP 06-0003-EC-PCI-WC-CAL-6002-6003- (000) AES Document No. PCI-5304-S01 Structural  
Creek/Callaway
Evaluation of the Containment Sump Strainers, Revision 1  
ULNRC-05124, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
NUREG/CR-6914, Vol. 4, Integrated Chemical Effects Test, Revision 0  
Operating License NPF-30 Response To Generic Letter 2004-02, Potential Impact of Debris
SWE07848, Containment Coating Condition Assessment  
Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water
TDI-6002/TDI-6003, Sure-Flow Suction Strainer Qualification Report and Addendums, Wolf  
Reactors.
Creek/Callaway  
ULNRC-05194, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
ULNRC-05124, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility  
Operating License NPF-30 September 1, 2005, Response To Generic Letter 2004-02, Potential
Operating License NPF-30 Response To Generic Letter 2004-02, Potential Impact of Debris  
Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At
Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water  
Pressurized-Water Reactors.
Reactors.  
ULNRC-05295, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
ULNRC-05194, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility  
Operating License NPF-30 Response Update To Generic Letter 2004-02, Potential Impact of
Operating License NPF-30 September 1, 2005, Response To Generic Letter 2004-02, Potential  
Debris Blockage On Emergency Recirculation During Design Basis Accidents At
Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At  
Pressurized-Water Reactors.
Pressurized-Water Reactors.  
ULNRC-05408, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
ULNRC-05295, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility  
Operating License NPF-30 Update For Response To Generic Letter 2004-02, Potential Impact
Operating License NPF-30 Response Update To Generic Letter 2004-02, Potential Impact of  
of Debris Blockage On Emergency Recirculation During Design Basis Accidents At
Debris Blockage On Emergency Recirculation During Design Basis Accidents At  
Pressurized-Water Reactors.
Pressurized-Water Reactors.  
                                          A-10                            Attachment
ULNRC-05408, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility  
Operating License NPF-30 Update For Response To Generic Letter 2004-02, Potential Impact  
of Debris Blockage On Emergency Recirculation During Design Basis Accidents At  
Pressurized-Water Reactors.  


ULNRC-05461, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
Operating License NPF-30 Request for Extension Of Completion Date For Corrective Actions
Associated with NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On
A-11
Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.
Attachment
ULNRC-05465, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility
ULNRC-05461, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility  
Operating License NPF-30 Supplement to Request for Extension of Corrective Actions
Operating License NPF-30 Request for Extension Of Completion Date For Corrective Actions  
Completion Date For NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On
Associated with NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On  
Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.
Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.  
WCAP-16568-P, Jet Impingement Testing to Determine the Zone of Influence (ZOI) for
ULNRC-05465, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility  
BAQualified/Acceptable Coatings (Proprietary)
Operating License NPF-30 Supplement to Request for Extension of Corrective Actions  
Wolf Creek/Callaway Comments on Calculation PCI-5304-S01, Structural Evaluation of the
Completion Date For NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On  
Containment Sump Strainers.
Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.  
Section 4OA7: Licensee-Identified Violations
WCAP-16568-P, Jet Impingement Testing to Determine the Zone of Influence (ZOI) for
Callaway Action Requests
BAQualified/Acceptable Coatings (Proprietary)  
200802618                         200803462                       200800461
Wolf Creek/Callaway Comments on Calculation PCI-5304-S01, Structural Evaluation of the  
Generic Communication
Containment Sump Strainers.  
Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation
Section 4OA7: Licensee-Identified Violations  
During Design Basis Accidents at Pressurized Water Reactors, dated September 13, 2004
Callaway Action Requests  
Calculation
200802618  
TDI-6002-05
200803462  
Correspondence
200800461  
Amendment 180 to Facility Operating License NPF-30 from Mr. J. Donohew, Senior Project
Manager, Office of Nuclear Reactor Regulation to Mr. C. Naslund, AmerenUE
Generic Communication  
Procedure
Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation  
APA-ZZ-00408, Professional Service Agreements and Nuclear Fuel Contracts, Revision 12
During Design Basis Accidents at Pressurized Water Reactors, dated September 13, 2004  
AmerenUE Callaway Plant Nuclear Plant Operating Quality Assurance Manual, Section 3,
Revision 25
Calculation  
Audits
TDI-6002-05  
Quality Assurance Audit of Design Control AP08-003
Independent Technical Review Report, SEGR 08-012, Temperature Correction Factor for
Correspondence  
Amendment 180 to Facility Operating License NPF-30 from Mr. J. Donohew, Senior Project  
Manager, Office of Nuclear Reactor Regulation to Mr. C. Naslund, AmerenUE  
Procedure  
APA-ZZ-00408, Professional Service Agreements and Nuclear Fuel Contracts, Revision 12  
AmerenUE Callaway Plant Nuclear Plant Operating Quality Assurance Manual, Section 3,  
Revision 25  
Audits  
Quality Assurance Audit of Design Control AP08-003  
Independent Technical Review Report, SEGR 08-012, Temperature Correction Factor for  
Strainer Stack Orifice Head Losses
Strainer Stack Orifice Head Losses
                                          A-11                            Attachment
}}
}}

Latest revision as of 15:44, 14 January 2025

IR 05000483-08-003, on 3/25 - 6/24/08, Callaway Plant, Operability Evaluations, Postmaintenance Testing, Surveillance Testing, and Identification and Resolution of Problems
ML082180851
Person / Time
Site: Callaway Ameren icon.png
Issue date: 08/05/2008
From: Vincent Gaddy
NRC/RGN-IV/DRP/RPB-B
To: Heflin A
Union Electric Co
References
EA-08-190 IR-08-003
Download: ML082180851 (58)


See also: IR 05000483/2008003

Text

August 5, 2008

EA-08-190

Mr. Adam C. Heflin, Senior Vice

President and Chief Nuclear Officer

Union Electric Company

P.O. Box 620

Fulton, MO 65251

SUBJECT: CALLAWAY PLANT - NRC INTEGRATED INSPECTION

REPORT AND NOTICE OF VIOLATION 05000483/2008003

Dear Mr. Heflin:

On June 24, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Callaway Plant. The enclosed report documents the inspection results, which

were discussed on June 24, 2008, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, one violation is cited in the enclosed Notice of

Violation (Notice) and the circumstances surrounding this violation are described in detail in the

enclosed report. The violation involved failure to implement corrective actions to preclude the

repetition of void formation in the emergency core cooling piping (EA-08-190). Although

determined to be of very low safety significance (Green), this violation is being cited because

one of the criteria specified in Section VI.A.1 of the NRC Enforcement Policy for a noncited

violation was satisfied. Specifically, AmerenUE failed to restore compliance within a reasonable

time after the violation was last identified in NRC Inspection Report 05000483/2006002-012.

Please note that you are required to respond to this letter and should follow the instructions

specified in the enclosed Notice when preparing your response. The NRC will use your

response, in part, to determine whether further enforcement action is necessary to ensure

compliance with regulatory requirements.

This report also documents four NRC-identified and self-revealing findings of very low safety

significance (Green). These findings were determined to involve violations of NRC

requirements. Additionally, two licensee-identified violations which were determined to be of

very low safety significance are listed in this report. However, because of the very low safety

significance and because they were entered into your corrective action program, the NRC is

treating these findings as NCVs consistent with Section VI.A of the NRC Enforcement Policy. If

you contest these NCVs, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

UNITED STATES

NUCLEAR REGULATORY COMMISSION

R E GI ON I V

612 EAST LAMAR BLVD, SUITE 400

ARLINGTON, TEXAS 76011-4125

Union Electric Company

- 2 -

ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional

Administrator, U.S. Nuclear Regulatory Commission Region IV, 612 East Lamar Drive,

Suite 400, Arlington, Texas 76011-4125; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at the

Callaway Plant.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its

enclosures will be made available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records component of NRCs document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA/

Vincent G. Gaddy, Chief,

Projects Branch B

Division of Reactor Projects

Docket: 50-483

License: NPF-30

Enclosures: Notice of Violation and

NRC Inspection Report 05000483/2008003

w/attachment: Supplemental Information

cc w/enclosure:

John ONeill, Esq.

Pillsbury Winthrop Shaw Pittman LLP

2300 N. Street, N.W.

Washington, DC 20037

Scott A. Maglio, Assistant Manager

Regulatory Affairs

AmerenUE

P.O. Box 620

Fulton, MO 65251

Missouri Public Service Commission

Governors Office Building

200 Madison Street

P.O. Box 360

Jefferson City, MO 65102-0360

H. Floyd Gilzow

Deputy Director for Policy

Missouri Department of Natural Resources

P. O. Box 176

Jefferson City, MO 65102-0176

Rick A. Muench, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

Kathleen Smith, Executive Director and

Kay Drey, Representative Board of

Directors

Missouri Coalition for the Environment

6267 Delmar Boulevard, Suite 2E

St. Louis City, MO 63130

Lee Fritz, Presiding Commissioner

Callaway County Courthouse

10 East Fifth Street

Fulton, MO 65251

Les H. Kanuckel, Manager

Quality Assurance

AmerenUE

P.O. Box 620

Fulton, MO 65251

Union Electric Company

- 3 -

Director, Missouri State Emergency

Management Agency

P.O. Box 116

Jefferson City, MO 65102-0116

Scott Clardy, Director

Section for Environmental Public Health

Missouri Department of Health and

Senior Services

P.O. Box 570

Jefferson City, MO 65102-0570

Luke H. Graessle, Manager

Regulatory Affairs

AmerenUE

P.O. Box 620

Fulton, MO 65251

Thomas B. Elwood, Supervising Engineer

Regulatory Affairs and Licensing

AmerenUE

P.O. Box 620

Fulton, MO 65251

Certrec Corporation

4200 South Hulen, Suite 422

Fort Worth, TX 76109

Keith G. Henke, Planner III

Division of Community and Public Health

Office of Emergency Coordination

Missouri Department of Health and

Senior Services

930 Wildwood,

P.O. Box 570

Jefferson City, MO 65102

Technical Services Branch Chief

FEMA Region VII

2323 Grand Boulevard, Suite 900

Kansas City, MO 64108-2670

Ronald L. McCabe, Chief

Technological Hazards Branch

National Preparedness Division

DHS/FEMA

9221 Ward Parkway, Suite 300

Kansas City, MO 64114-3372

Union Electric Company

- 4 -

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

DRP Director (Dwight.Chamberlain@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

DRS Deputy Director (Troy.Pruett@nrc.gov)

Senior Resident Inspector (David.Dumbacher@nrc.gov)

Branch Chief, DRP/B (Vincent.Gaddy@nrc.gov)

Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)

Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Only inspection reports to the following:

DRS STA (Dale.Powers@nrc.gov)

M. Cox, OEDO RIV Coordinator (Mark.Cox@nrc.gov)

OEMail.Resource@nrc.gov

Enforcement Officer (Michael.Vasquez@nrc.gov)

Chief Allegation Coordination/Enforcement Staff (William.Jones@nrc.gov)

Office of Enforcement (Alexander.Sapountizis@nrc.gov)

ROPreports

CWY Site Secretary (Dawn.Yancey@nrc.gov)

SUNSI Review Completed: VGG ADAMS:  ; Yes No Initials: __VGG__

Publicly Available

Non-Publicly Available Sensitive

Non-Sensitive

R:\\_Reactors\\_CW\\2008\\CW 2008003RP-DED.doc

ML 082180851

RIV:SRI:DRP/B

C:DRS/OB

C:DRS/PSB1

C:DRS/EB2

C:DRS/EB1

DDumbacher

RELantz

MPShannon

NFO'Keefe

RLBywater

/RA/ VGGaddy for /RA/

/RA/

/RA/ MFRunyan for /RA/

07/29/2008

07/9/2008

07/14/2008

07/15/2008

07/11/2008

C:DRS/PSB2

DRS/SRA

ACES

C:DRP/B

D:DRP

GEWerner

DPLoveless

GMVasquez

VGGaddy

DDChamberlain

/RA/

/RA/

/RA/

/RA/

/RA/

07/17/2008

07/15/2008

07/24/2008

08/5/2008

07/28/2008

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

- 1 -

Enclosure 1

NOTICE OF VIOLATION

AmerenUE

Docket 50-483

Callaway Plant

License NPF-30

EA-08-190

During an NRC inspection conducted March 24 through June 24, 2008, a violation of NRC

requirements was identified. In accordance with the NRC Enforcement Policy, the violation is

listed below:

10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that

measures shall be established to ensure that, for significant conditions adverse to

quality, the cause of the condition is determined and corrective action taken to preclude

repetition.

Contrary to this, from December 26, 2006, through May 21, 2008, the licensee failed to

take corrective actions to preclude repetition of safety-related emergency core cooling

system pipe voiding, and the licensee determined that this condition was a significant

condition adverse to quality.

This violation is associated with a Green Significance Determination Process finding.

Pursuant to the provisions of 10 CFR 2.201, AmerenUE is hereby required to submit a written

statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document

Control Desk, Washington, DC 20555 with a copy to the Regional Administrator, Region IV,

and a copy to the NRC Senior Resident Inspector at the facility that is the subject of this Notice

of Violation (Notice), within 30 days of the date of the letter transmitting this Notice. This reply

should be clearly marked as a "Reply to Notice of Violation EA-08-190," and should include:

(1) the reason for the violation, or, if contested, the basis for disputing the violation or severity

level, (2) the corrective steps that have been taken and the results achieved, (3) the corrective

steps that will be taken to avoid further violations, and (4) the date when full compliance will be

achieved. Your response may reference or include previous docketed correspondence, if the

correspondence adequately addresses the required response. If an adequate reply is not

received within the time specified in this Notice, an order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or why such other

action as may be proper should not be taken. Where good cause is shown, consideration will

be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), accessible from the

NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not

include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. If personal privacy or proprietary information is

necessary to provide an acceptable response, then please provide a bracketed copy of your

response that identifies the information that should be protected and a redacted copy of your

response that deletes such information. If you request withholding of such material, you must

specifically identify the portions of your response that you seek to have withheld and provide in

- 2 -

Enclosure 1

detail the bases for your claim of withholding (e.g., explain why the disclosure of information will

create an unwarranted invasion of personal privacy or provide the information required by

10 CFR 2.390(b) to support a request for withholding confidential commercial or financial

information). If safeguards information is necessary to provide an acceptable response, please

provide the level of protection described in 10 CFR 73.21.

Dated this 5th day of July 2008

- 1 -

Enclosure 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

50-483

License:

NPF-30

Report:

05000483/2008003

Licensee:

Union Electric Company

Facility:

Callaway Plant

Location:

Junction Highway CC and Highway O

Fulton, MO

Dates:

March 25 - June 24, 2008

Inspectors:

D. Dumbacher, Senior Resident Inspector

J. Groom, Resident Inspector

J. Drake, Senior Reactor Inspector, Plant Support, Branch 2

G. Guerra, CHP, Health Physicist, Plant Support Branch 1

Approved By:

V. Gaddy, Chief, Project Branch B

Division of Reactor Projects

- 2 -

Enclosure 2

SUMMARY OF FINDINGS

IR 05000483/2008003: 3/25 - 6/24/2008; Callaway Plant, Operability Evaluations,

Postmaintenance Testing, Surveillance Testing, and Identification and Resolution of Problems.

This report covered a 3-month period of inspection by resident inspectors. The significance of

most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual

Chapter 0609, "Significance Determination Process." Findings for which the Significance

Determination Process does not apply may be Green or assigned a severity level after NRC

management review. The NRCs program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,

dated December 2006.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. The inspectors identified a noncited violation of Technical

Specification 3.5.2, "Emergency Core Cooling Systems," after an inadequate

surveillance procedure resulted in the licensee failing to maintain the emergency

core cooling system full of water as required per Technical Specification 3.5.2.

On May 21, 2008, Callaway Plant engineering discovered that a section of the

cold leg recirculation piping, specifically the discharge of the residual heat

removal pumps to the safety injection pumps, contained 6.6 cubic feet of air.

Callaway monthly surveillance Procedure OSP-SA-00003, "Emergency Core

Cooling Flow Path Verification and Venting," had a purpose to: "Verify the ECCS

is full of water," in accordance with Technical Specification Surveillance

Requirement 3.5.2.3. The monthly verification and vent procedure was not

comprehensive enough to ensure all the emergency core cooling system was full

of water.

This finding was more than minor because it was similar to Example 3e of NRC

Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues," and

met the Not Minor If, criteria because the failure to meet the licensees

administrative requirement for allowable void fraction impacted the ability of the

Train A safety injection system to function upon initiation of high-pressure

recirculation. This finding affected the mitigating systems cornerstone procedure

quality attribute. Using the Manual Chapter 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, the inspectors determined that this finding

should be evaluated using the Phase 2 process described in Manual

Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection

Findings for At-Power Situations. As described in Section III, of Appendix A,

given that the presolved table did not contain a suitable target or surrogate for

this finding, the senior reactor analyst used the risk-informed notebook to

evaluate the significance of this finding affecting only high-pressure recirculation

as very low risk significance (Green). This finding has a crosscutting aspect in

the area of human performance associated with the decision making component

because the licensee failed to use conservative assumptions in decision making

and did not adopt a requirement to demonstrate that a single vent valve was

sufficient to vent the affected line rather than assuming that an additional

- 3 -

Enclosure 2

installed valve was not necessary to completely fill, vent, and test the line H.1(b)

(Section 1R15).

Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B,

Criterion XVI, "Corrective Action," was identified after the licensee failed to

promptly correct leakage from diesel generator jacket water o-rings. On

February 20, 2008, during a normal surveillance run of Emergency Diesel

Generator B, Callaway operations personnel identified an approximately

80 drop-per-minute jacket water leak caused by premature failure of Nitrile type

o-rings. Following restoration of Emergency Diesel Generator B, the licensee

re-evaluated the preventative maintenance frequency for jacket water o-ring

replacement and reduced the replacement frequency from once every 3 years to

once every refueling cycle. Then, on May 28, 2008, during a routine surveillance

run of Emergency Diesel Generator A, Callaway operations personnel identified

that Emergency Diesel Generator A had a 200 drop-per-minute jacket water leak.

Similar to the condition observed on Emergency Diesel Generator B on

February 20, 2008, the source of the leakage was from Nitrile type o-rings within

the jacket water system. The o-rings responsible for jacket water leakage were

found to be of similar age to those that failed during the February 20, 2008,

surveillance but had not been replaced despite the change to the licensee's

preventive maintenance frequency.

This finding, failure to implement adequate corrective actions for degraded Nitrile

type o-rings in Emergency Diesel Generator A after previously identifying the

adverse condition on Emergency Diesel Generator B, was more than minor

because, if left uncorrected, degraded diesel generator jacket water o-rings could

become a more significant safety concern. This finding affected the mitigating

systems cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial

Screening and Characterization of Findings, this finding was determined to be of

very low safety significance because it was a design deficiency confirmed not to

result in loss of operability. This finding has a crosscutting aspect in the area of

human performance associated with the work controls component because the

licensee failed to plan work activities to support long-term equipment reliability by

addressing known degraded conditions in a more reactive than preventative

manner H.3(b) (Section 1R19).

Green. The inspectors identified a violation of 10 CFR Part 50, Appendix B,

Criterion XVI, "Corrective Action," because the licensee failed to take corrective

actions to preclude repetition of void formation in emergency core cooling system

piping, a significant condition adverse to quality. After experiencing void

formations in 2005 and 2006, the NRC identified violations of Criterion XVI.

However, licensee corrective actions did not preclude repetition of void

formations that were discovered on May 21, 2008. On that date, Callaway Plant

engineering performed ultrasonic inspection of the safety injection system

common suction piping Line EM023-HCB - 6" and discovered a 6.6 cubic foot

voided area. This exceeded the allowable void fraction of 2.1 cubic feet required

for operability. This voided piping, determined to have existed for over a year,

was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The

maintenance restoration failed to perform an adequate fill and vent to ensure the

suction pipe was full of water. The inspectors identified several related examples

where the licensee had performed either inadequate operating experience

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Enclosure 2

evaluations, inadequate extent of condition reviews, or inadequate procedure

corrections. The violation is being cited in a Notice of Violation because the

licensee failed to restore compliance with a reasonable time after a violation was

last identified in 2006.

This finding, failure to restore compliance to prevent recurrence of emergency

core cooling system voids, was more than minor because it is similar to

Example 3e of NRC Inspection Manual Chapter 0612, Appendix E, "Examples of

Minor Issues," criteria because the failure impacted the ability of the emergency

core cooling system to function upon initiation of high-pressure recirculation.

Using the Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, the inspectors determined that this finding should

be evaluated using the Phase 2 process described in Manual Chapter 0609,

Appendix A, Determining the Significance of Reactor Inspection Findings for

At-Power Situations. As described in Section III, of Appendix A, given that the

presolved table did not contain a suitable target or surrogate for this finding, the

senior reactor analyst used the risk-informed notebook to evaluate the

significance of this finding as very low risk significance (Green). This finding has

a crosscutting aspect in the area of problem identification and resolution

associated with the corrective action program component because AmerenUE

failed to thoroughly evaluate voiding problems such that the resolutions

addressed causes and extent of condition, as necessary P.1(c) (Section 4OA2).

Cornerstone: Barrier Integrity

Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, was identified after determining that the licensee

had not adequately selected and reviewed the suitability of the design of the

containment air cooler control circuitry. On March 26, 2008, Containment Air

Cooler A fan shut down when shifted from fast to slow speed. Troubleshooting

by the licensee determined that voltage was lost to the control power circuitry

when the fast speed thermal overload tripped. Since the overload contacts were

wired in series, Containment Air Cooler A experienced a complete loss of control

power rendering it inoperable. The licensee determined the trip to be caused by

operation of containment air coolers in fast speed, during a period of higher than

normal containment pressure. The licensee analyzed the potential impact of the

newly discovered adverse containment cooler design vulnerability against design

basis accident scenarios. The licensee determined that a hot zero power main

steam line break results in a delayed safety injection signal allowing the fan

motor overloads to trip prior to being shed by the load sequencer. The

containment air coolers would then experience a complete loss of control power

and would not be capable of automatically restarting in slow speed. The analysis

revealed that the peak containment pressure limit of 48.1 psig would be

preserved. The licensee submitted a licensee event report as required by

10 CFR 50.73 since the inadequate containment air cooler control circuitry

resulted in a condition prohibited by the plants Technical Specifications.

This finding, failure to ensure the design of the containment air cooler control

circuitry was suitable for all plant conditions, was more than minor because it was

associated with the barrier integrity cornerstone attribute of design control and

affects the associated cornerstone objective to provide reasonable assurance

- 5 -

Enclosure 2

that physical design barriers protect the public from radio nuclide releases

caused by accidents or releases. Using Manual Chapter 0609, Appendix H,

Containment Integrity Significance Determination Process," this finding was

determined to be a Type B finding since it was related to a degraded condition

that has potentially important implications for the integrity of the containment,

without affecting the likelihood of core damage. This finding was found to be of

very low safety significance because containment coolers are structures,

systems or components that are not significant contributors to the large early

release frequency. The inspectors determined that this finding does not have a

crosscutting aspect associated with it since the performance deficiency was not

indicative of current licensee performance (Section 1R15).

Green. The inspectors identified a noncited violation of Technical

Specification 5.4.1.a, Procedures, after Callaway control room operators

improperly entered a wrong Technical Specification action statement due to the

failure to maintain the Technical Specification Bases current. On June 17, 2008,

during surveillance testing, Valve EMHV8823 failed to indicate fully closed.

Since EMHV8823 is an isolation valve for containment Penetration 49, the

licensee entered Technical Specification 3.6.3, Containment Isolation Valves,

Condition C, with an action to restore the valve to an operable status or isolate

the penetration within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> after Valve EMHV8823

had been declared inoperable, Callaway licensing personnel contacted the

control room and informed them of an approved Technical Specification Bases

change that did not allow Technical Specification 3.6.3, Condition C, to be

applicable to containment Penetration 49. The Technical Specification Bases

change was effective May 1, 2008, but had not been issued to the control room.

The licensee determined that the more restrictive Technical Specification 3.6.3,

Condition A, should have been entered with an action to isolate the affected

penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. The licensee performed a containment entry

following discovery of entry into Technical Specification 3.6.3, Condition A, and

found that Valve EMHV8823 failed its surveillance due to out of adjustment

position indicator limit switches. The valve was verified closed and isolated

allowing exit from Technical Specification 3.6.3, Condition A.

This finding, failure to ensure the Technical Specification Bases were maintained

current and available to the Callaway control room staff, was more than minor

because if left uncorrected, the failure to maintain the Technical Specification

Bases current could become a more significant safety concern. This finding was

determined to affect the barrier integrity cornerstone. Using Manual

Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,

this finding is determined to be of very low safety significance since this finding

did not represent an actual open pathway in the physical integrity of reactor

containment and did not involve an actual reduction in function of hydrogen

ignitors in the reactor containment. This finding has a crosscutting aspect in the

area of human performance associated with the decision making component

because the licensee failed to communicate, in a timely manner, decisions to

personnel who have a need to know the information in order to perform work

safely H.1(c) (Section 1R22).

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Enclosure 2

B.

Licensee-Identified Violations

Two violations of very low safety significance, which were identified by the licensee,

have been reviewed by the inspectors. Corrective actions taken or planned by the

licensee have been entered into the licensees corrective action program. These

violations and corrective action tracking numbers are listed in Section 4OA7.

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Enclosure 2

REPORT DETAILS

Summary of Plant Status

AmerenUE operated the Callaway Plant at near 100 percent for the entire quarter.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1

Readiness of Offsite and Alternate AC Power System

a. Inspection Scope

The inspectors reviewed the licensees plant features, training lesson plans, and

procedures for operation and continued availability of offsite and alternate AC power

systems to verify they were appropriate. The review included communication protocols

and agreement procedures between the transmission system operator and the nuclear

power plant to verify that appropriate information is exchanged when issues arise that

could impact the offsite power system. Specifically, the procedures were verified to

ensure they specified:

Required actions needed when notified by the transmission system operator that

posttrip voltage of the offsite power system would not be acceptable to assure

the continued operation of safety related loads without transferring to the onsite

power supply.

Compensatory actions needed when it is not possible to predict the posttrip

voltage at the nuclear power plant for current grid conditions.

Required assessment of plant risk based on maintenance activities which could

affect grid reliability, or the ability of the transmission system to provide the offsite

power system.

Required communications between the nuclear power plant and the transmission

system operator when changes at the nuclear power plant could impact the

transmission system, or when the capability of the transmission system to

provide adequate offsite system power is challenged.

On May 16, 2008, the inspectors evaluated the licensee staffs preparations for summer

readiness of offsite and AC power systems against the sites procedures and determined

that the staffs actions were adequate. Documents reviewed are listed in the

attachment.

These activities constituted one readiness of offsite power inspection sample as defined

by Inspection Procedure 71111.01.

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Enclosure 2

b. Findings

No findings of significance were identified.

.2

Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

On May 2, 2008, the inspectors completed a review of the licensee's readiness for

impending adverse weather involving severe thunderstorms. The inspectors:

(1) reviewed plant procedures, the Final Safety Analysis Report (FSAR), and Technical

Specifications to ensure that operator actions defined in adverse weather procedures

maintained the readiness of essential systems; (2) walked down portions of the

emergency diesel generators and offsite power systems to ensure that adverse weather

protection features were sufficient to support operability; (3) reviewed maintenance

records to determine that applicable surveillance requirements were current before the

anticipated severe thunderstorms developed; and (4) reviewed plant modifications,

procedure revisions, and operator work arounds to determine if recent facility changes

challenged plant operation. Documents reviewed by the inspectors are listed in the

attachment.

These activities constituted one readiness for impending adverse weather inspection

sample as defined by Inspection Procedure 71111.01.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignments (71111.04)

.1

Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

June 3, 2008, Train A auxiliary feedwater system while the Train B motor-driven

auxiliary feedwater pump was out of service for planned maintenance.

June 10, 2008, Train A 480 volt NG Class 1E switchgear while the Train B

emergency diesel generator was out of service for planned and emergent

maintenance issues.

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, FSAR, Technical Specification requirements, outstanding work orders,

corrective action documents, and the impact of ongoing work activities on redundant

trains of equipment in order to identify conditions that could have rendered the systems

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Enclosure 2

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify components and support equipment were

aligned correctly and were operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the

corrective action program with the appropriate significance characterization. Documents

reviewed are listed in the attachment.

These activities constituted two partial system walkdown samples as defined by

Inspection Procedure 71111.04.

b. Findings

No findings of significance were identified.

.2

Complete System Walkdown (71111.04S)

a. Inspection Scope

On April 17, 2008, the inspectors performed a complete system alignment inspection of

Train B of the residual heat removal system to verify the functional capability of the

system. The inspectors selected this system because it was considered both

safety-significant and risk-significant in the licensees probabilistic risk assessment. The

inspectors walked down the system to review mechanical and electrical equipment line

ups, electrical power availability, system pressure and temperature indications, as

appropriate, component labeling, component lubrication, component and equipment

cooling, hangers and supports, operability of support systems, and to ensure that

ancillary equipment or debris did not interfere with equipment operation. The inspectors

reviewed a sample of past and outstanding work orders to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the corrective action program database to ensure that system equipment

alignment problems were being identified and appropriately resolved. The documents

used for the walkdown and issue review are listed in the attachment.

These activities constituted one complete system walkdown sample as defined by

Inspection Procedure 71111.04.

b. Findings

No findings of significance were identified.

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Enclosure 2

1R05 Fire Protection (71111.05)

.1

Quarterly Fire Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

March 27, 2008, Fire Area C-21, Lower Cable Spreading Room

April 16, 2008, Fire Area A-17, Electrical Penetration Room (South)

April 25, 2008, Condensate Storage Tank

April 29, 2008, Fire Area A-23, Main Steam and Feedwater Isolation Valve

Enclosure

April 30, 2008, Reactor Building

June 18, 2008, Fire Area A-1, North Pipe Chase

The inspectors reviewed areas to assess if the licensee implemented a fire protection

program that adequately controlled combustibles and ignition sources within the plant,

effectively maintained fire detection and suppression capability, maintained passive fire

protection features in good material condition, and implemented adequate compensatory

measures for out of service, degraded or inoperable fire protection equipment, systems,

or features in accordance with the licensees fire plan. The inspectors selected fire

areas based on their overall contribution to internal fire risk as documented in the plants

Individual Plant Examination of External Events with later additional insights, their

potential to impact equipment which could initiate or mitigate a plant transient, or their

impact on the plants ability to respond to a security event. The inspectors verified that

fire hoses and extinguishers were in their designated locations and available for

immediate use; that fire detectors and sprinklers were unobstructed, that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. Documents reviewed are listed in the

attachment.

These activities constituted six quarterly fire protection inspection samples as defined by

Inspection Procedure 71111.05.

b. Findings

No findings of significance were identified.

.2

Annual Fire Protection Drill Observation (71111.05A)

a. Inspection Scope

On March 27, 2008, the inspectors observed a fire brigade activation due to a report of

smoke in the laundry decontamination area. The observation evaluated the readiness of

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Enclosure 2

the plant fire brigade to fight fires. The inspectors verified that the licensee staff

identified deficiencies; openly discussed them in a self-critical manner at the drill debrief,

and took appropriate corrective actions. Specific attributes evaluated were: (1) proper

wearing of turnout gear and self-contained breathing apparatus; (2) proper use and

layout of fire hoses; (3) employment of appropriate fire fighting techniques; (4) sufficient

firefighting equipment brought to the scene; (5) effectiveness of fire brigade leader

communications, command, and control; (6) search for victims and propagation of the

fire into other plant areas; (7) smoke removal operations; (8) utilization of preplanned

strategies; (9) adherence to the preplanned drill scenario; and (10) drill objectives.

Documents reviewed are listed in the attachment.

These activities constituted one annual fire protection inspection sample as defined by

Inspection Procedure 71111.05.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures (71111.06)

Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk-significant plant design features and licensee

procedures intended to protect the plant and its safety related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the FSAR, engineering calculations, and abnormal operating procedures for

licensee commitments. The inspectors reviewed licensee drawings to identify areas and

equipment that may be affected by internal flooding caused by the failure or

misalignment of nearby sources of water. The inspectors also reviewed the licensees

corrective actions for previously identified flood-related items. The inspectors performed

a walkdown of the following plant area to assess the adequacy of any watertight doors

and verify drains and sumps were clear of debris and operable, and that the licensee

complied with its flooding related commitments:

June 23, 2008, Control Building West Corridor

The document reviewed during this inspection is listed as follows:

Callaway Action Request 200805189

This inspection constituted one internal flooding sample as defined in Inspection

Procedure 71111.06.

b. Findings

No findings of significance were identified.

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Enclosure 2

1R11 Licensed Operator Requalification Program (71111.11)

a. Inspection Scope

On June 2, 2008, the inspectors observed a crew of licensed operators perform a

Cycle 08-3 as found scenario in the plants simulator to verify that operator performance

was adequate, evaluators were identifying and documenting crew performance

problems, and that training was being conducted in accordance with licensee

procedures. The scenario involved an operating design basis earthquake with a lockout

on essential 4 kV Bus NB01. The inspectors evaluated the crew in the following areas:

Licensed operator performance

Crew clarity and formality of communications

Ability to take timely actions in the conservative direction

Prioritization, interpretation, and verification of annunciator alarms

Correct use and implementation of abnormal and emergency procedures

Control board manipulations

Oversight and direction from supervisors

Ability to identify and implement appropriate Technical Specification actions and

Emergency Plan actions and notifications

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the attachment.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

May 15, 2008, Callaway Action Request (CAR) 200801644, an additional anode

was found in the north end of the Train A emergency diesel generator intercooler

May 15, 2008, CAR 200802854, KKJ01A (Train A emergency diesel generator)

engine oil sump high

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Enclosure 2

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of risk-important systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

Implementing appropriate work practices

Identifying and addressing common cause failures

Scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule

Characterizing system reliability issues for performance

Charging unavailability time

Trending key parameters for condition monitoring

Ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or reclassification

Verifying appropriate performance criteria for structures, systems, and

components/functions classified as (a)(2) or appropriate and adequate goals and

corrective actions for systems classified as (a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. The inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Documents reviewed are listed in the attachment.

This inspection constituted two quarterly maintenance effectiveness samples as defined

in Inspection Procedure 71111.12Q.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

April 3, 2008, Routine - Work on turbine-driven auxiliary feedwater

Valve KAPCV-0102

April 21, 2008, Emergency Diesel Generator A lube oil trouble shooting

April 28, 2008, Routine - associated with Loose Creek-Callaway 345 kV line

outage

- 14 -

Enclosure 2

June 10, 2008, Risk management actions associated with Emergency Diesel

Generator B jacket water o-ring replacement outage

These activities were selected based on their potential risk significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed Technical

Specification requirements and walked down portions of redundant safety systems,

when applicable, to verify risk analysis assumptions were valid and applicable

requirements were met. Documents reviewed are listed in the attachment.

These activities constituted four samples as defined by Inspection Procedure 71111.13.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

March 26, 2008, CARs 200802348, 200802365, and 200802264, Containment

coolers inoperable in fast speed

April 4, 2008, CARs 200800461 and 200802625, Containment recirculation sump

operability determination, Revisions 3 and 4

April 9, 2008, Source Range Channel N32 inoperable due to a failed surveillance

April 23, 2008, Component cooling water system following Valve EGHV0069

failing inservice test stroke time surveillance

April 30, 2008, CAR 200803465, Emergency diesel generator Garlock flexible

expansion joints

May 6, 2008, CAR 200803462, Voiding identified in containment spray pump

piping from sump

May 22, 2008, CAR 200904000, Line EM-023 allowable void fraction exceeded

The inspectors selected potential operability issues based on the risk significance of the

associated components and systems. The inspectors evaluated the technical adequacy

of the evaluations to ensure that Technical Specification operability was properly justified

and the subject component or system remained available such that no unrecognized

increase in risk occurred. The inspectors compared the operability and design criteria in

the appropriate sections of the Technical Specifications and FSAR to the licensees

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Enclosure 2

evaluations to determine whether the components or systems were operable. Where

compensatory measures were required to maintain operability, the inspectors

determined whether the measures in place would function as intended and were

properly controlled. The inspectors determined, where appropriate, compliance with

bounding limitations associated with the evaluations. Additionally, the inspectors

reviewed a sample of corrective action documents to verify that the licensee was

identifying and correcting deficiencies associated with operability evaluations.

Documents reviewed are listed in the attachment.

This inspection constituted seven samples as defined in Inspection Procedure 71111.15.

b. Findings

.1

Introduction. A self-revealing Green noncited violation (NCV) of 10 CFR Part 50,

Appendix B, Criterion III, Design Control, was identified after determining that the

licensee had not adequately selected and reviewed the suitability of the design of the

containment air cooler control circuitry.

Description. On March 26, 2008, Containment Air Cooler A fan shut down when shifted

from fast to slow speed. Troubleshooting by the licensee determined that voltage was

lost to the control power circuitry when the fast speed thermal overload tripped. Since

the overload contacts were wired in series, Containment Air Cooler A experienced a

complete loss of control power rendering it inoperable. AmerenUE personnel noted that

Precaution 3.6 of Procedure OTN-GN-00001, Containment Cooling and CRDM

Cooling, Revision 14, cautioned that high pressure and cool temperatures across

containment coolers will cause the coolers to operate close to the setpoint of the thermal

overloads. However, the licensees operability determination dismissed the 1987

precaution as not having a technical basis believing it was implemented to address

discrepancies in motor overload setpoints. Later, the licensee determined that operation

of containment air coolers in fast speed, during a period of higher than normal

containment pressure, challenged the fast speed thermal overload setpoint and resulted

in the trip of Containment Air Cooler A on March 26, 2008. As an interim measure to

prevent a trip from fast speed, the licensee imposed a standing order to maintain the

containment coolers in slow speed.

The licensee analyzed the potential impact of the newly discovered adverse containment

cooler design vulnerability against design basis accident scenarios. The licensee

determined that a hot zero power main steam line break results in a delayed safety

injection signal allowing the fan motor overloads to trip prior to being shed by the load

sequencer. The containment air coolers would then experience a complete loss of

control power and would not be capable of automatically restarting in slow speed. The

analysis revealed that in this scenario, utilizing assumed accident conditions, the peak

containment pressure would exceed the 48.1 psig limit described in the FSAR.

However, analysis using actual plant conditions determined that the peak containment

pressure limit of 48.1 psig would be preserved. The licensee submitted a licensee event

report (LER) as required by 10 CFR 50.73 since the inadequate containment air cooler

control circuitry resulted in a condition prohibited by the plants Technical Specifications.

The inspectors review of the licensees LER is described in Section 4OA3 of this report.

To address the design deficiency associated with the containment air cooler control

circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit

- 16 -

Enclosure 2

such that tripping of the fast speed overloads would not impact the safety-related slow

speed function of the containment air coolers.

Analysis. The performance deficiency associated with this finding involved the

licensees failure to ensure the design of the containment air cooler control circuitry was

suitable for all plant conditions. This finding was greater than minor because it was

associated with the barrier integrity cornerstone attribute of design control and affects

the associated cornerstone objective to provide reasonable assurance that physical

design barriers protect the public from radio nuclide releases caused by accidents or

releases. Using Manual Chapter 0609, Appendix H, Containment Integrity Significance

Determination Process," this finding was determined to be a Type B finding since it was

related to a degraded condition that has potentially important implications for the integrity

of the containment, without affecting the likelihood of core damage. This finding was

found to be of very low safety significance since containment coolers are structures,

systems, and components that have no impact on large early release frequency. The

inspectors determined that this finding does not have a crosscutting aspect associated

with it since the performance deficiency is not indicative of current licensee performance.

Enforcement. 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in

part, that measures be established for the selection and review for suitability of

application of materials, parts, equipment, and processes that are essential to the

safety-related functions of structures, systems, and components. Contrary to the above,

prior to April 2, 2008, the licensee failed to ensure that the containment air coolers would

be able to perform their safety-related function in all accident scenarios due to a design

deficiency associated with the overload contacts in the containment air cooler control

circuitry. Because this finding is of very low safety significance and has been entered

into the corrective action program as CAR 200702264, this violation is being treated as

an NCV consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000483/2008003-01, Failure to Ensure the Suitability of the Design of the

Containment Air Cooler Control Circuitry.

.2

Introduction. The inspectors identified a Green NCV of Technical Specification 3.5.2,

"Emergency Core Cooling Systems," after an inadequate surveillance procedure

resulted in the licensee failing to maintain the emergency core cooling system (ECCS)

full of water as required per Technical Specification 3.5.2.

Description. On May 21, 2008, Callaway Plant engineering discovered that a section of

the cold leg recirculation piping, specifically the discharge of the residual heat removal

pumps to the safety injection pumps, contained 6.6 cubic feet of air. This exceeded the

allowable void fraction of 2.1 cubic feet required for operability. Callaway monthly

surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow Path

Verification and Venting," had a purpose to: "Verify the ECCS is full of water," in

accordance with Technical Specification Surveillance Requirement 3.5.2.3. This

monthly surveillance was reviewed as part of significant condition adverse to quality

(SCAQ) CAR 200501092 corrective actions. Callaway engineering had determined that

residual heat removal pump discharge vent Valve EJV0193 to the safety injection

system was the high point vent for these lines and was thus sufficient to vent

Line EM-023-HCB - 6" to the safety injection pumps. However, this vent valve was not

adequate due to the pipe sloping issues and normally closed Valves EMHIS8807A/B.

Venting through Valve EMV0179 was necessary to completely fill, vent, and test the line.

The monthly verification and vent procedure was inadequate to identify and remove air

- 17 -

Enclosure 2

introduced by relief valve maintenance on May 7, 2007, and thus ensure the ECCS was

full of water. See Violation (VIO)05000483/2008003-05 in Section 4OA2.

Analysis. Failure to adequately verify ECCS piping was full of water as required by

Technical Specification 3.5.2 is a performance deficiency. This finding affected the

mitigating system cornerstone procedure quality attribute. This finding is more than

minor because it was similar to Example 3e of NRC Inspection Manual Chapter 0612,

Appendix E, "Examples of Minor Issues," and met the Not Minor If, criteria because the

failure to meet the licensees administrative requirement for allowable void fraction

impacted the ability of the Train A safety injection system to function upon initiation of

high-pressure recirculation. Using Manual Chapter 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, the inspectors determined that this finding should be

evaluated using the Phase 2 process described in Manual Chapter 0609, Appendix A,

Determining the Significance of Reactor Inspection Findings for At-Power Situations.

As described in Section III of Appendix A, given that the presolved table did not contain

a suitable target or surrogate for this finding, the senior reactor analyst used the

risk-informed notebook to evaluate the significance of this finding. Table 2 provides the

definitions for acronyms and initialisms used in the risk-informed notebook and

discussed in this inspection report.

TABLE 2

Acronyms and Initialisms used in Phase 2 Notebook

Initialism

Initiating Event or Mitigating Function

TPCS

Transient with Loss of the Power Conversion System

SLOCA

Small-Break Loss of Coolant Accident

MLOCA

Medium-Break Loss of Coolant Accident

LLOCA

Large-Break Loss of Coolant Accident

LOOP

Loss of Offsite Power

MSLB

Main Steam Line Break

LBDC

Loss of Vital Direct-Current Bus

AFW

Auxiliary Feedwater

PCS

Power Conversion System (Steam and Feed)

HPR

High Pressure Recirculation

DEPR

Depressurization of the Reactor Coolant System

EAC

Emergency Power (Alternating Current)

TDAFW

Turbine-Driven Auxiliary Feedwater Pump Train

SEAL

Reactor Coolant Pump Seal Integrity

STIN

Operators Stop High-Pressure Injection

MDAFW

Motor-Driven Auxiliary Feedwater Pump Train

The analyst performed a Phase 2 estimation in accordance with Inspection Manual

Chapter 0609, Appendix A, Attachment 2, Site Specific Risk-Informed Inspection

Notebook Usage Rules. Given that the performance deficiency was known to have

existed for 378 days (May 7, 2007, until May 21, 2008) the analyst used 1 year as the

exposure period. In accordance with Table 2 of the risk-informed notebook, the analyst

evaluated all worksheets except LLOCA. All worksheets were evaluated using the

nominal 1-year initiating event frequency. Because this finding only affected system

functionality during recirculation, nominal mitigation credit was given for all functions with

the exception of HPR. For HPR, the analyst made the bounding assumption that either

- 18 -

Enclosure 2

both centrifugal charging pumps or both safety injection pumps would be affected. This

assumption was supported by licensee evaluation. The analyst solved each applicable

worksheet and the dominant sequences are documented in Table 1.

TABLE 1

Phase 2 Dominant Sequences

Initiating Event

Sequence

Number

Mitigating Functions

Results

Transients

1

AFW-PCS-HPR

9

TPCS

1

AFW-HPR

8

SLOCA

2

DEPR-HPR

8

MLOCA

2

DEPR-HPR

9

1

AFW-HPR

9

5

EAC-TDAFW-HPR

9

LOOP

9

EAC-SEAL-HPR

9

MSLB

8

STIN-HPR

8

LBDC

8

TDAFW-MDAFW-HPR

8

Using Inspection Manual Chapter 0609, Appendix A, Attachment 1, Table 5, Counting

Rule Worksheet, the analyst determined that the risk contribution of this finding from

internal initiating events was of very low risk significance. In accordance with

Appendix A, Attachment 1, Steps 2.2.5 and 2.2.6, the analyst and determined that the

risk contribution of this finding from external initiating events or the contribution from

large-early release frequency were very low. Therefore, this finding was of very low risk

significance (Green). This finding has a crosscutting aspect in the area of human

performance associated with the decision making component because the licensee

failed to use conservative assumptions in decision making and did not adopt a

requirement to demonstrate that the single vent Valve EJV0193 was sufficient to vent

the Line EM-023-HCB - 6" rather than assuming that installed Valve EMV0179 was not

necessary to completely fill, vent, and test the line H.1(b).

Enforcement. Technical Specification 3.5.2 "Emergency Core Cooling Systems,"

Surveillance Requirement 3.5.2.3, required that the licensee verify that ECCS piping is

full of water every 31 days. Contrary to the above, from June 2007 through April 2008,

AmerenUE surveillance Procedure OSP-SA-00003, "Emergency Core Cooling Flow

Path Verification and Venting," was inadequate to meet Technical Specification

Surveillance Requirement 3.5.2.3. Because this finding is of very low safety significance

and was entered into the licensee's corrective action program as CAR 200804000, this

violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC

Enforcement Policy: NCV 05000483/2008003-02, Inadequate Surveillance Procedure

Resulted in an Inoperable ECCS.

- 19 -

Enclosure 2

1R18 Plant Modifications (71111.18)

a. Inspection Scope

The inspectors reviewed the design adequacy of the listed modifications. This included

verifying that the modification preparation did not impair the following: (a) in-plant

emergency/abnormal operating procedure actions, (b) key safety functions, and

(c) operator response to loss of key safety functions.

The inspectors verified that postmodification testing maintained the plant in a safe

configuration during testing and that the postmodification testing established operability

by: (a) verifying that unintended system interactions did not occur; (b) verifying that

performance characteristics, which could have been affected by the modification, met

the design bases; (c) validating the appropriateness of modification design assumptions;

and (d) demonstrating that the modification test acceptance criteria had been met.

April 18, 2008, Modification M-08-0013 to separate fast and slow speed overload

contacts for containment air coolers

June 1, 2008, Temporary Modification TM 08-0003 for the instrument air system

to provide an additional diesel-driven air compressor to improve system reliability

while the system was in degraded reliability

Documents reviewed are listed in the attachment.

These activities constituted two samples as defined by Inspection Procedure 71111.18.

b. Findings

No findings of significance were identified

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

April 10, 2008, Job 08002765.900, Source Range N32 postmaintenance test

April 17, 2008, Postmaintenance test containment Cooler D,

Modification 0800267/950(951)(952)

May 7, 2008, Job 06524419.940, Emergency Diesel Generator B

May 28, 2008, Job 08003910, Postmaintence test of Emergency Diesel

Generator A following repair of jacket water leaks

May 30, 2008, Job 08001080, Postmaintenance local leakrate test of

containment personnel hatch door

- 20 -

Enclosure 2

These activities were selected based upon the structure, system, and component's

ability to impact risk. The inspectors evaluated these activities to verify (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

Technical Specifications, the FSAR, 10 CFR Part 50 requirements, licensee procedures,

and various NRC generic communications to ensure that the test results adequately

ensured that the equipment met the licensing basis and design requirements. In

addition, the inspectors reviewed corrective action documents associated with

postmaintenance tests to determine whether the licensee was identifying problems and

entering them in the corrective action program and that the problems were being

corrected commensurate with their importance to safety. Documents reviewed are listed

in the attachment.

This inspection constitutes five samples as defined in Inspection Procedure 71111.19.

b. Findings

Introduction. A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion XVI,

"Corrective Action," was identified after the licensee failed to promptly correct leakage

from diesel generator jacket water o-rings.

Description. On February 20, 2008, during performance of Procedure OSP-NE-0001B,

Standby Diesel Generator B Periodic Tests, Callaway operations personnel identified

that the Emergency Diesel Generator B had an approximately 80 drop-per-minute jacket

water leak. Analysis by the licensee determined the cause of the leakage to be from

premature failure of Nitrile type o-rings in the jacket water supply and return headers.

Operational history at Callaway revealed o-ring failures prior to reaching 3 years of

service life. The o-rings responsible for the February 20, 2008, leakage had been in

service since Refueling Outage 14 in October 2005. Following restoration of Emergency

Diesel Generator B, the licensee re-evaluated the preventative maintenance frequency

for jacket water o-ring replacement. Based on a review of prior o-ring failures, the

replacement schedule for diesel generator jacket water o-rings was reduced from once

every 3 years to once every refueling cycle.

On May 28, 2008, during performance of Procedure OSP-NE-0001A, Standby Diesel

Generator A Periodic Tests, Callaway operations personnel identified that Emergency

Diesel Generator A had a 200 drop-per-minute jacket water leak. Based on the quantity

of the leakage, operations personnel declared Emergency Diesel Generator A

inoperable. Similar to the condition observed on Emergency Diesel Generator B on

February 20, 2008, the source of the leakage was from Nitrile type o-rings within the

jacket water system. While the licensee replaced the o-rings responsible for jacket

water leakage following the February 20, 2008, surveillance, several Nitrile type o-rings

installed during Refueling Outage 14 in October 2005 remained in service in both

Emergency Diesel Generators Trains A and B including those that failed during the

May 28, 2008, surveillance.

- 21 -

Enclosure 2

Subsequent analysis by the licensee determined that the required mission time of the

Emergency Diesel Generator A was preserved since adequate inventory in the jacket

water expansion tank existed such that the leakage observed on May 28, 2008, would

not have impacted the net positive suction head analysis for the jacket water cooling

pump.

Analysis. The performance deficiency associated with this finding involved the

licensees failure to implement adequate corrective actions for an adverse condition.

Specifically, the licensee failed to correct degraded Nitrile type o-rings in Emergency

Diesel Generator A after previously identifying the adverse condition on Emergency

Diesel Generator B. This finding was greater than minor because, if left uncorrected,

degraded diesel generator jacket water o-rings could become a more significant safety

concern. This finding affected the mitigating systems cornerstone. Using Manual

Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, this

finding was determined be of very low safety significance because it was a design

deficiency confirmed not to result in loss of operability. This finding had a crosscutting

aspect in the area of human performance associated with the work control component

because the licensee failed to plan work activities to support long-term equipment

reliability by addressing known degraded conditions in a more reactive than preventative

manner H.3(b).

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires,

in part, that measures be established to assure conditions adverse to quality are

promptly identified and corrected. Contrary to the above, the licensee failed to

implement adequate corrective actions for the identified adverse condition that Nitrile

type o-rings would prematurely fail prior to the completion of the regularly scheduled

3-year replacement interval. Because this violation is of very low safety significance and

has been entered into the licensee's corrective action program as CAR 200804164, this

violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC

Enforcement Policy: NCV 05000483/2008003-03, Failure to Correct a Condition

Adverse to Quality for Diesel Generator Jacket Water O-Rings.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and Technical Specification requirements:

April 2, 2008, Job 07513515.500, Routine surveillance auxiliary building Train A

negative pressure test

April 4, 2008, Job 08501501, Routine surveillance Slave Relay K645 test of

essential service water component lineup

April 18, 2008, Job 08501499, Routine surveillance Slave Relay K615 test

April 29, 2008, Job 08501254.500, Residual heat removal Pump A inservice test

- 22 -

Enclosure 2

May 5, 2008, Jobs 08502271 and 08503327, Routine surveillance containment

base strong motion accelerometer seismic monitor calibration

May 14, 2008, Job 07505653, Residual heat removal Train B valve inservice test

June 11, 2008, Job 08504820, Routine surveillance diesel generator Train B

1-hour run

June 17, 2008, Job 08503115, Safety injection system Train A valve inservice

test

June 18, 2008, Job 08505155, Routine surveillance ECCS flow path verification

and venting

June 23, 2008, Job 08506247, Reactor coolant system leakage surveillance,

reactor coolant system inventory balance, plant status

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine whether: any preconditioning occurred; effects of the testing were

adequately addressed by control room personnel or engineers prior to the

commencement of the testing; acceptance criteria were clearly stated, demonstrated

operational readiness, and were consistent with the system design basis; plant

equipment calibration was correct, accurate, and properly documented; as left setpoints

were within required ranges; the calibration frequency was in accordance with Technical

Specifications, the FSAR, procedures, and applicable commitments; measuring and test

equipment calibration was current; test equipment was used within the required range

and accuracy; applicable prerequisites described in the test procedures were satisfied;

test frequencies met Technical Specification requirements to demonstrate operability

and reliability; tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored where

used; test data and results were accurate, complete, within limits, and valid; test

equipment was removed after testing; where applicable, test results not meeting

acceptance criteria were addressed with an adequate operability evaluation or the

system or component was declared inoperable; where applicable for safety-related

instrument control surveillance tests, reference setting data were accurately incorporated

in the test procedure; equipment was returned to a position or status required to support

the performance of the safety functions; and all problems identified during the testing

were appropriately documented and dispositioned in the corrective action program.

Documents reviewed are listed in the attachment.

The inspectors completed six routine, three inservice test, and one reactor coolant

system leakage samples.

b. Findings

Introduction. A self-revealing Green NCV of Technical Specification 5.4.1.a,

Procedures, was identified after Callaway control room operators improperly entered

the wrong Technical Specification action statement due to the failure to maintain the

Technical Specification Bases current.

- 23 -

Enclosure 2

Description. On June 17, 2008, during surveillance testing, Valve EMHV8823 failed to

indicate fully closed. Since EMHV8823 is an isolation valve for containment

Penetration 49, the licensee entered Technical Specification 3.6.3, Containment

Isolation Valves," Condition C, with an action to restore the valve to an operable status

or isolate the penetration within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The control room staff believed the

appropriate action statement was entered since Condition C is described in the

Technical Specification Bases as applicable to flow paths that meet the requirements of

a closed system per the Callaway FSAR. Chapter 6.2.6.3 of the Callaway FSAR

described Containment Penetration 49 as a closed engineered safety feature

containment penetration.

Approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> after Valve EMHV8823 had been declared inoperable, Callaway

licensing personnel contacted the control room and informed them of an approved

Technical Specification Bases change that did not allow the classification of containment

Penetration 49 as a closed system. Procedure APA-ZZ-00108, Primary Licensing

Document; Change/Revision Process," required that the change be implemented within

45 days following approval. The Technical Specification Bases change was effective

May 1, 2008, but had not been issued to the control room. The change resulted in

Condition C of Technical Specification 3.6.3 applying specifically to penetrations for

which a single containment isolation valve is credited per flow path. Since containment

Penetration 49 relies on multiple valves for flow path isolation, the licensee determined

that Condition C of Technical Specification 3.6.3 was not applicable for Penetration 49,

and the wrong Technical Specification action statement had been entered following the

failed surveillance on Valve EMHV8823. The licensee determined that the more

restrictive Technical Specification 3.6.3, Condition A, should have been entered with an

action to isolate the affected penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

The licensee performed a containment entry following discovery of entry into Technical

Specification 3.6.3, Condition A, and found that Valve EMHV8823 had failed its

surveillance due to out-of-adjustment position indicator limit switches. The valve was

verified closed with power removed allowing exit from Technical Specification 3.6.3,

Condition A.

Analysis. The performance deficiency associated with this finding involved the

licensees failure to ensure the Technical Specification Bases were maintained current

and available to the Callaway control room staff. This finding was greater than minor

because, if left uncorrected, the failure to maintain the Technical Specification Bases

current could become a more significant safety concern. This finding was determined to

affect the barrier integrity cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial

Screening and Characterization of Findings," this finding is determined to be of very low

safety significance since this finding did not represent an actual open pathway in the

physical integrity of reactor containment and did not involve an actual reduction in

function of hydrogen ignitors in the reactor containment. This finding had a crosscutting

aspect in the area of human performance associated with the decision making

component because the licensee failed to communicate, in a timely manner, decisions to

personnel who have a need to know the information in order to perform work safely

H.1(c).

Enforcement. Technical Specification 5.4.1.a, Procedures, required that written

procedures be established and implemented covering activities specified in Appendix A,

Typical Procedures for Pressurized Water Reactors, of Regulatory Guide 1.33, Quality

- 24 -

Enclosure 2

Assurance Program Requirements (Operation), February 1978. Regulatory Guide 1.33,

Appendix A, Section 1, required administrative procedures for procedure review and

approval. Procedure APA-ZZ-00108 provides a process for implementing Technical

Specification Bases change notices. Contrary to the above, on May 1, 2008,

Procedure APA-ZZ-00108 was not adequate to ensure changes to the Technical

Specification Bases were implemented in a timely manner. Because of the very low

safety significance and AmerenUEs action to place this issue in their corrective action

program as CAR 200805283, this violation is being treated as an NCV in accordance

with Section VI.A.1 of the Enforcement Policy: NCV 05000483/2008003-04, Failure to

Maintain an Adequate Technical Specification Bases Change Process.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

a. Inspection Scope

This area was inspected to assess the licensees performance in implementing physical

and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspectors used the

requirements in 10 CFR Part 20, the Technical Specifications, and the licensees

procedures required by Technical Specifications as criteria for determining compliance.

During the inspection, the inspectors interviewed the radiation protection manager,

radiation protection supervisors, and radiation workers. The inspectors performed

independent radiation dose rate measurements and reviewed the following items:

Performance indicator events and associated documentation packages reported

by the licensee in the occupational radiation safety cornerstone

Controls (surveys, posting, and barricades) of radiation, high radiation, or

airborne radioactivity areas

Radiation work permits, procedures, engineering controls, and air sampler

locations

Physical and programmatic controls for highly activated or contaminated

materials (non-fuel) stored within spent fuel and other storage pools

Self-assessments, audits, LERs, and special reports related to the access control

program since the last inspection

Changes in licensee procedural controls of high dose rate - high radiation areas

and very high radiation areas

Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

Posting and locking of entrances to accessible high dose rate - high radiation

areas and very high radiation areas

- 25 -

Enclosure 2

Documents reviewed are listed in the attachment.

The inspectors completed 8 of the required 21 samples.

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02)

a. Inspection Scope

The inspectors assessed licensee performance with respect to maintaining individual

and collective radiation exposures as low as is reasonably achievable (ALARA). The

inspectors used the requirements in 10 CFR Part 20 and the licensees procedures

required by technical specifications as criteria for determining compliance. The

inspectors interviewed licensee personnel and reviewed:

Current 3-year rolling average collective exposure

Site-specific trends in collective exposures, plant historical data, and source-term

measurements

Site-specific ALARA procedures

Work activities of highest exposure significance during the inspection

Integration of ALARA requirements into work procedure and radiation work

permit documents

Post-job (work activity) reviews

Workers use of the low dose waiting areas

First-line job supervisors contribution to ensuring work activities are conducted in

a dose efficient manner

Records detailing the historical trends and current status of tracked plant source

terms and contingency plans for expected changes in the source term due to

changes in plant fuel performance issues or changes in plant primary chemistry

Source-term control strategy or justifications for not pursuing such exposure

reduction initiatives

Specific sources identified by the licensee for exposure reduction actions,

priorities established for these actions, and results achieved since the last

refueling cycle

Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

- 26 -

Enclosure 2

Declared pregnant workers during the current assessment period, monitoring

controls, and the exposure results

Self-assessments, audits, and special reports related to the ALARA program

since the last inspection

Resolution through the corrective action process of problems identified through

post-job reviews and post-outage ALARA report critiques

Corrective action documents related to the ALARA program and follow-up

activities, such as initial problem identification, characterization, and tracking

Effectiveness of self-assessment activities with respect to identifying and

addressing repetitive deficiencies or significant individual deficiencies

Documents reviewed are listed in the attachment.

The inspectors completed 9 of the required 15 samples and 8 of the optional samples.

b. Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1

Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the first

Quarter 2008 performance indicators for any obvious inconsistencies prior to its public

release in accordance with IMC 0608, Performance Indicator Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b. Findings

No findings of significance were identified.

.2

Safety System Functional Failures

Cornerstone: Mitigating Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the safety system functional failures

performance indicator for the period March 2007 until March 2008. To determine the

accuracy of the performance indicator data reported during this period, performance

indicator definitions and guidance contained in the Nuclear Energy Institute (NEI)

- 27 -

Enclosure 2

Document 99-02, Revision 5, Regulatory Assessment Performance Indicator

Guideline, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73,"

definitions and guidance were used. The inspectors reviewed the licensees operator

narrative logs, operability assessments, maintenance rule records, maintenance work

orders, issue reports, event reports and NRC integrated inspection reports for the period

of 2nd Quarter 2007, through 1st Quarter 2008 to validate the accuracy of the

submittals. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the performance indicator data

collected or transmitted for this indicator and none were identified. Documents reviewed

are listed in the attachment.

This inspection constitutes one safety system functional failures sample as defined by

Inspection Procedure 71151.

b. Findings

No findings of significance were identified.

.3

Mitigating Systems Performance Index - High Pressure Injection Systems

Cornerstone: Mitigating Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the mitigating systems performance

index - high pressure injection systems performance indicator for the period from

March 2007 until March 2008. To determine the accuracy of the performance indicator

data reported during this period, performance indicator definitions and guidance

contained in the NEI Document 99-02, 5, Regulatory Assessment Performance

Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees

operator narrative logs, issue reports, mitigating systems performance index derivation

reports, event reports, and NRC integrated inspection reports for the period of

2nd Quarter 2007 through 1st Quarter 2008 to validate the accuracy of the submittals.

The inspectors reviewed the mitigating systems performance index component risk

coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable NEI

guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the performance indicator data

collected or transmitted for this indicator and none were identified. Documents reviewed

are listed in the attachment.

This inspection constitutes one mitigating systems performance index high pressure

injection systems sample as defined by Inspection Procedure 71151.

b. Findings

No findings of significance were identified.

- 28 -

Enclosure 2

.4

Occupational Exposure Control Effectiveness

Cornerstone: Occupational Radiation Safety

a. Inspection Scope

The inspectors reviewed licensee documents from October 1, 2007, through March 31,

2008. The review included corrective action documentation that identified occurrences

in locked high radiation areas (as defined in the licensees Technical Specifications),

very high radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel

exposures (as defined in NEI 99-02, "Regulatory Assessment Indicator Guideline,"

Revision 5). Additional records reviewed included ALARA records and whole body

counts of selected individual exposures. The inspectors interviewed licensee personnel

that were accountable for collecting and evaluating the performance indicator data. In

addition, the inspectors toured plant areas to verify that high radiation, locked high

radiation, and very high radiation areas were properly controlled. Performance indicator

definitions and guidance contained in NEI 99-02, Revision 5, were used to verify the

basis in reporting for each data element.

The inspectors completed the required sample (1) in this cornerstone.

b. Findings

No findings of significance were identified.

.5

Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

Cornerstone: Public Radiation Safety

a. Inspection Scope

The inspectors reviewed licensee documents from October 1, 2007, through March 31,

2008. Licensee records reviewed included corrective action documentation that

identified occurrences for liquid or gaseous effluent releases that exceeded performance

indicator thresholds and those reported to the NRC. The inspectors interviewed licensee

personnel that were accountable for collecting and evaluating the performance indicator

data. Performance indicator definitions and guidance contained in NEI 99-02,

Revision 5, were used to verify the basis in reporting for each data element.

The inspectors completed the required sample (1) in this cornerstone.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical

Protection

- 29 -

Enclosure 2

.1

Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

to verify that they were being entered into the licensees corrective action program at an

appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. The attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent of condition reviews, and previous occurrence reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples.

b. Findings

No findings of significance were identified.

.2

Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. This review was

accomplished through inspection of the stations daily condition report packages.

These daily reviews were performed, by procedure, as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings of significance were identified.

.3

Selected Issue Follow-up Inspection

a. Inspection Scope

The inspectors selected the below listed issues for a more in-depth review. The

inspectors considered the following during the review of AmerenUE's actions:

(1) complete and accurate identification of the problem in a timely manner; (2) evaluation

and disposition of operability/reportability issues; (3) consideration of extent of condition,

generic implications, common cause, and previous occurrences; (4) classification and

prioritization of the resolution of the problem; (5) identification of root and contributing

causes of the problem; (6) identification of corrective actions; and (7) completion of

corrective actions in a timely manner.

- 30 -

Enclosure 2

Voiding discovered in the common residual heat removal discharge piping for

high pressure recirculation.

FSAR changes/updates

Documents reviewed are listed in the attachment.

This inspection constituted two in-depth problem identification and resolution samples.

b. Findings

Introduction. The inspectors identified a Green violation of 10 CFR Part 50, Appendix B,

Criterion XVI, "Corrective Action," because the licensee failed to take corrective actions

to preclude repetition of void formations in the ECCS, a significant condition adverse to

quality (SCAQ). Contributors to the violation included: (1) the failure of corrective

actions from inspection report findings NCV 05000483/2005002-01, 05000483/2006012-04 and CAR 200501092 to ensure adequate fill and vent of

systems following maintenance to replace safety injection system relief valves, and

(2) inadequate extent of condition reviews in responding to internal and external

operating experience associated with pipe sloping issues in the safety injection system.

Description. On May 21, 2008, the Callaway Plant staff initiated CAR 200804000, a

SCAQ corrective action document, indicating that some piping in Train A safety injection

system suction lines had incorrect sloping and were susceptible to voiding due to high

points. Callaway Plant engineering performed ultrasonic inspection of the safety

injection system common suction piping Line EM023-HCB - 6" and discovered a

6.6 cubic foot voided area. This exceeded the allowable void fraction of 2.1 cubic feet

required for operability. This voided piping, determined to have existed for over a year,

was caused by relief valve maintenance on Valve EM8858A (May 7, 2007). The

maintenance restoration failed to perform an adequate fill and vent to ensure the suction

pipe was full of water.

In 2005 and 2006 the NRC issued NCVs regarding ineffective corrective actions related

to safety injection system voids in discharge piping (05000483/2005002-01 dated May 6,

2005, and 05000483/2006012-04 dated December 26, 2006). These were each 10 CFR

Part 50, Appendix B, Criterion XVI, NCVs, each for SCAQ. The Callaway Plant staff

issued CAR 200501092 as a SCAQ corrective action document. The CAR determined

that the causes of the voids (2004, 2005, and 2006) were related to incorrect pipe

sloping (allowing high points where voids could not be swept away by normal online

pump surveillances) and inadequate postmaintenance fill and vent operations (following

discharge piping relief Valve EM8853A replacement) to ensure the piping was full of

water.

Inadequate Operating Experience and Extent of Condition Corrections: The

inspectors identified several related examples where the licensee had performed either

inadequate operating experience evaluations, inadequate extent of condition reviews, or

inadequate procedure corrections.

Callaway CAR 200501092 referenced industry operating experience at Beaver Valley

Unit 2 in 2002: "The void was located in the piping used following a loss of coolant

- 31 -

Enclosure 2

accident after the transfer to containment sump recirculation. The piping containing the

void led to a common suction header for both trains of high head pumps." This was the

same location as the voiding discovered at Callaway Plant on May 21, 2008.

NRC Information Notice 2006-21, "Operating Experience Regarding Entrainment of Air

into Emergency Core Cooling and Containment Spray Systems," dated September 21,

2006, discussed mechanisms that could result in air entrainment on the suction sides of

emergency core cooling pumps. The notice emphasized the importance of ensuring that

entrained air will not enter suction supply lines and impair the ability of the ECCS and

containment spray pumps to perform their safety function.

The licensee's evaluation of NRC Information Notice 2006-21 was documented in

CAR 200608956. It stated that the information notice was applicable to Callaway and

that past review of these operating experiences and Callaway procedures and practices

were adequate. The CAR was closed December 5, 2006.

Callaway CAR 200501092 had Action 7 assigned to address the previous NRC

violations discussed above. The action required that system specific fill and vent

restoration guidance be developed to address maintenance on ECCS safety-related

systems. Initially, operating department Standing Order 05-002 dated June 8, 2005,

stated that the CAR 200501092 common cause analysis supported the need for

formalized restoration instructions. Until the system specific restoration instructions

were developed, the standing order required reactor operators to perform reviews to

ensure dynamic filling and venting occurred to reduce the susceptibility of voiding. Also

nuclear engineering department staff were to provide concurrence on such restoration

plans. Night Order ODP-ZZ-00310, "System Fill and Vent," issued February 13, 2006,

reiterated that reactor operator reviews and engineering concurrence were required

when these risk-significant systems were drained. However, on May 7, 2007,

Procedure OTN-EM-00001, "Safety Injection System," (developed to address filling and

venting evaluations) had Line EM-023-HCB - 6" isolated by Valve EMHIS8807B being

closed. The procedure did not include use of the available installed vent Valve EM179

for this line.

Callaway monthly Surveillance OSP-SA-00003, "Emergency Core Cooling Flow Path

Verification and Venting," had a purpose to: "Verify the ECCS is full of water in

accordance with Technical Specification Surveillance Requirement 3.5.2.3." This

monthly surveillance was reviewed as part of CAR 200501092 corrective actions.

Callaway engineering had determined that residual heat removal pump discharge vent

Valve EJV0193 to the safety injection suction line was the high point vent for these lines

and was thus sufficient to vent supply Line EM-023-HCB - 6" to the safety injection

pumps. However, this vent valve was not adequate due to the pipe sloping issues and

normally closed Valves EMHIS8807A/B. The monthly verification and vent procedure

was inadequate to remove the air entrained by the May 7, 2007, relief valve

maintenance. See Section 1R15, NCV 05000483/2008003-02.

Callaway CARs 200800226 and 200800246, initiated in January 2008, discussed

operating experience at Wolf Creek Nuclear Operating Corporation describing gas

voiding in the residual heat removal piggyback Line EM-022-HCB - 6" to the suction of

centrifugal charging pumps and safety injection pumps. The CARs stated that Callaway

had taken a proactive approach and had immediately performed ultrasonic testing to

demonstrate that the associated piping was water solid. However, the adjacent

- 32 -

Enclosure 2

connecting Line EM-023-HCB - 6" had not been vented nor had ultrasonic testing

occurred since the May 7, 2007, relief Valve EM8858A maintenance.

NRC Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal, and Containment Spray Systems," was issued January 11, 2008.

The Callaway Plant staff initiated CAR 200800298 to respond to the generic letter. The

generic letter identified that a licensing basis concern existed for some plants, such as

Callaway, that Technical Specifications require verifying that ECCS discharge piping is

full of water but may not include verification of the suction piping despite the realistic

concern that gas accumulation in suction piping may be more serious than gas

accumulation in discharge piping. The void found in Line EM-023-HCB - 6" was the

discharge of the residual heat removal pumps providing suction to the Train A safety

injection pump. The Callaway monthly Surveillance OSP-SA-00003, "Emergency Core

Cooling Flow Path Verification and Venting," did not test for or vent the discharge line

from residual heat removal to safety injection pump suction piping.

Analysis. The inspectors determined that the failure to restore compliance within a

reasonable time by establishing measures to prevent void formation in ECCS suction

piping for the Train A safety injection system was a performance deficiency. This finding

is more than minor because it was similar to Example 3e of NRC Inspection Manual

Chapter 0612, Appendix E, "Examples of Minor Issues," and met the Not Minor If,

criteria because the failure to meet the licensees administrative requirement for

allowable void fraction impacted the ability of the Train A safety injection system to

function upon initiation of high-pressure recirculation. Using Manual Chapter 0609.04,

Phase 1 - Initial Screening and Characterization of Findings, the inspectors determined

that this finding should be evaluated using the Phase 2 process described in Manual

Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection Findings

for At-Power Situations.

The senior reactor analyst determined that the risk of this finding was bounded by that

analyzed for NCV 05000423/2008003-02 (See Section 1R15.b.2). Therefore, this

finding was of very low risk significance (Green).

This finding has a crosscutting aspect in the area of problem identification and resolution

associated with the corrective action component because AmerenUE failed to thoroughly

evaluate voiding problems such that the resolutions addressed causes and extent of

condition, as necessary. This also includes, for significant problems, conducting

effectiveness reviews of corrective actions to ensure that the problems are resolved

P.1(c).

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires

the licensee to, in the case of SCAQ, establish measures to assure that the cause of the

condition is determined and corrective action is taken to preclude repetition. Contrary to

the above, from December 26, 2006, to May 21, 2008, the licensee did not implement

corrective action to preclude repetition of void formation in the safety injection piping

which the licensee categorized as an SCAQ. Specifically, void formation recurred after

performing maintenance on relief valve. Valve EM8858A, on May 7, 2007. Previously

discovered voiding of the safety injection system was last documented as an SCAQ in

NCV 05000483/2006012-04 dated December 26, 2006. For each instance of the

previously discovered voids, the causes were determined to be related to inadequate fill

and vent of the system piping following relief valve replacements and design deficiencies

- 33 -

Enclosure 2

associated with inadequate sloping of the piping. It was a reasonable assumption that

maintenance that drained either the suction or discharge piping could create significant

void areas.

Although this violation is of very low safety significance, the violation is being

cited in a Notice of Violation consistent with Section VI.A.1 of the NRC Enforcement

Policy because the licensee did not restore compliance within a reasonable

time after a previous violation NCV 05000483/2006012-04 was identified:

VIO 05000483/2008003-05, Failure to Prevent Recurrence of Voids in ECCS Cold Leg

Recirculation Piping. This finding has been entered into the licensee's corrective action

program as a SCAQ in CAR 200804000.

.4

Semiannual Trend Review

The inspectors assessed trends that might indicate the existence of a more significant

safety issue. These issues included trends that might not rise to the level of an

inspection finding.

NRC-Identified Trends

The NRC identified emergency diesel generator material condition and design control

issues degrading diesel reliability:

CAR 200801270: 80 Drops per minute jacket water leak identified on Diesel

Generator B

CAR 200801644: Additional sacrificial anode found in Emergency Diesel

Generator A intercooler heat exchanger

CAR 200802019: Emergency Diesel Generator B declared inoperable due to

fuel oil leaks

CAR 200802177: Cracked fuel oil return line fitting identified on Emergency

Diesel Generator A

CAR 200804164: Emergency Diesel Generator A declared inoperable due to a

200 drops per minute jacket water leak

Licensee-Identified Trends

The licensee identified a continued trend in plant status control and configuration control

with a key causal factor being procedure adherence.

CAR 200706832: This trend CAR from Third Quarter 2007 identified the cause

of plant status control issues to be a "Failure to follow written instructions."

CAR 200801457: A gauge was installed on an incorrect component during Test

Procedure OSP-EN-P001A.

CAR 200800580: A trend of critical steps not being included in work packages

was identified.

- 34 -

Enclosure 2

CAR 200802603: Component cooling water pump autostarted due to an

interlock with the centrifugal charging pumps. The operator failed to wait the

procedure prerequisite 30 minutes prior to securing the component cooling water

pump.

CAR 200802818: Source range Channel N31 was not restored to "block" as

required by procedure in Mode 1.

CAR 200800328: Not following procedures resulted in gaseous Radiation

Monitor RM-11 trip setpoint not being capable of isolating the waste gas decay

tank release.

CAR 200803351: Steam generator blowdown tripped due to an incorrect

demineralizer valve lineup.

CAR 200804483: Train B motor-driven auxiliary feedwater pump made

inoperable when its room cooler was taken to "stop" vice "auto." This was

performed outside the out of service restoration process.

This inspection constituted one semiannual trend review sample.

4OA3 Event Follow-up (71153)

(Closed) LER 05000483/2008-001-00, Containment Cooler Inoperability

On March 26, 2008, Containment Air Cooler A fan shut down when shifted from fast to

slow speed. The licensee determined that operation of containment air coolers in fast

speed, during a period of higher than normal containment pressure, would challenge the

fast speed thermal overload setpoint. Additionally, since the overload contacts are wired

in series, containment air coolers were determined to experience a complete loss of

control power following a trip from fast speed. The licensee analyzed the potential

impact of the containment cooler design vulnerability against design basis accident

scenarios. The licensee determined that a hot zero power main steam line break results

in a delayed safety injection signal allowing the fan motor overloads to trip prior to being

shed from the load sequencer. In this scenario, utilizing actual plant conditions, the peak

containment pressure would not exceed the 48.1 psig limit described in the FSAR. To

address the design deficiency associated with the containment air cooler control

circuitry, the licensee completed a modification in April 2008 to reconfigure the circuit

such that tripping of the fast speed overloads would not impact the safety-related slow

speed function of the containment air coolers. This finding is of very low safety

significance because the containment coolers are structures, systems, and components

that are not significant contributors to the large early release frequency. Licensee

corrective actions were recorded in CAR 200802264. The inspectors reviewed the LER

and identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design

Control, for the licensees failure to adequately review the suitability of the design of the

containment air cooler control circuitry (Section 1R15). This LER is closed.

This inspection constituted one sample of follow-up of events.

- 35 -

Enclosure 2

4OA5 Other Activities

.1

Quarterly Resident Inspector Observations of Security Personnel and Activities

a.

During the inspection period, the inspectors performed the following observations of

security force personnel and activities to ensure that the activities were consistent with

licensees security procedures and regulatory requirements relating to nuclear plant

security. These observations took place during both normal and off-normal plant

working hours.

These quarterly resident inspector observation of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors normal plant status review and inspection activities.

b.

Findings

No findings of significance were identified.

.2

(Closed) NRC Temporary Instruction 2515/166: Pressurized Water Reactor

Containment Sump Blockage

a. Inspection Scope

From March 17-19, 2008, the inspectors reviewed the licensees implementation of plant

modifications and design modification packages associated with their response to

Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency

Recirculation During Design Basis Accidents at Pressurized Water Reactors. The

inspectors reviewed various aspects of the on-going procedural changes. Those

changes that have been completed were verified to be properly documented in

accordance with the requirements of 10 CFR 50.59. At the completion of this inspection,

the licensee had completed the installation stage of the new sump strainers; many of the

procedural changes associated with the modifications had not been completed.

The inspectors compared and evaluated the recirculation sump modifications to the

original design basis using Temporary Instruction 2515/166 and referred to Regulatory

Guide 1.82, Revision 0, Water Sources for Long-Term Recirculation Cooling Following

a Loss-of-Coolant Accident.

Status of the implementation of the plant modifications and procedure changes

committed to by the licensee in their Generic Letter 2004-02 response is:

1.

Containment walkdown to provide current assessment of Callaway's containment

coatings and latent debris.

The licensee completed a containment walkdown and latent debris assessment

during Refueling Outage 14. The resident inspectors completed a walkdown of

the containment prior to reactor startup following the outage. The licensee

report, Containment Building Latent Debris Assessment Refuel 14 Fall 2005,

was reviewed by the inspectors.

- 36 -

Enclosure 2

2.

The following corrective action activities will be completed:

a.

Replacement sump strainer structural analysis.

The strainers were not built in accordance with the design. As a result,

calculations needed to be revised due to the deviations of the as built

condition from design and errors in temperature correction values used in

the initial calculations. Completion date: June 30, 2008

b.

Downstream effects evaluation

Completion date: June 30, 2008

c.

Upstream effects evaluation

Completion date: June 30, 2008

d.

Resolution of debris generation calculation unverified assumption of 5D

ZOI for qualified coatings (via coatings testing)

Completion date: June 30, 2008

e.

Replacement sump screen head loss testing

Completion date: June 30, 2008

3.

Provide an update of the information contained in Section 2(c) regarding analysis

methodology.

Completion date: June 30, 2008

4.

The following evaluations and testing will be completed.

a.

Industry chemical effects testing

Completion date: June 30, 2008

b.

Nuclear Energy Institute 04-07 debris generation calculation

Completion date: June 30, 2008

c.

Evaluation of chemical effects impact on sump-strainer head loss

Completion date: June 30, 2008

d.

Confirmation that the replacement sump strainer design provides for

available Net Positive Suction Head (NPSH) to be in excess of required

NPSH

Completion date: June 30, 2008

- 37 -

Enclosure 2

e.

Completion of the final site acceptance review of the Westinghouse team

analysis summary report

Completion date: June 30, 2008

5.

Callaway Plant will complete the following items during Refueling Outage15:

a.

Replacement of containment recirculation sump strainers

Completed. As noted in the previous Temporary Instruction 166 report,

the resident inspectors had observed the installation of sump strainers

and debris barriers during their containment walkdown; however, the

strainers were not built in accordance with the design. The licensee has

completed their initial determination of operability and was finalizing their

acceptance calculations.

b.

Modification of containment debris barriers and interceptors as required

Completed. As noted in the previous Temporary Instruction 166 report,

the resident inspectors had observed the installation of sump strainers

and debris barriers during their containment walkdown.

c.

Evaluation and implementation of potential modification to the safety

injection system to address downstream effects

Completion date: June 30, 2008

6.

Callaway Plant will complete removal of containment spray system pump cyclone

separators, if required, based on the results of the downstream effects

evaluation.

Completion date: June 30, 2008

7.

The following programs and controls will be implemented at Callaway Plant to

control debris sources:

a.

Changes to design change process procedures to ensure that necessary

engineering evaluations will be performed for plant design that either

directly or indirectly affects containment, ECCS, or CSS.

Changes are being processed.

b.

Changes to containment entry and material control procedure

requirements for control of materials during work activities conducted in

the containment

c.

The following procedures were reviewed and completed as of

December 2007:

APA-ZZ-01004, Radiological Work Standards, Revision 9

HDP-ZZ-06100, Reactor Building Access, Revision 7

- 38 -

Enclosure 2

MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22

OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6

OSP-SA-00004, Visual Inspection of Containment for Loose Debris,

Revision 19

OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices,

Revision 2

d.

Changes to programs and procedures that have the potential to add tags

and labels inside containment

Completed: December 2007

The following documents were reviewed:

APA-ZZ-01004, Radiological Work Standards, Revision 9

HDP-ZZ-06100, Reactor Building Access, Revision 7

MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22

OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6

OSP-SA-00004, Visual Inspection of Containment for Loose Debris,

Revision 19

OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices,

Revision 2

e.

Implementation of a containment coatings assessment program

Licensee reported as complete. The inspectors reviewed SWE07848,

Containment Coating Condition Assessment. A preventative

maintenance item has been scheduled to perform containment coating

assessments with a periodicity of each refueling cycle.

f.

Implementation of a containment latent debris assessment program

Licensee reported as complete. The inspectors reviewed report,

Containment Building Latent Debris Assessment Refuel 14 Fall 2005,

and Procedure OSP-SA-00004, Visual Inspection of Containment for

Loose Debris, Revision 019. A preventative maintenance item has been

scheduled for a visual inspection of containment for loose debris with a

periodicity of each refueling cycle.

g.

Implementation of changes to the inspection processes for the installed

sump strainers

Licensee reported as complete. Reviewed Procedure OSP-EJ-00003,

Containment Recirculation Sump Inspection, Revision 6

- 39 -

Enclosure 2

8.

A final response will be submitted to the NRC to provide a final status of actions

requested by Generic Letter 2004-02.

Completion date: June 30, 2008

The Office of Nuclear Reactor Regulation will determine the adequacy of the sump

modifications with respect to Generic Safety Issue 191. This temporary instruction is

closed.

Documents reviewed by the inspectors are listed in the attachment.

b. Findings

No findings of significance were identified.

4OA6 Management Meetings

Exit Meeting Summary

On April 25, 2008, the health physics inspector presented the occupational radiation

safety inspection results to Mr. T. Herrmann and other members of his staff who

acknowledged the findings. The inspector confirmed that proprietary information was

not provided or examined during the inspection.

On June 18, 2008, the Temporary Instruction 2515/166 inspector presented the

inspection results to Mr. S. Maglio and other members of his staff who acknowledged the

findings. The inspector confirmed that proprietary information provided or examined

during the inspection had been returned.

On June 24, 2008, the resident inspectors presented the inspection results to

Mr. C. Naslund, Senior Vice President and Chief Nuclear Officer, and other members of

the licensee staff. The licensee acknowledged the issues presented. The inspectors

understood and acknowledged that proprietary information reviewed would not be

retained following report issuance.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the

licensee and were violations of NRC requirements which meet the criteria of Section VI

of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.

10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part,

that applicable regulatory requirements and the design basis are correctly

translated into specifications, drawings, procedures, and instructions.

Contrary to the above, on March 5, 2008, the licensee identified that a 4-foot

section of suction piping within containment spray system, Train A was

approximately 50 percent voided. Voiding within the containment spray

system was due to a design deficiency that did not allow for a proper fill and

vent of the system. This was entered in the licensees corrective action

program as CAR 200803462. This finding is greater than minor because it is

similar to the Example 3j in Manual Chapter 0612, Appendix E, "Examples of

- 40 -

Enclosure 2

Minor Issues," in that the presence of air within the containment spray system

suction header resulted in a condition where there was reasonable doubt on

the operability of the system. This finding is of very low safety significance

because it was a design or qualification deficiency confirmed not to result in

loss of operability.

10 CFR Part 50, Appendix B, Criterion III, requires measures be established

to assure that applicable regulatory requirements and design basis be

correctly translated into specifications, drawings, procedures, and

instructions. Technical Specifications 3.5.2 and 3.6.6 require that residual

heat removal and containment spray system components remain operable.

Contrary to this, measures were not adequate to assure installed center tube

diameters for the containment recirculation sump modification were correctly

accounted for by an accurate net positive suction head calculation.

The vendor supplying AmerenUE the containment recirculation sump strainer

identified that associated Vendor Calculation TDI-6002-05 for clean strainer

head loss did not account for the installed orifices located in the strainer

support plate. The size of the orifice beneath each strainer was smaller than

assumed in head loss calculations and was not large enough to prevent head

loss in excess of the net positive suction head required as defined in the

purchase specification supplied to the strainer vendor. The additional head

loss due to the calculation translation error was 2.28 feet. This resulted in

required net positive suction head being less than available. AmerenUE

performed three separate operability determination reviews to demonstrate

that the head loss margin could be recovered. The initial operability

determination on January 22, 2008, addressed the smaller support plate

orifice holes by using a separate vendor's flow analysis of the residual heat

removal and containment spray piping systems to demonstrate lower flow

and head losses than described in the FSAR. This operability determination

resulted in the limiting case flow path being the hot leg recirculation flow path.

Another operability review on March 12, 2008, addressed a nonconservative

temperature correction through the orifices. Subsequent to this, the licensee

informed the NRC that the additional nonconservative inputs were used in

the January 22, 2008, flow re-analysis of the residual heat removal system.

Additional analyses were performed to regain margin. This resulted in the

limiting case flow path changing from hot leg recirculation to cold leg

recirculation.

This example of inadequate design control was captured in the licensees

corrective action program as CARs 200800461 and 200802618. These

corrective action reviews documented three causes related to the following

design error:

Time pressure to address Generic Letter 2004-02

A complex design with parallel sequencing of different parts of the

design

AmerenUE not independently verifying the vendor's design due to

perceived expertise and an approved 10 CFR Part 50, Appendix B,

- 41 -

Enclosure 2

Quality Assurance program. AmerenUE did not perform a review of

the design, nor did they contract to have a third party engineering

review of the design.

This finding is greater than minor because it is similar to the Example 3j in

Manual Chapter 0612, Appendix E, Examples of Minor Issues, in that the

contractor error translating the design to the calculations resulted in a

condition where there was reasonable doubt on the operability of the ECCS.

This finding is of very low safety significance because it was a design or

qualification deficiency confirmed not to result in loss of operability. This

licensee-identified violation closes out Unresolved

Item 05000483/2008002-01.

ATTACHMENT: SUPPLEMENTAL INFORMATION

A-1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

B. Barton, Training Manager

M. Brandes, Consulting Engineer, Nuclear Engineering - Major Modifications

K. Bruckerhoff, Supervisor, Emergency Preparedness

F. Diya, Plant Director

T. Elwood, Supervising Engineer, Licensing

R. Farnam, Manager, Radiation Protection

K. Gilliam, Supervisor, Radiation Protection

L. Graessle, Manager, Regulatory Affairs

A. Heflin, Vice President, Nuclear

T. Herrmann, Vice President, Engineering

B. Holderness, Senior Health Physicist, Environmental Services

L. Kanuckel, Manager, Quality Assurance

D. Lantz, Superintendent of Operations Training

S. Maglio, Assistant Manager, Regulatory Affairs

R. Myatt, Supervisor, Engineering

K. Mills, Manager, Engineering

D. Neterer, Manager, Nuclear Operations

T. Parker, Trainer, Radiation Protection

S. Petzel, Engineer, Regulatory Affairs

J. Pitts, Component Engineer

V. Rider, ALARA Specialist, Radiation Protection

LIST OF ITEMS OPENED AND CLOSED

Opened 05000483/2008003-05

VIO

Failure to Prevent Recurrence of Voids in ECCS Cold Leg

Recirculation Piping (Section 4OA2)

Opened and Closed 05000483/2008003-01

NCV

Failure to Ensure the Suitability of the Design of the

Containment Air Cooler Control Circuitry (Section 1R15)05000483/2008003-02

NCV

Inadequate Surveillance Procedure Resulted in an

Inoperable ECCS (Section 1R15)05000483/2008003-03

NCV

Failure to Correct a Condition Adverse to Quality for

Diesel Generator Jacket Water O-Rings (Section 1R19)05000483/2008003-04

NCV

Failure to Maintain an Adequate Technical Specification

Bases Change Process (Section 1R22)

Closed 05000483/2008001-00

LER

Containment Cooler Inoperability (Section 4OA3)05000483/2008002-01

URI

Containment Recirculation Sump Operability

(Section 4OA7)

A-2

Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 1R01: Adverse Weather Protection

Procedures

ODP-ZZ-00001, Operations Department - Code of Conduct, Revision 41

OSP-NB-00001, Class 1E Electrical Source Verification, Revision 032

OTN-NB-0001A, 4.16 KV Vital (Class 1E) Electrical System - A Train, Revision 12

OTN-NB-0001A, Addendum 5, NB01 Loss of Power Recovery, Revision 0

OTO-ZZ-00012, Severe Weather, Revision 10

Miscellaneous

AmerenUE Response to Generic Letter 2006-02, Grid Reliability and the Impact on Plant Risk

and the Operability of Offsite Power

Training Lesson Plan LP-01, Systems, Switchyard MD

Training Lesson Plan T61.0110.6, Systems, Switchyard MD

Section 1RO4: Equipment Alignment

Drawings

M-22AL01A, Piping and Instrumentation Diagram Auxiliary Feedwater System, Revision 33

M-22BB01(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 30

M-22BB03A(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9

M-22BB03B(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 9

M-22BB03C(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7

M-22BB03D(Q), Piping and Instrumentation Diagram Reactor Coolant System, Revision 7

M-22BG01(Q), Piping and Instrumentation Diagram Chemical and Volume Control System,

Revision 28

M-22BG03(Q), Piping and Instrumentation Diagram Chemical and Volume Control System,

Revision 52

A-3

Attachment

M-22EJ01(Q), Piping and Instrumentation Diagram Residual Heat Removal System,

Revision 57

M-22EM01(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System,

Revision 33

M-22EM02(Q), Piping and Instrumentation Diagram High Pressure Coolant Injection System,

Revision 19

M-22EP01(Q), Piping and Instrumentation Diagram Accumulator and Safety Injection,

Revision 16

Section 1RO5: Fire Protection

Miscellaneous

Drill Number 08-01, Evaluate Fire Brigade Response in a Radiation Area, dated March 27, 2008

Drill Critique Number 08-01, Unannounced Fire Drill, dated March 27, 2008

FSAR, Appendix 9.5B, Fire Hazard Analysis

Section 1R11: Licensed Operator Requalification Program

Procedures

OTA-RK-00024, Addendum 98D, Seismic Event, Revision 0

OTO-SG-0001, Design Basis Earthquake, Revision 13

Section 1R12: Maintenance Effectiveness

Procedures

EDP-ZZ-01128, Maintenance Rule Program, Revision 8

NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear

Power Plants, Revision 3

Callaway Action Requests

200706892

200801644

200802854

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

Procedure

EDP-ZZ-01129, Callaway Plant Risk Assessment, Revision 14

Section 1R15: Operability Evaluations

Calculations

ARC-687, AFT Fathom 6.0 Output, Revision 0

A-4

Attachment

M-FL-18, LOCA and MSLB Containment Flood Level, Revision 1

WES-009-CALC-001, Wolf Creek/Callaway Post-LOCA Containment Water Level Calculation,

Revision 0

Callaway Action Requests

200800461

200802231

200802264

200802348

200802352

200802365

200802618

200803252

200803462

200804000

Drawings

E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19

E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19

E-018-00273, Motor Control Center Ambient Compensated Overload Relay Heater Chart,

Revision 3

E-018-00847, Overload Relay Time Current Characteristics, Revision 4

E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11

E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12

E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5

E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12

E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13

J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,

Revision 2

J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,

Revision 1

M-018-00943, 206 Ez-Flo Expansion Joint, Revision 0

M-22BG03, Piping and Instrumentation Diagram Chemical and Volume Control System,

Revision 52

M-22EM01, Piping and Instrumentation Diagram High Pressure Coolant Injection System,

Revision 33

M-23BG02, Piping Isometric CVCS-Max Charging Flow A and B Train Auxiliary Building,

Revision 12

A-5

Attachment

Procedures

ECA-0.1, Loss of All AC Power Recover Without Safety Injection Required, Revision 8

ECA-1.1, Loss of Emergency Coolant Recirculation, Revision 8

EDP-ZZ-04021, Review of Supplier Documents, Revision 5

ISF-SE-00N32, FCTNAL-NUC INSTM SOURCE RANGE N32, Revision 20

OSP-EJ-PV04A, Train A RHR and RCS Check Valve Inservice Test -IPTE, Revision 0

OSP-EJ-PV04B, Train B RHR and RCS Check Valve Inservice Test -IPTE, Revision 1

OTN-EN-00001, Containment Spray System, Revision 14

OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 1

Miscellaneous

Job 07513275 for SEN0032

Letter ULNRC-04884, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co.,

Facility Operating License NPF-30, Response to NRC Bulletin 2003-01, Potential Impact of

Debris Blockage on Emergency Sump Recirculation at Pressurized Water Reactor, dated

August 3, 2003

Letter ULNRC-05481, Docket Number 50-483, Callaway Plant Unit 1, Union Electric Co.,

Facility Operating License NPF-30 Response to Request for Additional Information, Response

to NRC Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency

Recirculation During Design Basis Accidents at Pressurized Water Reactors, dated

February 29, 2008

Garlock Sealing Technologies Customer Requested Test 206 Ez-Flo Expansion Test, dated

November 15, 2006

Section 1R18: Plant Modifications

Procedure

OTN-KA-00001, Compressed Air System, Revision 18

Drawings

E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19

E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19

E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11

E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12

E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5

A-6

Attachment

E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12

E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13

J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,

Revision 2

J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,

Revision 1

M-22KA01, Piping and Instrumentation Diagram Compressed Air System, Revision 016A

M-22KA06, Piping and Instrumentation Diagram Instrument Air Filter/Dryer Turbine, Building,

Revision 30A

Miscellaneous

Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change,

Revision 0

Job

08003842

Section 1R19: Postmaintenance Testing

Procedures

APA-ZZ-00330, Preventative Maintenance Program, Revision 29

OTN-GN-00001, Containment Cooling and CRDM Cooling, Revision 14

Callaway Action Requests

200801270

200802810

200804164

Jobs

06524419

07006905

08001080

08002676

08002765

08003910

Drawings

E-018-00141, Sz. 5 2SP-1WD Schematic, Revision 19

E-018-00214, Wiring Diagram 2SP-1WD (Size 5), Revision 19

E-018-00853, Wiring Diagram 2SP 1WD (Size 5), Revision 12

E-018-00852, Sz. 5 2SP-1WD Schematic, Revision 11

E-22NF01, Load Shedding and Emergency Load Sequencing Logic, Revision 5

A-7

Attachment

E-23GN02, Schematic Diagram Containment Cooler Fans A and C, Revision 12

E-23GN02A, Schematic Diagram Containment Cooler Fans B and D, Revision 13

J-22GN02A, Containment Cooling System Containment Cooling Fans SGN01A and SGN01C,

Revision 2

J-22GN02C, Containment Cooling System Containment Cooling Fans SGN01B and SGN01D,

Revision 1

Miscellaneous

Modification Package 08-0013, Containment Coolers DSGN01A/B/C/D Control Circuit Change,

Revision 0

Simple Surveillance SP08-017, Containment Cooler Control Circuit Changes, dated April 16,

2008

Section 1R22: Surveillance Testing

Procedures

EDP-ZZ-04107, HVAC Pressure Boundary Control, Revision 19

FDP-ZZ-00101, Technical Specification Bases Control Program, Revision 6

OSP-GL-0001A, Auxiliary Building Train A Negative Pressure Test, Revision 6

OSP-EJ-P001A, RHR Train A inservice Test - Group A, Revision 44

OSP-EJ-V001B, Residual heat removal Train B valve inservice test, Revision 21

OSP-NE-0001B, Standby Diesel Generator B Periodic Tests, Revision 29

OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting,

Revision 30

Section 2OS1: Access Controls to Radiologically Significant Areas and

Section 2OS2: ALARA Planning and Controls

Callaway Action Requests

200703726

200703956

200710799

200711181

200711846

200711875

200711880

200711881

200711883

200800219

200800438

200800631

200800632

200800633

200800727

200800838

200800887

200800888

200800891

200800957

200800973

200800988

200800991

200801135

200801390

200801430

200802003

200802280

200803141

200803204

200803205

200803208

A-8

Attachment

Audits and Self-Assessments

Quality Assurance Audit of Radiation Protection AP08-001, February 28, 2008

Quality Assurance Supplemental Audit of Radwaste AP07-012, October 30, 2007

Simple Self-assessment Report SA07-RP-S06, January 9, 2008

Radiation Work Permits/ALARA Reviews

RWP 803321RESIN, Transfer Spent Resin from Primary Tank to Liner

ALARA Package 07-03120, Reinstall Bladders into the Recycle Hold Up Tanks

Other/Meetings/Training/Work Review

ALARA Simulator Class

Callaway Plant Long Range Dose and Source Term Reduction Plan, Revision 2

Hot Spot and Shielding Log

Job 08000834 Transfer Spent Resin from Primary Tank to Liner

Plant ALARA Review Committee Meeting

Procedures

APA-ZZ-00405, Special Nuclear Material Control and Accounting, Revision 20

APA-ZZ-01000, Callaway Plant Radiation Protection Program, Revision 26

APA-ZZ-01001, Callaway Plant ALARA Program, Revision 11

APA-ZZ-01106, Lock and Key Control, Revision 16

HDP-ZZ-01100, ALARA Planning and Review, Revision 6

HDP-ZZ-01200, Radiation Work Permits, Revision 9

HTP-ZZ-01203, Radiological Area Access Control, Revision 36

HTP-ZZ-06001, High Radiation/Very High Radiation Area Access, Revision 31

HTP-ZZ-06028, Radiological Controls for Pools that Contain or Store Spent Fuel, Revision 5

RTS-HC-00350, Primary Spent Resin Storage Tank Transfer to Bulk Waste Disposal Station,

Revision 3

Section 4OA1: Performance Indicator Verification

Procedure

NOD-QP-40, NRC Performance Indicator Program, Revision 2

Miscellaneous

Various Callaway Control Room Logs, dated March 2007 through March 2008

Callaway Integrated Inspection Report 05000483/2007002

A-9

Attachment

Callaway Integrated Inspection Report 05000483/2007003

Callaway Integrated Inspection Report 05000483/2007004

Callaway Integrated Inspection Report 05000483/2008002

Section 4OA2: Identification and Resolution of Problems

Inspection Findings

NCV 05000483/2005002-01

NCV 05000483/2006012-04

Callaway Action Requests

200501192

200709819

200711496

200800246

200800298

200800355

200800522

200801270

200801529

200801830

200804000

200804164

200805049

200805122

200808956

Generic Communications

NRC Information Notice 2006-21, OE Regarding Entrainment of Air into Emergency Core

Cooling and Containment Spray Systems, September 21, 2006

Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat

Removal , and Containment Spray Systems, January 11, 2009

Procedures

OTN-EM0001, Safety Injection System, Revision 27

OSP-SA-00003, Emergency Core Cooling System Flow Path Verification and Venting,

Revision 27

Section 4OA5: Other

Procedures

APA-ZZ-01004, Radiological Work Standards, Revision 9

HDP-ZZ-06100, Reactor Building Access, Revision 7

MDP-ZZ-S0001, Scaffolding Installation and Evaluation, Revision 22

OSP-EJ-00003, Containment Recirculation Sump Inspection, Revision 6

OSP-SA-00004, Visual Inspection of Containment for Loose Debris, Revision 19

OTS-ZZ-06032, Addendum 1, Debris and Particulate Control Devices, Revision 2

Calculations

Calculation BG-75, Impact of MP 06-0003, Replacement Containment Recirculation Sump

Strainers, and MP 06-0027, TSP Basket Relocation, Revision 0

Calculation BN-21, Impact of MP 06-0003, Replacement Containment Recirculation Sump

Strainer on BN21, Revision 0

A-10

Attachment

Calculation BN-22, Impact of MP 06-0003, Replacement Containment Recirculation Sump

Strainer on BN22, Revision 0

Calculation EJ-29, NPSH Margin for RHR Pumps at Transition to Recirculation When NPSH

Margin is at its Minimum Value, Revision 1

Calculation TDI-6002-05/TDI-6003-05, Clean Head Loss - Wolf Creek/Callaway, Revision 0

Callaway Action Request

200800461, Prompt Operability Determination for Containment Spray and Residual Heat

Removal Systems, Revision 0

Miscellaneous

Ameren/UE comments on ECI-PCI-WC-CAL-6002-6003-1001

Callaway Plant Containment Building Latent Debris Assessment Report Refuel 14 Fall 2005

EC-PCI-WC/CAL-6002/6003-1001, AES Calculation No. PCI-5304-S01 Structural Evaluation of

the Containment Sump Strainers, Revision 1

MP 06-0003-EC-PCI-WC-CAL-6002-6003- (000) AES Document No. PCI-5304-S01 Structural

Evaluation of the Containment Sump Strainers, Revision 1

NUREG/CR-6914, Vol. 4, Integrated Chemical Effects Test, Revision 0

SWE07848, Containment Coating Condition Assessment

TDI-6002/TDI-6003, Sure-Flow Suction Strainer Qualification Report and Addendums, Wolf

Creek/Callaway

ULNRC-05124, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 Response To Generic Letter 2004-02, Potential Impact of Debris

Blockage On Emergency Recirculation During Design Basis Accidents At Pressurized-Water

Reactors.

ULNRC-05194, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 September 1, 2005, Response To Generic Letter 2004-02, Potential

Impact of Debris Blockage On Emergency Recirculation During Design Basis Accidents At

Pressurized-Water Reactors.

ULNRC-05295, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 Response Update To Generic Letter 2004-02, Potential Impact of

Debris Blockage On Emergency Recirculation During Design Basis Accidents At

Pressurized-Water Reactors.

ULNRC-05408, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 Update For Response To Generic Letter 2004-02, Potential Impact

of Debris Blockage On Emergency Recirculation During Design Basis Accidents At

Pressurized-Water Reactors.

A-11

Attachment

ULNRC-05461, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 Request for Extension Of Completion Date For Corrective Actions

Associated with NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On

Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.

ULNRC-05465, Docket Number 50-483 Callaway Plant Unit 1 Union Electric Co. Facility

Operating License NPF-30 Supplement to Request for Extension of Corrective Actions

Completion Date For NRC Generic Letter 2004-02, Potential Impact of Debris Blockage On

Emergency Recirculation During Design Basis Accidents At Pressurized-Water Reactors.

WCAP-16568-P, Jet Impingement Testing to Determine the Zone of Influence (ZOI) for

BAQualified/Acceptable Coatings (Proprietary)

Wolf Creek/Callaway Comments on Calculation PCI-5304-S01, Structural Evaluation of the

Containment Sump Strainers.

Section 4OA7: Licensee-Identified Violations

Callaway Action Requests

200802618

200803462

200800461

Generic Communication

Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation

During Design Basis Accidents at Pressurized Water Reactors, dated September 13, 2004

Calculation

TDI-6002-05

Correspondence

Amendment 180 to Facility Operating License NPF-30 from Mr. J. Donohew, Senior Project

Manager, Office of Nuclear Reactor Regulation to Mr. C. Naslund, AmerenUE

Procedure

APA-ZZ-00408, Professional Service Agreements and Nuclear Fuel Contracts, Revision 12

AmerenUE Callaway Plant Nuclear Plant Operating Quality Assurance Manual, Section 3,

Revision 25

Audits

Quality Assurance Audit of Design Control AP08-003

Independent Technical Review Report, SEGR 08-012, Temperature Correction Factor for

Strainer Stack Orifice Head Losses